11-24-2004 | On September 24, 2004, at approximately 11:55 hours, Operations manually tripped the reactor as a result of decreasing 23 Steam Generator ( SG) level.T Prior to the event Control Room (CR) operators observed decreasing 23 SG level and received an alarm for 23 SG level control deviation.T CR operators attempted manual control of 23 FW regulating valve ( FRV) FCV-437 without success in restoring SG level.T The 23 SG level continued to decrease and as directed, the CR operator tripped the reactor at 15 percent SG level.TAll control rods fully inserted and all primary systems functioned properly.TThe plant was stabilized in hot standby with decay heat being removed by the main condenser. There was no radiation release.T Offsite power remained available therefore the emergency diesel generators did not start. The Auxiliary FW system automatically started as a result of a SG low level due to shrink effect. The cause of the event was de-energization of Solenoid Operated Valve ( SOV) FCV-SOV-437-E due to disconnection of wiring to the SOV coil causing the SOV to fail open resulting in closure of The failed connection was caused by the incorrect 23 FW FCV-437.
orientation of the SOV due to a modification that lacked sufficient information due to a failure to follow the Planning and Engineering procedure for the modification and lack of a questioning attitude.T Significant corrective actions were replacement of the FCV-437-SOV-E solenoid, inspection of remaining SOV connections and coaching on maintaining aiquestioning attitude.T Planning and Engineering procedures are to be reviewed and revised as necessary.
The event had no effect on public health and safety 1 |
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Note: The Energy Industry Identification System Codes are identified within brackets { }
DESCRIPTION OF EVENT
On September 24, 2004, at approximately 11:55 hours, while at 100% steady state reactor power, Operations manually tripped {JC} the reactor {RCT} as a result of decreasing 23 Main Feedwater (FW) {SJ} flow and 23 Steam Generator (SG) {S13} level. Prior to the event at 11:53 hours, a balance of plant (BOP) Control Room (CR) Operator observed decreasing 23 SG level and received an alarm for SG level control deviation. CR operators attempted manual control of 23 FW regulating valve FCV-437 and opened the low flow regulating valves for the 23 SG without success in restoring SG level. The level for the 23 SG continued to lower and as directed, the CR operator tripped the reactor at 15 percent SG level. All control rods fully inserted and all primary systems functioned properly. The plant was stabilized in hot standby with decay heat being removed by the main condenser.
There was no radiation release. Offsite power remained available therefore the emergency diesel generators did not start. The Auxiliary FW system automatically started as a result of a SG low level normally experienced on trips from full power (shrink effect). The 23 FW regulating valve FCV-437 Solenoid Operating Valve (SOV) FCV-SOV-437-E is a 125 VDC solenoid valve, Model No. HC8210C35, manufactured by ASCO. CR operators observed the rod bottom lights, Reactor Trip (RT) First Out Annunciator (Manual Trip). CR Operators entered procedure ES-0.1, secured the Main Boiler FW Pumps and subsequently transitioned to procedure POP- 3.2. The plant was stabilized in hot standby with decay heat being released to the main condenser via the steam dump valves 06. At 1320 hours0.0153 days <br />0.367 hours <br />0.00218 weeks <br />5.0226e-4 months <br />, a 4-hour non- emergency notification was made to the NRC for a reactor trip while critical under 10CFR50.72(b)(2)(iv)(B) and an AFW actuation under 10CFR50.72(b)(3)(iv)(A) (8- hour) (Incident Log No. 41066). Operations recorded the RT event in the corrective action program (CAP) as Condition Report CR-IP2-2004-04522. A post transient evaluation was performed on September 24, 2004. An investigation discovered that the FW regulating valve solenoid valve FCV-437-SOV-E had a failed electrical connection. An extent of condition investigation was performed for conduit/wiring connections to the remaining three FW regulating valve SOV's.
Engineering investigations were performed for all CAT-A Copes-Vulcan reverse acting AOV solenoids and a representative sample of the remaining non-reverse acting CAT-A AOV solenoid valves to verify proper configuration/orientation. The inspections were completed on November 6, 2004, and two discrepancies were identified (SOV-896A and SOV-896B). CR-IP2-2004-05743 recorded the condition and Work Orders were initiated. Operations determined there were no operability concerns with the conditions. An investigation into the cause of the FCV-437-SOV- E connection failure determined that during Unit 2 refueling outage cycle 15 (2R15) in October 2002, a design change package installed quick disconnects on Air Operated Valve (AOV) FCV-437 vent line. During the installation, the orientation of the SOV in that line was changed from its original design position (vertical) to a horizontal position without the required engineering analysis being performed. The FCV-437 actuator is a reverse acting type and therefore the actuator and the SOV move up and down when the valve is stroked lending itself to greater stresses when in the incorrect orientation.
Stress on the SOV was experienced on September 1, 2004, due to FW flow oscillations and flow perturbations that caused a thermal-hydraulic transient and FW pipe movement as a result of failed FW regulating valve FCV-427. After the RT for the September 1 event, a walk down discovered a broken conduit/condulet fastener for FCV-437-SOV-E associated with an adjacent AOV (FCV-437), and repairs performed. A CR recorded the broken conduit fastener, which was fixed immediately, but no degradation was noted for the SOV at that time. Following startup from the trip, two additional FW thermal-hydraulic transients/shutdowns occurred due to problems with FCV-427. On September 20, an inspection discovered the L-Tab of the FCV-437- SOV-E valve was pulled out of its housing. The condition was assessed and determined by the valve engineer to be degraded but still functional and repair should be deferred to the upcoming outage due to the trip risk for repair at power.
Subsequently, the conduit and its wiring pulled away from the SOV de-energizing it.
CAUSE OF EVENT
The cause of the manual reactor scram was decreasing 23 SG FW flow and level.
The cause of the decreasing 23 SG FW flow and level was a de-energized solenoid operated valve FCV-SOV-437-E as a result of a SOV wiring disconnection to the SOV coil which caused the SOV to fail open. The failed open FCV-SOV-437-E vented air off the air operated FW Regulating valve FCV-437 causing it to close and stop FW flow to SG 23. The direct cause of the wiring disconnection to the SOV was the failure of the housing L-Tab of FCV-SOV-437-E due to an improper change to the orientation of the SOV during a quick disconnect modification installation in 2002. The improper horizontal orientation of the SOV allowed the lateral forces from one of several thermal-hydraulic transients that preceded the failure, to negatively impact the integrity of the tab causing it to fail. There were two root causes (RC) identified. RC-1: The design modification and its associated work package for installation of the SOV quick disconnects did not contain sufficient detail to ensure the proper installation due to failure to follow Planning and Engineering procedures. Previous requirements of maintaining the SOV in the vertical orientation were not carried through from the original requirement. Only the impact of the air supply to the AOV was evaluated. RC-2:
The improper installation of quick disconnect modification to FCV-SOV-437-E was also due to inadequate verification of the accuracy of the change. Although the modification package was weak, a change to the orientation of the SOV from the as-found condition should have been checked and validated. The improper installation resulted in an orientation of the SOV that was not in accordance with the original intended position of the valve. The improper orientation of this SOV caused stresses to the structural components of the SOV that were greater and different than those seen by the vertically mounted valves. These stresses were sufficient to cause the L-Tab to be pulled outside of its housing and allowed it to be subjected to the movement of the pipe and actuator, now wholly unsupported, leading to the eventual failure of the L-Tab. A contributing cause was lack of attention to detail/questioning attitude in modification installation and review. During the installation of the SOV modification, the solenoid orientation was changed to a horizontal position from the as-found vertical position but was not questioned.
This new orientation was outside the original design for the component. This change to the orientation of the SOV was not recognized by the work planner, the installation workers, the contract supervisor overseeing the installation of the modification, the Quality Control inspector, or the design engineer verifying completion of the installation. A number of other additional enhancement corrective actions were taken as recorded in the CAP CR for this event.
CORRECTIVE ACTIONS
The following corrective actions have been or will be performed under the CAP to address the causes of this event and prevent recurrence.
1.Communicated to all site personnel the importance of maintaining a questioning attitude towards all work performed and discussed the event via a Red Memo and reset the Station Event Free Clock on September 27, 2004.
2.The FCV-437-SOV-E solenoid was replaced and returned to the proper vertical orientation and conduit/wiring properly connected. Repair was completed on September 25, 2004.
3.Engineering performed an extent of condition inspection of the FRV's following the Unit 2 trip. No other issues with tabs outside of the SOV housing were noted. The SOVs for the remaining FRV's showed no signs of metal fatigue or cracking. Four work orders were prepared to inspect and tighten any loose conduits. Action completed September 24, 2004.
4. IPEC Design Engineering (DE) performed a review of all open modifications where the work is not complete that could directly or indirectly affect the seismic evaluation, configuration or orientation of the solenoids associated with the FCV's. No modifications were found.
5.The current IPEC Design Engineering procedures will be reviewed and revised as necessary to ensure proper carry through of important design criteria for all Engineering Requests (ERs) and to ensure there's a requirement that all modification packages record the before and after orientation of all safety related components and equipment to ensure proper orientation is maintained unless otherwise specified by the Modification. Scheduled completion is March 1, 2005.
6.IPEC Planning, Scheduling and Outage (PS&O) procedures will be revised to include a requirement to ensure that all work package step lists record before and after orientation of all safety related components and equipment to ensure proper design orientation is maintained, unless otherwise specified by the Modification. Scheduled completion is January 3, 2005.
7.Project Managers and Engineers will be coached on the importance of field verifying Modification completion prior to signing off work packages as complete.
Scheduled completion is March 1, 2005.
8.A Supervisor tool kit was provided to Maintenance management for improved briefings containing a detailed discussion on verifying component orientation and maintaining a questioning attitude through use of proper Human Performance Tools and expectations on their use.
EVENT ANALYSIS
The event is reportable under 10CFR50.73(a)(2)(iv)(A). The licensee shall report any event or condition that resulted in manual or automatic actuation of any of the systems listed under 10CFR50.73(a)(2)(iv)(B). Systems to which the requirements of 10CFR50.73(a)(2)(iv)(A) apply includes the reactor protection system (RPS) including reactor scram or reactor trip, and AFWS. This event meets the reporting criteria because the RPS was actuated by manual trip and the AFWS actuated on low level due to steam generator level changes in response to the manual RT, which occurs after a RT from full power as a result of SG shrink.
PAST SIMILAR EVENTS
A review of the past two years of Licensee Event Reports (LERs) for events that involved a RT caused by FW flow transients identified LER-2004-001 dated October 25, 2004. This LER reported a manual reactor trip as a result of oscillating FW flow and SG level caused by a failed FW regulating valve FCV-427. The direct causes for these LERs are different however both have related causes of procedure deficiencies although the specific procedures involved are different.
SAFETY SIGNIFICANCE
This event had no effect on the health and safety of the public. There were no actual safety consequences for the event because the event was an uncomplicated reactor trip with no other transients or accidents. Required safety systems performed as designed when the manual RT was initiated. The AFWS actuation was an expected reaction as a result of decreasing SG water level due to the reduction of SG void fraction (shrink), which occurs after automatic RT/TT from full load.
There were no significant potential safety consequences of this event under reasonable and credible alternative conditions. The low SG level due to closure of the FCV as a result of the failure of the FCV SOV housing L-Tab and associated wiring/conduit is bounded by the worst case FW transient that could be a reasonable and credible alternate condition per the analyzed events described in FSAR Section 14.1.9, Loss of Normal Feedwater, and FSAR Section 14.1.10, Excessive Heat Removal due to a FW System Malfunction. The plant performed as expected and the event was bounded by the FSAR analysis. Redundant safety SG level instrumentation was available for a low SG level actuation which automatically initiates a RT and AFWS start providing an alternate source of FW.
For this event rod control was in automatic and the reactor scrammed immediately upon a manual reactor trip. RCS pressure remained below the set point for pressurizer PORV or code safety valve operation and above the set point for automatic safety injection actuation.
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05000348/LER-2004-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000333/LER-2004-001 | Inadvertent Actuation of ECCS and EDGs While in Refueling Mode | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000306/LER-2004-001 | | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000315/LER-2004-001 | Failure To Comply With Technical Specification 3 .7 .5 .1, Control Room Emergency Ventilation System | | 05000301/LER-2004-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000313/LER-2004-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000285/LER-2004-001 | Failure To Perform A Leakage Test Due To Lack Of Understanding of Penetration Design | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000271/LER-2004-001 | Main Steam Isolation Valve Leakage Exceeds a Technical Specification Leakage Rate Limit | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000266/LER-2004-001 | | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000318/LER-2004-001 | . Reactor Trip Due to Low Steam Generator Water Level After Feed Pump Trip | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000289/LER-2004-001 | | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000263/LER-2004-001 | | | 05000247/LER-2004-001 | Manual Reactor Trip Due to Oscillating Feedwater Flow and Steam Generator Level with Flow Perturbations Caused by a Degraded Feed Water Regulating Valve | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(iv), System Actuation | 05000244/LER-2004-001 | Gaps in the Control Room Emergency Zone Boundary | | 05000255/LER-2004-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000364/LER-2004-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000461/LER-2004-001 | Clinton Power Station 05000461 1 OF 4 | | 05000414/LER-2004-001 | relPowere Vice President A Duke Energy Company Duke Power Catawba Nuclear Station 4800 Concord Rd. / CNO1VP York, SC 29745-9635 803 831 4251 803 831 3221 fax November 9, 2004
U. S. Nuclear Regulatory Commission
ATTENTION: Document Control Desk
Washington, DC 20555-0001
SUBJECT: Duke Energy Corporation
Catawba Nuclear Station Unit 2
Docket No. 50-414
Licensee Event Report 414/04-001 Revision 0
Reactor Coolant System Pressure Boundary Leakage
Due to Small Cracks Found in Steam Generator
Channel Head Bowl Drain Line on 2C & 2D Steam
Generators
Attached please find Licensee Event Report 414/04-001
Revision 0, entitled "Reactor Coolant System Pressure
Boundary Leakage Due to Small Cracks Found in.Steam
Generator Channel Head Bowl Drain Line on 2C & 2D Steam
Generators."
This Licensee Event Report does not contain any regulatory
commitments. Questions regarding this Licensee Event Report
should be directed to R. D. Hart at (803) 831-3622.
Sincerely,
Dhiaa Jamil
Attachment
www.dukepower.corn 00- U.S. Nuclear Reguldhory Commission
November 9, 2004
Page 2
XC: W.D. Travers
U.S. Nuclear Regulatory Commission
Regional Administrator, Region II
Atlanta Federal Center
61 Forsyth St., SW, Suite 23T85
Atlanta, GA 30303
E.F. Guthrie
Senior Resident Inspector (CNS)
U.S. Nuclear Regulatory Commission
Catawba Nuclear Station
S.E. Peters (addressee only)
NRC Project Manager (CNS)
U.S. Nuclear Regulatory Commission
One White Flint North, Mail Stop 10-B3
11555 Rockville Pike
Rockville, MD 20852-2738
NRC FORM 366� U.S. NUCLEAR REGULATORY APPROVED BY OMB: NO. 3150-0104 EXPIRES: 06/30/2007 (6-2004)� COMMISSION Estimated burden per response to comply with this mandatory collection request 50
hours. Reported lessons learned are Incorporated Into the licensing process and fed back
to Industry. Send comments regarding burden estimate to the Records and FOIA/Privacy
Service Branch (T-5 F52), U.S. Nuclear Regulatory Commission, WashinMon, DC 2055
LICENSEE EN/ENT REPORT (LER) 0001, or by Internet e-mail to infocollects@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104). Office of Management(See reverse for required number of and Budget, Washington, DC 20503. If a means used to impose an Information col ectiond( inverse �for each block) does not display a currently valid OMB control number, the NRC may not conduct or sponsor. and a person Is not required to respond o. the Information collection. 1. FACILITY NAME 2. DOCKET NUMBER 3. PAGE Catawba Nuclear Station, Unit 2 050- 00414 1 OF�6 4. TITLE Reactor Coolant System Pressure Boundary Leakage Due to Small Cracks Found in
Steam Generator Channel Head Bowl Drain Line on 2C & 2D Steam Generators | | 05000368/LER-2004-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000423/LER-2004-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000334/LER-2004-001 | Control Rod Shutdown Bank Anomaly Causes Entry into Technical Specification 3.0.3 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000413/LER-2004-001 | Gas Accumulation in Centrifugal Charging Pump Suction Piping | 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000395/LER-2004-001 | Reactor Trip Due to Valve Failure During Forced Shutdown | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000390/LER-2004-001 | Automatic Reactor Trip Due to a Invalid Turbine Trip Signal (P-4) | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000369/LER-2004-001 | Auxiliary Feedwater System in prohibited condition due to inadequate procedure. | | 05000454/LER-2004-001 | Exelent
Exelon Generation Company, LLCRwww.exeloncorp.com NuclearByron Station 4450 North German Church Road Byron, IL 61010-9794 October 17, 2004 LTR: BYRON 2004-0111 File: 2.01.0700 United States Nuclear Regulatory Commission ATTN: Document Control Desk Washington, DC 20555-0001 Subject:RLicensee Event Report (LER) 454-2004-001-00, "Reactor Containment Fan Coolers Flow Rates Below Technical Specification Requirements Due to Inaccurate Flow Indication" Byron Station, Unit 1
Facility Operating License No. NPF-37
NRC Docket No. STN 50-454
Enclosed is an LER involving the August 17, 2004, event involving low flow conditions discovered in Unit 1 Reactor Containment Fan Coolers for a time period longer than allowed by the Technical Specifications. This event is reportable to the NRC in accordance with 10CFR 50.73 (a)(2)(i)(B), as a condition prohibited by Technical Specifications. Should you have any questions concerning this matter, please contact Mr. William Grundmann, Regulatory Assurance. Manager, at (815) 234-5441, extension 2800. Respectfully, Stephen E. Kuczynski Site Vice President Byron Nuclear Generating Station Attachment LER 454-2004-001-00 cc:RRegional Administrator, Region III, NRC NRC Senior Resident Inspector— Byron Station NRC FORM 366 U.S. NUCLEAR REGULATORY APPROVED BY OMB NO. 3150-0104 EXPIRES 7-31-2004 (7.2001) COMMISSION Estimated burden per response to comply with this mandatory information collection request 50 hours. Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the Records Management Branch (T.6 E6), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by Internet e-mail toLICENSEE EVENT REPORT (LER) *I@ nrc.gov, and to the Desk Officer, Office of Informabon and Regulatory Affairs, NEOB:10202 (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose information collection does not display a currently valid OMB control number, the NRC may not _ conduct or sponsor, and a person is not required to respond to, the information collection. 1 rand ITV NAUP o natuerr An warn q par= . Byron Station, Unit 1 0500454 1 OF 5 4. Reactor Containment Fan Coolers Flow Rates Below Technical Specifications Requirements Due to Inaccurate Flow Indication | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000305/LER-2004-001 | | 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | 05000336/LER-2004-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000364/LER-2004-002 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000423/LER-2004-002 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000237/LER-2004-002 | Dresden Nuclear Power Station Unit 2 05000237 1 of 5 | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000261/LER-2004-002 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000244/LER-2004-002 | Consolidated Rod Storage Canister Placed in Incorrect Storage Location | | 05000530/LER-2004-002 | Main Turbine Control System Malfunction Results in Automatic Reactor Trip on Low DNBR | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000305/LER-2004-002 | | | 05000247/LER-2004-002 | Manual Reactor Trip Due to Decreasing 23 Steam Generator Level Caused by Feedwater Regulating Valve Closure Due to a De-energized Solenoid Operated Valve from Wiring Failure | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000414/LER-2004-002 | Manual Reactor Trip Initiated Due to Control Rods from Shutdown Bank D Dropping into the Core | | 05000251/LER-2004-002 | AAA | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(iv)(b) | 05000397/LER-2004-002 | | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000346/LER-2004-002 | Reactor Trip During Reactor Trip Breaker Testing Due To Fuse Failure | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000395/LER-2004-002 | Emergency Diesel Generator Start and Load Due to Momentary Fault on Incoming Feed | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000269/LER-2004-002 | eif Powere RON A. JONES Vice President A Duke Energy Company Oconee Nuclear Site Duke Power ONO1VP / 7800 Rochester Highway Seneca, SC 29672 864 885 3158 864 885 3564 fax September 9, 2004
U.S. Nuclear Regulatory Commission
Document Control Desk
Washington, D.C. 20555
Subject: Oconee Nuclear Station
Docket Nos. 50-269,-270, -287
Licensee Event Report 269/2004-02, Revision 1
Problem Investigation Process No.: 0-04-2808
Gentlemen:
Pursuant to 10 CFR 50.73 Sections (a)(1) and (d), attached
is Licensee Event Report 269/2004-02, Revision 1, regarding
a Main Steam Line Break mitigation design/analysis
deficiency which could result in the main and startup
feedwater control valves being technically inoperable for
mitigation of some steam line break scenarios.
This report is being submitted to supplement Revision 0
submitted July 6, 2004. At that time the root cause
investigation and an analysis of the consequences of
potentially exceeding the Environment Qualification (EQ)
envelope curve were still in progress.
This event is being reported in accordance with 10 CFR
50.73 (a)(2)(i)(B) as a condition prohibited by Technical
Specifications, 50.73(a)(2)(ii)(B) as an Unanalyzed
Condition, and 50.73(a)(2)(V)(D) as a potential loss of
safety function for Accident Mitigation. This event is
considered to be of no significance with respect to the
health and safety of the public.
www.dukepower.corn Document Control Desk
Date: September 9, 2004
Page 2
Attachment: Licensee Event Report 269/2004-02, Revision 1
cc: Mr. William D. Travers
Administrator, Region II
U.S. Nuclear Regulatory Commission
61 Forsyth Street, S. W., Suite 23T85
Atlanta, GA 30303
Mr. L. N. Olshan
Project Manager
U.S. Nuclear Regulatory Commission
Office of Nuclear Reactor Regulation
Washington, D.C. 20555
Mr. M. C. Shannon
NRC Senior Resident Inspector
Oconee Nuclear Station
INPO (via E-mail)
NRC FORM 366 U.S. NUCLEAR REGULATORY APPROVED BY OMB NO. 3150-0104 EXPIRES 7-31-2004 (7-2001) COMMISSION Estimated burden per response to comply with this mandatory information collection request: 50 hours. Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the Records Management Branch (T-6 E6), U.S. Nuclear Regulatory Commission, Washington. DCLICENSEE EVENT REPORT (LER) 20555-0001, or by Internet e-mail to bpi @nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202 (3150-0104), Office of Management and(See reverse for required number of Budget, Washington, DC 20503. If a means used to impose information collection doesdigits/characters for each block) not display a currently valid OMB control number, the NRC may not conduct or sponsor, and,1 nnmnn lc not rent Owl to tocnnni-I to the intnrmatinn rntlentinn 1. FACILITY NAME 2. DOCKET NUMBER 3. PAGE Oconee Nuclear Station, Unit 1 050-81 OF 0269 11 4. TITLE Main Steam Line Break Mitigation Design/Analysis Deficiency | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | 05000313/LER-2004-002 | | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000271/LER-2004-002 | Special Nuclear Material Inventory Location Discrepancy | | 05000285/LER-2004-002 | Inoperable Diesel Generator for 28 Days Due to Blown Fuse During Shutdown | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000336/LER-2004-002 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000311/LER-2004-002 | Failure To Comply With Technical Specifications During Reactor Protection Instrument Calibration . | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000254/LER-2004-002 | Quad Cities Nuclear Power Station Unit 1 05000254 1 of 4 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000263/LER-2004-002 | | | 05000302/LER-2004-002 | Emergency Diesel Generator Inoperable Due To Fuel Oil Header Outlet Check Valve Leaking Past Seat | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
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