ML19211C915

From kanterella
Revision as of 13:00, 19 October 2019 by StriderTol (talk | contribs) (Created page by program invented by StriderTol)
Jump to navigation Jump to search
Revised Operational Summary to Monthly Operating Rept for Nov 1979
ML19211C915
Person / Time
Site: Davis Besse Cleveland Electric icon.png
Issue date: 01/08/1980
From:
TOLEDO EDISON CO.
To:
Shared Package
ML19211C914 List:
References
NUDOCS 8001150473
Download: ML19211C915 (2)


Text

OPERATIONAL

SUMMARY

NOVEMBER, 1979

.The unit shutdown which was initiated on October 25, 1979, when Reactor Coolant Pump (RCP) 2-2 tripped L am a blown fut i, continued until 1811 hours0.021 days <br />0.503 hours <br />0.00299 weeks <br />6.890855e-4 months <br /> on November 20, 1979, when the turbine-generator was synchronized. Below is a list of the major work items performed during the outage:

1. All four RCP seals were replaced.
2. A new expansion joint for 1-4-2 heater extraction was rewelded.
3. A design change to the Couch relays in the RCP starting interlock circuits was made. This initiated a similar change .in sixteen safety related cir-cuits.
4. NI-3 was pulled and a new detector was installed. A new section of cable between the containment penetration and the NI-1 pre-amp was installed.

1

5. Several pipe restraints were modified as a result of IE Bulletin 79-14 findings.

11/20/79 - 11/21/79 The unit returned on line at 1811 hours0.021 days <br />0.503 hours <br />0.00299 weeks <br />6.890855e-4 months <br /> on November 20, 1979, and reactor power was increased to 81% of full power with generator gross load at 760 MWe on November 21, 1979.

11/22/79 Reactor Coolant System (RCS) flow inidcation was determined to be less than required by Technical Specification 3.2.5 at 0300 hours0.00347 days <br />0.0833 hours <br />4.960317e-4 weeks <br />1.1415e-4 months <br />. Reactor power was decreased to 73% at which point RCS flow indication was back within allowable limits. At 0400 hours0.00463 days <br />0.111 hours <br />6.613757e-4 weeks <br />1.522e-4 months <br /> generator gross load was 684 MPe.

11/23/79 - 11/25/79 Reactor power was maintained lat approximately 73% until 0620 hours0.00718 days <br />0.172 hours <br />0.00103 weeks <br />2.3591e-4 months <br /> on November 25, 1979, when RCS flow indication was again determined to be less than that required by Tec'..nical Specifi-cations. Reactor power was decreased to 67% at which point the RCS flow indication was again back within tolerance. The cause of the low flow indication is still being investigated.

11/26/79 Reactor power was maintained at approximately 69% of full power. At 2145 hours0.0248 days <br />0.596 hours <br />0.00355 weeks <br />8.161725e-4 months <br /> on November 26, 1979, RCP 1-2 was manu-ally tripped due to a lower motor bearing low oil level alarm.

11/27/79 - 11/28/79_ The unit remained at approximately 68% of full power with generator gross load of 635 MWe until 0645 hours0.00747 days <br />0.179 hours <br />0.00107 weeks <br />2.454225e-4 months <br /> on November 28, 1979, when it was determined that the power range nuclear instrumentation (NIs) were reading slightly greater than 2%

below the calculated heat balance. Reactor power was reduced to 50% to bring the in tolerance and to run another heat balance to get the n - in tolerance.

1/65 17i 8001150Yh

.

.

OPERATIONAL SUFNARY NOVElBER, 1979 PAGE 2 0F 2 1 11/20/79 Group 7, Rod 5 was declared inoperable at 0640 hour0.00741 days <br />0.178 hours <br />0.00106 weeks <br />2.4352e-4 months <br />s-initiat-ing a reduction in reactor power to approximately 42% and reset-ting the high flux trip setpoint to 54%.

11/30/79 Reactor power was reduced and the turbine-generator taken off line at 1910 hours0.0221 days <br />0.531 hours <br />0.00316 weeks <br />7.26755e-4 months <br /> to investigate the lower motor bearing oil level alarm on RCP l-2; to fix Group 7, Rod 5 and Group 5, Rod 11 API.

.

1765 172