Safety Evaluation Approving Util Mods to Containments & Torus Attached Piping as Documented in COM-02-041-1 Through 7 Entitled, Technical Evaluation of Dresden Nuclear Power Station Units 2 & 3,Plant-Unique Analysis Rept.ML17195A953 |
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Site: |
Dresden |
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Issue date: |
09/18/1985 |
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From: |
Office of Nuclear Reactor Regulation |
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Shared Package |
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ML17195A951 |
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References |
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NUDOCS 8509230625 |
Download: ML17195A953 (3) |
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Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
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[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20249C8491999-09-30030 September 1999 1999 Third Quarter Rept of Completed Changes,Tests & Experiments Evaluated,Per 10CFR50.59(b)(2), for Dresden Nuclear Power Station. with ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20210R6081999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Dresden Nuclear Power,Units 1,2 & 3.With ML20209E1291999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Dresden Nuclear Power Station,Units 1,2 & 3.With ML20209J3481999-06-30030 June 1999 1999 Second Quarter Rept of Completed Changes,Tests & Experiments, Per 10CFR50.59.With ML20210D3071999-06-30030 June 1999 Corrected Page 8 to MOR for June 1999 for DNPS Unit 3 ML20195G6381999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Dresden Nuclear Power Station,Units 1,2 & 3.With ML20195B2591999-05-19019 May 1999 Rev 66a to CE-1-A,consisting of Proposed Changes to QAP for Dnps,Qcs,Znps,Lcs,Byron & Braidwood Stations ML20206N2821999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Dresden Nuclear Power Station,Units 1,2 & 3.With ML20206B1901999-03-31031 March 1999 First Quarter Rept of Completed Changes,Tests & Experiments Per 10CFR50.59 for Dresden Nuclear Power Station. with ML20205N7491999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Dresden Nuclear Power Station,Units 1,2 & 3.With ML20207M6921999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Dresden Nuclear Power Station,Units 1,2 & 3.With ML20207E9311999-02-26026 February 1999 Part 21 Rept Re Sprague Model TE1302 Aluminum Electrolytic Capacitors with Date Code of 9322H.Caused by Aluminum Electrolytic Capacitors.Affected Capacitors Replaced ML20199M0891999-01-22022 January 1999 Part 21 Rept Re Failure of Square Root Converters.Caused by Failed Aluminum Electrolytic Capacitory Spargue Electric Co (Model Number TE1302 with Mfg Date Code 9322H).Sent Square Root Converters Back to Mfg,Barker Microfarads,Inc ML20199D3261998-12-31031 December 1998 10CFR50.59 SER for 1998-04 Quarter, of Changes,Tests & Experiments.With ML20199C8951998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Dnps,Units 1,2 & 3 ML20205M7061998-12-31031 December 1998 Unicom Corp 1998 Summary Annual Rept. with ML20197G8591998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Dresden Nuclear Power Station.With ML20196A4191998-11-19019 November 1998 Safety Evaluation Accepting QA TR CE-1-A,Rev 66 Re Changes in Independent & Onsite Review Organization by Creating NSRB ML20196J0061998-11-19019 November 1998 Rev 66 to Topical Rept CE-1-A, QA Program ML20195D2861998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Dresden Nuclear Power Station.With ML20154L3681998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Dresden Nuclear Power Station,Units 1,2 & 3.With ML20154N4131998-09-30030 September 1998 1998 Third Quarter 10CFR50.59 Rept, for Dresden Nuclear Power Station of Completed Changes,Tests & Experiments ML20153C5061998-09-21021 September 1998 SER Accepting Qualified Unit 1 Supervisor Initial & Continuing Training Program for Dresden Nuclear Power Station,Unit 1 ML20151Y2711998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Dresden Nuclear Power Station,Units 1,2 & 3.With ML20237E2331998-08-21021 August 1998 Revised Pages of Section 20 of Rev 66 to CE-1-A, QA Topical Rept ML20237A7161998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Dresden Nuclear Power Station,Units 1,2 & 3 ML20236Q5851998-06-30030 June 1998 1998 Second Quarter 10CFR50.59 Rept, for Dresden Nuclear Power Station of Completed Changes,Tests & Experiments ML20236F8131998-06-30030 June 1998 Rev 0 to Defueled SAR Dresden Nuclear Power Station Unit 1 Commonwealth Edison Co ML20236T8331998-06-30030 June 1998 COLR for Dresden Station Unit 3,Cycle 15 ML20236T8391998-06-30030 June 1998 Rev 1 to EMF-96-141, Dresden Unit 3 Cycle 15 Reload Analysis Rept ML20236M6041998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Dresden Nuclear Power Station,Units 1,2 & 3 ML20248M3021998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Dresden Nuclear Power Station,Units 1,2 & 3 ML20248F3531998-05-21021 May 1998 Part 21 Rept Re Electronic Equipment Repaired or Reworked by Integrated Resources,Inc from Approx 930101-980501.Caused by 1 Capacitor in Each Unit Being Installed W/Reverse Polarity. 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[Table view] |
Text
UNITED STATES NUCLEAR REGULATORY COMMISSION*
WASHINGTON, D. C. 20555 SAFETY EVALUATION BY THE OFFICE OF NUCLEAR REACTOR REGULATION*
RELATED TO MARK I CONTAINMENT LONri-TERM PROGRAM STRUCTURAL REVIE~
COMMONWEALTH EDISON COMPANY DOCKET NOS. 50-237/249
1.0 INTRODUCTION
ThP. capability of the boiling water reactor (BWR) Mark I containment structures and pipin9 systems to withstand the effect of hydrodynamic loads resulting from a loss of coolant accident (LOCA) and/or a safety relief valve (SRV) discharge was not considered in the original design of the structures. The resolution of this issue was divided into a short-term program and a long-term program.
Based on the results of the short-term program, which verified that each Mark I containment would maintain its integrity and functional capability when subjected to the loads induced by a design-basis LOCA, the NRC staff granted an exemption relating to the structural safety requirements of 10 CFR 50.SSa. The study was reported in NUREG-0408, "Mark I Containment Short Term Program".
The objective of the long-term program was to maintain a margin of safety when the Mark I containment structures and piping system are subjected to additional hydrodynamic loads. The detailed guidance of the long-term program are contained in the NRC Safety Evaluation Report, NUREG-0661, "Mark_
I Containment Long-Term Program" and its supplement which describe the generic hydrodynamic load definition and structural acceptance criteria consistent with the requirements of the applicable codes and standards.
To fulfill the objective of the long-term program, Commonwealth Edison
. Company (CECo) has completed all modifications on the Dresden Nuclear Power Station, Unit ffos. 2 and 3 containments and torus attached piping.
The adequacy of these modifications was documented in a report prepared by the Nutech Engineers, Inc. (Nutech)~and Sargent and Lundy Engineers (S&L) COM-02-041-1 through 7 titled "Dresden Nuclear Power Station, Units 2 and 3, ... Plant Unique Analysis Report "(PUA Report). ---
The Franklin Research Center (FRC) was contracted to review the structural adequacy issue for compliance with the staff's acceptance criteria.
- .r
- 2. 0 EVALUATION The Mark I long-term program of Dresden llnits 2 and 3 was described jn the plant-unique analysis report (PUAR) prepared by Nutech and S&L. This report describes modifications performed on containment structures and torus attached piping at Dresden Units 2 and 3. Areas covered by the report include the torus shell, external support system, vent header system, .internal structures, torus attached pipings, SRV lines and vent pipe penetrations. Thamaterials, desiq" and fabrication requirements of the modifications were in accordance with the American Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel (B&PV) Code, Division 1,Section III with Addenda through Summer 1977 and Code Case N-197, 11 Service Limits for Containment Vessels 11
- Modifications were performed in accordance with the requirements of Section XI of the same codP. To determine the appropriate code allowable service limits for the specified loading combinations, the repnrt followed guidelines of NUREG-0661 and the GE report, NED0-24583-1, 11 Mark I Containment Program Structural Acceptance Criteria Plant Unique Analysis Application Guide. 11 The portion of the report applicable to loadings and loading combinations was audited by BNL, and results of that audit are discussed in a separate Safety Evaluation.
Using the properly determined loadings and loading combinations, Nutech and S&L employed the computer programs STARDYNE, PISTAR and PIPSYS as major tools to perform the analyses. Results of the analyses were sununarized to show that modifications are adequate under various loading combinations.
The adequacy of the modified containment structures and torus attached pipi~g was audited hy the FRC. FRC developed audit procedures for all Mark I long-tenn program users, which is described in detail in the FRC TER-C5506-308, "Audit Procedures for Mark I Containment Long-Term Program - Structural Analysis." The -review performed by FRC followed this document closely.
Results and conclusions of this effort were reported in FRC TER-C5506-324, "Audit for Mark I Containment Long-Term Program - Structural Analysis for Operating Reactors - Commonwealth Edison Company - Dresden Nuclear Power Station, Units 2 and 3. 11 The audit verified analyses by examining mathematical models and loading combinations used, and summarized the results to see whether the modifications met the required criteria. A check list was compiled to ensure the completeness of the auditing. The staff has reviewed the FRC report and concurs ..with its conclusions that the modifications meet the Mark I Containment Long-Term Program objective. An augmented fatigue evaluation method for ASME Code Class 2/3 piping was developed by MPR for GE in MPR Report-751, titled, 11 Augmented Class ~/3 Fatigue Evaluation Method and .
Results for Typical Torus attached on SRV Piping System", dated November 1982. This report was reviewed by the staff and the conclusion-that all torus piping systems have a fatigue usage of less than 0.5 during the plant life is acceptable for Dresden Units 2 and 3.
3.0 CONCLUSION
S The modifications perfonned at Dresden Units 2 and 3 followed the ouidelines rif N11Prn-Ofi61 and its supplement and met the respective requirements *of Sections III and XI of thP. ASME Boiler and Pressure Vessel Code r.nd are, therefor~, acceptable. CECo analyses have been verified by the FRC audit and approved by the staff*under the LOCA and SRV discharge loads.
4.0 ACKNOWLEDGEMENT Principal Contributor: H. Shaw Date: Septembe~ 18~ 1985.
Attached: TER prepared by Franklin Research Center, dated June ?l, 1985