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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20045A4291993-06-0303 June 1993 LER 93-003-00:on 930505,new Source of Natural Gas Introduced within 0.5 Miles of ISFSI & Reactor Bldg W/O Prior NRC Approval.Caused by Field Routing of Natural Gas Pipe.Well Isolated by Well operator.W/930603 Ltr ML20043E0991990-05-31031 May 1990 LER 89-018-01:on 890827,cracking Found in Incoloy Alloy 800 Main Steam Ringheaders & Condition Determined to Have Generic Implications.Caused by Creep Failure.Main Steam Ringheaders repaired.W/900531 Ltr ML20042G4211990-05-10010 May 1990 LER 90-001-00:on 900410,non-essential Bus 5,4160/480-volt Transformer N-9215 Experienced Fault.Caused by Breakdown of Insulation on Secondary Coils of Transformer.Coils of Transformer rewound.W/900510 Ltr ML20011D4641989-12-20020 December 1989 LER 89-014-01:on 890818,four Fire Barrier Penetration Seals in Bldg 10 Did Not Meet Foam Seal Structure Criteria of Seal Spec.Caused by Improper Curing During Installation.Fire Watch Established & Seals repaired.W/891220 Ltr ML20024E0021983-07-29029 July 1983 LER 83-023/03L-0:on 830701 & 02,emergency Feedwater Unavailable to Drive Loop I Helium Circulation Water Turbines.Caused by Normal Wear of Valve PV-21243.Valve Internals Replaced & Valve calibr.W/830729 Ltr ML20024B9861983-07-0101 July 1983 LER 83-020/03L-0:on 830604,emergency Feedwater Header Supply to Loop I Helium Circulator Turbine Water Drive Isolated & Bearing Water Make Up Pump Taken Out of Svc.Caused by Flexitallic Gasket Failure Due to Normal wear.W/830701 Ltr ML20024A8521983-06-22022 June 1983 Updated LER 80-041/03X-2:on 800724,one of 12 Helium Circulator Seal Malfunction Pressure Differential Switches Discovered W/Trip Point Outside Tech Spec Limits.Caused by Dirt Accumulation in Electrical switches.W/830622 Ltr ML20023D9021983-05-26026 May 1983 LER 83-017/01T-0:on 830512,insp Performed Per IE Bulletin 83-03 Identified Six of Eight Check Valves Frozen in mid- Position.Caused by Corrosion & Rusting Valve Internal Parts. Valves Cleaned & Internal Components Replaced ML20028G2831983-01-28028 January 1983 LER 82-053/03L-0:on 821229,fuel Storage Well Pressure Exceeded Atmospheric Pressure While Reactor Was Shut Down. Caused by One Gas Compressor Being Out of Svc for Maint and Other Pumping Less than Capacity.Compressors Repaired ML20028G2711983-01-28028 January 1983 LER 82-054/03L-0:on 821229,outlet Temps Exceeded 120 F Limit When Reactor Became Critical During Isolation of Svc Water Flow to Pcrv Cooling Water Hx.Caused by Lack of Cooling Source.Design Change Initiated ML20028F2401983-01-19019 January 1983 LER 82-051/03L-0:on 821220,during Surveillance Test,One of Six Steam Pipe Rupture & One of 12 Steam Pipe Rupture Channels Identified Inoperable Due to Low Response to Calibr Noise.Caused by Failure of Resistor ML20028F2881983-01-17017 January 1983 LER 83-001/01T-0:on 830101 & 02,reactor Operated W/O Min Number of Operable Moisture Monitor Channels Required Per Table 4.4.1 of Limiting Conditions for Operation.Caused by Personnel Misinterpretation of Tech Specs ML20028A3101982-11-10010 November 1982 LER 82-042/03L-0:on 821013,unplanned Radioactive Gas Release Occurred W/Reactor Shutdown & Depressurized.Caused by High Airborne Activity in Reactor Bldg Due to Leaking Blank Flange.Emergency Procedures Initiated.Flange Repaired ML20028A2861982-11-10010 November 1982 LER 82-041/03L-0:on 821011,during Calibr of Radioactive Liquid Effluent Monitors,Trip Point for RIS-6212 Found to Be Less Conservative than Required.Caused by Instrument Drift. High Voltage & Discriminator Settings Adjusted ML20023A7451982-10-0808 October 1982 LER 82-036/03L-0:on 820908,one of Two Bearing Water Makeup Pumps Removed from Svc.Caused by Need to Rebuild Mechanical Seal Due to Normal Wear.Seal Rebuilt ML20052H9881982-05-12012 May 1982 LER 82-011/03L-0:during 820412-20,plant Operated in Degraded Mode of Limiting Conditions for Operation 4.2.11 Three Times & 4.2.10 Once.Caused by Offgas of Moisture from Core as Plant Returned to Power from Maint Outage ML20052H8751982-05-12012 May 1982 LER 82-013/03L-0:on 820412,separation in Axial Positions of Two Partially Inserted Control Rod Groups Fell Slightly Below Limit of 10 Ft.Cause Not Stated.Control Rods Repositioned ML20052G4151982-05-10010 May 1982 LER 82-012/03L-0:on 820410,at 10% Power,Instrument Air Compressor 1C Temporarily Taken Out of Svc to Repair after- Cooler Leak.Water Leak Caused by Normal Wear of after- Cooler.Air Compressor Returned to Svc After Repairs ML20052A3331982-04-27027 April 1982 LER 81-044 Has Been Cancelled ML20050B2541982-03-19019 March 1982 LER 82-006/03L-0:on 820218,primary Coolant Moisture Exceeded Tech Specs.Caused by Contamination W/Moisture During Maint Outage.Reactor Shutdown & Coolant Purification Trains Utilized to Reduce Impurity Levels ML20042B8231982-03-17017 March 1982 LER 82-005/03L-0:on 820215,loop 2 Steam Generator Penetration Rupture Disk 1 Leak Alarm Pressure Switch Found Isolated.Caused by Closed Pressure Switch Isolation Valve.Valve Opened ML20041F5791982-03-0808 March 1982 LER 82-007/01T-0:on 820222,control Rod Pairs for Regions 7 & 28 Did Not Insert Automatically Following Manual Scram. Possibly Caused by Binding or Sticking of Control Rod Drive Mechanism.Control Rods Exercised to Eliminate Sticking ML20041C3231982-02-19019 February 1982 LER 82-002/03L-0:on 820121,during Surveillance Testing, W/Reactor Shut Down,Three Loss of Bearing Water Pressure Differential Switches Found W/Setpoints Less Conservative than Required.Caused by Instrument Drift.Switches Recalibr ML20041C2761982-02-19019 February 1982 LER 82-003/03L-0:on 820122,one Drain Malfunction Pressure Differential Switch on 1C Helium Circulator Found Less Conservative than Tech Specs.Caused by Dirty Contacts. Contacts Cleaned & Switch Recalibr ML20041A9891982-02-16016 February 1982 LER 82-004/01T-0:on 820202,inadvertent Radioactive Liquid Waste Release Occurred from Receiver a During Plant Shutdown for Design Mods to Circulator Auxiliary Sys.Caused by Improper Valve Lineup.Event Reviewed W/Operators ML20040G9511982-02-0505 February 1982 LER 82-001/03L-0:on 820108,18 Snubbers Found Inoperable During Surveillance Testing,Indicating Inoperability During Reactor Operation.Caused by Seal Leakage & Deficiencies in Piston Position & Oil Level.Snubbers Repaired ML20040B8081982-01-13013 January 1982 LER 81-074/03L-0:on 811214,cold Reheat Snubber CRS-219 Found Detached from Pipe Mounting,Rendering Snubber Operable.Caused by Failure of Cotter Pin,Allowing Eyebolt to Be Displaced Out of Pipe & Snubber Rod Mounting ML20040B7911982-01-12012 January 1982 LER 81-075/03L-0:on 811221,two Sample Flow Circuits Found Out of Calibr During Annual Calibr of Primary Coolant Moisture Scram Instrumentation.Caused by Change in Instrument Characteristics.Procedures Being Revised ML20039F4911982-01-0404 January 1982 LER 81-073/03L-0:on 811208,one Helium Circulator Bearing Drain Pressure Low Switch Found to Have Trip Point Outside Required Limits.Caused by Dirt Accumulation in Electrical Switch That Impeded Contact ML20039C6321981-12-17017 December 1981 LER 81-072/03L-0:on 811117,PCRV Rupture Disk M-11701 Setpoint Exceeded Tech Specs Limits.Caused by Belleville Washer Operating Point Drift.Disks Under Evaluation ML20011A6371981-10-22022 October 1981 LER 81-060/03L-0:between 810922-1013,emergency Feedwater to Loop 1 Helium Circulator Water Turbine Drives Was Isolated on Three Occasions.Caused by Leakage Between Seat Ring & Valve Body Pressure Control Valve ML20010H9131981-09-11011 September 1981 LER 81-052/03L-0:on 810812,standby Bearing Water Makeup Pump Removed from Svc.Caused by Need to Repair Bonnet Leak in Valve in Suction Line to Pump.Pump Returned to Svc After Repair Completed ML20010J0141981-09-11011 September 1981 LER 81-050/03L-0:on 810814,total Dissolved Solids in Plant Nonradioactive Liquid Waste Effluent for 810809 Was Discovered to Have Exceeded Tech Specs.Caused by Improper Circulating Water Blowdown Arrangement.Blowdown Adjusted ML20010H8821981-09-0404 September 1981 LER 81-048/03L-0:on 810808 & 25 Loop 1 Prestressed Concrete Reactor Vessel Cooling Water Outlet Temp Exceeded 120 F Due to Failure of Temp Controller.Caused by Cold Solder Joint & Failure of Transistor in Output Circuit,Respectively ML20010H9301981-09-0101 September 1981 LER 81-049/03L-0:during 810802-07,increase Occurred in Offgassing from Core & Core Outlet Temps.Caused by Increased Primary Coolant Moisture & Oxidants from Refueling Shutdown ML20010G2711981-08-26026 August 1981 LER 81-046/03L-0:on 810728,emergency Feedwater Supply to Loop 1 Helium Circular Water Turbines Isolated to Repair Leaking 2-inch Consolidated Safety Relief Valves.Caused by Valve Leakage Downstream of Pressure Control Valve ML20010G1691981-08-26026 August 1981 LER 81-045/03L-0:on 810727,during Normal Startup Operation, Primary Coolant Dewpoint Exceeded Tech Spec Limits.Caused by Contamination Due to Moisture.Contaminants Removed from Primary Coolant ML20010G3371981-08-20020 August 1981 LER 81-051/03L-0:on 810721,Class I Snubbers Removed from Svc for Structural Mods W/Plant Operating at Power.Caused by Seismic Restraint Analysis Program.Snubbers Returned to Svc Following Mods ML20010G3181981-08-14014 August 1981 LER 81-043/03L-0:on 810717 & 0807,reactor Operated at Power W/One Class I Snubber Inoperable.Caused by Empty Oil Reservoirs on BFS-398E & MSS-149 Due to Leaking Fitting on Valve Block & Leaking Piston Seal.Fitting Tightened ML20010A1601981-07-16016 July 1981 LER 81-041/03L-0:on 810616,control Room Exhaust Damper Failed to Close.Caused by Dust Accumulation on Damper Vanes. Damper Operated Properly When Retested.Preventive Maint Program to Be Developed to Inspect & Clean Vanes ML20009E5101981-07-0202 July 1981 LER 81-039/03L-0:on 810602,following Routine Chlorination of Circulating Water Sys,Sample Indicated Excessive Residual Chlorine in Plant Liquid Effluent.Cause Unknown.Subsequent Chlorinations Showed No Abnormalities ML20009E5581981-07-0202 July 1981 LER 81-040/03L-0:between 810604 & 09,eight Hydraulic Shock Suppressors Were Found Out of Oil.Caused by Empty Hydraulic Oil Reservoirs Due to Leaking Seals & O-rings in Snubbers. Reservoirs Cleaned.Seals & O-rings Replaced ML20009E7191981-06-18018 June 1981 Revised LER 81-008/03X-1:on 810120,during Shutdown Maint & Primary Coolant Pressure Scram Calibr,Voltage Outputs of Pressure Transmitter Discovered High.Caused by Instrument Drift.Transmitter Calibr.Surveillance Test Completed ML20009E7011981-06-10010 June 1981 LER 81-035/03L-0:on 810511,w/plant at 70% Thermal Power During a Diesel Generator Set Surveillance Test,B Engine Tripped & Declutched.Caused by Failed Exhaust Temp Switch. Switch Repaired.Test Completed.Generator Returned to Svc ML20009A5501981-06-0505 June 1981 LER 81-038/03L-0:on 810507,two Class I Hydraulic Shock Suppressors Removed from Svc.Caused by Decision to Modify Suppressors to Original Configuration W/Zero Bleed Rate Block Valves ML20009A5341981-06-0303 June 1981 LER 81-034/03L-0:on 810504,equipment Necessary to Terminate Release from Liquid Waste Sys & Reactor Sump Found Not Operating Properly.Caused by Plugged Sense Lines on Flow Element Associated W/Control Valve ML20009A5281981-05-28028 May 1981 LER 81-032/03L-0:on 810428,hot Reheat Snubber HRS-244 Found Inoperable.Caused by Empty Hydraulic Oil Reservoir Due to Leaking Elbow Fitting.Fitting Tightened,Reservoir Refilled & Snubber Returned to Svc ML20004D5781981-05-27027 May 1981 LER 81-036/01T-0:on 810512,liquid Waste Discharge Exceeded Specified Limit for Tritium Concentration.Caused by Design Deficiency.Downstream of Valve HV 6212,150-200 Gallon Dead Leg Released Regardless of Dilution Flow Adequacy ML20004D7171981-05-27027 May 1981 LER 81-031/03L-0:on 810427,during Normal Surveillance Testing,Diesel Engine B Tripped & Declutched on Starting. Caused by Load Imbalance Between Engines a & B Due to Normal Wear of Linkage.Linkage Was Adjusted ML20004D6661981-05-27027 May 1981 LER 81-033/03L-0:on 810427,helium Circulator 1C Speed/Wobble Modifier Malfunctioned Causing Loss of Plant Protective Sys Functions to High Speed Trip Circuits.Caused by Electronic Circuit Unbalance.Spare Speed Element Installed 1993-06-03
[Table view] Category:RO)
MONTHYEARML20045A4291993-06-0303 June 1993 LER 93-003-00:on 930505,new Source of Natural Gas Introduced within 0.5 Miles of ISFSI & Reactor Bldg W/O Prior NRC Approval.Caused by Field Routing of Natural Gas Pipe.Well Isolated by Well operator.W/930603 Ltr ML20043E0991990-05-31031 May 1990 LER 89-018-01:on 890827,cracking Found in Incoloy Alloy 800 Main Steam Ringheaders & Condition Determined to Have Generic Implications.Caused by Creep Failure.Main Steam Ringheaders repaired.W/900531 Ltr ML20042G4211990-05-10010 May 1990 LER 90-001-00:on 900410,non-essential Bus 5,4160/480-volt Transformer N-9215 Experienced Fault.Caused by Breakdown of Insulation on Secondary Coils of Transformer.Coils of Transformer rewound.W/900510 Ltr ML20011D4641989-12-20020 December 1989 LER 89-014-01:on 890818,four Fire Barrier Penetration Seals in Bldg 10 Did Not Meet Foam Seal Structure Criteria of Seal Spec.Caused by Improper Curing During Installation.Fire Watch Established & Seals repaired.W/891220 Ltr ML20024E0021983-07-29029 July 1983 LER 83-023/03L-0:on 830701 & 02,emergency Feedwater Unavailable to Drive Loop I Helium Circulation Water Turbines.Caused by Normal Wear of Valve PV-21243.Valve Internals Replaced & Valve calibr.W/830729 Ltr ML20024B9861983-07-0101 July 1983 LER 83-020/03L-0:on 830604,emergency Feedwater Header Supply to Loop I Helium Circulator Turbine Water Drive Isolated & Bearing Water Make Up Pump Taken Out of Svc.Caused by Flexitallic Gasket Failure Due to Normal wear.W/830701 Ltr ML20024A8521983-06-22022 June 1983 Updated LER 80-041/03X-2:on 800724,one of 12 Helium Circulator Seal Malfunction Pressure Differential Switches Discovered W/Trip Point Outside Tech Spec Limits.Caused by Dirt Accumulation in Electrical switches.W/830622 Ltr ML20023D9021983-05-26026 May 1983 LER 83-017/01T-0:on 830512,insp Performed Per IE Bulletin 83-03 Identified Six of Eight Check Valves Frozen in mid- Position.Caused by Corrosion & Rusting Valve Internal Parts. Valves Cleaned & Internal Components Replaced ML20028G2831983-01-28028 January 1983 LER 82-053/03L-0:on 821229,fuel Storage Well Pressure Exceeded Atmospheric Pressure While Reactor Was Shut Down. Caused by One Gas Compressor Being Out of Svc for Maint and Other Pumping Less than Capacity.Compressors Repaired ML20028G2711983-01-28028 January 1983 LER 82-054/03L-0:on 821229,outlet Temps Exceeded 120 F Limit When Reactor Became Critical During Isolation of Svc Water Flow to Pcrv Cooling Water Hx.Caused by Lack of Cooling Source.Design Change Initiated ML20028F2401983-01-19019 January 1983 LER 82-051/03L-0:on 821220,during Surveillance Test,One of Six Steam Pipe Rupture & One of 12 Steam Pipe Rupture Channels Identified Inoperable Due to Low Response to Calibr Noise.Caused by Failure of Resistor ML20028F2881983-01-17017 January 1983 LER 83-001/01T-0:on 830101 & 02,reactor Operated W/O Min Number of Operable Moisture Monitor Channels Required Per Table 4.4.1 of Limiting Conditions for Operation.Caused by Personnel Misinterpretation of Tech Specs ML20028A3101982-11-10010 November 1982 LER 82-042/03L-0:on 821013,unplanned Radioactive Gas Release Occurred W/Reactor Shutdown & Depressurized.Caused by High Airborne Activity in Reactor Bldg Due to Leaking Blank Flange.Emergency Procedures Initiated.Flange Repaired ML20028A2861982-11-10010 November 1982 LER 82-041/03L-0:on 821011,during Calibr of Radioactive Liquid Effluent Monitors,Trip Point for RIS-6212 Found to Be Less Conservative than Required.Caused by Instrument Drift. High Voltage & Discriminator Settings Adjusted ML20023A7451982-10-0808 October 1982 LER 82-036/03L-0:on 820908,one of Two Bearing Water Makeup Pumps Removed from Svc.Caused by Need to Rebuild Mechanical Seal Due to Normal Wear.Seal Rebuilt ML20052H9881982-05-12012 May 1982 LER 82-011/03L-0:during 820412-20,plant Operated in Degraded Mode of Limiting Conditions for Operation 4.2.11 Three Times & 4.2.10 Once.Caused by Offgas of Moisture from Core as Plant Returned to Power from Maint Outage ML20052H8751982-05-12012 May 1982 LER 82-013/03L-0:on 820412,separation in Axial Positions of Two Partially Inserted Control Rod Groups Fell Slightly Below Limit of 10 Ft.Cause Not Stated.Control Rods Repositioned ML20052G4151982-05-10010 May 1982 LER 82-012/03L-0:on 820410,at 10% Power,Instrument Air Compressor 1C Temporarily Taken Out of Svc to Repair after- Cooler Leak.Water Leak Caused by Normal Wear of after- Cooler.Air Compressor Returned to Svc After Repairs ML20052A3331982-04-27027 April 1982 LER 81-044 Has Been Cancelled ML20050B2541982-03-19019 March 1982 LER 82-006/03L-0:on 820218,primary Coolant Moisture Exceeded Tech Specs.Caused by Contamination W/Moisture During Maint Outage.Reactor Shutdown & Coolant Purification Trains Utilized to Reduce Impurity Levels ML20042B8231982-03-17017 March 1982 LER 82-005/03L-0:on 820215,loop 2 Steam Generator Penetration Rupture Disk 1 Leak Alarm Pressure Switch Found Isolated.Caused by Closed Pressure Switch Isolation Valve.Valve Opened ML20041F5791982-03-0808 March 1982 LER 82-007/01T-0:on 820222,control Rod Pairs for Regions 7 & 28 Did Not Insert Automatically Following Manual Scram. Possibly Caused by Binding or Sticking of Control Rod Drive Mechanism.Control Rods Exercised to Eliminate Sticking ML20041C3231982-02-19019 February 1982 LER 82-002/03L-0:on 820121,during Surveillance Testing, W/Reactor Shut Down,Three Loss of Bearing Water Pressure Differential Switches Found W/Setpoints Less Conservative than Required.Caused by Instrument Drift.Switches Recalibr ML20041C2761982-02-19019 February 1982 LER 82-003/03L-0:on 820122,one Drain Malfunction Pressure Differential Switch on 1C Helium Circulator Found Less Conservative than Tech Specs.Caused by Dirty Contacts. Contacts Cleaned & Switch Recalibr ML20041A9891982-02-16016 February 1982 LER 82-004/01T-0:on 820202,inadvertent Radioactive Liquid Waste Release Occurred from Receiver a During Plant Shutdown for Design Mods to Circulator Auxiliary Sys.Caused by Improper Valve Lineup.Event Reviewed W/Operators ML20040G9511982-02-0505 February 1982 LER 82-001/03L-0:on 820108,18 Snubbers Found Inoperable During Surveillance Testing,Indicating Inoperability During Reactor Operation.Caused by Seal Leakage & Deficiencies in Piston Position & Oil Level.Snubbers Repaired ML20040B8081982-01-13013 January 1982 LER 81-074/03L-0:on 811214,cold Reheat Snubber CRS-219 Found Detached from Pipe Mounting,Rendering Snubber Operable.Caused by Failure of Cotter Pin,Allowing Eyebolt to Be Displaced Out of Pipe & Snubber Rod Mounting ML20040B7911982-01-12012 January 1982 LER 81-075/03L-0:on 811221,two Sample Flow Circuits Found Out of Calibr During Annual Calibr of Primary Coolant Moisture Scram Instrumentation.Caused by Change in Instrument Characteristics.Procedures Being Revised ML20039F4911982-01-0404 January 1982 LER 81-073/03L-0:on 811208,one Helium Circulator Bearing Drain Pressure Low Switch Found to Have Trip Point Outside Required Limits.Caused by Dirt Accumulation in Electrical Switch That Impeded Contact ML20039C6321981-12-17017 December 1981 LER 81-072/03L-0:on 811117,PCRV Rupture Disk M-11701 Setpoint Exceeded Tech Specs Limits.Caused by Belleville Washer Operating Point Drift.Disks Under Evaluation ML20011A6371981-10-22022 October 1981 LER 81-060/03L-0:between 810922-1013,emergency Feedwater to Loop 1 Helium Circulator Water Turbine Drives Was Isolated on Three Occasions.Caused by Leakage Between Seat Ring & Valve Body Pressure Control Valve ML20010H9131981-09-11011 September 1981 LER 81-052/03L-0:on 810812,standby Bearing Water Makeup Pump Removed from Svc.Caused by Need to Repair Bonnet Leak in Valve in Suction Line to Pump.Pump Returned to Svc After Repair Completed ML20010J0141981-09-11011 September 1981 LER 81-050/03L-0:on 810814,total Dissolved Solids in Plant Nonradioactive Liquid Waste Effluent for 810809 Was Discovered to Have Exceeded Tech Specs.Caused by Improper Circulating Water Blowdown Arrangement.Blowdown Adjusted ML20010H8821981-09-0404 September 1981 LER 81-048/03L-0:on 810808 & 25 Loop 1 Prestressed Concrete Reactor Vessel Cooling Water Outlet Temp Exceeded 120 F Due to Failure of Temp Controller.Caused by Cold Solder Joint & Failure of Transistor in Output Circuit,Respectively ML20010H9301981-09-0101 September 1981 LER 81-049/03L-0:during 810802-07,increase Occurred in Offgassing from Core & Core Outlet Temps.Caused by Increased Primary Coolant Moisture & Oxidants from Refueling Shutdown ML20010G2711981-08-26026 August 1981 LER 81-046/03L-0:on 810728,emergency Feedwater Supply to Loop 1 Helium Circular Water Turbines Isolated to Repair Leaking 2-inch Consolidated Safety Relief Valves.Caused by Valve Leakage Downstream of Pressure Control Valve ML20010G1691981-08-26026 August 1981 LER 81-045/03L-0:on 810727,during Normal Startup Operation, Primary Coolant Dewpoint Exceeded Tech Spec Limits.Caused by Contamination Due to Moisture.Contaminants Removed from Primary Coolant ML20010G3371981-08-20020 August 1981 LER 81-051/03L-0:on 810721,Class I Snubbers Removed from Svc for Structural Mods W/Plant Operating at Power.Caused by Seismic Restraint Analysis Program.Snubbers Returned to Svc Following Mods ML20010G3181981-08-14014 August 1981 LER 81-043/03L-0:on 810717 & 0807,reactor Operated at Power W/One Class I Snubber Inoperable.Caused by Empty Oil Reservoirs on BFS-398E & MSS-149 Due to Leaking Fitting on Valve Block & Leaking Piston Seal.Fitting Tightened ML20010A1601981-07-16016 July 1981 LER 81-041/03L-0:on 810616,control Room Exhaust Damper Failed to Close.Caused by Dust Accumulation on Damper Vanes. Damper Operated Properly When Retested.Preventive Maint Program to Be Developed to Inspect & Clean Vanes ML20009E5101981-07-0202 July 1981 LER 81-039/03L-0:on 810602,following Routine Chlorination of Circulating Water Sys,Sample Indicated Excessive Residual Chlorine in Plant Liquid Effluent.Cause Unknown.Subsequent Chlorinations Showed No Abnormalities ML20009E5581981-07-0202 July 1981 LER 81-040/03L-0:between 810604 & 09,eight Hydraulic Shock Suppressors Were Found Out of Oil.Caused by Empty Hydraulic Oil Reservoirs Due to Leaking Seals & O-rings in Snubbers. Reservoirs Cleaned.Seals & O-rings Replaced ML20009E7191981-06-18018 June 1981 Revised LER 81-008/03X-1:on 810120,during Shutdown Maint & Primary Coolant Pressure Scram Calibr,Voltage Outputs of Pressure Transmitter Discovered High.Caused by Instrument Drift.Transmitter Calibr.Surveillance Test Completed ML20009E7011981-06-10010 June 1981 LER 81-035/03L-0:on 810511,w/plant at 70% Thermal Power During a Diesel Generator Set Surveillance Test,B Engine Tripped & Declutched.Caused by Failed Exhaust Temp Switch. Switch Repaired.Test Completed.Generator Returned to Svc ML20009A5501981-06-0505 June 1981 LER 81-038/03L-0:on 810507,two Class I Hydraulic Shock Suppressors Removed from Svc.Caused by Decision to Modify Suppressors to Original Configuration W/Zero Bleed Rate Block Valves ML20009A5341981-06-0303 June 1981 LER 81-034/03L-0:on 810504,equipment Necessary to Terminate Release from Liquid Waste Sys & Reactor Sump Found Not Operating Properly.Caused by Plugged Sense Lines on Flow Element Associated W/Control Valve ML20009A5281981-05-28028 May 1981 LER 81-032/03L-0:on 810428,hot Reheat Snubber HRS-244 Found Inoperable.Caused by Empty Hydraulic Oil Reservoir Due to Leaking Elbow Fitting.Fitting Tightened,Reservoir Refilled & Snubber Returned to Svc ML20004D5781981-05-27027 May 1981 LER 81-036/01T-0:on 810512,liquid Waste Discharge Exceeded Specified Limit for Tritium Concentration.Caused by Design Deficiency.Downstream of Valve HV 6212,150-200 Gallon Dead Leg Released Regardless of Dilution Flow Adequacy ML20004D7171981-05-27027 May 1981 LER 81-031/03L-0:on 810427,during Normal Surveillance Testing,Diesel Engine B Tripped & Declutched on Starting. Caused by Load Imbalance Between Engines a & B Due to Normal Wear of Linkage.Linkage Was Adjusted ML20004D6661981-05-27027 May 1981 LER 81-033/03L-0:on 810427,helium Circulator 1C Speed/Wobble Modifier Malfunctioned Causing Loss of Plant Protective Sys Functions to High Speed Trip Circuits.Caused by Electronic Circuit Unbalance.Spare Speed Element Installed 1993-06-03
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20196G6731997-07-0101 July 1997 Informs Commission That Decommissioning Process Has Been Completed at PSC of Colorado Fsvngs,Unit 1 Located in Town of Platteville in Weld County,Co ML20141K9961997-05-0505 May 1997 Safety Evaluation Supporting Amend 89 to License DPR-34 ML20140E1121997-04-10010 April 1997 Confirmatory Survey of Group Effluent Discharge Pathway Areas for Fsv Nuclear Station,Platteville,Co ML20134D1661997-01-30030 January 1997 Rev 1,Vol 6 to Final Survey Rept,Final Survey of Group E (Book 2A of 2) ML20137S6111996-12-31031 December 1996 Annual Rept Pursuant to Section 13 or 15(d) of Securities Exchange Act 1934, for Fy Ended Dec 1996 ML20134G6401996-10-29029 October 1996 Rev 0,Volume 6,Books 1 & 2 of 2 to Final Survey of Group E ML20134G6171996-10-29029 October 1996 Rev 2,Volume 1,Books 1 & 2 of 2 to Final Survey Description & Results ML20134G7271996-10-29029 October 1996 Rev 0,Volume 11,Book 1 of 1 to Final Survey of Group J ML20134G6861996-10-29029 October 1996 Rev 0,Volume 8,Books 1 & 2 of 2 to, Final Survey of Group G ML20134G6321996-10-26026 October 1996 Rev 1,Volume 5,Books 2 & 3 of 3 to Final Survey of Group D ML20133D7831996-10-22022 October 1996 Preliminary Rept - Orise Support of NRC License Insp at Fsv on 960930-1003 ML20116A4661996-07-19019 July 1996 Fsv Final Survey Exposure Rate Measurements ML20112J6861996-05-31031 May 1996 June 1996 Quarterly 10CFR50.59 Rept of Changes,Tests & Experiments for Fsv Decommissioning.Rept Covers Period of 960216-0531 ML20112C1531996-05-17017 May 1996 Fsv Final Survey Exposure Rate Measurements ML20101G5521996-03-21021 March 1996 Confirmatory Survey Activities for Fsv Nuclear Station PSC Platteville,Co, Final Rept ML20097E3201996-01-31031 January 1996 Nonproprietary Fort St Vrain Technical Basis Documents for Piping Survey Instrumentation ML20095K4131995-12-26026 December 1995 Rev 3 to Decommissioning Plan ML20095H7211995-12-20020 December 1995 Revs to Fort St Vrain Decommissioning Fire Protection Plan Update ML20095K9751995-12-15015 December 1995 Fort St Vrain Project Update Presentation to NRC, on 951207 & 15 ML20096C1671995-12-13013 December 1995 Rev 4 to Decommissioning Fire Protection Plan ML20094M1651995-11-30030 November 1995 Nonproprietary Fsv Technical Basis Documents for Piping Survey Implementation ML20092F3461995-09-14014 September 1995 Quarterly 10CFR50.59 Rept of Changes,Tests & Experiments for Fsv Decommissioning, Covering Period of 950516-0815.W/ ML20137H3531994-12-31031 December 1994 Partially Withheld, Rept of Independent Counsel Investigation Concerning Issues at Fort St Vrain Nuclear Generating Station Decommissioning Project, App D,Comments by Mkf & Westinghouse Team & Responses ML20137S2331994-12-31031 December 1994 Rept of Independent Counsel Investigation Concerning Issues at Fort St Vrain Nuclear Generating Station Decommissioning Project, Dec 1994 ML20029C6031993-12-31031 December 1993 1993 Annual Rept Public Svc Co of Colorado. W/940405 Ltr ML20058Q3791993-12-21021 December 1993 Rev 1 to Decommissioning Plan for Fort St Vrain Nuclear Generating Station ML20045B3641993-06-30030 June 1993 June 1993 Quarterly 10CFR50.59 Rept of Changes,Tests & Experiments for Fsv Decommissioning. ML20045A4291993-06-0303 June 1993 LER 93-003-00:on 930505,new Source of Natural Gas Introduced within 0.5 Miles of ISFSI & Reactor Bldg W/O Prior NRC Approval.Caused by Field Routing of Natural Gas Pipe.Well Isolated by Well operator.W/930603 Ltr ML20077D1631993-05-10010 May 1993 Enforcement Conference, in Arlington,Tx ML20125C7161992-12-0707 December 1992 Part 21 Rept Re Possibility for Malfunction of Declutching Mechanisms in SMB/SB-000 & SMB/SB/SBD-00 Actuators. Malfunction Only Occurs During Seismic Event.Balanced Levers May Be Purchased from Vendor.List of Affected Utils Encl ML20128D7191992-12-0101 December 1992 Safety Evaluation Approving Exemption from Requirement of 10CFR50.54(q) to Change to Biennial Emergency Plan Exercise Rather than Annual Following Completion of Next Scheduled Exercise at Plant ML20127P5861992-11-23023 November 1992 Followup to 921005 Part 21 Rept Re Potential Defect in SB/SBD-1 Housing Cover Screws.Procedure Re Replacement of SBD-1 Spring Cover Bolts Encl.All Fasteners Should Be Loosened & Removed.List of Affected Utils Encl ML20127F5691992-11-0303 November 1992 Informs Commission of Intent to Issue Order Approving Plant Decommissioning Plan & Corresponding Amend to License DPR-34 ML20101E5761992-05-31031 May 1992 Monthly Defueling Operations Rept for May 1992 for Fort St Vrain ML20096E8221992-04-30030 April 1992 Monthly Operating Rept for Apr 1992 for Fort St Vrain.W/ ML20095E9601992-04-17017 April 1992 Rev to Fort St Vrain Proposed Decommissioning Plan ML20100R7431992-03-31031 March 1992 Monthly Operating Rept for Mar 1992 for Fort St Vrain.W/ ML20090L0621992-02-29029 February 1992 Monthly Operating Rept for Feb 1992 for Fort St Vrain Unit 1 ML20092D0081992-01-31031 January 1992 Monthly Operating Rept for Jan 1992 for Fort St Vrain Nuclear Generating Station ML20102B2241992-01-22022 January 1992 Fort St Vrain Station Annual Rept of Changes,Tests & Experiments Not Requiring Prior Commission Approval Per 10CFR50.59, for Period 910123-920122 ML20094N6701991-12-31031 December 1991 Public Svc Co Annual Financial Rept for 1991 ML20091J6251991-12-31031 December 1991 Monthly Operating Rept for Dec 1991 for Fort St Vrain.W/ ML20094D6711991-11-30030 November 1991 Monthly Operating Rept for Nov 1991 for Fort St Vrain Unit 1 ML20090M1871991-11-20020 November 1991 FOSAVEX-91 Scenario for 1991 Plant Exercise of Defueling Emergency Response Plan ML20086D6891991-11-15015 November 1991 Proposed Decommissioning Plan for Fort St Vrain Nuclear Generating Station ML20085N1451991-11-0505 November 1991 Revised Ro:Operability Date of 910830 for Electric Motor Driven Fire Water Pump P-4501 Not Met.Pump Not Actually Declared Operable Until 911025.Caused by Unforseen Matl & Testing Problems.Equivalent Pump Available ML20086C5451991-10-31031 October 1991 Monthly Operating Rept for Oct 1991 for Fort St Vrain.W/ ML20085H6611991-10-10010 October 1991 Assessment of Mgt Modes for Graphite from Reactor Decommissioning ML20091D7671991-10-0101 October 1991 Rev B to Engineering Evaluation of Prestressed Concrete Reactor Vessel & Core Support Floor Structures for Proposed Sys 46 Temp Change ML20085D9861991-09-30030 September 1991 Monthly Operating Rept for Sept 1991 for Fort St Vrain.W/ 1997-07-01
[Table view] |
Text
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- s. ; _
@ Public Service' =1 16805 WCR 19 1/2, Platteville, Colorado. 80651
-1 May 31, 1990 i y Fort St. Vrain Unit No, 1-P-90150 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk ,
Washington, D.C. 20555 Docket No. 50-267.
4
SUBJECT:
Licensee Event Report 89-018-01, Final Report
REFERENCE:
Facility Operating License No OPR-34 Gentlemen:
Enclosed, please find a copy of Licensee Event Report S-No. 50-267/89-018-01, Final, submitted. per the requirements- of u.
10 CFR 50.73(a)(2)(v). ,
If _ you have any questions, please contact Mr. M. H. Holmes at (303) 480-6960. ;
Sincerely, e
>e 4$ l C. H. Fuller Manager, Nuclear Production and Station Manager CHF/1mb i
~
Enciosure-cc: Regional Administrator, Region IV Mr. J. B. Baird ATTN:
Tecnnical Assistant Division of Reactor Projects Mr. R. E. Farrell !
Senior Resident Inspector, FSV l 9006120074 900531 .
PDR ADOCK 05000267 s PDC l
i i ane . att u auc6un ...usatoav cannet AP98tovt0 o884 000 3mtes UCENSEE EVENT REPORT (LER) * **'au l *
Fort St. Vrain, Unit No. 1
, 016 t o lo 10121617 S loFl 019 CRACKING IN INCOLOY ALLOY B00 MAIN STEAM RINGHEADERS Sv. t .An i., u =v t. i., .t.o.?o.n ni 01 4. acnitiet i=vosvio .,
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CAU$t tyttlW COMPONENT Ng$0' TO ' 68 $*VII ITITI" CO"'ONINI t ONR B Al B SIG1 1 G IO 1613 Y l i i i l I i l I I I i l i l 1 1 I I I I SveFLlutNT AL hlP041 S KPGCitD Itai ses0Niet Day vtAm t t$ 199 yet, eenwho.e Sk9ttfl0 SV0utSSION DA tti NO l l l t ..cf ,t-,. .e , . e-.e. . e . -. e.e, ~.e. .,,e -e ~,,-,es - n .i l On August 25, 1989, Public Service Company sf Colorado (PSC) discovered a leak in the main steam ringheader of one of the Loop 1 steam generator modules. Upon further investigation, on August 27, 1989, 37 crack indications were found in I the Incoloy Alloy 800 ringheaders in 8 of the 12 modules, and the condition was determined to have generic implications.
l PSC's metallurgical examination determined that the cracking was caused by creep i failure, with the principle failure mechanism being a reduction of creep l ductility of the material. Various factors could have contributed to this i reduction of creep ductility, including cold working without solution annealing, I low titaniym/ carbon ratio, high titanium plus aluminum content, and a coarse-l y 41ned M crostructure. .
Bred on the extent of the ringheader cracking and other operational I considerations, on August 29, 1989, PSC decided to permanently shut down Fort St. Vrain.
Weld repair activities have been performed to the extent necessary to ensure j decay heat removal capability during shutdown and defueling conditions, i
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011 012 0F 01 9 um e . s .mm anc a w on BACKGROUNDt l The two Fort St. Vrain (FSV) steam generators each include six once-through modules arranged in parallel within the cavity of the Prestressed Concrete Reactor Vessel (PCRV) as shown in Figure 1. Each module includes an Economizer-Evaporator-Superheater (EES) section and a reheater section.
~
l The EES tube bundle in each module includes 54 tubes that are combined into 18 l subheaders. The 18 subheaders are directed out of the bottom of the PCRV and l are collected in a main steam ringheader for each module, from which steam is l then directed to the main steam piping.
l The twelve main steam ringheaders are manufactured from nickel-iron-chromium l Incoloy Alloy 800, in accordance with the specifications of ASME SB-407 Grade 1.
They are fabricated from 5.563" 0.0. pipe with a nominal wall thickness of l 0.75", and are formed into 51" diameter rings, each with eighteen 1.315" 0.0.
nozzle attachments. Fabrication methods, pro;edures and practices were in accordance with ASME Boiler and Pressure Vessel Code Section Ill, Class A, 1965 Edition, through the Winter 1966 Addenda.
EVENT DESCRIPTION:
On August 25, 1989, with the reactor shut down for control rod (AA)*
replacement, a water leak was discovered in the main steam ringheader ( AB)* for Loop 1 steam generator module B-1-4 At the time, the Loop I EES section was being supplied with condenspte for decay heat removal, at a pressure of less than 300 psig.
The leak was observed to be coming from an approximately 5 inch long crack in the ringheadet, roughly parallel to one of the nozzle attachment welds. The crack was in the base metal.
To determine the extent of the cracking problem, PSC removed the insulation and performed a liquid penetrant examination on the remaining welds of the B-1-4 ringheader. One additional crack indication was observed. Based on the potential generic nature of the crack indications, PSC then performed liquid l penetrant examination on the most accessible portions of all of the Incoloy main I steam ringheaders and found a total of 37 crack indications. Crack indications I were not found on four of the twelve ringneaders.
On August 27, 1989, PSC management rev'ewed the extent of the ringheader cracking. The generic nature of the condition could conceivably have impaired the Safe Shutdown Cooling capability of the plant and at 2255 hours0.0261 days <br />0.626 hours <br />0.00373 weeks <br />8.580275e-4 months <br />, NRC notification was made per 10 CFR 50.72(b)(2)(iii).
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l The root cause of cracking in the Incoloy Alloy 800 main steam ringheaders has l been determined by metallurgical examination to be creep failure, with the !
I principle mechanism being a reduction of the creep ductility of the material, l PSC's metallurgical examination identified several potential contributing l factors in the FSV ringheader material that reduce creep ductility in Incoloy l Alloy 800 material, These factors were not known at the time the ringheaders l were manufactured, and they include the following:
l 1. Cold working during forming, without subsequent solution annealing, l 2. A low titanium (T1) to carbon (C) ratio, l 3. A Ti plus aluminum (A1) con,ent in excess of 0.6'4, and l 4. Cearse grained microstructure.
SAFETY ANALYSIS:
The main steam ringheader crack that was found on August 25, 1989 and the more extensive crack indications found on August 27, 1989 could conceivably have impaired the Safe Shutdown Cooling capability of Fort St. Vrain. As such, this condition is being reported per the requirements cf 10 CFR 50.73(a)(2)(v).
I Safe Shutdown Cooling can be accomplished with either Loop I or Loop 11 steam l generator EES sections. If the through-wall crack on loop I steara generator module B-1-4 had occurred during power operations, and if it had progressed to the point of complete ringheader failure, PSC could still have safely shut down the reactor with the Loop II EES section. Also, the reheater sections of both l steam generators were available for core heat removal, although the reheaters l have been determined inadequate for Safe Shutcown Cooling heat removal from full power operating conditions, I The cracking observed on the eight ringheaders is considered to have generic I implications, but PSC does not consider it likely that all Safe Shutdown Cooling I capability would have been lost. Complete loss of Safe Shutdown Cooling l capability would have required the simultaneous through-wall cracking and I f ailure of a ringheader in both Loop I and Loop II. A ringheader crack would I most likely leak before a complete break and the ringheaders are accessible l during plant operation, With main steam conditions during operations of 1000 l degree F at 2400 psig, a ringheader steam leak would be detectable by plant i opeettors in time to support a safe plant shutdown.
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01510 lo lo l 21617 Q 118 014 0F Feet st. Vrain. Unit No 1 8 ! 9_ 011 019 van e - . a . . man = = o.- an w nn i In addition, if a ringheader failed / ruptured during power operations, the Steam Line Rupture Detection / Isolation System (SLRDIS) would have detected and isolated the break. Safe Shutdown Cooling could then have been achieved with equipment qualified for the resulting harsh environment. The rupture of a ringheader is bounded by the complete offset rupture of a main steam line as analyzed in FSAR Section 1.4.6. The consequences of this event are acceptable ,
and public health and safety would be protected.
Although highly unlikely, if both Loop I and 'oop II EES sections failed and forced circulation was lost from full power 1 nditions, the PCRV liner cooling system is capable of maintaining containment integrity, so that public health I and sr.fety would be protected. Although fuel damage would occur during such an I event, activity would be contained, as analyzed in FSAR Section 14.10, Permanent loss of Forced Circulation, DBA-1.
METALLURGICAL EVAL.UATIONi l PSC performed a metallurgical examination on samples of the FSV ringheader i cracks, including macroscopic evaluation, replication, microscopic evaluation I (using both light and scanning electron microscopes), chemical analysis, and l hardness testing. (Reference 1) l The configuration of a typical EES ringheader is shown in Figure 2. The I through-wall crack found in module B-1-4 was observed adjacent to the nozzle l weld designated N-118, as illustrated. The linear indications on all l ringheaders were located adjacent to nozzle welds.
l The ringheaders were originally annealed at 1800 degrees F, followed by a water l quench. The material was then cold formed to shape at 1000 degrees F and no l final solution annealing heat treatment was performed. The ringheaders were I designed for typical operating conditions of 1025 degrees F at 2400 psig.
I Average main steam temperatures were actually controlled at 1000 degrees F l during plant operation, with individual module temperatures typically controlled l to within 20 degrees of the average.
l In general, the ringheader material properties were found to be typical for l Incoloy Alloy 800 material. The chemical analysis of the base material met the l Alloy 800 requirements, the grain size was very coarse but in accordance with l ASME SB-407 requirements for Alloy 800 material, the microstructure was typical I of Alloy 800 material, and the hardness was consistent with hardness values l published for Alloy 800 material that had experienced similar service I conditions.
l The metallurgical examination found no contaminants that would be expected if j l the cracking was due to corrosion. Also, the crack surfaces were noted to have I a heavy oxide coating, indicating that they had existed for some time.
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l' l Failure of the ringheaders was determined to have occurred by intergranular l cracking, with negligible material deformation. Examination of failed areas l revealed extensive grain boundary microvoids associated with the cracks, which l indicates that failure occurred due to creep damage. Creep damage is a i
l thermally-dependent deformation process which occurs in a material after l l exposure to constant stress at high temperature. Creep cracking occurs by the f l initiation and coalescenet of microvoids within the material, which eventually l forms microcracks, leading to macrocracking and ultimate failure.
l PSC's metallurgical analysis examined several factors that are now known to l affect the creep failure susceptibility of Alloy 800 material. These factors l are as follows:
l- Ti/C ratio and grain size. The Ti/C ratio was 4.86 which is on the low end l and typically would result in a coarse grain size, as was observed. The l degree of embrittlement is reported in the literature to be more severe for l coarse grained materials than for fine grained materials, l
l- Ti + Al content. Th'e Ti + Al content was 0.694, and it has been reported l l that Alloy 800 material with a Ti + Al content in excess of 0.6'. exhibits l l poor creep ductility.
l l
l- Degree of cold working and solution annealing heat treatment temperature, i l Cold working up to 10% has been observed to decrease creep ductility in l Alloy 800 material, and to increase notch sensitivity. Solution annealing I at 1500 to 1550 degrees F is recommended to reduce susceptibility to i l premature failure. Since the ringheaders were not solution annealed after l I cold working, the effects of cold working are considered to be significant '
I factors in their premature failure.
l The ringheaders were not solution annealed during manufacture because many
- l factors which influence the creep ductility of Incoloy Alloy 800 material, as l noted above, were not known at the time of design or manufacture.
l PSC's metallurgical examination identified other possible contributing factors, l l the significance of which could not be determined without additional testing and l l a complete stress analysis. These include higher than expected operating l temperature or stress, and unanticipated notch effects due to the weld joint .
l configuration. Due to PSC's decision to permanently shut down Fort St. Vrain, I l additional analysis and testing are not planned.
l l' l REPAIR ACTIVITIES l PSC investigated the feasibility of repairing the cracks to allow continued l
l operation. Several areas were ground, liquid penetrant tested, and found l l acceptable for repair. However, PSC was not confident that all of the cracks l could be repaired and restored to full operating conditions due to the l microcracking which was discussed previously in the Metallurgical Evaluation.
l This microcracking would not be identified during the liquid penetrant l examination but it could contribute to later ringheader failure, j geoa= =.na .u s oro ie*+e:4 5*4ss
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011 Ol 6 0F 0 19 un a . a .ammw ame a answim PSC had previously announced that plant operations would not continue beyond June 30, 1990. In light of this limited amount of potential operation, PSC decided that complete repair and restart efforts were not feasible and Fort St.
Vrain was shut down permanently.
Under reactor shutdown conditions, decay heat removal is normally accomplished l by supplying condensate to a steam generator EES or reheater section in a single I loop, where each loop contains six steam generator modules. PSC re-evaluated the ringheader cracks for the maximum service conditions available with the condensate pumps, which have a shutoff head of 340 psig. Using conservative conditions of 400 psig and 300 degrees F, a minimum calculated wall thickness of 0.0758 inches was determined. A minimum acceptance criteria of 0.250 inches was then conservatively established and weld repairs were made to cracks in modules B-1-1, B-1-3, and B-1-4. No other weld repairs were required. With these repairs, the EES ringheaders of either loop are acceptable for heat removal during the remaining FSV shutdown conditions. Because of the reduced heat removal requirements during shutdown conditions, any future conceivable ringheader failures would have no safety significance.
CORRECTIVE ACTION:
On August 29, 1989, PSC management announced that Fort St. Vrain would not be restarted and that the operational phase of the plant had ended.
l The main steam ringheaders have been repaired to the extent necessary for decay l heat removal during shutdown and defueling conditions. Shutdown heat removal l will use condensate with a maximum pressure of 340 psig.
I l
l Reference 1. PSC Metallurgy Laboratory Report No. 225, Failure Analysis of the l Fort St. Vrain Steam Generator Main Steam Ring Headers, February l 12, 1990.
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E C 7:au aena *U S OPO 1986 0 624 636 466
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