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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20042F9581990-05-0707 May 1990 LER 90-001-01:on 900124,shift Surveillance Log Did Not Meet Requirements of Tech Specs.Caused by Deficient Procedure. Surveillance Log Revised to Include Daily Instrument Check. W/900507 Ltr ML19332E7591989-11-27027 November 1989 LER 89-008-00:on 891027,primary Containment Isolation Sys Group II & III Isolations Occurred When Spurious Reactor Low Level Signal Sensed by Instruments.Possibly Caused by Air Bubble in Sensing Lines.Line backfilled.W/891127 Ltr ML20003C3331981-02-23023 February 1981 LER 81-014/03L-0:on 810131,Leeds & Northrup Model W multi-point Temp Recorder TR-2-10-131 Found Not Recording Suppression Chamber Water Temp Per Tech Spec.Caused by Bound Drive Motor.Instrument Repaired & Returned to Svc on 810202 ML19331C7811980-06-19019 June 1980 LER 80-012/03L-0:on 800520,during Full Power Operation, Routine Testing Revealed Pressure Switch 5121B Setpoint at 700 Psi Above Tech Spec.Caused by Personnel Error.Setpoint Adjusted.Technician Instructed ML19210D6251979-11-16016 November 1979 LER 79-049/01T-0:on 791101,four Seismic Supports Found W/Safety Factors of Less than Two.Caused by Engineering Design Deficiency.Redesign Performed.Corrective Action Implemented within Seven Days ML19247A0721979-07-20020 July 1979 LER 79-031/03L-0 on 790622:during Electrical Storm,Lost Main Stack Sampling Sys & Automatic Initiation Capability. Caused by Blown Fuses from lightning-induced Electrical Transient.Fuses Replaced 1990-05-07
[Table view] Category:RO)
MONTHYEARML20042F9581990-05-0707 May 1990 LER 90-001-01:on 900124,shift Surveillance Log Did Not Meet Requirements of Tech Specs.Caused by Deficient Procedure. Surveillance Log Revised to Include Daily Instrument Check. W/900507 Ltr ML19332E7591989-11-27027 November 1989 LER 89-008-00:on 891027,primary Containment Isolation Sys Group II & III Isolations Occurred When Spurious Reactor Low Level Signal Sensed by Instruments.Possibly Caused by Air Bubble in Sensing Lines.Line backfilled.W/891127 Ltr ML20003C3331981-02-23023 February 1981 LER 81-014/03L-0:on 810131,Leeds & Northrup Model W multi-point Temp Recorder TR-2-10-131 Found Not Recording Suppression Chamber Water Temp Per Tech Spec.Caused by Bound Drive Motor.Instrument Repaired & Returned to Svc on 810202 ML19331C7811980-06-19019 June 1980 LER 80-012/03L-0:on 800520,during Full Power Operation, Routine Testing Revealed Pressure Switch 5121B Setpoint at 700 Psi Above Tech Spec.Caused by Personnel Error.Setpoint Adjusted.Technician Instructed ML19210D6251979-11-16016 November 1979 LER 79-049/01T-0:on 791101,four Seismic Supports Found W/Safety Factors of Less than Two.Caused by Engineering Design Deficiency.Redesign Performed.Corrective Action Implemented within Seven Days ML19247A0721979-07-20020 July 1979 LER 79-031/03L-0 on 790622:during Electrical Storm,Lost Main Stack Sampling Sys & Automatic Initiation Capability. Caused by Blown Fuses from lightning-induced Electrical Transient.Fuses Replaced 1990-05-07
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEAR05000278/LER-1999-005-03, :on 990920,uplanned Esfas During Planned Mod Activitives in Main CR Were Noted.Caused by Inattention to Detail by Individuals Performing Work.All CR Mods Were Ceased to Allow Review of Mod Work Packages.With1999-10-20020 October 1999
- on 990920,uplanned Esfas During Planned Mod Activitives in Main CR Were Noted.Caused by Inattention to Detail by Individuals Performing Work.All CR Mods Were Ceased to Allow Review of Mod Work Packages.With
ML20217K9931999-10-14014 October 1999 Safety Evaluation Supporting Amend 234 to License DPR-56 ML20217B4331999-10-0505 October 1999 Safety Evaluation Supporting Amend 233 to License DPR-56 05000278/LER-1999-004-03, :on 990901,3A RPS Bus Was Inadvertently Deenergized,During Planned Mod Activities on Main CR Panel. Caused by Electrician Failing to Self Check Work.All CR Work Was Ceased Immediately & Shutdown Meeting Held1999-10-0101 October 1999
- on 990901,3A RPS Bus Was Inadvertently Deenergized,During Planned Mod Activities on Main CR Panel. Caused by Electrician Failing to Self Check Work.All CR Work Was Ceased Immediately & Shutdown Meeting Held
ML20217G3541999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Pbaps,Units 2 & 3. with ML20216H7091999-09-24024 September 1999 Safety Evaluation Supporting Amends 229 & 232 to Licenses DPR-44 & DPR-56,respectively ML15112A7681999-09-20020 September 1999 SER Accepting Revision 25 of Pump & Valve Inservice Testing Program,Third 10-year Interval for Plant,Units 1,2 & 3 ML20212D1281999-09-17017 September 1999 Safety Evaluation Supporting Proposed Alternatives CRR-03, 05,08,09,10 & 11 05000278/LER-1999-003-03, :on 990814,HPCIS Was Declared Inoperable Due to Erratic Behavior Resulting in Loss of Single High Train Safety Sys.Caused by Weakness in Procedural Guidance. Readjusted Hydraulic Governor Needle Valve.With1999-09-13013 September 1999
- on 990814,HPCIS Was Declared Inoperable Due to Erratic Behavior Resulting in Loss of Single High Train Safety Sys.Caused by Weakness in Procedural Guidance. Readjusted Hydraulic Governor Needle Valve.With
ML20212A5871999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Peach Bottom,Units 2 & 3.With ML20211D5501999-08-23023 August 1999 Safety Evaluation Supporting Amends 228 & 231 to Licenses DPR-44 & DPR-56,respectively ML20212H6311999-08-19019 August 1999 Rev 2 to PECO-COLR-P2C13, COLR for Pbaps,Unit 2,Reload 12 Cycle 13 ML20210N7641999-07-31031 July 1999 Monthly Operating Repts for Jul 1999 for PBAPS Units 2 & 3. with 05000277/LER-1999-005-01, :on 990616,failure to Maintain Provisions of FP Program Occurred.Caused by Less than Adequate Engineering Rigor in Both Development & Review Analysis.Fire Watch Immediately Established.With1999-07-16016 July 1999
- on 990616,failure to Maintain Provisions of FP Program Occurred.Caused by Less than Adequate Engineering Rigor in Both Development & Review Analysis.Fire Watch Immediately Established.With
ML20209H1121999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Pbaps,Units 2 & 3. with ML20195H8841999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Pbaps,Units 2 & 3. with 05000278/LER-1999-002-02, :on 990406,safeguard Sys to Unrelated Door Was Inadvertently Disabled by Security Alarm Station Operator. Caused by Noncompliance with Procedures & Less than Adequate Shift Turnover.Briefed Personnel on Event.With1999-05-0606 May 1999
- on 990406,safeguard Sys to Unrelated Door Was Inadvertently Disabled by Security Alarm Station Operator. Caused by Noncompliance with Procedures & Less than Adequate Shift Turnover.Briefed Personnel on Event.With
ML20206N1661999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Pbaps,Units 2 & 3. with ML20206A2921999-04-20020 April 1999 Safety Evaluation Concluding That Proposed Changes to EALs for PBAPS Are Consistent with Guidance in NUMARC/NESP-007 & Identified Deviations Meet Requirements of 10CFR50.47(b)(4) & App E to 10CFR50 05000278/LER-1999-001-03, :on 990312,ESF Actuation of Rcics Occurred Due to High Steam Flow Signal During Sys Restoration.Temporary Change to Restoration Procedure Was Initiated to Open RCIC Outboard Steam Isolation Valve in Smaller Increments1999-04-0808 April 1999
- on 990312,ESF Actuation of Rcics Occurred Due to High Steam Flow Signal During Sys Restoration.Temporary Change to Restoration Procedure Was Initiated to Open RCIC Outboard Steam Isolation Valve in Smaller Increments
ML20205K7411999-04-0707 April 1999 Safety Evaluation Supporting Amends 227 & 230 to Licenses DPR-44 & DPR-56,respectively ML20205P5851999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Peach Bottom Units 2 & 3.With ML20207G9971999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Peach Bottom Units 2 & 3.With 05000278/LER-1998-009-01, :on 981227,unplanned Esfa Were Noted.Caused by Transformer Insulator Failure.Replaced Failed Insulator. with1999-01-20020 January 1999
- on 981227,unplanned Esfa Were Noted.Caused by Transformer Insulator Failure.Replaced Failed Insulator. with
ML20206D3651998-12-31031 December 1998 1998 PBAPS Annual 10CFR50.59 & Commitment Rev Rept. with ML20206D3591998-12-31031 December 1998 1998 PBAPS Annual 10CFR72.48 Rept. with ML20205K0381998-12-31031 December 1998 PECO Energy 1998 Annual Rept. with ML20199E3471998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Peach Bottom,Units 1 & 2.With ML20206P1651998-12-31031 December 1998 Fire Protection for Operating Nuclear Power Plants, Section Iii.F, Automatic Fire Detection 05000277/LER-1998-008-01, :on 981130,circuit Breaker SU-25 Tripped.Caused by Less than Adequate Procedural Guidance.Operators Verified Sys Integrity & Successfully Returned Sys to Svc.With1998-12-30030 December 1998
- on 981130,circuit Breaker SU-25 Tripped.Caused by Less than Adequate Procedural Guidance.Operators Verified Sys Integrity & Successfully Returned Sys to Svc.With
05000277/LER-1998-007-02, :on 981107,failure to Meet TS & Associated LCO Requirments of Absolute Difference in APRM & Calculated Power of Less than 2% Was Noted.Caused by Substitute Valves Being Used.Removed Substitute Valves.With1998-12-0404 December 1998
- on 981107,failure to Meet TS & Associated LCO Requirments of Absolute Difference in APRM & Calculated Power of Less than 2% Was Noted.Caused by Substitute Valves Being Used.Removed Substitute Valves.With
ML20196G7021998-12-0202 December 1998 SER Authorizing Proposed Alternative to Delay Exam of Reactor Pressure Vessel Shell Circumferential Welds by Two Operating Cycles ML20198B8591998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Pbaps,Units 2 & 3. with ML20196E8261998-11-30030 November 1998 Response to NRC RAI Re Reactor Pressure Vessel Structural Integrity at Peach Bottom Units 2 & 3 05000278/LER-1998-005-03, :on 981025,inadvertent Unit 3 Electrical Bus E33 Trip (Esfa) During Performance of Unit 2 Electrical Bus E32 Surveillance Test Was Noted.Caused by Personnel Error. Sp S12M-54-E32-XXF4 Was Completed.With1998-11-20020 November 1998
- on 981025,inadvertent Unit 3 Electrical Bus E33 Trip (Esfa) During Performance of Unit 2 Electrical Bus E32 Surveillance Test Was Noted.Caused by Personnel Error. Sp S12M-54-E32-XXF4 Was Completed.With
ML20206R2571998-11-17017 November 1998 PBAPS Graded Exercise Scenario Manual (Sections 1.0 - 5.0) Emergency Preparedness 981117 Scenario P84 ML20198C6751998-11-0505 November 1998 Rev 3 to COLR for PBAPS Unit 3,Reload 11,Cycle 12 ML20195E5341998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Pbaps,Units 2 & 3. with ML20155C6071998-10-26026 October 1998 Safety Evaluation Supporting Amend 226 to License DPR-44 ML20155C1681998-10-22022 October 1998 Safety Evaluation Accepting Proposed Alternative Plan for Exam of Reactor Pressure Vessel Shell Longitudinal Welds ML20155H7721998-10-12012 October 1998 Rev 1 to COLR for Peach Bottom Atomic Power Station Unit 2, Reload 12,Cycle 13 05000277/LER-1998-006-02, :on 980915,automatic RWCU Isolation Occurred While Placing RWCU Sys in Svc.Caused by Unexpected Surge of Water.Procedure Change Was Initiated to Open MO-2-12-74 & RWCU Sys Was Successfully Returned to Svc.With1998-10-0909 October 1998
- on 980915,automatic RWCU Isolation Occurred While Placing RWCU Sys in Svc.Caused by Unexpected Surge of Water.Procedure Change Was Initiated to Open MO-2-12-74 & RWCU Sys Was Successfully Returned to Svc.With
ML20154H4771998-10-0505 October 1998 Safety Evaluation Supporting Amends 225 & 229 to Licenses DPR-44 & DPR-56,respectively ML20154J2401998-10-0505 October 1998 Safety Evaluation Supporting Amends 224 & 228 to Licenses DPR-44 & DPR-56,respectively ML20154G6631998-10-0101 October 1998 Safety Evaluation Supporting Amends 223 & 227 to Licenses DPR-44 & DPR-56,respectively ML20154G6821998-10-0101 October 1998 SER Related to Request for Relief 01A-VRR-1 Re Inservice Testing of Automatic Depressurization Sys Safety Relief Valves at Peach Bottom Atomic Power Station,Units 2 & 3 ML20154H5541998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Pbaps,Units 2 & 3. with 05000277/LER-1998-005-02, :on 980824,noted Failure to Meet TS Actions for Suppression chamber-to-drywell Vacuum Breaker Not Being Fully Seated.Caused by Personnel Failing to Take All TS Required Actions.Temporary Procedure Changes Were Made1998-09-18018 September 1998
- on 980824,noted Failure to Meet TS Actions for Suppression chamber-to-drywell Vacuum Breaker Not Being Fully Seated.Caused by Personnel Failing to Take All TS Required Actions.Temporary Procedure Changes Were Made
05000278/LER-1998-004-03, :on 980820,automatic RWCU Isolation Occurred While Placing B RWCU Sys Demineralizer in Svc.Caused by less-than-adequate Control of Equipment.Isolated B Demineralizer & Returned RWCU Sys to Svc1998-09-18018 September 1998
- on 980820,automatic RWCU Isolation Occurred While Placing B RWCU Sys Demineralizer in Svc.Caused by less-than-adequate Control of Equipment.Isolated B Demineralizer & Returned RWCU Sys to Svc
ML20153B9651998-09-14014 September 1998 Safety Evaluation Supporting Amend 9 to License DPR-12 1999-09-30
[Table view] |
Text
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CCN-90-14108-
. PHILADELPHIA ELECTRIC COMPANY PEACll BOTIDM ATOMIC POWER STATION R. D 1, Box 208
, Delta, Itnnsyh ania !?314 esua mornw-nas rowsm or xcrit Nc (717) 456-7014 l
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May 30, 1990 Docket No. 50-278 Document Control Desk U. S._ Nuclear Regulatory Commission Washington, DC 20555
SUBJECT:
Licensee Event Report Peach Bottom Atomic Power Station - Unit 3 )
This LER concerns the untimely performance of a-Technical Specification f Surveillance. j
\
Reference:
Docket No. 50-278 Report Number: 3-90-004 j Revision Number: 00 l Event Date:- 04/30/90 1 Report Date: 05/30/90 Facility: Peach Bottom Atomic Power Station RD 1, Box 208, Delta, PA 17314 l
This LER is being submitted pursuant to the requirements of 10 CFR ]
50.73(a)(2)(1)(B). !
i Sincerely, l t
lant Manager ,
cc: J. J. Lyash, USNRC Senior Re-ident Inspector T. T. Martin, USNRC, Region I 1 l
i 9006050349 900530 l PDR ADOCK 05000278 \ \
S PDC \ -
]
i NRC Form 386 U $. NUCLE A715.E1ULATORY COMMIS$10N
, APMOVED OMO EO 315&O104 LICENSEE EVENT REPORT (LF.R) ' " "a ' 8 '
F ACILITY NAME til DOCKE T NUMBER (2) P AGE i3' Peach Bottom Atomic Power Station - Unit 3 015 l 0 [0 l 0121718 1 lOFl o 13
"' Technical Specification Violation Due To Late Surveillance Caused By Test Omission I Because Of A Deficient Proceduro EVENT DATE (51 LE R NUMBER 16) REPORY DATE (7) OYMER F ACILITIES INVOLVEG 181 MONT H DAY YEAR YEAR " '
, MONTH DAY YEAR r ac4ut v hAMEs DOCKEI NUMBEH!Si 015101010 1 I l
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0l4 3l 0 9 o 9l 0 0l 0 l4 0 l0 0l 5 3l0 9l o 0 l5! 0l0[0l l l Teils REPORT IS SUOMITTED PURSUANT TO THE REQUIREMENTS OF to CF R fr ICh* pa. o' *** of t". fe'Io*mel (11)
OPE RATING
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J 20.406(aH1 Het 60 73(a H2Hm! 50.73isH2Hal LICENSEE CONT ACT FOR TH11 LER titi NAMt TELEPHONE NUMBER A. A. Fulvio, Regulatory Engineer 7111 7 4 [5 l6 l -l 710 l 1l 4 COMPLETE ONE LINE FOR E ACH COMPONENT F AILURE DESCRISED IN THl$ REPQRT (131 REPORTA LE C- LE CAUSE SYSTEM COMPONENT MANyt CAUSE SY ST E M COMPONENT R E,POR gpq f A I I I f I I I I I I I I I I I l l I l l l l l l l 1 l l
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On 4/30/90, it was discovered that Technical Specifications (Tech Specs) were violated when Main Steam Isolation Valve closure timing testing was not performed in ,
its surveillance interval which expired 4/29/90. Tech Specs require this testing to be performed every quarter during power operations. . Testing-is required to be-performed at a reduced reactor power of less then 75%. The cause of the event is an ambiguous. test procedure in that the test frequency requirement was stated as every 3 months when power is less than 75%. The test was incorrectly omitted on the basis that plant power was above 75%. The surveillance test was performed satisfactorily on 5/1/90. There were no safety consequences as a result of this event. The ambiguous surveillance test has been revised to clarify the test frequency requ rement. Other surveillances will be reviewed for similar ambiguities.
i There were 2 previous similar events identified.
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NRC Form astA .
U.S. NUCLEAll KEiULAfoRY COMMISSION /a
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. .UCENSEE EVENT REPORT (LER) TEXT CONTINUATION senoveo oue no neo-oio4
, ,.,- EXPIT.ES: 8/31/*;3
FACst:Tv Nanet up . DOCKET NUMBER (23 LGR NUMetR (4) PAOt (3)
P:ach Bottom Atomic. Power Station "'" TN UsN
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, itXT II rnere spece e reWrect, use ed*oone/ NAC Form J864W H7) .
Requirement: for the Report
<This report is required per 10 CFR 50.73(a)(2)(1)(B) because.of a condition
- prohibited by Technical ~ Specifications (Tech Specs).
~
y Unit Status at Time of the Event (4/29/90)
Unit 3 was-in the RUN-Mode at 99.8% rated power.
There~were no structures, components or systems that were inoperable at the time of
~
the' event that contributed to the event.
Description of the Event On:4/30/90,-Operations Management personnel discovered that Tech Spec 4.7,0.1.b(2)
- was violated when Main Steam Isolation Valve (EIIS:V) closure timing testing was not i performed within its surveillance interval. Surveillance Test (ST) 6.4, " Main-Steam Isolation Valve Closure Timing" is required to be performed every quarter during l power operation conditions. The 25% late grace period allowed by Tech Specs expired on 4/29/90 for this test. Tech Spec requires the performance of this surveillance to be done at a reduced Reactor (EIIS:RPV) power less than 75% of rated. A Reactor
. power reduction was started 5/1/90, 0008 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />, and the surveillance was completed satisfactorily by 5/1/90, 0333 hours0.00385 days <br />0.0925 hours <br />5.505952e-4 weeks <br />1.267065e-4 months <br />.
Cause of the Event The root cause of this event is an ambiguous surveillance test procedure that resulted in an error in omitting ST 6.4 from the test schedule. ST 6.4 is ambiguous 3 Lin that the test frequency indicates that the test is required to be performed every three months when reactor power is less than 75%. Tech Spec 4.7,0.1.b(2) requires the test to be performed during power operations evfry quarter at a power-level less than 75%. The-test had been incorrectly omitted on 3/6/90 by.the Operations cognizant engineer who coordinates surveillance performance (Non-utility, Non-licensed). . The test was scheduled to be performed during the week starting 3/12/90.
The test was omitted on the basis that it was required to be performed when operating
~
at a Reactor power of less-than 75% and although the-plant was shutdown on 3/6/90, it.
was expected.to be at full power before the scheduled week of performance. .!
1A-contributing cause to this event is ambiguity within the Tech Spec surveillance requirement 4.7,0.1.b(2). This Tech Spec states "with reactor power less.than 75%
' trip main steam isolation valves individually and verify closure time". On 3/10/90,
-the Operations Unit Coordinator (Utility, Licensed) reviewed the omission of this
-test. He consulted Tech Specs but believed that this Tech Spec required the testing only if the reactor is being operated c.t a power of less than 75%. Since it was expected that Reactor power would be greater than 75% by the scheduled performance, the Operations Unit Coordinator concurred with the omission.
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". LICENSEE EVENT REPORT ILER) TEXT CONTINUATION uenovEo ous No mo-oio4 y, . .%' (XPIRES: $/$1C FActLITY NAME (1) DOCKET NUMeER (2) LER NUMe(R le) PAGE(3) i 1Paach Bottom Atomic Power Station "'" "UN#' :
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ol0 ol3 oF ol 3 TEXT W mese spece 4 tr7pired, ano sapeanst 44C Form 354 W (1h
, Analysis of the Event L)
There were no actual safety consequences that occurred as a result of this event.
. Surveillance testing performed on 5/1/90 proved that the Main Steam Isolation Valves i (MSIVs) were operable. NRC' Generic Letter 37-09 states that it is overly conservative to assume that systems or components are inoperable when a surveillance ,
has not oeen performed. The purpose of ST 6.4 is to verify that the MSIVs are capable of closing in 3 to 5 seconds to limit the release of radioactive materials and' reactor coolant in design basis events.
Corrective Actions-ST 6.4 has bsen revised to clarify the test frequency requirements. A review of other surveillance tests will be performed to detect ambiguity in test. frequency requirements. Surveillance tests will be revised as-required, j It is expected that the test frequency ambiguity that exists in Tech Specs will be corrected.in the Technical Specification improvement Program that is being pursued by .
PECo in accordance with the Boiling Water Reactor (BWR) Owner's Group's improved BWR'
- Tech Specs effort.
Previous-Similar Events There were 2 previous similar events identified in which surveillance tests were incorrectly placed on the omitted test report resulting in Tech Spec violations. LER
'2-90-005 concerned omitting a Radiation Monitor functional Test Surveillance due to
-personnel error involving a misinterpretation of Tech Specs. LER 2-89-032 concerned omitting a Control Rod Exercise Surveillance due to personnel error in failing to follcw procedures. Corrective actions for these LERs involved personnel counseling and enhanced omitted test report review. These corrective actions did not prevent this event because the ccuse-was an ambiguous test procedure.
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