ML020280505

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IR 05000317/2001-012, IR 05000318/2001-012, on 11/11-12/29/2001, Calvert Cliffs Nuclear Plant, Inc.; Calvert Cliffs Nuclear Power Plant, Units 1 & 2. Problem Identification and Resolution. Three Non-Cited Violations Noted
ML020280505
Person / Time
Site: Calvert Cliffs  Constellation icon.png
Issue date: 01/28/2002
From: Marilyn Evans
Reactor Projects Branch 1
To: Cruse C
Constellation Nuclear
References
IR-01-012
Download: ML020280505 (23)


See also: IR 05000317/2001012

Text

Mr. Charles H. Cruse

Vice President

Constellation Nuclear

Calvert Cliffs Nuclear Power Plant, Inc.

1650 Calvert Cliffs Parkway

Lusby, MD 20657-4702

SUBJECT: CALVERT CLIFFS NUCLEAR POWER PLANT - NRC INSPECTION REPORT

50-317/01-12, 50-318/01-12

Dear Mr. Cruse:

On December 29, 2001, the NRC completed an inspection at your Calvert Cliffs Nuclear Power

Plant Units 1 & 2. The enclosed report documents the inspection findings which were

discussed on January 18, 2001, with Mr. Katz and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

Immediately following the terrorist attacks on the World Trade Center and the Pentagon, the

NRC issued an advisory recommending that nuclear power plant licensees go to the highest

level of security, and all promptly did so. With continued uncertainty about the possibility of

additional terrorist activities, the Nation's nuclear power plants remain at the highest level of

security and the NRC continues to monitor the situation. This advisory was followed by

additional advisories, and although the specific actions are not releaseable to the public, they

generally include increased patrols, augmented security forces and capabilities, additional

security posts, heightened coordination with law enforcement and military authorities, and more

limited access of personnel and vehicles to the sites. The NRC has conducted various audits of

your response to these advisories and your ability to respond to terrorist attacks with the

capabilities of the current design basis threat (DBT). From these audits, the NRC has

concluded that your security program is adequate at this time.

Based on the results of this inspection, the inspectors identified three issues of very low safety

significance (Green). Two of these issues were determined to involve a violation of NRC

requirements. However, because of their very low safety significance and because they have

been entered into your corrective action program, the NRC is treating these issues as Non-cited

Violations, in accordance with Section VI.A.1 of the NRCs Enforcement Policy. If you deny

these Non-cited Violation, you should provide a response with the basis for your denial, within

30 days of the date of this inspection report, to the Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington DC 20555-0001; with copies to the Regional

Administrator, Region I; the Director, Office of Enforcement; and the NRC Resident Inspector at

the Calvert Cliffs facility.

Charles H. Cruse 2

In accordance with 10 CFR 2.790 of the NRC's "Rules of Practice," a copy of this letter and its

enclosure will be available electronically for public inspection in the NRC Public Document

Room or from the Publicly Available Records (PARS) component of the NRCs document

system (ADAMS). ADAMS is accessible from the NRC Web Site at http://www.nrc.gov/reading-

rm.html (the Public Electronic Reading Room).

Sincerely,

Michele G. Evans, Chief

Projects Branch 1

Division of Reactor Projects

Docket Nos. 50-317

50-318

License Nos. DPR-53

DPR-69

Enclosures: Inspection Report 50-317/01-12 and 50-318/01-12

Attachment 1 - Supplemental Information

cc w/encl: M. Geckle, Director, Nuclear Regulatory Matters (CCNPPI)

R. McLean, Administrator, Nuclear Evaluations

J. Walter, Engineering Division, Public Service Commission of Maryland

K. Burger, Esquire, Maryland People's Counsel

R. Ochs, Maryland Safe Energy Coalition

J. Petro, Constellation Power Source

State of Maryland (2)

Charles H. Cruse 3

Distribution w/encl: H. Miller, RA/J. Wiggins, DRA (1)

T. Bergman, RI EDO Coordinator

D. Beaulieu - SRI - Calvert Cliffs

E. Adensam, NRR (ridsnrrdlpmlpdi)

D. Skay, PM, NRR

P. Tam, PM, NRR (Backup)

M. Evans, DRP

W. Cook, DRP

S. Barr, DRP

P. Torres, DRP

R. Junod, DRP

Region I Docket Room (with concurrences)

DOCUMENT NAME: G:\BRANCH1\CCSTUFF\CC0112.WPD

After declaring this document An Official Agency Record it will be released to the Public. To

receive a copy of this document, indicate in the box: "C" = Copy without

attachment/enclosure "E" = Copy with attachment/enclosure "N" = No copy

OFFICE RI/DRP RI/DRP

NAME DBeaulieu MEvans

DATE 01/ /02 01/ /02

OFFICIAL RECORD COPY

U.S. NUCLEAR REGULATORY COMMISSION

REGION I

Docket Nos: 50-317, 50-318

License Nos.: DPR-53, DPR-69

Report Nos: 50-317/01-12;

50-318/01-12

Licensee: Calvert Cliffs Nuclear Power Plant, Inc.

Facility: Calvert Cliffs Nuclear Power Plant, Units 1 and 2

Location: 1650 Calvert Cliffs Parkway

Lusby, MD 20657-4702

Dates: November 11, 2001 - December 29, 2001

Inspectors: David Beaulieu, Senior Resident Inspector

Leonard Cline, Resident Inspector

Ron Nimitz, Senior Health Physicist

Nancy McNamara, Emergency Preparedness Inspector

John Caruso, Senior Operations Engineer

Charles Payne, Senior Operations Engineer, Region II

Approved by: Michele G. Evans, Chief, Projects Branch 1

Division of Reactor Projects

SUMMARY OF FINDINGS

IR 05000317/01-12, IR 05000318/01-12, on 11/11-12/29/2001, Calvert Cliffs Nuclear Plant,

Inc.; Calvert Cliffs Nuclear Power Plant, Units 1 & 2. Problem Identification and Resolution.

The report covered a six week period of inspection by resident inspectors, Senior Operations

Engineers, an Emergency Preparedness Inspector, and a Senior Health Physicist. The

inspection identified three Green findings, two which were treated as non-cited violations. The

significance of most findings is indicated by their color (Green, White, Yellow, Red) using IMC 0609 Significance Determination Process (SDP). Findings for which the SDP does not apply

are indicated by No Color or by the severity level of the applicable violation. The NRC's

program for overseeing the safe operation of commercial nuclear power reactors is described at

its Reactor Oversight Process website at http://www.nrc.gov/NRR/OVERSIGHT/index.html.

A. Inspector Identified Findings

Cornerstone: Mitigating Systems

GREEN. A non-cited violation of 10CFR50, Appendix B, Criterion XVI was identified

because the licensee failed to take timely and effective corrective action to mitigate

excessive train unavailability for the switchgear ventilation system. The Unit 1 and Unit

2 switchgear ventilation systems have been classified maintenance rule (a)(1) since the

fourth quarter of 1996, and the systems have exceeded maintenance rule performance

criteria every quarter since 1996. Although the corrective action plan that has been in

place since 1996 specified replacing the pneumatic controls, the fans, and the

compressors, three fans and all four compressors have not yet been replaced.

This issue has a credible impact on safety because the failure of the switchgear

ventilation system to maintain switchgear room temperatures could result in the failure

of safety related electrical busses in the switchgear room, as well as, the safety related

equipment supplied by these busses. The finding was considered to be of very low

safety significance, because the poor performance of this system has not resulted in

switchgear room temperatures in excess of design limits. (Section 4OA2)

GREEN. A non-cited violation of 10CFR50, Appendix B, Criterion XVI, was identified

because the licensee failed to identify and correct a condition adverse to quality on the

12 switchgear ventilation train. On October 8, 2001, the licensee failed to write an issue

report to document that when the failure of both the 11 and 12 switchgear refrigeration

compressors necessitated aligning the system in the fresh air mode, the 12 switchgear

ventilation train was unable to maintain switchgear room temperature. When the

inspector identified during a review of control room logs that no issue report had been

written, the licensee wrote the issue report on October 24, 2001. No corrective action

was taken by the licensee to investigate or correct the degraded condition until it

repeated itself on October 27, 2001, when they found that misadjusted damper

actuators resulted in 50% fresh air rather than 100%.

This issue has a credible impact on safety because the failure of the switchgear

ventilation system to maintain switchgear room temperatures would result in the failure

ii

Summary of Findings (contd)

of several safety significant mitigating systems. The finding was considered to be of

very low safety significance, because following the failure of the 12 switchgear

ventilation unit in the fresh air mode, the 11 switchgear ventilation train was placed in

service and returned switchgear room temperature to normal. (Section 4OA2)

Cornerstone: Occupational Radiation Safety

GREEN. The licensee has not established effective problem resolution for recurring

issues involving failure to conduct adequate radiological surveys to support planning and

conduct of radiological work activities. On July 13, 2001, the licensee failed to conduct

adequate pre-job and ongoing radiological surveys to detect elevated levels of

radioactive contamination within the No. 22 Chemical and Volume Control system ion

exchange pit for work therein. This contributed to elevated airborne radioactivity and

limited intakes of airborne radioactive material by workers during the work activities.

The licensees root cause analysis and NRC review identified that similar inadequate

radiological surveys had been identified on previous events and that some of these

problems were repeated during the event despite the implementation of corrective

actions. The failure to implement effective corrective actions is a cross-cutting issue

determined to be more than minor. The issue was evaluated under the Occupational

Radiation Safety Significance Determination Process (SDP) and determined to be a

finding of very low safety significance. The issue was not an as low as reasonably

achievable (ALARA) finding, did not involve an overexposure or substantial potential,

and did not affect the ability to assess dose. The issue was included in the licensees

corrective action process (IR3-072-016 and Causal Analysis PD200100011). (Section

4OA2)

B. Licensee Identified Findings

A violation of very low safety significance which was identified by the licensee has been

reviewed by the inspector. Corrective actions taken or planned by the licensee appear

reasonable. This violation is summarized in Section 4OA7 of this report.

iii

Report Details

Units 1 and 2 operated at or near 100 percent power for the entire inspection period.

1. Reactor Safety

Cornerstone: Initiating Events, Mitigating Systems, Barrier Integrity and Emergency

Preparedness

1R01 Adverse Weather Protection

a. Inspection Scope

The inspector verified that safety related systems, structures, and components such as

the condensate and refueling water storage tanks would remain functional when

challenged by cold weather and freezing conditions. The inspector reviewed the

Updated Final Safety Analysis Report (UFSAR), Individual Plant Examination of External

Events, Technical Specifications, and Operations Administrative Policy (OAP) 92-09,

"Cold Weather Operations," for cold weather operation requirements. To verify

adequate implementation of these requirements, the inspector observed a plant

operator perform Operations Performance Evaluation, PE 0-102-4-O-M, Revision 7,

Freeze Protected Equipment, on December 18, 2001.

b. Findings

No findings of significance were identified.

1R04 Equipment Alignment

.1 Partial Walkdown

a. Inspection Scope

The inspectors conducted an equipment alignment partial walkdown to evaluate the

operability of a selected redundant train or backup system, while the affected train or

system was inoperable or out of service. The walkdown included a review of system

operating instructions to determine correct system lineup and verification of critical

components to identify any discrepancies which could affect operability of the redundant

train or backup system. The inspectors performed a partial system walkdown on the

following system:

The inspectors reviewed the following Calvert Cliffs Nuclear Power Plant documentation:

  • Operating Instruction OI-21B, 2B Diesel Generator

b. Findings

No findings of significance were identified.

.2 Complete Walkdown

2

a. Inspection Scope

The inspectors performed a complete walkdown of a risk-important support system for

mitigating systems, the Unit 1 Electrical Switchgear Room Air Conditioning and

Ventilation (HVAC) system, to identify any discrepancies between the existing

equipment lineup and the required lineup. Operating Procedure OI-22H, Switchgear

Ventilation and Air Conditioning, the system description number 32, and Drawing No.

60-722-E, Auxiliary Building Ventilation System, were used to verify that electrical power

was available as required; major system components were correctly labeled, lubricated,

cooled, and ventilated; essential support systems were operational; and ancillary

equipment and debris did not interfere with system performance. To assess the

systems material condition, the inspectors reviewed the status of approximately

20 maintenance work orders (MOs) and over 15 issue reports (IRs) written over the

previous two years. Specific attention was focused on IRs written and MOs worked on

Unit 1 switchgear HVAC in September and October 2001, when several 11 and 12

switchgear HVAC compressor trips occurred. The documentation reviewed included:

  • PE 1-32-2-O-M, Operations Performance Evaluation for Switchgear HVAC
  • ES1996011050, Revision 1, Evaluate the Reliability of Equipment in the 27 foot

Switchgear Room in an Appendix R Fire

  • CA04511, Revision 0, Switchgear Room Transient Temperature Analysis

Evaluating Probabilistic Risk Assessment Scenarios

  • CA04658, Revision 0, Use of Outside Air Only to Cool the Unit 1 and Unit 2

Switchgear Rooms

  • CA00086, Revision 3, Switchgear Emergency Ventilation Fans
  • RAN 98-042, Revision 0, Switchgear Room Heat Load Analysis

b. Findings

No findings of significance were identified.

1R07 Heat Sink Performance

a. Inspection Scope

The inspectors reviewed data for the 21A and 21B service water (SRW) heat exchanger

thermal performance test completed on October 3, 2001; the statistical evaluation for

the 11A and 11B SRW heat exchanger thermal performance test completed on June 25,

2001, and; the results of the continuous monitoring thermal performance test conducted

on 12A and 12B, and 22A and 22B SRW heat exchangers. The inspectors analyzed the

data and results to verify that the SRW heat exchangers are capable of removing design

basis heat loads as described in the UFSAR. The inspectors also verified that the

licensees testing methods were consistent with their response to Generic Letter 89-13,

Service Water System Problems Affecting Safety-Related Equipment, and were

sufficient to detect heat exchanger degradation prior to a loss of required heat removal

capabilities. The documentation reviewed included:

  • Calculation CA04710, Revision 1, SRW Plate Heat Exchanger Thermal

Performance Test Evaluation Methodology and Software Development

3

  • Calculation CA03477, Revision 2, Service Water Plate Heat Exchanger Thermal

Performance Evaluation

  • Engineering Test Procedure ETP 99-001R, 21A and 21B SRW Heat Exchanger

Thermal Performance Test

  • Statistical Evaluation for Engineering Test Procedure ETP 98-040R, 11A and

11B SRW Heat Exchanger Thermal Performance Test

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification

.1 Requalification Activities Review by Resident Inspector

a. Inspection Scope

On November 13, 2001, the inspector observed licensed operator simulator training to

assess operator performance for a scenario involving a loss of closed cooling water. In

particular, the inspector observed operators trip reactor coolant pumps due to the loss of

cooling water to the seals, which the licensees probabilistic risk assessment has

determined to be an important operator action.

b. Findings

No findings of significance were identified.

.2 Requalification Program Review By Regional Specialist

a. Inspection Scope

A review was conducted of recent operating history documentation found in inspection

reports, licensee event reports, the licensees corrective action program, and the most

recent NRC plant issues matrix. The senior resident inspector was also consulted for

insights regarding licensed operator performance. These reviews did not detect any

operational events that were indicative of possible training deficiencies.

The following inspection activities were performed using NUREG 1021, Revision 8,

"Operator Licensing Examination Standards for Power Reactors," Inspection Procedure

Attachment 71111.11, "Licensed Operator Requalification Program," Appendix A

"Checklist for Evaluating Facility Testing Material.

The inspectors reviewed the quality and performance of operating and written exams

administered the week of November 12, 2001, as well as, a sample of several other

exams administered to crews during prior exam weeks.

The results of the annual operating tests for years 2000 and 2001 and the written exam

for 2001 were reviewed for quality, performance and grading. The inspector assessed

whether failure rates were consistent with the guidance of NUREG-1021, Revision 8,

4

and NRC Manual Chapter 0609, Appendix I, "Operator Requalification Human

Performance Significance Determination Process (SDP)." The SDP review verified the

following:

  • Crew pass rates were greater than 80%. (Pass rate was 100%)
  • Individual pass rates on the written exam were greater than 80%. (Pass rate

was 98.8%)

were greater than 80%. (Pass rate was 97.6%)

  • More than 75% of the individuals passed all portions of the exam. (97.6% of the

individuals passed all portions of the exam)

Observations were made of the dynamic simulator exams and job performance

measures administered during the week of November 12, 2001. These observations

included facility evaluations of crew and individual performance during the dynamic

simulator exams and individual performance of 5 job performance measures.

The remediation plans for individual failures over the past two year requalification

program cycle were reviewed to assess the effectiveness of the remedial training.

There were no crew failures during this period.

License reactivations for the past two year requalification program cycle were also

reviewed to ensure that 10 CFR 55.53 license conditions and applicable program

requirements were met.

Instructors and training/operations management were interviewed for feedback

regarding the implementation of the licensed operator requalification program.

Simulator performance and fidelity were reviewed for conformance to the reference

plant control room.

A sample of records for requalification training attendance, program feedback, reporting,

and medical examinations were reviewed for compliance with license conditions,

including NRC regulations.

5

b. Findings

The licensees methods and standards used to reactivate staff licensees to support

refueling outages appeared to be inconsistent with the requirements of 10 CFR

55.53(f)(2). The site practice has been to have staff licensees stand one shift of under-

instruction watch in the control room, conduct a tour of refueling equipment, and attend

four hours of pre-refueling classroom training as a basis for reactivation as a limited

refueling senior reactor operator. 10 CFR 55.53(f)(2) requires that the under-instruction

watch be stood in the position to which the individual will be assigned. The under-

instruction time in the control room appears to not have met the intent of the rule. This

item will be treated as unresolved pending further guidance and clarification from the

Operator Licensing Branch, Office of Nuclear Reactor Regulation. (URI 50-317;

50-318/01-012-01)

1R12 Maintenance Rule Implementation

a. Inspection Scope

The inspectors reviewed performance-based problems involving selected in-scope

structures, systems, or components (SSCs) to assess the effectiveness of the

maintenance program. Reviews focused on: (1) proper maintenance rule scoping, in

accordance with 10 CFR 50.65; (2) characterization of failed SSCs; (3) safety

significance classifications; (4) 10 CFR 50.65 (a)(1) and (a)(2) classifications; and (5)

the appropriateness of performance criteria for SSCs classified as (a)(2), and goals and

corrective actions for SSCs classified as (a)(1). The inspectors reviewed the most

recent system health reports and system functional failures of the last two years. The

following SSCs were reviewed:

  • Unit 1 and Unit 2 Switchgear ventilation system. The licensee appropriately

classified this system as (a)(1) due to excessive unavailability, and excessive

and repeat functional failures. Recent failures of the Unit 1 No. 11 and No. 12

switchgear HVAC system refrigeration unit compressors, in September and

October 2001, continued the systems poor performance trend. The inspector

evaluated the acceptability of the licensees corrective action plan as

documented in Issue Report IR3-009-491, the evaluation, corrective action, and

goal setting plan for the switchgear HVAC system, and the corrective actions

specified in the recent IRs written in September and October 2001.

  • The inspector reviewed the licensee data base of system unavailability for all

equipment from November 20 to December 20, 2001, to verify that out-of-service

times were entered into maintenance rule unavailability tracking as required.

The inspectors also reviewed the following Calvert Cliffs Nuclear Power Plant

documentation:

  • Station Procedure MN-1-112, Managing System Performance
  • Maintenance Rule Scoping Document, Revision 17
  • Maintenance Rule Indicator Report, October 2001

6

b. Findings

Two non-cited violations of very low safety significance (GREEN) of 10CFR50, Appendix

B, Criterion XVI, Corrective Action, were identified during this inspection. The details

of these findings are discussed in section 4OA2 of this report.

1R13 Maintenance Risk Assessments and Emergent Work Evaluation

a. Inspection Scope

For the selected maintenance orders listed below, the inspectors verified: (1) risk

assessments were performed in accordance with Calvert Cliffs procedure NO-1-117,

Integrated Risk Management; (2) risk of scheduled work was managed through the

use of compensatory actions; and (3) applicable contingency plans were properly

identified in the integrated work schedule.

  • MO2200002578 Replace 21 Switchgear HVAC fan
  • MO1200004788 Replace 12 High Pressure Safety Injection Pump

Outboard Bearing End Cover Gasket

  • MO1200101956 Remove Spare Reactor Trip Circuit Breaker and Reinstall

Trip Circuit Breaker 8

b. Findings

No findings of significance were identified.

1R19 Post-Maintenance Testing

a. Inspection Scope

The inspectors reviewed post-maintenance test procedures and associated testing

activities for selected risk significant mitigating systems to assess whether: (1) the

effect of testing on the plant had been adequately addressed by control room and

engineering personnel; (2) testing was adequate for the maintenance performed; (3)

acceptance criteria were clear and adequately demonstrated operational readiness,

consistent with design and licensing basis documents; (4) test instrumentation had

current calibrations, range, and accuracy for the application; (5) tests were performed,

as written, with applicable prerequisites satisfied; and (6) that equipment was returned

to the status required to perform its safety function. The following maintenance orders

were reviewed:

  • MO2199700801, Replace 21 Switchgear HVAC fan, which was retested by

performing air flow measurements with the fan operating in the maximum

recirculation mode and the 100% outside air mode. The acceptance criteria for

both measurements based on the systems design basis was 12,000 cubic feet

per minute (CFM).

b. Findings

7

No findings of significance were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors witnessed performance of surveillance test procedures and reviewed test

data of the selected risk-significant system to assess whether they satisfied Technical

Specifications, Updated Final Safety Analysis Report, Technical Requirements Manual,

and licensee procedure requirements. The inspectors assessed whether the testing

appropriately demonstrated that the system was operationally ready and capable of

performing its intended safety functions. The following test was witnessed:

  • STP O-70-1, Monthly Test of A train Containment Cooling Units, Iodine

Removal Units and Penetration Exhaust Filter was inspected on December 3,

2001.

b. Findings

No findings of significance were identified.

1EP2 Alert and Notification System (ANS) Testing

a. Inspection Scope

On November 5, 2001, the licensee notified the NRC (Event Notification 38466) that

while conducting their annual full cycle offsite siren test, all 49 sirens in Calvert County

failed to activate. There are 72 total sirens covering the 10 mile Plume Exposure

Emergency Planning Zone (EPZ). The apparent cause was that an activation icon,

located on a computer at Calvert Countys 911 Center, may have been inadvertently

removed. The other two risk counties emergency operating centers were not affected.

The licensee immediately initiated a task force to review this issue and documented their

results. On November 15, 2001, the licensee reported resolution of the computer

activation problem with a successful siren test which included full siren activation.

During the 10 day period of vulnerability, the licensee was relying on automatic route

alerting for notification of the public in Calvert County in the event of an emergency at

the Calvert Cliffs nuclear plant. The licensees review was to establish how long the

vulnerability existed prior to November 5, 2001. The licensee noted that automatic route

alerting has been in effect since the inception of the system in the early 1980s. On a

periodic basis, the inspector received status reports on the problem from licensee

representatives.

8

b. Findings

Preliminarily, the licensees review established that there was a human error while

attempting to simplify the County 911 Centers computer screen. A contractor hired by

Calvert County inadvertently removed the icon for proper actuation of the sirens in

Calvert County. The licensees backup public notification system is route alerting. The

inspector determined that the Calvert Countys Emergency Plan states that automatic

route alerting would be initiated simultaneously with the activation of the emergency

sirens. Therefore, although the sirens were incapable of being activated during the

period of vulnerability, had a radiological event occurred, the licensee believes that the

public would have been properly notified via route alerting.

At the end of this inspection report period, the inspector was gathering additional

information from the licensee pertaining to the Countys siren activation and route

alerting processes. The inspector was also assessing the adequacy of the capability to

notify the public within the EPZ as required by 10 CFR Part 50, 5.47(b)(5) and Appendix

E.IV.D.3, and system design objectives as noted in FEMA-REP-10. Therefore, this

issue is considered an Unresolved Item pending the completion of the licensees review

and the inspectors assessment. (URI 50-317; 50-318/01-012-02)

1. RADIATION SAFETY

Cornerstone: Occupational Radiation Safety

2OS1 Access Control To Radiologically Significant Areas

a. Inspection Scope

The inspector conducted the following activities and reviewed the following documents

to determine the effectiveness of radiologically controls including access controls to

radiologically significant areas.

The inspector toured portions of Unit 1 and Unit 2 Auxiliary Building and reviewed

access controls to locked High Radiation Areas. Four locked High Radiation Area

access points were physically inspected to determine if access controls were sufficient

to preclude unauthorized entry, as appropriate. Also reviewed was access and egress

control to the radiological controlled area (RCA) including personnel monitoring

practices to detect personnel contamination during RCA egress.

The inspector reviewed the radiological controls provided and accrued occupational

radiation doses received by divers performing underwater work activities in the Unit 1

spent fuel pool on December 5, 2001.

The inspector reviewed the planned reorganization of the radiological controls

organization relative to Technical Specification 5.2.1.

The reviews in this area were against criteria contained in 10 CFR 20 and applicable

licensee radiation protection procedures.

9

b. Findings

No findings of significance were identified.

2OS2 ALARA Planning and Controls

a Inspection Scope

The inspector selectively reviewed the adequacy and the effectiveness of the licensees

program to reduce occupational radiation exposure to ALARA. Specifically, the

inspector reviewed the licensees planning and preparation for the upcoming Unit 1

outage. The review was against criteria contained in 10 CFR 20 and applicable licensee

procedures. The following matters were reviewed:

  • The current status of integrated work planning including the status of planned

work, the status of completion of ALARA planning efforts, principal exposure

reduction efforts to be implemented, the radiological risk classification efforts of

selected planned activities, implementation of lessons learned.

  • ALARA planning for tasks with projected exposure greater than 5 person-rem

including radiation safety, maintenance activities, scaffolding, reactor assembly

and disassembly and vessel head penetration work, implementation of lessons

learned.

b. Findings

No findings of significance were identified.

2OS3 Radiation Monitoring Instrumentation

a. Inspection Scope

The inspector selectively reviewed elements of the radiation monitoring instrumentation

calibration program to evaluate the adequacy and effectiveness of the program.

Specifically, the inspector reviewed the use, calibration, and source checking of three

laboratory radiation counting systems to verify that the instruments were calibrated and

source checked as required by station procedures. The inspector reviewed applicable

statistical control charts for the instruments. The instruments reviewed were: NMC-

14(Sn. 84-2660-14), SPA-3(Sn.138), and SAC 4(Sn. 578).

The review was against applicable station procedures and 10 CFR 20.

10

b. Findings

No findings of significance were identified.

4 OTHER ACTIVITIES (OA)

40A1 Performance Indicator Verification

a. Inspection Scope

The inspectors reviewed performance indicator (PI) data for the Mitigating Systems

cornerstone, Emergency AC Power System Unavailability, for Units 1 and 2, to verify

individual PI accuracy and completeness. This inspection examined data and plant

records from third quarter of 2000 through the third quarter of 2001, including a review

of PI Data Summary Reports, Licensee Event Reports, operator narrative logs, and

maintenance rule records.

b. Findings

No findings of significance were identified.

4. OTHER ACTIVITIES

4OA2 Identification and Resolution of Problems

.1 Switchgear Ventilation

a. Inspection Scope

The inspector evaluated the acceptability of the licensees corrective action plan to

address the poor performance of the switchgear HVAC system as documented in Issue

Report IR3-009-491, the maintenance rule (a)(1) evaluation, corrective action, and goal

setting plan for the system, and in the issue reports (IRs) written to address the Unit 1

switchgear HVAC compressor trips and damper failures that occurred in September and

October 2001.

b. Findings

Two non-cited violations of very low safety significance (GREEN) of 10CFR50, Appendix

B, Criterion XVI, Corrective Action, were identified. Following a brief discussion of

system operation, the details of each finding are discussed below.

The switchgear HVAC system for Unit 1 and 2 are identical. On each unit the system

provides cooling to the A and B train safety related switchgear rooms. The system

consists of two redundant HVAC units that include a supply fan, cooling coil, and

refrigeration compressor. The HVAC units in each system discharge to a common

supply header for both the A and B train switchgear rooms, and take suction from

outside air and a common exhaust header from the switchgear rooms. The temperature

limits for the switchgear rooms are 104-F for continuous operation, and 150-F for peak

11

operations. The temperature limits are based on ensuring switchgear operability by

maintaining switchgear bus bar hot-spot temperatures less than 185-F.

A non-cited violation of very low safety significance (GREEN) of 10CFR50, Appendix B,

Criterion XVI was identified because the licensee failed to take timely and effective

corrective action to mitigate excessive train unavailability for the switchgear HVAC.

The Unit 1 and Unit 2 switchgear HVAC systems have been classified maintenance rule

(a)(1) since the fourth quarter of 1996. In IR1-050-852, dated October 21, 1996, the

licensee classified the switchgear HVAC systems on both units as (a)(1) under the

maintenance rule. In its (a)(1) Evaluation, Corrective Action and Goal Setting plan for

the system, the licensee attributed the high unavailability to obsolete equipment and

refrigeration system design issues. The corrective action plan specified replacing the

pneumatic controls, the fans, and the compressors. As of December 2001, five years

after the system was classified (a)(1), only the pneumatic control system has been

upgraded for all four switchgear HVAC trains. For fan replacement, the licensee

initiated ES19961674 in January 1996. Only the 21 switchgear HVAC fan has been

replaced. The 22 switchgear HVAC fan is scheduled for installation in May 2002, and

the fans for the 11 and 12 switchgear HVACs will be installed in the Fall 2002. For

compressor replacement, ES199602324 was initiated in November 1996, but currently

no new compressors have been installed. The compressors for 21 and 22 switchgear

HVAC are scheduled for installation in May 2002. The 11 and 12 switchgear HVAC

compressors are scheduled for the fall 2002.

Interim corrective actions, since 1996, have also been ineffective at maintaining system

reliability. Since that time, in every quarter, at least three of the four switchgear HVAC

trains have exceeded the unavailability performance criteria of 250 hours0.00289 days <br />0.0694 hours <br />4.133598e-4 weeks <br />9.5125e-5 months <br /> per train per 2

year period, and in many cases train unavailability has been more than four times the

performance criteria. In addition, the Unit 1 switchgear HVAC system has exceeded the

functional failure performance criteria of less than five functional failures per two year

period every quarter since 1996.

The failure to implement timely and effective corrective action to address the poor

performance of the switchgear HVAC system has a credible impact on safety because

the failure of the switchgear HVAC system to maintain switchgear room temperatures

within the design limits of 104-F and 150-F would lead to switchgear failure. This would

result in the failure of several safety significant mitigating systems. This issue was

assessed as very low safety significance, because the poor performance of this system

has not resulted in switchgear room temperatures in excess of 104-F.

The failure to take timely and effective corrective action to address poor reliability and

unavailability of the switchgear HVAC system is a violation of 10CFR50, Appendix B,

Criterion XVI, Corrective Action, which requires prompt correction of conditions

adverse to quality. This violation is being treated as a Non-cited Violation, consistent

with Section VI.A of the NRC Enforcement Policy, issued on May 1, 2000 (65FR25368)

(NCV 50-317;50-318/01-012-03). The licensee entered the issue into its corrective

action program as IR3-080-027.

12

A second non-cited violation of very low safety significance (GREEN) of 10CFR50,

Appendix B, Criterion XVI was identified because the licensee failed to identify and

correct a condition adverse to quality on 12 switchgear HVAC.

On October 8, 2001, the 12 switchgear HVAC train was placed in service in the fresh air

mode because both switchgear HVAC refrigerant compressors had tripped and were

considered unavailable. At that time outside air temperature was approximately 50-F,

low enough that based on licensee engineering calculations, the fresh air mode could

maintain switchgear room temperature below the design limit of 104-F. Six hours later,

operators received a Unit 1 safety related switchgear room high temperature alarm.

Operators secured the 12 switchgear HVAC train placed the 11 switchgear HVAC in

service in the fresh air mode, and as expected, switchgear room temperature returned

to normal. On that day, no action was taken to investigate the cause of the failure of the

12 switchgear HVAC to perform as expected in the fresh air mode. During a review of

control room logs and meteorological tower data for outside air temperature, the

inspector identified that the licensee did not write an issue report to investigate and

correct the 12 switchgear HVAC problem. On October 24, 2001, the licensee wrote IR3-

050-297 to document the inspectors concern but no immediate corrective action was

taken. On October 27, 2001, after both switchgear HVAC compressors had tripped,

operators again placed the 12 switchgear HVAC in service in the fresh air mode, and at

12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> later the 12 switchgear HVAC could no longer maintain switchgear room

temperature. Operators placed 11 switchgear HVAC in service in the fresh air mode to

return switchgear room temperature to normal, and documented the issue in IR3-077-

133. Troubleshooting determined that the cause of the 12 switchgear HVAC problem

was a misadjusted actuator for the mixing dampers resulting in only 50% fresh air rather

than 100%. The condition was corrected on October 29, 2001. The licensee verified

that a similar condition did not exist on the other switchgear HVAC trains.

The failure to identify and correct the degraded condition of the 12 switchgear HVAC

unit on October 8, 2001, had a credible impact on safety because the failure of the

switchgear ventilation system to maintain switchgear room temperatures could result in

the failure of safety related electrical busses in the switchgear room, as well as, the

safety related equipment supplied by these busses. This issue was assessed as very

low safety significance because following the failure of the 12 switchgear HVAC unit in

the fresh air mode, the 11 switchgear HVAC returned switchgear room temperature to

normal.

The failure to identify and correct the degraded condition of the 12 switchgear HVAC fan

on October 8, 2001, was a violation of 10CFR50, Appendix B, Criterion XVI, Corrective

Action, which requires the identification and resolution of conditions adverse to quality.

This violation is being treated as a Non-cited Violation, consistent with Section VI.A of

the NRC Enforcement Policy, issued o May 1, 2000 (65FR25368) (NCV 50-317/01-012-

04). The licensee has entered this issue into its corrective action program as IR3-014-

145.

.2 Radiation Safety

a. Inspection Scope

13

The inspector reviewed the licensees root cause analysis for an airborne radioactivity

event associated with work in the No. 22 Chemical Volume and Control System (CVCS)

ion exchanger pit on July 13, 2001. The radiological controls aspect of the event were

reviewed during NRC Combined Inspection No. 50-317;50-318/2001-006. During the

previous inspection, one Non-cited licensee identified violation was identified and one

inspector identified violation was identified and documented in that NRC report. During

this current inspection, the inspector focused on the adequacy of the licensees

corrective actions for previous events.

b. Findings

GREEN. The licensee has not established effective problem resolution relative to

recurring issues involving failure to conduct adequate radiological surveys to support

planning and conduct of radiological work activities.

On July 13, 2001, the licensee failed to conduct adequate pre-job and ongoing

radiological surveys to detect elevated levels of radioactive contamination within the

No. 22 CVCS ion exchange pit for work therein. This contributed to elevated airborne

radioactivity and limited intakes of airborne radioactive material by workers during the

work activities. The licensees root cause analysis for this event and the inspectors

review indicated that inadequate radiological surveys had been identified on previous

events and that some of these problems were repeated during the event (e.g.,

inadequate job planning, inadequate radiological job coverage). For example, on May 3,

2001, the licensee experienced elevated airborne radioactivity during work in the Unit 2

containment resulting in limited intakes of airborne radioactive material. The licensees

root cause analysis for the May 3, 2001, event (IR3-076-089; RCAR IR2-001-0404)

identified inadequate radiological surveys, lack of specific work permit instructions and

lack of a questioning attitude as contributing causes for this event. Similarly, on April 8,

2000 (IR3-054-967;IR3-044-244), the licensee failed to conduct radiological

contamination surveys of bags of material prior to removing the surface contaminated

bags from the Unit 1 reactor cavity to a non-contaminated area in the Unit 1 Auxiliary

Building. This resulted in personnel and clean area contamination. (These issues were

documented in NRC Inspection Report Nos. 50-317;50-318/2001-006, 2001-005, and

2000-009). Although the licensee recognized the inadequacies in the radiological

surveys, had taken various corrective actions for the previous issues, and none of the

events resulted in significant personnel contamination or intakes of radioactive material,

the occurrence of the July 13, 2001, event indicates that the licensees corrective

actions for previous radiological events (e.g., more thorough planning and provision of

minimum expectations for surveys by technicians for job coverage) has not been

effective in resolving issues involving the conduct of effective radiological evaluations to

support work activities.

The failure to implement effective corrective actions is a cross-cutting issue as defined

in NRC MC 0610* in that the issue has the potential to affect multiple cornerstones.

This issue was determined to be more than minor in that failure to implement effective

corrective actions could be reasonably viewed as a precursor to a more significant

event. Further, the issue is associated with conditions contrary to licensee procedures.

The issue was evaluated under the Occupational Radiation Safety Significance SDP

and determined to be a finding of very low safety significance (GREEN). The issue was

14

not an ALARA finding in that no significant personnel exposures have occurred, the

issue did not involve an overexposure or substantial potential for such an exposure, and

the ability to assess dose was not compromised. The issue was included in the

licensees corrective action process (IR3-072-016 and Causal Analysis PD200100011)

(FIN 50-317;50-318/01-012-05)

4OA5 Steam Generator Replacement (50001)

a. Inspection Scope

The inspector reviewed planned radiological controls for the upcoming steam generator

replacement project (SGRP). The inspector discussed the project with project team

representatives and reviewed various plans and procedures supporting the project. The

following matters were reviewed:

+ ALARA planning

+ project dose estimates and dose tracking

+ project exposure controls including temporary shielding

+ surface and airborne contamination controls including restoration of containment

openings

+ radioactive material management including source term analysis, waste storage,

and disposal plans project radiological work plans and controls

+ project staffing and training plans

+ emergency contingencies

+ radiological safety plans for storage of the steam generators including conduct of

public and potential worker dose assessments plans and radiological

environmental monitoring

+ evaluation of radiological source terms for dose assessment purposes

+ surveillance and planned audits of work activities including resolution of worker

concerns

+ the licensees efforts to identify and implement lessons learned from previous

steam generator replacements at other facilities.

The review was against criteria contained in 10 CFR 19.12, 10 CFR 20, site Technical

Specifications, and applicable site and project procedures.

b. Findings

No findings of significance were identified.

4OA6 Management Meetings

.1 Exit Meeting Summary

The inspectors presented the inspection results to members of licensee management at

the conclusion of the inspection on January 18, 2001.

The inspectors asked the licensee whether any of the material examined during the

inspection should be considered proprietary. No proprietary information was identified.

15

4OA7 Licensee Identified Violations

The following finding of very low safety significance (GREEN) was identified by the

licensee and is a violation of NRC requirements which meetsSection VI of the NRC

Enforcement Policy, NUREG-1600, for being dispositioned as a Non-Cited Violation.

NCV Tracking Number Requirement Licensee Failed to Meet

50-317;50-318/01-012-06 10 CFR71.87 requires the licensee to load shipments of

radioactive material in accordance with written procedures.

On September 5, 2001, the licensee did not adhere to

procedure RPS 2-231, for the loading of a Type B

shipment of radioactive material. Specifically, the licensee

did not ensure hardware compatibility ratings for hoisting

operations and used a crane hook, rated to 6,000 pounds,

to raise and transfer in air an approximately 7000 pound

container of waste containing approximately 91 curies of

mixed radionuclides. The licensee identified the issue on

November 6, 2001, and subsequently determined the hook

had been load tested to 9,000 pounds. The licensee took

various corrective and preventative actions and placed the

issue into its corrective action process (IR3-059-464).

16

ATTACHMENT 1

a. Key Points of Contact

W. Birney, Supervisor, Requalification Training Unit

C. Cruse, Vice President

P. Katz, Plant General Manager

M. Geckle, Director, Nuclear Regulatory Matters

M. Haney, Radiation Protection Supervisor

D. Holm, Superintendent, Nuclear Operations

J. Hornick, Supervisor, Initial Training Unit

J. Kellum, Senior Operations Instructor

M. Korsnick, Superintendent, Work Management

K. Mills, General Supervisor, Nuclear Plant Operations

M. Navin, Superintendent, Technical Support

K. Nietmann, Manager, Nuclear Performance Assessment Department

T. Pritchett, Manager, Nuclear Engineering Department

E. Roach, Radioactive Waste Supervisor

S. Sanders, General Supervisor-Radiation Safety

J. Sickle, General Supervisor, Nuclear Training

J. Spina, Superintendent, Nuclear Maintenance

R. Szoch, General Supervisor, Plant Engineering

L. Weckbaugh, Manager, Nuclear Support Services

R. Wyvill, ALARA Supervisor

J. York, Assistant General Radiation Supervisor

b. List of Items Opened, Closed, or Discussed

Opened

50-317;50-318/01-012-001 URI Licensees methods and standards used to reactivate staff

licensees to support refueling outages appeared to be

inconsistent with the requirements of 10 CFR 55.53(f)(2).

(IR Section 1.R11)

50-317;50-318/01-012-002 URI During a November 5, 2001, full cycle offsite siren test

none of the 49 sirens in Calvert County activated. It

appears that planning standard 10CFR50.47(b)(5) and the

requirements of 10CFR50 Appendix E.IV.D.3 have been

violated.(IR Section 1EP2)

Opened and Closed

50-317;50-318/01-012-003 NCV Failure to take timely and effective corrective action to

mitigate excessive train unavailability for the switchgear

HVAC in accordance with 10CFR50, Appendix B, Criterion

XVI (IR Section 4OA2)

Attachment 1 (contd) 17

50-317/01-012-004 NCV Failure to identify and correct a condition adverse to

quality on the 12 switchgear HVAC in accordance with

10CFR50, Appendix B, Criterion XVI (IR Section 4AO2)

50-317;50-318/01-012-005 FIN Failure to implement effective corrective actions for issues

involving inadequate radiological evaluations to support

work activities (IR Section 4AO2)

50-317;50-318/01-012-006 NCV Failure to implement 10 CFR71.87 regarding adherence to

cask loading procedures (IR Section 4AO7)

c. List of Acronyms

ALARA As Low As Reasonably Achievable

CFM Cubic feet per minute

CFR Code of Federal Regulations

CVCS Chemical and Volume Control System

DBT Design Basis Threat

EPZ Emergency Planning Zone

FEMA Federal Emergency Management Agency

FIN Finding

HVAC Ventilation System

IR Issue Report

MC Inspection Manual Chapter

MO Maintenance Order

NCV Non-cited Violation

NRC Nuclear Regulatory Commission

OAP Operations Administrative Policy

PI Performance Indicator

RCA Radiologically Controlled Area

SDP Significance Determination Process

SGRP Steam Generator Replacement Project

SRW Service Water System

SSC Structure, System and Component

UFSAR Updated Final Safety Analysis Report

URI Unresolved Item