ML18102A769

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Forwards Memo Which Discusses Event Re LER 96-040-00
ML18102A769
Person / Time
Site: Salem PSEG icon.png
Issue date: 01/19/1997
From: Garchow D
Public Service Enterprise Group
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
Shared Package
ML18102A770 List:
References
LR-N970039, NUDOCS 9701240309
Download: ML18102A769 (2)


Text

Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038-0236 Nuclear Business Unit JAN 191997 LR-N970039 U.S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 LER 272/96-040-00 SALEM GENERATING STATION - UNIT 1 FACILITY OPERATING LICENSE NO. D£R-70 DOCKET NO. 50-272.

Gentlemen:

This Licensee Event Report entitled "Buffer Relays Omitted From Technical Specification Required Response Time Surveillance Tests" is being submitted pursuant to the requirements of the Code of Federal Regula~ions 10CFRSO. 73 (a) (2) (i) (B).

Sincerely, G12f.~~/

General Manager Salem Operations Attachment

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LER File 3.7 9701240309 970119 PDR ADOCK 05000272 S PDR The power is in your hands.

95-2168 REV. 6/94

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Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038-0236 Nuclear Business Unit

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TO: Lou Storz FROM: David F. Garchow

SUBJECT:

LER #272/96-040-00 DATE: JAN 191997

Title:

Buffer Relays Omitted From Technical Specification Required Response Time Surveillance Tests

  • Root Cause:

The cause of this occurrence was determined to be inadequate implementation of Technical Specification requirements. This resulted in inadequate procedures for testing of the ESFAS functions.

  • Systems affected:

Engineered Safety Feature Actuation System

  • There were no safety consequences with this LER. The health and safety of the public was not affected.
  • Corrective Actions:
1. The Salem Unit 2 time response procedures will be revised and testing of the omitted relays will be completed prior to Salem Unit 2 entering Mode 4.
2. The procedures for Salem Unit 1 will be revised and testing performed prior to Unit 1 entering Mode 4.
3. A Technical Specification Surveillance Improvement Program (TSSIP) has been initiated foL Salem Units 1 and 2. The scope and content of the TSSIP program was described previously in LER 311/96-008-00. The TSSIP review is expected to be completed by December 31, 1397.

The pmver is in your hands.

95-2168 REV. 6/94