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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20029D0261994-04-22022 April 1994 LER 94-002-00:on 940329,inadvertent Automatic Closure of Primary Containment Isolation Valves & ESF Actuations Occurred Due to Malfunctioning Handswitch.Caused by Weak Electrical Contact Spring.Handswitch replaced.W/940422 Ltr ML20046B4961993-07-30030 July 1993 LER 93-008-00:on 930627,MCR Annunciator Alarmed Indicating That Outside Atmosphere Reactor Encl (Re) Negative Differential Pressure Decayed Due to Failure of Normal Re Ventilation Fan Motor.Subj Fan replaced.W/930730 Ltr ML20046C3961993-07-30030 July 1993 LER 92-011-01:on 920605,discovered Potential Physical Electrical Separation Deficiency in Panel 10C790.Plant Electrical Maint I&C Technicians Received Training on Electrical Separation Requirements ML20046B5051993-07-30030 July 1993 LER 91-015-01:on 910912,HPCI Sys Discovered to Be in Degraded Condition When HPCI Turbine Steam Supply Valve Failed to Fully Open.Recommendations of EPRI Improved MOV Lubricant Program implemented.W/930730 Ltr ML20046B5001993-07-30030 July 1993 LER 93-008-00:on 930630,determined That TS SR on Fire Rated Assemblies Not Satisfied Due to Personnel Error During Procedure Preparation.Surveillance Test Procedure ST-7-022-922-0 Will Be revised.W/930730 Ltr ML20046A4431993-07-19019 July 1993 LER 93-007-00:on 930617,alarm Indicated TIP Sys Shear Valve Was Inoperable.Cause Interminate.Isolated Occurrence. W/930719 Ltr ML20045D3931993-06-21021 June 1993 LER 93-007-00:on 930521,primary Containment Isolation Valve Inoperable & TS Action Statement & SR Not Implemented in Required Time.Caused by Personnel Error.Ltr Issued to Personnel Emphasizing Requirement ML20044E7431993-05-20020 May 1993 LER 93-002-01:on 930124,discovered That EDG Inoperable Since 930119 Due to Improperly Connected Wires in Circuit Breaker. Wires Restored to Proper Position & Tested Satisfactorily. Procedural & Training Changes Also Implemented ML20044D1761993-05-0707 May 1993 LER 87-028-01:on 870610,hourly Fire Watch Required by TS 3.7.7 Not Performed Due to Personnel Error.Plant Security Organization Accepted Responsibility for Hourly Firewatch Patrol Required by Ts,Effective 930104 ML20044C9231993-05-0505 May 1993 LER 93-004-00:on 930405,primary Containment & Reactor Vessel Isolation Control Sys Actuation Occurred During Test of NSSSS-refueling Area Ventilation Exhaust Duct.Caused by Personnel Error.Technician counseled.W/930505 Ltr ML20024H0901991-05-10010 May 1991 LER 91-007-00:on 910410,handling of Control Rod Prohibited by Tech Spec Surveillance Requirements 4.9.6.3b.Caused by Inadequate Procedure.Maint Procedure Changed Deleting Provisions to Reposition Mechanical stop.W/910510 Ltr ML20024G6981991-04-22022 April 1991 LER 91-003-00:on 910324,inadvertent Actuation of Reactor Protection Sys Occurred.Caused by Personnel Error.Procedural Guidance Developed,Shift Training Bulletin Issued & Operator Requalification Training Module revised.W/910422 Ltr ML20029A8251991-02-27027 February 1991 LER 91-005-00:on 910130,pressure Differential Switch Restored Incorrectly,Causing Spurious Drywell Pressure Signal & ESF Actuation.Caused by Personnel Error.Personnel Counseled & Warning Labels added.W/910227 Ltr ML20029A7101991-02-22022 February 1991 LER 91-004-00:on 910123,determined That TS Section 3.3.7.5 Surveillance Requirements Not Satisfied for Fuel Zone Level & Neutron Flux Instrumentation.Caused by Misinterpretation of Ts.Calibr Procedures revised.W/910222 Ltr ML20028H7121991-01-22022 January 1991 LER 90-035-00:on 901224,14 Valves Associated W/Various Sys & Required to Perform Function of Isolating Primary Containment Determined Inoperable.Caused by Installation Error During Initial const.W/910122 Ltr ML20028H6791991-01-18018 January 1991 LER 91-002-00:on 910109,replacement Cassette Drive Unit to Replace Inoperable Seismic Monitoring Sys Not Received by 910109,rendering Sys Inoperable for More than 30 Days.Caused by Grit on Gear.Sys repaired.W/910118 Ltr ML20024F7361990-12-0707 December 1990 LER 90-025-00:on 901110,spurious LOCA Signal Resulted in ESF actuations.W/901207 Ltr ML20028G9221990-09-26026 September 1990 LER 90-017-00:on 900828,ESF Actuation of Primary Containment & Reactor Vessel Isolation Control Sys Occurred.Caused by Technician Inadvertently Shorting Power Supply During Installation of Test Jack.Blown Fuse replaced.W/900926 Ltr ML20044A9761990-07-12012 July 1990 LER 90-013-00:on 900611,dc Distribution Sys Identified to Have Inadequate Isolation Capability Between Class IE & non-Class IE Components.Cause of Event Under Investigation. Hourly Fire Watches Established Until 900626.W/900712 Ltr ML20043C5231990-06-0101 June 1990 LER 90-003-01:on 900208,HPCI Sys Isolation Valve Inadvertently Isolated During Surveillance Test.Caused by Both Channels of Isolation Logic Being in Tripped Condition at Same Time.Isolation of HPCI Sys reset.W/900601 Ltr ML20043C3211990-05-30030 May 1990 LER 90-012-00:on 900426,inoperability of RHR Sys Modes Occurred Due to Physical Separation Deficiencies.Caused by Drawing Deficiency Resulting in Installation Error During Original Const.Nonclass 1E Cable sleeved.W/900530 Ltr ML20043B1331990-05-21021 May 1990 LER 90-011-00:on 900420,discovered That Emergency Svc Water Pump B Discharge Check Valve Not Preventing Reverse Flow. Caused by Personnel Error in That Actuating Arm Incorrectly Assembled.Actuating Arm repositioned.W/900521 Ltr ML20043B1311990-05-18018 May 1990 LER 90-006-01:on 900223,determined That Capability to Activate Emergency Public Notification Sys Sirens from Counties Lost from 900112-0205.Caused by Disconnection of Phone Lines.Lines Reconnected for All counties.W/900518 Ltr ML20043A7651990-05-17017 May 1990 LER 90-008-00:on 900417,HPCI Sys Isolation & Inoperability Occurred Due to Failure of Differential Pressure Transmitter.Cause of Transmittal Failure Under Investigation.Transmitter Returned to mfg.W/900517 Ltr ML20043A6321990-05-15015 May 1990 LER 89-060-01:on 891212,standby Gas Treatment Sys Charcoal Filter Discovered in Degraded Condition W/Possible Bypass Leakage Paths.Similar Condition Discovered on 891218.Caused by Holes in Charcoal Filter assemblies.W/900515 Ltr ML20043A4261990-05-15015 May 1990 LER 90-010-00:on 900415,ESF Actuation Occurred Closing Three Containment Isolation Valves for Analyzers.Cause Unknown. Isolation Reset,Analyzers Returned to Svc & Voltmeter Not Being Used Pending Determination of cause.W/900515 Ltr ML20042G0521990-05-0404 May 1990 LER 90-009-00:on 900405,control Room Chlorine Isolation of Habitability Control Room Isolation Sys & ESF Initiated. Caused by Failure of B Toxic Gas Detector & False Signal from Untested Analyzer.Detector replaced.W/900504 Ltr ML20012C9361990-03-12012 March 1990 LER 90-005-00:on 900211,no Fire Watch Insps for Rooms 103, 114 & 117 on Elevation 177 Ft in Reactor Encl Performed by Personnel.Caused by Personnel Error.Person Involved Disciplined.Training Program improved.W/900312 Ltr ML20012C5541990-03-12012 March 1990 LER 90-004-00:on 900209,station Personnel Discovered That on 890708,22-s Reactor Power Transient Occurred in Which Reactor Thermal Power Changed by More than 15% of Rated Thermal Power in 1 H.Procedure revised.W/900312 Ltr ML20012C7071990-03-12012 March 1990 LER 90-003-00:on 900208,HPCI Sys Inboard Isolation Valve Inadvertently Isolated & Closed When One Channel of Isolation Logic Tripped.Caused by Degradation of Darlington Output Transistor.Isolation reset.W/900312 Ltr ML20011F7911990-02-26026 February 1990 LER 90-002-00:on 900125,identified That Main Control Room Ventilation Sys Outside Design Basis.Caused by Misapplication of Design Basis Assumptions.No Immediate Actions Taken as Existing Procedures adequate.W/900226 Ltr ML20006E4271990-02-0909 February 1990 LER 90-001-00:on 900122,discovered That Monthly Instrument Channel Functional Test for RCIC Steam Supply Pressure Low Missed.Caused by Deficiency in Computer Program Used to Schedule Tests.Computer Program revised.W/900209 Ltr ML20006E3451990-02-0808 February 1990 LER 90-003-00:on 900112,primary Containment & Reactor Vessel Isolation Control Sys Isolation Signals Initiated, Closing Inboard & Outboard Isolation Valves for Rwcu.Caused by Lifting Relief Valve.Opening Time reset.W/900208 Ltr ML20006E2851990-02-0707 February 1990 LER 90-002-00:on 900105,containment H2/O2 Analyzer Declared Inoperable During Containment Inerting.Caused by Reversed Tubing Connections in Installation of Analyzer Due to Mislabeling.Analyzer restored.W/900207 Ltr ML20006D5171990-02-0707 February 1990 LER 90-001-00:on 900108,Tech Spec Violation & Reactor Encl Ventilation Isolation Occurred.Caused by Personnel Error. Chief Operator Counseled on Importance of Communicating All Pertinent info.W/900207 Ltr ML20006A8801990-01-19019 January 1990 LER 89-015-00:on 891223 & 24,problem W/Reactor Protection Sys (Rps)/Uninterruptable Power Supply Static Inverter Caused Loss of Power to RPS Panel.Caused by Failure of Gate Drive Boost Card.Isolations reset.W/900119 Ltr ML20005F9441990-01-10010 January 1990 LER 89-060-00:on 891212,standby Gas Treatment Sys Charcoal Filter a Discovered to Be Degraded W/Possible Bypass Leakage Paths.On 891218,filter B Found W/Similar Condition.Caused by Failure of Spot Welds.Filters repaired.W/900110 Ltr ML20005E6841990-01-0303 January 1990 LER 89-059-00:on 891206,instrumentation & Controls Technician Inadvertently Grounded Test Jack,Resulting in Blown Fuse.Caused by Personnel Error.Fuse Replaced. Technicians counseled.W/900103 Ltr ML20042D1961989-12-29029 December 1989 LER 89-009-02:on 890820 & 0925,RCIC Sys Injections Into RCS Occurred During Startup Test.From 891023-26,three HPCI Sys Injections Into RCS Occurred During Test.Injections Anticipated.Startup Tests performed.W/891229 Ltr ML20005E3301989-12-29029 December 1989 LER 89-014-00:on 891202,unexpected Actuation of Primary Containment & Reactor Vessel Isolation Control Sys Occurred. Caused by Insufficient Guidance in General Plant Procedure. Appropriate Procedures Reviewed & revised.W/891229 Ltr ML20005E0961989-12-26026 December 1989 LER 89-058-00:on 891123,actuation of Group III Primary Containment & Reactor Vessel Isolation Control Sys Resulted in Automatic Isolation of Rwcu.Caused by Failure of Flow Summer Card.Card replaced.W/891226 Ltr ML20011D2291989-12-19019 December 1989 LER 89-057-00:on 891120,refuel Floor Secondary Containment Isolated on Low Flow Differential Pressure,Causing Initiation of Standby Gas Treatment Sys.Caused by Severe Storm.Normal Ventilation Restored to floor.W/891219 Ltr ML19332F8631989-12-13013 December 1989 LER 89-056-00:on 891119,unexpected Nuclear Steam Supply Shutoff Sys Group Iii,Div 4 Isolation Initiated ESF Actuation.Caused by Defective read-set Selector Switch. Switch repositioned.W/891213 Ltr ML19332F7761989-12-11011 December 1989 LER 89-013-00:on 891110,reactor Scram Occurred Following Main Turbine Trip,Causing Initiation Signals on HPCI & RCIC Sys Due to Spiking of Level Transformers.Caused by Design Error.Hpci Turbine secured.W/891211 Ltr ML19332F7751989-12-11011 December 1989 LER 89-012-00:on 891110,RWCU Sys Differential Flow Oscillations Observed While Placing RWCU 2A Filter/ Demineralizer Into Svc.Caused by Leakage in Reactor HX Tube Side Safety Relief Valve.Valve removed.W/891211 Ltr ML19332F2961989-11-29029 November 1989 LER 89-009-01:on 890820,eight RCIC Sys Injections Into RCS Occurred Under Purview of Facility start-up Test Program. Caused by Abnormal Plant Conditions Requiring Safety Sys Actuations.Rcic & HPCI Sys Tests completed.W/891129 Ltr ML19332D6331989-11-27027 November 1989 LER 89-011-00:on 891027,outboard Nuclear Steam Supply Shutoff Sys Isolation Valves Isolated.Caused by Personnel Error Due to Lack of Attention to Detail by Technicians. Event Discussed at All Hands meeting.W/891127 Ltr ML19332D6251989-11-27027 November 1989 LER 89-055-00:on 891025,reactor Protection Sys 1A Shunt Trip Breaker Tripped on Undervoltage,Causing Loss of Power to Distribution Panel 1AY160 & ESF Isolation.Caused by Relief Valve Failures.Isolations reset.W/891127 Ltr ML19332C1781989-11-17017 November 1989 LER 89-053-00:on 891022,control Room Personnel Manually Initiated Ventilation Sys Chlorine Isolation,Esf.Caused by High Vinyl Chloride Concentration in Outside Air Intake Plenum.Special Event Procedure implemented.W/891117 Ltr ML19332B9841989-11-15015 November 1989 LER 89-054-01:on 891025,discovered That Daily Channel Check Surveillance Requirement for Channel D High Level Trip Not Met.Caused by Procedural Deficiency Since Initial Plant Operation.Associated Log Procedures revised.W/891115 Ltr 1994-04-22
[Table view] Category:RO)
MONTHYEARML20029D0261994-04-22022 April 1994 LER 94-002-00:on 940329,inadvertent Automatic Closure of Primary Containment Isolation Valves & ESF Actuations Occurred Due to Malfunctioning Handswitch.Caused by Weak Electrical Contact Spring.Handswitch replaced.W/940422 Ltr ML20046B4961993-07-30030 July 1993 LER 93-008-00:on 930627,MCR Annunciator Alarmed Indicating That Outside Atmosphere Reactor Encl (Re) Negative Differential Pressure Decayed Due to Failure of Normal Re Ventilation Fan Motor.Subj Fan replaced.W/930730 Ltr ML20046C3961993-07-30030 July 1993 LER 92-011-01:on 920605,discovered Potential Physical Electrical Separation Deficiency in Panel 10C790.Plant Electrical Maint I&C Technicians Received Training on Electrical Separation Requirements ML20046B5051993-07-30030 July 1993 LER 91-015-01:on 910912,HPCI Sys Discovered to Be in Degraded Condition When HPCI Turbine Steam Supply Valve Failed to Fully Open.Recommendations of EPRI Improved MOV Lubricant Program implemented.W/930730 Ltr ML20046B5001993-07-30030 July 1993 LER 93-008-00:on 930630,determined That TS SR on Fire Rated Assemblies Not Satisfied Due to Personnel Error During Procedure Preparation.Surveillance Test Procedure ST-7-022-922-0 Will Be revised.W/930730 Ltr ML20046A4431993-07-19019 July 1993 LER 93-007-00:on 930617,alarm Indicated TIP Sys Shear Valve Was Inoperable.Cause Interminate.Isolated Occurrence. W/930719 Ltr ML20045D3931993-06-21021 June 1993 LER 93-007-00:on 930521,primary Containment Isolation Valve Inoperable & TS Action Statement & SR Not Implemented in Required Time.Caused by Personnel Error.Ltr Issued to Personnel Emphasizing Requirement ML20044E7431993-05-20020 May 1993 LER 93-002-01:on 930124,discovered That EDG Inoperable Since 930119 Due to Improperly Connected Wires in Circuit Breaker. Wires Restored to Proper Position & Tested Satisfactorily. Procedural & Training Changes Also Implemented ML20044D1761993-05-0707 May 1993 LER 87-028-01:on 870610,hourly Fire Watch Required by TS 3.7.7 Not Performed Due to Personnel Error.Plant Security Organization Accepted Responsibility for Hourly Firewatch Patrol Required by Ts,Effective 930104 ML20044C9231993-05-0505 May 1993 LER 93-004-00:on 930405,primary Containment & Reactor Vessel Isolation Control Sys Actuation Occurred During Test of NSSSS-refueling Area Ventilation Exhaust Duct.Caused by Personnel Error.Technician counseled.W/930505 Ltr ML20024H0901991-05-10010 May 1991 LER 91-007-00:on 910410,handling of Control Rod Prohibited by Tech Spec Surveillance Requirements 4.9.6.3b.Caused by Inadequate Procedure.Maint Procedure Changed Deleting Provisions to Reposition Mechanical stop.W/910510 Ltr ML20024G6981991-04-22022 April 1991 LER 91-003-00:on 910324,inadvertent Actuation of Reactor Protection Sys Occurred.Caused by Personnel Error.Procedural Guidance Developed,Shift Training Bulletin Issued & Operator Requalification Training Module revised.W/910422 Ltr ML20029A8251991-02-27027 February 1991 LER 91-005-00:on 910130,pressure Differential Switch Restored Incorrectly,Causing Spurious Drywell Pressure Signal & ESF Actuation.Caused by Personnel Error.Personnel Counseled & Warning Labels added.W/910227 Ltr ML20029A7101991-02-22022 February 1991 LER 91-004-00:on 910123,determined That TS Section 3.3.7.5 Surveillance Requirements Not Satisfied for Fuel Zone Level & Neutron Flux Instrumentation.Caused by Misinterpretation of Ts.Calibr Procedures revised.W/910222 Ltr ML20028H7121991-01-22022 January 1991 LER 90-035-00:on 901224,14 Valves Associated W/Various Sys & Required to Perform Function of Isolating Primary Containment Determined Inoperable.Caused by Installation Error During Initial const.W/910122 Ltr ML20028H6791991-01-18018 January 1991 LER 91-002-00:on 910109,replacement Cassette Drive Unit to Replace Inoperable Seismic Monitoring Sys Not Received by 910109,rendering Sys Inoperable for More than 30 Days.Caused by Grit on Gear.Sys repaired.W/910118 Ltr ML20024F7361990-12-0707 December 1990 LER 90-025-00:on 901110,spurious LOCA Signal Resulted in ESF actuations.W/901207 Ltr ML20028G9221990-09-26026 September 1990 LER 90-017-00:on 900828,ESF Actuation of Primary Containment & Reactor Vessel Isolation Control Sys Occurred.Caused by Technician Inadvertently Shorting Power Supply During Installation of Test Jack.Blown Fuse replaced.W/900926 Ltr ML20044A9761990-07-12012 July 1990 LER 90-013-00:on 900611,dc Distribution Sys Identified to Have Inadequate Isolation Capability Between Class IE & non-Class IE Components.Cause of Event Under Investigation. Hourly Fire Watches Established Until 900626.W/900712 Ltr ML20043C5231990-06-0101 June 1990 LER 90-003-01:on 900208,HPCI Sys Isolation Valve Inadvertently Isolated During Surveillance Test.Caused by Both Channels of Isolation Logic Being in Tripped Condition at Same Time.Isolation of HPCI Sys reset.W/900601 Ltr ML20043C3211990-05-30030 May 1990 LER 90-012-00:on 900426,inoperability of RHR Sys Modes Occurred Due to Physical Separation Deficiencies.Caused by Drawing Deficiency Resulting in Installation Error During Original Const.Nonclass 1E Cable sleeved.W/900530 Ltr ML20043B1331990-05-21021 May 1990 LER 90-011-00:on 900420,discovered That Emergency Svc Water Pump B Discharge Check Valve Not Preventing Reverse Flow. Caused by Personnel Error in That Actuating Arm Incorrectly Assembled.Actuating Arm repositioned.W/900521 Ltr ML20043B1311990-05-18018 May 1990 LER 90-006-01:on 900223,determined That Capability to Activate Emergency Public Notification Sys Sirens from Counties Lost from 900112-0205.Caused by Disconnection of Phone Lines.Lines Reconnected for All counties.W/900518 Ltr ML20043A7651990-05-17017 May 1990 LER 90-008-00:on 900417,HPCI Sys Isolation & Inoperability Occurred Due to Failure of Differential Pressure Transmitter.Cause of Transmittal Failure Under Investigation.Transmitter Returned to mfg.W/900517 Ltr ML20043A6321990-05-15015 May 1990 LER 89-060-01:on 891212,standby Gas Treatment Sys Charcoal Filter Discovered in Degraded Condition W/Possible Bypass Leakage Paths.Similar Condition Discovered on 891218.Caused by Holes in Charcoal Filter assemblies.W/900515 Ltr ML20043A4261990-05-15015 May 1990 LER 90-010-00:on 900415,ESF Actuation Occurred Closing Three Containment Isolation Valves for Analyzers.Cause Unknown. Isolation Reset,Analyzers Returned to Svc & Voltmeter Not Being Used Pending Determination of cause.W/900515 Ltr ML20042G0521990-05-0404 May 1990 LER 90-009-00:on 900405,control Room Chlorine Isolation of Habitability Control Room Isolation Sys & ESF Initiated. Caused by Failure of B Toxic Gas Detector & False Signal from Untested Analyzer.Detector replaced.W/900504 Ltr ML20012C9361990-03-12012 March 1990 LER 90-005-00:on 900211,no Fire Watch Insps for Rooms 103, 114 & 117 on Elevation 177 Ft in Reactor Encl Performed by Personnel.Caused by Personnel Error.Person Involved Disciplined.Training Program improved.W/900312 Ltr ML20012C5541990-03-12012 March 1990 LER 90-004-00:on 900209,station Personnel Discovered That on 890708,22-s Reactor Power Transient Occurred in Which Reactor Thermal Power Changed by More than 15% of Rated Thermal Power in 1 H.Procedure revised.W/900312 Ltr ML20012C7071990-03-12012 March 1990 LER 90-003-00:on 900208,HPCI Sys Inboard Isolation Valve Inadvertently Isolated & Closed When One Channel of Isolation Logic Tripped.Caused by Degradation of Darlington Output Transistor.Isolation reset.W/900312 Ltr ML20011F7911990-02-26026 February 1990 LER 90-002-00:on 900125,identified That Main Control Room Ventilation Sys Outside Design Basis.Caused by Misapplication of Design Basis Assumptions.No Immediate Actions Taken as Existing Procedures adequate.W/900226 Ltr ML20006E4271990-02-0909 February 1990 LER 90-001-00:on 900122,discovered That Monthly Instrument Channel Functional Test for RCIC Steam Supply Pressure Low Missed.Caused by Deficiency in Computer Program Used to Schedule Tests.Computer Program revised.W/900209 Ltr ML20006E3451990-02-0808 February 1990 LER 90-003-00:on 900112,primary Containment & Reactor Vessel Isolation Control Sys Isolation Signals Initiated, Closing Inboard & Outboard Isolation Valves for Rwcu.Caused by Lifting Relief Valve.Opening Time reset.W/900208 Ltr ML20006E2851990-02-0707 February 1990 LER 90-002-00:on 900105,containment H2/O2 Analyzer Declared Inoperable During Containment Inerting.Caused by Reversed Tubing Connections in Installation of Analyzer Due to Mislabeling.Analyzer restored.W/900207 Ltr ML20006D5171990-02-0707 February 1990 LER 90-001-00:on 900108,Tech Spec Violation & Reactor Encl Ventilation Isolation Occurred.Caused by Personnel Error. Chief Operator Counseled on Importance of Communicating All Pertinent info.W/900207 Ltr ML20006A8801990-01-19019 January 1990 LER 89-015-00:on 891223 & 24,problem W/Reactor Protection Sys (Rps)/Uninterruptable Power Supply Static Inverter Caused Loss of Power to RPS Panel.Caused by Failure of Gate Drive Boost Card.Isolations reset.W/900119 Ltr ML20005F9441990-01-10010 January 1990 LER 89-060-00:on 891212,standby Gas Treatment Sys Charcoal Filter a Discovered to Be Degraded W/Possible Bypass Leakage Paths.On 891218,filter B Found W/Similar Condition.Caused by Failure of Spot Welds.Filters repaired.W/900110 Ltr ML20005E6841990-01-0303 January 1990 LER 89-059-00:on 891206,instrumentation & Controls Technician Inadvertently Grounded Test Jack,Resulting in Blown Fuse.Caused by Personnel Error.Fuse Replaced. Technicians counseled.W/900103 Ltr ML20042D1961989-12-29029 December 1989 LER 89-009-02:on 890820 & 0925,RCIC Sys Injections Into RCS Occurred During Startup Test.From 891023-26,three HPCI Sys Injections Into RCS Occurred During Test.Injections Anticipated.Startup Tests performed.W/891229 Ltr ML20005E3301989-12-29029 December 1989 LER 89-014-00:on 891202,unexpected Actuation of Primary Containment & Reactor Vessel Isolation Control Sys Occurred. Caused by Insufficient Guidance in General Plant Procedure. Appropriate Procedures Reviewed & revised.W/891229 Ltr ML20005E0961989-12-26026 December 1989 LER 89-058-00:on 891123,actuation of Group III Primary Containment & Reactor Vessel Isolation Control Sys Resulted in Automatic Isolation of Rwcu.Caused by Failure of Flow Summer Card.Card replaced.W/891226 Ltr ML20011D2291989-12-19019 December 1989 LER 89-057-00:on 891120,refuel Floor Secondary Containment Isolated on Low Flow Differential Pressure,Causing Initiation of Standby Gas Treatment Sys.Caused by Severe Storm.Normal Ventilation Restored to floor.W/891219 Ltr ML19332F8631989-12-13013 December 1989 LER 89-056-00:on 891119,unexpected Nuclear Steam Supply Shutoff Sys Group Iii,Div 4 Isolation Initiated ESF Actuation.Caused by Defective read-set Selector Switch. Switch repositioned.W/891213 Ltr ML19332F7761989-12-11011 December 1989 LER 89-013-00:on 891110,reactor Scram Occurred Following Main Turbine Trip,Causing Initiation Signals on HPCI & RCIC Sys Due to Spiking of Level Transformers.Caused by Design Error.Hpci Turbine secured.W/891211 Ltr ML19332F7751989-12-11011 December 1989 LER 89-012-00:on 891110,RWCU Sys Differential Flow Oscillations Observed While Placing RWCU 2A Filter/ Demineralizer Into Svc.Caused by Leakage in Reactor HX Tube Side Safety Relief Valve.Valve removed.W/891211 Ltr ML19332F2961989-11-29029 November 1989 LER 89-009-01:on 890820,eight RCIC Sys Injections Into RCS Occurred Under Purview of Facility start-up Test Program. Caused by Abnormal Plant Conditions Requiring Safety Sys Actuations.Rcic & HPCI Sys Tests completed.W/891129 Ltr ML19332D6331989-11-27027 November 1989 LER 89-011-00:on 891027,outboard Nuclear Steam Supply Shutoff Sys Isolation Valves Isolated.Caused by Personnel Error Due to Lack of Attention to Detail by Technicians. Event Discussed at All Hands meeting.W/891127 Ltr ML19332D6251989-11-27027 November 1989 LER 89-055-00:on 891025,reactor Protection Sys 1A Shunt Trip Breaker Tripped on Undervoltage,Causing Loss of Power to Distribution Panel 1AY160 & ESF Isolation.Caused by Relief Valve Failures.Isolations reset.W/891127 Ltr ML19332C1781989-11-17017 November 1989 LER 89-053-00:on 891022,control Room Personnel Manually Initiated Ventilation Sys Chlorine Isolation,Esf.Caused by High Vinyl Chloride Concentration in Outside Air Intake Plenum.Special Event Procedure implemented.W/891117 Ltr ML19332B9841989-11-15015 November 1989 LER 89-054-01:on 891025,discovered That Daily Channel Check Surveillance Requirement for Channel D High Level Trip Not Met.Caused by Procedural Deficiency Since Initial Plant Operation.Associated Log Procedures revised.W/891115 Ltr 1994-04-22
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217D1211999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Lgs,Units 1 & 2. with ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212A8861999-09-13013 September 1999 Safety Evaluation Authorizing First & Second 10 Yr Interval Inservice Insp Plan Requestss for Relief RR-01 ML20212A4481999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Limerick Generating Station,Units 1 & 2.With ML20211E9891999-08-20020 August 1999 LGS Unit 2 Summary Rept for 970228 to 990525 Periodic ISI Rept Number 5 ML20210L7051999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Limerick Generating Station,Units 1 & 2.With ML20209G0211999-06-30030 June 1999 GE-NE-B13-02010-33NP, Evaluation of Limerick Unit 2 Shroud Cracking for at Least One Fuel Cycle of Operation ML20209D7741999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Limerick Generating Station,Units 1 & 2 ML20207H8331999-05-31031 May 1999 Non-proprietary Rev 0 to 1H61R, LGS - Unit 2 Core Shroud Ultrasonic Exam ML20195G4651999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Lgs,Units 1 & 2 ML20209D7791999-05-31031 May 1999 Revised Monthly Operating Repts for May 1999 for Limerick Generating Station,Units 1 & 2 ML20195B3021999-05-0606 May 1999 Rev 0 to PECO-COLR-L2R5, COLR for Lgs,Unit 2 Reload 5 Cycle 6 ML20206N2901999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Limerick Generating Station,Units 1 & 2.With ML20195G4761999-04-30030 April 1999 Revised Monthly Operating Repts for Apr 1999 for Lgs,Units 1 & 2 ML20206D8971999-04-22022 April 1999 Rev 2 to PECO-COLR-L1R7, COLR for Lgs,Unit 2 Reload 7, Cycle 8 ML20205N8341999-04-0101 April 1999 Part 21 Rept Re Automatic Switch Co Nuclear Grade Series X206380 & X206832 Solenoid Valves Ordered Without Lubricants That Were Shipped with Std Lubrication to PECO & Tva.Affected Plants Were Notified ML20205N9311999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Limerick Generating Station,Units 1 & 2.With ML20204G9851999-03-11011 March 1999 Safety Evaluation Re Revised Emergency Action Levels for Limerick Generating Station,Units 1 & 2 ML20207J7461999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Limerick,Units 1 & 2.With ML20199G2371999-01-31031 January 1999 Rev 0 to NEDO-32645, Limerick Generating Station,Units 1 & 2 SRV Setpoint Tolerance Relaxation Licensing Rept ML20199L5301999-01-19019 January 1999 Special Rept:On 981214,seismic Monitor Was Declared Inoperable.Caused by Spectral Analyzer Not Running.Attempted to Reboot Sys & Then Sent Spectral Analyzer to Vendor for Analysis & Rework.Upgraded Sys Will Be Operable by 990331 B110078, Rev 1 to GE-NE-B1100786-01, Surveillance Specimen Program Evaluation for Limerick Generating Station,Unit 11998-12-31031 December 1998 Rev 1 to GE-NE-B1100786-01, Surveillance Specimen Program Evaluation for Limerick Generating Station,Unit 1 ML20205K0381998-12-31031 December 1998 PECO Energy 1998 Annual Rept. with ML20199F9611998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Limerick Generating Station.With ML20198C7151998-12-10010 December 1998 Rev 1 to COLR for LGS Unit 1,Reload 7,Cycle 8 ML20198A3871998-12-10010 December 1998 Safety Evaluation Supporting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power- Operated Gate Valves ML20206N4061998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Limerick Generating Station,Units 1 & 2.With ML20199E3281998-11-23023 November 1998 Rev 2 to PECO-COLR-L2R4, COLR for Lgs,Unit 2,Reload 4,Cycle 5 ML20195C9771998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Limerick Generating Station,Units 1 & 2.With ML20154H5691998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Limerick Generating Station,Units 1 & 2.With ML20151X3511998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Limerick Generating Station Units 1 & 2.With ML20237F0291998-08-27027 August 1998 Special Suppl Rept:On 960425,one Loose Part Detection Sys (Lpds) Was Identified to Be Inoperable.Initially Reported on 960531.Caused by Loose Parts Detector Module.Repairs Performed & Intermittent Ground No Longer Present ML20237D1041998-08-17017 August 1998 Books 1 & 2 of LGS Unit 1 Summary Rept for 960301-980521 Periodic ISI Rept 7 ML20237A7761998-08-10010 August 1998 SER Accepting Licensee Response to NRC Bulleting 95-002, Unexpected Clogging of RHR Pump Strainer While Operating in Suppression Pool Cooling Mode ML20236X7641998-07-31031 July 1998 Rev 0 to SIR-98-079, Response to NRC RAI Re RPV Structural Integrity at Lgs,Units 1 & 2 ML20237B4711998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Limerick Generating Station,Units 1 & 2 ML20236N6751998-07-0909 July 1998 Part 21 & Deficiency Rept Re Notification of Potential Safety Hazard from Breakage of Cast Iron Suction Heads in Apkd Type Pumps.Caused by Migration of Suction Head Journal Sleeve Along Lower End of Pump Shaft.Will Inspect Pumps ML20151Z4881998-06-30030 June 1998 GE-NE-B1100786-02, Surveillance Specimen Program Evaluation for Limerick Generating Station,Unit 2 ML20236P9781998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Limerick Generating Station,Units 1 & 2 ML20196K1801998-06-30030 June 1998 Annual 10CFR50.59 & Commitment Rev Rept for 970701-980630 for Lgs,Units 1 & 2. with ML20249B3501998-06-11011 June 1998 Rev 1 to PECO-COLR-L2R4, COLR for LGS Unit 2 Reload 4,Cycle 5 ML20249A5331998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Limerick Units 1 & 2 ML20247M7071998-05-14014 May 1998 Safety Evaluation Supporting Amend 128 to License NPF-39 ML20217Q5101998-05-0404 May 1998 Safety Evaluation Supporting Amend 127 to License NPF-39 ML20247H5071998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Limerick Generating Station ML20216F3601998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Limerick Generating Station,Units 1 & 2 ML20217M0791998-03-31031 March 1998 Safety Evaluation Supporting Amends 125 & 89 to Licenses NPF-39 & NPF-85,respectively ML20217D5701998-03-20020 March 1998 Part 21 Rept 40 Re Governor Valve Stems Made of Inconel 718 Matl Which Caused Loss of Governor Control.Control Problems Have Been Traced to Valve Stems Mfg by Bw/Ip.Id of Carbon Spacer Should Be Increased to at Least .5005/.5010 ML20216F9471998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Limerick Generating Station,Units 1 & 2 ML20216F3471998-02-28028 February 1998 Revised Monthly Operating Rept for Feb 1998 for Limerick Genrating Station,Unit 1 1999-09-30
[Table view] |
Text
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i SAN ATOG A, PENNSYLV ANI A 19464 ;
I tri s) 327.i 200 axv. 2000 January 3, 1990-
'u. 4. u cco nuic a. .; .. . z. . Docket Nos. 50-352 n..,......-
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' 50-353 -
License'.Nos. NPF-39i ,
NPF-85. ;
, U.Sh Nuclear Regulatory Commission r
. Attn:: Document' Control Desk-l Washington, DC 20555- !
SUBJECT:
Licensee Event Report Limerick Generating Station - Unit 1 .i This LER reports an actuation of the Primary Containment.
Reactor' Vessel Isolation Control System, an Engineered' Safety Feature, due.to a personnel error resulting from the improper use of test equipment during the performance of a Surveillance Test.
[
Reference:
Docket Nos. 50-352-50-353 L-. ' Report Number: 1-89-059
' Revision Number: 00 Event ~Date: December 6, 1989 Report Date: January 3,: 1990 -
Facility: Limerick Generating Station P.O. Box A, Sanatoga, PA 19464
.This LER is being submitted pursuant to the requirements of 10 CFR 50.73(a)(2)(iv).
Very truly yours, p
DMS:ch cc: W. T. Russell, Ao..inistrator, Region I, USNRC T. J. Kenny, USNRC Senior Resident Inspector, LGS l
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- DOCast an, mesa op Fees G Lincrick Generating Station, Unit 1 o is Io ;o ; o i 3l5;2 i lopl 0 ;6 flika se Unit I and 2 Primary Containment Reactor Vessel Isolation Control System Actuations due to a personnel error during surveillance testinge av,vr ute is. I sia mun.ia see i a po.1 oar m I orwin eacism u =vo6vio mi wo.rt. - 04, Tsaa j viaa isl"U'.U s ' M',,"fll ucat-l ca r ivsaa * *
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Op December 6, 1989, at 0958 hours0.0111 days <br />0.266 hours <br />0.00158 weeks <br />3.64519e-4 months <br />, while Unit 1 was at power and a Unit 2 was shutdown for an outage, an Instrumentation and a Controls (I&C) technician inadvertently grounded a test jack
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which resulted in a blown fuse during the performance of a Unit 1 Surveillance Test. This loss of power caused by the blown fuse resulted in automatic Primary Containment Reactor Vessel Isolation Control System (PCRVICS) actuations of Unit'l and Unit
' 2 isolation valves and systems, Engineered Safety Features. The blown fuse was then replaced by the I&C technicians. All PCRVICS isolations were reset, and normal system operations were restored by.the. Main Control Room operators by 1030 hours0.0119 days <br />0.286 hours <br />0.0017 weeks <br />3.91915e-4 months <br />. The consequences of this event were minimal. The Unit 1 PCRVICS isolation valves and system actuations functioned as. designed..
Unit 2 was shutdown, and there were no adverse consequences.
associated with the valve actuations that occurred on Unit 2.
The cause of this event was a personnel error due to a lack of
' attention to detail by an I&C technician. The IGC technicians involved with this event were counseled. Several corrective
' actions will be implemented to minimize the possibility of similar events.
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-Unit Conditions Prior to the-Event:
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. Unit'l Unit 2
- c Operating Condition: lL(Power Operation) 4--(Cold Shutdown)
Power Level: 100% -0% .
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. Unit 2 was shutdown for an outage.
Descriotion of the Event:
On December 6, 1989, Instrumentation and Controls (I&C) .
technicians were performing Unit 1 Surveillance Test-(ST) I
. procedure ST-2-026-618-1, "NSSSS - Reactor Enclosure Ventilation l Exhaust Duct Radiation - High; Division IA, Channel A Functional-Test." At 0958 hours0.0111 days <br />0.266 hours <br />0.00158 weeks <br />3.64519e-4 months <br />, during performance'of thi.C test, an I&C- -
technician inadvertently grounded a test jack which resulted in a )
blown fuse (EIIS:FU), B21-F101A, in the- Auxiliary Equipment Room l (AER) panel'10C622, " Inboard Valve Relays NSSSS Div 1." q This' loss of power caused by the blown fuse resulted in automatic Primary Containment. Reactor Vessel Isolation Control System (PCRVICS) (EIIS:JM) actuations, an Engineered Safety Feature (ESF), closing their outboard primary containment isolation valves; o Unit 1 Primary Containment Instrument Gas (PCIG) Process Lines (EIIS:LK), and o Unit 1 and Unit 2 Primary Containment Nitrogen Inerting Block Valves.
The outboard isolation valves in the following Unit 1 and Unit 2 PCRVICS subsystems received a signal to close, however no valve ,
movement occurred since the associated valves were already closed due to plant conditions prior to the event; o Primary Containment Purge Supply and Exhaust, and o Primary Containment Exhaust to Reactor Enclosure Equipment Compartment Exhaust (REECE).
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- ' UCENSEE EVENT REP'jRT (LER) TEXT CONTINUATION ~
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' Additionally, the..following' Unit.1 ESF,actuations occurred; o Reactor Enclosure Ventilation (EIIS:VA) System isola.ted, t
o the 'A' train of Reactor Enclosure Recirculation, System.
(RERS)'(EIIS:VA) initiated, and-o the 'A' train of Standby Gas Treatment System-(SGTS)
(EIIStBH) initiated. ,
At 0958 hours0.0111 days <br />0.266 hours <br />0.00158 weeks <br />3.64519e-4 months <br /> on~ December 6, 1989, licensed Main Control Room (MCR) operators observed annunciator indication in the MCR for-isolations of the above-listed PCRVICS valves. Additionally, the l I&C technicians immediately notified the MCR operators that the-test jack was inadvertently grounded.
MCR operators restored the PCIG system at :1004' hours on December 6, 1989', using PCRVICS isolation bypass switches in accordance with General Plant (GP) procedure GP-8, " Primary and Secondary
' Containment Isolation Verification and Reset." The blown fuse was then replaced by the I&C technicians. MCR operators then reset and restored the remaining isolations by 1030 hours0.0119 days <br />0.286 hours <br />0.0017 weeks <br />3.91915e-4 months <br /> on December 6, 1989, using GP-8. All PCRVICS isolations previously-mentioned above.were reset, and normal system operations were restored within 32 minutes. The'I&C technicians then proceeded with the ST, .and completed:it satisfactorily.
A four'(4) hour notification was made to the NRC on December 6, 1989, at 1146 hours0.0133 days <br />0.318 hours <br />0.00189 weeks <br />4.36053e-4 months <br /> in accordance with the requirements of 10 CFR ,
50 72 (b)(2)(ii), since this event resulted in automatic actuations of ESFs. Accordingly, this report is being submitted ~l in accordance with the requirements of 10 CFR 50.73 (a)(2)(iv). )
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LICENSEE EVENT REPORT (LER) TEXT CONTINUATION - amoveo ove nomio cio.
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- j. Consequences'of the Event:
The" consequences of this event were minimal. There was no release of-. radioactive = material to the environment as a result-of ;
-this event. The Unit-1 PCRVICS isolation valves and system actuations functioned as designed;under the loss of the system i
control logic power condition created by the blown power' supply fuse. The Unit 1 isolations were bypassed or reset.- The affected systems were restored to their pre-transient conditions by operators in accordance with plant procedures within 32 minutes. This prevented any adverse impact on plant systems.
Unit 2 was shutdown for an outage, there were no consequences.
associated with the valve actuations that occurred on Unit 2.
Had Unit 2 been at power, the consequences of only the PCRVICS valve actuations would have been the same as described for Unic 1 above.
Immediate and follow-up actions to this type of event (i.e., loss of logic power) are provided in procedure GP-8. Licensed operators receive requalification training to review and. perform operator responses to transients of this type. This training provides practice on immediate operator actions and minimi::es the length of time certain systems are isolated reducing the adverse impact on the plant. Therefore, as a result.of adequate procedural guidance, training, and prompt operator actions, the ,
event duration was limited and no adverse plant conditions developed.
Additionally, if the fault introduced der : the performance of ,
the ST had resulted in this logic system he inoperable, the redundant PCRVICS isolation logic channe? ave been available to isolate the PCRVICS system ir Icq * ', The redundant trains of RERS and SGTS were unaffect.e,2 a this event.
Both trains were available if the other train had S iled and an actual. event requiring their use had occurred.
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The cause of this event was a personnel error due to a lack of i attention to, detail by an I&C technician performing procedure ST- I 2-026-618-1. During performance of the ST, a procedural step l L instructs the technician to obtain voltage readings from the i
radiation monitor trip unit test jack. A key switch located l directly above the trip unit test jack is used to place the trip unit from the normal condition to the test condition. The technician inserted the key, which was on a key ring with other i keys, into the trip unit key switch, and turned the key to'the test position. A contributing factor to the cause of this-event was the fact that the voltage meter jumper lead was not long enough to allow the meter to be placed on the AER floor, and the technician had to hold the voltage meter in one hand while performing the ST. As the technician was inserting the voltage meter jumper lead into-the trip unit test jack using his other
.- hand, he-simultaneously contacted one of the keys hanging from the key ring with the test jack, causing a short to ground. This short caused the system control logic power supply fuse, B21-F101A, to blow initiating the previous mentioned isolations and system actuations.
Corrective Actions:
In accordance with procedure GP-8, the Unit 1 PCIG system isolation was bypassed at 1004 hours0.0116 days <br />0.279 hours <br />0.00166 weeks <br />3.82022e-4 months <br /> on December 6, 1989. The I&C technicians then replaced the blown logic power supply fuse.
MCR operators reset and restored the remaining Unit 1 and Unit 2 isolations and systems by 1030' hours on December 6, 1989, in accordance with GP-8, returning both units to pre-transient conditions. The I&C technicians then proceeded with the ST, and completed it satisfactorily.
Actions Taken to Prevent Recurrence:
The I&C technicians involved with this event were counseled to -
stress the importance of a higher level of attention to detail
'while performing work tasks. The following corrective actions will be implemented by January 31, 1990 to minimize the possibility of similar events.
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L 1. Teni(10) foot test' leads will be issued to all I&C b technicians.- This will allow the technician access to difficult-test coint locations, while the associated, test'
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L equipment ~ remains in a safe environment. ,
- 2. An I&C test key issuance control program is.being developed. d' This will assure that the test' switch keys are issued singularly for testing purposes. ,
- 3. This event will be discussed at the next I&C All Hands .
Meeting. This discussion.will also convey the continuous need to use proper techniques while performing testing or ,
troubleshooting and the importance of using precautions to prevent exposed metal surfaces on test leads-and tools from ,
shorting to ground.- Both the proper test lead lengths and l' the I&C. key control program will be discussed at the next meeting.
Additionally,Han I&C task force was assembled following the i occurrence.of LER 2-89-011, which reported a blown fuse in the AER due to personnel error. This task force performed a root j cause analysis of LER 2-89-011, in addition to an analysis of the previous similar LERs listed below. These similar LERs also resulted from personnel errors by I&C technicians working in the AER. On November 16, 1989, the root cause analysis was completed '
and the following corrective action will be implemented.
o An I&C Technician Cood Practice Guideline that provides specific examples of what is considered good work practices has been developed. The Guideline focuses specifically on ,
surveillance testing in the AER. This Guideline has been formulated to enhance technician work practices and to stimulate higher-level thought processes (awareness of the big picture, while performing specific tasks) used by the technicians during the performance of STs. The Guideline will be presented at the next series of I&C continuing training sessions starting on January 9, 1990.
Previous Similar Occurrences:
LERs 1-84-021, 1-84-030, 1-85-011, 1-85-012, 1-85-049, 1-85-074, -
1-86-045, 1-87-021, 1-87-038, 1-89-006, and 2-89-011 also
' reported PCRVICS isolations due to a blown fuse as a result of personnel error.
Tracking Codes: (A) Personnel Error j l
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