ML20050B254

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LER 82-006/03L-0:on 820218,primary Coolant Moisture Exceeded Tech Specs.Caused by Contamination W/Moisture During Maint Outage.Reactor Shutdown & Coolant Purification Trains Utilized to Reduce Impurity Levels
ML20050B254
Person / Time
Site: Fort Saint Vrain Xcel Energy icon.png
Issue date: 03/19/1982
From: Fuller C
PUBLIC SERVICE CO. OF COLORADO
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML20050B249 List:
References
LER-82-006-03L, LER-82-6-3L, NUDOCS 8204050146
Download: ML20050B254 (1)


Text

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NRC FORM 3Ee6

\ U. S. NUCLEA'1 E.EcVLAToRY COMMtSSION (7 77).

  • '~ LICENSEE EVENT REPORT (PLEASE PRINT OR TYPE ALL REQUIRED INFoRMATIONI CONTROL BLOCK: l i

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EVENT o&$CRIPT1oN AND PROB ABLE CONSEQUENCES h .

lO 121 IWith the reactor at less tban 2% power, the <fespoint moisture limit of Fioure 4.2.11-11 g lwas exceeded on four occadions. This is repo'rtable as a _<1ectaded mode of __ l i o i.ii ILC0 4.2.11 per Fort St. Vrain Technical Specification AC 7.5.2(b)2. No accomoanvino l

[irTT1 l occurrence. No affect on public health or safety. Similar reports: 76-06, 77-02, I lo 16 1 177-13, 78-16, 78-39, 79-02, 79-31, 79-43, 80-11, 80-19, 80-33, 80-36. 80-09. 80-20. I I

F5Tn I and 81-45.

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l i 101 lDuring a maintenance / modification outage, the primary coolant became contaminated withi (

lilil imoisture. The reactor was shutdown and the coolant purification trains are beino I FrT-I lutilized to reduce the impurity levels. No other corrective actions are I g ] anticipated or recuired. I l

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NAME of PREPARER PHON E:

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