09-16-2004 | Unit Status: At the time of the event, Unit 1 and Unit 2 were in Mode 1 (Power Operation) at 100 percent power.
Event Description: In October 2001, procedure actions were implemented to close and remove motive electrical power from valve CA86A, "A" train assured water supply to the Turbine Driven Auxiliary Feedwater Pump. This condition rendered each Unit's Turbine Driven Auxiliary Feedwater Pump inoperable for approximately eight days.A The failure to recognize this condition resulted in a failure to satisfy Auxiliary Feedwater System Technical Specification requirements.A (a)(2)(i)(B). This condition is reportable as per 10 CFR 50.73A This event was not significant with respect to the health and safety of the public.
Event Cause: Inadequate procedure revision resulted in inoperable Turbine Driven Auxiliary Feedwater Pumps.
Corrective Action: Applicable procedures were revised to adequately address operability. Performed a review of other station procedures that close and remove motive electrical power from CA86A and revised any procedures with similar discrepancies or placed them on hold. Evaluation will be performed to verify that procedure revisions were adequately justified. |
---|
LER-2004-001, Auxiliary Feedwater System in prohibited condition due to inadequate procedure.Docket Number |
Event date: |
00-16-2001 |
---|
Report date: |
09-16-2004 |
---|
3692004001R00 - NRC Website |
|
BACKGROUND
Auxiliary Feedwater System [BA](CA):
The CA system provides an emergency feedwater supply to the steam generators [SG](SG) if the respective Unit's Condensate and Feedwater System [KA-SJ](CF) is not available. The CA system is capable of transferring fission product decay heat and other residual heat loads from the reactor coolant system [AB](NC) to a heat sink during both normal operation and accident conditions. The CA system also supports the operation of the Standby Shutdown System [ED](SSS).
Each Unit's CA system contains an "A" and "B" train motor driven pump [P] (MDCAP) and a "C" train turbine driven pump [P](TDCAP) configured into three trains. The normal suction source of water for the MDCAPs and TDCAP is the CA storage tank [TK](CAST). The Nuclear Service Water System [BI](RN) provides the assured suction source of water for the CA pumps when the normal suction supply from the CAST is not available.
The "A" and "B" train MDCAPs are supplied assured suction water from the "A" and "B" RN train discharge headers respectively. The TDCAP was designed to be supplied an assured source of suction water from either the "A" RN train discharge header via isolation valve CA86A or by the "B" RN train discharge header via isolation valve CA116B. To this end, these normally closed valves are designed to automatically open upon receipt of an Engineered Safety Feature [JE](ESF) CA pump low suction pressure signal. CA86A and CA116B are supplied motive power from the respective train's emergency diesel generator [EK](EDG).
RN System:
Each Unit's RN system is comprised of an "A" and "B" train. Lake Norman [ES] and the Standby Nuclear Service Water Pond (SNSWP) serve as the worst case design basis accident (DBA) heat sinks/cooling water reservoirs for RN. The SNSWP, which is seismically designed, serves as the most severe natural phenomena (earthquake) heat sink/cooling water reservoir for RN assuming Lake Norman is lost due to its' non-seismic design.
During normal operation, both the "A" and "B" trains of RN are aligned to take suction off Lake Norman. After use by components served by the system, the RN water is returned to Lake Norman via RN discharge headers. However, to support infrequent plant evolutions, either or both of the RN trains can be aligned to the SNSWP using station procedures OP/1/A/6400/006 (Unit 1) and OP/2/A/6400/006 (Unit 2).
McGuire Technical Specification (TS) 3.7.5 - Auxiliary Feedwater System:
The TS 3.7.5 Limiting Condition for Operation (LCO) specifies that a Unit's three CA trains shall be operable in Mode 1. As per TS 3.7.5, Condition B, if one of the required trains is inoperable, Unit operation may proceed provided the inoperable train is restored to operable status within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> and within 10 days of discovery of a failure to meet the LCO. If the required action and associated completion time of Condition B are not met, then TS 3.7.5, Condition C states that the respective Unit must be in MODE 3 within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in MODE 4 within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.
Summary of Applicable Reporting Requirements For This Event:
On July 21, 2004, McGuire Nuclear Station identified that, in October of 2001, Unit 1 and Unit 2 were in a condition which rendered each Unit's TDCAP inoperable for a period longer than permitted by TS 3.7.5, Condition B. Since this condition was not recognized, the required actions and associated completion time of TS 3.7.5, Condition C, were not satisfied. This is being reported as a condition prohibited by TSs.
At the time of the October 2001 event described above, both Units were in MODE 1 at approximately 100 percent power. No additional structures, systems, or components were out of service at the time of the event which contributed to either the events occurrence or significance.
EVENT DESCRIPTION
February 1993:
Unit 1 and 2 procedures were revised to address the potential for air in the "A" RN train discharge header to migrate to the suction of the TDCAP during the infrequent alignment of that discharge header to the SNSWP (reference (Unit 1) and OP/2/A/6400/006 (Unit 2) were changed to close CA86A ("A" RN train assured water supply to the TDCAP) and remove motive electrical power from that valve prior to aligning the "A" RN train discharge header to the SNSWP. These actions did not require the TDCAP to be declared inoperable.
October 2003:
The February, 1993 revisions to OP/1/A/6400/006 and OP/2/A/6400/006 were deemed inadequate to maintain the TDCAPs operable. Whenever CA86A is closed with motive electrical power removed and the TDCAP not declared inoperable, it would be necessary to assume a worst case single failure concurrent with an event requiring actuation of the TDCAP. The assumed single failure would be a "B" EDG failure preventing operation of normally closed CA116B, the "B" RN train assured water supply valve to the TDCAP. This, in conjunction with the inability to operate CA86A, would result in the unavailability of both the "A" and "B" RN train assured water supplies to the TDCAP. Since this condition would preclude the pump from satisfying required redundancy requirements, the TDCAP would be inoperable. Upon identifying this problem, OP/1/A/6400/006 and OP/2/A/6400/006 were placed on hold, precluding performance of the actions that close and remove motive electrical power from CA86A.
November 2003:
OP/1/A/6400/006 and OP/2/A/6400/006 were revised to ensure, prior to closing CA86A and removing motive electrical power, either:
- The "B" RN train assured water supply is manually aligned to provide a suction source of water for the TDCAP.
These revised actions adequately addressed the TDCAP operability concerns identified in October, 2003 with respect to the availability of an assured water supply. Therefore, OP/1/A/6400/006 and OP/2/A/6400/006 were removed from hold status.
July 21, 2004:
McGuire identified that performances of OP/1/A/6400/006 and OP/2/A/6400/006 in 2001 rendered each Unit's TDCAP inoperable for a period longer than the 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> allowed by TS 3.7.5, Condition B. Specifically, the Unit 1 CA86A valve was closed with motive power removed from approximately 2151 on CA86A valve was in the same condition from approximately 2152 on October 13, 2001 through approximately 2141 on October 21, 2001. No other structures, systems, or components were out of service during these periods which contributed to either the event occurrence or significance. Since, in 2001, it was not recognized that this condition rendered the Unit 1 and 2 TDCAPs inoperable for a period longer than allowed by TS 3.7.5, Condition B, the required actions and associated completion time of TS 3.7.5, Condition C, were not satisfied. This represented a TS prohibited condition reportable under the requirements of 10 CFR 50.73 (a)(2)(i)(B). Note that non-assured suction sources for the TDCA pump were available and the "A" and "B" MDCAPs remained operable.
CAUSAL FACTORS
Procedure Deficiency:
In 1993, McGuire station procedures OP/1/A/6400/006 and OP/2/A/6400/006 were changed to close CA86A and remove motive electrical power from that valve prior to aligning the "A" RN train discharge header to the SNSWP. These actions did not require the TDCAP to be declared inoperable. However, since these actions did not ensure availability of an assured water supply to the TDCAP, these changes were inadequate to maintain the TDCAPs operable.
CORRECTIVE ACTIONS
1) OP/1/A/6400/006 and OP/2/A/6400/006 were revised in November, 2003 to address the inadequacies identified in October, 2003.
2) A review was performed of other station procedures that close and remove motive electrical power from CA86A. Procedures with similar discrepancies were either revised to adequately address operability or they were placed on hold.
3) During preparation of this LER, a question arose regarding the adequacy of the basis for the 1993 and 2003 revisions to OP/1/A/6400/006 and OP/2/A/6400/006. Pending completion of an evaluation, portions of those procedures that allow closing and removing motive electrical power from CA86A without declaring the TDCAP inoperable have been placed on hold. Other administrative controls have been implemented to address TDCAP operability. If further evaluation identifies information significant to the understanding of this event or it results in substantial changes to the corrective action plan, a revised LER will be submitted providing this information.
SAFETY ANALYSIS
A probabilistic risk assessment of this event determined that, for the amount of time that CA86A was closed and motive power removed beyond the 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> allowed by TS 3.7.5, Condition B, the increase in the estimated core damage frequency (CDF) or large early release frequency (LERF) was insignificant. The basis for this is the limited impact that the inoperable valve has on the functionality of the CA System given the availability of non-assured suction sources for the TDCA pump and the fact that the "A" and "B" MDCAPs remained operable.
Based upon the above, the condition described in this LER had a very minor impact on the ability to mitigate risk significant accidents and the risk increase attributable to this event was not significant with respect to the health and safety of the public.
ADDITIONAL INFORMATION
In October 2003, when it was recognized that the February, 1993 revisions to OP/1/A/6400/006 and OP/2/A/6400/006 were inadequate to maintain the TDCAPs operable, a reportability review was conducted.
That review failed to identify any reportable conditions. This failure is being addressed by McGuire's corrective action program.
A review of the McGuire corrective action database did not identify any previous occurrences of a similar event.
Applicable Energy Industry Identification (EIIS) system and component codes are enclosed within brackets. McGuire unique system and component identifiers are contained within parentheses.
|
---|
|
|
| | Reporting criterion |
---|
05000348/LER-2004-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000333/LER-2004-001 | Inadvertent Actuation of ECCS and EDGs While in Refueling Mode | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000306/LER-2004-001 | | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000315/LER-2004-001 | Failure To Comply With Technical Specification 3 .7 .5 .1, Control Room Emergency Ventilation System | | 05000301/LER-2004-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000313/LER-2004-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000285/LER-2004-001 | Failure To Perform A Leakage Test Due To Lack Of Understanding of Penetration Design | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000271/LER-2004-001 | Main Steam Isolation Valve Leakage Exceeds a Technical Specification Leakage Rate Limit | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000266/LER-2004-001 | | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000318/LER-2004-001 | . Reactor Trip Due to Low Steam Generator Water Level After Feed Pump Trip | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000289/LER-2004-001 | | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000263/LER-2004-001 | | | 05000247/LER-2004-001 | Manual Reactor Trip Due to Oscillating Feedwater Flow and Steam Generator Level with Flow Perturbations Caused by a Degraded Feed Water Regulating Valve | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(iv), System Actuation | 05000244/LER-2004-001 | Gaps in the Control Room Emergency Zone Boundary | | 05000255/LER-2004-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000364/LER-2004-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000461/LER-2004-001 | Clinton Power Station 05000461 1 OF 4 | | 05000414/LER-2004-001 | relPowere Vice President A Duke Energy Company Duke Power Catawba Nuclear Station 4800 Concord Rd. / CNO1VP York, SC 29745-9635 803 831 4251 803 831 3221 fax November 9, 2004
U. S. Nuclear Regulatory Commission
ATTENTION: Document Control Desk
Washington, DC 20555-0001
SUBJECT: Duke Energy Corporation
Catawba Nuclear Station Unit 2
Docket No. 50-414
Licensee Event Report 414/04-001 Revision 0
Reactor Coolant System Pressure Boundary Leakage
Due to Small Cracks Found in Steam Generator
Channel Head Bowl Drain Line on 2C & 2D Steam
Generators
Attached please find Licensee Event Report 414/04-001
Revision 0, entitled "Reactor Coolant System Pressure
Boundary Leakage Due to Small Cracks Found in.Steam
Generator Channel Head Bowl Drain Line on 2C & 2D Steam
Generators."
This Licensee Event Report does not contain any regulatory
commitments. Questions regarding this Licensee Event Report
should be directed to R. D. Hart at (803) 831-3622.
Sincerely,
Dhiaa Jamil
Attachment
www.dukepower.corn 00- U.S. Nuclear Reguldhory Commission
November 9, 2004
Page 2
XC: W.D. Travers
U.S. Nuclear Regulatory Commission
Regional Administrator, Region II
Atlanta Federal Center
61 Forsyth St., SW, Suite 23T85
Atlanta, GA 30303
E.F. Guthrie
Senior Resident Inspector (CNS)
U.S. Nuclear Regulatory Commission
Catawba Nuclear Station
S.E. Peters (addressee only)
NRC Project Manager (CNS)
U.S. Nuclear Regulatory Commission
One White Flint North, Mail Stop 10-B3
11555 Rockville Pike
Rockville, MD 20852-2738
NRC FORM 366� U.S. NUCLEAR REGULATORY APPROVED BY OMB: NO. 3150-0104 EXPIRES: 06/30/2007 (6-2004)� COMMISSION Estimated burden per response to comply with this mandatory collection request 50
hours. Reported lessons learned are Incorporated Into the licensing process and fed back
to Industry. Send comments regarding burden estimate to the Records and FOIA/Privacy
Service Branch (T-5 F52), U.S. Nuclear Regulatory Commission, WashinMon, DC 2055
LICENSEE EN/ENT REPORT (LER) 0001, or by Internet e-mail to infocollects@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104). Office of Management(See reverse for required number of and Budget, Washington, DC 20503. If a means used to impose an Information col ectiond( inverse �for each block) does not display a currently valid OMB control number, the NRC may not conduct or sponsor. and a person Is not required to respond o. the Information collection. 1. FACILITY NAME 2. DOCKET NUMBER 3. PAGE Catawba Nuclear Station, Unit 2 050- 00414 1 OF�6 4. TITLE Reactor Coolant System Pressure Boundary Leakage Due to Small Cracks Found in
Steam Generator Channel Head Bowl Drain Line on 2C & 2D Steam Generators | | 05000368/LER-2004-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000423/LER-2004-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000334/LER-2004-001 | Control Rod Shutdown Bank Anomaly Causes Entry into Technical Specification 3.0.3 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000413/LER-2004-001 | Gas Accumulation in Centrifugal Charging Pump Suction Piping | 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000395/LER-2004-001 | Reactor Trip Due to Valve Failure During Forced Shutdown | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000390/LER-2004-001 | Automatic Reactor Trip Due to a Invalid Turbine Trip Signal (P-4) | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000369/LER-2004-001 | Auxiliary Feedwater System in prohibited condition due to inadequate procedure. | | 05000454/LER-2004-001 | Exelent
Exelon Generation Company, LLCRwww.exeloncorp.com NuclearByron Station 4450 North German Church Road Byron, IL 61010-9794 October 17, 2004 LTR: BYRON 2004-0111 File: 2.01.0700 United States Nuclear Regulatory Commission ATTN: Document Control Desk Washington, DC 20555-0001 Subject:RLicensee Event Report (LER) 454-2004-001-00, "Reactor Containment Fan Coolers Flow Rates Below Technical Specification Requirements Due to Inaccurate Flow Indication" Byron Station, Unit 1
Facility Operating License No. NPF-37
NRC Docket No. STN 50-454
Enclosed is an LER involving the August 17, 2004, event involving low flow conditions discovered in Unit 1 Reactor Containment Fan Coolers for a time period longer than allowed by the Technical Specifications. This event is reportable to the NRC in accordance with 10CFR 50.73 (a)(2)(i)(B), as a condition prohibited by Technical Specifications. Should you have any questions concerning this matter, please contact Mr. William Grundmann, Regulatory Assurance. Manager, at (815) 234-5441, extension 2800. Respectfully, Stephen E. Kuczynski Site Vice President Byron Nuclear Generating Station Attachment LER 454-2004-001-00 cc:RRegional Administrator, Region III, NRC NRC Senior Resident Inspector— Byron Station NRC FORM 366 U.S. NUCLEAR REGULATORY APPROVED BY OMB NO. 3150-0104 EXPIRES 7-31-2004 (7.2001) COMMISSION Estimated burden per response to comply with this mandatory information collection request 50 hours. Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the Records Management Branch (T.6 E6), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by Internet e-mail toLICENSEE EVENT REPORT (LER) *I@ nrc.gov, and to the Desk Officer, Office of Informabon and Regulatory Affairs, NEOB:10202 (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose information collection does not display a currently valid OMB control number, the NRC may not _ conduct or sponsor, and a person is not required to respond to, the information collection. 1 rand ITV NAUP o natuerr An warn q par= . Byron Station, Unit 1 0500454 1 OF 5 4. Reactor Containment Fan Coolers Flow Rates Below Technical Specifications Requirements Due to Inaccurate Flow Indication | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000305/LER-2004-001 | | 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | 05000336/LER-2004-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000364/LER-2004-002 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000423/LER-2004-002 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000237/LER-2004-002 | Dresden Nuclear Power Station Unit 2 05000237 1 of 5 | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000261/LER-2004-002 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000244/LER-2004-002 | Consolidated Rod Storage Canister Placed in Incorrect Storage Location | | 05000530/LER-2004-002 | Main Turbine Control System Malfunction Results in Automatic Reactor Trip on Low DNBR | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000305/LER-2004-002 | | | 05000247/LER-2004-002 | Manual Reactor Trip Due to Decreasing 23 Steam Generator Level Caused by Feedwater Regulating Valve Closure Due to a De-energized Solenoid Operated Valve from Wiring Failure | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000414/LER-2004-002 | Manual Reactor Trip Initiated Due to Control Rods from Shutdown Bank D Dropping into the Core | | 05000251/LER-2004-002 | AAA | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(iv)(b) | 05000397/LER-2004-002 | | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000346/LER-2004-002 | Reactor Trip During Reactor Trip Breaker Testing Due To Fuse Failure | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000395/LER-2004-002 | Emergency Diesel Generator Start and Load Due to Momentary Fault on Incoming Feed | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000269/LER-2004-002 | eif Powere RON A. JONES Vice President A Duke Energy Company Oconee Nuclear Site Duke Power ONO1VP / 7800 Rochester Highway Seneca, SC 29672 864 885 3158 864 885 3564 fax September 9, 2004
U.S. Nuclear Regulatory Commission
Document Control Desk
Washington, D.C. 20555
Subject: Oconee Nuclear Station
Docket Nos. 50-269,-270, -287
Licensee Event Report 269/2004-02, Revision 1
Problem Investigation Process No.: 0-04-2808
Gentlemen:
Pursuant to 10 CFR 50.73 Sections (a)(1) and (d), attached
is Licensee Event Report 269/2004-02, Revision 1, regarding
a Main Steam Line Break mitigation design/analysis
deficiency which could result in the main and startup
feedwater control valves being technically inoperable for
mitigation of some steam line break scenarios.
This report is being submitted to supplement Revision 0
submitted July 6, 2004. At that time the root cause
investigation and an analysis of the consequences of
potentially exceeding the Environment Qualification (EQ)
envelope curve were still in progress.
This event is being reported in accordance with 10 CFR
50.73 (a)(2)(i)(B) as a condition prohibited by Technical
Specifications, 50.73(a)(2)(ii)(B) as an Unanalyzed
Condition, and 50.73(a)(2)(V)(D) as a potential loss of
safety function for Accident Mitigation. This event is
considered to be of no significance with respect to the
health and safety of the public.
www.dukepower.corn Document Control Desk
Date: September 9, 2004
Page 2
Attachment: Licensee Event Report 269/2004-02, Revision 1
cc: Mr. William D. Travers
Administrator, Region II
U.S. Nuclear Regulatory Commission
61 Forsyth Street, S. W., Suite 23T85
Atlanta, GA 30303
Mr. L. N. Olshan
Project Manager
U.S. Nuclear Regulatory Commission
Office of Nuclear Reactor Regulation
Washington, D.C. 20555
Mr. M. C. Shannon
NRC Senior Resident Inspector
Oconee Nuclear Station
INPO (via E-mail)
NRC FORM 366 U.S. NUCLEAR REGULATORY APPROVED BY OMB NO. 3150-0104 EXPIRES 7-31-2004 (7-2001) COMMISSION Estimated burden per response to comply with this mandatory information collection request: 50 hours. Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the Records Management Branch (T-6 E6), U.S. Nuclear Regulatory Commission, Washington. DCLICENSEE EVENT REPORT (LER) 20555-0001, or by Internet e-mail to bpi @nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202 (3150-0104), Office of Management and(See reverse for required number of Budget, Washington, DC 20503. If a means used to impose information collection doesdigits/characters for each block) not display a currently valid OMB control number, the NRC may not conduct or sponsor, and,1 nnmnn lc not rent Owl to tocnnni-I to the intnrmatinn rntlentinn 1. FACILITY NAME 2. DOCKET NUMBER 3. PAGE Oconee Nuclear Station, Unit 1 050-81 OF 0269 11 4. TITLE Main Steam Line Break Mitigation Design/Analysis Deficiency | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | 05000313/LER-2004-002 | | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000271/LER-2004-002 | Special Nuclear Material Inventory Location Discrepancy | | 05000285/LER-2004-002 | Inoperable Diesel Generator for 28 Days Due to Blown Fuse During Shutdown | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000336/LER-2004-002 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000311/LER-2004-002 | Failure To Comply With Technical Specifications During Reactor Protection Instrument Calibration . | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000254/LER-2004-002 | Quad Cities Nuclear Power Station Unit 1 05000254 1 of 4 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000263/LER-2004-002 | | | 05000302/LER-2004-002 | Emergency Diesel Generator Inoperable Due To Fuel Oil Header Outlet Check Valve Leaking Past Seat | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
|