05000267/LER-1981-049-03, /03L-0:during 810802-07,increase Occurred in Offgassing from Core & Core Outlet Temps.Caused by Increased Primary Coolant Moisture & Oxidants from Refueling Shutdown

From kanterella
(Redirected from ML20010H930)
Jump to navigation Jump to search
/03L-0:during 810802-07,increase Occurred in Offgassing from Core & Core Outlet Temps.Caused by Increased Primary Coolant Moisture & Oxidants from Refueling Shutdown
ML20010H930
Person / Time
Site: Fort Saint Vrain Xcel Energy icon.png
Issue date: 09/01/1981
From: Mcbride L
PUBLIC SERVICE CO. OF COLORADO
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML20010H926 List:
References
LER-81-049-03L, LER-81-49-3L, NUDOCS 8109290423
Download: ML20010H930 (1)


LER-1981-049, /03L-0:during 810802-07,increase Occurred in Offgassing from Core & Core Outlet Temps.Caused by Increased Primary Coolant Moisture & Oxidants from Refueling Shutdown
Event date:
Report date:
2671981049R03 - NRC Website

text

-. - -. - -...

NRC FORM X4 U. S. NUCLE AD I EGULATCY COMMISSION (7 77)

L!0ENSEE EVENT REPORT

  • ' - P CONTROL BLOCK: l l

l l

l l lh (PLEASE PRINT OR TYPE ALL REQUIRED INFOIMATliN) i lo lil lc lo Ir Is lv li l@l ol ol l ol of of ol ol l of ol@l al il 1121 ol@l i

l@

7 8 9 UCENSEE CODE le IS L CENSE NUMSER 25 26 LICENSE TYPE JG 57 CAT 58 CON'T loIiI ILhl0151010 10 12 !6 17 @l 01 Sl 0 l 2 l 81 1hd.j_0 l1 l 81 1 l@

3 uRCE 7

8 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 PEPORT DATE 80 EVENT DESCRIPTION AND PROB ABLE CONSEQUENCE.S h t o 121 l Durint the oeriod from August 2.1981, to Augus t 7.1981. the plant was operated in I

g l a degraded mode cf L,CO 4.2.10 on three occasions.

These events are reportable per l

l o 141 l Fort St. Vrain Technical Specification AC 7.5.2(b)2. No accocipanying occurrence. No l [ois) i effect on public health or safety. Similar repot3s 'to 81-009,81-015, 81-020, and l

l o i s 1 I 81-02 7.

l l o 171 1 I

l 0 l $) I

_]

"O 7

8 9 E

CODE SUSC E COMPONENT CODE SUSCODE SU E

toJ_.j I c is l@ W@ L.z_J@ i z i z i z i z i z i z i@ I z i@ tz_l @

7 8

9 10 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISloN LER EVENT YEAR R EPORT NO.

CCOE TYPE No.

O agao 18111 Lj 1014191 [d

16111 O

l-l 10 1 g

su 21 22 23 24 26 27 28 29 JQ 31 32 KN A ON O P NT VE HOURS S8 i FOR 8.

SUP Li MANUFACTURER LyJ@l_J@

L2J@

L7J@

loIoIoIOI LrJ@

Lsj@

lzl@

lzIaI9I9l@

33 34 34 06 3/

4G 41 42 47 44 47 CAUSE OESCRIPTION AND CORRECTIVE ACTIONS h l i t o l l The increascd primary coolant moisture and orf.dants from the refueling shutdown per-l gl iod resulted in increased off-gassing from the core when the. plant returned to power i and core outlet temperatures weru elevate d.

The primary coolant purification system I ggl i,,3 g l was util2 zed to restore primary coolant uxidant levels to acceptable limits.

l l

l i l41 !

80 7

8 9 ST

% POWER OTHER STATUS DIS O Y

DISCOVERY DESCRIPTION l i i s_] l E ih l0 l4 11 lhi N/A I

I A lhl primarv Coolant Chemisttv Analysis I

4CT1vtry CO TENT RcLEASED OF RELEASE AMOUN f OF ACTIv1TV LOCATION OF RELEASE Ii_LJ l z ] @ l zl@l n/A I

I N/a I

PERSONNEt ExPOSuEe3 cESCRiPrioN @

[ t l 711010 l 0 lhlTYPEZlhlN/A NuM8eR l

PE RSoNN E'L'tNJU' IES NU4 8ER DESCRtPTION lW l 0 l 0 j o l@l N/A l

80 7

8 9 11 12 LOSS oF oR DAMAGE To FACILITY TYPE

DESCRIPTION

@l N/A l

i 9 PususTv c

8109290423 810901 NRc usE oNLY l

N/A C

PDR j

l l I ! I I 1 ! I I I 1 1 :1 iSSuEo PM ADOCK 05000267

('__2Tsl I sj@oESCRiPrioN \\*.y 68 89 80 g 7

8 9 10

( 30 3) 785-2224 2

PHONE:

NAME OF PREPAREi1