IR 05000311/1979019

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Updated LER 79-054/01X-1:on 790824,three Snubbers on Main Feedwater 14 During Refueling Outage Per Followup to NRC Insp Rept 50-311/79-19.Caused by Extreme Shock Load.Snubbers Replaced
ML18081A672
Person / Time
Site: Salem PSEG icon.png
Issue date: 11/10/1979
From: KAPPLE A W
Public Service Enterprise Group
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML18081A671 List:
References
LER-79-054-01X, LER-79-54-1X, NUDOCS 7912040395
Download: ML18081A672 (1)


Text


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REPORT -p'Ot:A.us REPORT DATE 9 /7 /7 9 17-771 LICENSEE EVENT REPORT .NUCLEAR REGULATURY COMMISSION CONTROL BLOCK: I 1 I 11(!) 6 (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) (ITl] I N !J I s I G I s I 1 IG)l o I. o I -1 o I o I o I o I o I -I o I o 101 4 I 1 I l I 1 I l 101 I I G) 7 8 9 L.ICENSEE COOE 1-4 15 L.ICENSE NUMBER 25 26 L.ICENSE TYPE ;JO 57 CAT SS CON'T lIIT1 7 8 LlJG) 1 * o I *s I *o I o I *o I 2 I 7 I 2 GI o 1 *s I 2 I 4 1 7 l 9 I© I 1 11 tL *I o I 1 I 9 10 60 61 DOCKET NUMBER 68 69 EVENT CATE 74 75 REPORT CATE 80 EVENT. OESCRIPT10N ANO PROBABLE CONSEOUENCes@)

!During the refueling outage, as follow-up to NRC Inspection 50-311/79-19, three (]l!J tsnubbers on No. 14 Main Feedwater were found to have failed. These_ snubbers were [Q:rrl f included in the stress calculations for the seismic safety analysis of the nuclear []]!] !Portion of the main feed water piping. Stress calculations indicated the increase I. []Jr) lin stress in the piping is small and remains well below the allowable stress rIIZJ llimit. Seismic stresses would not be affected as the snubbers would be locked (]]]J !under that condition. 7 8 9 @El *7 8 SYSTEM CAUSE CAUSE COMP. cooE CODE suBCODE COMPONENT CODE suscooE lclRI@ lslulPIOIRITI@)

L.QJ@) 9 10 '1 12 13 18 19 -. SEQUENTIAL OCCURRENCE REPORT REPORT NO. . CODE TYPE VALVE SUBCOOE 20 /;':;\ L.ER!RO LVENTYEAR

\:.:.J REPORT I 7 I 9 I NUMBER 21 22 I I Io ls 14 I 1......-1 Io I 1 I W bl 23 24 26 27 28 29 30 31 REVISION NC. UJ 32 ., 80 ACTION FUTURE EFFECT SHUTDOWN t.;::;\ ATTACHMENT NPRD--4 PRIME COMP. TAKEN . ACTION. ON PL.ANT METHOD HOURS SUBMITTED FORM :;us. SUPPLIER COMPONENT MANUFACTURER 1£.J@l.K.J@

Li.JC,§) W Io I o Io I o I l..XJ@ ll!J@) 33 34 . 35 36 37 "40 "41 . "42 "43 IP 10 I 219 I@ CAUSE DESCRIPTION ANO CORRECTIVE ACTIONS @ 44 47 jThe failure of the snubbers appears to be an extreme shock load or occurred when o::DJ tthe snubber was in the fully retracted conditio The snubbers were replaced in kindj o::IiJ I and corresponding snubbers on 11, 12 and 13. lines were checked satisfactory

  • . OJI) I I.nstrumentation will be installed to measure and record acceleration and linear [!I!J !displacement of the piping at the snubber location. 7 8 9 FACILITY IJQ\ METHOD OF (.;;\ STATUS. 1' POWER OŽER STATU.S \;;:::/ DISCOVERY DISCOVERY DE$Cl'lll"fl0N ITlIJ L£J@) I 0 I O! 0 l@I N/A I 1..£.J@I Follow-Up to NRC Inspection 8 9 ' 10 12 1'3 "" 45 46 ACTIVITY CONT£NT * . RELEASED OF RELEASE AMOUNT OF ACTIVITY . OJI] l.!J@ l!J@I N/A I 1 a s 10 11 7 LOCATION OF REL.EASE @ * N/A BO BO 80 PERSONNEL EXPOSURES t::::-.. NUMBER ITIIJ J o I o I o

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___, 7 B 9 11 12 13 PERSONNE INJURIES I'.:':\ NUMBER ITTIJ lololol@)..._

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___________________________ 7 8 SI t t 12 L.OSS OF OR DAMAGE TO FACILITY 1.i3' TYPE DESCRIPTION

\::;::I ITTIJ LIJ@) . N A 7 s 9 BO BO PUBLICITY C\ E ISSUEOC,;'\

NRC US ONL y filEJ

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__, I I I 11 I I I I I I I I 7 8 SI 10 68 69 80 NAMEOFPREPARER

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