05000369/LER-2022-001, Both Control Room Area Chilled Water System Trains Inoperable Due to Human Error

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Both Control Room Area Chilled Water System Trains Inoperable Due to Human Error
ML22230C557
Person / Time
Site: McGuire, Mcguire  Duke Energy icon.png
Issue date: 08/18/2022
From: Pigott E
Duke Energy Carolinas
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
RA-22-0246 LER 2022-001-00
Download: ML22230C557 (7)


LER-2022-001, Both Control Room Area Chilled Water System Trains Inoperable Due to Human Error
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(v), Loss of Safety Function
3692022001R00 - NRC Website

text

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~ ENERGY Serial No: RA-22-0246 August 18, 2022 U.S. Nuclear Regulatory Commission Washington, D.C. 20555 ATTENTION: Document Control Desk

Subject:

Duke Energy Carolinas, LLC McGuire Nuclear Station, Units 1 and 2 Docket Nos. 50-369 and 50-370 Renewed License No. NPF-9, NPF-17 Licensee Event Report 2022-001, Revision 0 Nuclear Condition Report Number 02432084 Edward R. Pigott Site Vice President McGuire Nuclear Station Duke Energy MG01VP 112700 Hagers Ferry Road Huntersville, NC 28078 o: 980.875.4805 Edward.Pigott@duke-energy.com 10 CFR 50.73 Pursuant to 10 CFR 50. 73 Section (a)(2)(v)(D), attached is Unit 1 and 2 Licensee Event Report (LER) 2022-001, Revision 0, regarding concurrent inoperability of both trains of Control Room Area Chilled Water System (CRACWS) due to human error.

This event is considered to have no significance with respect to the health and safety of the public. There are no regulatory commitments contained in this LER.

If questions arise regarding this LER, please contact Jeff Sanders at 980-875-4680.

Sincerely, Edward R. Pigott Duke Energy McGuire Nuclear Station Site Vice President Attachment

U.S. Nuclear Regulatory Commission RA-22-0125 Page 2 cc:

Laura A. Dudes Administrator Region II U.S. Nuclear Regulatory Commission Marquis One Plaza 245 Peachtree Center Avenue NE Suite 1200, 30303-1257 J. Klos Project Manager (McGuire)

U.S. Nuclear Regulatory Commission Mail Stop O-9-E3 11555 Rockville Pike Rockville, MD 20852 Andy Hutto NRC Senior Resident Inspector McGuire Nuclear Station

Abstract

At 2240 [EST] on June 21, 2022, with Unit 1 and Unit 2 operating at approximately 100 percent power and the A train of the Control Room Area Chilled Water System (CRACWS) inoperable for planned maintenance, a loss of safety function occurred when the B train CRACWS chiller tripped. A clearance required for maintenance on the A train was being performed when a non-licensed auxiliary operator (AO) opened the breaker feeding the oil pump associated with the running and operable B train. This resulted in an inadvertent trip of the B Chiller. With both CRACWS trains inoperable, Operations entered Abnormal Procedure AP-39 (Control Room High Temperature) and restored the B train within thirty-five minutes.

The cause of this event is attributed to a human performance error in which the AO did not effectively use human performance tools to ensure the correct component was identified prior to operation. In addition to prompt restoration of the B Train of CRACWS and the system's safety function, corrective actions were initiated to improve accountability of the operator associated with this event, and implementation of additional layers of defense when placing clearances.

This event had no impact on the health and safety of the public.

BACKGROUND YEAR 2022 SEQUENTIAL NUMBER

- 001 REV NO.
- 00 The following information is provided to assist readers in understanding the event described in this LER.

Applicable Energy Industry Identification [EIIS] system and component codes are enclosed within brackets.

Control Room Area Chilled Water System [KM]

The purpose of the Control Room Area Chilled Water System (CRACWS) [KM] is to provide chilled water to the Control Room and Control Room Area Ventilation (CRA VS) [VI] equipment to maintain temperature within Technical Specification limits.

The CRACWS system has two redundant trains (A and B) serving the CRA VS air handling units providing cooling of recirculated control room air. The CRACWS operates in conjunction with the CRA VS and are shared between both McGuire units. These trains are normally not cross-connected. Each CRACWS train consists of a compression tank to provide water surge protection, a chilled water pump and a control area chiller. Chilled water circulates in a closed loop. Each chiller has its own separate refrigeration system. The CRACWS water exchanges heat with the refrigerant in the evaporator to be chilled to a desired temperature.

The CRACWS is an emergency system which also operates during normal unit operations. A single train will provide the required temperature control to maintain the control room at approximately 75°F. The control room is shared between units.

NRC FORM 3666 (08-2020)

Page 2 of 5 (08-2020)

U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY 0MB: NO. 3150-0104 EXPIRES: 08/31/2023 LICENSEE EVENT REPORT (LER)

CONTINUATION SHEET (See NUREG-1022, R.3 for instruction and guidance for completing this form https://www.nrc.gov/reading-rm/doc-collections/nuregs/staff/sr1022/r30

3. LER NUMBER YEAR McGuire Nuclear Station, Unit 1 05000-369 SEQUENTIAL NUMBER REV NO.

2022

- 001
- 00

EVENT DESCRIPTION

At 2240 on June 21, 2022, a loss of safety function occurred due to concurrent inoperability of both required CRACWS trains for 35 minutes. A clearance required for planned maintenance on the A CRACWS chiller was being performed when a non-licensed operator incorrectly opened the breaker supplying the oil pump associated with the running and operable B CRACWS Chiller. Prior to opening the incorrect breaker, the A CRACWS train was declared inoperable due to disconnecting the A CRACWS chiller compressor supply breaker per the approved clearance. Opening the B CRACWS chiller oil pump breaker resulted in a B CRACWS chiller trip which was supplying cooling to its required loads.

As a result of the loss of cooling, the control room staff entered Abnormal Procedure AP-39, the incorrectly opened breaker was reclosed, and the B CRACWS chiller was restarted. The chiller started as expected, and control room temperatures returned to normal. Engineering data was collected on the B CRACWS chiller, and all parameters indicated the chiller was functioning properly. The AP was exited after normal operation of the B CRACWS was confirmed.

Sequence of Events (times are approximate):

06/21 20:39, Clearance for the A CRACWS chiller was approved to hang in support of maintenance.

06/21 21 :24, A CRACWS declared inoperable due to the associated clearance.

06/21 22:40, Abnormal Procedure AP-39 was entered due to elevated control room temperature. Unit 1 and Unit 2 entered the appropriate Technical Specifications.

06/21 22:52, The B CRACWS chiller oil pump breaker was reclosed.

06/21 23:13, B CRACWS Chiller re-started per the Abnormal Procedure AP-39.

06/21 23:15, Unit 1 and Unit 2 exited the Technical Specifications required for two inoperable CRACWS.

06/21 23:38, Control room temperatures returned to pre-event conditions and Abnormal Procedure AP-39 was exited.

06/22 02:26, 8 Hour Notification made to NRC per 1 0CFR50.72(b)(3)(v)(D).

REPORTABILITY DETERMINATION The concurrent inoperability of both trains of CRACWS was initially reported, as required, under 10 CFR 50.72(b)(3)(v)(D), "Any event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident."

This LER satisfies the corresponding written reporting criteria in 10 CFR 50.73(a)(2)(v)(D), "Any event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequence of an accident."

NRC FORM 3666 (08-2020)

Page 3 of 5 (08-2020)

U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY 0MB: NO. 3150-0104 EXPIRES: 08/31/2023 LICENSEE EVENT REPORT (LER)

CONTINUATION SHEET (See NUREG-1022, R.3 for instruction and guidance for completing this form https:/lwww.nrc.gov/reading-rm/doc-collections/nuregs/staff/sr1022/r3D

3. LER NUMBER YEAR McGuire Nuclear Station, Unit 1 05000-369 SEQUENTIAL NUMBER REV NO.

2022

- 001
- 00 CAUSAL FACTORS A cause investigation was completed for this event. The cause was found to be a non-licensed auxiliary operator did not use human performance tools effectively to ensure the correct component was identified prior to operation. A contributing cause was identified as a lack of adequate risk plan development and implementation by supervisors.

CORRECTIVE ACTIONS

Immediate Actions:

1. Restored power to the B CRACWS Chiller oil pump and restarted the chiller.

Interim and Subsequent Actions:

1. Appropriate accountability and remediation actions performed.
2. Department focus on activities involving clearances that require plant manipulations and associated procedures including additional layers of defense when placing clearances.
3. Develop and implement training solutions focused on risk recognition and risk plan implementation.

SAFETY ANALYSIS

The safety significance of the CRACWS is low because of the opportunity to mitigate the consequences of its loss with preplanned measures as described in plant Abnormal Procedures. As a result, the loss of the CRACWS system, including the chillers, has been screened out of the McGuire PRA as either an initiating event or as a support system failure. Therefore, the CRACWS has no impact on the calculated Core Damage Frequency (CDF) or Large Early Release Frequency (LERF) at McGuire. Additionally, during this event, maximum recorded control room temperature reached 81.4F prior to the restart of the B CRACWS chiller which is below the Technical Specification required maximum temperature of 90F.

There were no adverse effects on control room instrumentation, controls, or habitability during this event.

Given the above, this event was determined to be of no significance to the health and safety of the public.

NRC FORM 3666 (08-2020)

Page 4 of 5 (08-2020)

U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY 0MB: NO. 3150-0104 EXPIRES: 08/31/2023

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LICENSEE EVENT REPORT (LER)

CONTINUATION SHEET

1. FACILITY NAME
2. DOCKETNUMBER
3. LERNUMBER McGuire Nuclear Station, Unit 1 05000-369

ADDITIONAL INFORMATION

YEAR 2022 SEQUENTIAL NUMBER

- 001 A review of the McGuire corrective action program was conducted to determine if this was a recurring event (i.e., similar event with the same cause or same failure mode). No previous similar events were identified within the past three years associated with a loss of safety function due to human error.

Therefore, this is not considered a recurring event.

REV NO.

- 00 A review of previous reportable events for the past three years did not identify any additional similar LER events. Page 5 of 5