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{{#Wiki_filter:UNITED STATES
{{#Wiki_filter:UNITED STATES  
                            NUCLEAR REGULATORY COMMISSION
NUCLEAR REGULATORY COMMISSION  
                                              REGION III
REGION III  
                                2443 WARRENVILLE ROAD, SUITE 210
2443 WARRENVILLE ROAD, SUITE 210  
                                        LISLE, IL 60532-4352
LISLE, IL 60532-4352  
                                            August 3, 2012
Mr. Larry Meyer
Site Vice President
August 3, 2012  
NextEra Energy Point Beach, LLC
6610 Nuclear Road
Two Rivers, WI 54241
SUBJECT:       POINT BEACH NUCLEAR PLANT, UNITS 1 AND 2
Mr. Larry Meyer  
                NRC INTEGRATED INSPECTION REPORT 05000266/2012003 AND
Site Vice President  
                05000301/2012003
NextEra Energy Point Beach, LLC  
Dear Mr. Meyer:
6610 Nuclear Road  
On June 30, 2012, the U.S. Nuclear Regulatory Commission (NRC) completed an integrated
Two Rivers, WI 54241  
inspection at your Point Beach Nuclear Plant, Units 1 and 2. The enclosed report documents
SUBJECT:  
the inspection findings, which were discussed on June 26, 2012, with you and members of your
POINT BEACH NUCLEAR PLANT, UNITS 1 AND 2  
staff.
The inspection examined activities conducted under your license as they relate to safety and
NRC INTEGRATED INSPECTION REPORT 05000266/2012003 AND  
compliance with the Commissions rules and regulations and with the conditions of your license.
05000301/2012003  
The inspectors reviewed selected procedures and records, observed activities, and interviewed
Dear Mr. Meyer:
personnel.
On June 30, 2012, the U.S. Nuclear Regulatory Commission (NRC) completed an integrated  
Two NRC-identified findings and one self-revealing finding of very low safety significance were
inspection at your Point Beach Nuclear Plant, Units 1 and 2. The enclosed report documents  
identified during this inspection.
the inspection findings, which were discussed on June 26, 2012, with you and members of your  
These findings were determined to involve violations of NRC requirements. The NRC is treating
staff.  
these violations as non-cited violations (NCVs), consistent with Section 2.3.2 of the
The inspection examined activities conducted under your license as they relate to safety and  
Enforcement Policy.
compliance with the Commissions rules and regulations and with the conditions of your license.
If you contest the subject or severity of these NCVs, you should provide a response within
The inspectors reviewed selected procedures and records, observed activities, and interviewed  
30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear
personnel.  
Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with a
Two NRC-identified findings and one self-revealing finding of very low safety significance were  
copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III,
identified during this inspection.  
2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement,
These findings were determined to involve violations of NRC requirements. The NRC is treating  
U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector
these violations as non-cited violations (NCVs), consistent with Section 2.3.2 of the  
Office at the Point Beach Nuclear Plant. In addition, if you disagree with the cross-cutting
Enforcement Policy.  
aspect assigned to any finding in this report, you should provide a response within 30 days of
If you contest the subject or severity of these NCVs, you should provide a response within  
the date of this inspection report, with the basis for your disagreement, to the Regional
30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear  
Administrator, Region III, and the NRC Resident Inspector at the Point Beach Nuclear Plant.
Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with a  
copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III,  
2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement,  
U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector  
Office at the Point Beach Nuclear Plant. In addition, if you disagree with the cross-cutting  
aspect assigned to any finding in this report, you should provide a response within 30 days of  
the date of this inspection report, with the basis for your disagreement, to the Regional  
Administrator, Region III, and the NRC Resident Inspector at the Point Beach Nuclear Plant.  


L. Meyer                                     -2-
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its
enclosure, and your response (if any) will be available electronically for public inspection in the
L. Meyer  
NRC Public Document Room or from the Publicly Available Records System (PARS)
-2-  
component of NRC's Agencywide Document Access and Management System (ADAMS).
ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html
(the Public Electronic Reading Room).
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its  
                                            Sincerely,
enclosure, and your response (if any) will be available electronically for public inspection in the  
                                            /RA/
NRC Public Document Room or from the Publicly Available Records System (PARS)  
                                            Michael A. Kunowski, Branch Chief
component of NRC's Agencywide Document Access and Management System (ADAMS).
                                            Branch 5
ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html
                                            Division of Reactor Projects
(the Public Electronic Reading Room).  
Docket Nos.: 05000266; 05000301
Sincerely,  
License Nos.: DPR-24; DPR-27
Enclosure: Inspection Report 05000266/2012003 and 05000301/2012003;
/RA/  
                w/Attachment: Supplemental Information
cc w/encl:     Distribution via ListServ
Michael A. Kunowski, Branch Chief  
Branch 5  
Division of Reactor Projects  
Docket Nos.: 05000266; 05000301  
License Nos.: DPR-24; DPR-27  
Enclosure: Inspection Report 05000266/2012003 and 05000301/2012003;  
  w/Attachment: Supplemental Information  
cc w/encl:  
Distribution via ListServ  


          U.S. NUCLEAR REGULATORY COMMISSION
                          REGION III
Enclosure
Docket Nos.:       05000266; 05000301
U.S. NUCLEAR REGULATORY COMMISSION  
License Nos.:       DPR-24; DPR-27
REGION III  
Report No.:         05000266/2012003; 05000301/2012003
Docket Nos.:  
Licensee:           NextEra Energy Point Beach, LLC
05000266; 05000301  
Facility:           Point Beach Nuclear Plant, Units 1 and 2
License Nos.:  
Location:           Two Rivers, WI
DPR-24; DPR-27  
Dates:             April 1, 2012, through June 30, 2012
Report No.:  
Inspectors:         S. Burton, Senior Resident Inspector
05000266/2012003; 05000301/2012003  
                    M. Thorpe-Kavanaugh, Resident Inspector
Licensee:  
                    R. Krsek, Senior Resident Inspector (Kewaunee)
NextEra Energy Point Beach, LLC  
                    M. Phalen, Senior Health Physicist
Facility:  
                    V. Myers, Health Physicist
Point Beach Nuclear Plant, Units 1 and 2  
                    T. Bilik, Senior Reactor Engineer
Location:  
                    V. Meghani, Reactor Inspector
Two Rivers, WI  
                    A. Dahbur, Senior Reactor Engineer
Dates:  
                    M. Learn, Reactor Engineer
April 1, 2012, through June 30, 2012  
                    J. Bozga, Reactor Engineer
Inspectors:  
                    C. Zoia, Operations Engineer
S. Burton, Senior Resident Inspector
Approved by:       Michael A. Kunowski, Branch Chief
                    Branch 5
M. Thorpe-Kavanaugh, Resident Inspector  
                    Division of Reactor Projects
                                                                  Enclosure
R. Krsek, Senior Resident Inspector (Kewaunee)  
M. Phalen, Senior Health Physicist  
V. Myers, Health Physicist  
T. Bilik, Senior Reactor Engineer  
V. Meghani, Reactor Inspector  
A. Dahbur, Senior Reactor Engineer  
M. Learn, Reactor Engineer  
J. Bozga, Reactor Engineer  
C. Zoia, Operations Engineer  
Approved by:  
Michael A. Kunowski, Branch Chief  
Branch 5  
Division of Reactor Projects  


                                        TABLE OF CONTENTS
SUMMARY OF FINDINGS ......................................................................................................... 1
Enclosure
REPORT DETAILS .................................................................................................................... 4
TABLE OF CONTENTS  
  Summary of Plant Status ........................................................................................................ 4
SUMMARY OF FINDINGS ......................................................................................................... 1  
  1.   REACTOR SAFETY .................................................................................................... 4
      1R01     Adverse Weather Protection (71111.01) ............................................................ 4
REPORT DETAILS .................................................................................................................... 4  
      1R04     Equipment Alignment (71111.04) ...................................................................... 6
   
      1R05     Fire Protection (71111.05) ................................................................................. 7
Summary of Plant Status ........................................................................................................ 4  
      1R06     Flooding (71111.06) .......................................................................................... 7
      1R11     Licensed Operator Requalification Program (71111.11) .................................... 8
1.  
      1R12     Maintenance Effectiveness (71111.12) .............................................................. 9
REACTOR SAFETY .................................................................................................... 4  
      1R13     Maintenance Risk Assessments and Emergent Work Control (71111.13) ........10
1R01  
      1R15     Operability Determinations and Functional Assessments (71111.15) ...............11
Adverse Weather Protection (71111.01) ............................................................ 4  
      1R18     Plant Modifications (71111.18) .........................................................................11
1R04  
      1R19     Post-Maintenance Testing (71111.19) ..............................................................12
Equipment Alignment (71111.04) ...................................................................... 6  
      1R20     Outage Activities (71111.20) ............................................................................15
1R05  
      1R22     Surveillance Testing (71111.22) .......................................................................15
Fire Protection (71111.05) ................................................................................. 7  
      1EP6 Drill Evaluation (71114.06) ...............................................................................16
1R06  
  2.   RADIATION SAFETY .................................................................................................17
Flooding (71111.06) .......................................................................................... 7  
      2RS3 In-Plant Airborne Radioactivity Control and Mitigation (71124.03) ....................17
1R11  
  4.   OTHER ACTIVITIES ...................................................................................................19
Licensed Operator Requalification Program (71111.11) .................................... 8  
      4OA1 Performance Indicator Verification (71151) .......................................................19
1R12  
      4OA2 Identification and Resolution of Problems (71152) ............................................22
Maintenance Effectiveness (71111.12) .............................................................. 9  
      4OA3 Follow-Up of Events and Notices of Enforcement Discretion (71153) ...............25
1R13
      4OA5 Other Activities .................................................................................................28
Maintenance Risk Assessments and Emergent Work Control (71111.13) ........10  
      4OA6 Management Meetings .....................................................................................29
1R15  
      4OA7 Licensee-Identified Violations ...........................................................................29
Operability Determinations and Functional Assessments (71111.15) ...............11  
SUPPLEMENTAL INFORMATION............................................................................................. 1
1R18  
  Key Points of Contact ............................................................................................................. 1
Plant Modifications (71111.18) .........................................................................11  
  List of Items Opened, Closed and Discussed ......................................................................... 2
1R19  
  List of Documents Reviewed .................................................................................................. 3
Post-Maintenance Testing (71111.19) ..............................................................12  
  List of Acronyms Used...........................................................................................................15
1R20  
                                                                                                                      Enclosure
Outage Activities (71111.20) ............................................................................15  
1R22  
Surveillance Testing (71111.22) .......................................................................15  
1EP6  
Drill Evaluation (71114.06) ...............................................................................16  
2.  
RADIATION SAFETY .................................................................................................17  
2RS3  
In-Plant Airborne Radioactivity Control and Mitigation (71124.03) ....................17  
4.  
OTHER ACTIVITIES ...................................................................................................19  
4OA1  
Performance Indicator Verification (71151) .......................................................19  
4OA2  
Identification and Resolution of Problems (71152) ............................................22  
4OA3
Follow-Up of Events and Notices of Enforcement Discretion (71153) ...............25  
4OA5  
Other Activities .................................................................................................28  
4OA6
Management Meetings .....................................................................................29  
4OA7  
Licensee-Identified Violations ...........................................................................29  
SUPPLEMENTAL INFORMATION ............................................................................................. 1  
   
Key Points of Contact ............................................................................................................. 1  
   
List of Items Opened, Closed and Discussed ......................................................................... 2  
   
List of Documents Reviewed .................................................................................................. 3  
   
List of Acronyms Used ...........................................................................................................15  


                                        SUMMARY OF FINDINGS
IR 05000266/2012003, 05000301/2012003; 04/01/2012 - 06/30/2012; Point Beach Nuclear
1
Plant, Units 1 and 2; Post-Maintenance Testing; In-Plant Airborne Radioactivity Control and
Enclosure
Mitigation; and Follow-Up of Events and Notices of Enforcement Discretion.
SUMMARY OF FINDINGS  
This report covers a 3-month period of inspection by resident inspectors and announced
IR 05000266/2012003, 05000301/2012003; 04/01/2012 - 06/30/2012; Point Beach Nuclear  
baseline inspections by regional inspectors. Two Green NRC-identified findings and one Green
Plant, Units 1 and 2; Post-Maintenance Testing; In-Plant Airborne Radioactivity Control and  
self-revealing finding were identified during this inspection. The findings were considered
Mitigation; and Follow-Up of Events and Notices of Enforcement Discretion.  
non-cited violations (NCVs) of NRC regulations. The significance of most findings is indicated
This report covers a 3-month period of inspection by resident inspectors and announced  
by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609,
baseline inspections by regional inspectors. Two Green NRC-identified findings and one Green  
Significance Determination Process (SDP). Findings for which the SDP does not apply may
self-revealing finding were identified during this inspection. The findings were considered  
be Green or be assigned a severity level after NRC management review. The NRCs program
non-cited violations (NCVs) of NRC regulations. The significance of most findings is indicated  
for overseeing the safe operation of commercial nuclear power reactors is described in
by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609,  
NUREG-1649, Reactor Oversight Process, Revision 4, dated December 2006.
Significance Determination Process (SDP). Findings for which the SDP does not apply may  
A.     NRC-Identified and Self-Revealed Findings
be Green or be assigned a severity level after NRC management review. The NRCs program  
        Cornerstone: Initiating Events
for overseeing the safe operation of commercial nuclear power reactors is described in
    *  Green. A finding of very low safety significance and associated non-cited violation of
NUREG-1649, Reactor Oversight Process, Revision 4, dated December 2006.  
        10 CFR 50.65(a)(3) was self-revealed when an unplanned reactor trip of Unit 2 occurred
A.  
        on June 13, 2011, as a result of the failure of a source range detector during low power
Cornerstone:  Initiating Events
        physics testing. Specifically, the licensee failed to adequately evaluate operating
NRC-Identified and Self-Revealed Findings  
        experience and incorporate it into its preventive maintenance program to periodically
*
        replace aging electrical subcomponents in nuclear instrumentation systems and a
Green
        subsequent age-related failure resulted in initiating a plant transient. The licensee
        entered this issue into the corrective action program, and corrective actions to prevent
The finding was determined to be more than minor in accordance with Inspection  
        recurrence were initiated.
Manual Chapter 0612, Power Reactor Inspection Reports, Appendix B, Issue  
        The finding was determined to be more than minor in accordance with Inspection
Screening, dated December 24, 2009, because the finding was associated with the  
        Manual Chapter 0612, Power Reactor Inspection Reports, Appendix B, Issue
Initiating Events Cornerstone attribute of equipment performance. Specifically, the  
        Screening, dated December 24, 2009, because the finding was associated with the
availability and reliability of the nuclear instruments was degraded to a point where an  
        Initiating Events Cornerstone attribute of equipment performance. Specifically, the
instrument failure caused a reactor trip, an event that adversely impacted the  
        availability and reliability of the nuclear instruments was degraded to a point where an
cornerstone objective to limit the likelihood of those events that upset plant stability and  
        instrument failure caused a reactor trip, an event that adversely impacted the
challenge critical safety functions during power operations. The finding has a  
        cornerstone objective to limit the likelihood of those events that upset plant stability and
cross-cutting aspect in the area of corrective action program, evaluation/extent of  
        challenge critical safety functions during power operations. The finding has a
condition. Specifically, the licensee failed to thoroughly evaluate related nuclear  
        cross-cutting aspect in the area of corrective action program, evaluation/extent of
instrument failure rates so that the resolutions addressed the causes and extent of  
        condition. Specifically, the licensee failed to thoroughly evaluate related nuclear
conditions for age-related failures of electrical subcomponents (P.1(c)).
        instrument failure rates so that the resolutions addressed the causes and extent of
(Section 4OA3.4)  
        conditions for age-related failures of electrical subcomponents (P.1(c)).
.  A finding of very low safety significance and associated non-cited violation of
        (Section 4OA3.4)
10 CFR 50.65(a)(3) was self-revealed when an unplanned reactor trip of Unit 2 occurred
        Cornerstone: Mitigating Systems
on June 13, 2011, as a result of the failure of a source range detector during low power
    *   Green. The inspectors identified a finding of very low safety significance and associated
physics testing.  Specifically, the licensee failed to adequately evaluate operating
        non-cited violation of 10 CFR Part 50, Appendix B, Criterion XI, "Test Control," because
experience and incorporate it into its preventive maintenance program to periodically
        the licensee failed to establish routine testing procedure that demonstrated room
replace aging electrical subcomponents in nuclear instrumentation systems and a
        temperatures would be maintained. Specifically, on March 29, 2012, the inspectors
subsequent age-related failure resulted in initiating a plant transient.  The licensee
        identified that the licensee failed to establish routine testing procedure that demonstrated
entered this issue into the corrective action program, and corrective actions to prevent
                                                    1                                      Enclosure
recurrence were initiated.
Cornerstone: Mitigating Systems  
*  
Green. The inspectors identified a finding of very low safety significance and associated  
non-cited violation of 10 CFR Part 50, Appendix B, Criterion XI, "Test Control," because  
the licensee failed to establish routine testing procedure that demonstrated room  
temperatures would be maintained. Specifically, on March 29, 2012, the inspectors  
identified that the licensee failed to establish routine testing procedure that demonstrated  


  the air flows for emergency diesel generators G-01 and G-02 ventilation systems would
  perform adequately to ensure that the room temperatures would be maintained. The
2
  licensee entered this issue into its corrective action program, and corrective actions
Enclosure
  included performance of air flow measurements on the fan units, creation of a preventive
the air flows for emergency diesel generators G-01 and G-02 ventilation systems would  
  maintenance requirement for taking periodic flow measurements, and assessment of the
perform adequately to ensure that the room temperatures would be maintained. The  
  identified issue through a condition evaluation.
licensee entered this issue into its corrective action program, and corrective actions  
  The finding was determined to be more than minor in accordance with Inspection
included performance of air flow measurements on the fan units, creation of a preventive  
  Manual Chapter 0612, Appendix B, Issue Screening, dated December 24, 2009. The
maintenance requirement for taking periodic flow measurements, and assessment of the  
  inspectors determined that this finding was more than minor because it was associated
identified issue through a condition evaluation.  
  with the Mitigating Systems Cornerstone attribute for design control. Specifically, it
The finding was determined to be more than minor in accordance with Inspection  
  adversely affected the Mitigating System Cornerstone objective to ensure the reliability
Manual Chapter 0612, Appendix B, Issue Screening, dated December 24, 2009. The  
  of systems that respond to initiating events to prevent undesirable consequences. This
inspectors determined that this finding was more than minor because it was associated  
  finding has a cross-cutting aspect in the area of human performance, decision-making.
with the Mitigating Systems Cornerstone attribute for design control. Specifically, it  
  Specifically, the licensee did not use conservative assumptions regarding the verification
adversely affected the Mitigating System Cornerstone objective to ensure the reliability  
  of the proper air flow through the safety-related gravity dampers in the emergency diesel
of systems that respond to initiating events to prevent undesirable consequences. This  
  generators G-01 and G-02 rooms (H.1(b)). (Section 1R19)
finding has a cross-cutting aspect in the area of human performance, decision-making.
  Cornerstone: Occupational Radiation Safety
Specifically, the licensee did not use conservative assumptions regarding the verification  
* Green. The inspectors identified a finding of very low safety significance and associated
of the proper air flow through the safety-related gravity dampers in the emergency diesel  
  non-cited violation of 10 CFR 20.1701. Specifically, the inspectors identified
generators G-01 and G-02 rooms (H.1(b)). (Section 1R19)
  deficiencies, as of January 19, 2012, in the licensees testing program for assuring that
Cornerstone: Occupational Radiation Safety  
  the technical support center (TSC) ventilation system was in compliance with the
*  
  systems design basis. The licensees TSC high efficiency particulate air and charcoal
Green
  filter efficiencies were not tested to the design criteria. The licensee documented this
The finding was more than minor because it was associated with the program and  
  issue in its corrective action program and the corrective actions included revising
process attribute of exposure control of the Occupational Radiation Safety Cornerstone  
  applicable procedures. In addition, the licensee performed a calculation to show
and adversely affected the cornerstone objective of ensuring the adequate protection of  
  that the TSC ventilation system was capable of maintaining a radiological habitability of
worker health and safety from exposure radiation and radioactive material. Specifically,  
  less than 5 Rem total effective dose equivalent for the duration of the design base
inappropriately testing installed emergency ventilation system filters designed to  
  accidents. The calculation was based on actual historical filter testing efficiencies.
mitigate workers radiation exposures did not validate that the TSC ventilation system  
  The finding was more than minor because it was associated with the program and
was capable of performing its intended design function of minimizing worker exposures  
  process attribute of exposure control of the Occupational Radiation Safety Cornerstone
to airborne radioactive materials. The finding was assessed using the occupational  
  and adversely affected the cornerstone objective of ensuring the adequate protection of
radiation safety significance determination process and was determined to be of very  
  worker health and safety from exposure radiation and radioactive material. Specifically,
low safety significance (Green) because it was not an as-low-as-is-reasonable-
  inappropriately testing installed emergency ventilation system filters designed to
achievable planning issue, there was no overexposure or potential for overexposure,  
  mitigate workers radiation exposures did not validate that the TSC ventilation system
and the licensees ability to assess dose was not compromised. The inspectors  
  was capable of performing its intended design function of minimizing worker exposures
determined that the most significant contributor to the finding was a cross-cutting aspect  
  to airborne radioactive materials. The finding was assessed using the occupational
in the area of human performance, resources. Specifically, the licensee failed to ensure  
  radiation safety significance determination process and was determined to be of very
that the TSC ventilation filter testing protocol assured compliance to the systems  
  low safety significance (Green) because it was not an as-low-as-is-reasonable-
designed margins (H.2(a)). (Section 2RS3)  
  achievable planning issue, there was no overexposure or potential for overexposure,
.  The inspectors identified a finding of very low safety significance and associated
  and the licensees ability to assess dose was not compromised. The inspectors
non-cited violation of 10 CFR 20.1701.  Specifically, the inspectors identified
  determined that the most significant contributor to the finding was a cross-cutting aspect
deficiencies, as of January 19, 2012, in the licensees testing program for assuring that
  in the area of human performance, resources. Specifically, the licensee failed to ensure
the technical support center (TSC) ventilation system was in compliance with the
  that the TSC ventilation filter testing protocol assured compliance to the systems
systems design basis.  The licensees TSC high efficiency particulate air and charcoal
  designed margins (H.2(a)). (Section 2RS3)
filter efficiencies were not tested to the design criteria.  The licensee documented this
                                            2                                      Enclosure
issue in its corrective action program and the corrective actions included revising
applicable procedures.  In addition, the licensee performed a calculation to show 
that the TSC ventilation system was capable of maintaining a radiological habitability of
less than 5 Rem total effective dose equivalent for the duration of the design base
accidents.  The calculation was based on actual historical filter testing efficiencies.


B. Licensee-Identified Violations
  No violations were identified.
3
                                  3 Enclosure
Enclosure
B.  
No violations were identified.  
Licensee-Identified Violations


                                          REPORT DETAILS
Summary of Plant Status
4
Unit 1 was at 100 percent power throughout the entire inspection period with the exception of
Enclosure
brief downpowers to conduct planned maintenance and surveillance activities.
REPORT DETAILS  
Unit 2 was at 100 percent power for the majority of the period with the exception of two planned
Unit 1 was at 100 percent power throughout the entire inspection period with the exception of  
downpowers and one forced outage. Unit 2 was downpowered on April 20, 2012, to
brief downpowers to conduct planned maintenance and surveillance activities.  
approximately 15 percent power for switchyard work and on June 18, 2012, for routine auxiliary
Summary of Plant Status
feedwater system testing. On June 27, 2012, the unit was tripped due to a turbine control
system malfunction and remained shut down until the end of the inspection period.
Unit 2 was at 100 percent power for the majority of the period with the exception of two planned  
1.     REACTOR SAFETY
downpowers and one forced outage. Unit 2 was downpowered on April 20, 2012, to  
        Cornerstone: Initiating Events, Mitigating Systems, and Barrier Integrity
approximately 15 percent power for switchyard work and on June 18, 2012, for routine auxiliary  
1R01 Adverse Weather Protection (71111.01)
feedwater system testing. On June 27, 2012, the unit was tripped due to a turbine control  
  .1    Summer Seasonal Readiness Preparations
system malfunction and remained shut down until the end of the inspection period.  
    a.  Inspection Scope
        The inspectors performed a review of the licensees preparations for summer weather
1.  
        for selected systems, including conditions that could lead to an extended drought. The
REACTOR SAFETY  
        inspectors reviews focused specifically on the following plant systems:
Cornerstone: Initiating Events, Mitigating Systems, and Barrier Integrity  
        *       service water (SW);
1R01 Adverse Weather Protection
        *       component cooling water (CCW); and
.1
        *       primary auxiliary building (PAB) ventilation.
(71111.01)  
        During the inspection, the inspectors focused on plant specific design features and the
a.  
        licensees procedures used to mitigate or respond to adverse weather conditions.
Summer Seasonal Readiness Preparations  
        Additionally, the inspectors reviewed the Final Safety Analysis Report (FSAR) and
The inspectors performed a review of the licensees preparations for summer weather  
        performance requirements for systems selected for inspection, and verified that operator
for selected systems, including conditions that could lead to an extended drought. The  
        actions were appropriate as specified by plant specific procedures. The inspectors also
inspectors reviews focused specifically on the following plant systems:  
        reviewed corrective action program (CAP) items to verify that the licensee was
Inspection Scope
        identifying adverse weather issues at an appropriate threshold and entering them into
*  
        the CAP in accordance with station corrective action procedures. Documents reviewed
service water (SW);  
        are listed in the Attachment to this report.
*  
        This inspection constituted one seasonal adverse weather sample as defined in
component cooling water (CCW); and
        Inspection Procedure (IP) 71111.01-05.
*  
    b. Findings
primary auxiliary building (PAB) ventilation.  
        No findings were identified.
During the inspection, the inspectors focused on plant specific design features and the  
                                                  4                                    Enclosure
licensees procedures used to mitigate or respond to adverse weather conditions.
Additionally, the inspectors reviewed the Final Safety Analysis Report (FSAR) and  
performance requirements for systems selected for inspection, and verified that operator  
actions were appropriate as specified by plant specific procedures. The inspectors also  
reviewed corrective action program (CAP) items to verify that the licensee was  
identifying adverse weather issues at an appropriate threshold and entering them into  
the CAP in accordance with station corrective action procedures. Documents reviewed  
are listed in the Attachment to this report.  
This inspection constituted one seasonal adverse weather sample as defined in  
Inspection Procedure (IP) 71111.01-05.  
b.  
No findings were identified.  
Findings


.2   Readiness for Impending Adverse Weather Condition - Solar Magnetic Disturbances
  a. Inspection Scope
5
    Since solar magnetic disturbances were forecast in the vicinity of the facility for
Enclosure
    April 23, 2012, the inspectors reviewed the licensees overall preparations/protection for
.2  
    the expected weather conditions. On April 23, 2012, the inspectors walked down the
a.
    offsite power system, in addition to the licensees emergency alternating current (AC)
Readiness for Impending Adverse Weather Condition - Solar Magnetic Disturbances  
    power systems, because their safety-related (SR) functions could be affected or required
Since solar magnetic disturbances were forecast in the vicinity of the facility for  
    as a result of solar magnetic flares. The inspectors evaluated the licensees
April 23, 2012, the inspectors reviewed the licensees overall preparations/protection for  
    preparations against the sites procedures and determined that the staffs actions were
the expected weather conditions. On April 23, 2012, the inspectors walked down the  
    adequate. During the inspection, the inspectors focused on plant-specific design
offsite power system, in addition to the licensees emergency alternating current (AC)  
    features and the licensees procedures used to respond to specified adverse weather
power systems, because their safety-related (SR) functions could be affected or required  
    conditions. Additionally, inspection activities included a review of the FSAR, the
as a result of solar magnetic flares. The inspectors evaluated the licensees  
    licensees adverse weather procedures, daily monitoring of the off-normal environmental
preparations against the sites procedures and determined that the staffs actions were  
    conditions, and that operator actions specified by plant-specific procedures were
adequate. During the inspection, the inspectors focused on plant-specific design  
    appropriate to ensure operability of the facilitys systems. The inspectors also reviewed
features and the licensees procedures used to respond to specified adverse weather  
    a sample of CAP items to verify that the licensee identified adverse weather issues at an
conditions. Additionally, inspection activities included a review of the FSAR, the  
    appropriate threshold and dispositioned them through the CAP in accordance with
licensees adverse weather procedures, daily monitoring of the off-normal environmental  
    station corrective action procedures. Documents reviewed are listed in the Attachment
conditions, and that operator actions specified by plant-specific procedures were  
    to this report.
appropriate to ensure operability of the facilitys systems. The inspectors also reviewed  
    This inspection constituted one readiness for impending adverse weather condition
a sample of CAP items to verify that the licensee identified adverse weather issues at an  
    sample as defined in IP 71111.01-05.
appropriate threshold and dispositioned them through the CAP in accordance with  
  b. Findings
station corrective action procedures. Documents reviewed are listed in the Attachment  
    No findings were identified.
to this report.  
.3   Readiness for Impending Adverse Weather Condition - Severe Thunderstorm Watch
Inspection Scope
  a. Inspection Scope
This inspection constituted one readiness for impending adverse weather condition  
    Since thunderstorms with potential tornados and high winds were forecast in the vicinity
sample as defined in IP 71111.01-05.  
    of the facility for June 17, 2012, the inspectors reviewed the licensees overall
b.  
    preparations/protection for the expected weather conditions. The inspectors reviewed
No findings were identified.  
    the actions taken by the licensee in response to the adverse weather condition while the
Findings
    associated meteorological tower was out of service. The inspectors reviewed the
.3  
    potential impact of the adverse weather conditions on SR equipment, in addition to the
a.
    licensees emergency AC power systems. The inspectors evaluated the licensees
Readiness for Impending Adverse Weather Condition - Severe Thunderstorm Watch
    preparations against the sites procedures and determined that the licensees actions
Since thunderstorms with potential tornados and high winds were forecast in the vicinity  
    were adequate. During the inspection, the inspectors focused on plant-specific design
of the facility for June 17, 2012, the inspectors reviewed the licensees overall  
    features and the licensees procedures used to respond to specified adverse weather
preparations/protection for the expected weather conditions. The inspectors reviewed  
    conditions. The inspectors evaluated operator staffing and accessibility of controls and
the actions taken by the licensee in response to the adverse weather condition while the  
    indications for those systems required to control the plant. Additionally, the inspectors
associated meteorological tower was out of service. The inspectors reviewed the  
    reviewed the FSAR and performance requirements for systems selected for inspection,
potential impact of the adverse weather conditions on SR equipment, in addition to the  
    and verified that operator actions were appropriate as specified by plant specific
licensees emergency AC power systems. The inspectors evaluated the licensees  
    procedures. The inspectors also reviewed a sample of CAP items to verify that the
preparations against the sites procedures and determined that the licensees actions  
    licensee identified adverse weather issues at an appropriate threshold and dispositioned
were adequate. During the inspection, the inspectors focused on plant-specific design  
    them through the CAP in accordance with station corrective action procedures.
features and the licensees procedures used to respond to specified adverse weather  
    Documents reviewed are listed in the Attachment to this report.
conditions. The inspectors evaluated operator staffing and accessibility of controls and  
                                                5                                        Enclosure
indications for those systems required to control the plant. Additionally, the inspectors  
reviewed the FSAR and performance requirements for systems selected for inspection,  
and verified that operator actions were appropriate as specified by plant specific  
procedures. The inspectors also reviewed a sample of CAP items to verify that the  
licensee identified adverse weather issues at an appropriate threshold and dispositioned  
them through the CAP in accordance with station corrective action procedures.
Documents reviewed are listed in the Attachment to this report.  
Inspection Scope


      This inspection constituted one readiness for impending adverse weather condition
      sample as defined in IP 71111.01-05.
6
  b. Findings
Enclosure
      No findings were identified.
This inspection constituted one readiness for impending adverse weather condition  
1R04 Equipment Alignment (71111.04)
sample as defined in IP 71111.01-05.  
.Quarterly Partial System Walkdowns
b.  
  a. Inspection Scope
No findings were identified.  
      The inspectors performed partial system walkdowns of the following risk-significant
Findings
      system:
1R04 Equipment Alignment
      *       Unit 2 safety injection (SI) system B, during surveillance testing on the opposite
.1
              train; and
(71111.04)  
      *       Unit 1 turbine-driven auxiliary feedwater (TDAFW) pump after returned to service
a.  
              following maintenance.
Quarterly Partial System Walkdowns  
      The inspectors selected this system based on its risk significance relative to the Reactor
The inspectors performed partial system walkdowns of the following risk-significant  
      Safety Cornerstones at the time it was inspected. The inspectors attempted to identify
system:  
      any discrepancies that could impact the function of the system and, therefore, potentially
Inspection Scope
      increase risk. The inspectors reviewed applicable operating procedures, system
*  
      diagrams, FSAR, Technical Specification (TS) requirements, outstanding work orders
Unit 2 safety injection (SI) system B, during surveillance testing on the opposite  
      (WOs), condition reports (CRs), and the impact of ongoing work activities on redundant
train; and  
      trains of equipment in order to identify conditions that could have rendered the systems
*  
      incapable of performing their intended functions. The inspectors also walked down
Unit 1 turbine-driven auxiliary feedwater (TDAFW) pump after returned to service  
      accessible portions of the system to verify system components and support equipment
following maintenance.  
      were aligned correctly and operable. The inspectors examined the material condition of
The inspectors selected this system based on its risk significance relative to the Reactor  
      the components and observed operating parameters of equipment to verify that there
Safety Cornerstones at the time it was inspected. The inspectors attempted to identify  
      were no obvious deficiencies. The inspectors also verified that the licensee had properly
any discrepancies that could impact the function of the system and, therefore, potentially  
      identified and resolved equipment alignment problems that could cause initiating events
increase risk. The inspectors reviewed applicable operating procedures, system  
      or impact the capability of mitigating systems or barriers and entered them into the CAP
diagrams, FSAR, Technical Specification (TS) requirements, outstanding work orders  
      with the appropriate significance characterization. Documents reviewed are listed in the
(WOs), condition reports (CRs), and the impact of ongoing work activities on redundant  
      Attachment to this report.
trains of equipment in order to identify conditions that could have rendered the systems  
      These activities constituted two partial system walkdown samples as defined in
incapable of performing their intended functions. The inspectors also walked down  
      IP 71111.04-05.
accessible portions of the system to verify system components and support equipment  
  b. Findings
were aligned correctly and operable. The inspectors examined the material condition of  
      No findings were identified.
the components and observed operating parameters of equipment to verify that there  
                                                6                                        Enclosure
were no obvious deficiencies. The inspectors also verified that the licensee had properly  
identified and resolved equipment alignment problems that could cause initiating events  
or impact the capability of mitigating systems or barriers and entered them into the CAP  
with the appropriate significance characterization. Documents reviewed are listed in the  
Attachment to this report.  
These activities constituted two partial system walkdown samples as defined in  
IP 71111.04-05.  
b.  
No findings were identified.  
Findings


1R05 Fire Protection (71111.05)
.1  Routine Resident Inspector Tours (71111.05Q)
7
  a. Inspection Scope
Enclosure
      The inspectors conducted fire protection (FP) walkdowns which were focused on
1R05 Fire Protection
      availability, accessibility, and the condition of firefighting equipment in the following
.1
      risk-significant plant areas:
(71111.05)  
      *       fire zone 187 (monitor tank room);
Routine Resident Inspector Tours
      *       fire zone 596 (Unit 2 façade);
a.
      *       fire zone 151 (SI pump room); and
(71111.05Q)  
      *       fire zone 318 (cable spreading room).
The inspectors conducted fire protection (FP) walkdowns which were focused on  
      The inspectors reviewed areas to assess if the licensee had implemented an FP
availability, accessibility, and the condition of firefighting equipment in the following  
      program that adequately controlled combustibles and ignition sources within the plant,
risk-significant plant areas:  
      effectively maintained fire detection and suppression capability, maintained passive FP
Inspection Scope
      features in good material condition, and implemented adequate compensatory measures
*  
      for out-of-service, degraded or inoperable FP equipment, systems, or features in
fire zone 187 (monitor tank room);  
      accordance with the licensees fire plan. The inspectors selected fire areas based on
*  
      their overall contribution to internal fire risk as documented in the plants Individual Plant
fire zone 596 (Unit 2 façade);  
      Examination of External Events with later additional insights, their potential to impact
*  
      equipment which could initiate or mitigate a plant transient, or their impact on the plants
fire zone 151 (SI pump room); and  
      ability to respond to a security event. Using the documents listed in the Attachment to
*  
      this report, the inspectors verified that fire hoses and extinguishers were in their
fire zone 318 (cable spreading room).  
      designated locations and available for immediate use; that fire detectors and sprinklers
The inspectors reviewed areas to assess if the licensee had implemented an FP  
      were unobstructed; that transient material loading was within the analyzed limits; and fire
program that adequately controlled combustibles and ignition sources within the plant,  
      doors, dampers, and penetration seals appeared to be in satisfactory condition. The
effectively maintained fire detection and suppression capability, maintained passive FP  
      inspectors also verified that minor issues identified during the inspection were entered
features in good material condition, and implemented adequate compensatory measures  
      into the CAP. Documents reviewed are listed in the Attachment to this report.
for out-of-service, degraded or inoperable FP equipment, systems, or features in  
      These activities constituted four quarterly fire protection inspection samples as defined in
accordance with the licensees fire plan. The inspectors selected fire areas based on  
      IP 71111.05-05.
their overall contribution to internal fire risk as documented in the plants Individual Plant  
  b. Findings
Examination of External Events with later additional insights, their potential to impact  
      No findings were identified.
equipment which could initiate or mitigate a plant transient, or their impact on the plants  
1R06 Flooding (71111.06)
ability to respond to a security event. Using the documents listed in the Attachment to  
.Internal Flooding
this report, the inspectors verified that fire hoses and extinguishers were in their  
  a. Inspection Scope
designated locations and available for immediate use; that fire detectors and sprinklers  
      The inspectors reviewed selected risk important plant design features and licensee
were unobstructed; that transient material loading was within the analyzed limits; and fire  
      procedures intended to protect the plant and its SR equipment from internal flooding
doors, dampers, and penetration seals appeared to be in satisfactory condition. The  
      events. The inspectors reviewed flood analyses and design documents, including the
inspectors also verified that minor issues identified during the inspection were entered  
      FSAR, engineering calculations, and abnormal operating procedures (AOPs) to identify
into the CAP. Documents reviewed are listed in the Attachment to this report.  
      licensee commitments. In addition, the inspectors reviewed licensee drawings to identify
These activities constituted four quarterly fire protection inspection samples as defined in  
      areas and equipment that may be affected by internal flooding caused by the failure or
IP 71111.05-05.  
                                                  7                                        Enclosure
b.  
No findings were identified.  
Findings
1R06 Flooding
.1
(71111.06)  
a.  
Internal Flooding  
The inspectors reviewed selected risk important plant design features and licensee  
procedures intended to protect the plant and its SR equipment from internal flooding  
events. The inspectors reviewed flood analyses and design documents, including the  
FSAR, engineering calculations, and abnormal operating procedures (AOPs) to identify  
licensee commitments. In addition, the inspectors reviewed licensee drawings to identify  
areas and equipment that may be affected by internal flooding caused by the failure or  
Inspection Scope


      misalignment of nearby sources of water, such as the fire suppression or the circulating
      water systems. The inspectors also reviewed the licensees corrective action documents
8
      with respect to past flood-related items identified in the CAP to verify the adequacy of
Enclosure
      the corrective actions. The inspectors performed a walkdown of the following plant area
misalignment of nearby sources of water, such as the fire suppression or the circulating  
      to assess the adequacy of watertight doors and verify drains and sumps were clear of
water systems. The inspectors also reviewed the licensees corrective action documents  
      debris and were operable, and that the licensee complied with its commitments.
with respect to past flood-related items identified in the CAP to verify the adequacy of  
      Documents reviewed are listed in the Attachment to this report.
the corrective actions. The inspectors performed a walkdown of the following plant area  
      *       residual heat removal (RHR) rooms.
to assess the adequacy of watertight doors and verify drains and sumps were clear of  
      This inspection constituted one internal flooding sample as defined in IP 71111.06-05.
debris and were operable, and that the licensee complied with its commitments.
  b. Findings
Documents reviewed are listed in the Attachment to this report.  
      No findings were identified.
*  
1R11 Licensed Operator Requalification Program (71111.11)
residual heat removal (RHR) rooms.  
.1  Resident Inspector Quarterly Review (71111.11Q)
This inspection constituted one internal flooding sample as defined in IP 71111.06-05.  
  a. Inspection Scope
b.  
      On May 21, 2012, the inspectors observed a crew of licensed operators in the plants
No findings were identified.
      simulator during licensed operator requalification examinations to verify that operator
Findings
      performance was adequate, evaluators were identifying and documenting crew
1R11 Licensed Operator Requalification Program
      performance problems, and that training was being conducted in accordance with
.1
      licensee procedures. The inspectors evaluated the following areas:
(71111.11)  
      *       licensed operator performance;
Resident Inspector Quarterly Review
      *       crews clarity and formality of communications;
a.
      *       ability to take timely actions in the conservative direction;
(71111.11Q)  
      *       prioritization, interpretation, and verification of annunciator alarms;
On May 21, 2012, the inspectors observed a crew of licensed operators in the plants  
      *       correct use and implementation of abnormal and emergency procedures;
simulator during licensed operator requalification examinations to verify that operator  
      *       control board manipulations;
performance was adequate, evaluators were identifying and documenting crew  
      *       oversight and direction from supervisors; and
performance problems, and that training was being conducted in accordance with  
      *       ability to identify and implement appropriate TS actions and Emergency Plan
licensee procedures. The inspectors evaluated the following areas:  
              actions and notifications.
Inspection Scope
      The crews performance in these areas was compared to pre-established operator action
*  
      expectations and successful critical task completion requirements. Documents reviewed
licensed operator performance;  
      are listed in the Attachment to this report.
*  
      This inspection constituted one quarterly licensed operator requalification program
crews clarity and formality of communications;  
      simulator sample as defined in IP 71111.11.
*  
  b. Findings
ability to take timely actions in the conservative direction;  
      No findings were identified.
*  
                                                  8                                    Enclosure
prioritization, interpretation, and verification of annunciator alarms;  
*  
correct use and implementation of abnormal and emergency procedures;  
*  
control board manipulations;  
*  
oversight and direction from supervisors; and  
*  
ability to identify and implement appropriate TS actions and Emergency Plan  
actions and notifications.  
The crews performance in these areas was compared to pre-established operator action  
expectations and successful critical task completion requirements. Documents reviewed  
are listed in the Attachment to this report.  
This inspection constituted one quarterly licensed operator requalification program  
simulator sample as defined in IP 71111.11.  
b.  
No findings were identified.  
Findings


  .2   Resident Inspector Quarterly Observation of Heightened Activity or Risk (71111.11Q)
   
  a. Inspection Scope
9
      On April 20 and 21, 2012, the inspectors observed activities in the control room during
Enclosure
      the high risk activity of a Unit 2 downpower to 15 percent to secure one train of main
.2  
      feedwater (FW). This was an activity that required heightened awareness or was related
Resident Inspector Quarterly Observation of Heightened Activity or Risk
      to increased risk. The inspectors evaluated the following areas:
a.
      *       licensed operator performance;
  (71111.11Q)  
      *       crews clarity and formality of communications;
On April 20 and 21, 2012, the inspectors observed activities in the control room during  
      *       ability to take timely actions in the conservative direction;
the high risk activity of a Unit 2 downpower to 15 percent to secure one train of main  
      *       prioritization, interpretation, and verification of annunciator alarms;
feedwater (FW). This was an activity that required heightened awareness or was related  
      *       correct use and implementation of procedures;
to increased risk. The inspectors evaluated the following areas:  
      *       control board manipulations; and
Inspection Scope
      *       oversight and direction from supervisors.
*  
      The performance in these areas was compared to pre-established operator action
licensed operator performance;  
      expectations, procedural compliance, and task completion requirements. Documents
*  
      reviewed are listed in the Attachment to this report.
crews clarity and formality of communications;  
      This inspection constituted one quarterly licensed operator heightened activity/risk
*  
      sample as defined in IP 71111.11.
ability to take timely actions in the conservative direction;  
  b. Findings
*  
      No findings were identified.
prioritization, interpretation, and verification of annunciator alarms;  
1R12 Maintenance Effectiveness (71111.12)
*  
.1  Routine Quarterly Evaluations (71111.12Q)
correct use and implementation of procedures;  
  a. Inspection Scope
*  
      The inspectors evaluated degraded performance issues involving the following
control board manipulations; and  
      risk-significant system:
*  
      *       TDAFW system.
oversight and direction from supervisors.  
      The inspectors reviewed events, such as where ineffective equipment maintenance had
The performance in these areas was compared to pre-established operator action  
      resulted in valid or invalid automatic actuations of engineered safeguards systems, and
expectations, procedural compliance, and task completion requirements. Documents  
      independently verified the licensee's actions to address system performance or condition
reviewed are listed in the Attachment to this report.  
      problems in terms of the following:
This inspection constituted one quarterly licensed operator heightened activity/risk  
      *       implementing appropriate work practices;
sample as defined in IP 71111.11.  
      *       identifying and addressing common cause failures;
b.  
      *       scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;
No findings were identified.  
      *       characterizing system reliability issues for performance;
Findings
      *       charging unavailability for performance;
1R12 Maintenance Effectiveness
      *       trending key parameters for condition monitoring;
.1
      *       ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or re-classification; and
(71111.12)  
                                                  9                                      Enclosure
Routine Quarterly Evaluations
a.
(71111.12Q)  
The inspectors evaluated degraded performance issues involving the following  
risk-significant system:  
Inspection Scope
*  
TDAFW system.  
The inspectors reviewed events, such as where ineffective equipment maintenance had  
resulted in valid or invalid automatic actuations of engineered safeguards systems, and  
independently verified the licensee's actions to address system performance or condition  
problems in terms of the following:  
*  
implementing appropriate work practices;  
*  
identifying and addressing common cause failures;  
*  
scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;  
*  
characterizing system reliability issues for performance;  
*  
charging unavailability for performance;  
*  
trending key parameters for condition monitoring;  
*  
ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or re-classification; and  


      *       verifying appropriate performance criteria for structures, systems, and
              components (SSCs)/functions classified as (a)(2), or appropriate and adequate
10
              goals and corrective actions for systems classified as (a)(1).
Enclosure
      The inspectors assessed performance issues with respect to the reliability, availability,
*  
      and condition monitoring of the system. In addition, the inspectors verified maintenance
verifying appropriate performance criteria for structures, systems, and  
      effectiveness issues were entered into the CAP with the appropriate significance
components (SSCs)/functions classified as (a)(2), or appropriate and adequate  
      characterization. Documents reviewed are listed in the Attachment to this report.
goals and corrective actions for systems classified as (a)(1).  
      This inspection constituted one quarterly maintenance effectiveness samples as defined
The inspectors assessed performance issues with respect to the reliability, availability,  
      in IP 71111.12-05.
and condition monitoring of the system. In addition, the inspectors verified maintenance  
  b. Findings
effectiveness issues were entered into the CAP with the appropriate significance  
      No findings were identified.
characterization. Documents reviewed are listed in the Attachment to this report.  
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)
This inspection constituted one quarterly maintenance effectiveness samples as defined  
.Maintenance Risk Assessments and Emergent Work Control
in IP 71111.12-05.  
  a. Inspection Scope
b.  
      The inspectors reviewed the licensee's evaluation and management of plant risk for the
No findings were identified.  
      maintenance and emergent work activities affecting risk-significant and SR equipment
Findings
      listed below to verify that the appropriate risk assessments were performed prior to
1R13 Maintenance Risk Assessments and Emergent Work Control
      removing equipment for work:
.1
      *       risk management of 345-kilovolt (kV) output breaker hotspot with increasing
(71111.13)  
              outside air temperatures;
a.  
      *       risk management with CCW heat exchanger C inoperable but available;
Maintenance Risk Assessments and Emergent Work Control  
      *       risk management with emergency diesel generators (EDGs) G-01 and G-02
The inspectors reviewed the licensee's evaluation and management of plant risk for the  
              inoperable week of April 26; and
maintenance and emergent work activities affecting risk-significant and SR equipment  
      *       risk management with Unit 1 TDAFW pump and gas turbine generator
listed below to verify that the appropriate risk assessments were performed prior to  
              out-of-service.
removing equipment for work:  
      These activities were selected based on their potential risk significance relative to the
Inspection Scope
      Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified that
*  
      risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate
risk management of 345-kilovolt (kV) output breaker hotspot with increasing  
      and complete. When emergent work was performed, the inspectors verified that the
outside air temperatures;  
      plant risk was promptly reassessed and managed. The inspectors reviewed the scope
*  
      of maintenance work, discussed the results of the assessment with the licensee's
risk management with CCW heat exchanger C inoperable but available;  
      probabilistic risk analyst or shift technical advisor, and verified plant conditions were
*  
      consistent with the risk assessment. The inspectors also reviewed TS requirements and
risk management with emergency diesel generators (EDGs) G-01 and G-02  
      walked down portions of redundant safety systems, when applicable, to verify risk
inoperable week of April 26; and  
      analysis assumptions were valid and applicable requirements were met. Documents
*  
      reviewed are listed in the Attachment to this report.
risk management with Unit 1 TDAFW pump and gas turbine generator  
      These activities constituted four maintenance risk assessments and emergent work
out-of-service.  
      control samples as defined in IP 71111.13-05.
These activities were selected based on their potential risk significance relative to the  
                                                10                                        Enclosure
Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified that  
risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate  
and complete. When emergent work was performed, the inspectors verified that the  
plant risk was promptly reassessed and managed. The inspectors reviewed the scope  
of maintenance work, discussed the results of the assessment with the licensee's  
probabilistic risk analyst or shift technical advisor, and verified plant conditions were  
consistent with the risk assessment. The inspectors also reviewed TS requirements and  
walked down portions of redundant safety systems, when applicable, to verify risk  
analysis assumptions were valid and applicable requirements were met. Documents  
reviewed are listed in the Attachment to this report.  
These activities constituted four maintenance risk assessments and emergent work  
control samples as defined in IP 71111.13-05.  


  b. Findings
      No findings were identified.
11
1R15 Operability Determinations and Functional Assessments (71111.15)
Enclosure
.Operability Evaluations
b.  
  a. Inspection Scope
No findings were identified.  
      The inspectors reviewed the following operability issues:
Findings
      *       control room board deficiencies and abandoned in-place modifications;
1R15 Operability Determinations and Functional Assessments
      *       containment fan cooler unit closed drain valves (Unit 2);
.1
      *       SI with non-conservative gas void acceptance criteria;
(71111.15)  
      *       water leaking in steam generator A vault (Unit 2) (partial);
a.  
      *       TDAFW failed coupling (Unit 1) (partial); and
Operability Evaluations  
      *       cable spreading room.
The inspectors reviewed the following operability issues:  
      The inspectors selected these potential operability issues based on the risk significance
Inspection Scope
      of the associated components and systems. The inspectors evaluated the technical
*  
      adequacy of the evaluations to ensure that TS operability was properly justified and the
control room board deficiencies and abandoned in-place modifications;  
      subject component or system remained available such that no unrecognized increase in
*  
      risk occurred. The inspectors compared the operability and design criteria in the
containment fan cooler unit closed drain valves (Unit 2);  
      appropriate sections of the TSs and FSAR to the licensees evaluations to determine
*  
      whether the components or systems were operable. Where compensatory measures
SI with non-conservative gas void acceptance criteria;  
      were required to maintain operability, the inspectors determined whether the measures
*  
      in place would function as intended and were properly controlled. The inspectors
water leaking in steam generator A vault (Unit 2) (partial);  
      determined, where appropriate, compliance with bounding limitations associated with the
*  
      evaluations. Additionally, the inspectors reviewed a sampling of corrective action
TDAFW failed coupling (Unit 1) (partial); and  
      documents to verify that the licensee was identifying and correcting any deficiencies
*  
      associated with operability evaluations. Documents reviewed are listed in the
cable spreading room.  
      Attachment to this report.
The inspectors selected these potential operability issues based on the risk significance  
      This inspection constituted four completed and two partial operability samples as defined
of the associated components and systems. The inspectors evaluated the technical  
      in IP 71111.15-05.
adequacy of the evaluations to ensure that TS operability was properly justified and the  
  b. Findings
subject component or system remained available such that no unrecognized increase in  
      No findings were identified.
risk occurred. The inspectors compared the operability and design criteria in the  
1R18 Plant Modifications (71111.18)
appropriate sections of the TSs and FSAR to the licensees evaluations to determine  
.Plant Modifications
whether the components or systems were operable. Where compensatory measures  
  a. Inspection Scope
were required to maintain operability, the inspectors determined whether the measures  
      The inspectors reviewed the following modification(s):
in place would function as intended and were properly controlled. The inspectors  
      *       main feedwater isolation valve (MFIV) curtains (permanent);
determined, where appropriate, compliance with bounding limitations associated with the  
      *       main steam isolation valve (MSIV) air line leak repair (temporary);
evaluations. Additionally, the inspectors reviewed a sampling of corrective action  
      *       EDG exhaust (temporary) (partial); and
documents to verify that the licensee was identifying and correcting any deficiencies  
                                              11                                    Enclosure
associated with operability evaluations. Documents reviewed are listed in the  
Attachment to this report.  
This inspection constituted four completed and two partial operability samples as defined  
in IP 71111.15-05.  
b.  
No findings were identified.  
Findings
1R18 Plant Modifications
.1
(71111.18)  
a.  
Plant Modifications  
The inspectors reviewed the following modification(s):  
Inspection Scope
*  
main feedwater isolation valve (MFIV) curtains (permanent);  
*  
main steam isolation valve (MSIV) air line leak repair (temporary);  
*  
EDG exhaust (temporary) (partial); and  


      *       480-volt temporary power to 1B-42 loads (temporary).
      The inspectors reviewed the configuration changes and associated 10 CFR 50.59 safety
12
      evaluation screening against the design basis, the FSAR, and the TSs, as applicable, to
Enclosure
      verify that the modification did not affect the operability or availability of the affected
*  
      systems. The inspectors, as applicable, observed ongoing and completed work
480-volt temporary power to 1B-42 loads (temporary).  
      activities to ensure that the modifications were installed as directed and consistent with
The inspectors reviewed the configuration changes and associated 10 CFR 50.59 safety  
      the design control documents; the modifications operated as expected; post-modification
evaluation screening against the design basis, the FSAR, and the TSs, as applicable, to  
      testing adequately demonstrated continued system operability, availability, and reliability;
verify that the modification did not affect the operability or availability of the affected  
      and that operation of the modifications did not impact the operability of any interfacing
systems. The inspectors, as applicable, observed ongoing and completed work  
      systems. As applicable, the inspectors verified that relevant procedure, design, and
activities to ensure that the modifications were installed as directed and consistent with  
      licensing documents were properly updated. Lastly, the inspectors discussed the plant
the design control documents; the modifications operated as expected; post-modification  
      modification with operations, engineering, and training personnel to ensure that the
testing adequately demonstrated continued system operability, availability, and reliability;  
      individuals were aware of how the operation with the plant modification in place could
and that operation of the modifications did not impact the operability of any interfacing  
      impact overall plant performance. Documents reviewed are listed in the Attachment to
systems. As applicable, the inspectors verified that relevant procedure, design, and  
      this report.
licensing documents were properly updated. Lastly, the inspectors discussed the plant  
      This inspection constituted two completed temporary modification samples, one partial
modification with operations, engineering, and training personnel to ensure that the  
      temporary modification sample, and one permanent plant modification sample as
individuals were aware of how the operation with the plant modification in place could  
      defined in IP 71111.18-05.
impact overall plant performance. Documents reviewed are listed in the Attachment to  
  b. Findings
this report.  
      No findings were identified.
This inspection constituted two completed temporary modification samples, one partial  
1R19 Post-Maintenance Testing (71111.19)
temporary modification sample, and one permanent plant modification sample as  
.Post-Maintenance Testing
defined in IP 71111.18-05.  
  a. Inspection Scope
b.  
      The inspectors reviewed the following post-maintenance testing (PMT) activities to verify
No findings were identified.  
      that procedures and test activities were adequate to ensure system operability and
Findings
      functional capability:
1R19 Post-Maintenance Testing
      *       PMT of PAB ventilation following low flow switch replacement (Units 1 and 2);
.1
      *       PMT of EDG room exhaust fan testing (Units 1 and 2);
(71111.19)  
      *       PMT of EDG G-01 starting air compressor;
a.  
      *       PMT of TDAFW pump after coupling repairs (Unit 1);
Post-Maintenance Testing  
      *       PMT of EDG modification (Unit 2);
The inspectors reviewed the following post-maintenance testing (PMT) activities to verify  
      *       PMT of main generator output breaker disconnects following hotspot repair
that procedures and test activities were adequate to ensure system operability and  
              (Unit 2); and
functional capability:  
      *       PMT of main steam dump 2MS 2052 to condenser dump control valve (Unit 2).
Inspection Scope
      These activities were selected based upon the SSCs ability to impact risk. The
*  
      inspectors evaluated these activities for the following (as applicable): the effect of testing
PMT of PAB ventilation following low flow switch replacement (Units 1 and 2);  
      on the plant had been adequately addressed; testing was adequate for the maintenance
*  
      performed; acceptance criteria were clear and demonstrated operational readiness; test
PMT of EDG room exhaust fan testing (Units 1 and 2);  
      instrumentation was appropriate; tests were performed as written in accordance with
*  
      properly reviewed and approved procedures; equipment was returned to its operational
PMT of EDG G-01 starting air compressor;  
      status following testing (temporary modifications or jumpers required for test
*  
                                                12                                          Enclosure
PMT of TDAFW pump after coupling repairs (Unit 1);  
*  
PMT of EDG modification (Unit 2);  
*  
PMT of main generator output breaker disconnects following hotspot repair  
(Unit 2); and  
*  
PMT of main steam dump 2MS 2052 to condenser dump control valve (Unit 2).  
These activities were selected based upon the SSCs ability to impact risk. The  
inspectors evaluated these activities for the following (as applicable): the effect of testing  
on the plant had been adequately addressed; testing was adequate for the maintenance  
performed; acceptance criteria were clear and demonstrated operational readiness; test  
instrumentation was appropriate; tests were performed as written in accordance with  
properly reviewed and approved procedures; equipment was returned to its operational  
status following testing (temporary modifications or jumpers required for test  


  performance were properly removed after test completion); and test documentation was
  properly evaluated. The inspectors evaluated the activities against TSs, the FSAR,
13
  10 CFR Part 50 requirements, licensee procedures, and various NRC generic
Enclosure
  communications to ensure that the test results adequately ensured that the equipment
performance were properly removed after test completion); and test documentation was  
  met the licensing basis and design requirements. In addition, the inspectors reviewed
properly evaluated. The inspectors evaluated the activities against TSs, the FSAR,  
  corrective action documents associated with PMTs to determine whether the licensee
10 CFR Part 50 requirements, licensee procedures, and various NRC generic  
  was identifying problems and entering them in the CAP, and that the problems were
communications to ensure that the test results adequately ensured that the equipment  
  being corrected commensurate with their importance to safety. Documents reviewed are
met the licensing basis and design requirements. In addition, the inspectors reviewed  
  listed in the Attachment to this report.
corrective action documents associated with PMTs to determine whether the licensee  
  This inspection constituted seven post-maintenance testing samples as defined in
was identifying problems and entering them in the CAP, and that the problems were  
  IP 71111.19-05.
being corrected commensurate with their importance to safety. Documents reviewed are  
b. Findings
listed in the Attachment to this report.  
  Failure to Establish Emergency Diesel Generator Ventilation Damper Testing
This inspection constituted seven post-maintenance testing samples as defined in  
  Introduction: The inspectors identified an issue of very low safety significance (Green)
IP 71111.19-05.  
  and associated non-cited violation (NCV) of 10 CFR Part 50, Appendix B, Criterion XI,
b.  
  "Test Control," because the licensee failed to establish a routine testing procedure to
Findings  
  demonstrate that the air flows for the ventilation systems in the G-01 and G-02 EDG
Failure to Establish Emergency Diesel Generator Ventilation Damper Testing  
  rooms were sufficient to keep room temperatures maintained at or below the design
Introduction: The inspectors identified an issue of very low safety significance (Green)  
  basis. The licensee entered this issue into its CAP for evaluation and development of
and associated non-cited violation (NCV) of 10 CFR Part 50, Appendix B, Criterion XI,  
  corrective actions.
"Test Control," because the licensee failed to establish a routine testing procedure to  
  Description: The TS 3.8.1 required, in part, that independent and redundant sources of
demonstrate that the air flows for the ventilation systems in the G-01 and G-02 EDG  
  power be provided to the Engineered Safety Feature Systems. This was met through
rooms were sufficient to keep room temperatures maintained at or below the design  
  each safeguard bus having a normal offsite power source and a standby emergency
basis. The licensee entered this issue into its CAP for evaluation and development of  
  power source (EDG). There were two EDGs (G-01 and G-02) that supplied power to the
corrective actions.  
  Train A buses. These diesels were considered operable when the diesel room
Description
  temperature was less than 115 degrees Fahrenheit with the EDG carrying design basis
Based on this information, the inspectors reviewed the acceptance criteria for the gravity  
  accident loads. For the room temperature to be maintained, three of the four gravity
operator louvers and found none. In response, the licensee stated the gravity louvers  
  operated louvers must be opened.
had to open freely; however, a specified amount was not necessary. Additionally, the  
  Based on this information, the inspectors reviewed the acceptance criteria for the gravity
licensee stated that the gravity operated louvers did not have specific acceptance criteria  
  operator louvers and found none. In response, the licensee stated the gravity louvers
established to ensure air flows were met and that, instead, the fan motors were used to  
  had to open freely; however, a specified amount was not necessary. Additionally, the
determine air flows. The inspectors then questioned the licensee regarding the ability to  
  licensee stated that the gravity operated louvers did not have specific acceptance criteria
accurately predict fan air flow outputs based on the fan motors. Also, the inspectors  
  established to ensure air flows were met and that, instead, the fan motors were used to
questioned what additional monitoring was performed on the fans to ensure that there  
  determine air flows. The inspectors then questioned the licensee regarding the ability to
was no degradation of the fan blades, no friction on the bearings, or that no bypass flow  
  accurately predict fan air flow outputs based on the fan motors. Also, the inspectors
was occurring, as well as how the test was performed in a consistent manner. The  
  questioned what additional monitoring was performed on the fans to ensure that there
licensee provided that there was no periodic testing to ensure air flows.  
  was no degradation of the fan blades, no friction on the bearings, or that no bypass flow
:  The TS 3.8.1 required, in part, that independent and redundant sources of
  was occurring, as well as how the test was performed in a consistent manner. The
power be provided to the Engineered Safety Feature Systems.  This was met through
  licensee provided that there was no periodic testing to ensure air flows.
each safeguard bus having a normal offsite power source and a standby emergency
  On March 29, 2012, the licensee initiated CR01750276 in response to the inspectors
power source (EDG).  There were two EDGs (G-01 and G-02) that supplied power to the
  concerns regarding the louvers in the G-01 and G-02 EDG rooms. Specifically, the CR
Train A buses.  These diesels were considered operable when the diesel room
  identified that air flows had not been routinely taken to ensure that adequate air flow
temperature was less than 115 degrees Fahrenheit with the EDG carrying design basis
  requirements were met. At the conclusion of the inspection period, the licensees
accident loads.  For the room temperature to be maintained, three of the four gravity
  corrective actions included performance of air flow measurements on the fan units,
operated louvers must be opened.
                                            13                                      Enclosure
On March 29, 2012, the licensee initiated CR01750276 in response to the inspectors  
concerns regarding the louvers in the G-01 and G-02 EDG rooms. Specifically, the CR  
identified that air flows had not been routinely taken to ensure that adequate air flow  
requirements were met. At the conclusion of the inspection period, the licensees  
corrective actions included performance of air flow measurements on the fan units,  


creation of a preventive maintenance requirement for taking periodic flow
measurements, and assessment of the identified issue through a condition evaluation.
14
Additionally, the inspectors noted that the licensee had taken air flow measurements on
Enclosure
the fans in 1998 and 2007, but had not established acceptance criteria and routine
creation of a preventive maintenance requirement for taking periodic flow  
testing. The inspectors noted differences between the 1998 and 2007 data obtained,
measurements, and assessment of the identified issue through a condition evaluation.  
and that the licensee had used the lesser-conservative data from these tests to support
Additionally, the inspectors noted that the licensee had taken air flow measurements on  
the design calculation. The inspectors questioned the use of non-conservative data
the fans in 1998 and 2007, but had not established acceptance criteria and routine  
values in the design calculations for the maximum temperatures in the EDG rooms to
testing. The inspectors noted differences between the 1998 and 2007 data obtained,  
support operability. This concern was captured in CR1769204. The licensees planned
and that the licensee had used the lesser-conservative data from these tests to support  
corrective actions were to revise the calculation to use the accurate data.
the design calculation. The inspectors questioned the use of non-conservative data  
Analysis: The inspectors determined that the failure to establish a routine testing
values in the design calculations for the maximum temperatures in the EDG rooms to  
procedure to demonstrate that the air flows for the G-01 and G-02 rooms would keep
support operability. This concern was captured in CR1769204. The licensees planned  
room temperatures at or below the maximum allowable temperatures when the EDGs
corrective actions were to revise the calculation to use the accurate data.  
were carrying design basis accident loads was a performance deficiency warranting
Analysis
further review. Using IMC 0612, Appendix B, Issue Screening, dated
The inspectors determined the finding could be evaluated using IMC 0609, Significance  
December 24, 2009, the inspectors determined that this finding was more than minor
Determination Process, Attachment 0609.04, Phase 1 - Initial Screening and  
because it was associated with the Mitigating Systems Cornerstone attribute for design
Characterization of Findings, Tables 3b and 4a, for the Mitigating Systems Cornerstone,  
control. Specifically, it adversely affected the Mitigating System Cornerstone objective to
dated January 10, 2008. The inspectors answered No to all of the questions in the  
ensure the reliability of systems that respond to initiating events to prevent undesirable
Mitigating Systems column of Table 4a; therefore, the finding screened as having very  
consequences.
low safety significance (Green). The licensee entered this issue into the CAP as  
The inspectors determined the finding could be evaluated using IMC 0609, Significance
AR01750276. The licensees corrective actions included performance of air flow  
Determination Process, Attachment 0609.04, Phase 1 - Initial Screening and
measurements on the fan units, creation of a preventive maintenance requirement for  
Characterization of Findings, Tables 3b and 4a, for the Mitigating Systems Cornerstone,
taking periodic flow measurements, and assessment of the identified issue through a  
dated January 10, 2008. The inspectors answered No to all of the questions in the
condition evaluation.
Mitigating Systems column of Table 4a; therefore, the finding screened as having very
:  The inspectors determined that the failure to establish a routine testing
low safety significance (Green). The licensee entered this issue into the CAP as
procedure to demonstrate that the air flows for the G-01 and G-02 rooms would keep
AR01750276. The licensees corrective actions included performance of air flow
room temperatures at or below the maximum allowable temperatures when the EDGs
measurements on the fan units, creation of a preventive maintenance requirement for
were carrying design basis accident loads was a performance deficiency warranting
taking periodic flow measurements, and assessment of the identified issue through a
further review.  Using IMC 0612, Appendix B, Issue Screening, dated
condition evaluation.
December 24, 2009, the inspectors determined that this finding was more than minor
This finding has a cross-cutting aspect in the area of human performance,
because it was associated with the Mitigating Systems Cornerstone attribute for design
decision-making. Specifically, the licensee did not use conservative assumptions
control.  Specifically, it adversely affected the Mitigating System Cornerstone objective to
regarding the verification of the proper air flow through the SR gravity dampers in the
ensure the reliability of systems that respond to initiating events to prevent undesirable
EDG G-01 and G-02 rooms (H.1(b)). The inspectors reviewed the licensees causal
consequences.  
assessment and found that this assessment was consistent with their assessment of the
This finding has a cross-cutting aspect in the area of human performance,  
condition.
decision-making. Specifically, the licensee did not use conservative assumptions  
Enforcement: Title 10 CFR 50, Appendix B, Criterion XI, "Test Control," requires, in part,
regarding the verification of the proper air flow through the SR gravity dampers in the  
that a test program be established to assure that all testing required to demonstrate that
EDG G-01 and G-02 rooms (H.1(b)). The inspectors reviewed the licensees causal  
components will perform satisfactorily in service is identified and performed in
assessment and found that this assessment was consistent with their assessment of the  
accordance with written test procedures which incorporate the requirements and
condition.  
acceptance limits contained in applicable design documents. Contrary to this, on
Enforcement: Title 10 CFR 50, Appendix B, Criterion XI, "Test Control," requires, in part,  
March 29, 2012, the inspectors identified that the licensee failed to establish a routine
that a test program be established to assure that all testing required to demonstrate that  
testing procedure to demonstrate that the air flows for EDGs G-01 and G-02 ventilation
components will perform satisfactorily in service is identified and performed in  
systems would keep the room temperatures at or below the maximum allowable
accordance with written test procedures which incorporate the requirements and  
temperatures when the EDGs were carrying design basis accident loads. Because this
acceptance limits contained in applicable design documents. Contrary to this, on  
violation was of very low safety significance, and it was entered into the licensees CAP
March 29, 2012, the inspectors identified that the licensee failed to establish a routine  
                                          14                                      Enclosure
testing procedure to demonstrate that the air flows for EDGs G-01 and G-02 ventilation  
systems would keep the room temperatures at or below the maximum allowable  
temperatures when the EDGs were carrying design basis accident loads. Because this  
violation was of very low safety significance, and it was entered into the licensees CAP  


      (as CR1750276), this violation is being treated as an NCV, consistent with Section 2.3.2
      of the NRC Enforcement Policy (NCV 05000266/2012003-01; 05000301/2012003-01;
15
      Failure to Establish Emergency Diesel Generator Ventilation System Testing).
Enclosure
1R20 Outage Activities (71111.20)
(as CR1750276), this violation is being treated as an NCV, consistent with Section 2.3.2  
.Other Outage Activities
of the NRC Enforcement Policy (NCV 05000266/2012003-01; 05000301/2012003-01;  
  a. Inspection Scope
Failure to Establish Emergency Diesel Generator Ventilation System Testing).  
      The inspectors evaluated outage activities for an unplanned Unit 2 outage that began on
1R20 Outage Activities
      June 27, 2012, and continued through the end of the inspection period. The outage
.1
      occurred as a result of a turbine control system malfunction that resulted in a turbine
(71111.20)  
      load reject which terminated when the reactor operators inserted a manual reactor trip.
a.  
      The inspectors reviewed activities to ensure that the licensee considered risk in
Other Outage Activities  
      developing, planning, and implementing the outage schedule.
The inspectors evaluated outage activities for an unplanned Unit 2 outage that began on  
      The inspectors observed or reviewed the reactor shutdown and cooldown, outage
June 27, 2012, and continued through the end of the inspection period. The outage  
      equipment configuration and risk management, electrical lineups, selected clearances,
occurred as a result of a turbine control system malfunction that resulted in a turbine  
      control and monitoring of decay heat removal, control of containment activities,
load reject which terminated when the reactor operators inserted a manual reactor trip.
      personnel fatigue management, startup and heatup activities, and identification and
The inspectors reviewed activities to ensure that the licensee considered risk in  
      resolution of problems associated with the outage.
developing, planning, and implementing the outage schedule.  
      This inspection constituted one other partial outage sample as defined in
Inspection Scope
      IP 71111.20-05.
The inspectors observed or reviewed the reactor shutdown and cooldown, outage  
  b. Findings
equipment configuration and risk management, electrical lineups, selected clearances,  
      No findings were identified.
control and monitoring of decay heat removal, control of containment activities,  
1R22 Surveillance Testing (71111.22)
personnel fatigue management, startup and heatup activities, and identification and  
.Surveillance Testing
resolution of problems associated with the outage.  
  a. Inspection Scope
This inspection constituted one other partial outage sample as defined in  
      The inspectors reviewed the test results for the following activities to determine whether
IP 71111.20-05.  
      risk-significant systems and equipment were capable of performing their intended safety
b.  
      function, and to verify testing was conducted in accordance with applicable procedural
No findings were identified.  
      and TS requirements:
Findings
      *       PAB ventilation TS-87 system monthly test (routine);
1R22 Surveillance Testing
      *       TDAFW quarterly pump and valve test (Unit 1) (inservice testing);
.1
      *       instrument air valves quarterly SR (Unit 2) (containment isolation valve); and
(71111.22)  
      *       reactor coolant system (RCS) leak rate (Unit 2) (RCS).
a.  
      The inspectors observed in-plant activities and reviewed procedures and associated
Surveillance Testing  
      records to determine the following:
The inspectors reviewed the test results for the following activities to determine whether  
      *       did preconditioning occur;
risk-significant systems and equipment were capable of performing their intended safety  
      *       were the effects of the testing adequately addressed by control room personnel
function, and to verify testing was conducted in accordance with applicable procedural  
              or engineers prior to the commencement of the testing;
and TS requirements:  
                                              15                                      Enclosure
Inspection Scope
*  
PAB ventilation TS-87 system monthly test (routine);  
*  
TDAFW quarterly pump and valve test (Unit 1) (inservice testing);  
*  
instrument air valves quarterly SR (Unit 2) (containment isolation valve); and  
*  
reactor coolant system (RCS) leak rate (Unit 2) (RCS).  
The inspectors observed in-plant activities and reviewed procedures and associated  
records to determine the following:  
*  
did preconditioning occur;
*  
were the effects of the testing adequately addressed by control room personnel  
or engineers prior to the commencement of the testing;  


      *       were acceptance criteria clearly stated, demonstrated operational readiness, and
              consistent with the system design basis;
16
      *       plant equipment calibration was correct, accurate, and properly documented;
Enclosure
      *       as-left setpoints were within required ranges; and the calibration frequency was
*  
              in accordance with TSs, the FSAR, procedures, and applicable commitments;
were acceptance criteria clearly stated, demonstrated operational readiness, and  
      *       measuring and test equipment calibration was current;
consistent with the system design basis;  
      *       test equipment was used within the required range and accuracy; applicable
*  
              prerequisites described in the test procedures were satisfied;
plant equipment calibration was correct, accurate, and properly documented;  
      *       test frequencies met TS requirements to demonstrate operability and reliability;
*  
              tests were performed in accordance with the test procedures and other
as-left setpoints were within required ranges; and the calibration frequency was  
              applicable procedures; jumpers and lifted leads were controlled and restored
in accordance with TSs, the FSAR, procedures, and applicable commitments;  
              where used;
*  
      *       test data and results were accurate, complete, within limits, and valid;
measuring and test equipment calibration was current;  
      *       test equipment was removed after testing;
*  
      *       where applicable for inservice testing activities, testing was performed in
test equipment was used within the required range and accuracy; applicable  
              accordance with the applicable version of Section XI, American Society of
prerequisites described in the test procedures were satisfied;  
              Mechanical Engineers (ASME) code, and reference values were consistent with
*  
              the system design basis;
test frequencies met TS requirements to demonstrate operability and reliability;  
      *       where applicable, test results not meeting acceptance criteria were addressed
tests were performed in accordance with the test procedures and other  
              with an adequate operability evaluation or the SSC was declared inoperable;
applicable procedures; jumpers and lifted leads were controlled and restored  
      *       where applicable for SR instrument control surveillance tests, reference setting
where used;  
              data were accurately incorporated in the test procedure;
*  
      *       where applicable, actual conditions encountering high resistance electrical
test data and results were accurate, complete, within limits, and valid;  
              contacts were such that the intended safety function could still be accomplished;
*  
      *       prior procedure changes had not provided an opportunity to identify problems
test equipment was removed after testing;  
              encountered during the performance of the surveillance or calibration test;
*  
      *       equipment was returned to a position or status required to support the
where applicable for inservice testing activities, testing was performed in  
              performance of its safety functions; and
accordance with the applicable version of Section XI, American Society of  
      *       all problems identified during the testing were appropriately documented and
Mechanical Engineers (ASME) code, and reference values were consistent with  
              dispositioned in the CAP.
the system design basis;  
      Documents reviewed are listed in the Attachment to this report.
*  
      This inspection constituted one routine surveillance testing sample, one inservice testing
where applicable, test results not meeting acceptance criteria were addressed  
      sample, one reactor coolant system leak detection inspection sample, and one
with an adequate operability evaluation or the SSC was declared inoperable;  
      containment isolation valve sample as defined in IP 71111.22, Sections -02 and -05.
*  
  b. Findings
where applicable for SR instrument control surveillance tests, reference setting  
      No findings were identified.
data were accurately incorporated in the test procedure;  
      Cornerstone: Emergency Preparedness
*  
1EP6 Drill Evaluation (71114.06)
where applicable, actual conditions encountering high resistance electrical  
.Emergency Preparedness Observation
contacts were such that the intended safety function could still be accomplished;  
  a. Inspection Scope
*  
      The inspectors evaluated the response to a declaration of an alert condition on
prior procedure changes had not provided an opportunity to identify problems  
      April 25 to 26, 2012, to identify any weaknesses and deficiencies in classification,
encountered during the performance of the surveillance or calibration test;  
                                                16                                      Enclosure
*  
equipment was returned to a position or status required to support the  
performance of its safety functions; and  
*  
all problems identified during the testing were appropriately documented and  
dispositioned in the CAP.  
Documents reviewed are listed in the Attachment to this report.  
This inspection constituted one routine surveillance testing sample, one inservice testing  
sample, one reactor coolant system leak detection inspection sample, and one  
containment isolation valve sample as defined in IP 71111.22, Sections -02 and -05.  
b.  
No findings were identified.  
Findings
Cornerstone: Emergency Preparedness
1EP6 Drill Evaluation
.1
(71114.06)  
a.  
Emergency Preparedness Observation  
The inspectors evaluated the response to a declaration of an alert condition on  
April 25 to 26, 2012, to identify any weaknesses and deficiencies in classification,  
Inspection Scope


      notification, and protective action recommendation development activities. The licensee
      declared the alert after exhaust gasses from an EDG were inadvertently taken back into
17
      the EDG room during a test. The inspectors observed emergency response operations
Enclosure
      in the control room and technical support center (TSC) to determine whether the event
notification, and protective action recommendation development activities. The licensee  
      classification, notifications, and protective action recommendations were performed in
declared the alert after exhaust gasses from an EDG were inadvertently taken back into  
      accordance with procedures. No deficiencies were identified. Documents reviewed are
the EDG room during a test. The inspectors observed emergency response operations  
      listed in the Attachment to this report.
in the control room and technical support center (TSC) to determine whether the event  
      This inspection constituted one sample as defined in IP 71114.06-05.
classification, notifications, and protective action recommendations were performed in  
  b. Findings
accordance with procedures. No deficiencies were identified. Documents reviewed are  
      No findings were identified.
listed in the Attachment to this report.  
2.   RADIATION SAFETY
This inspection constituted one sample as defined in IP 71114.06-05.  
      Cornerstone: Occupational Radiation Safety
b.  
2RS3 In-Plant Airborne Radioactivity Control and Mitigation (71124.03)
No findings were identified.  
      This inspection constituted a partial sample as defined in IP 71124.03-05.
Findings
  .1   Engineering Controls (02.02)
2.  
  a. Inspection Scope
RADIATION SAFETY  
      An unresolved item (URI) was documented in NRC Integrated Inspection Report (IR)
Cornerstone: Occupational Radiation Safety  
      05000266/2012002; 05000301/2012002, concerning additional information that was
2RS3 In-Plant Airborne Radioactivity Control and Mitigation
      needed by the inspectors to assess the licensees TSC ventilation system filter testing
This inspection constituted a partial sample as defined in IP 71124.03-05.  
      program. Supplemental calculations and reviews were performed by the licensee, and
  (71124.03)
      the additional information was reviewed by the inspectors. Specifically, selected
.1  
      procedures, system design calculations, plant configuration drawings, and related
Engineering Controls
      licensee documentation were reviewed. The inspectors completed these reviews to
a.
      verify that the licensees program and its implementation met the requirements of
(02.02)  
      10 CFR 20.1701 and were consistent with NRC guidance.
An unresolved item (URI) was documented in NRC Integrated Inspection Report (IR)  
  b. Findings
05000266/2012002; 05000301/2012002, concerning additional information that was  
      Non-Compliance With 10 CFR 20.1701 to Control the Concentration of Radioactive
needed by the inspectors to assess the licensees TSC ventilation system filter testing  
      Material in Air and Ensure That Radiological Airborne Hazards Would Be Minimized in
program. Supplemental calculations and reviews were performed by the licensee, and  
      the Technical Support Center During a Design-Basis Accident
the additional information was reviewed by the inspectors. Specifically, selected  
      Introduction: The inspectors identified a finding of very low safety significance (Green)
procedures, system design calculations, plant configuration drawings, and related  
      and associated NCV of 10 CFR 20.1701, Use of Process or Other Engineering
licensee documentation were reviewed. The inspectors completed these reviews to  
      Controls. The inspectors identified that the licensee failed to establish adequate high
verify that the licensees program and its implementation met the requirements of  
      efficiency particulate air (HEPA) and charcoal filter testing procedures for ensuring that
10 CFR 20.1701 and were consistent with NRC guidance.  
      radiological airborne hazards would be minimized and the habitability of the TSC would
Inspection Scope
      be maintained under accident conditions. Specifically, the licensee failed to ensure
b.  
      engineering controls that were in place to minimize the concentration of radioactive
Findings  
      material in air in the TSC were maintained in accordance with the design bases.
Non-Compliance With 10 CFR 20.1701 to Control the Concentration of Radioactive  
                                                17                                    Enclosure
Material in Air and Ensure That Radiological Airborne Hazards Would Be Minimized in  
the Technical Support Center During a Design-Basis Accident  
Introduction: The inspectors identified a finding of very low safety significance (Green)  
and associated NCV of 10 CFR 20.1701, Use of Process or Other Engineering  
Controls. The inspectors identified that the licensee failed to establish adequate high  
efficiency particulate air (HEPA) and charcoal filter testing procedures for ensuring that  
radiological airborne hazards would be minimized and the habitability of the TSC would  
be maintained under accident conditions. Specifically, the licensee failed to ensure  
engineering controls that were in place to minimize the concentration of radioactive  
material in air in the TSC were maintained in accordance with the design bases.  


Description: The TSC is an onsite emergency response facility intended to support plant
operations under emergency conditions. The TSC ventilation system is designed to
18
remove radioactive material from the air, thereby minimizing the radioactive material
Enclosure
entering the TSC during postulated accident scenarios.
Description
The inspectors identified that, for an extended period of time, the licensee did not
The inspectors identified that, for an extended period of time, the licensee did not  
validate that the removal efficiencies in the TSC ventilation filter design bases were
validate that the removal efficiencies in the TSC ventilation filter design bases were  
being achieved. Specifically, testing of the TSC ventilation HEPA and charcoal filters did
being achieved. Specifically, testing of the TSC ventilation HEPA and charcoal filters did  
not demonstrate that filter performance was in compliance with the design criteria. The
not demonstrate that filter performance was in compliance with the design criteria. The  
design bases for the TSC ventilation system HEPA filter was 99 percent for particulate
design bases for the TSC ventilation system HEPA filter was 99 percent for particulate  
radioactive material removal efficiency. The licensees surveillance test acceptance
radioactive material removal efficiency. The licensees surveillance test acceptance  
criterion was95 percent. In addition, the design basis for the charcoal filter laboratory
criterion was95 percent. In addition, the design basis for the charcoal filter laboratory  
analysis was 95 percent removal efficiency of radioactive iodine. The surveillance test
analysis was 95 percent removal efficiency of radioactive iodine. The surveillance test  
required 80 percent. Consequently, there was no assurance that the installed TSC
required 80 percent. Consequently, there was no assurance that the installed TSC  
ventilation equipment would perform at its designed radioactive material removal
ventilation equipment would perform at its designed radioactive material removal  
capacity, thereby minimizing the radiological exposures to the occupants of the TSC
capacity, thereby minimizing the radiological exposures to the occupants of the TSC  
during postulated accidents.
during postulated accidents.  
Analysis: The inspectors determined that the failure to establish testing criteria in
: The TSC is an onsite emergency response facility intended to support plant
accordance with the system design bases was a performance deficiency consistent
operations under emergency conditions. The TSC ventilation system is designed to  
with IMC 0612, Power Reactor Inspection Reports. The inspectors determined that the
remove radioactive material from the air, thereby minimizing the radioactive material
licensee failed to meet the requirements of 10 CFR 20.1701 to use installed process
entering the TSC during postulated accident scenarios. 
equipment to reasonably minimize the level of airborne radioactive materials. The
Analysis
performance deficiency was reasonably within the licensees ability to foresee and
The inspectors reviewed IMC 0612, Appendix B, "Issue Screening," dated December 24,  
correct and was indicative of current performance, in that, the licensee had recent
2009, and found no similar examples. However, the inspectors determined that the  
opportunities to self-identify and correct the issue, including when performing recent
finding was more than minor because it was associated with the program and process  
technical reviews for NRC license amendment submittals for license renewal, alternate
attribute of exposure control of the occupational radiation safety cornerstone and  
source term, and extended power uprate.
adversely affected the cornerstone objective of ensuring the adequate protection of  
The inspectors reviewed IMC 0612, Appendix B, "Issue Screening," dated December 24,
worker health and safety from exposure radiation and radioactive material. Specifically,  
2009, and found no similar examples. However, the inspectors determined that the
by testing the installed emergency ventilation system filters to removal efficiencies less  
finding was more than minor because it was associated with the program and process
than their design criteria, the licensee did not validate that the TSC ventilation system  
attribute of exposure control of the occupational radiation safety cornerstone and
was capable of performing its design function and minimize worker exposures to  
adversely affected the cornerstone objective of ensuring the adequate protection of
airborne radioactive materials.  
worker health and safety from exposure radiation and radioactive material. Specifically,
:  The inspectors determined that the failure to establish testing criteria in
by testing the installed emergency ventilation system filters to removal efficiencies less
accordance with the system design bases was a performance deficiency consistent
than their design criteria, the licensee did not validate that the TSC ventilation system
with IMC 0612, Power Reactor Inspection Reports.  The inspectors determined that the
was capable of performing its design function and minimize worker exposures to
licensee failed to meet the requirements of 10 CFR 20.1701 to use installed process
airborne radioactive materials.
equipment to reasonably minimize the level of airborne radioactive materials.  The
The finding was assessed using IMC 0609, Appendix C, Occupational Radiation Safety
performance deficiency was reasonably within the licensees ability to foresee and
Significance Determination Process, (SDP) and was determined to be of very low safety
correct and was indicative of current performance, in that, the licensee had recent
significance (Green) because it was not an as-low-as-is-reasonably-achievable (ALARA)
opportunities to self-identify and correct the issue, including when performing recent
planning issue, there was no overexposure or potential for overexposure, and the
technical reviews for NRC license amendment submittals for license renewal, alternate
licensees ability to assess dose was not compromised. The licensee documented this
source term, and extended power uprate. 
issue in its corrective action program. Corrective actions included revising applicable
The finding was assessed using IMC 0609, Appendix C, Occupational Radiation Safety  
procedures and based on actual historical filter testing efficiencies, calculating that the
Significance Determination Process, (SDP) and was determined to be of very low safety  
TSC ventilation system was capable of maintaining a radiological habitability of less than
significance (Green) because it was not an as-low-as-is-reasonably-achievable (ALARA)  
5 Rem total effective dose equivalent (TEDE) for the duration of the design-basis
planning issue, there was no overexposure or potential for overexposure, and the  
accidents.
licensees ability to assess dose was not compromised. The licensee documented this  
                                          18                                        Enclosure
issue in its corrective action program. Corrective actions included revising applicable  
procedures and based on actual historical filter testing efficiencies, calculating that the  
TSC ventilation system was capable of maintaining a radiological habitability of less than  
5 Rem total effective dose equivalent (TEDE) for the duration of the design-basis  
accidents.  


      The inspectors identified that the most significant contributor to the finding was a
      cross-cutting aspect in the area of human performance, resources. Specifically, the
19
      licensee failed to ensure that the TSC ventilation filter testing protocol assured
Enclosure
      compliance to the systems designed margins in that the TSC ventilation filter testing
The inspectors identified that the most significant contributor to the finding was a  
      acceptance criteria were established independent of the system design requirements
cross-cutting aspect in the area of human performance, resources. Specifically, the  
      (H.2(a)).
licensee failed to ensure that the TSC ventilation filter testing protocol assured  
      Enforcement: Title 10 CFR 20.1701 requires that licensees use, to the extent practical,
compliance to the systems designed margins in that the TSC ventilation filter testing  
      process or other engineering controls (e.g., containment, decontamination, or ventilation)
acceptance criteria were established independent of the system design requirements  
      to control the concentration of radioactive material in air. Contrary to the above, as of
(H.2(a)).  
      January 19, 2012, the licensee failed to ensure that effective engineering controls were
Enforcement
      implemented to control the concentration of radioactive material in air in the TSC in
4.
      accordance with the facilitys design bases. Because the issue was of very low safety
OTHER ACTIVITIES
      significance and has been entered into the licensees CAP (as CR01752498), the
: Title 10 CFR 20.1701 requires that licensees use, to the extent practical,  
      violation is being treated as an NCV consistent with Section 2.3.2 of the NRC
process or other engineering controls (e.g., containment, decontamination, or ventilation)  
      Enforcement Policy (NCV 05000266/2012003-02; 05000301/2012003-02;
to control the concentration of radioactive material in air. Contrary to the above, as of  
      Non-Compliance With 10 CFR 20.1701 to Control the Concentration of Radioactive
January 19, 2012, the licensee failed to ensure that effective engineering controls were  
      Material in Air and Ensure that Radiological Airborne Hazards Would Be Minimized in
implemented to control the concentration of radioactive material in air in the TSC in  
      the Technical Support Center During a Design-Basis Accident). This NCV closes
accordance with the facilitys design bases. Because the issue was of very low safety  
      URI 05000266/2012002-05; 05000301/2012002-05, TSC Filter Testing May Be
significance and has been entered into the licensees CAP (as CR01752498), the  
      Inadequate," in Section 4OA5.2.
violation is being treated as an NCV consistent with Section 2.3.2 of the NRC  
4.    OTHER ACTIVITIES
Enforcement Policy (NCV 05000266/2012003-02; 05000301/2012003-02;  
      Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency
Non-Compliance With 10 CFR 20.1701 to Control the Concentration of Radioactive  
      Preparedness, Public Radiation Safety, Occupational Radiation Safety, and
Material in Air and Ensure that Radiological Airborne Hazards Would Be Minimized in  
      Physical Protection
the Technical Support Center During a Design-Basis Accident). This NCV closes  
4OA1 Performance Indicator Verification (71151)
URI 05000266/2012002-05; 05000301/2012002-05, TSC Filter Testing May Be  
.Unplanned Scrams with Complications
Inadequate," in Section 4OA5.2.  
  a. Inspection Scope
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency  
      The inspectors sampled licensee submittals for the Unplanned Scrams with
Preparedness, Public Radiation Safety, Occupational Radiation Safety, and  
      Complications performance indicator (PI) for Units 1 and 2, for the third quarter 2011
Physical Protection  
      through the second quarter 2012. To determine the accuracy of the PI data reported, PI
4OA1 Performance Indicator Verification
      definitions and guidance contained in the Nuclear Energy Institute (NEI) Document
.1
      99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6, dated
(71151)  
      October 2009, were used. The inspectors reviewed the licensees operator narrative
a.  
      logs, CRs, event reports, and NRC integrated IRs to validate the accuracy of the
Unplanned Scrams with Complications  
      submittals. The inspectors also reviewed the licensees CAP to determine if any
The inspectors sampled licensee submittals for the Unplanned Scrams with  
      problems had been identified with the PI data collected or transmitted for this indicator
Complications performance indicator (PI) for Units 1 and 2, for the third quarter 2011  
      and none were identified. Documents reviewed are listed in the Attachment to this
through the second quarter 2012. To determine the accuracy of the PI data reported, PI  
      report.
definitions and guidance contained in the Nuclear Energy Institute (NEI) Document  
      This inspection constituted two unplanned scrams with complications samples as
99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6, dated  
      defined in IP 71151-05.
October 2009, were used. The inspectors reviewed the licensees operator narrative  
  b. Findings
logs, CRs, event reports, and NRC integrated IRs to validate the accuracy of the  
      No findings were identified.
submittals. The inspectors also reviewed the licensees CAP to determine if any  
                                              19                                        Enclosure
problems had been identified with the PI data collected or transmitted for this indicator  
and none were identified. Documents reviewed are listed in the Attachment to this  
report.  
Inspection Scope
This inspection constituted two unplanned scrams with complications samples as  
defined in IP 71151-05.  
b.  
No findings were identified.  
Findings


.2   Reactor Coolant System Leakage
  a.  Inspection Scope
20
      The inspectors sampled licensee submittals for the RCS Leakage PI for Units 1 and 2,
Enclosure
      for the third quarter 2011 through the second quarter 2012. To determine the accuracy
.2  
      of the PI data reported, PI definitions and guidance contained in the NEI
a.
      Document 99-02, Regulatory Assessment Performance Indicator Guideline,
Reactor Coolant System Leakage  
      Revision 6, dated October 2009, were used. The inspectors reviewed the licensees
The inspectors sampled licensee submittals for the RCS Leakage PI for Units 1 and 2,  
      operator logs, RCS leakage tracking data, CRs, event reports, and NRC integrated IRs
for the third quarter 2011 through the second quarter 2012. To determine the accuracy  
      to validate the accuracy of the submittals. The inspectors also reviewed the licensees
of the PI data reported, PI definitions and guidance contained in the NEI  
      CAP to determine if any problems had been identified with the PI data collected or
Document 99-02, Regulatory Assessment Performance Indicator Guideline,  
      transmitted for this indicator and none were identified. Documents reviewed are listed in
Revision 6, dated October 2009, were used. The inspectors reviewed the licensees  
      the Attachment to this report.
operator logs, RCS leakage tracking data, CRs, event reports, and NRC integrated IRs  
      This inspection constituted two reactor coolant system leakage samples as defined in
to validate the accuracy of the submittals. The inspectors also reviewed the licensees  
      IP 71151-05.
CAP to determine if any problems had been identified with the PI data collected or  
  b. Findings
transmitted for this indicator and none were identified. Documents reviewed are listed in  
      No findings were identified.
the Attachment to this report.  
.3   Reactor Coolant System Specific Activity
Inspection Scope
  a. Inspection Scope
This inspection constituted two reactor coolant system leakage samples as defined in  
      In the first quarter of 2012, the inspectors sampled licensee submittals for the RCS
IP 71151-05.  
      specific activity PI for Units 1 and 2 for the fourth quarter 2010 through the fourth quarter
b.  
      2011. The inspectors used PI definitions and guidance contained in the
No findings were identified.  
      NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline,
Findings
      Revision 6, dated October 2009, to determine the accuracy of the PI data reported. The
.3  
      inspectors reviewed the licensees RCS chemistry samples, TS requirements, CRs,
a.
      event reports, and NRC integrated IRs to validate the accuracy of the submittals. The
Reactor Coolant System Specific Activity  
      inspectors also reviewed the licensees CAP to determine if any problems had been
In the first quarter of 2012, the inspectors sampled licensee submittals for the RCS  
      identified with the PI data collected or transmitted for this indicator and none were
specific activity PI for Units 1 and 2 for the fourth quarter 2010 through the fourth quarter  
      identified. In addition to record reviews, the inspectors observed a chemistry technician
2011. The inspectors used PI definitions and guidance contained in the  
      obtain and analyze an RCS sample. Documents reviewed are listed in the Attachment
NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline,  
      to this report.
Revision 6, dated October 2009, to determine the accuracy of the PI data reported. The  
      This inspection constituted two reactor coolant system specific activity samples as
inspectors reviewed the licensees RCS chemistry samples, TS requirements, CRs,  
      defined in IP 71151-05.
event reports, and NRC integrated IRs to validate the accuracy of the submittals. The  
  b. Findings
inspectors also reviewed the licensees CAP to determine if any problems had been  
      No findings were identified.
identified with the PI data collected or transmitted for this indicator and none were  
                                                  20                                    Enclosure
identified. In addition to record reviews, the inspectors observed a chemistry technician  
obtain and analyze an RCS sample. Documents reviewed are listed in the Attachment  
to this report.  
Inspection Scope
This inspection constituted two reactor coolant system specific activity samples as  
defined in IP 71151-05.  
b.  
No findings were identified.  
Findings


.4   Occupational Exposure Control Effectiveness
  a. Inspection Scope
21
      In the first quarter of 2012, the inspectors sampled licensee submittals for the
Enclosure
      occupational radiological occurrences PI for the fourth quarter 2010 through the fourth
.4  
      quarter 2011. The inspectors used PI definitions and guidance contained in the NEI
a.
      Document 99-02, Regulatory Assessment Performance Indicator Guideline,
Occupational Exposure Control Effectiveness  
      Revision 6, dated October 2009, to determine the accuracy of the PI data reported. The
In the first quarter of 2012, the inspectors sampled licensee submittals for the  
      inspectors reviewed the licensees assessment of the PI for occupational radiation safety
occupational radiological occurrences PI for the fourth quarter 2010 through the fourth  
      to determine if indicator related data was adequately assessed and reported. To assess
quarter 2011. The inspectors used PI definitions and guidance contained in the NEI  
      the adequacy of the licensees PI data collection and analyses, the inspectors discussed
Document 99-02, Regulatory Assessment Performance Indicator Guideline,  
      with radiation protection staff, the scope and breadth of its data review and the results of
Revision 6, dated October 2009, to determine the accuracy of the PI data reported. The  
      those reviews. The inspectors independently reviewed electronic personal dosimetry
inspectors reviewed the licensees assessment of the PI for occupational radiation safety  
      dose rate and accumulated dose alarms and dose reports and the dose assignments for
to determine if indicator related data was adequately assessed and reported. To assess  
      any intakes that occurred during the time period reviewed to determine if there were
the adequacy of the licensees PI data collection and analyses, the inspectors discussed  
      potentially unrecognized occurrences. The inspectors also conducted walkdowns of
with radiation protection staff, the scope and breadth of its data review and the results of  
      numerous locked high and very-high radiation area entrances to determine the
those reviews. The inspectors independently reviewed electronic personal dosimetry  
      adequacy of the controls in place for these areas. Documents reviewed are listed in the
dose rate and accumulated dose alarms and dose reports and the dose assignments for  
      Attachment to this report.
any intakes that occurred during the time period reviewed to determine if there were  
      This inspection constituted one occupational exposure control effectiveness sample as
potentially unrecognized occurrences. The inspectors also conducted walkdowns of  
      defined in IP 71151-05.
numerous locked high and very-high radiation area entrances to determine the  
  b. Findings
adequacy of the controls in place for these areas. Documents reviewed are listed in the  
      No findings were identified.
Attachment to this report.  
.5   Radiological Effluent Technical Specification/Offsite Dose Calculation Manual
Inspection Scope
      Radiological Effluent Occurrences
This inspection constituted one occupational exposure control effectiveness sample as  
  a. Inspection Scope
defined in IP 71151-05.  
      In the first quarter of 2012, the inspectors sampled licensee submittals for the
b.  
      radiological effluent Technical Specification/Offsite Dose Calculation Manual radiological
No findings were identified.  
      effluent occurrences PI for the fourth quarter 2010 through the fourth quarter 2011. The
Findings
      inspectors used PI definitions and guidance contained in the NEI Document 99-02,
.5  
      Regulatory Assessment Performance Indicator Guideline, Revision 6, dated
a.
      October 2009, to determine the accuracy of the PI data reported. The inspectors
Radiological Effluent Technical Specification/Offsite Dose Calculation Manual  
      reviewed the licensees CAP and selected individual reports generated since this
Radiological Effluent Occurrences  
      indicator was last reviewed to identify any potential occurrences such as unmonitored,
In the first quarter of 2012, the inspectors sampled licensee submittals for the  
      uncontrolled, or improperly calculated effluent releases that may have impacted offsite
radiological effluent Technical Specification/Offsite Dose Calculation Manual radiological  
      dose. The inspectors reviewed gaseous effluent summary data and the results of
effluent occurrences PI for the fourth quarter 2010 through the fourth quarter 2011. The  
      associated offsite dose calculations for selected dates to determine if indicator results
inspectors used PI definitions and guidance contained in the NEI Document 99-02,  
      were accurately reported. The inspectors also reviewed the licensees methods for
Regulatory Assessment Performance Indicator Guideline, Revision 6, dated  
      quantifying gaseous and liquid effluents and determining effluent dose. Documents
October 2009, to determine the accuracy of the PI data reported. The inspectors  
      reviewed are listed in the Attachment to this report.
reviewed the licensees CAP and selected individual reports generated since this  
      This inspection constituted one Radiological Effluent Technical Specification/Offsite
indicator was last reviewed to identify any potential occurrences such as unmonitored,  
      Dose Calculation Manual radiological effluent occurrences sample as defined in
uncontrolled, or improperly calculated effluent releases that may have impacted offsite  
      IP 71151-05.
dose. The inspectors reviewed gaseous effluent summary data and the results of  
                                                21                                      Enclosure
associated offsite dose calculations for selected dates to determine if indicator results  
were accurately reported. The inspectors also reviewed the licensees methods for  
quantifying gaseous and liquid effluents and determining effluent dose. Documents  
reviewed are listed in the Attachment to this report.  
Inspection Scope
This inspection constituted one Radiological Effluent Technical Specification/Offsite  
Dose Calculation Manual radiological effluent occurrences sample as defined in  
IP 71151-05.  


  b. Findings
      No findings were identified.
22
4OA2 Identification and Resolution of Problems (71152)
Enclosure
.Routine Review of Items Entered into the Corrective Action Program
b.  
  a. Inspection Scope
No findings were identified.  
      As part of the various baseline inspection procedures discussed in previous sections of
Findings
      this report, the inspectors routinely reviewed issues during baseline inspection activities
4OA2 Identification and Resolution of Problems
      and plant status reviews to verify that they were being entered into the licensees CAP at
.1
      an appropriate threshold, that adequate attention was being given to timely corrective
(71152)  
      actions, and that adverse trends were identified and addressed. Attributes reviewed
a.  
      included: identification of the problem was complete and accurate; timeliness was
Routine Review of Items Entered into the Corrective Action Program  
      commensurate with the safety significance; evaluation and disposition of performance
As part of the various baseline inspection procedures discussed in previous sections of  
      issues, generic implications, common causes, contributing factors, root causes,
this report, the inspectors routinely reviewed issues during baseline inspection activities  
      extent-of-condition reviews, and previous occurrences reviews were proper and
and plant status reviews to verify that they were being entered into the licensees CAP at  
      adequate; and that the classification, prioritization, focus, and timeliness of corrective
an appropriate threshold, that adequate attention was being given to timely corrective  
      actions were commensurate with safety and sufficient to prevent recurrence of the issue.
actions, and that adverse trends were identified and addressed. Attributes reviewed  
      Minor issues entered into the licensees CAP as a result of the inspectors observations
included: identification of the problem was complete and accurate; timeliness was  
      are included in the Attachment to this report.
commensurate with the safety significance; evaluation and disposition of performance  
      These routine reviews for the identification and resolution of problems did not constitute
issues, generic implications, common causes, contributing factors, root causes,  
      any additional inspection samples. Instead, by procedure they were considered an
extent-of-condition reviews, and previous occurrences reviews were proper and  
      integral part of the inspections performed during the quarter and documented in
adequate; and that the classification, prioritization, focus, and timeliness of corrective  
      Section 1 of this report.
actions were commensurate with safety and sufficient to prevent recurrence of the issue.
  b. Findings
Minor issues entered into the licensees CAP as a result of the inspectors observations  
      No findings were identified.
are included in the Attachment to this report.  
.2   Daily Corrective Action Program Reviews
Inspection Scope
  a. Inspection Scope
These routine reviews for the identification and resolution of problems did not constitute  
      In order to assist with the identification of repetitive equipment failures and specific
any additional inspection samples. Instead, by procedure they were considered an  
      human performance issues for follow-up, the inspectors performed a daily screening of
integral part of the inspections performed during the quarter and documented in  
      items entered into the licensees CAP. This review was accomplished through
Section 1 of this report.  
      inspection of the stations daily condition report packages.
b.  
      These daily reviews were performed by procedure as part of the inspectors daily plant
No findings were identified.  
      status monitoring activities and, as such, did not constitute any separate inspection
Findings
      samples.
.2  
  b. Findings
a.
      No findings were identified.
Daily Corrective Action Program Reviews  
                                                22                                      Enclosure
In order to assist with the identification of repetitive equipment failures and specific  
human performance issues for follow-up, the inspectors performed a daily screening of  
items entered into the licensees CAP. This review was accomplished through  
inspection of the stations daily condition report packages.  
Inspection Scope
These daily reviews were performed by procedure as part of the inspectors daily plant  
status monitoring activities and, as such, did not constitute any separate inspection  
samples.  
b.  
No findings were identified.  
Findings


.3   Annual Sample: Review of Operator Workarounds
  a. Inspection Scope
23
    The inspectors evaluated the licensees implementation of the process used to identify,
Enclosure
    document, track, and resolve operational challenges. Inspection activities included, but
.3  
    were not limited to, a review of the cumulative effects of the operator workarounds
a.
    (OWAs) on system availability and the potential for improper operation of the system, for
Annual Sample: Review of Operator Workarounds  
    potential impacts on multiple systems, and on the ability of operators to respond to plant
The inspectors evaluated the licensees implementation of the process used to identify,  
    transients or accidents.
document, track, and resolve operational challenges. Inspection activities included, but  
    The inspectors performed a review of the cumulative effects of OWAs. The documents
were not limited to, a review of the cumulative effects of the operator workarounds  
    listed in the Attachment to this report were reviewed to accomplish the objectives of the
(OWAs) on system availability and the potential for improper operation of the system, for  
    inspection procedure. The inspectors reviewed both current and historical operational
potential impacts on multiple systems, and on the ability of operators to respond to plant  
    challenge records to determine whether the licensee was identifying operator challenges
transients or accidents.  
    at an appropriate threshold, had entered them into the CAP, and proposed or
Inspection Scope
    implemented appropriate and timely corrective actions which addressed each issue.
The inspectors performed a review of the cumulative effects of OWAs. The documents  
    Reviews were conducted to determine if any operator challenge could increase the
listed in the Attachment to this report were reviewed to accomplish the objectives of the  
    possibility of an Initiating Event, if the challenge was contrary to training, required a
inspection procedure. The inspectors reviewed both current and historical operational  
    change from long-standing operational practices, or created the potential for
challenge records to determine whether the licensee was identifying operator challenges  
    inappropriate compensatory actions. Additionally, all temporary modifications were
at an appropriate threshold, had entered them into the CAP, and proposed or  
    reviewed to identify any potential effect on the functionality of Mitigating Systems,
implemented appropriate and timely corrective actions which addressed each issue.
    impaired access to equipment, or required equipment uses for which the equipment was
Reviews were conducted to determine if any operator challenge could increase the  
    not designed. Daily plant and equipment status logs, degraded instrument logs, and
possibility of an Initiating Event, if the challenge was contrary to training, required a  
    operator aids or tools being used to compensate for material deficiencies were also
change from long-standing operational practices, or created the potential for  
    assessed to identify any potential sources of unidentified OWAs.
inappropriate compensatory actions. Additionally, all temporary modifications were  
    This review constituted one operator workaround annual inspection sample as defined in
reviewed to identify any potential effect on the functionality of Mitigating Systems,  
    IP 71152-05.
impaired access to equipment, or required equipment uses for which the equipment was  
  b. Findings
not designed. Daily plant and equipment status logs, degraded instrument logs, and  
    No findings were identified.
operator aids or tools being used to compensate for material deficiencies were also  
.4   Selected Issue Follow-Up Inspection: Partial Turnover of Extended Power Uprate
assessed to identify any potential sources of unidentified OWAs.  
    Modifications
This review constituted one operator workaround annual inspection sample as defined in  
  a. Inspection Scope
IP 71152-05.  
    The inspectors reviewed items entered in the licensees CAP and identified various
b.  
    corrective action item reports identifying problems with the modification turnover process
No findings were identified.  
    of extended power uprate (EPU) modifications installed during recent refueling outages.
Findings
    The inspectors elected to review this practice as a selected issue follow-up item.
.4  
    This review constituted the completion of one in-depth problem identification and
a.
    resolution sample as defined in IP 71152-05, completing the partial sample referenced
Selected Issue Follow-Up Inspection: Partial Turnover of Extended Power Uprate  
    previously in integrated IR 05000266/2012002; 05000301/2012002.
Modifications  
  b. Findings
The inspectors reviewed items entered in the licensees CAP and identified various  
    Partial Turnover of Extended Power Uprate Modifications
corrective action item reports identifying problems with the modification turnover process  
                                                23                                      Enclosure
of extended power uprate (EPU) modifications installed during recent refueling outages.
The inspectors elected to review this practice as a selected issue follow-up item.  
Inspection Scope
This review constituted the completion of one in-depth problem identification and  
resolution sample as defined in IP 71152-05, completing the partial sample referenced  
previously in integrated IR 05000266/2012002; 05000301/2012002.  
b.  
Findings  
Partial Turnover of Extended Power Uprate Modifications  


    Introduction: During the inspectors review of the licensees partial turnover process, the
    inspectors identified a URI associated with the process.
24
    Description: The inspectors selected the licensees partial turnover process as a
Enclosure
    selected issue follow-up due to the potential inadequacies associated with the process.
Introduction: During the inspectors review of the licensees partial turnover process, the  
    As previously identified in IRs 05000266/2011008; 05000301/2011008, and
inspectors identified a URI associated with the process.  
    05000266/2012002; 05000301/2012002, the inspectors identified problems and
Description
    violations associated with the licensees partial turnover process where systems had
During the second quarter, the inspectors received portions of the requested
    been partially turned over and declared operable, and it was later discovered that
documentation.  The issue is unresolved pending review of the portions of the previously
    portions of the modification were not tested prior to being placed in-service. With the
requested documentation (URI 05000266/2012003-03; 05000301/2012003-03, Partial
    additional identification of problems associated with the partial turnover process
Turnover of Extended Power Uprate Modifications).
    referenced in CRs in Integrated IRs 05000266/2012002; 05000301/2012002, the
: The inspectors selected the licensees partial turnover process as a  
    inspectors were concerned that additional systems may be subject to similar issues as a
selected issue follow-up due to the potential inadequacies associated with the process.
    result of the partial turnover process. At the completion of the first quarter inspection
As previously identified in IRs 05000266/2011008; 05000301/2011008, and  
    period, the inspectors were awaiting the requested documentation from the licensee to
05000266/2012002; 05000301/2012002, the inspectors identified problems and  
    complete their review of this issue.
violations associated with the licensees partial turnover process where systems had  
    During the second quarter, the inspectors received portions of the requested
been partially turned over and declared operable, and it was later discovered that  
    documentation. The issue is unresolved pending review of the portions of the previously
portions of the modification were not tested prior to being placed in-service. With the  
    requested documentation (URI 05000266/2012003-03; 05000301/2012003-03, Partial
additional identification of problems associated with the partial turnover process  
    Turnover of Extended Power Uprate Modifications).
referenced in CRs in Integrated IRs 05000266/2012002; 05000301/2012002, the  
.5  Selected Issue Follow-Up Inspection: Licensed Operator Respirator Qualifications And
inspectors were concerned that additional systems may be subject to similar issues as a  
    Control Room Staffing
result of the partial turnover process. At the completion of the first quarter inspection  
  a. Inspection Scope
period, the inspectors were awaiting the requested documentation from the licensee to  
    During a review of items entered in the licensees CAP, the inspectors found recent
complete their review of this issue.  
    corrective action items documenting repetitive occurrences associated the licensed
.5
    operator respirator qualifications. These CRs related to AR01670172 which
a.  
    documented a condition where shift staffing was challenged due to having expired
Selected Issue Follow-Up Inspection: Licensed Operator Respirator Qualifications And  
    licensed operator respirator qualifications. The inspectors questioned the licensees
Control Room Staffing  
    evaluation of the CR regarding the conclusions reached. Specifically, the inspectors
During a review of items entered in the licensees CAP, the inspectors found recent  
    noted that the individual was credited with watch-standing during the period of expired
corrective action items documenting repetitive occurrences associated the licensed  
    qualifications and that the procedures for the annual requirements conflicted. The
operator respirator qualifications. These CRs related to AR01670172 which  
    licensee entered the inspectors concerns in the CAP as AR01747333 and AR1772196.
documented a condition where shift staffing was challenged due to having expired  
    The licensee was able to demonstrate through timed entries and door logs that control
licensed operator respirator qualifications. The inspectors questioned the licensees  
    room staffing was not compromised due to the expired respirator qualification.
evaluation of the CR regarding the conclusions reached. Specifically, the inspectors  
    Additionally, the licensees corrective actions created a report to track licensed operator
noted that the individual was credited with watch-standing during the period of expired  
    respirator qualifications as well as initiated a procedure change requests to more clearly
qualifications and that the procedures for the annual requirements conflicted. The  
    document licensed operator watch-standing requirements and clarify the definitions for
licensee entered the inspectors concerns in the CAP as AR01747333 and AR1772196.
    annual requirements.
The licensee was able to demonstrate through timed entries and door logs that control  
    This review constituted one in-depth problem identification and resolution sample as
room staffing was not compromised due to the expired respirator qualification.
    defined in IP 71152-05.
Additionally, the licensees corrective actions created a report to track licensed operator  
  b. Findings
respirator qualifications as well as initiated a procedure change requests to more clearly  
    No findings were identified.
document licensed operator watch-standing requirements and clarify the definitions for  
                                                24                                      Enclosure
annual requirements.  
Inspection Scope
This review constituted one in-depth problem identification and resolution sample as  
defined in IP 71152-05.  
b.  
No findings were identified.  
Findings


4OA3 Follow-Up of Events and Notices of Enforcement Discretion (71153)
.Unit 2 Planned Downpower to Repair Switchyard Hotspot
25
  a. Inspection Scope
Enclosure
      The inspectors reviewed the plants response to a planned downpower on Unit 2. Unit 2
4OA3 Follow-Up of Events and Notices of Enforcement Discretion
      was taken offline while remaining critical on April 21, 2012, to allow repair of two hot
.1
      spots on two phases of a disconnect switch in the switchyard. The repairs were
(71153)  
      successful and the unit was placed back online on April 22, 2012. Documents reviewed
a.  
      are listed in the Attachment to this report.
Unit 2 Planned Downpower to Repair Switchyard Hotspot  
      This event follow-up review constituted one sample as defined in IP 71153-05.
The inspectors reviewed the plants response to a planned downpower on Unit 2. Unit 2  
  b. Findings
was taken offline while remaining critical on April 21, 2012, to allow repair of two hot  
      No findings were identified.
spots on two phases of a disconnect switch in the switchyard. The repairs were  
.2   Alert Declared Due To Toxic Gas
successful and the unit was placed back online on April 22, 2012. Documents reviewed  
  a. Inspection Scope
are listed in the Attachment to this report.  
      The inspectors reviewed the plants response to an Alert on April 25 to 26, 2012, that
Inspection Scope 
      was declared during a special maintenance run of the G-02 EDG. During the EDG run,
This event follow-up review constituted one sample as defined in IP 71153-05.  
      exhaust fumes entered the adjacent air compressor room, a vital area, and the levels of
b.  
      toxic gas from these fumes exceeded Occupational Safety and Health Administration
No findings were identified.  
      (OSHA) limits. The EDG was immediately secured and the room ventilated. The
Findings
      licensee corrected the system configuration problem that caused the inleakage and re-
.2  
      performed the run. Documents reviewed are listed in the Attachment to this report.
a.
      This event follow-up review constituted one sample as defined in IP 71153-05.
Alert Declared Due To Toxic Gas  
  b. Findings
The inspectors reviewed the plants response to an Alert on April 25 to 26, 2012, that  
      No findings were identified.
was declared during a special maintenance run of the G-02 EDG. During the EDG run,  
.3   Failure of Turbine-Driven Auxiliary Feedwater Pump Coupling
exhaust fumes entered the adjacent air compressor room, a vital area, and the levels of  
  a. Inspection Scope
toxic gas from these fumes exceeded Occupational Safety and Health Administration  
      On May 21, 2012, the inspectors reviewed the plants response to the failure of the
(OSHA) limits. The EDG was immediately secured and the room ventilated. The  
      Unit 1 TDAFW pump coupling and related unplanned entry into a 72-hour limiting
licensee corrected the system configuration problem that caused the inleakage and re-
      condition for operation action statement. The inspectors reviewed the repair and other
performed the run. Documents reviewed are listed in the Attachment to this report.  
      activities the licensee performed to be able to return the pump to service within the
Inspection Scope 
      allowed completion time. Documents reviewed are listed in the Attachment to this
This event follow-up review constituted one sample as defined in IP 71153-05.  
      report.
b.  
      This event follow-up review constituted one sample defined in IP 71153-05.
No findings were identified.  
  b. Findings
Findings
      No findings were identified.
.3  
                                              25                                        Enclosure
a.
Failure of Turbine-Driven Auxiliary Feedwater Pump Coupling  
On May 21, 2012, the inspectors reviewed the plants response to the failure of the  
Unit 1 TDAFW pump coupling and related unplanned entry into a 72-hour limiting  
condition for operation action statement. The inspectors reviewed the repair and other  
activities the licensee performed to be able to return the pump to service within the  
allowed completion time. Documents reviewed are listed in the Attachment to this  
report.  
Inspection Scope 
This event follow-up review constituted one sample defined in IP 71153-05.  
b.  
No findings were identified.  
Findings


.4 (Closed) Licensee Event Reports (LERs) 05000301/2011-004-00 and
  05000301/2011-004-01, Automatic Reactor Trip During Startup Physics Testing Due to
26
  Source Range
Enclosure
  Introduction: A Green NCV of 10 CFR 50.65(a)(3) was self-revealed when an
.4  
  unplanned reactor trip occurred as a result of the failure of a source range detector
(Closed) Licensee Event Reports (LERs) 05000301/2011-004-00 and  
  during low power physics testing. Specifically, the licensee failed to adequately evaluate
05000301/2011-004-01, Automatic Reactor Trip During Startup Physics Testing Due to  
  operating experience and incorporate it into preventive maintenance programs to
Source Range  
  periodically replace aging electrical subcomponents in nuclear instrumentation systems
Introduction: A Green NCV of 10 CFR 50.65(a)(3) was self-revealed when an  
  and a subsequent age-related failure resulted in initiating a plant transient.
unplanned reactor trip occurred as a result of the failure of a source range detector  
  Description: On June 13, 2011, during the performance of beginning of life (BOL) low
during low power physics testing. Specifically, the licensee failed to adequately evaluate  
  power physics testing, and with reactor power decreasing due to inserting reactor control
operating experience and incorporate it into preventive maintenance programs to  
  rods to obtain test data, power decreased below the setpoint that actuates and
periodically replace aging electrical subcomponents in nuclear instrumentation systems  
  automatically places source range monitoring (SRM) instrumentation in service. When
and a subsequent age-related failure resulted in initiating a plant transient.  
  SRMs were actuated, channel 2N31 experienced a failure of the associated high voltage
Description
  power supply. This failure satisfied the SRM high flux reactor trip logic and resulted in
Subsequent review by the licensee determined that the failure was due to age-related
  an automatic reactor trip.
degradation and that the most likely cause of the failure was because the output filter
  Subsequent review by the licensee determined that the failure was due to age-related
capacitors were degraded.  The licensee indicated that the recent failures were
  degradation and that the most likely cause of the failure was because the output filter
experienced on power supplies manufactured in the 1970s, and that the date codes on
  capacitors were degraded. The licensee indicated that the recent failures were
the capacitors in the subject units was also from the 1970s.  Additionally, the licensee
  experienced on power supplies manufactured in the 1970s, and that the date codes on
noted that many of the components used in the construction of the related units were
  the capacitors in the subject units was also from the 1970s. Additionally, the licensee
40 years old.
  noted that many of the components used in the construction of the related units were
: On June 13, 2011, during the performance of beginning of life (BOL) low  
  40 years old.
power physics testing, and with reactor power decreasing due to inserting reactor control  
  The licensees root cause analysis identified historical operating experience as early as
rods to obtain test data, power decreased below the setpoint that actuates and  
  1992, which reflected the need to periodically repair or replace power supplies; and that
automatically places source range monitoring (SRM) instrumentation in service. When  
  in 1998, Westinghouse provided a recommendation to replace power supplies; or at a
SRMs were actuated, channel 2N31 experienced a failure of the associated high voltage  
  minimum, replace filtering capacitors every 10 years. In 1998, the licensee made a
power supply. This failure satisfied the SRM high flux reactor trip logic and resulted in  
  decision not to incorporate the vendor recommendations into the preventive
an automatic reactor trip.  
  maintenance program.
The licensees root cause analysis identified historical operating experience as early as  
  The licensee concluded that the root cause could be attributed to life cycle management
1992, which reflected the need to periodically repair or replace power supplies; and that  
  and preventive maintenance program deficiencies. The corrective action to prevent
in 1998, Westinghouse provided a recommendation to replace power supplies; or at a  
  recurrence was related to the life cycle management plan for the nuclear instruments.
minimum, replace filtering capacitors every 10 years. In 1998, the licensee made a  
  The inspectors considered that this action was adequate to address concerns related to
decision not to incorporate the vendor recommendations into the preventive  
  the nuclear instruments. The inspectors reviewed the issue with the licensee with
maintenance program.  
  respect to subcomponent aging management. The licensee had indicated that
The licensee concluded that the root cause could be attributed to life cycle management  
  subsequent to this event and industry reviews, it had expanded the subcomponent aging
and preventive maintenance program deficiencies. The corrective action to prevent  
  management program. The licensee provided evidence which demonstrated that a
recurrence was related to the life cycle management plan for the nuclear instruments.
  program for subcomponent aging and management was in the final stage of
The inspectors considered that this action was adequate to address concerns related to  
  development, and that the program was reviewing several categories of subcomponents
the nuclear instruments. The inspectors reviewed the issue with the licensee with  
  consisting of over 4,000 items. Additionally, the program was looking at single point
respect to subcomponent aging management. The licensee had indicated that  
  vulnerabilities and risk prioritization of reviews. The inspectors concluded that this
subsequent to this event and industry reviews, it had expanded the subcomponent aging  
  program appeared to approach subcomponent aging management systematically and
management program. The licensee provided evidence which demonstrated that a  
  would provide a strong barrier to preclude similar failures in the future.
program for subcomponent aging and management was in the final stage of  
  Analysis: The inspectors determined that the failure to incorporate operating experience
development, and that the program was reviewing several categories of subcomponents  
  related to aging of electrical subcomponents specific to nuclear instrument source range
consisting of over 4,000 items. Additionally, the program was looking at single point  
                                              26                                    Enclosure
vulnerabilities and risk prioritization of reviews. The inspectors concluded that this  
program appeared to approach subcomponent aging management systematically and  
would provide a strong barrier to preclude similar failures in the future.  
Analysis: The inspectors determined that the failure to incorporate operating experience  
related to aging of electrical subcomponents specific to nuclear instrument source range  


monitors into preventive maintenance programs was a performance deficiency
warranting further review. The finding was determined to be more than minor in
27
accordance with IMC 0612, Power Reactor Inspection Reports, Appendix B, Issue
Enclosure
Screening, dated December 24, 2009, because the finding was associated with the
monitors into preventive maintenance programs was a performance deficiency  
Initiating Events Cornerstone attribute of equipment performance. Specifically, the
warranting further review. The finding was determined to be more than minor in  
availability and reliability of the nuclear instruments was degraded to a point where an
accordance with IMC 0612, Power Reactor Inspection Reports, Appendix B, Issue  
instrument failure caused a reactor trip, an event that adversely affected the cornerstone
Screening, dated December 24, 2009, because the finding was associated with the  
objective to limit the likelihood of those events that upset plant stability and challenge
Initiating Events Cornerstone attribute of equipment performance. Specifically, the  
critical safety functions during power operations.
availability and reliability of the nuclear instruments was degraded to a point where an  
The inspectors determined that the finding could be evaluated using IMC 0609,
instrument failure caused a reactor trip, an event that adversely affected the cornerstone  
Significance Determination Process, Attachment 0609.04, Phase 1 - Initial Screening
objective to limit the likelihood of those events that upset plant stability and challenge  
and Characterization of Findings, Table 4a for the Initiating Events Cornerstone, dated
critical safety functions during power operations.  
January 10, 2008. The inspectors determined that the finding did not contribute to both
The inspectors determined that the finding could be evaluated using IMC 0609,  
the likelihood of a reactor event and the likelihood that mitigation equipment or functions
Significance Determination Process, Attachment 0609.04, Phase 1 - Initial Screening  
would not be available; therefore, the issue screened as having very low safety
and Characterization of Findings, Table 4a for the Initiating Events Cornerstone, dated  
significance (Green).
January 10, 2008. The inspectors determined that the finding did not contribute to both  
The inspectors reviewed the licensees root cause analysis. The licensee considered
the likelihood of a reactor event and the likelihood that mitigation equipment or functions  
the issue a legacy issue related to the 1998 decision to ignore 1992 operating
would not be available; therefore, the issue screened as having very low safety  
experience and a 1998 vendor recommendation to replace power supplies at 10-year
significance (Green).  
intervals. Because the adverse decision occurred in 1998, the licensee concluded that
The inspectors reviewed the licensees root cause analysis. The licensee considered  
no crosscutting aspect occurred. However, the inspectors noted that the licensee
the issue a legacy issue related to the 1998 decision to ignore 1992 operating  
continued to amass internal and external operating experience from 1998 to 2011,
experience and a 1998 vendor recommendation to replace power supplies at 10-year  
including a 2010 NRC-identified trend of source range monitoring failures as
intervals. Because the adverse decision occurred in 1998, the licensee concluded that  
documented in IR 05000266/2010002; 05000301/2010002, Section 4OA2.3,
no crosscutting aspect occurred. However, the inspectors noted that the licensee  
Semiannual Trend, and that a rigorous and thorough evaluation of these issues could
continued to amass internal and external operating experience from 1998 to 2011,  
have precluded the most recent failure. Therefore, the inspectors determined that the
including a 2010 NRC-identified trend of source range monitoring failures as  
issue had a crosscutting aspect in the area of corrective action program,
documented in IR 05000266/2010002; 05000301/2010002, Section 4OA2.3,  
evaluation/extent of condition. Specifically, the licensee failed to thoroughly evaluate
Semiannual Trend, and that a rigorous and thorough evaluation of these issues could  
related nuclear instrument failure rates such that the resolutions addressed the causes
have precluded the most recent failure. Therefore, the inspectors determined that the  
and extent of conditions for age-related failures of electrical subcomponents (P.1(c)).
issue had a crosscutting aspect in the area of corrective action program,  
Enforcement: Title 10 CFR 50.65(a)(3) states, in part, that preventive maintenance
evaluation/extent of condition. Specifically, the licensee failed to thoroughly evaluate  
activities shall be evaluated at least every refueling cycle and take into account, where
related nuclear instrument failure rates such that the resolutions addressed the causes  
practical, industry-wide operating experience. Contrary to this requirement, the licensee
and extent of conditions for age-related failures of electrical subcomponents (P.1(c)).  
failed to evaluate its preventative maintenance activities to take into account a
Enforcement
Westinghouse Infogram, dated August 8, 1998, that recommended replacement of
Because this violation was of very low safety significance and it was entered into the
power supplies every 10 years, and other industry-wide operating experience issued
licensees CAP (as root cause evaluation (RCE) 01660378-02), this violation is being 
since 1998 related to the replacement of aging electrical subcomponents. This failure
: Title 10 CFR 50.65(a)(3) states, in part, that preventive maintenance  
resulted in electrical subcomponents of a source range monitor not being replaced since
activities shall be evaluated at least every refueling cycle and take into account, where  
the 1970s. A failure of one of these subcomponents resulted in a trip of the Unit 2
practical, industry-wide operating experience. Contrary to this requirement, the licensee  
reactor on June 13, 2011.
failed to evaluate its preventative maintenance activities to take into account a  
Because this violation was of very low safety significance and it was entered into the
Westinghouse Infogram, dated August 8, 1998, that recommended replacement of  
licensees CAP (as root cause evaluation (RCE) 01660378-02), this violation is being
power supplies every 10 years, and other industry-wide operating experience issued  
                                            27                                      Enclosure
since 1998 related to the replacement of aging electrical subcomponents. This failure  
resulted in electrical subcomponents of a source range monitor not being replaced since  
the 1970s. A failure of one of these subcomponents resulted in a trip of the Unit 2  
reactor on June 13, 2011.  


      treated as an NCV, consistent with Section 2.3.2 of the NRC enforcement Policy
      (NCV 05000266/2012003-04; 05000301/2012003-04, Failure to Incorporate Industry
28
      Operating Experience Into Preventive Maintenance Programs for Nuclear
Enclosure
      Instrumentation).
treated as an NCV, consistent with Section 2.3.2 of the NRC enforcement Policy  
      This event follow-up review constituted one sample as defined in IP 71153-05.
(NCV 05000266/2012003-04; 05000301/2012003-04, Failure to Incorporate Industry  
4OA5 Other Activities
Operating Experience Into Preventive Maintenance Programs for Nuclear  
.1   (Closed) URI 05000266/2011005-02; 05000301/2011005-02, Determining an
Instrumentation).  
      Individuals Dose of Record with Discrepant TLD/ED Data Inputs
This event follow-up review constituted one sample as defined in IP 71153-05.  
      The URI described a condition where additional information was needed by the
4OA5  
      inspectors to assess the licensees program when determining an individuals
.1  
      radiological dose of record. This item was discussed and closed by
Other Activities
      NCV 05000266/2012002-06, Determining an Individuals Dose of Record With
The URI described a condition where additional information was needed by the  
      Discrepant TLD/ED Data Inputs.
inspectors to assess the licensees program when determining an individuals  
.2   (Closed) URI 05000266/2012002-05; 05000301/2012002-05, TSC Filter Testing May Be
radiological dose of record. This item was discussed and closed by  
      Inadequate
NCV 05000266/2012002-06, Determining an Individuals Dose of Record With  
  a. Inspection Scope
Discrepant TLD/ED Data Inputs.  
      The URI described a condition where additional information was needed by the
(Closed) URI 05000266/2011005-02; 05000301/2011005-02, Determining an
      inspectors to assess the licensees TSC ventilation system filter testing program. This
Individuals Dose of Record with Discrepant TLD/ED Data Inputs
      item was closed and discussed in Section 2RS3 by NCV 05000266/2012003-02;
.2  
      05000301/2012003-02, Non-Compliance with 10 CFR 20.1701 to Control the
a.
      Concentration of Radioactive Material in Air and Ensure That Radiological Airborne
(Closed) URI 05000266/2012002-05; 05000301/2012002-05, TSC Filter Testing May Be  
      Hazards Would Be Minimized in the Technical Support Center During a Design-Basis
Inadequate  
      Accident.
The URI described a condition where additional information was needed by the  
.3   Temporary Instruction (TI)-2515/182 - Review of the Industry Initiative to Control
inspectors to assess the licensees TSC ventilation system filter testing program. This  
      Degradation of Underground Piping and Tanks
item was closed and discussed in Section 2RS3 by NCV 05000266/2012003-02;  
  a. Inspection Scope
05000301/2012003-02, Non-Compliance with 10 CFR 20.1701 to Control the  
      Leakage from buried and underground pipes has resulted in ground water contamination
Concentration of Radioactive Material in Air and Ensure That Radiological Airborne  
      incidents with associated heightened NRC and public interest. The industry issued a
Hazards Would Be Minimized in the Technical Support Center During a Design-Basis  
      guidance document, NEI 09-14, Guideline for the Management of Buried Piping
Accident.  
      Integrity, (ADAMS Accession No. ML1030901420), to describe the goals and required
Inspection Scope
      actions (commitments made by the licensee) resulting from this underground piping and
.3  
      tank initiative. On December 31, 2010, NEI issued Revision 1 to NEI 09-14, Guidance
a.
      for the Management of Underground Piping and Tank Integrity, (ADAMS Accession
Temporary Instruction (TI)-2515/182 - Review of the Industry Initiative to Control  
      No. ML110700122), with an expanded scope of components which included
Degradation of Underground Piping and Tanks  
      underground piping that was not in direct contact with the soil and underground tanks.
Leakage from buried and underground pipes has resulted in ground water contamination  
      On November 17, 2011, the NRC issued TI-2515/182, Review of the Industry Initiative
incidents with associated heightened NRC and public interest. The industry issued a  
      to Control Degradation of Underground Piping and Tanks, to gather information related
guidance document, NEI 09-14, Guideline for the Management of Buried Piping  
      to the industrys implementation of this initiative.
Integrity, (ADAMS Accession No. ML1030901420), to describe the goals and required  
      The inspectors reviewed the licensees programs for buried pipe, underground piping,
actions (commitments made by the licensee) resulting from this underground piping and  
      and tanks in accordance with TI-2515/182 to determine if the program attributes and
tank initiative. On December 31, 2010, NEI issued Revision 1 to NEI 09-14, Guidance  
      completion dates identified in Sections 3.3 A and 3.3 B of NEI 09-14, Revision 1, were
for the Management of Underground Piping and Tank Integrity, (ADAMS Accession  
                                              28                                    Enclosure
No. ML110700122), with an expanded scope of components which included  
underground piping that was not in direct contact with the soil and underground tanks.
On November 17, 2011, the NRC issued TI-2515/182, Review of the Industry Initiative  
to Control Degradation of Underground Piping and Tanks, to gather information related  
to the industrys implementation of this initiative.  
Inspection Scope
The inspectors reviewed the licensees programs for buried pipe, underground piping,  
and tanks in accordance with TI-2515/182 to determine if the program attributes and  
completion dates identified in Sections 3.3 A and 3.3 B of NEI 09-14, Revision 1, were  


        contained in the licensees program and implementing procedures. For the buried pipe
        and underground piping program attributes with completion dates that had passed, the
29
        inspectors reviewed records to determine if the attribute was in fact complete and to
Enclosure
        determine if the attribute was accomplished in a manner which reflected good or poor
contained in the licensees program and implementing procedures. For the buried pipe  
        practices in program management.
and underground piping program attributes with completion dates that had passed, the  
        Based upon the scope of the review described above, Phase I of TI-2515/182 was
inspectors reviewed records to determine if the attribute was in fact complete and to  
        completed.
determine if the attribute was accomplished in a manner which reflected good or poor  
  b.   Observations
practices in program management.
        The licensees buried piping and underground piping and tanks program was inspected
Based upon the scope of the review described above, Phase I of TI-2515/182 was  
        in accordance with Paragraphs 03.01.a through 03.01.c of TI-2515/182, and was found
completed.  
        to meet all applicable aspects of NEI 09-14, Revision 1, as set forth in Table 1 of the TI.
b.  
    c. Findings
The licensees buried piping and underground piping and tanks program was inspected  
        No findings were identified.
in accordance with Paragraphs 03.01.a through 03.01.c of TI-2515/182, and was found  
4OA6 Management Meetings
to meet all applicable aspects of NEI 09-14, Revision 1, as set forth in Table 1 of the TI.  
.1     Exit Meeting Summary
Observations
        On June 26, 2012, the inspectors presented the inspection results to Mr. L. Meyer and
c.  
        other members of the licensee staff. The licensee acknowledged the issues presented.
No findings were identified.  
        The inspectors confirmed that none of the potential report input discussed was
Findings
        considered proprietary.
4OA6
.2     Interim Exit Meetings
.1  
        Interim exits were conducted for:
Management Meetings
        *       the Review of the Industry Initiative to Control Degradation of Underground
On June 26, 2012, the inspectors presented the inspection results to Mr. L. Meyer and  
                Piping and Tanks (TI-2515/182) with Program Engineering Supervisor,
other members of the licensee staff. The licensee acknowledged the issues presented.
                Mr. E. Schmidt, and other members of the licensee staff on May 1, 2012. The
The inspectors confirmed that none of the potential report input discussed was  
                licensee confirmed that none of the potential report input discussed was
considered proprietary.  
                considered proprietary; and
Exit Meeting Summary
        *       the inspection results of the unresolved item with Mr. J. Petro, Acting Licensing
.2  
                Manager, on June 12, 2012.
Interim exits were conducted for:  
The inspectors confirmed that none of the potential report input discussed was considered
Interim Exit Meetings
proprietary. Proprietary material received during the inspection was returned to the licensee.
*  
4OA7 Licensee-Identified Violations
the Review of the Industry Initiative to Control Degradation of Underground  
        None.
Piping and Tanks (TI-2515/182) with Program Engineering Supervisor,
ATTACHMENT: SUPPLEMENTAL INFORMATION
Mr. E. Schmidt, and other members of the licensee staff on May 1, 2012. The  
                                                  29                                      Enclosure
licensee confirmed that none of the potential report input discussed was  
considered proprietary; and  
*  
the inspection results of the unresolved item with Mr. J. Petro, Acting Licensing  
Manager, on June 12, 2012.  
The inspectors confirmed that none of the potential report input discussed was considered  
proprietary. Proprietary material received during the inspection was returned to the licensee.  
4OA7  
None.
Licensee-Identified Violations  
ATTACHMENT: SUPPLEMENTAL INFORMATION


                              SUPPLEMENTAL INFORMATION
                                KEY POINTS OF CONTACT
1
Licensee
Attachment
E. Schmidt, Program Engineering Supervisor
A. Watry, Buried Pipe Engineer
SUPPLEMENTAL INFORMATION  
B. Scherwinski, Licensing
KEY POINTS OF CONTACT  
B. Hennessy, Licensing Supervisor
E. Schmidt, Program Engineering Supervisor  
J. Petro, Acting Licensing Manager
Licensee
Nuclear Regulatory Commission
A. Watry, Buried Pipe Engineer  
M. Kunowski, Chief, Reactor Projects Branch 5
B. Scherwinski, Licensing  
                                            1          Attachment
B. Hennessy, Licensing Supervisor  
J. Petro, Acting Licensing Manager  
M. Kunowski, Chief, Reactor Projects Branch 5  
Nuclear Regulatory Commission


                LIST OF ITEMS OPENED, CLOSED AND DISCUSSED
Opened
2
05000266/2012003-01;   NCV   Failure to Establish Emergency Diesel Generator Ventilation
Attachment
05000301/2012003-01          System Testing (Section 1R19)
05000266/2012003-02;   NCV   Non-Compliance With 10 CFR 20.1701 to Control the
LIST OF ITEMS OPENED, CLOSED AND DISCUSSED  
05000301/2012003-02          Concentration of Radioactive Material in Air and Ensure That
                            Radiological Airborne Hazards Would Be Minimized in the
Opened  
                            Technical Support Center During a Design-Basis Accident
05000266/2012003-01;  
                            (Section 2RS3)
05000301/2012003-01
05000266/2012003-03;   URI   Partial Turnover of Extended Power Uprate Modifications
NCV  
05000301/2012003-03          (Section 4OA2.4)
Failure to Establish Emergency Diesel Generator Ventilation  
05000266/2012003-04;   NCV   Failure to Incorporate Industry Operating Experience Into
System Testing (Section 1R19)  
05000301/2012003-04          Preventive Maintenance Programs for Nuclear
05000266/2012003-02;  
                            Instrumentation (Section 4OA3.4)
05000301/2012003-02
Closed
NCV  
05000266/2012003-01;   NCV   Failure to Establish Emergency Diesel Generator Ventilation
Non-Compliance With 10 CFR 20.1701 to Control the  
05000301/2012003-01          System Testing (Section 1R19)
Concentration of Radioactive Material in Air and Ensure That  
05000266/2012003-02;   NCV   Non-Compliance With 10 CFR 20.1701 to Control the
Radiological Airborne Hazards Would Be Minimized in the  
05000301/2012003-02          Concentration of Radioactive Material in Air and Ensure That
Technical Support Center During a Design-Basis Accident
                            Radiological Airborne Hazards Would Be Minimized in the
(Section 2RS3)  
                            Technical Support Center During a Design-Basis Accident
05000266/2012003-03;  
                            (Section 2RS3)
05000301/2012003-03
05000301/2011-004-00   LER   Automatic Reactor Trip During Startup Physics Testing Due
URI  
                            to Source Range (Section 4OA3.4)
Partial Turnover of Extended Power Uprate Modifications  
05000301/2011-004-01   LER   Automatic Reactor Trip During Startup Physics Testing Due
(Section 4OA2.4)  
                            to Source Range (Section 4OA3.4)
05000266/2012003-04;  
05000266/2012003-04;   NCV   Failure to Incorporate Industry Operating Experience Into
05000301/2012003-04
05000301/2012003-04          Preventive Maintenance Programs for Nuclear
NCV  
                            Instrumentation (Section 4OA3.4)
Failure to Incorporate Industry Operating Experience Into  
05000266/2011005-02;   URI   Determining An Individuals Dose Of Record With Discrepant
Preventive Maintenance Programs for Nuclear  
05000301/2011005-02          TLD/ED Data Inputs (Section 4OA5.1)
Instrumentation (Section 4OA3.4)  
05000266/2012002-05;   URI   TSC Filter Testing May Be Inadequate (Section 4OA5.2)
05000301/2012002-05
                                          2                                    Attachment
Closed  
05000266/2012003-01;  
05000301/2012003-01
NCV  
Failure to Establish Emergency Diesel Generator Ventilation  
System Testing (Section 1R19)  
05000266/2012003-02;  
05000301/2012003-02
NCV  
Non-Compliance With 10 CFR 20.1701 to Control the  
Concentration of Radioactive Material in Air and Ensure That  
Radiological Airborne Hazards Would Be Minimized in the  
Technical Support Center During a Design-Basis Accident
(Section 2RS3)  
05000301/2011-004-00  
LER  
Automatic Reactor Trip During Startup Physics Testing Due  
to Source Range (Section 4OA3.4)  
05000301/2011-004-01  
LER  
Automatic Reactor Trip During Startup Physics Testing Due  
to Source Range (Section 4OA3.4)  
05000266/2012003-04;  
05000301/2012003-04
NCV  
Failure to Incorporate Industry Operating Experience Into  
Preventive Maintenance Programs for Nuclear  
Instrumentation (Section 4OA3.4)  
05000266/2011005-02;  
05000301/2011005-02
URI  
Determining An Individuals Dose Of Record With Discrepant  
TLD/ED Data Inputs (Section 4OA5.1)  
05000266/2012002-05;  
05000301/2012002-05
URI  
TSC Filter Testing May Be Inadequate (Section 4OA5.2)  


                                  LIST OF DOCUMENTS REVIEWED
The following is a partial list of documents reviewed during the inspection. Inclusion on this list
3
does not imply that the NRC inspector reviewed the documents in their entirety, but rather that
Attachment
selected sections or portions of the documents were evaluated as part of the overall inspection
effort. Inclusion of a document on this list does not imply NRC acceptance of the document or
LIST OF DOCUMENTS REVIEWED  
any part of it, unless this is stated in the body of the inspection report.
The following is a partial list of documents reviewed during the inspection. Inclusion on this list  
1R01 Adverse Weather Protection
does not imply that the NRC inspector reviewed the documents in their entirety, but rather that  
- 2011 Summer Readiness Package; May 24, 2011
selected sections or portions of the documents were evaluated as part of the overall inspection  
- 2012 Summer Readiness Package; May 24, 2012
effort. Inclusion of a document on this list does not imply NRC acceptance of the document or  
- AOP-13C; Severe Weather Conditions; Revision 26
any part of it, unless this is stated in the body of the inspection report.  
- AOP-31; Solar Magnetic Disturbance Alert Response; Revision 0
- 2011 Summer Readiness Package; May 24, 2011  
- AR01675202; Solar Disturbance
1R01 Adverse Weather Protection
- AR01675213; FRCC And NERC On A Solar Flare That May Impact Earth 8/5 Strong Solar
- 2012 Summer Readiness Package; May 24, 2012  
  Activity
- AOP-13C; Severe Weather Conditions; Revision 26  
- AR01725580; 2012 Site Excellence Plan: Engineering (Improved Margin)
- AOP-31; Solar Magnetic Disturbance Alert Response; Revision 0  
- AR01728251; Summer Readiness Period Action Items
- AR01675202; Solar Disturbance  
- AR01749094; AOP-13C Severe Weather Conditions Requires Emergent Changes
- AR01675213; FRCC And NERC On A Solar Flare That May Impact Earth 8/5 Strong Solar  
- AR01757855; OI 155 Chemical Treatment of SW/Potential Impact On U2 B RCP
Activity  
- AR01764102; HX38 Condenser Summer Readiness Issue
- AR01725580; 2012 Site Excellence Plan: Engineering (Improved Margin)  
- AR01767718; Solar Magnetic Disturbance Impact On 1X-03 Is Unknown
- AR01728251; Summer Readiness Period Action Items  
- AR0176879; AOP-13B Number Used In 1996 Almost Reused Document
- AR01749094; AOP-13C Severe Weather Conditions Requires Emergent Changes  
- AR01776849; F52-Q303, 345KV Breaker Tripped Open From Lightning Strike
- AR01757855; OI 155 Chemical Treatment of SW/Potential Impact On U2 B RCP  
- ARP 1-PPCS-008; Priority Alarm Met Tower Unit 1; Revision 2
- AR01764102; HX38 Condenser Summer Readiness Issue  
- ARP 2-PPCS-008; Priority Alarm Met Tower Unit 2; Revision 2
- AR01767718; Solar Magnetic Disturbance Impact On 1X-03 Is Unknown  
- BG AOP-13C; Severe Weather Conditions; Revision 14
- AR0176879; AOP-13B Number Used In 1996 Almost Reused Document  
- DBD-20; 345 KVAC System; Revision 8
- AR01776849; F52-Q303, 345KV Breaker Tripped Open From Lightning Strike  
- Email From J. Schweitzer; Subject: NERC Communication Release: Major Solar
- ARP 1-PPCS-008; Priority Alarm Met Tower Unit 1; Revision 2  
  Disturbance On The Way?; August 4, 2011
- ARP 2-PPCS-008; Priority Alarm Met Tower Unit 2; Revision 2  
- EPMP 6.0; Alert And Notification System (ANS); Revision 10
- BG AOP-13C; Severe Weather Conditions; Revision 14  
- EPMP 9.0; Equipment Important To Emergency Preparedness; Revision 1
- DBD-20; 345 KVAC System; Revision 8  
- FSAR Section 7.5; Operating Control Stations; UFSAR 2010
- Email From J. Schweitzer; Subject: NERC Communication Release: Major Solar  
- FSAR Section 8.0; Introduction To The Electrical Distribution Systems; UFSAR 2010
Disturbance On The Way?; August 4, 2011  
- FSAR Section 8.1; 345K VAC Electrical Distribution System (345 kV); UFSAR 2010
- EPMP 6.0; Alert And Notification System (ANS); Revision 10  
- ICP 06.003-2; Meteorological System Calibration; Revision 1
- EPMP 9.0; Equipment Important To Emergency Preparedness; Revision 1  
- ICP 06.055; Meteorological Tower Instrumentation 6 Month Calibration Procedure; Revision 5
- FSAR Section 7.5; Operating Control Stations; UFSAR 2010  
- Log Entries Report; January 24 To April 23, 2012
- FSAR Section 8.0; Introduction To The Electrical Distribution Systems; UFSAR 2010  
- National Weather Service Hazardous Weather Outlook; June 18, 2012
- FSAR Section 8.1; 345K VAC Electrical Distribution System (345 kV); UFSAR 2010  
- Needs Assessment Worksheet For TRR 01675202; September 27, 2011
- ICP 06.003-2; Meteorological System Calibration; Revision 1  
- NOAA Space Weather Scales; March 1, 2005
- ICP 06.055; Meteorological Tower Instrumentation 6 Month Calibration Procedure; Revision 5  
- NP 2.1.5; Electrical Communications, Switchyard Access And Work Planning; Revision 21
- Log Entries Report; January 24 To April 23, 2012  
- NRC Information Notice No. 90-42: Failure Of Electrical Power Equipment Due To Solar
- National Weather Service Hazardous Weather Outlook; June 18, 2012  
  Magnetic Disturbances; June 19, 1990
- Needs Assessment Worksheet For TRR 01675202; September 27, 2011  
- ODI.104; Solar Magnetic Disturbance Alert Response; Revision 00
- NOAA Space Weather Scales; March 1, 2005  
- OI 35B; Electrical Equipment General Information; Revision 17
- NP 2.1.5; Electrical Communications, Switchyard Access And Work Planning; Revision 21  
- OP-AA-102-1002; Seasonal Readiness; Revision 0
- NRC Information Notice No. 90-42: Failure Of Electrical Power Equipment Due To Solar  
- PB MR 91-161; System 345kV; June 20, 1991
Magnetic Disturbances; June 19, 1990  
- PBN Seasonal Readiness Report; 2012 Winter Readiness Concerns/Issues; April 2012
- ODI.104; Solar Magnetic Disturbance Alert Response; Revision 00  
                                                  3                                    Attachment
- OI 35B; Electrical Equipment General Information; Revision 17  
- OP-AA-102-1002; Seasonal Readiness; Revision 0  
- PB MR 91-161; System 345kV; June 20, 1991  
- PBN Seasonal Readiness Report; 2012 Winter Readiness Concerns/Issues; April 2012  


- PBNP System Engineering Summer Readiness Review; Component Cooling Water;
  February 15, 2012
4
- PBNP System Engineering Summer Readiness Review; HVAC Rs And NR;
Attachment
  February 21, 2012
- PBNP System Engineering Summer Readiness Review; Service Water; February 21, 2012
- PBNP System Engineering Summer Readiness Review; Component Cooling Water;  
- PJM; Weather And Environmental Emergencies; November 1, 2011
February 15, 2012  
- Safety Logs; June 17, 2012
- PBNP System Engineering Summer Readiness Review; HVAC Rs And NR;  
- Station Log; June 17, 2012
February 21, 2012  
1R04 Equipment Alignment
- PBNP System Engineering Summer Readiness Review; Service Water; February 21, 2012  
- CL 13E Part 1; Auxiliary Feedwater Valve Lineup Turbine-Driven Unit 1; Revision 45
- PJM; Weather And Environmental Emergencies; November 1, 2011  
- CL 7A; Safety Injection System Checklist Unit 2; Revision 31
- Safety Logs; June 17, 2012  
- Drawing 018974; Safety Injection System; Revision 53
- Station Log; June 17, 2012  
- Drawing 018975; Safety Injection System; Revision 54
- CL 13E Part 1; Auxiliary Feedwater Valve Lineup Turbine-Driven Unit 1; Revision 45  
- Drawing 018976; Safety Injection System; Revision 47
1R04 Equipment Alignment
- OI 129; SI System Fill And Vent Unit 2; Revision 6
- CL 7A; Safety Injection System Checklist Unit 2; Revision 31  
1R05 Fire Protection
- Drawing 018974; Safety Injection System; Revision 53  
- DBD-T-40; Fire Protection/Appendix R; Revision 9
- Drawing 018975; Safety Injection System; Revision 54  
- Drawing 290583; Fire Protection For Site Plan; Revision 11
- Drawing 018976; Safety Injection System; Revision 47  
- Drawing 290585; Fire Protection For Turbine Building, Aux Building, And Containment,
- OI 129; SI System Fill And Vent Unit 2; Revision 6  
  Elev. 8-0; Revision 21
- DBD-T-40; Fire Protection/Appendix R; Revision 9  
- Drawing 290587; Fire Protection For Turbine Building, Aux Building, And Containment;
1R05 Fire Protection
  Revision 11
- Drawing 290583; Fire Protection For Site Plan; Revision 11  
- Drawing 290590; Fire Protection For Turbine Building, Aux Building, And Containment,
- Drawing 290585; Fire Protection For Turbine Building, Aux Building, And Containment,  
  Elev. 44-0; Revision 09
Elev. 8-0; Revision 21  
- Drawing 290600; Fire Protection For Turbine Building, Aux Building, And Containment,
- Drawing 290587; Fire Protection For Turbine Building, Aux Building, And Containment;  
  Elev. 66-0; Revision 06
Revision 11  
- Duke Engineering And Services Fire Area Analysis Summary Report; Fire Area: A01-B
- Drawing 290590; Fire Protection For Turbine Building, Aux Building, And Containment,  
  PAB 26 Elevation - Monitor Tank Area (FZ 187); August 8, 2005
Elev. 44-0; Revision 09  
- Duke Engineering And Services Fire Area Analysis Summary Report; Fire Area: A01-H Unit 2
- Drawing 290600; Fire Protection For Turbine Building, Aux Building, And Containment,  
  Façade; August 8, 2005
Elev. 66-0; Revision 06  
- FEP 4.6; Façade Unit 2; Revision 8
- Duke Engineering And Services Fire Area Analysis Summary Report; Fire Area: A01-B  
- FOP 1.2; Potential Fire Affected Safe Shutdown Components; Revision 21
PAB 26 Elevation - Monitor Tank Area (FZ 187); August 8, 2005  
- OM 1.1; Conduct Of Plant Operations, PBNP Specific; Revision 40
- Duke Engineering And Services Fire Area Analysis Summary Report; Fire Area: A01-H Unit 2  
- OM 3.1; Operations Shift Staffing Requirements; Revision 16
Façade; August 8, 2005  
- OM 3.27; Control Of Fire Protection & Appendix R Safe Shutdown Equipment; Revision 44
- FEP 4.6; Façade Unit 2; Revision 8  
1R06 Flood Protection
- FOP 1.2; Potential Fire Affected Safe Shutdown Components; Revision 21  
- AR01633384; IER1 11-1 Unanalyzed Challenge From Non-Seismic Int Flooding
- OM 1.1; Conduct Of Plant Operations, PBNP Specific; Revision 40  
- AR01752182; Draft NEI Flood Walkdown Document Not Available
- OM 3.1; Operations Shift Staffing Requirements; Revision 16  
- AR01762831; Water Entering SEI-06211 During Water Intrusion
- OM 3.27; Control Of Fire Protection & Appendix R Safe Shutdown Equipment; Revision 44  
- AR01762834; U1 Façade Southwest Corner Significant Water Entry
- AR01633384; IER1 11-1 Unanalyzed Challenge From Non-Seismic Int Flooding  
- AR01763180; U1 Façade Elevator Pit Flooded - Again
1R06 Flood Protection
- AR01763259; 1P-10A Cubicle Had Accumulated Ground Water
- AR01752182; Draft NEI Flood Walkdown Document Not Available  
- AR01763352; RE-113 PAB Area Monitor HI Alarm From Spiking
- AR01762831; Water Entering SEI-06211 During Water Intrusion  
- AR01765294; Groundwater Intrusion Into The 1P-10A RHR Cubicle
- AR01762834; U1 Façade Southwest Corner Significant Water Entry  
- AR01765466; Schedule Scrub Results Concerning Unit 2 RCP Seal Issues
- AR01763180; U1 Façade Elevator Pit Flooded - Again  
                                              4                                    Attachment
- AR01763259; 1P-10A Cubicle Had Accumulated Ground Water  
- AR01763352; RE-113 PAB Area Monitor HI Alarm From Spiking  
- AR01765294; Groundwater Intrusion Into The 1P-10A RHR Cubicle  
- AR01765466; Schedule Scrub Results Concerning Unit 2 RCP Seal Issues  


- AR01765723; Groundwater Intrusion Into The 1P-10A RHR Cubicle
- AR01767771; Plugging Elevator Sump Drains Not The Right Thing To Do
5
- CE 01633384-01; Six Bulk Storage Tanks In PAB Not Contained In Dikes Or Rooms
Attachment
- Floodable Volume Of The -19 Ft Elevation; Completed April 1, 2011
- FSAR Section 10.2; Auxiliary Feedwater System (AF); UFSAR 2010
- AR01765723; Groundwater Intrusion Into The 1P-10A RHR Cubicle  
- FSAR Section 6.2; Safety Injection System (SI); UFSAR 2010
- AR01767771; Plugging Elevator Sump Drains Not The Right Thing To Do  
- FSAR Section 9.2; Residual Heat Removal (RHR); UFSAR 2010
- CE 01633384-01; Six Bulk Storage Tanks In PAB Not Contained In Dikes Or Rooms  
- NPC-27204; Letter From S. Burstein, Western Electric Power Company, To G. Lear, NRC;
- Floodable Volume Of The -19 Ft Elevation; Completed April 1, 2011  
  Subject: Docket Nos. 50-266 And 50-301, Flooding Resulting From Non-Category I Failure,
- FSAR Section 10.2; Auxiliary Feedwater System (AF); UFSAR 2010  
  Point Beach Nuclear Plant - Units 1 And 2; February 17, 1975
- FSAR Section 6.2; Safety Injection System (SI); UFSAR 2010  
- NPC-28670; Letter From C. W. Fay, Western Electric Power Company, To H. R. Denton,
- FSAR Section 9.2; Residual Heat Removal (RHR); UFSAR 2010  
  NRC; Subject: Docket Nos. 50-266 And 50-301, Final Resolution Of Generic Letter 81-14,
- NPC-27204; Letter From S. Burstein, Western Electric Power Company, To G. Lear, NRC;  
  Seismic Qualification Of Auxiliary Feedwater System, Point Beach Nuclear Plant - Units 1
Subject: Docket Nos. 50-266 And 50-301, Flooding Resulting From Non-Category I Failure,  
  And 2; April 26, 1985
Point Beach Nuclear Plant - Units 1 And 2; February 17, 1975  
- POD 01633384; Unanalyzed Challenge From Non-Seismic Internal Flooding (Monitor Tanks
- NPC-28670; Letter From C. W. Fay, Western Electric Power Company, To H. R. Denton,  
  And Waste Distillate Tanks); Revision 0
NRC; Subject: Docket Nos. 50-266 And 50-301, Final Resolution Of Generic Letter 81-14,  
- Station Log; May 8-12, 2012
Seismic Qualification Of Auxiliary Feedwater System, Point Beach Nuclear Plant - Units 1  
- TAR 01633384; Unanalyzed Challenge From Non-Seismic Internal Flooding (Monitor Tanks
And 2; April 26, 1985  
  And Waste Distillate Tanks); Revision 0
- POD 01633384; Unanalyzed Challenge From Non-Seismic Internal Flooding (Monitor Tanks  
1R11 Licensed Operator Requalification Program
And Waste Distillate Tanks); Revision 0  
- AR01747380; Simulator Reliability Below Expectations
- Station Log; May 8-12, 2012  
- AR01748808; Simulator PPCS Stopped Functioning During LOI Training
- TAR 01633384; Unanalyzed Challenge From Non-Seismic Internal Flooding (Monitor Tanks  
- AR01748875; Nuclear Oversight Finding: Management Oversight Of Simulator
And Waste Distillate Tanks); Revision 0  
- FP-T-SAT-73; Licensed Operator Requalification Program Examinations; Revision 8
- AR01747380; Simulator Reliability Below Expectations  
- NARS Form For Training Evolution; May 21, 2012
1R11 Licensed Operator Requalification Program
- OM 1.1; Conduct Of Plant Operations, PBNP Specific; Revision 40
- AR01748808; Simulator PPCS Stopped Functioning During LOI Training  
- OP 3A Unit 2; Power Operation To Hot Standby Unit 2; Revision 7
- AR01748875; Nuclear Oversight Finding: Management Oversight Of Simulator  
- OP-AA-100-1000; Conduct Of Operations: Revision 6
- FP-T-SAT-73; Licensed Operator Requalification Program Examinations; Revision 8  
- PBNP LOCT Cycle 12C Schedule; Revision 2
- NARS Form For Training Evolution; May 21, 2012  
- Simulator Differences List; Cycle 12C; May 21, 2012
- OM 1.1; Conduct Of Plant Operations, PBNP Specific; Revision 40  
1R12 Maintenance Rule Effectiveness
- OP 3A Unit 2; Power Operation To Hot Standby Unit 2; Revision 7  
- ACE 01670189-02; Erratic Operation Displayed During Performance Of IT-08A Cold Start Of
- OP-AA-100-1000; Conduct Of Operations: Revision 6  
  Turbine-Driven Auxiliary Feed Pump And Valve Test (Unit 1); Revision 1
- PBNP LOCT Cycle 12C Schedule; Revision 2  
- RCA For AR1173557-02; Unit 2 Turbine Driven Auxiliary Feedwater Pump (2P-29-T) Casing
- Simulator Differences List; Cycle 12C; May 21, 2012  
  Leak Identified During Start Of IT-09A; Completed July 6, 2010
- ACE 01670189-02; Erratic Operation Displayed During Performance Of IT-08A Cold Start Of  
- RMP 9044-1; Auxiliary Feedwater Pump Terry Turbine Overhaul; Revision 11
Turbine-Driven Auxiliary Feed Pump And Valve Test (Unit 1); Revision 1  
- System Health Report; Unit 1 Auxiliary Feedwater; January 1 To March 31, 2012
1R12 Maintenance Rule Effectiveness
- System Health Report; Unit 2 Auxiliary Feedwater; January 1 To March 31, 2012
- RCA For AR1173557-02; Unit 2 Turbine Driven Auxiliary Feedwater Pump (2P-29-T) Casing  
- Thomas Series 54 Couplings; Installation Instruction
Leak Identified During Start Of IT-09A; Completed July 6, 2010  
1R13 Maintenance Risk Assessments and Emergent Work Control
- RMP 9044-1; Auxiliary Feedwater Pump Terry Turbine Overhaul; Revision 11  
- 2-SOP-CC-001; Component Cooling System; Revision 22
- System Health Report; Unit 1 Auxiliary Feedwater; January 1 To March 31, 2012  
- AOP-9B Unit 1; Component Cooling System Malfunction; Revision 22
- System Health Report; Unit 2 Auxiliary Feedwater; January 1 To March 31, 2012  
- AR01731219; Thermography Reading For 2F52-142 Breaker Limited Users
- Thomas Series 54 Couplings; Installation Instruction  
- AR01737362; While Performing IT-805, 2CC-726C Leaked By 85 Gal In 5 Min.
- 2-SOP-CC-001; Component Cooling System; Revision 22  
- AR01748666; Valve Is Difficult To Operate
1R13 Maintenance Risk Assessments and Emergent Work Control
                                              5                                    Attachment
- AOP-9B Unit 1; Component Cooling System Malfunction; Revision 22  
- AR01731219; Thermography Reading For 2F52-142 Breaker Limited Users  
- AR01737362; While Performing IT-805, 2CC-726C Leaked By 85 Gal In 5 Min.  
- AR01748666; Valve Is Difficult To Operate  


- AR01748700; Cross Unit CC Leakage During The Performance Of IT 805
- AR01766439; Request Review Of HX-12C Operability
6
- Calc No. 97-0118; Capacity To Achieve Cold Shutdown In Both Units With One CCW Pump
Attachment
  And Two CCW Heat Exchangers; April 27, 2011
- CCW Surge Tank Level, Units 1 And 2, 1LI-6188; March 25 To March 27, 2012
- AR01748700; Cross Unit CC Leakage During The Performance Of IT 805  
- CE 01748700-01; Component Cooling Leakage Occurred During Performance Of IT 805;
- AR01766439; Request Review Of HX-12C Operability  
  April 4, 2012
- Calc No. 97-0118; Capacity To Achieve Cold Shutdown In Both Units With One CCW Pump  
- Drawing 018982; Auxiliary Coolant System, Unit 1; Revision 42
And Two CCW Heat Exchangers; April 27, 2011  
- EOP-1.3 Unit 1; Transfer To Containment Sump Recirculation - Low Head Injection;
- CCW Surge Tank Level, Units 1 And 2, 1LI-6188; March 25 To March 27, 2012  
  Revision 47
- CE 01748700-01; Component Cooling Leakage Occurred During Performance Of IT 805;  
- FSAR Appendix A.6; Shared System Analysis; UFSAR 2008
April 4, 2012  
- FSAR Section 9.1; Component Cooling Water (CC); UFSAR 2010
- Drawing 018982; Auxiliary Coolant System, Unit 1; Revision 42  
- Hypothetical Risk Management Worksheet, Units 1 And 2; April 26, 2012
- EOP-1.3 Unit 1; Transfer To Containment Sump Recirculation - Low Head Injection;  
- IT 805; Component Cooling Water System Valves U-2; Completed March 26, 2012
Revision 47  
- Log Entries Report; Various Dates February 23 To March, 26, 2012
- FSAR Appendix A.6; Shared System Analysis; UFSAR 2008  
- NP 10.3.7; On-Line Safety Assessment; Revision 26
- FSAR Section 9.1; Component Cooling Water (CC); UFSAR 2010  
- OP 2B; 345 kV Transmission System Impacts Upon PBNP Station Operations; Revision 4
- Hypothetical Risk Management Worksheet, Units 1 And 2; April 26, 2012  
- PB - 2F52-142 Unit 2 Generator Breaker A Phase Monitoring Plan
- IT 805; Component Cooling Water System Valves U-2; Completed March 26, 2012  
- PB032221-11; Letter From L. Gundrum, NRC, To R. Grigg; Subject: Issuance Of
- Log Entries Report; Various Dates February 23 To March, 26, 2012  
  Amendments Re: Technical Specification Changes For Revised System Requirements To
- NP 10.3.7; On-Line Safety Assessment; Revision 26  
  Ensure Post-Accident Containment Cooling Capability (TAC Nos. M96741 And M96742);
- OP 2B; 345 kV Transmission System Impacts Upon PBNP Station Operations; Revision 4  
  July 9, 1997
- PB - 2F52-142 Unit 2 Generator Breaker A Phase Monitoring Plan  
- POD 01766439; Request Review Of HX-12C Operability; Revision 0
- PB032221-11; Letter From L. Gundrum, NRC, To R. Grigg; Subject: Issuance Of  
- PRA 5.14; Component Cooling Water System Notebook; Revision 0
Amendments Re: Technical Specification Changes For Revised System Requirements To  
- Responses To NRC Questions; Received June 12, 2012
Ensure Post-Accident Containment Cooling Capability (TAC Nos. M96741 And M96742);  
- Risk Management Worksheets, Units 1 And 2; April 21-28, 2012
July 9, 1997  
- Safety Monitor, Unit 1; April 3, 2012
- POD 01766439; Request Review Of HX-12C Operability; Revision 0  
- Safety Monitor, Unit 1; Various Dates February 22 To March 26, 2012
- PRA 5.14; Component Cooling Water System Notebook; Revision 0  
- Station Log; April 12, 2012
- Responses To NRC Questions; Received June 12, 2012  
- Station Log; February 3, 2012
- Risk Management Worksheets, Units 1 And 2; April 21-28, 2012  
- TLB-9; Component Cooling Water Surge; ID W 685-J-114, Tank 1(2)T-12; Revision 3
- Safety Monitor, Unit 1; April 3, 2012  
- Trend Display 3; CCW Temp; March 26, 2012
- Safety Monitor, Unit 1; Various Dates February 22 To March 26, 2012  
1R15 Operability Evaluations
- Station Log; April 12, 2012  
- AR01165060; Gas Void - Negligible Void Found At 2SI-V14
- Station Log; February 3, 2012  
- AR01165062; ECs Possibly Not In Correct Status
- TLB-9; Component Cooling Water Surge; ID W 685-J-114, Tank 1(2)T-12; Revision 3  
- AR01166814; Gas Void - Negligible, Smaller Void Found At 2SI-V14
- Trend Display 3; CCW Temp; March 26, 2012  
- AR01657344; 1P-29-T Governor Valve Stem Steam Leak
- AR01165060; Gas Void - Negligible Void Found At 2SI-V14  
- AR01667491; Voiding In U2 RHR Core Deluge Line (A Train)
1R15 Operability Evaluations
- AR01670550; 1P-29 Gov. Shaft Has Increased Steam Leakage
- AR01165062; ECs Possibly Not In Correct Status  
- AR01680372; Very Small Void Found At 2SI-V14
- AR01166814; Gas Void - Negligible, Smaller Void Found At 2SI-V14  
- AR01684317; PB2 Inside Containment Gas Void UT Results
- AR01657344; 1P-29-T Governor Valve Stem Steam Leak  
- AR01693921; Small Gas Voids Found, PB2 LHSI Train A
- AR01667491; Voiding In U2 RHR Core Deluge Line (A Train)  
- AR01701509; CFC Fan Motor Cooler Condensate Drain Valve Position
- AR01670550; 1P-29 Gov. Shaft Has Increased Steam Leakage  
- AR01705654; Very Small Gas Voids, PB2 Inside Containment
- AR01680372; Very Small Void Found At 2SI-V14  
- AR01712999; Operability Concern: U2 CFC Accident Fan Cooler Drn Vlvs
- AR01684317; PB2 Inside Containment Gas Void UT Results  
- AR01714813; Very Small Gas Voids, PB2 Inside Containment
- AR01693921; Small Gas Voids Found, PB2 LHSI Train A  
- AR01716079; Wires Inside U-1 Control Boards Not Spared Correctly
- AR01701509; CFC Fan Motor Cooler Condensate Drain Valve Position  
- AR01723005; 1C-03 Horizontal Wireway PL-A Cannot Close
- AR01705654; Very Small Gas Voids, PB2 Inside Containment  
- AR01723012; C-02 Riser 32 Train Separation Wireway PB22 Missing Cover
- AR01712999; Operability Concern: U2 CFC Accident Fan Cooler Drn Vlvs  
                                              6                                  Attachment
- AR01714813; Very Small Gas Voids, PB2 Inside Containment  
- AR01716079; Wires Inside U-1 Control Boards Not Spared Correctly  
- AR01723005; 1C-03 Horizontal Wireway PL-A Cannot Close  
- AR01723012; C-02 Riser 32 Train Separation Wireway PB22 Missing Cover  


- AR01723019; C-02 Remove Sound Powered Headphone Permanently Wired In
- AR01723362; 1C-004 Internal Risers 7 & 9 Have Large Openings In Wireways
7
- AR01723700; Lift Wires And Remove Minalites For CS-2130 Abandonment
Attachment
- AR01734709; Verification Of Wire Terminations For 1C-04 MOB-42 And 43
- AR01745582; 2012 Mid-Cycle: Safety - Extension Cords In CR >90 Days
- AR01723019; C-02 Remove Sound Powered Headphone Permanently Wired In  
- AR01747782; Gas Void Accept. Criterion For 1-IC-SI-D11 Non-Conservative
- AR01723362; 1C-004 Internal Risers 7 & 9 Have Large Openings In Wireways  
- AR01749161; Review Of Overall Control Room ARs
- AR01723700; Lift Wires And Remove Minalites For CS-2130 Abandonment  
- AR01750355; QC Inspection points Not Included In Work Tasks
- AR01734709; Verification Of Wire Terminations For 1C-04 MOB-42 And 43  
- AR01768931; TDAFWP Coupling Ejected Pieces During Run
- AR01745582; 2012 Mid-Cycle: Safety - Extension Cords In CR >90 Days  
- AR01769140; Flush Required On 1P29 TDAFWP Prior To Return To Service
- AR01747782; Gas Void Accept. Criterion For 1-IC-SI-D11 Non-Conservative  
- AR01769277; Pump Holddown Bolt In Southwest Corner Not Tight
- AR01749161; Review Of Overall Control Room ARs  
- AR01769697; Coupling For 1P-29 Did Not Come With Full Set Of Bolting
- AR01750355; QC Inspection points Not Included In Work Tasks  
- AR01769990; Small SW Leak Found
- AR01768931; TDAFWP Coupling Ejected Pieces During Run  
- AR01770001; Drain Trap Union Leaking
- AR01769140; Flush Required On 1P29 TDAFWP Prior To Return To Service  
- AR01770007; 1P-29 Turb. Outboard Bearing Temperatures During IT-8A
- AR01769277; Pump Holddown Bolt In Southwest Corner Not Tight  
- AR01770266; TDAFW Pump Mission Time In DBD-P-54 Questioned By NRC
- AR01769697; Coupling For 1P-29 Did Not Come With Full Set Of Bolting  
- AR01770327; Cable Spreading Room Temperature Out Of Spec High
- AR01769990; Small SW Leak Found
- AR01770729; Low Margin On VNCSR Creates Elevated Risk
- AR01770001; Drain Trap Union Leaking  
- AR01770731; Suspected Leak By Causing Elevated Temperature In CSR
- AR01770007; 1P-29 Turb. Outboard Bearing Temperatures During IT-8A  
- AR01771841; 1P-29-T TDAFW Turbine Bolting Changes
- AR01770266; TDAFW Pump Mission Time In DBD-P-54 Questioned By NRC  
- AR01772353; Condition Adverse To Quality - 1P-29-T
- AR01770327; Cable Spreading Room Temperature Out Of Spec High  
- AR01772594; Replace Shim Packs On The 1P-29-T Coupling
- AR01770729; Low Margin On VNCSR Creates Elevated Risk  
- AR01772637; Replace East Hold Down Studs On 1P-29-T
- AR01770731; Suspected Leak By Causing Elevated Temperature In CSR  
- AR01772640; Correct 1P-29-T Exhaust Flange Misalignment
- AR01771841; 1P-29-T TDAFW Turbine Bolting Changes  
- AR01774453; DY0C RMP Is Quarantined
- AR01772353; Condition Adverse To Quality - 1P-29-T  
- AR01774906; Old Abandoned AFW Cables Are Not Properly Spared
- AR01772594; Replace Shim Packs On The 1P-29-T Coupling  
- AR01774944; Performance Of IT 16 Can Increase CSR Temperature
- AR01772637; Replace East Hold Down Studs On 1P-29-T  
- AR01775121; Planned Maintenance Outages On Sirens K-004, K-005,K-006
- AR01772640; Correct 1P-29-T Exhaust Flange Misalignment  
- AR01775202; Unexpected Alarm HP Feedwater Heater SA Or B High Or Low
- AR01774453; DY0C RMP Is Quarantined  
- AR01775325; EPRI Issued NDE Alert Letter Based On North Anna OE
- AR01774906; Old Abandoned AFW Cables Are Not Properly Spared  
- AR01775418; Simulator Scenario Programs Not Working Properly
- AR01774944; Performance Of IT 16 Can Increase CSR Temperature  
- AR01775425; Change In Stroke Open Time For 2CV-1296
- AR01775121; Planned Maintenance Outages On Sirens K-004, K-005,K-006  
- Basis For Immediate Operability (CR01712999); December 6, 2011
- AR01775202; Unexpected Alarm HP Feedwater Heater SA Or B High Or Low  
- Drawing 171951; Containment Vent Fan Motor Base And Motor Cooling Coil Housing;
- AR01775325; EPRI Issued NDE Alert Letter Based On North Anna OE  
  Revision 09
- AR01775418; Simulator Scenario Programs Not Working Properly  
- Drawing 275461; Service Water System; Revision 13
- AR01775425; Change In Stroke Open Time For 2CV-1296  
- Drawing 332894; Fan Motor Cooler; Revision 3
- Basis For Immediate Operability (CR01712999); December 6, 2011  
- Drawing 335353; 24x66 Containment Fan Coolers With Supply Lower Left; Revision 3
- Drawing 171951; Containment Vent Fan Motor Base And Motor Cooling Coil Housing;  
- Drawing 35476; Unit 2 Heating And Ventilation Containment Area 11 Plan El. Above 66-0;
Revision 09  
  Revision 08
- Drawing 275461; Service Water System; Revision 13  
- Drawing 35477; Unit 2 Heating And Ventilation Containment Area 11 Plan El. 46-0;
- Drawing 332894; Fan Motor Cooler; Revision 3  
  Revision 05
- Drawing 335353; 24x66 Containment Fan Coolers With Supply Lower Left; Revision 3  
- Drawing 35478; Unit 2 Heating And Ventilation Containment Area 11 Plan El. 21-0;
- Drawing 35476; Unit 2 Heating And Ventilation Containment Area 11 Plan El. Above 66-0;  
  Revision 03
Revision 08  
- Drawing 35480; Unit 2 Heating And Ventilation Containment Area 11 Sections; Revision 06
- Drawing 35477; Unit 2 Heating And Ventilation Containment Area 11 Plan El. 46-0;  
- Drawing 35481; Unit 1 And 2 Heating And Ventilation Containment Areas 7 And 11;
Revision 05  
  Revision 07
- Drawing 35478; Unit 2 Heating And Ventilation Containment Area 11 Plan El. 21-0;  
- EC 276517; 1P-029-T Coupling Alignment Review For WO 342825; Revision 9; May 23, 2012
Revision 03  
- Email From N. Reckelberg To B. Beltz; Subject: CFC Motor Cooler Question; June 5, 2012
- Drawing 35480; Unit 2 Heating And Ventilation Containment Area 11 Sections; Revision 06  
                                            7                                    Attachment
- Drawing 35481; Unit 1 And 2 Heating And Ventilation Containment Areas 7 And 11;  
Revision 07  
- EC 276517; 1P-029-T Coupling Alignment Review For WO 342825; Revision 9; May 23, 2012  
- Email From N. Reckelberg To B. Beltz; Subject: CFC Motor Cooler Question; June 5, 2012  


- Engineering Evaluation No. EC 276517; 1P-029-T Coupling Alignment Review For
  WO 342825
8
- FSAR Section 6.3; Containment Air Recirculation Cooling System (VNCC); UFSAR 2010
Attachment
- NRC Inspection Question No. 1; May 31, 2012
- NRC Inspection Question No. 10; May 31, 2012
- Engineering Evaluation No. EC 276517; 1P-029-T Coupling Alignment Review For  
- NRC Inspection Question No. 11; June 1, 2012
WO 342825  
- NRC Inspection Question No. 2; May 31, 2012
- FSAR Section 6.3; Containment Air Recirculation Cooling System (VNCC); UFSAR 2010  
- NRC Inspection Question No. 3; June 1, 2012
- NRC Inspection Question No. 1; May 31, 2012  
- NRC Inspection Question No. 4; May 31, 2012
- NRC Inspection Question No. 10; May 31, 2012  
- NRC Inspection Question No. 5; May 31, 2012
- NRC Inspection Question No. 11; June 1, 2012  
- NRC Inspection Question No. 6; June 1, 2012
- NRC Inspection Question No. 2; May 31, 2012  
- NRC Inspection Question No. 7; May 31, 2012
- NRC Inspection Question No. 3; June 1, 2012  
- NRC Inspection Question No. 8; May 31, 2012
- NRC Inspection Question No. 4; May 31, 2012  
- NRC Inspection Question No. 9; June 1, 2012
- NRC Inspection Question No. 5; May 31, 2012  
- OI 155; Chemical Treatment Of Service Water For Mussels; Revision 34
- NRC Inspection Question No. 6; June 1, 2012  
- Operator Rounds; June 18-19, 2012
- NRC Inspection Question No. 7; May 31, 2012  
- PI-AA-100-1008; Condition Evaluation; Revision 3
- NRC Inspection Question No. 8; May 31, 2012  
- POD 01712999; Operability Concern: U2 CFC Accident Fan Cooler Drn Vlvs; Revision 0
- NRC Inspection Question No. 9; June 1, 2012  
- POD 01770327; Cable Spreading Room Temperature Out Of Spec High; Revision 0
- OI 155; Chemical Treatment Of Service Water For Mussels; Revision 34  
- POD For CR 1771762; NRC Questions On G01/G02 Tornado Missile Temp Modification
- Operator Rounds; June 18-19, 2012  
- POD For CR1772353; Condition Adverse To Quality - 1P-29-T; Revision 0
- PI-AA-100-1008; Condition Evaluation; Revision 3  
- SCR 2011-0324; Revise 1/2-SOP-VNCC-001 Through 004, 1/2W-1A1 Through 1/2W-1D1
- POD 01712999; Operability Concern: U2 CFC Accident Fan Cooler Drn Vlvs; Revision 0  
  Accident Fan Recirculation Unit Draining, Filling And Venting Procedures; November 27, 2011
- POD 01770327; Cable Spreading Room Temperature Out Of Spec High; Revision 0  
- SCR 2012-0089; 1P-29 Turbine Driven Aux Feed Pump Turbine Alignment; May 23, 2012
- POD For CR 1771762; NRC Questions On G01/G02 Tornado Missile Temp Modification  
- TAR 01667491; Voiding In U2 RHR Core Deluge Line (A Train); Revision 0
- POD For CR1772353; Condition Adverse To Quality - 1P-29-T; Revision 0  
1R18 Plant Modifications
- SCR 2011-0324; Revise 1/2-SOP-VNCC-001 Through 004, 1/2W-1A1 Through 1/2W-1D1  
- AOP-13C; Severe Weather Conditions; Revision 26
Accident Fan Recirculation Unit Draining, Filling And Venting Procedures; November 27, 2011  
- AR01728544; PSS Design Functions Not Considered In Modification
- SCR 2012-0089; 1P-29 Turbine Driven Aux Feed Pump Turbine Alignment; May 23, 2012  
- AR01752847; 2MS-380B IA Leak
- TAR 01667491; Voiding In U2 RHR Core Deluge Line (A Train); Revision 0  
- AR01763193; 1CS-3124 And 1CS-3125 Comp. Actions For AOP-13C
- AOP-13C; Severe Weather Conditions; Revision 26  
- AR01763196; 2CS-3124 And 2CS-3125 Comp. Actions For AOP-13C
1R18 Plant Modifications
- AR01763206; Cold Weather Actions - AOP-13C Guidance
- AR01728544; PSS Design Functions Not Considered In Modification  
- AR01779751; 2Q12 Green NCV - G01/G02 Room Fan And Damper Test Control
- AR01752847; 2MS-380B IA Leak  
- B 3.7.2; MSIVs And Non-Return Check Valves; Unit 2 - Amendment No. 245
- AR01763193; 1CS-3124 And 1CS-3125 Comp. Actions For AOP-13C  
- B 3.7.3; MFIVs, MFRVs, And MFRV Bypass Valves; Unit 2 - Amendment No. 245
- AR01763196; 2CS-3124 And 2CS-3125 Comp. Actions For AOP-13C  
- CE For AR01752847-01; Air Leak Fount on 2MS-380B
- AR01763206; Cold Weather Actions - AOP-13C Guidance  
- CRN 262425; Revise Cold Weather Strategy; Revision 2
- AR01779751; 2Q12 Green NCV - G01/G02 Room Fan And Damper Test Control  
- CRN 262894; Manufacturers Recommended Minimum Ambient Temperature For Hiller
- B 3.7.2; MSIVs And Non-Return Check Valves; Unit 2 - Amendment No. 245  
  Actuator Components Is -20°F; Revision 0
- B 3.7.3; MFIVs, MFRVs, And MFRV Bypass Valves; Unit 2 - Amendment No. 245  
- Design Input Consultation Forms; EC 276081 Temporary Instrument Air Leak Repair
- CE For AR01752847-01; Air Leak Fount on 2MS-380B  
  Upstream Of 2MS-380B; Various Dates April 9 To April 16, 2012
- CRN 262425; Revise Cold Weather Strategy; Revision 2  
- Drawing 084854; Main & Reheat Steam System; Revisions 01 And 51
- CRN 262894; Manufacturers Recommended Minimum Ambient Temperature For Hiller  
- EC 273303; Provide Temp Power To Select 1B-42 Loads; Revision 1; October 6, 2011
Actuator Components Is -20°F; Revision 0  
- EC 276081; Instrument Air Leak At 2MS-280B Temporary Repair Of Air Line Leak
- Design Input Consultation Forms; EC 276081 Temporary Instrument Air Leak Repair  
- FP-E-MOD-03; Temporary Modifications; Revisions 9 And 10
Upstream Of 2MS-380B; Various Dates April 9 To April 16, 2012  
- Modification Classification; Install Temp Mod On 2MS-02017 Per EC 276081; Completed
- Drawing 084854; Main & Reheat Steam System; Revisions 01 And 51  
  April 13, 2012
- EC 273303; Provide Temp Power To Select 1B-42 Loads; Revision 1; October 6, 2011  
- Modification Classification; Provide Temp Power To Select 1B-42 Loads, Per EC 273303;
- EC 276081; Instrument Air Leak At 2MS-280B Temporary Repair Of Air Line Leak  
  Completed September 28, 2011
- FP-E-MOD-03; Temporary Modifications; Revisions 9 And 10  
                                                8                                  Attachment
- Modification Classification; Install Temp Mod On 2MS-02017 Per EC 276081; Completed  
April 13, 2012  
- Modification Classification; Provide Temp Power To Select 1B-42 Loads, Per EC 273303;  
Completed September 28, 2011  


- MR No. 96-014-B; MSIV Control Solenoid Replacement; October 7, 1998
- PC 49 Part 4; Auxiliary Building Miscellaneous And Facades; Revision 27
9
- SCR 2011-0207-01; EC 273303; Provide Temporary Power To Select 1B-42 Loads;
Attachment
  February 1, 2012
- SCR 2012-0057; Install Temp Mod On 2MS-00380B Per EC 276081; April 12, 2012
- MR No. 96-014-B; MSIV Control Solenoid Replacement; October 7, 1998  
- Station Logs; Various Dates April 6 To June 12, 2012
- PC 49 Part 4; Auxiliary Building Miscellaneous And Facades; Revision 27  
- Temp Mod Extension; Install Temp Mod On 2MS-02017 Per EC 276081; Completed
- SCR 2011-0207-01; EC 273303; Provide Temporary Power To Select 1B-42 Loads;  
  April 13, 2012
February 1, 2012  
- WO Package 40155064 01; 2MS-380B IA Leak
- SCR 2012-0057; Install Temp Mod On 2MS-00380B Per EC 276081; April 12, 2012  
1R19 Post-Maintenance Testing
- Station Logs; Various Dates April 6 To June 12, 2012  
- 0-SOP-G02-001; Maintenance Operation For EDG G-02; Completed April 26, 2012
- Temp Mod Extension; Install Temp Mod On 2MS-02017 Per EC 276081; Completed  
- AR01722333; VNDG-04178-M / Replace Broken Motor Operator
April 13, 2012  
- AR01750276; G-01 And G-02 Diesel Room Air Flow NRC Concern
- WO Package 40155064 01; 2MS-380B IA Leak  
- AR01753241; VNPAB Inoperable Due To FS-3297
- 0-SOP-G02-001; Maintenance Operation For EDG G-02; Completed April 26, 2012  
- AR01769204; Calculation 2005-0054 Rev. 2 Potential Non-Conservatism
1R19 Post-Maintenance Testing
- B 3.8.1; AC Sources - Operating; January 18, 2010; June 1, 2009; January 19, 2008;
- AR01722333; VNDG-04178-M / Replace Broken Motor Operator  
  May 31, 2007; Unit 1-Amendment No. 215, Unit 2-Amendment No. 220; Unit 1-Amendment
- AR01750276; G-01 And G-02 Diesel Room Air Flow NRC Concern  
  No. 201, Unit 2-Amendment No. 206
- AR01753241; VNPAB Inoperable Due To FS-3297  
- Calc 2005-0054; Control Building GOTHIC Temperature Calculation; Revisions 1 And 2
- AR01769204; Calculation 2005-0054 Rev. 2 Potential Non-Conservatism  
- CE 1750276-01; NRC Concern With Proper Air Flow In G-01 And G-02 Diesel Rooms
- B 3.8.1; AC Sources - Operating; January 18, 2010; June 1, 2009; January 19, 2008;  
- EN47896; Licensed Operating Supervisor Tested Positive For A For-Cause Test For Alcohol;
May 31, 2007; Unit 1-Amendment No. 215, Unit 2-Amendment No. 220; Unit 1-Amendment  
  May 3, 2012
No. 201, Unit 2-Amendment No. 206  
- IT 08A; Cold Start Of Turbine-Driven Auxiliary Feed Pump And Valve Test (Quarterly) Unit 1;
- Calc 2005-0054; Control Building GOTHIC Temperature Calculation; Revisions 1 And 2  
  Revision 65
- CE 1750276-01; NRC Concern With Proper Air Flow In G-01 And G-02 Diesel Rooms  
- NARS Forms; April 25, 2012
- EN47896; Licensed Operating Supervisor Tested Positive For A For-Cause Test For Alcohol;  
- NP 10.3.7; On-Line Safety Assessment; Revision 27
May 3, 2012  
- PBTP 157; G01/G02 Diesel Room Exhaust Fan Flow Measurement; Completed July 6, 2007
- IT 08A; Cold Start Of Turbine-Driven Auxiliary Feed Pump And Valve Test (Quarterly) Unit 1;  
- PBTP-249; EDG Stack Test; Completed April 30, 2012
Revision 65  
- PdMA Report 360458 0W-012B-M MCE; MCE Testing On 02/09/2010 For 0W-012B-M,
- NARS Forms; April 25, 2012  
  G-01 Room Exhaust Fan Motor; February 9, 2010
- NP 10.3.7; On-Line Safety Assessment; Revision 27  
- PdMA Report 360458 0W-012C-M MCE; MCE Testing Of 0W-012C-M; February 22, 2010
- PBTP 157; G01/G02 Diesel Room Exhaust Fan Flow Measurement; Completed July 6, 2007  
- RMP 9044-1; Auxiliary Feedwater Pump Terry Turbine Overhaul; Revision 28
- PBTP-249; EDG Stack Test; Completed April 30, 2012  
- Station Log; Various Dates From April 8 To April 27, 2012
- PdMA Report 360458 0W-012B-M MCE; MCE Testing On 02/09/2010 For 0W-012B-M,  
- TAR 1766629; Review G-01 Operability Versus Gravity Louvers; Revision 0
G-01 Room Exhaust Fan Motor; February 9, 2010  
- Troubleshooting Log For AR176931; May 23, 2012
- PdMA Report 360458 0W-012C-M MCE; MCE Testing Of 0W-012C-M; February 22, 2010  
- TS 81; Emergency Diesel Generator G-01 Monthly; Completed May 20, 2012
- RMP 9044-1; Auxiliary Feedwater Pump Terry Turbine Overhaul; Revision 28  
- TS 87; Primary Auxiliary Building Ventilation System Monthly Checks; Completed
- Station Log; Various Dates From April 8 To April 27, 2012  
  April 10, 2012
- TAR 1766629; Review G-01 Operability Versus Gravity Louvers; Revision 0  
- WO 40106974; 2F52-142 A Phase - Output Side Bolded Connection Hot
- Troubleshooting Log For AR176931; May 23, 2012  
- WO Package 00342825-16; 1P-029-T Contingency Work Order To Overhaul If Required -2C
- TS 81; Emergency Diesel Generator G-01 Monthly; Completed May 20, 2012  
- WO Package 00360458-01; W-012B-M, MCE Analyze Motor (2 B52-329H/2B-32)
- TS 87; Primary Auxiliary Building Ventilation System Monthly Checks; Completed  
- WO Package 00360459-01; W-012C-MCE Analyze Motor (2 B52-328M/2B-32)
April 10, 2012  
- WO Package 40070360 01; 2MS-02052-O Replace Actuator
- WO 40106974; 2F52-142 A Phase - Output Side Bolded Connection Hot  
- WO Package 40110297 07; K-004A Inspect And Maintain Diesel Air Start Compressor
- WO Package 00342825-16; 1P-029-T Contingency Work Order To Overhaul If Required -2C  
1R20 Unplanned Outage
- WO Package 00360458-01; W-012B-M, MCE Analyze Motor (2 B52-329H/2B-32)  
- 2F3201 Forced Outage Critical Path; June 27, 2012
- WO Package 00360459-01; W-012C-MCE Analyze Motor (2 B52-328M/2B-32)  
- 2F32HS Forced Outage Issues And Actions
- WO Package 40070360 01; 2MS-02052-O Replace Actuator  
                                                9                                Attachment
- WO Package 40110297 07; K-004A Inspect And Maintain Diesel Air Start Compressor  
- 2F3201 Forced Outage Critical Path; June 27, 2012  
1R20 Unplanned Outage
- 2F32HS Forced Outage Issues And Actions  


- Daily Status Report; June 29, 2012
- EN 48053; Unit 2 Manual Reactor Actuated Due To Indications Of 100% Load Rejection;
10
  June 27, 2012
Attachment
- NP 5.3.3; Incident Investigation And Post-Trip Reviews; Completed June 27, 2012
- OP 3A Unit 1; Power Operation To Hot Standby Unit 1; Revision 9
- Daily Status Report; June 29, 2012  
- OP 3B; Reactor Shutdown; Revision 43
- EN 48053; Unit 2 Manual Reactor Actuated Due To Indications Of 100% Load Rejection;  
- PBNP Outage Status Report; June 29, 2012
June 27, 2012  
- PBNP Shutdown Safety Assessment And Fire Condition; Unit 2; June 29, 2012
- NP 5.3.3; Incident Investigation And Post-Trip Reviews; Completed June 27, 2012  
- PBNP Unit 2; Forced Outage List; As Of June 29, 2012
- OP 3A Unit 1; Power Operation To Hot Standby Unit 1; Revision 9  
- Safety Monitor, Unit 1; June 27 To 28, 2012
- OP 3B; Reactor Shutdown; Revision 43  
- Safety Monitor, Unit 2; June 27, 2012
- PBNP Outage Status Report; June 29, 2012  
- Station Log; June 27 To June 29, 2012
- PBNP Shutdown Safety Assessment And Fire Condition; Unit 2; June 29, 2012  
1R22 Surveillance Testing
- PBNP Unit 2; Forced Outage List; As Of June 29, 2012  
- Safety Monitor, Unit 1; June 27 To 28, 2012  
- Safety Monitor, Unit 2; June 27, 2012  
- Station Log; June 27 To June 29, 2012  
- 3.3.3; Post Accident Monitoring (PAM) Instrumentation; Unit 1 - Amendment No. 215, Unit 2 -
- 3.3.3; Post Accident Monitoring (PAM) Instrumentation; Unit 1 - Amendment No. 215, Unit 2 -
  Amendment No. 220; Unit 1 - Amendment No. 201, Unit 2 - Amendment No. 206
Amendment No. 220; Unit 1 - Amendment No. 201, Unit 2 - Amendment No. 206  
- 3.4.13; RCS Operational Leakage; Unit 1 - Amendment No. 223, Unit 2 - Amendment No. 229;
1R22 Surveillance Testing
  And Unit 1 - Amendment No. 201, Unit 2 - Amendment No. 206
- 3.4.13; RCS Operational Leakage; Unit 1 - Amendment No. 223, Unit 2 - Amendment No. 229;  
- 3.6.3; Containment Isolation Valves; Unit 1 - Amendment No. 201, Unit 2 - Amendment
And Unit 1 - Amendment No. 201, Unit 2 - Amendment No. 206  
  No. 206; Unit 1 - Amendment No. 231, Unit 2 - Amendment No. 236
- 3.6.3; Containment Isolation Valves; Unit 1 - Amendment No. 201, Unit 2 - Amendment  
- AOP-1B; Reactor Coolant Pump Malfunction; Revision 20
No. 206; Unit 1 - Amendment No. 231, Unit 2 - Amendment No. 236  
- AR01681115; Air Fitting Leak
- AOP-1B; Reactor Coolant Pump Malfunction; Revision 20  
- AR01752323; Increased Leakoff From Unit 2 B RCP #2 Seal
- AR01681115; Air Fitting Leak  
- AR01753068; AOP-1B, RCP Malfunction, Entered Due To Hi RCP Seal Leakage
- AR01752323; Increased Leakoff From Unit 2 B RCP #2 Seal  
- AR01753241; VNPAB Inoperable Due To FS-3297
- AR01753068; AOP-1B, RCP Malfunction, Entered Due To Hi RCP Seal Leakage  
- AR01754554; AOP-1B Entry Due To Reactor Coolant Pump Seal Problems
- AR01753241; VNPAB Inoperable Due To FS-3297  
- AR01755405; Momentary 2P-1B Seal Flow Low Alarm
- AR01754554; AOP-1B Entry Due To Reactor Coolant Pump Seal Problems  
- AR01762008; 2P-001B Seal Performance During Fan Starts
- AR01755405; Momentary 2P-1B Seal Flow Low Alarm  
- Control Room Log - Modes 1-3, Unit 2; April 5 To 8, 2012
- AR01762008; 2P-001B Seal Performance During Fan Starts  
- FSAR Section 1.3; General Design Criteria; UFSAR 2010
- Control Room Log - Modes 1-3, Unit 2; April 5 To 8, 2012  
- FSAR Section 4.1; Reactor Coolant System - Design Basis; UFSAR 2008
- FSAR Section 1.3; General Design Criteria; UFSAR 2010  
- FSAR Section 6.5; Leakage Detection Systems; UFSAR 2008
- FSAR Section 4.1; Reactor Coolant System - Design Basis; UFSAR 2008  
- IT 115; Instrument Air Valves (Quarterly) Unit 2; Completed May 18, 2012
- FSAR Section 6.5; Leakage Detection Systems; UFSAR 2008  
- NP 10.3.78; On-Line Safety Assessment; Revision 27
- IT 115; Instrument Air Valves (Quarterly) Unit 2; Completed May 18, 2012  
- OI 55; Primary Leak Rate Calculation; Performed March 16, 2012
- NP 10.3.78; On-Line Safety Assessment; Revision 27  
- OM 3.26; Use Of Dedicated / Assigned Operators; Revision 15
- OI 55; Primary Leak Rate Calculation; Performed March 16, 2012  
- Operational Decision Making; Increased 2P-1B, RCP, No. 2 Seal Leakage Transients;
- OM 3.26; Use Of Dedicated / Assigned Operators; Revision 15  
  Revised April 13, 2012
- Operational Decision Making; Increased 2P-1B, RCP, No. 2 Seal Leakage Transients;  
- Station Log; April 6 To 7, 2012; May 18, 2012
Revised April 13, 2012  
- Station Log; April 8, 2012
- Station Log; April 6 To 7, 2012; May 18, 2012  
- TS 87; Primary Auxiliary Building Ventilation System Monthly Checks; Completed
- Station Log; April 8, 2012  
  April 10, 2012
- TS 87; Primary Auxiliary Building Ventilation System Monthly Checks; Completed  
1EP6 Emergency Preparedness
April 10, 2012  
- EN 47863; Alert Declared Due To Toxic Gas Build Up Following An Emergency Diesel
- EN 47863; Alert Declared Due To Toxic Gas Build Up Following An Emergency Diesel  
  Generator Test Run; April 25, 2012
Generator Test Run; April 25, 2012  
- EPIP 1.1; Course Of Actions; Revision 63
1EP6 Emergency Preparedness
- EPIP 1.2; Emergency Classification; Revision 50
- EPIP 1.1; Course Of Actions; Revision 63  
- EPIP 1.2.1; Emergency Action Level Technical Basis; Revision 8
- EPIP 1.2; Emergency Classification; Revision 50  
                                                10                                Attachment
- EPIP 1.2.1; Emergency Action Level Technical Basis; Revision 8  


2RS3 In-Plant Airborne Radioactivity Control and Mitigation
- AR01696182; Lack Of 50.59 Screening For EPU LOCA Dose Calculations
11
- AR01724172; Discrepancy In F-13 Filter Efficiency Tested In HPIP 11
Attachment
- AR01779750; 2Q12 Green NCV - TSC Ventilation Filter Testing
- Calculation No. 129187-M-0112; Technical Support Center Direct Shine Dose Due To A Loss
- AR01696182; Lack Of 50.59 Screening For EPU LOCA Dose Calculations  
  Of Coolant Accident Following Extended Power Up-Rate And Using Alternative Source Term
2RS3 In-Plant Airborne Radioactivity Control and Mitigation
  Methodology; Revision 1
- AR01724172; Discrepancy In F-13 Filter Efficiency Tested In HPIP 11  
- Calculation No. 13612; Power/RP, PR-001; Calculate The Doses And Dose Rates In The
- AR01779750; 2Q12 Green NCV - TSC Ventilation Filter Testing  
  Technical Support Center Due To Intake And In-Leakage Following A LOCA, Assuming 4 Inch
- Calculation No. 129187-M-0112; Technical Support Center Direct Shine Dose Due To A Loss  
  Deep Activated Charcoal Beds Are Installed; May 19, 1980
Of Coolant Accident Following Extended Power Up-Rate And Using Alternative Source Term  
- HPIP 11.50; Filter Testing; Revisions 20 And 21
Methodology; Revision 1  
- HPIP 11.52; HEPA (High Efficiency Particulate Absolute) And Charcoal Filter Administrative
- Calculation No. 13612; Power/RP, PR-001; Calculate The Doses And Dose Rates In The  
  Control; Revisions 3 And 4
Technical Support Center Due To Intake And In-Leakage Following A LOCA, Assuming 4 Inch  
- HPIP 11.54; Control Room F-16 Filter Testing; Revisions 17 And 18
Deep Activated Charcoal Beds Are Installed; May 19, 1980  
4OA1 Performance Indicator Verification
- HPIP 11.50; Filter Testing; Revisions 20 And 21  
- 1Q/2012 Performance Indicators; Reactor Coolant System Leakage, Units 1 And 2
- HPIP 11.52; HEPA (High Efficiency Particulate Absolute) And Charcoal Filter Administrative  
- 2Q/2011 Performance Indicators; Reactor Coolant System Leakage, Units 1 And 2
Control; Revisions 3 And 4  
- 3Q/2011 Performance Indicators; Reactor Coolant System Leakage, Units 1 And 2
- HPIP 11.54; Control Room F-16 Filter Testing; Revisions 17 And 18  
- 4Q/2011 Performance Indicators; Reactor Coolant System Leakage, Units 1 And 2
- 1Q/2012 Performance Indicators; Reactor Coolant System Leakage, Units 1 And 2  
- Gamma Spectrum Analysis; Sample Date February 29, 2012
4OA1 Performance Indicator Verification
- H33; Performance Indicator Reporting; Revision 11
- 2Q/2011 Performance Indicators; Reactor Coolant System Leakage, Units 1 And 2  
- Log Entries Report; Various Dates From April 9, 2011 To March 14, 2012
- 3Q/2011 Performance Indicators; Reactor Coolant System Leakage, Units 1 And 2  
- Monthly Effluent Release Offsite Dose Summary; December 2011
- 4Q/2011 Performance Indicators; Reactor Coolant System Leakage, Units 1 And 2  
- NEI 99-02; Regulatory Assessment Performance Indicator Guideline; Revision 6;
- Gamma Spectrum Analysis; Sample Date February 29, 2012  
  October 2009
- H33; Performance Indicator Reporting; Revision 11  
- NP 5.2.16; NRC Performance Indicators; Completed March 28 And March 2, 2012
- Log Entries Report; Various Dates From April 9, 2011 To March 14, 2012  
- QF-0445; NRC/INPO/WANO Data Collection And Submittal Forms; 3rd Quarter 2011
- Monthly Effluent Release Offsite Dose Summary; December 2011  
- QF-0445; NRC/INPO/WANO Data Collection And Submittal Forms; 4th Quarter 2011
- NEI 99-02; Regulatory Assessment Performance Indicator Guideline; Revision 6;  
- ROP Parent Process Data Review, Unit 1; 2nd Quarter 2011 To 1st Quarter 2012
October 2009  
- RPIP 1013; Occupational Radiation Safety Performance Indicators; Revision 5
- NP 5.2.16; NRC Performance Indicators; Completed March 28 And March 2, 2012  
- RPIP 3332; Dose Equivalent Iodine-131; Revision 10
- QF-0445; NRC/INPO/WANO Data Collection And Submittal Forms; 3rd Quarter 2011  
- RPIP 3382; Reactor Coolant Sample Preparation And Analysis; Revision 13
- QF-0445; NRC/INPO/WANO Data Collection And Submittal Forms; 4th Quarter 2011  
- RPIP 4521; Monthly Effluent Release Offsite Dose Calculations; Revision 7
- ROP Parent Process Data Review, Unit 1; 2nd Quarter 2011 To 1st Quarter 2012  
4OA2 Identification and Resolution of Problems
- RPIP 1013; Occupational Radiation Safety Performance Indicators; Revision 5  
- ACE 01670172; Licensed Operator Had Expired Respirator Qualifications
- RPIP 3332; Dose Equivalent Iodine-131; Revision 10  
- ANSI N18-1-1971; Selection And Training Of Nuclear Power Plant Personnel; March 8, 1971
- RPIP 3382; Reactor Coolant Sample Preparation And Analysis; Revision 13  
- ANSI/ANS-3.4-1996; Medical Certification And Monitoring Of Personnel Requiring Operator
- RPIP 4521; Monthly Effluent Release Offsite Dose Calculations; Revision 7  
  Licenses For Nuclear Power Plants; February 7, 1996
- ACE 01670172; Licensed Operator Had Expired Respirator Qualifications  
- AR01670172; Challenge To Shift Staffing Due To Expired Respirator Quals
4OA2 Identification and Resolution of Problems
- AR01747094; Documentation Error For Proficiency Watch
- ANSI N18-1-1971; Selection And Training Of Nuclear Power Plant Personnel; March 8, 1971  
- AR01747333; Alignment Question With Proficiency Watch Procedures
- ANSI/ANS-3.4-1996; Medical Certification And Monitoring Of Personnel Requiring Operator  
- AR01761339; Med- Changes Made To Respiratory Protection Program
Licenses For Nuclear Power Plants; February 7, 1996  
- AR01763219; Individual Did Not Show Up For Fit Tests
- AR01670172; Challenge To Shift Staffing Due To Expired Respirator Quals  
- AR01764968; Operations Respiration Qual Check Shortcomings
- AR01747094; Documentation Error For Proficiency Watch  
- AR01765896; Individual Respirator Fit Tested Not IAW Procedure
- AR01747333; Alignment Question With Proficiency Watch Procedures  
- AR01772196; Definition Of Annual In Site Programs Needs Review
- AR01761339; Med- Changes Made To Respiratory Protection Program  
                                              11                                  Attachment
- AR01763219; Individual Did Not Show Up For Fit Tests  
- AR01764968; Operations Respiration Qual Check Shortcomings  
- AR01765896; Individual Respirator Fit Tested Not IAW Procedure  
- AR01772196; Definition Of Annual In Site Programs Needs Review  


- AR01772226; Four Watch Restrictions Due To Respirator Fit Test Inserts
- AR01772307; CR 01764968 Completed With Incomplete Actions
12
- AR01779753; 2Q12 NRC URI - Modification Turnover Process
Attachment
- ES-605; License Maintenance, License Renewal Applications, And Requests For
  Administrative Reviews And Hearings
- AR01772226; Four Watch Restrictions Due To Respirator Fit Test Inserts  
- FPER; Fire Protection Evaluation Report; Revision 12
- AR01772307; CR 01764968 Completed With Incomplete Actions  
- FSAR Section 11.4; Radiation Protection Program; UFSAR 2010
- AR01779753; 2Q12 NRC URI - Modification Turnover Process  
- NP 1.1.4; Use And Adherence Of Procedures; Revision 27
- ES-605; License Maintenance, License Renewal Applications, And Requests For  
- NP 2.1.1; Conduct Of Operations; Revision 13
Administrative Reviews And Hearings  
- NP 4.2.32; Respiratory Protection Program; Revision 7
- FPER; Fire Protection Evaluation Report; Revision 12  
- NRC Information Notice 95-23; Control Room Staffing Below Minimum Regulatory
- FSAR Section 11.4; Radiation Protection Program; UFSAR 2010  
  Requirements; April 24, 1995
- NP 1.1.4; Use And Adherence Of Procedures; Revision 27  
- NRC Information Notice 97-66; Failure To Provide Special Lenses For Operators Using
- NP 2.1.1; Conduct Of Operations; Revision 13  
  Respirator Or Self-Contained Breathing apparatus During Emergency Operations;
- NP 4.2.32; Respiratory Protection Program; Revision 7  
  August 20, 1997
- NRC Information Notice 95-23; Control Room Staffing Below Minimum Regulatory  
- NUREG/CR-6838; Technical Basis For Regulatory Guidance For Assessing Exemption
Requirements; April 24, 1995  
  Requests From The Nuclear Power Plant Licenses Operator Staffing Requirements Specified
- NRC Information Notice 97-66; Failure To Provide Special Lenses For Operators Using  
  In 10 CFR 50.54(m); February 2004
Respirator Or Self-Contained Breathing apparatus During Emergency Operations;  
- OM 1.1; Conduct Of Plant Operations, PBNP Specific; Revision 36
August 20, 1997  
- OM 3.1; Operations Shift Staffing Requirements; Revision 16
- NUREG/CR-6838; Technical Basis For Regulatory Guidance For Assessing Exemption  
- OM 3.10; Operations Personnel Assignments And Scheduling; Revision 31
Requests From The Nuclear Power Plant Licenses Operator Staffing Requirements Specified  
- OM 3.9; Watchstation Status Checks And Watchstander Turnover Guides; Revision 17
In 10 CFR 50.54(m); February 2004  
- OP-AA-100-1000; Conduct Of Operations; Revision 1
- OM 1.1; Conduct Of Plant Operations, PBNP Specific; Revision 36  
- Operations Department Clock Reset - Yellow Sheet, CAP 01670172; Completed
- OM 3.1; Operations Shift Staffing Requirements; Revision 16  
  July 25, 2011
- OM 3.10; Operations Personnel Assignments And Scheduling; Revision 31  
- PBN IS TP; Training Program Description; Revision 14
- OM 3.9; Watchstation Status Checks And Watchstander Turnover Guides; Revision 17  
- PBN LOC TPD; Training Program Description; Completed September 12, 2011
- OP-AA-100-1000; Conduct Of Operations; Revision 1  
- Plateau Curricula Status List; As Of May 9, 2012
- Operations Department Clock Reset - Yellow Sheet, CAP 01670172; Completed  
- Unit Staff Qualifications 5.3; Unit - Amendment No. 211, Unit 2 - Amendment No. 216
July 25, 2011  
- WO Package 40118739-01; Verify Operators Respiratory Qualifications
- PBN IS TP; Training Program Description; Revision 14  
4OA3 Follow-Up of Events and Notices of Enforcement Discretion
- PBN LOC TPD; Training Program Description; Completed September 12, 2011  
- 0-SOP-G02-001; Maintenance Operation For EDG G-02; Completed April 26, 2012
- Plateau Curricula Status List; As Of May 9, 2012  
- 1ICP 10.046; Check Of Rod Control System Redundant Power Supplies; Revision 1
- Unit Staff Qualifications 5.3; Unit - Amendment No. 211, Unit 2 - Amendment No. 216  
- 2F3201 Forced Outage Critical Path; June 27, 2012
- WO Package 40118739-01; Verify Operators Respiratory Qualifications  
- 2F32HS Forced Outage Issues And Actions
- 0-SOP-G02-001; Maintenance Operation For EDG G-02; Completed April 26, 2012  
- 2-SOP-19KV-001; Transformers 2X-01/2X-02 Outages And Electrical Operations; Completed
4OA3 Follow-Up of Events and Notices of Enforcement Discretion
  April 11, 2012
- 1ICP 10.046; Check Of Rod Control System Redundant Power Supplies; Revision 1  
- ACE 01640098-01; AFI In The Area Of Equipment Reliability During January 2011 INPO E&A;
- 2F3201 Forced Outage Critical Path; June 27, 2012  
  Revision 3
- 2F32HS Forced Outage Issues And Actions  
- Agenda For Operations Burden Review Meeting; May 30, 2012
- 2-SOP-19KV-001; Transformers 2X-01/2X-02 Outages And Electrical Operations; Completed  
- AR01640098; 2011 INPO Eval AFI ER.2-1: PMS Of Some Electrical Components
April 11, 2012  
- AR01724425; Controller Not Controlling At Set Flow Rate
- ACE 01640098-01; AFI In The Area Of Equipment Reliability During January 2011 INPO E&A;  
- AR01743615; Increase In Operations Requested Emergent PCRS
Revision 3  
- AR01752251; Control Room Deficiencies Changed From White To Yellow
- Agenda For Operations Burden Review Meeting; May 30, 2012  
- AR01757638; Unanticipated Axial Flux Response During Load Swing
- AR01640098; 2011 INPO Eval AFI ER.2-1: PMS Of Some Electrical Components  
- CE For AR01750489; Progress On INPO AFI ER.2-1; April 12, 2012
- AR01724425; Controller Not Controlling At Set Flow Rate  
- Daily Status Report; June 29, 2012
- AR01743615; Increase In Operations Requested Emergent PCRS  
- EC 274720; 2F52-142; A And C Phase Grid Side Jumpers
- AR01752251; Control Room Deficiencies Changed From White To Yellow  
                                              12                                  Attachment
- AR01757638; Unanticipated Axial Flux Response During Load Swing  
- CE For AR01750489; Progress On INPO AFI ER.2-1; April 12, 2012  
- Daily Status Report; June 29, 2012  
- EC 274720; 2F52-142; A And C Phase Grid Side Jumpers  


- EN48053; Unit 2 Manual Reactor Actuated Due To Indications Of 100% Load Rejection;
  June 27, 2012
13
- EN47896; Licensed Operating Supervisor Tested Positive For A For-Cause Test For Alcohol;
Attachment
  May 3, 2012
- ER.2-1 Strength Plan
- EN48053; Unit 2 Manual Reactor Actuated Due To Indications Of 100% Load Rejection;  
- Incident Investigation And Post-Trip Reviews; Completed June 27, 2012
June 27, 2012  
- NARS Forms; April 25, 2012
- EN47896; Licensed Operating Supervisor Tested Positive For A For-Cause Test For Alcohol;  
- Nextera Energy Life Cycle Management Plan; November 26, 2012
May 3, 2012  
- NP 2.1.4; Operator Burdens; Revision 14
- ER.2-1 Strength Plan  
- NPM 2012-0111; Internal Correspondence From D. Weber; Subject: Operator Burden Review
- Incident Investigation And Post-Trip Reviews; Completed June 27, 2012  
  Board Meeting Minutes; April 4, 2012
- NARS Forms; April 25, 2012  
- OI 38; Circulating Water System Operation; Revision 56
- Nextera Energy Life Cycle Management Plan; November 26, 2012  
- OP 1C; Startup To Power Operation Unit 2; Revision 24
- NP 2.1.4; Operator Burdens; Revision 14  
- OP 3A Unit 1; Power Operation To Hot Standby Unit 1; Revision 9
- NPM 2012-0111; Internal Correspondence From D. Weber; Subject: Operator Burden Review  
- OP 3B; Reactor Shutdown; Revision 43
Board Meeting Minutes; April 4, 2012  
- OP-AA-108; Oversight And Control Of Operator Burdens; Revision 0
- OI 38; Circulating Water System Operation; Revision 56  
- Open POD List; Indicator OX-14; April 2012
- OP 1C; Startup To Power Operation Unit 2; Revision 24  
- PBNP Outage Status Report; June 29, 2012
- OP 3A Unit 1; Power Operation To Hot Standby Unit 1; Revision 9  
- PBNP Shutdown Safety Assessment And Fire Condition; Unit 2; June 29, 2012
- OP 3B; Reactor Shutdown; Revision 43  
- PBNP Subcomponent PM Optimization Charter; April 10, 2012
- OP-AA-108; Oversight And Control Of Operator Burdens; Revision 0  
- PBNP Unit 2 Forced Outage List; As Of April 17, April 19, 2012
- Open POD List; Indicator OX-14; April 2012  
- PBNP Unit 2; Forced Outage List; As Of June 29, 2012
- PBNP Outage Status Report; June 29, 2012  
- PFNP U2 cycle 32 F52-142 Repair Mode; April 13, April 17, 2012
- PBNP Shutdown Safety Assessment And Fire Condition; Unit 2; June 29, 2012  
- POD; May 2, 2012
- PBNP Subcomponent PM Optimization Charter; April 10, 2012  
- Response to NRC Questions Received; Dated June 11, 2012
- PBNP Unit 2 Forced Outage List; As Of April 17, April 19, 2012  
- Safety Monitor, Unit 1; June 27 To 28, 2012
- PBNP Unit 2; Forced Outage List; As Of June 29, 2012  
- Safety Monitor, Unit 2; June 27, 2012
- PFNP U2 cycle 32 F52-142 Repair Mode; April 13, April 17, 2012  
- Station Log; April 19 To April 21, 2012
- POD; May 2, 2012  
- Station Log; June 27 To June 29, 2012
- Response to NRC Questions Received; Dated June 11, 2012  
- Station Log; Various Dates From April 8 To April 27, 2012
- Safety Monitor, Unit 1; June 27 To 28, 2012  
- Unit 2 Planned Outage Shift Coverage; Begins April 19, 2012
- Safety Monitor, Unit 2; June 27, 2012  
- Westinghouse Simulator Handbook; Summary Of Protection Grade Interlocks; Revision 1107
- Station Log; April 19 To April 21, 2012  
- WO 40106974-01; Unit 2 345 KV Output Breaker; April 12, 2012
- Station Log; June 27 To June 29, 2012  
4OA5 Other Activities
- Station Log; Various Dates From April 8 To April 27, 2012  
- AR01380059; NEI Buried Piping Initiative; January 11, 2010
- Unit 2 Planned Outage Shift Coverage; Begins April 19, 2012  
- AR01660378; 2N-31 SRNI HVPS Failed High
- Westinghouse Simulator Handbook; Summary Of Protection Grade Interlocks; Revision 1107  
- AR01687256; June 13 Unit 2 Rx Trip LER/PI Data Needs Revision
- WO 40106974-01; Unit 2 345 KV Output Breaker; April 12, 2012  
- AR01762573 Buried And Underground Piping And Tanks Inspection; May 2, 2012
- AR01380059; NEI Buried Piping Initiative; January 11, 2010  
- ENG-ER-AA-102; Buried Piping Program Manager Qualification Guide; Revision 1
4OA5 Other Activities
- ER-AA-102; Buried Piping Program; Revision 3
- AR01660378; 2N-31 SRNI HVPS Failed High  
- ER-AA-102-1000; Buried Piping Examination Procedure; Revision 1
- AR01687256; June 13 Unit 2 Rx Trip LER/PI Data Needs Revision  
- LER 05000301/2011-004-00; Automatic Reactor Trip During Startup Physics Testing Due To
- AR01762573 Buried And Underground Piping And Tanks Inspection; May 2, 2012  
  Source Range Detector Failure; July 25, 2011
- ENG-ER-AA-102; Buried Piping Program Manager Qualification Guide; Revision 1  
- LER 05000301/2011-004-01; Automatic Reactor Trip During Startup Physics Testing Due To
- ER-AA-102; Buried Piping Program; Revision 3  
  Source Range Detector Failure; October 13, 2011
- ER-AA-102-1000; Buried Piping Examination Procedure; Revision 1  
- LR-AMP-018-BSMON; Buried Services Monitoring Program Basis Document For License
- LER 05000301/2011-004-00; Automatic Reactor Trip During Startup Physics Testing Due To  
  Renewal; Revision 0
Source Range Detector Failure; July 25, 2011  
- PBNP Buried Piping Inspection Plan; Revision 1
- LER 05000301/2011-004-01; Automatic Reactor Trip During Startup Physics Testing Due To  
- PBSA-12-21; Quick Hit Assessment Report; March 29, 2012
Source Range Detector Failure; October 13, 2011  
                                              13                                Attachment
- LR-AMP-018-BSMON; Buried Services Monitoring Program Basis Document For License  
Renewal; Revision 0  
- PBNP Buried Piping Inspection Plan; Revision 1  
- PBSA-12-21; Quick Hit Assessment Report; March 29, 2012  


- Program Health Report; Buried Piping; January 1 To March 31, 2012
- Program Health Report; Cathodic Protection; January 1 To March 31, 2012
14
- RCA 01660378; Unit 2 Reactor Trip Due To 2N31 High Level Trip; July 26 And July 14, 2011
Attachment
- SEM 8.0; Buried Services Monitoring Program; Revision 0
                                            14                                  Attachment
- Program Health Report; Buried Piping; January 1 To March 31, 2012  
- Program Health Report; Cathodic Protection; January 1 To March 31, 2012  
- RCA 01660378; Unit 2 Reactor Trip Due To 2N31 High Level Trip; July 26 And July 14, 2011  
- SEM 8.0; Buried Services Monitoring Program; Revision 0  


                        LIST OF ACRONYMS USED
AC   Alternating Current
15
ADAMS Agencywide Document Access Management System
Attachment
AFW   Auxiliary Feedwater
ALARA As-Low-As-Is-Reasonably-Achievable
LIST OF ACRONYMS USED  
AOP   Abnormal Operating Procedure
AC  
ASME American Society of Mechanical Engineers
Alternating Current  
BOL   Beginning Of Life
ADAMS  
CAP   Corrective Action Program
Agencywide Document Access Management System  
CCW   Component Cooling Water
AFW  
CFR   Code of Federal Regulations
Auxiliary Feedwater  
CR   Condition Report
ALARA  
DRP   Division of Reactor Projects
As-Low-As-Is-Reasonably-Achievable  
EDG   Emergency Diesel Generator
AOP  
EPU   Extended Power Uprate
Abnormal Operating Procedure  
FP   Fire Protection
ASME  
FSAR Final Safety Analysis Report
American Society of Mechanical Engineers  
FW   Feedwater
BOL  
HEPA High Efficiency Particulate Air
Beginning Of Life  
IP   Inspection Procedure
CAP  
IR   Inspection Report
Corrective Action Program  
kV   Kilovolt
CCW  
LER   Licensee Event Report
Component Cooling Water  
MFIV Main Feedwater Isolation Valve
CFR  
MSIV Main Steam Isolation Valve
Code of Federal Regulations  
NCV   Non-Cited Violation
CR  
NEI   Nuclear Energy Institute
Condition Report  
NFPA National Fire Protection Association
DRP  
NRC   U.S. Nuclear Regulatory Commission
Division of Reactor Projects  
OWA   Operator Workaround
EDG  
PAB   Primary Auxiliary Building
Emergency Diesel Generator  
PARS Publicly Available Records System
EPU  
PI   Performance Indicator
Extended Power Uprate  
PMT   Post-Maintenance Testing
FP  
RCS   Reactor Coolant System
Fire Protection  
RHR   Residual Heat Removal
FSAR  
SDP   Significance Determination Process
Final Safety Analysis Report  
SI   Safety Injection
FW  
SR   Safety-Related
Feedwater  
SRM   Source Range Monitor
HEPA  
SSC   Structure, System, and Component
High Efficiency Particulate Air  
SW   Service Water
IP  
TDAFW Turbine-Driven Auxiliary Feedwater
Inspection Procedure  
TEDE Total Effective Dose Equivalent
IR  
TI   Temporary Instruction
Inspection Report  
TS   Technical Specification
kV  
TSC   Technical Support Center
Kilovolt
URI   Unresolved Item
LER  
WO   Work Order
Licensee Event Report  
                                      15          Attachment
MFIV  
Main Feedwater Isolation Valve  
MSIV  
Main Steam Isolation Valve  
NCV  
Non-Cited Violation  
NEI  
Nuclear Energy Institute  
NFPA  
National Fire Protection Association  
NRC  
U.S. Nuclear Regulatory Commission  
OWA  
Operator Workaround  
PAB  
Primary Auxiliary Building  
PARS  
Publicly Available Records System  
PI  
Performance Indicator  
PMT  
Post-Maintenance Testing  
RCS  
Reactor Coolant System  
RHR  
Residual Heat Removal  
SDP  
Significance Determination Process  
SI  
Safety Injection  
SR  
Safety-Related  
SRM  
Source Range Monitor  
SSC  
Structure, System, and Component  
SW  
Service Water  
TDAFW  
Turbine-Driven Auxiliary Feedwater  
TEDE  
Total Effective Dose Equivalent  
TI  
Temporary Instruction  
TS  
Technical Specification  
TSC  
Technical Support Center  
URI  
Unresolved Item  
WO  
Work Order  


L. Meyer                                                                   -2-
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its
enclosure, and your response (if any) will be available electronically for public inspection in the
L. Meyer  
NRC Public Document Room or from the Publicly Available Records System (PARS)
-2-  
component of NRC's Agencywide Document Access and Management System (ADAMS).
ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html
(the Public Electronic Reading Room).
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its  
                                                                          Sincerely,
enclosure, and your response (if any) will be available electronically for public inspection in the  
                                                                          /RA/
NRC Public Document Room or from the Publicly Available Records System (PARS)  
                                                                          Michael A. Kunowski, Branch Chief
component of NRC's Agencywide Document Access and Management System (ADAMS).
                                                                          Branch 5
ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html
                                                                          Division of Reactor Projects
(the Public Electronic Reading Room).  
Docket Nos.: 05000266; 05000301
Sincerely,  
License Nos.: DPR-24; DPR-27
Enclosure: Inspection Report 05000266/2012003 and 05000301/2012003;
/RA/  
                            w/Attachment: Supplemental Information
cc w/encl:               Distribution via ListServ
DISTRIBUTION:
Michael A. Kunowski, Branch Chief  
See next page
Branch 5  
DOCUMENT NAME: PTBH 2012003.docx
Division of Reactor Projects  
    Publicly Available                           Non-Publicly Available                   Sensitive                 Non-Sensitive
To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" = Copy with attach/encl "N" = No copy
Docket Nos.: 05000266; 05000301  
  OFFICE             RIII                                 RIII                           RIII                               RIII
License Nos.: DPR-24; DPR-27  
  NAME               MKunowski:rj
Enclosure: Inspection Report 05000266/2012003 and 05000301/2012003;  
  DATE               08/03/12
  w/Attachment: Supplemental Information  
                                                          OFFICIAL RECORD COPY
cc w/encl:  
Distribution via ListServ  
DISTRIBUTION:  
See next page  
DOCUMENT NAME: PTBH 2012003.docx
Publicly Available  
Non-Publicly Available  
Sensitive  
Non-Sensitive  
To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" = Copy with attach/encl "N" = No copy  
   
OFFICE  
RIII  
RIII  
RIII  
RIII  
   
NAME  
MKunowski:rj  
   
DATE  
08/03/12  
OFFICIAL RECORD COPY  


Letter to L. Meyer from M. Kunowski dated August 3, 2012
SUBJECT:       POINT BEACH NUCLEAR PLANT, UNITS 1 AND 2
              NRC INTEGRATED INSPECTION REPORT 05000266/2012003 AND
Letter to L. Meyer from M. Kunowski dated August 3, 2012  
              05000301/2012003
DISTRIBUTION:
SUBJECT:  
Silas Kennedy
POINT BEACH NUCLEAR PLANT, UNITS 1 AND 2  
RidsNrrDorlLpl3-1 Resource
RidsNrrPMPointBeach
NRC INTEGRATED INSPECTION REPORT 05000266/2012003 AND  
RidsNrrDirsIrib Resource
05000301/2012003  
Chuck Casto
Cynthia Pederson
DISTRIBUTION:  
Steven Orth
Silas Kennedy
Jared Heck
RidsNrrDorlLpl3-1 Resource  
Allan Barker
RidsNrrPMPointBeach  
Carole Ariano
RidsNrrDirsIrib Resource  
Linda Linn
Chuck Casto  
DRPIII
Cynthia Pederson  
DRSIII
Steven Orth  
Patricia Buckley
Jared Heck  
Tammy Tomczak
Allan Barker  
Carole Ariano  
Linda Linn  
DRPIII  
DRSIII  
Patricia Buckley  
Tammy Tomczak  
ROPreports.Resource@nrc.gov
ROPreports.Resource@nrc.gov
}}
}}

Latest revision as of 23:11, 11 January 2025

IR 05000266-12-003, 05000301-12-003; 04/01/2012 - 06/30/2012; Point Beach Nuclear Plant, Units 1 and 2; Post-Maintenance Testing; In-Plant Airborne Radioactivity Control and Mitigation; and Follow Up of Events and Notices of Enforcement Dis
ML12216A393
Person / Time
Site: Point Beach  NextEra Energy icon.png
Issue date: 08/03/2012
From: Michael Kunowski
NRC/RGN-III/DRP/B5
To: Meyer L
Point Beach
References
IR-12-003
Download: ML12216A393 (50)


See also: IR 05000266/2012003

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION III

2443 WARRENVILLE ROAD, SUITE 210

LISLE, IL 60532-4352

August 3, 2012

Mr. Larry Meyer

Site Vice President

NextEra Energy Point Beach, LLC

6610 Nuclear Road

Two Rivers, WI 54241

SUBJECT:

POINT BEACH NUCLEAR PLANT, UNITS 1 AND 2

NRC INTEGRATED INSPECTION REPORT 05000266/2012003 AND

05000301/2012003

Dear Mr. Meyer:

On June 30, 2012, the U.S. Nuclear Regulatory Commission (NRC) completed an integrated

inspection at your Point Beach Nuclear Plant, Units 1 and 2. The enclosed report documents

the inspection findings, which were discussed on June 26, 2012, with you and members of your

staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

Two NRC-identified findings and one self-revealing finding of very low safety significance were

identified during this inspection.

These findings were determined to involve violations of NRC requirements. The NRC is treating

these violations as non-cited violations (NCVs), consistent with Section 2.3.2 of the

Enforcement Policy.

If you contest the subject or severity of these NCVs, you should provide a response within

30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear

Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with a

copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III,

2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement,

U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector

Office at the Point Beach Nuclear Plant. In addition, if you disagree with the cross-cutting

aspect assigned to any finding in this report, you should provide a response within 30 days of

the date of this inspection report, with the basis for your disagreement, to the Regional

Administrator, Region III, and the NRC Resident Inspector at the Point Beach Nuclear Plant.

L. Meyer

-2-

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its

enclosure, and your response (if any) will be available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records System (PARS)

component of NRC's Agencywide Document Access and Management System (ADAMS).

ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html

(the Public Electronic Reading Room).

Sincerely,

/RA/

Michael A. Kunowski, Branch Chief

Branch 5

Division of Reactor Projects

Docket Nos.: 05000266; 05000301

License Nos.: DPR-24; DPR-27

Enclosure: Inspection Report 05000266/2012003 and 05000301/2012003;

w/Attachment: Supplemental Information

cc w/encl:

Distribution via ListServ

Enclosure

U.S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket Nos.:

05000266; 05000301

License Nos.:

DPR-24; DPR-27

Report No.:

05000266/2012003; 05000301/2012003

Licensee:

NextEra Energy Point Beach, LLC

Facility:

Point Beach Nuclear Plant, Units 1 and 2

Location:

Two Rivers, WI

Dates:

April 1, 2012, through June 30, 2012

Inspectors:

S. Burton, Senior Resident Inspector

M. Thorpe-Kavanaugh, Resident Inspector

R. Krsek, Senior Resident Inspector (Kewaunee)

M. Phalen, Senior Health Physicist

V. Myers, Health Physicist

T. Bilik, Senior Reactor Engineer

V. Meghani, Reactor Inspector

A. Dahbur, Senior Reactor Engineer

M. Learn, Reactor Engineer

J. Bozga, Reactor Engineer

C. Zoia, Operations Engineer

Approved by:

Michael A. Kunowski, Branch Chief

Branch 5

Division of Reactor Projects

Enclosure

TABLE OF CONTENTS

SUMMARY OF FINDINGS ......................................................................................................... 1

REPORT DETAILS .................................................................................................................... 4

Summary of Plant Status ........................................................................................................ 4

1.

REACTOR SAFETY .................................................................................................... 4

1R01

Adverse Weather Protection (71111.01) ............................................................ 4

1R04

Equipment Alignment (71111.04) ...................................................................... 6

1R05

Fire Protection (71111.05) ................................................................................. 7

1R06

Flooding (71111.06) .......................................................................................... 7

1R11

Licensed Operator Requalification Program (71111.11) .................................... 8

1R12

Maintenance Effectiveness (71111.12) .............................................................. 9

1R13

Maintenance Risk Assessments and Emergent Work Control (71111.13) ........10

1R15

Operability Determinations and Functional Assessments (71111.15) ...............11

1R18

Plant Modifications (71111.18) .........................................................................11

1R19

Post-Maintenance Testing (71111.19) ..............................................................12

1R20

Outage Activities (71111.20) ............................................................................15

1R22

Surveillance Testing (71111.22) .......................................................................15

1EP6

Drill Evaluation (71114.06) ...............................................................................16

2.

RADIATION SAFETY .................................................................................................17

2RS3

In-Plant Airborne Radioactivity Control and Mitigation (71124.03) ....................17

4.

OTHER ACTIVITIES ...................................................................................................19

4OA1

Performance Indicator Verification (71151) .......................................................19

4OA2

Identification and Resolution of Problems (71152) ............................................22

4OA3

Follow-Up of Events and Notices of Enforcement Discretion (71153) ...............25

4OA5

Other Activities .................................................................................................28

4OA6

Management Meetings .....................................................................................29

4OA7

Licensee-Identified Violations ...........................................................................29

SUPPLEMENTAL INFORMATION ............................................................................................. 1

Key Points of Contact ............................................................................................................. 1

List of Items Opened, Closed and Discussed ......................................................................... 2

List of Documents Reviewed .................................................................................................. 3

List of Acronyms Used ...........................................................................................................15

1

Enclosure

SUMMARY OF FINDINGS

IR 05000266/2012003, 05000301/2012003; 04/01/2012 - 06/30/2012; Point Beach Nuclear

Plant, Units 1 and 2; Post-Maintenance Testing; In-Plant Airborne Radioactivity Control and

Mitigation; and Follow-Up of Events and Notices of Enforcement Discretion.

This report covers a 3-month period of inspection by resident inspectors and announced

baseline inspections by regional inspectors. Two Green NRC-identified findings and one Green

self-revealing finding were identified during this inspection. The findings were considered

non-cited violations (NCVs) of NRC regulations. The significance of most findings is indicated

by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609,

Significance Determination Process (SDP). Findings for which the SDP does not apply may

be Green or be assigned a severity level after NRC management review. The NRCs program

for overseeing the safe operation of commercial nuclear power reactors is described in

NUREG-1649, Reactor Oversight Process, Revision 4, dated December 2006.

A.

Cornerstone: Initiating Events

NRC-Identified and Self-Revealed Findings

Green

The finding was determined to be more than minor in accordance with Inspection

Manual Chapter 0612, Power Reactor Inspection Reports, Appendix B, Issue

Screening, dated December 24, 2009, because the finding was associated with the

Initiating Events Cornerstone attribute of equipment performance. Specifically, the

availability and reliability of the nuclear instruments was degraded to a point where an

instrument failure caused a reactor trip, an event that adversely impacted the

cornerstone objective to limit the likelihood of those events that upset plant stability and

challenge critical safety functions during power operations. The finding has a

cross-cutting aspect in the area of corrective action program, evaluation/extent of

condition. Specifically, the licensee failed to thoroughly evaluate related nuclear

instrument failure rates so that the resolutions addressed the causes and extent of

conditions for age-related failures of electrical subcomponents (P.1(c)).

(Section 4OA3.4)

. A finding of very low safety significance and associated non-cited violation of

10 CFR 50.65(a)(3) was self-revealed when an unplanned reactor trip of Unit 2 occurred

on June 13, 2011, as a result of the failure of a source range detector during low power

physics testing. Specifically, the licensee failed to adequately evaluate operating

experience and incorporate it into its preventive maintenance program to periodically

replace aging electrical subcomponents in nuclear instrumentation systems and a

subsequent age-related failure resulted in initiating a plant transient. The licensee

entered this issue into the corrective action program, and corrective actions to prevent

recurrence were initiated.

Cornerstone: Mitigating Systems

Green. The inspectors identified a finding of very low safety significance and associated

non-cited violation of 10 CFR Part 50, Appendix B, Criterion XI, "Test Control," because

the licensee failed to establish routine testing procedure that demonstrated room

temperatures would be maintained. Specifically, on March 29, 2012, the inspectors

identified that the licensee failed to establish routine testing procedure that demonstrated

2

Enclosure

the air flows for emergency diesel generators G-01 and G-02 ventilation systems would

perform adequately to ensure that the room temperatures would be maintained. The

licensee entered this issue into its corrective action program, and corrective actions

included performance of air flow measurements on the fan units, creation of a preventive

maintenance requirement for taking periodic flow measurements, and assessment of the

identified issue through a condition evaluation.

The finding was determined to be more than minor in accordance with Inspection

Manual Chapter 0612, Appendix B, Issue Screening, dated December 24, 2009. The

inspectors determined that this finding was more than minor because it was associated

with the Mitigating Systems Cornerstone attribute for design control. Specifically, it

adversely affected the Mitigating System Cornerstone objective to ensure the reliability

of systems that respond to initiating events to prevent undesirable consequences. This

finding has a cross-cutting aspect in the area of human performance, decision-making.

Specifically, the licensee did not use conservative assumptions regarding the verification

of the proper air flow through the safety-related gravity dampers in the emergency diesel

generators G-01 and G-02 rooms (H.1(b)). (Section 1R19)

Cornerstone: Occupational Radiation Safety

Green

The finding was more than minor because it was associated with the program and

process attribute of exposure control of the Occupational Radiation Safety Cornerstone

and adversely affected the cornerstone objective of ensuring the adequate protection of

worker health and safety from exposure radiation and radioactive material. Specifically,

inappropriately testing installed emergency ventilation system filters designed to

mitigate workers radiation exposures did not validate that the TSC ventilation system

was capable of performing its intended design function of minimizing worker exposures

to airborne radioactive materials. The finding was assessed using the occupational

radiation safety significance determination process and was determined to be of very

low safety significance (Green) because it was not an as-low-as-is-reasonable-

achievable planning issue, there was no overexposure or potential for overexposure,

and the licensees ability to assess dose was not compromised. The inspectors

determined that the most significant contributor to the finding was a cross-cutting aspect

in the area of human performance, resources. Specifically, the licensee failed to ensure

that the TSC ventilation filter testing protocol assured compliance to the systems

designed margins (H.2(a)). (Section 2RS3)

. The inspectors identified a finding of very low safety significance and associated

non-cited violation of 10 CFR 20.1701. Specifically, the inspectors identified

deficiencies, as of January 19, 2012, in the licensees testing program for assuring that

the technical support center (TSC) ventilation system was in compliance with the

systems design basis. The licensees TSC high efficiency particulate air and charcoal

filter efficiencies were not tested to the design criteria. The licensee documented this

issue in its corrective action program and the corrective actions included revising

applicable procedures. In addition, the licensee performed a calculation to show

that the TSC ventilation system was capable of maintaining a radiological habitability of

less than 5 Rem total effective dose equivalent for the duration of the design base

accidents. The calculation was based on actual historical filter testing efficiencies.

3

Enclosure

B.

No violations were identified.

Licensee-Identified Violations

4

Enclosure

REPORT DETAILS

Unit 1 was at 100 percent power throughout the entire inspection period with the exception of

brief downpowers to conduct planned maintenance and surveillance activities.

Summary of Plant Status

Unit 2 was at 100 percent power for the majority of the period with the exception of two planned

downpowers and one forced outage. Unit 2 was downpowered on April 20, 2012, to

approximately 15 percent power for switchyard work and on June 18, 2012, for routine auxiliary

feedwater system testing. On June 27, 2012, the unit was tripped due to a turbine control

system malfunction and remained shut down until the end of the inspection period.

1.

REACTOR SAFETY

Cornerstone: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection

.1

(71111.01)

a.

Summer Seasonal Readiness Preparations

The inspectors performed a review of the licensees preparations for summer weather

for selected systems, including conditions that could lead to an extended drought. The

inspectors reviews focused specifically on the following plant systems:

Inspection Scope

service water (SW);

component cooling water (CCW); and

primary auxiliary building (PAB) ventilation.

During the inspection, the inspectors focused on plant specific design features and the

licensees procedures used to mitigate or respond to adverse weather conditions.

Additionally, the inspectors reviewed the Final Safety Analysis Report (FSAR) and

performance requirements for systems selected for inspection, and verified that operator

actions were appropriate as specified by plant specific procedures. The inspectors also

reviewed corrective action program (CAP) items to verify that the licensee was

identifying adverse weather issues at an appropriate threshold and entering them into

the CAP in accordance with station corrective action procedures. Documents reviewed

are listed in the Attachment to this report.

This inspection constituted one seasonal adverse weather sample as defined in

Inspection Procedure (IP) 71111.01-05.

b.

No findings were identified.

Findings

5

Enclosure

.2

a.

Readiness for Impending Adverse Weather Condition - Solar Magnetic Disturbances

Since solar magnetic disturbances were forecast in the vicinity of the facility for

April 23, 2012, the inspectors reviewed the licensees overall preparations/protection for

the expected weather conditions. On April 23, 2012, the inspectors walked down the

offsite power system, in addition to the licensees emergency alternating current (AC)

power systems, because their safety-related (SR) functions could be affected or required

as a result of solar magnetic flares. The inspectors evaluated the licensees

preparations against the sites procedures and determined that the staffs actions were

adequate. During the inspection, the inspectors focused on plant-specific design

features and the licensees procedures used to respond to specified adverse weather

conditions. Additionally, inspection activities included a review of the FSAR, the

licensees adverse weather procedures, daily monitoring of the off-normal environmental

conditions, and that operator actions specified by plant-specific procedures were

appropriate to ensure operability of the facilitys systems. The inspectors also reviewed

a sample of CAP items to verify that the licensee identified adverse weather issues at an

appropriate threshold and dispositioned them through the CAP in accordance with

station corrective action procedures. Documents reviewed are listed in the Attachment

to this report.

Inspection Scope

This inspection constituted one readiness for impending adverse weather condition

sample as defined in IP 71111.01-05.

b.

No findings were identified.

Findings

.3

a.

Readiness for Impending Adverse Weather Condition - Severe Thunderstorm Watch

Since thunderstorms with potential tornados and high winds were forecast in the vicinity

of the facility for June 17, 2012, the inspectors reviewed the licensees overall

preparations/protection for the expected weather conditions. The inspectors reviewed

the actions taken by the licensee in response to the adverse weather condition while the

associated meteorological tower was out of service. The inspectors reviewed the

potential impact of the adverse weather conditions on SR equipment, in addition to the

licensees emergency AC power systems. The inspectors evaluated the licensees

preparations against the sites procedures and determined that the licensees actions

were adequate. During the inspection, the inspectors focused on plant-specific design

features and the licensees procedures used to respond to specified adverse weather

conditions. The inspectors evaluated operator staffing and accessibility of controls and

indications for those systems required to control the plant. Additionally, the inspectors

reviewed the FSAR and performance requirements for systems selected for inspection,

and verified that operator actions were appropriate as specified by plant specific

procedures. The inspectors also reviewed a sample of CAP items to verify that the

licensee identified adverse weather issues at an appropriate threshold and dispositioned

them through the CAP in accordance with station corrective action procedures.

Documents reviewed are listed in the Attachment to this report.

Inspection Scope

6

Enclosure

This inspection constituted one readiness for impending adverse weather condition

sample as defined in IP 71111.01-05.

b.

No findings were identified.

Findings

1R04 Equipment Alignment

.1

(71111.04)

a.

Quarterly Partial System Walkdowns

The inspectors performed partial system walkdowns of the following risk-significant

system:

Inspection Scope

Unit 2 safety injection (SI) system B, during surveillance testing on the opposite

train; and

Unit 1 turbine-driven auxiliary feedwater (TDAFW) pump after returned to service

following maintenance.

The inspectors selected this system based on its risk significance relative to the Reactor

Safety Cornerstones at the time it was inspected. The inspectors attempted to identify

any discrepancies that could impact the function of the system and, therefore, potentially

increase risk. The inspectors reviewed applicable operating procedures, system

diagrams, FSAR, Technical Specification (TS) requirements, outstanding work orders

(WOs), condition reports (CRs), and the impact of ongoing work activities on redundant

trains of equipment in order to identify conditions that could have rendered the systems

incapable of performing their intended functions. The inspectors also walked down

accessible portions of the system to verify system components and support equipment

were aligned correctly and operable. The inspectors examined the material condition of

the components and observed operating parameters of equipment to verify that there

were no obvious deficiencies. The inspectors also verified that the licensee had properly

identified and resolved equipment alignment problems that could cause initiating events

or impact the capability of mitigating systems or barriers and entered them into the CAP

with the appropriate significance characterization. Documents reviewed are listed in the

Attachment to this report.

These activities constituted two partial system walkdown samples as defined in

IP 71111.04-05.

b.

No findings were identified.

Findings

7

Enclosure

1R05 Fire Protection

.1

(71111.05)

Routine Resident Inspector Tours

a.

(71111.05Q)

The inspectors conducted fire protection (FP) walkdowns which were focused on

availability, accessibility, and the condition of firefighting equipment in the following

risk-significant plant areas:

Inspection Scope

fire zone 187 (monitor tank room);

fire zone 596 (Unit 2 façade);

fire zone 151 (SI pump room); and

fire zone 318 (cable spreading room).

The inspectors reviewed areas to assess if the licensee had implemented an FP

program that adequately controlled combustibles and ignition sources within the plant,

effectively maintained fire detection and suppression capability, maintained passive FP

features in good material condition, and implemented adequate compensatory measures

for out-of-service, degraded or inoperable FP equipment, systems, or features in

accordance with the licensees fire plan. The inspectors selected fire areas based on

their overall contribution to internal fire risk as documented in the plants Individual Plant

Examination of External Events with later additional insights, their potential to impact

equipment which could initiate or mitigate a plant transient, or their impact on the plants

ability to respond to a security event. Using the documents listed in the Attachment to

this report, the inspectors verified that fire hoses and extinguishers were in their

designated locations and available for immediate use; that fire detectors and sprinklers

were unobstructed; that transient material loading was within the analyzed limits; and fire

doors, dampers, and penetration seals appeared to be in satisfactory condition. The

inspectors also verified that minor issues identified during the inspection were entered

into the CAP. Documents reviewed are listed in the Attachment to this report.

These activities constituted four quarterly fire protection inspection samples as defined in

IP 71111.05-05.

b.

No findings were identified.

Findings

1R06 Flooding

.1

(71111.06)

a.

Internal Flooding

The inspectors reviewed selected risk important plant design features and licensee

procedures intended to protect the plant and its SR equipment from internal flooding

events. The inspectors reviewed flood analyses and design documents, including the

FSAR, engineering calculations, and abnormal operating procedures (AOPs) to identify

licensee commitments. In addition, the inspectors reviewed licensee drawings to identify

areas and equipment that may be affected by internal flooding caused by the failure or

Inspection Scope

8

Enclosure

misalignment of nearby sources of water, such as the fire suppression or the circulating

water systems. The inspectors also reviewed the licensees corrective action documents

with respect to past flood-related items identified in the CAP to verify the adequacy of

the corrective actions. The inspectors performed a walkdown of the following plant area

to assess the adequacy of watertight doors and verify drains and sumps were clear of

debris and were operable, and that the licensee complied with its commitments.

Documents reviewed are listed in the Attachment to this report.

residual heat removal (RHR) rooms.

This inspection constituted one internal flooding sample as defined in IP 71111.06-05.

b.

No findings were identified.

Findings

1R11 Licensed Operator Requalification Program

.1

(71111.11)

Resident Inspector Quarterly Review

a.

(71111.11Q)

On May 21, 2012, the inspectors observed a crew of licensed operators in the plants

simulator during licensed operator requalification examinations to verify that operator

performance was adequate, evaluators were identifying and documenting crew

performance problems, and that training was being conducted in accordance with

licensee procedures. The inspectors evaluated the following areas:

Inspection Scope

licensed operator performance;

crews clarity and formality of communications;

ability to take timely actions in the conservative direction;

prioritization, interpretation, and verification of annunciator alarms;

correct use and implementation of abnormal and emergency procedures;

control board manipulations;

oversight and direction from supervisors; and

ability to identify and implement appropriate TS actions and Emergency Plan

actions and notifications.

The crews performance in these areas was compared to pre-established operator action

expectations and successful critical task completion requirements. Documents reviewed

are listed in the Attachment to this report.

This inspection constituted one quarterly licensed operator requalification program

simulator sample as defined in IP 71111.11.

b.

No findings were identified.

Findings

9

Enclosure

.2

Resident Inspector Quarterly Observation of Heightened Activity or Risk

a.

(71111.11Q)

On April 20 and 21, 2012, the inspectors observed activities in the control room during

the high risk activity of a Unit 2 downpower to 15 percent to secure one train of main

feedwater (FW). This was an activity that required heightened awareness or was related

to increased risk. The inspectors evaluated the following areas:

Inspection Scope

licensed operator performance;

crews clarity and formality of communications;

ability to take timely actions in the conservative direction;

prioritization, interpretation, and verification of annunciator alarms;

correct use and implementation of procedures;

control board manipulations; and

oversight and direction from supervisors.

The performance in these areas was compared to pre-established operator action

expectations, procedural compliance, and task completion requirements. Documents

reviewed are listed in the Attachment to this report.

This inspection constituted one quarterly licensed operator heightened activity/risk

sample as defined in IP 71111.11.

b.

No findings were identified.

Findings

1R12 Maintenance Effectiveness

.1

(71111.12)

Routine Quarterly Evaluations

a.

(71111.12Q)

The inspectors evaluated degraded performance issues involving the following

risk-significant system:

Inspection Scope

TDAFW system.

The inspectors reviewed events, such as where ineffective equipment maintenance had

resulted in valid or invalid automatic actuations of engineered safeguards systems, and

independently verified the licensee's actions to address system performance or condition

problems in terms of the following:

implementing appropriate work practices;

identifying and addressing common cause failures;

scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;

characterizing system reliability issues for performance;

charging unavailability for performance;

trending key parameters for condition monitoring;

ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or re-classification; and

10

Enclosure

verifying appropriate performance criteria for structures, systems, and

components (SSCs)/functions classified as (a)(2), or appropriate and adequate

goals and corrective actions for systems classified as (a)(1).

The inspectors assessed performance issues with respect to the reliability, availability,

and condition monitoring of the system. In addition, the inspectors verified maintenance

effectiveness issues were entered into the CAP with the appropriate significance

characterization. Documents reviewed are listed in the Attachment to this report.

This inspection constituted one quarterly maintenance effectiveness samples as defined

in IP 71111.12-05.

b.

No findings were identified.

Findings

1R13 Maintenance Risk Assessments and Emergent Work Control

.1

(71111.13)

a.

Maintenance Risk Assessments and Emergent Work Control

The inspectors reviewed the licensee's evaluation and management of plant risk for the

maintenance and emergent work activities affecting risk-significant and SR equipment

listed below to verify that the appropriate risk assessments were performed prior to

removing equipment for work:

Inspection Scope

risk management of 345-kilovolt (kV) output breaker hotspot with increasing

outside air temperatures;

risk management with CCW heat exchanger C inoperable but available;

risk management with emergency diesel generators (EDGs) G-01 and G-02

inoperable week of April 26; and

risk management with Unit 1 TDAFW pump and gas turbine generator

out-of-service.

These activities were selected based on their potential risk significance relative to the

Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified that

risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate

and complete. When emergent work was performed, the inspectors verified that the

plant risk was promptly reassessed and managed. The inspectors reviewed the scope

of maintenance work, discussed the results of the assessment with the licensee's

probabilistic risk analyst or shift technical advisor, and verified plant conditions were

consistent with the risk assessment. The inspectors also reviewed TS requirements and

walked down portions of redundant safety systems, when applicable, to verify risk

analysis assumptions were valid and applicable requirements were met. Documents

reviewed are listed in the Attachment to this report.

These activities constituted four maintenance risk assessments and emergent work

control samples as defined in IP 71111.13-05.

11

Enclosure

b.

No findings were identified.

Findings

1R15 Operability Determinations and Functional Assessments

.1

(71111.15)

a.

Operability Evaluations

The inspectors reviewed the following operability issues:

Inspection Scope

control room board deficiencies and abandoned in-place modifications;

containment fan cooler unit closed drain valves (Unit 2);

SI with non-conservative gas void acceptance criteria;

water leaking in steam generator A vault (Unit 2) (partial);

TDAFW failed coupling (Unit 1) (partial); and

cable spreading room.

The inspectors selected these potential operability issues based on the risk significance

of the associated components and systems. The inspectors evaluated the technical

adequacy of the evaluations to ensure that TS operability was properly justified and the

subject component or system remained available such that no unrecognized increase in

risk occurred. The inspectors compared the operability and design criteria in the

appropriate sections of the TSs and FSAR to the licensees evaluations to determine

whether the components or systems were operable. Where compensatory measures

were required to maintain operability, the inspectors determined whether the measures

in place would function as intended and were properly controlled. The inspectors

determined, where appropriate, compliance with bounding limitations associated with the

evaluations. Additionally, the inspectors reviewed a sampling of corrective action

documents to verify that the licensee was identifying and correcting any deficiencies

associated with operability evaluations. Documents reviewed are listed in the

Attachment to this report.

This inspection constituted four completed and two partial operability samples as defined

in IP 71111.15-05.

b.

No findings were identified.

Findings

1R18 Plant Modifications

.1

(71111.18)

a.

Plant Modifications

The inspectors reviewed the following modification(s):

Inspection Scope

main feedwater isolation valve (MFIV) curtains (permanent);

main steam isolation valve (MSIV) air line leak repair (temporary);

EDG exhaust (temporary) (partial); and

12

Enclosure

480-volt temporary power to 1B-42 loads (temporary).

The inspectors reviewed the configuration changes and associated 10 CFR 50.59 safety

evaluation screening against the design basis, the FSAR, and the TSs, as applicable, to

verify that the modification did not affect the operability or availability of the affected

systems. The inspectors, as applicable, observed ongoing and completed work

activities to ensure that the modifications were installed as directed and consistent with

the design control documents; the modifications operated as expected; post-modification

testing adequately demonstrated continued system operability, availability, and reliability;

and that operation of the modifications did not impact the operability of any interfacing

systems. As applicable, the inspectors verified that relevant procedure, design, and

licensing documents were properly updated. Lastly, the inspectors discussed the plant

modification with operations, engineering, and training personnel to ensure that the

individuals were aware of how the operation with the plant modification in place could

impact overall plant performance. Documents reviewed are listed in the Attachment to

this report.

This inspection constituted two completed temporary modification samples, one partial

temporary modification sample, and one permanent plant modification sample as

defined in IP 71111.18-05.

b.

No findings were identified.

Findings

1R19 Post-Maintenance Testing

.1

(71111.19)

a.

Post-Maintenance Testing

The inspectors reviewed the following post-maintenance testing (PMT) activities to verify

that procedures and test activities were adequate to ensure system operability and

functional capability:

Inspection Scope

PMT of PAB ventilation following low flow switch replacement (Units 1 and 2);

PMT of EDG room exhaust fan testing (Units 1 and 2);

PMT of EDG G-01 starting air compressor;

PMT of TDAFW pump after coupling repairs (Unit 1);

PMT of EDG modification (Unit 2);

PMT of main generator output breaker disconnects following hotspot repair

(Unit 2); and

PMT of main steam dump 2MS 2052 to condenser dump control valve (Unit 2).

These activities were selected based upon the SSCs ability to impact risk. The

inspectors evaluated these activities for the following (as applicable): the effect of testing

on the plant had been adequately addressed; testing was adequate for the maintenance

performed; acceptance criteria were clear and demonstrated operational readiness; test

instrumentation was appropriate; tests were performed as written in accordance with

properly reviewed and approved procedures; equipment was returned to its operational

status following testing (temporary modifications or jumpers required for test

13

Enclosure

performance were properly removed after test completion); and test documentation was

properly evaluated. The inspectors evaluated the activities against TSs, the FSAR,

10 CFR Part 50 requirements, licensee procedures, and various NRC generic

communications to ensure that the test results adequately ensured that the equipment

met the licensing basis and design requirements. In addition, the inspectors reviewed

corrective action documents associated with PMTs to determine whether the licensee

was identifying problems and entering them in the CAP, and that the problems were

being corrected commensurate with their importance to safety. Documents reviewed are

listed in the Attachment to this report.

This inspection constituted seven post-maintenance testing samples as defined in

IP 71111.19-05.

b.

Findings

Failure to Establish Emergency Diesel Generator Ventilation Damper Testing

Introduction: The inspectors identified an issue of very low safety significance (Green)

and associated non-cited violation (NCV) of 10 CFR Part 50, Appendix B, Criterion XI,

"Test Control," because the licensee failed to establish a routine testing procedure to

demonstrate that the air flows for the ventilation systems in the G-01 and G-02 EDG

rooms were sufficient to keep room temperatures maintained at or below the design

basis. The licensee entered this issue into its CAP for evaluation and development of

corrective actions.

Description

Based on this information, the inspectors reviewed the acceptance criteria for the gravity

operator louvers and found none. In response, the licensee stated the gravity louvers

had to open freely; however, a specified amount was not necessary. Additionally, the

licensee stated that the gravity operated louvers did not have specific acceptance criteria

established to ensure air flows were met and that, instead, the fan motors were used to

determine air flows. The inspectors then questioned the licensee regarding the ability to

accurately predict fan air flow outputs based on the fan motors. Also, the inspectors

questioned what additional monitoring was performed on the fans to ensure that there

was no degradation of the fan blades, no friction on the bearings, or that no bypass flow

was occurring, as well as how the test was performed in a consistent manner. The

licensee provided that there was no periodic testing to ensure air flows.

The TS 3.8.1 required, in part, that independent and redundant sources of

power be provided to the Engineered Safety Feature Systems. This was met through

each safeguard bus having a normal offsite power source and a standby emergency

power source (EDG). There were two EDGs (G-01 and G-02) that supplied power to the

Train A buses. These diesels were considered operable when the diesel room

temperature was less than 115 degrees Fahrenheit with the EDG carrying design basis

accident loads. For the room temperature to be maintained, three of the four gravity

operated louvers must be opened.

On March 29, 2012, the licensee initiated CR01750276 in response to the inspectors

concerns regarding the louvers in the G-01 and G-02 EDG rooms. Specifically, the CR

identified that air flows had not been routinely taken to ensure that adequate air flow

requirements were met. At the conclusion of the inspection period, the licensees

corrective actions included performance of air flow measurements on the fan units,

14

Enclosure

creation of a preventive maintenance requirement for taking periodic flow

measurements, and assessment of the identified issue through a condition evaluation.

Additionally, the inspectors noted that the licensee had taken air flow measurements on

the fans in 1998 and 2007, but had not established acceptance criteria and routine

testing. The inspectors noted differences between the 1998 and 2007 data obtained,

and that the licensee had used the lesser-conservative data from these tests to support

the design calculation. The inspectors questioned the use of non-conservative data

values in the design calculations for the maximum temperatures in the EDG rooms to

support operability. This concern was captured in CR1769204. The licensees planned

corrective actions were to revise the calculation to use the accurate data.

Analysis

The inspectors determined the finding could be evaluated using IMC 0609, Significance

Determination Process, Attachment 0609.04, Phase 1 - Initial Screening and

Characterization of Findings, Tables 3b and 4a, for the Mitigating Systems Cornerstone,

dated January 10, 2008. The inspectors answered No to all of the questions in the

Mitigating Systems column of Table 4a; therefore, the finding screened as having very

low safety significance (Green). The licensee entered this issue into the CAP as

AR01750276. The licensees corrective actions included performance of air flow

measurements on the fan units, creation of a preventive maintenance requirement for

taking periodic flow measurements, and assessment of the identified issue through a

condition evaluation.

The inspectors determined that the failure to establish a routine testing

procedure to demonstrate that the air flows for the G-01 and G-02 rooms would keep

room temperatures at or below the maximum allowable temperatures when the EDGs

were carrying design basis accident loads was a performance deficiency warranting

further review. Using IMC 0612, Appendix B, Issue Screening, dated

December 24, 2009, the inspectors determined that this finding was more than minor

because it was associated with the Mitigating Systems Cornerstone attribute for design

control. Specifically, it adversely affected the Mitigating System Cornerstone objective to

ensure the reliability of systems that respond to initiating events to prevent undesirable

consequences.

This finding has a cross-cutting aspect in the area of human performance,

decision-making. Specifically, the licensee did not use conservative assumptions

regarding the verification of the proper air flow through the SR gravity dampers in the

EDG G-01 and G-02 rooms (H.1(b)). The inspectors reviewed the licensees causal

assessment and found that this assessment was consistent with their assessment of the

condition.

Enforcement: Title 10 CFR 50, Appendix B, Criterion XI, "Test Control," requires, in part,

that a test program be established to assure that all testing required to demonstrate that

components will perform satisfactorily in service is identified and performed in

accordance with written test procedures which incorporate the requirements and

acceptance limits contained in applicable design documents. Contrary to this, on

March 29, 2012, the inspectors identified that the licensee failed to establish a routine

testing procedure to demonstrate that the air flows for EDGs G-01 and G-02 ventilation

systems would keep the room temperatures at or below the maximum allowable

temperatures when the EDGs were carrying design basis accident loads. Because this

violation was of very low safety significance, and it was entered into the licensees CAP

15

Enclosure

(as CR1750276), this violation is being treated as an NCV, consistent with Section 2.3.2

of the NRC Enforcement Policy (NCV 05000266/2012003-01; 05000301/2012003-01;

Failure to Establish Emergency Diesel Generator Ventilation System Testing).

1R20 Outage Activities

.1

(71111.20)

a.

Other Outage Activities

The inspectors evaluated outage activities for an unplanned Unit 2 outage that began on

June 27, 2012, and continued through the end of the inspection period. The outage

occurred as a result of a turbine control system malfunction that resulted in a turbine

load reject which terminated when the reactor operators inserted a manual reactor trip.

The inspectors reviewed activities to ensure that the licensee considered risk in

developing, planning, and implementing the outage schedule.

Inspection Scope

The inspectors observed or reviewed the reactor shutdown and cooldown, outage

equipment configuration and risk management, electrical lineups, selected clearances,

control and monitoring of decay heat removal, control of containment activities,

personnel fatigue management, startup and heatup activities, and identification and

resolution of problems associated with the outage.

This inspection constituted one other partial outage sample as defined in

IP 71111.20-05.

b.

No findings were identified.

Findings

1R22 Surveillance Testing

.1

(71111.22)

a.

Surveillance Testing

The inspectors reviewed the test results for the following activities to determine whether

risk-significant systems and equipment were capable of performing their intended safety

function, and to verify testing was conducted in accordance with applicable procedural

and TS requirements:

Inspection Scope

PAB ventilation TS-87 system monthly test (routine);

TDAFW quarterly pump and valve test (Unit 1) (inservice testing);

instrument air valves quarterly SR (Unit 2) (containment isolation valve); and

reactor coolant system (RCS) leak rate (Unit 2) (RCS).

The inspectors observed in-plant activities and reviewed procedures and associated

records to determine the following:

did preconditioning occur;

were the effects of the testing adequately addressed by control room personnel

or engineers prior to the commencement of the testing;

16

Enclosure

were acceptance criteria clearly stated, demonstrated operational readiness, and

consistent with the system design basis;

plant equipment calibration was correct, accurate, and properly documented;

as-left setpoints were within required ranges; and the calibration frequency was

in accordance with TSs, the FSAR, procedures, and applicable commitments;

measuring and test equipment calibration was current;

test equipment was used within the required range and accuracy; applicable

prerequisites described in the test procedures were satisfied;

test frequencies met TS requirements to demonstrate operability and reliability;

tests were performed in accordance with the test procedures and other

applicable procedures; jumpers and lifted leads were controlled and restored

where used;

test data and results were accurate, complete, within limits, and valid;

test equipment was removed after testing;

where applicable for inservice testing activities, testing was performed in

accordance with the applicable version of Section XI, American Society of

Mechanical Engineers (ASME) code, and reference values were consistent with

the system design basis;

where applicable, test results not meeting acceptance criteria were addressed

with an adequate operability evaluation or the SSC was declared inoperable;

where applicable for SR instrument control surveillance tests, reference setting

data were accurately incorporated in the test procedure;

where applicable, actual conditions encountering high resistance electrical

contacts were such that the intended safety function could still be accomplished;

prior procedure changes had not provided an opportunity to identify problems

encountered during the performance of the surveillance or calibration test;

equipment was returned to a position or status required to support the

performance of its safety functions; and

all problems identified during the testing were appropriately documented and

dispositioned in the CAP.

Documents reviewed are listed in the Attachment to this report.

This inspection constituted one routine surveillance testing sample, one inservice testing

sample, one reactor coolant system leak detection inspection sample, and one

containment isolation valve sample as defined in IP 71111.22, Sections -02 and -05.

b.

No findings were identified.

Findings

Cornerstone: Emergency Preparedness

1EP6 Drill Evaluation

.1

(71114.06)

a.

Emergency Preparedness Observation

The inspectors evaluated the response to a declaration of an alert condition on

April 25 to 26, 2012, to identify any weaknesses and deficiencies in classification,

Inspection Scope

17

Enclosure

notification, and protective action recommendation development activities. The licensee

declared the alert after exhaust gasses from an EDG were inadvertently taken back into

the EDG room during a test. The inspectors observed emergency response operations

in the control room and technical support center (TSC) to determine whether the event

classification, notifications, and protective action recommendations were performed in

accordance with procedures. No deficiencies were identified. Documents reviewed are

listed in the Attachment to this report.

This inspection constituted one sample as defined in IP 71114.06-05.

b.

No findings were identified.

Findings

2.

RADIATION SAFETY

Cornerstone: Occupational Radiation Safety

2RS3 In-Plant Airborne Radioactivity Control and Mitigation

This inspection constituted a partial sample as defined in IP 71124.03-05.

(71124.03)

.1

Engineering Controls

a.

(02.02)

An unresolved item (URI) was documented in NRC Integrated Inspection Report (IR)

05000266/2012002; 05000301/2012002, concerning additional information that was

needed by the inspectors to assess the licensees TSC ventilation system filter testing

program. Supplemental calculations and reviews were performed by the licensee, and

the additional information was reviewed by the inspectors. Specifically, selected

procedures, system design calculations, plant configuration drawings, and related

licensee documentation were reviewed. The inspectors completed these reviews to

verify that the licensees program and its implementation met the requirements of

10 CFR 20.1701 and were consistent with NRC guidance.

Inspection Scope

b.

Findings

Non-Compliance With 10 CFR 20.1701 to Control the Concentration of Radioactive

Material in Air and Ensure That Radiological Airborne Hazards Would Be Minimized in

the Technical Support Center During a Design-Basis Accident

Introduction: The inspectors identified a finding of very low safety significance (Green)

and associated NCV of 10 CFR 20.1701, Use of Process or Other Engineering

Controls. The inspectors identified that the licensee failed to establish adequate high

efficiency particulate air (HEPA) and charcoal filter testing procedures for ensuring that

radiological airborne hazards would be minimized and the habitability of the TSC would

be maintained under accident conditions. Specifically, the licensee failed to ensure

engineering controls that were in place to minimize the concentration of radioactive

material in air in the TSC were maintained in accordance with the design bases.

18

Enclosure

Description

The inspectors identified that, for an extended period of time, the licensee did not

validate that the removal efficiencies in the TSC ventilation filter design bases were

being achieved. Specifically, testing of the TSC ventilation HEPA and charcoal filters did

not demonstrate that filter performance was in compliance with the design criteria. The

design bases for the TSC ventilation system HEPA filter was 99 percent for particulate

radioactive material removal efficiency. The licensees surveillance test acceptance

criterion was95 percent. In addition, the design basis for the charcoal filter laboratory

analysis was 95 percent removal efficiency of radioactive iodine. The surveillance test

required 80 percent. Consequently, there was no assurance that the installed TSC

ventilation equipment would perform at its designed radioactive material removal

capacity, thereby minimizing the radiological exposures to the occupants of the TSC

during postulated accidents.

The TSC is an onsite emergency response facility intended to support plant

operations under emergency conditions. The TSC ventilation system is designed to

remove radioactive material from the air, thereby minimizing the radioactive material

entering the TSC during postulated accident scenarios.

Analysis

The inspectors reviewed IMC 0612, Appendix B, "Issue Screening," dated December 24,

2009, and found no similar examples. However, the inspectors determined that the

finding was more than minor because it was associated with the program and process

attribute of exposure control of the occupational radiation safety cornerstone and

adversely affected the cornerstone objective of ensuring the adequate protection of

worker health and safety from exposure radiation and radioactive material. Specifically,

by testing the installed emergency ventilation system filters to removal efficiencies less

than their design criteria, the licensee did not validate that the TSC ventilation system

was capable of performing its design function and minimize worker exposures to

airborne radioactive materials.

The inspectors determined that the failure to establish testing criteria in

accordance with the system design bases was a performance deficiency consistent

with IMC 0612, Power Reactor Inspection Reports. The inspectors determined that the

licensee failed to meet the requirements of 10 CFR 20.1701 to use installed process

equipment to reasonably minimize the level of airborne radioactive materials. The

performance deficiency was reasonably within the licensees ability to foresee and

correct and was indicative of current performance, in that, the licensee had recent

opportunities to self-identify and correct the issue, including when performing recent

technical reviews for NRC license amendment submittals for license renewal, alternate

source term, and extended power uprate.

The finding was assessed using IMC 0609, Appendix C, Occupational Radiation Safety

Significance Determination Process, (SDP) and was determined to be of very low safety

significance (Green) because it was not an as-low-as-is-reasonably-achievable (ALARA)

planning issue, there was no overexposure or potential for overexposure, and the

licensees ability to assess dose was not compromised. The licensee documented this

issue in its corrective action program. Corrective actions included revising applicable

procedures and based on actual historical filter testing efficiencies, calculating that the

TSC ventilation system was capable of maintaining a radiological habitability of less than

5 Rem total effective dose equivalent (TEDE) for the duration of the design-basis

accidents.

19

Enclosure

The inspectors identified that the most significant contributor to the finding was a

cross-cutting aspect in the area of human performance, resources. Specifically, the

licensee failed to ensure that the TSC ventilation filter testing protocol assured

compliance to the systems designed margins in that the TSC ventilation filter testing

acceptance criteria were established independent of the system design requirements

(H.2(a)).

Enforcement

4.

OTHER ACTIVITIES

Title 10 CFR 20.1701 requires that licensees use, to the extent practical,

process or other engineering controls (e.g., containment, decontamination, or ventilation)

to control the concentration of radioactive material in air. Contrary to the above, as of

January 19, 2012, the licensee failed to ensure that effective engineering controls were

implemented to control the concentration of radioactive material in air in the TSC in

accordance with the facilitys design bases. Because the issue was of very low safety

significance and has been entered into the licensees CAP (as CR01752498), the

violation is being treated as an NCV consistent with Section 2.3.2 of the NRC

Enforcement Policy (NCV 05000266/2012003-02; 05000301/2012003-02;

Non-Compliance With 10 CFR 20.1701 to Control the Concentration of Radioactive

Material in Air and Ensure that Radiological Airborne Hazards Would Be Minimized in

the Technical Support Center During a Design-Basis Accident). This NCV closes

URI 05000266/2012002-05; 05000301/2012002-05, TSC Filter Testing May Be

Inadequate," in Section 4OA5.2.

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency

Preparedness, Public Radiation Safety, Occupational Radiation Safety, and

Physical Protection

4OA1 Performance Indicator Verification

.1

(71151)

a.

Unplanned Scrams with Complications

The inspectors sampled licensee submittals for the Unplanned Scrams with

Complications performance indicator (PI) for Units 1 and 2, for the third quarter 2011

through the second quarter 2012. To determine the accuracy of the PI data reported, PI

definitions and guidance contained in the Nuclear Energy Institute (NEI) Document

99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6, dated

October 2009, were used. The inspectors reviewed the licensees operator narrative

logs, CRs, event reports, and NRC integrated IRs to validate the accuracy of the

submittals. The inspectors also reviewed the licensees CAP to determine if any

problems had been identified with the PI data collected or transmitted for this indicator

and none were identified. Documents reviewed are listed in the Attachment to this

report.

Inspection Scope

This inspection constituted two unplanned scrams with complications samples as

defined in IP 71151-05.

b.

No findings were identified.

Findings

20

Enclosure

.2

a.

Reactor Coolant System Leakage

The inspectors sampled licensee submittals for the RCS Leakage PI for Units 1 and 2,

for the third quarter 2011 through the second quarter 2012. To determine the accuracy

of the PI data reported, PI definitions and guidance contained in the NEI

Document 99-02, Regulatory Assessment Performance Indicator Guideline,

Revision 6, dated October 2009, were used. The inspectors reviewed the licensees

operator logs, RCS leakage tracking data, CRs, event reports, and NRC integrated IRs

to validate the accuracy of the submittals. The inspectors also reviewed the licensees

CAP to determine if any problems had been identified with the PI data collected or

transmitted for this indicator and none were identified. Documents reviewed are listed in

the Attachment to this report.

Inspection Scope

This inspection constituted two reactor coolant system leakage samples as defined in

IP 71151-05.

b.

No findings were identified.

Findings

.3

a.

Reactor Coolant System Specific Activity

In the first quarter of 2012, the inspectors sampled licensee submittals for the RCS

specific activity PI for Units 1 and 2 for the fourth quarter 2010 through the fourth quarter

2011. The inspectors used PI definitions and guidance contained in the

NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline,

Revision 6, dated October 2009, to determine the accuracy of the PI data reported. The

inspectors reviewed the licensees RCS chemistry samples, TS requirements, CRs,

event reports, and NRC integrated IRs to validate the accuracy of the submittals. The

inspectors also reviewed the licensees CAP to determine if any problems had been

identified with the PI data collected or transmitted for this indicator and none were

identified. In addition to record reviews, the inspectors observed a chemistry technician

obtain and analyze an RCS sample. Documents reviewed are listed in the Attachment

to this report.

Inspection Scope

This inspection constituted two reactor coolant system specific activity samples as

defined in IP 71151-05.

b.

No findings were identified.

Findings

21

Enclosure

.4

a.

Occupational Exposure Control Effectiveness

In the first quarter of 2012, the inspectors sampled licensee submittals for the

occupational radiological occurrences PI for the fourth quarter 2010 through the fourth

quarter 2011. The inspectors used PI definitions and guidance contained in the NEI

Document 99-02, Regulatory Assessment Performance Indicator Guideline,

Revision 6, dated October 2009, to determine the accuracy of the PI data reported. The

inspectors reviewed the licensees assessment of the PI for occupational radiation safety

to determine if indicator related data was adequately assessed and reported. To assess

the adequacy of the licensees PI data collection and analyses, the inspectors discussed

with radiation protection staff, the scope and breadth of its data review and the results of

those reviews. The inspectors independently reviewed electronic personal dosimetry

dose rate and accumulated dose alarms and dose reports and the dose assignments for

any intakes that occurred during the time period reviewed to determine if there were

potentially unrecognized occurrences. The inspectors also conducted walkdowns of

numerous locked high and very-high radiation area entrances to determine the

adequacy of the controls in place for these areas. Documents reviewed are listed in the

Attachment to this report.

Inspection Scope

This inspection constituted one occupational exposure control effectiveness sample as

defined in IP 71151-05.

b.

No findings were identified.

Findings

.5

a.

Radiological Effluent Technical Specification/Offsite Dose Calculation Manual

Radiological Effluent Occurrences

In the first quarter of 2012, the inspectors sampled licensee submittals for the

radiological effluent Technical Specification/Offsite Dose Calculation Manual radiological

effluent occurrences PI for the fourth quarter 2010 through the fourth quarter 2011. The

inspectors used PI definitions and guidance contained in the NEI Document 99-02,

Regulatory Assessment Performance Indicator Guideline, Revision 6, dated

October 2009, to determine the accuracy of the PI data reported. The inspectors

reviewed the licensees CAP and selected individual reports generated since this

indicator was last reviewed to identify any potential occurrences such as unmonitored,

uncontrolled, or improperly calculated effluent releases that may have impacted offsite

dose. The inspectors reviewed gaseous effluent summary data and the results of

associated offsite dose calculations for selected dates to determine if indicator results

were accurately reported. The inspectors also reviewed the licensees methods for

quantifying gaseous and liquid effluents and determining effluent dose. Documents

reviewed are listed in the Attachment to this report.

Inspection Scope

This inspection constituted one Radiological Effluent Technical Specification/Offsite

Dose Calculation Manual radiological effluent occurrences sample as defined in

IP 71151-05.

22

Enclosure

b.

No findings were identified.

Findings

4OA2 Identification and Resolution of Problems

.1

(71152)

a.

Routine Review of Items Entered into the Corrective Action Program

As part of the various baseline inspection procedures discussed in previous sections of

this report, the inspectors routinely reviewed issues during baseline inspection activities

and plant status reviews to verify that they were being entered into the licensees CAP at

an appropriate threshold, that adequate attention was being given to timely corrective

actions, and that adverse trends were identified and addressed. Attributes reviewed

included: identification of the problem was complete and accurate; timeliness was

commensurate with the safety significance; evaluation and disposition of performance

issues, generic implications, common causes, contributing factors, root causes,

extent-of-condition reviews, and previous occurrences reviews were proper and

adequate; and that the classification, prioritization, focus, and timeliness of corrective

actions were commensurate with safety and sufficient to prevent recurrence of the issue.

Minor issues entered into the licensees CAP as a result of the inspectors observations

are included in the Attachment to this report.

Inspection Scope

These routine reviews for the identification and resolution of problems did not constitute

any additional inspection samples. Instead, by procedure they were considered an

integral part of the inspections performed during the quarter and documented in

Section 1 of this report.

b.

No findings were identified.

Findings

.2

a.

Daily Corrective Action Program Reviews

In order to assist with the identification of repetitive equipment failures and specific

human performance issues for follow-up, the inspectors performed a daily screening of

items entered into the licensees CAP. This review was accomplished through

inspection of the stations daily condition report packages.

Inspection Scope

These daily reviews were performed by procedure as part of the inspectors daily plant

status monitoring activities and, as such, did not constitute any separate inspection

samples.

b.

No findings were identified.

Findings

23

Enclosure

.3

a.

Annual Sample: Review of Operator Workarounds

The inspectors evaluated the licensees implementation of the process used to identify,

document, track, and resolve operational challenges. Inspection activities included, but

were not limited to, a review of the cumulative effects of the operator workarounds

(OWAs) on system availability and the potential for improper operation of the system, for

potential impacts on multiple systems, and on the ability of operators to respond to plant

transients or accidents.

Inspection Scope

The inspectors performed a review of the cumulative effects of OWAs. The documents

listed in the Attachment to this report were reviewed to accomplish the objectives of the

inspection procedure. The inspectors reviewed both current and historical operational

challenge records to determine whether the licensee was identifying operator challenges

at an appropriate threshold, had entered them into the CAP, and proposed or

implemented appropriate and timely corrective actions which addressed each issue.

Reviews were conducted to determine if any operator challenge could increase the

possibility of an Initiating Event, if the challenge was contrary to training, required a

change from long-standing operational practices, or created the potential for

inappropriate compensatory actions. Additionally, all temporary modifications were

reviewed to identify any potential effect on the functionality of Mitigating Systems,

impaired access to equipment, or required equipment uses for which the equipment was

not designed. Daily plant and equipment status logs, degraded instrument logs, and

operator aids or tools being used to compensate for material deficiencies were also

assessed to identify any potential sources of unidentified OWAs.

This review constituted one operator workaround annual inspection sample as defined in

IP 71152-05.

b.

No findings were identified.

Findings

.4

a.

Selected Issue Follow-Up Inspection: Partial Turnover of Extended Power Uprate

Modifications

The inspectors reviewed items entered in the licensees CAP and identified various

corrective action item reports identifying problems with the modification turnover process

of extended power uprate (EPU) modifications installed during recent refueling outages.

The inspectors elected to review this practice as a selected issue follow-up item.

Inspection Scope

This review constituted the completion of one in-depth problem identification and

resolution sample as defined in IP 71152-05, completing the partial sample referenced

previously in integrated IR 05000266/2012002; 05000301/2012002.

b.

Findings

Partial Turnover of Extended Power Uprate Modifications

24

Enclosure

Introduction: During the inspectors review of the licensees partial turnover process, the

inspectors identified a URI associated with the process.

Description

During the second quarter, the inspectors received portions of the requested

documentation. The issue is unresolved pending review of the portions of the previously

requested documentation (URI 05000266/2012003-03; 05000301/2012003-03, Partial

Turnover of Extended Power Uprate Modifications).

The inspectors selected the licensees partial turnover process as a

selected issue follow-up due to the potential inadequacies associated with the process.

As previously identified in IRs 05000266/2011008; 05000301/2011008, and

05000266/2012002; 05000301/2012002, the inspectors identified problems and

violations associated with the licensees partial turnover process where systems had

been partially turned over and declared operable, and it was later discovered that

portions of the modification were not tested prior to being placed in-service. With the

additional identification of problems associated with the partial turnover process

referenced in CRs in Integrated IRs 05000266/2012002; 05000301/2012002, the

inspectors were concerned that additional systems may be subject to similar issues as a

result of the partial turnover process. At the completion of the first quarter inspection

period, the inspectors were awaiting the requested documentation from the licensee to

complete their review of this issue.

.5

a.

Selected Issue Follow-Up Inspection: Licensed Operator Respirator Qualifications And

Control Room Staffing

During a review of items entered in the licensees CAP, the inspectors found recent

corrective action items documenting repetitive occurrences associated the licensed

operator respirator qualifications. These CRs related to AR01670172 which

documented a condition where shift staffing was challenged due to having expired

licensed operator respirator qualifications. The inspectors questioned the licensees

evaluation of the CR regarding the conclusions reached. Specifically, the inspectors

noted that the individual was credited with watch-standing during the period of expired

qualifications and that the procedures for the annual requirements conflicted. The

licensee entered the inspectors concerns in the CAP as AR01747333 and AR1772196.

The licensee was able to demonstrate through timed entries and door logs that control

room staffing was not compromised due to the expired respirator qualification.

Additionally, the licensees corrective actions created a report to track licensed operator

respirator qualifications as well as initiated a procedure change requests to more clearly

document licensed operator watch-standing requirements and clarify the definitions for

annual requirements.

Inspection Scope

This review constituted one in-depth problem identification and resolution sample as

defined in IP 71152-05.

b.

No findings were identified.

Findings

25

Enclosure

4OA3 Follow-Up of Events and Notices of Enforcement Discretion

.1

(71153)

a.

Unit 2 Planned Downpower to Repair Switchyard Hotspot

The inspectors reviewed the plants response to a planned downpower on Unit 2. Unit 2

was taken offline while remaining critical on April 21, 2012, to allow repair of two hot

spots on two phases of a disconnect switch in the switchyard. The repairs were

successful and the unit was placed back online on April 22, 2012. Documents reviewed

are listed in the Attachment to this report.

Inspection Scope

This event follow-up review constituted one sample as defined in IP 71153-05.

b.

No findings were identified.

Findings

.2

a.

Alert Declared Due To Toxic Gas

The inspectors reviewed the plants response to an Alert on April 25 to 26, 2012, that

was declared during a special maintenance run of the G-02 EDG. During the EDG run,

exhaust fumes entered the adjacent air compressor room, a vital area, and the levels of

toxic gas from these fumes exceeded Occupational Safety and Health Administration

(OSHA) limits. The EDG was immediately secured and the room ventilated. The

licensee corrected the system configuration problem that caused the inleakage and re-

performed the run. Documents reviewed are listed in the Attachment to this report.

Inspection Scope

This event follow-up review constituted one sample as defined in IP 71153-05.

b.

No findings were identified.

Findings

.3

a.

Failure of Turbine-Driven Auxiliary Feedwater Pump Coupling

On May 21, 2012, the inspectors reviewed the plants response to the failure of the

Unit 1 TDAFW pump coupling and related unplanned entry into a 72-hour limiting

condition for operation action statement. The inspectors reviewed the repair and other

activities the licensee performed to be able to return the pump to service within the

allowed completion time. Documents reviewed are listed in the Attachment to this

report.

Inspection Scope

This event follow-up review constituted one sample defined in IP 71153-05.

b.

No findings were identified.

Findings

26

Enclosure

.4

(Closed) Licensee Event Reports (LERs) 05000301/2011-004-00 and

05000301/2011-004-01, Automatic Reactor Trip During Startup Physics Testing Due to

Source Range

Introduction: A Green NCV of 10 CFR 50.65(a)(3) was self-revealed when an

unplanned reactor trip occurred as a result of the failure of a source range detector

during low power physics testing. Specifically, the licensee failed to adequately evaluate

operating experience and incorporate it into preventive maintenance programs to

periodically replace aging electrical subcomponents in nuclear instrumentation systems

and a subsequent age-related failure resulted in initiating a plant transient.

Description

Subsequent review by the licensee determined that the failure was due to age-related

degradation and that the most likely cause of the failure was because the output filter

capacitors were degraded. The licensee indicated that the recent failures were

experienced on power supplies manufactured in the 1970s, and that the date codes on

the capacitors in the subject units was also from the 1970s. Additionally, the licensee

noted that many of the components used in the construction of the related units were

40 years old.

On June 13, 2011, during the performance of beginning of life (BOL) low

power physics testing, and with reactor power decreasing due to inserting reactor control

rods to obtain test data, power decreased below the setpoint that actuates and

automatically places source range monitoring (SRM) instrumentation in service. When

SRMs were actuated, channel 2N31 experienced a failure of the associated high voltage

power supply. This failure satisfied the SRM high flux reactor trip logic and resulted in

an automatic reactor trip.

The licensees root cause analysis identified historical operating experience as early as

1992, which reflected the need to periodically repair or replace power supplies; and that

in 1998, Westinghouse provided a recommendation to replace power supplies; or at a

minimum, replace filtering capacitors every 10 years. In 1998, the licensee made a

decision not to incorporate the vendor recommendations into the preventive

maintenance program.

The licensee concluded that the root cause could be attributed to life cycle management

and preventive maintenance program deficiencies. The corrective action to prevent

recurrence was related to the life cycle management plan for the nuclear instruments.

The inspectors considered that this action was adequate to address concerns related to

the nuclear instruments. The inspectors reviewed the issue with the licensee with

respect to subcomponent aging management. The licensee had indicated that

subsequent to this event and industry reviews, it had expanded the subcomponent aging

management program. The licensee provided evidence which demonstrated that a

program for subcomponent aging and management was in the final stage of

development, and that the program was reviewing several categories of subcomponents

consisting of over 4,000 items. Additionally, the program was looking at single point

vulnerabilities and risk prioritization of reviews. The inspectors concluded that this

program appeared to approach subcomponent aging management systematically and

would provide a strong barrier to preclude similar failures in the future.

Analysis: The inspectors determined that the failure to incorporate operating experience

related to aging of electrical subcomponents specific to nuclear instrument source range

27

Enclosure

monitors into preventive maintenance programs was a performance deficiency

warranting further review. The finding was determined to be more than minor in

accordance with IMC 0612, Power Reactor Inspection Reports, Appendix B, Issue

Screening, dated December 24, 2009, because the finding was associated with the

Initiating Events Cornerstone attribute of equipment performance. Specifically, the

availability and reliability of the nuclear instruments was degraded to a point where an

instrument failure caused a reactor trip, an event that adversely affected the cornerstone

objective to limit the likelihood of those events that upset plant stability and challenge

critical safety functions during power operations.

The inspectors determined that the finding could be evaluated using IMC 0609,

Significance Determination Process, Attachment 0609.04, Phase 1 - Initial Screening

and Characterization of Findings, Table 4a for the Initiating Events Cornerstone, dated

January 10, 2008. The inspectors determined that the finding did not contribute to both

the likelihood of a reactor event and the likelihood that mitigation equipment or functions

would not be available; therefore, the issue screened as having very low safety

significance (Green).

The inspectors reviewed the licensees root cause analysis. The licensee considered

the issue a legacy issue related to the 1998 decision to ignore 1992 operating

experience and a 1998 vendor recommendation to replace power supplies at 10-year

intervals. Because the adverse decision occurred in 1998, the licensee concluded that

no crosscutting aspect occurred. However, the inspectors noted that the licensee

continued to amass internal and external operating experience from 1998 to 2011,

including a 2010 NRC-identified trend of source range monitoring failures as

documented in IR 05000266/2010002; 05000301/2010002, Section 4OA2.3,

Semiannual Trend, and that a rigorous and thorough evaluation of these issues could

have precluded the most recent failure. Therefore, the inspectors determined that the

issue had a crosscutting aspect in the area of corrective action program,

evaluation/extent of condition. Specifically, the licensee failed to thoroughly evaluate

related nuclear instrument failure rates such that the resolutions addressed the causes

and extent of conditions for age-related failures of electrical subcomponents (P.1(c)).

Enforcement

Because this violation was of very low safety significance and it was entered into the

licensees CAP (as root cause evaluation (RCE) 01660378-02), this violation is being

Title 10 CFR 50.65(a)(3) states, in part, that preventive maintenance

activities shall be evaluated at least every refueling cycle and take into account, where

practical, industry-wide operating experience. Contrary to this requirement, the licensee

failed to evaluate its preventative maintenance activities to take into account a

Westinghouse Infogram, dated August 8, 1998, that recommended replacement of

power supplies every 10 years, and other industry-wide operating experience issued

since 1998 related to the replacement of aging electrical subcomponents. This failure

resulted in electrical subcomponents of a source range monitor not being replaced since

the 1970s. A failure of one of these subcomponents resulted in a trip of the Unit 2

reactor on June 13, 2011.

28

Enclosure

treated as an NCV, consistent with Section 2.3.2 of the NRC enforcement Policy

(NCV 05000266/2012003-04; 05000301/2012003-04, Failure to Incorporate Industry

Operating Experience Into Preventive Maintenance Programs for Nuclear

Instrumentation).

This event follow-up review constituted one sample as defined in IP 71153-05.

4OA5

.1

Other Activities

The URI described a condition where additional information was needed by the

inspectors to assess the licensees program when determining an individuals

radiological dose of record. This item was discussed and closed by

NCV 05000266/2012002-06, Determining an Individuals Dose of Record With

Discrepant TLD/ED Data Inputs.

(Closed) URI 05000266/2011005-02; 05000301/2011005-02, Determining an

Individuals Dose of Record with Discrepant TLD/ED Data Inputs

.2

a.

(Closed) URI 05000266/2012002-05; 05000301/2012002-05, TSC Filter Testing May Be

Inadequate

The URI described a condition where additional information was needed by the

inspectors to assess the licensees TSC ventilation system filter testing program. This

item was closed and discussed in Section 2RS3 by NCV 05000266/2012003-02; 05000301/2012003-02, Non-Compliance with 10 CFR 20.1701 to Control the

Concentration of Radioactive Material in Air and Ensure That Radiological Airborne

Hazards Would Be Minimized in the Technical Support Center During a Design-Basis

Accident.

Inspection Scope

.3

a.

Temporary Instruction (TI)-2515/182 - Review of the Industry Initiative to Control

Degradation of Underground Piping and Tanks

Leakage from buried and underground pipes has resulted in ground water contamination

incidents with associated heightened NRC and public interest. The industry issued a

guidance document, NEI 09-14, Guideline for the Management of Buried Piping

Integrity, (ADAMS Accession No. ML1030901420), to describe the goals and required

actions (commitments made by the licensee) resulting from this underground piping and

tank initiative. On December 31, 2010, NEI issued Revision 1 to NEI 09-14, Guidance

for the Management of Underground Piping and Tank Integrity, (ADAMS Accession

No. ML110700122), with an expanded scope of components which included

underground piping that was not in direct contact with the soil and underground tanks.

On November 17, 2011, the NRC issued TI-2515/182, Review of the Industry Initiative

to Control Degradation of Underground Piping and Tanks, to gather information related

to the industrys implementation of this initiative.

Inspection Scope

The inspectors reviewed the licensees programs for buried pipe, underground piping,

and tanks in accordance with TI-2515/182 to determine if the program attributes and

completion dates identified in Sections 3.3 A and 3.3 B of NEI 09-14, Revision 1, were

29

Enclosure

contained in the licensees program and implementing procedures. For the buried pipe

and underground piping program attributes with completion dates that had passed, the

inspectors reviewed records to determine if the attribute was in fact complete and to

determine if the attribute was accomplished in a manner which reflected good or poor

practices in program management.

Based upon the scope of the review described above, Phase I of TI-2515/182 was

completed.

b.

The licensees buried piping and underground piping and tanks program was inspected

in accordance with Paragraphs 03.01.a through 03.01.c of TI-2515/182, and was found

to meet all applicable aspects of NEI 09-14, Revision 1, as set forth in Table 1 of the TI.

Observations

c.

No findings were identified.

Findings

4OA6

.1

Management Meetings

On June 26, 2012, the inspectors presented the inspection results to Mr. L. Meyer and

other members of the licensee staff. The licensee acknowledged the issues presented.

The inspectors confirmed that none of the potential report input discussed was

considered proprietary.

Exit Meeting Summary

.2

Interim exits were conducted for:

Interim Exit Meetings

the Review of the Industry Initiative to Control Degradation of Underground

Piping and Tanks (TI-2515/182) with Program Engineering Supervisor,

Mr. E. Schmidt, and other members of the licensee staff on May 1, 2012. The

licensee confirmed that none of the potential report input discussed was

considered proprietary; and

the inspection results of the unresolved item with Mr. J. Petro, Acting Licensing

Manager, on June 12, 2012.

The inspectors confirmed that none of the potential report input discussed was considered

proprietary. Proprietary material received during the inspection was returned to the licensee.

4OA7

None.

Licensee-Identified Violations

ATTACHMENT: SUPPLEMENTAL INFORMATION

1

Attachment

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

E. Schmidt, Program Engineering Supervisor

Licensee

A. Watry, Buried Pipe Engineer

B. Scherwinski, Licensing

B. Hennessy, Licensing Supervisor

J. Petro, Acting Licensing Manager

M. Kunowski, Chief, Reactor Projects Branch 5

Nuclear Regulatory Commission

2

Attachment

LIST OF ITEMS OPENED, CLOSED AND DISCUSSED

Opened 05000266/2012003-01; 05000301/2012003-01

NCV

Failure to Establish Emergency Diesel Generator Ventilation

System Testing (Section 1R19)05000266/2012003-02; 05000301/2012003-02

NCV

Non-Compliance With 10 CFR 20.1701 to Control the

Concentration of Radioactive Material in Air and Ensure That

Radiological Airborne Hazards Would Be Minimized in the

Technical Support Center During a Design-Basis Accident

(Section 2RS3)05000266/2012003-03; 05000301/2012003-03

URI

Partial Turnover of Extended Power Uprate Modifications

(Section 4OA2.4)05000266/2012003-04; 05000301/2012003-04

NCV

Failure to Incorporate Industry Operating Experience Into

Preventive Maintenance Programs for Nuclear

Instrumentation (Section 4OA3.4)

Closed 05000266/2012003-01; 05000301/2012003-01

NCV

Failure to Establish Emergency Diesel Generator Ventilation

System Testing (Section 1R19)05000266/2012003-02; 05000301/2012003-02

NCV

Non-Compliance With 10 CFR 20.1701 to Control the

Concentration of Radioactive Material in Air and Ensure That

Radiological Airborne Hazards Would Be Minimized in the

Technical Support Center During a Design-Basis Accident

(Section 2RS3)

05000301/2011-004-00

LER

Automatic Reactor Trip During Startup Physics Testing Due

to Source Range (Section 4OA3.4)

05000301/2011-004-01

LER

Automatic Reactor Trip During Startup Physics Testing Due

to Source Range (Section 4OA3.4)05000266/2012003-04; 05000301/2012003-04

NCV

Failure to Incorporate Industry Operating Experience Into

Preventive Maintenance Programs for Nuclear

Instrumentation (Section 4OA3.4)05000266/2011005-02; 05000301/2011005-02

URI

Determining An Individuals Dose Of Record With Discrepant

TLD/ED Data Inputs (Section 4OA5.1)05000266/2012002-05; 05000301/2012002-05

URI

TSC Filter Testing May Be Inadequate (Section 4OA5.2)

3

Attachment

LIST OF DOCUMENTS REVIEWED

The following is a partial list of documents reviewed during the inspection. Inclusion on this list

does not imply that the NRC inspector reviewed the documents in their entirety, but rather that

selected sections or portions of the documents were evaluated as part of the overall inspection

effort. Inclusion of a document on this list does not imply NRC acceptance of the document or

any part of it, unless this is stated in the body of the inspection report.

- 2011 Summer Readiness Package; May 24, 2011

1R01 Adverse Weather Protection

- 2012 Summer Readiness Package; May 24, 2012

- AOP-13C; Severe Weather Conditions; Revision 26

- AOP-31; Solar Magnetic Disturbance Alert Response; Revision 0

- AR01675202; Solar Disturbance

- AR01675213; FRCC And NERC On A Solar Flare That May Impact Earth 8/5 Strong Solar

Activity

- AR01725580; 2012 Site Excellence Plan: Engineering (Improved Margin)

- AR01728251; Summer Readiness Period Action Items

- AR01749094; AOP-13C Severe Weather Conditions Requires Emergent Changes

- AR01757855; OI 155 Chemical Treatment of SW/Potential Impact On U2 B RCP

- AR01764102; HX38 Condenser Summer Readiness Issue

- AR01767718; Solar Magnetic Disturbance Impact On 1X-03 Is Unknown

- AR0176879; AOP-13B Number Used In 1996 Almost Reused Document

- AR01776849; F52-Q303, 345KV Breaker Tripped Open From Lightning Strike

- ARP 1-PPCS-008; Priority Alarm Met Tower Unit 1; Revision 2

- ARP 2-PPCS-008; Priority Alarm Met Tower Unit 2; Revision 2

- BG AOP-13C; Severe Weather Conditions; Revision 14

- DBD-20; 345 KVAC System; Revision 8

- Email From J. Schweitzer; Subject: NERC Communication Release: Major Solar

Disturbance On The Way?; August 4, 2011

- EPMP 6.0; Alert And Notification System (ANS); Revision 10

- EPMP 9.0; Equipment Important To Emergency Preparedness; Revision 1

- FSAR Section 7.5; Operating Control Stations; UFSAR 2010

- FSAR Section 8.0; Introduction To The Electrical Distribution Systems; UFSAR 2010

- FSAR Section 8.1; 345K VAC Electrical Distribution System (345 kV); UFSAR 2010

- ICP 06.003-2; Meteorological System Calibration; Revision 1

- ICP 06.055; Meteorological Tower Instrumentation 6 Month Calibration Procedure; Revision 5

- Log Entries Report; January 24 To April 23, 2012

- National Weather Service Hazardous Weather Outlook; June 18, 2012

- Needs Assessment Worksheet For TRR 01675202; September 27, 2011

- NOAA Space Weather Scales; March 1, 2005

- NP 2.1.5; Electrical Communications, Switchyard Access And Work Planning; Revision 21

- NRC Information Notice No. 90-42: Failure Of Electrical Power Equipment Due To Solar

Magnetic Disturbances; June 19, 1990

- ODI.104; Solar Magnetic Disturbance Alert Response; Revision 00

- OI 35B; Electrical Equipment General Information; Revision 17

- OP-AA-102-1002; Seasonal Readiness; Revision 0

- PB MR 91-161; System 345kV; June 20, 1991

- PBN Seasonal Readiness Report; 2012 Winter Readiness Concerns/Issues; April 2012

4

Attachment

- PBNP System Engineering Summer Readiness Review; Component Cooling Water;

February 15, 2012

- PBNP System Engineering Summer Readiness Review; HVAC Rs And NR;

February 21, 2012

- PBNP System Engineering Summer Readiness Review; Service Water; February 21, 2012

- PJM; Weather And Environmental Emergencies; November 1, 2011

- Safety Logs; June 17, 2012

- Station Log; June 17, 2012

- CL 13E Part 1; Auxiliary Feedwater Valve Lineup Turbine-Driven Unit 1; Revision 45

1R04 Equipment Alignment

- CL 7A; Safety Injection System Checklist Unit 2; Revision 31

- Drawing 018974; Safety Injection System; Revision 53

- Drawing 018975; Safety Injection System; Revision 54

- Drawing 018976; Safety Injection System; Revision 47

- OI 129; SI System Fill And Vent Unit 2; Revision 6

- DBD-T-40; Fire Protection/Appendix R; Revision 9

1R05 Fire Protection

- Drawing 290583; Fire Protection For Site Plan; Revision 11

- Drawing 290585; Fire Protection For Turbine Building, Aux Building, And Containment,

Elev. 8-0; Revision 21

- Drawing 290587; Fire Protection For Turbine Building, Aux Building, And Containment;

Revision 11

- Drawing 290590; Fire Protection For Turbine Building, Aux Building, And Containment,

Elev. 44-0; Revision 09

- Drawing 290600; Fire Protection For Turbine Building, Aux Building, And Containment,

Elev. 66-0; Revision 06

- Duke Engineering And Services Fire Area Analysis Summary Report; Fire Area: A01-B

PAB 26 Elevation - Monitor Tank Area (FZ 187); August 8, 2005

- Duke Engineering And Services Fire Area Analysis Summary Report; Fire Area: A01-H Unit 2

Façade; August 8, 2005

- FEP 4.6; Façade Unit 2; Revision 8

- FOP 1.2; Potential Fire Affected Safe Shutdown Components; Revision 21

- OM 1.1; Conduct Of Plant Operations, PBNP Specific; Revision 40

- OM 3.1; Operations Shift Staffing Requirements; Revision 16

- OM 3.27; Control Of Fire Protection & Appendix R Safe Shutdown Equipment; Revision 44

- AR01633384; IER1 11-1 Unanalyzed Challenge From Non-Seismic Int Flooding

1R06 Flood Protection

- AR01752182; Draft NEI Flood Walkdown Document Not Available

- AR01762831; Water Entering SEI-06211 During Water Intrusion

- AR01762834; U1 Façade Southwest Corner Significant Water Entry

- AR01763180; U1 Façade Elevator Pit Flooded - Again

- AR01763259; 1P-10A Cubicle Had Accumulated Ground Water

- AR01763352; RE-113 PAB Area Monitor HI Alarm From Spiking

- AR01765294; Groundwater Intrusion Into The 1P-10A RHR Cubicle

- AR01765466; Schedule Scrub Results Concerning Unit 2 RCP Seal Issues

5

Attachment

- AR01765723; Groundwater Intrusion Into The 1P-10A RHR Cubicle

- AR01767771; Plugging Elevator Sump Drains Not The Right Thing To Do

- CE 01633384-01; Six Bulk Storage Tanks In PAB Not Contained In Dikes Or Rooms

- Floodable Volume Of The -19 Ft Elevation; Completed April 1, 2011

- FSAR Section 10.2; Auxiliary Feedwater System (AF); UFSAR 2010

- FSAR Section 6.2; Safety Injection System (SI); UFSAR 2010

- FSAR Section 9.2; Residual Heat Removal (RHR); UFSAR 2010

- NPC-27204; Letter From S. Burstein, Western Electric Power Company, To G. Lear, NRC;

Subject: Docket Nos. 50-266 And 50-301, Flooding Resulting From Non-Category I Failure,

Point Beach Nuclear Plant - Units 1 And 2; February 17, 1975

- NPC-28670; Letter From C. W. Fay, Western Electric Power Company, To H. R. Denton,

NRC; Subject: Docket Nos. 50-266 And 50-301, Final Resolution Of Generic Letter 81-14,

Seismic Qualification Of Auxiliary Feedwater System, Point Beach Nuclear Plant - Units 1

And 2; April 26, 1985

- POD 01633384; Unanalyzed Challenge From Non-Seismic Internal Flooding (Monitor Tanks

And Waste Distillate Tanks); Revision 0

- Station Log; May 8-12, 2012

- TAR 01633384; Unanalyzed Challenge From Non-Seismic Internal Flooding (Monitor Tanks

And Waste Distillate Tanks); Revision 0

- AR01747380; Simulator Reliability Below Expectations

1R11 Licensed Operator Requalification Program

- AR01748808; Simulator PPCS Stopped Functioning During LOI Training

- AR01748875; Nuclear Oversight Finding: Management Oversight Of Simulator

- FP-T-SAT-73; Licensed Operator Requalification Program Examinations; Revision 8

- NARS Form For Training Evolution; May 21, 2012

- OM 1.1; Conduct Of Plant Operations, PBNP Specific; Revision 40

- OP 3A Unit 2; Power Operation To Hot Standby Unit 2; Revision 7

- OP-AA-100-1000; Conduct Of Operations: Revision 6

- PBNP LOCT Cycle 12C Schedule; Revision 2

- Simulator Differences List; Cycle 12C; May 21, 2012

- ACE 01670189-02; Erratic Operation Displayed During Performance Of IT-08A Cold Start Of

Turbine-Driven Auxiliary Feed Pump And Valve Test (Unit 1); Revision 1

1R12 Maintenance Rule Effectiveness

- RCA For AR1173557-02; Unit 2 Turbine Driven Auxiliary Feedwater Pump (2P-29-T) Casing

Leak Identified During Start Of IT-09A; Completed July 6, 2010

- RMP 9044-1; Auxiliary Feedwater Pump Terry Turbine Overhaul; Revision 11

- System Health Report; Unit 1 Auxiliary Feedwater; January 1 To March 31, 2012

- System Health Report; Unit 2 Auxiliary Feedwater; January 1 To March 31, 2012

- Thomas Series 54 Couplings; Installation Instruction

- 2-SOP-CC-001; Component Cooling System; Revision 22

1R13 Maintenance Risk Assessments and Emergent Work Control

- AOP-9B Unit 1; Component Cooling System Malfunction; Revision 22

- AR01731219; Thermography Reading For 2F52-142 Breaker Limited Users

- AR01737362; While Performing IT-805, 2CC-726C Leaked By 85 Gal In 5 Min.

- AR01748666; Valve Is Difficult To Operate

6

Attachment

- AR01748700; Cross Unit CC Leakage During The Performance Of IT 805

- AR01766439; Request Review Of HX-12C Operability

- Calc No. 97-0118; Capacity To Achieve Cold Shutdown In Both Units With One CCW Pump

And Two CCW Heat Exchangers; April 27, 2011

- CCW Surge Tank Level, Units 1 And 2, 1LI-6188; March 25 To March 27, 2012

- CE 01748700-01; Component Cooling Leakage Occurred During Performance Of IT 805;

April 4, 2012

- Drawing 018982; Auxiliary Coolant System, Unit 1; Revision 42

- EOP-1.3 Unit 1; Transfer To Containment Sump Recirculation - Low Head Injection;

Revision 47

- FSAR Appendix A.6; Shared System Analysis; UFSAR 2008

- FSAR Section 9.1; Component Cooling Water (CC); UFSAR 2010

- Hypothetical Risk Management Worksheet, Units 1 And 2; April 26, 2012

- IT 805; Component Cooling Water System Valves U-2; Completed March 26, 2012

- Log Entries Report; Various Dates February 23 To March, 26, 2012

- NP 10.3.7; On-Line Safety Assessment; Revision 26

- OP 2B; 345 kV Transmission System Impacts Upon PBNP Station Operations; Revision 4

- PB - 2F52-142 Unit 2 Generator Breaker A Phase Monitoring Plan

- PB032221-11; Letter From L. Gundrum, NRC, To R. Grigg; Subject: Issuance Of

Amendments Re: Technical Specification Changes For Revised System Requirements To

Ensure Post-Accident Containment Cooling Capability (TAC Nos. M96741 And M96742);

July 9, 1997

- POD 01766439; Request Review Of HX-12C Operability; Revision 0

- PRA 5.14; Component Cooling Water System Notebook; Revision 0

- Responses To NRC Questions; Received June 12, 2012

- Risk Management Worksheets, Units 1 And 2; April 21-28, 2012

- Safety Monitor, Unit 1; April 3, 2012

- Safety Monitor, Unit 1; Various Dates February 22 To March 26, 2012

- Station Log; April 12, 2012

- Station Log; February 3, 2012

- TLB-9; Component Cooling Water Surge; ID W 685-J-114, Tank 1(2)T-12; Revision 3

- Trend Display 3; CCW Temp; March 26, 2012

- AR01165060; Gas Void - Negligible Void Found At 2SI-V14

1R15 Operability Evaluations

- AR01165062; ECs Possibly Not In Correct Status

- AR01166814; Gas Void - Negligible, Smaller Void Found At 2SI-V14

- AR01657344; 1P-29-T Governor Valve Stem Steam Leak

- AR01667491; Voiding In U2 RHR Core Deluge Line (A Train)

- AR01670550; 1P-29 Gov. Shaft Has Increased Steam Leakage

- AR01680372; Very Small Void Found At 2SI-V14

- AR01684317; PB2 Inside Containment Gas Void UT Results

- AR01693921; Small Gas Voids Found, PB2 LHSI Train A

- AR01701509; CFC Fan Motor Cooler Condensate Drain Valve Position

- AR01705654; Very Small Gas Voids, PB2 Inside Containment

- AR01712999; Operability Concern: U2 CFC Accident Fan Cooler Drn Vlvs

- AR01714813; Very Small Gas Voids, PB2 Inside Containment

- AR01716079; Wires Inside U-1 Control Boards Not Spared Correctly

- AR01723005; 1C-03 Horizontal Wireway PL-A Cannot Close

- AR01723012; C-02 Riser 32 Train Separation Wireway PB22 Missing Cover

7

Attachment

- AR01723019; C-02 Remove Sound Powered Headphone Permanently Wired In

- AR01723362; 1C-004 Internal Risers 7 & 9 Have Large Openings In Wireways

- AR01723700; Lift Wires And Remove Minalites For CS-2130 Abandonment

- AR01734709; Verification Of Wire Terminations For 1C-04 MOB-42 And 43

- AR01745582; 2012 Mid-Cycle: Safety - Extension Cords In CR >90 Days

- AR01747782; Gas Void Accept. Criterion For 1-IC-SI-D11 Non-Conservative

- AR01749161; Review Of Overall Control Room ARs

- AR01750355; QC Inspection points Not Included In Work Tasks

- AR01768931; TDAFWP Coupling Ejected Pieces During Run

- AR01769140; Flush Required On 1P29 TDAFWP Prior To Return To Service

- AR01769277; Pump Holddown Bolt In Southwest Corner Not Tight

- AR01769697; Coupling For 1P-29 Did Not Come With Full Set Of Bolting

- AR01769990; Small SW Leak Found

- AR01770001; Drain Trap Union Leaking

- AR01770007; 1P-29 Turb. Outboard Bearing Temperatures During IT-8A

- AR01770266; TDAFW Pump Mission Time In DBD-P-54 Questioned By NRC

- AR01770327; Cable Spreading Room Temperature Out Of Spec High

- AR01770729; Low Margin On VNCSR Creates Elevated Risk

- AR01770731; Suspected Leak By Causing Elevated Temperature In CSR

- AR01771841; 1P-29-T TDAFW Turbine Bolting Changes

- AR01772353; Condition Adverse To Quality - 1P-29-T

- AR01772594; Replace Shim Packs On The 1P-29-T Coupling

- AR01772637; Replace East Hold Down Studs On 1P-29-T

- AR01772640; Correct 1P-29-T Exhaust Flange Misalignment

- AR01774453; DY0C RMP Is Quarantined

- AR01774906; Old Abandoned AFW Cables Are Not Properly Spared

- AR01774944; Performance Of IT 16 Can Increase CSR Temperature

- AR01775121; Planned Maintenance Outages On Sirens K-004, K-005,K-006

- AR01775202; Unexpected Alarm HP Feedwater Heater SA Or B High Or Low

- AR01775325; EPRI Issued NDE Alert Letter Based On North Anna OE

- AR01775418; Simulator Scenario Programs Not Working Properly

- AR01775425; Change In Stroke Open Time For 2CV-1296

- Basis For Immediate Operability (CR01712999); December 6, 2011

- Drawing 171951; Containment Vent Fan Motor Base And Motor Cooling Coil Housing;

Revision 09

- Drawing 275461; Service Water System; Revision 13

- Drawing 332894; Fan Motor Cooler; Revision 3

- Drawing 335353; 24x66 Containment Fan Coolers With Supply Lower Left; Revision 3

- Drawing 35476; Unit 2 Heating And Ventilation Containment Area 11 Plan El. Above 66-0;

Revision 08

- Drawing 35477; Unit 2 Heating And Ventilation Containment Area 11 Plan El. 46-0;

Revision 05

- Drawing 35478; Unit 2 Heating And Ventilation Containment Area 11 Plan El. 21-0;

Revision 03

- Drawing 35480; Unit 2 Heating And Ventilation Containment Area 11 Sections; Revision 06

- Drawing 35481; Unit 1 And 2 Heating And Ventilation Containment Areas 7 And 11;

Revision 07

- EC 276517; 1P-029-T Coupling Alignment Review For WO 342825; Revision 9; May 23, 2012

- Email From N. Reckelberg To B. Beltz; Subject: CFC Motor Cooler Question; June 5, 2012

8

Attachment

- Engineering Evaluation No. EC 276517; 1P-029-T Coupling Alignment Review For

WO 342825

- FSAR Section 6.3; Containment Air Recirculation Cooling System (VNCC); UFSAR 2010

- NRC Inspection Question No. 1; May 31, 2012

- NRC Inspection Question No. 10; May 31, 2012

- NRC Inspection Question No. 11; June 1, 2012

- NRC Inspection Question No. 2; May 31, 2012

- NRC Inspection Question No. 3; June 1, 2012

- NRC Inspection Question No. 4; May 31, 2012

- NRC Inspection Question No. 5; May 31, 2012

- NRC Inspection Question No. 6; June 1, 2012

- NRC Inspection Question No. 7; May 31, 2012

- NRC Inspection Question No. 8; May 31, 2012

- NRC Inspection Question No. 9; June 1, 2012

- OI 155; Chemical Treatment Of Service Water For Mussels; Revision 34

- Operator Rounds; June 18-19, 2012

- PI-AA-100-1008; Condition Evaluation; Revision 3

- POD 01712999; Operability Concern: U2 CFC Accident Fan Cooler Drn Vlvs; Revision 0

- POD 01770327; Cable Spreading Room Temperature Out Of Spec High; Revision 0

- POD For CR 1771762; NRC Questions On G01/G02 Tornado Missile Temp Modification

- POD For CR1772353; Condition Adverse To Quality - 1P-29-T; Revision 0

- SCR 2011-0324; Revise 1/2-SOP-VNCC-001 Through 004, 1/2W-1A1 Through 1/2W-1D1

Accident Fan Recirculation Unit Draining, Filling And Venting Procedures; November 27, 2011

- SCR 2012-0089; 1P-29 Turbine Driven Aux Feed Pump Turbine Alignment; May 23, 2012

- TAR 01667491; Voiding In U2 RHR Core Deluge Line (A Train); Revision 0

- AOP-13C; Severe Weather Conditions; Revision 26

1R18 Plant Modifications

- AR01728544; PSS Design Functions Not Considered In Modification

- AR01752847; 2MS-380B IA Leak

- AR01763193; 1CS-3124 And 1CS-3125 Comp. Actions For AOP-13C

- AR01763196; 2CS-3124 And 2CS-3125 Comp. Actions For AOP-13C

- AR01763206; Cold Weather Actions - AOP-13C Guidance

- AR01779751; 2Q12 Green NCV - G01/G02 Room Fan And Damper Test Control

- B 3.7.2; MSIVs And Non-Return Check Valves; Unit 2 - Amendment No. 245

- B 3.7.3; MFIVs, MFRVs, And MFRV Bypass Valves; Unit 2 - Amendment No. 245

- CE For AR01752847-01; Air Leak Fount on 2MS-380B

- CRN 262425; Revise Cold Weather Strategy; Revision 2

- CRN 262894; Manufacturers Recommended Minimum Ambient Temperature For Hiller

Actuator Components Is -20°F; Revision 0

- Design Input Consultation Forms; EC 276081 Temporary Instrument Air Leak Repair

Upstream Of 2MS-380B; Various Dates April 9 To April 16, 2012

- Drawing 084854; Main & Reheat Steam System; Revisions 01 And 51

- EC 273303; Provide Temp Power To Select 1B-42 Loads; Revision 1; October 6, 2011

- EC 276081; Instrument Air Leak At 2MS-280B Temporary Repair Of Air Line Leak

- FP-E-MOD-03; Temporary Modifications; Revisions 9 And 10

- Modification Classification; Install Temp Mod On 2MS-02017 Per EC 276081; Completed

April 13, 2012

- Modification Classification; Provide Temp Power To Select 1B-42 Loads, Per EC 273303;

Completed September 28, 2011

9

Attachment

- MR No. 96-014-B; MSIV Control Solenoid Replacement; October 7, 1998

- PC 49 Part 4; Auxiliary Building Miscellaneous And Facades; Revision 27

- SCR 2011-0207-01; EC 273303; Provide Temporary Power To Select 1B-42 Loads;

February 1, 2012

- SCR 2012-0057; Install Temp Mod On 2MS-00380B Per EC 276081; April 12, 2012

- Station Logs; Various Dates April 6 To June 12, 2012

- Temp Mod Extension; Install Temp Mod On 2MS-02017 Per EC 276081; Completed

April 13, 2012

- WO Package 40155064 01; 2MS-380B IA Leak

- 0-SOP-G02-001; Maintenance Operation For EDG G-02; Completed April 26, 2012

1R19 Post-Maintenance Testing

- AR01722333; VNDG-04178-M / Replace Broken Motor Operator

- AR01750276; G-01 And G-02 Diesel Room Air Flow NRC Concern

- AR01753241; VNPAB Inoperable Due To FS-3297

- AR01769204; Calculation 2005-0054 Rev. 2 Potential Non-Conservatism

- B 3.8.1; AC Sources - Operating; January 18, 2010; June 1, 2009; January 19, 2008;

May 31, 2007; Unit 1-Amendment No. 215, Unit 2-Amendment No. 220; Unit 1-Amendment

No. 201, Unit 2-Amendment No. 206

- Calc 2005-0054; Control Building GOTHIC Temperature Calculation; Revisions 1 And 2

- CE 1750276-01; NRC Concern With Proper Air Flow In G-01 And G-02 Diesel Rooms

- EN47896; Licensed Operating Supervisor Tested Positive For A For-Cause Test For Alcohol;

May 3, 2012

- IT 08A; Cold Start Of Turbine-Driven Auxiliary Feed Pump And Valve Test (Quarterly) Unit 1;

Revision 65

- NARS Forms; April 25, 2012

- NP 10.3.7; On-Line Safety Assessment; Revision 27

- PBTP 157; G01/G02 Diesel Room Exhaust Fan Flow Measurement; Completed July 6, 2007

- PBTP-249; EDG Stack Test; Completed April 30, 2012

- PdMA Report 360458 0W-012B-M MCE; MCE Testing On 02/09/2010 For 0W-012B-M,

G-01 Room Exhaust Fan Motor; February 9, 2010

- PdMA Report 360458 0W-012C-M MCE; MCE Testing Of 0W-012C-M; February 22, 2010

- RMP 9044-1; Auxiliary Feedwater Pump Terry Turbine Overhaul; Revision 28

- Station Log; Various Dates From April 8 To April 27, 2012

- TAR 1766629; Review G-01 Operability Versus Gravity Louvers; Revision 0

- Troubleshooting Log For AR176931176931 May 23, 2012

- TS 81; Emergency Diesel Generator G-01 Monthly; Completed May 20, 2012

- TS 87; Primary Auxiliary Building Ventilation System Monthly Checks; Completed

April 10, 2012

- WO 40106974; 2F52-142 A Phase - Output Side Bolded Connection Hot

- WO Package 00342825-16; 1P-029-T Contingency Work Order To Overhaul If Required -2C

- WO Package 00360458-01; W-012B-M, MCE Analyze Motor (2 B52-329H/2B-32)

- WO Package 00360459-01; W-012C-MCE Analyze Motor (2 B52-328M/2B-32)

- WO Package 40070360 01; 2MS-02052-O Replace Actuator

- WO Package 40110297 07; K-004A Inspect And Maintain Diesel Air Start Compressor

- 2F3201 Forced Outage Critical Path; June 27, 2012

1R20 Unplanned Outage

- 2F32HS Forced Outage Issues And Actions

10

Attachment

- Daily Status Report; June 29, 2012

- EN 48053; Unit 2 Manual Reactor Actuated Due To Indications Of 100% Load Rejection;

June 27, 2012

- NP 5.3.3; Incident Investigation And Post-Trip Reviews; Completed June 27, 2012

- OP 3A Unit 1; Power Operation To Hot Standby Unit 1; Revision 9

- OP 3B; Reactor Shutdown; Revision 43

- PBNP Outage Status Report; June 29, 2012

- PBNP Shutdown Safety Assessment And Fire Condition; Unit 2; June 29, 2012

- PBNP Unit 2; Forced Outage List; As Of June 29, 2012

- Safety Monitor, Unit 1; June 27 To 28, 2012

- Safety Monitor, Unit 2; June 27, 2012

- Station Log; June 27 To June 29, 2012

- 3.3.3; Post Accident Monitoring (PAM) Instrumentation; Unit 1 - Amendment No. 215, Unit 2 -

Amendment No. 220; Unit 1 - Amendment No. 201, Unit 2 - Amendment No. 206

1R22 Surveillance Testing

- 3.4.13; RCS Operational Leakage; Unit 1 - Amendment No. 223, Unit 2 - Amendment No. 229;

And Unit 1 - Amendment No. 201, Unit 2 - Amendment No. 206

- 3.6.3; Containment Isolation Valves; Unit 1 - Amendment No. 201, Unit 2 - Amendment

No. 206; Unit 1 - Amendment No. 231, Unit 2 - Amendment No. 236

- AOP-1B; Reactor Coolant Pump Malfunction; Revision 20

- AR01681115; Air Fitting Leak

- AR01752323; Increased Leakoff From Unit 2 B RCP #2 Seal

- AR01753068; AOP-1B, RCP Malfunction, Entered Due To Hi RCP Seal Leakage

- AR01753241; VNPAB Inoperable Due To FS-3297

- AR01754554; AOP-1B Entry Due To Reactor Coolant Pump Seal Problems

- AR01755405; Momentary 2P-1B Seal Flow Low Alarm

- AR01762008; 2P-001B Seal Performance During Fan Starts

- Control Room Log - Modes 1-3, Unit 2; April 5 To 8, 2012

- FSAR Section 1.3; General Design Criteria; UFSAR 2010

- FSAR Section 4.1; Reactor Coolant System - Design Basis; UFSAR 2008

- FSAR Section 6.5; Leakage Detection Systems; UFSAR 2008

- IT 115; Instrument Air Valves (Quarterly) Unit 2; Completed May 18, 2012

- NP 10.3.78; On-Line Safety Assessment; Revision 27

- OI 55; Primary Leak Rate Calculation; Performed March 16, 2012

- OM 3.26; Use Of Dedicated / Assigned Operators; Revision 15

- Operational Decision Making; Increased 2P-1B, RCP, No. 2 Seal Leakage Transients;

Revised April 13, 2012

- Station Log; April 6 To 7, 2012; May 18, 2012

- Station Log; April 8, 2012

- TS 87; Primary Auxiliary Building Ventilation System Monthly Checks; Completed

April 10, 2012

- EN 47863; Alert Declared Due To Toxic Gas Build Up Following An Emergency Diesel

Generator Test Run; April 25, 2012

1EP6 Emergency Preparedness

- EPIP 1.1; Course Of Actions; Revision 63

- EPIP 1.2; Emergency Classification; Revision 50

- EPIP 1.2.1; Emergency Action Level Technical Basis; Revision 8

11

Attachment

- AR01696182; Lack Of 50.59 Screening For EPU LOCA Dose Calculations

2RS3 In-Plant Airborne Radioactivity Control and Mitigation

- AR01724172; Discrepancy In F-13 Filter Efficiency Tested In HPIP 11

- AR01779750; 2Q12 Green NCV - TSC Ventilation Filter Testing

- Calculation No. 129187-M-0112; Technical Support Center Direct Shine Dose Due To A Loss

Of Coolant Accident Following Extended Power Up-Rate And Using Alternative Source Term

Methodology; Revision 1

- Calculation No. 13612; Power/RP, PR-001; Calculate The Doses And Dose Rates In The

Technical Support Center Due To Intake And In-Leakage Following A LOCA, Assuming 4 Inch

Deep Activated Charcoal Beds Are Installed; May 19, 1980

- HPIP 11.50; Filter Testing; Revisions 20 And 21

- HPIP 11.52; HEPA (High Efficiency Particulate Absolute) And Charcoal Filter Administrative

Control; Revisions 3 And 4

- HPIP 11.54; Control Room F-16 Filter Testing; Revisions 17 And 18

- 1Q/2012 Performance Indicators; Reactor Coolant System Leakage, Units 1 And 2

4OA1 Performance Indicator Verification

- 2Q/2011 Performance Indicators; Reactor Coolant System Leakage, Units 1 And 2

- 3Q/2011 Performance Indicators; Reactor Coolant System Leakage, Units 1 And 2

- 4Q/2011 Performance Indicators; Reactor Coolant System Leakage, Units 1 And 2

- Gamma Spectrum Analysis; Sample Date February 29, 2012

- H33; Performance Indicator Reporting; Revision 11

- Log Entries Report; Various Dates From April 9, 2011 To March 14, 2012

- Monthly Effluent Release Offsite Dose Summary; December 2011

- NEI 99-02; Regulatory Assessment Performance Indicator Guideline; Revision 6;

October 2009

- NP 5.2.16; NRC Performance Indicators; Completed March 28 And March 2, 2012

- QF-0445; NRC/INPO/WANO Data Collection And Submittal Forms; 3rd Quarter 2011

- QF-0445; NRC/INPO/WANO Data Collection And Submittal Forms; 4th Quarter 2011

- ROP Parent Process Data Review, Unit 1; 2nd Quarter 2011 To 1st Quarter 2012

- RPIP 1013; Occupational Radiation Safety Performance Indicators; Revision 5

- RPIP 3332; Dose Equivalent Iodine-131; Revision 10

- RPIP 3382; Reactor Coolant Sample Preparation And Analysis; Revision 13

- RPIP 4521; Monthly Effluent Release Offsite Dose Calculations; Revision 7

- ACE 01670172; Licensed Operator Had Expired Respirator Qualifications

4OA2 Identification and Resolution of Problems

- ANSI N18-1-1971; Selection And Training Of Nuclear Power Plant Personnel; March 8, 1971

- ANSI/ANS-3.4-1996; Medical Certification And Monitoring Of Personnel Requiring Operator

Licenses For Nuclear Power Plants; February 7, 1996

- AR01670172; Challenge To Shift Staffing Due To Expired Respirator Quals

- AR01747094; Documentation Error For Proficiency Watch

- AR01747333; Alignment Question With Proficiency Watch Procedures

- AR01761339; Med- Changes Made To Respiratory Protection Program

- AR01763219; Individual Did Not Show Up For Fit Tests

- AR01764968; Operations Respiration Qual Check Shortcomings

- AR01765896; Individual Respirator Fit Tested Not IAW Procedure

- AR01772196; Definition Of Annual In Site Programs Needs Review

12

Attachment

- AR01772226; Four Watch Restrictions Due To Respirator Fit Test Inserts

- AR01772307; CR 01764968 Completed With Incomplete Actions

- AR01779753; 2Q12 NRC URI - Modification Turnover Process

- ES-605; License Maintenance, License Renewal Applications, And Requests For

Administrative Reviews And Hearings

- FPER; Fire Protection Evaluation Report; Revision 12

- FSAR Section 11.4; Radiation Protection Program; UFSAR 2010

- NP 1.1.4; Use And Adherence Of Procedures; Revision 27

- NP 2.1.1; Conduct Of Operations; Revision 13

- NP 4.2.32; Respiratory Protection Program; Revision 7

- NRC Information Notice 95-23; Control Room Staffing Below Minimum Regulatory

Requirements; April 24, 1995

- NRC Information Notice 97-66; Failure To Provide Special Lenses For Operators Using

Respirator Or Self-Contained Breathing apparatus During Emergency Operations;

August 20, 1997

- NUREG/CR-6838; Technical Basis For Regulatory Guidance For Assessing Exemption

Requests From The Nuclear Power Plant Licenses Operator Staffing Requirements Specified

In 10 CFR 50.54(m); February 2004

- OM 1.1; Conduct Of Plant Operations, PBNP Specific; Revision 36

- OM 3.1; Operations Shift Staffing Requirements; Revision 16

- OM 3.10; Operations Personnel Assignments And Scheduling; Revision 31

- OM 3.9; Watchstation Status Checks And Watchstander Turnover Guides; Revision 17

- OP-AA-100-1000; Conduct Of Operations; Revision 1

- Operations Department Clock Reset - Yellow Sheet, CAP 01670172; Completed

July 25, 2011

- PBN IS TP; Training Program Description; Revision 14

- PBN LOC TPD; Training Program Description; Completed September 12, 2011

- Plateau Curricula Status List; As Of May 9, 2012

- Unit Staff Qualifications 5.3; Unit - Amendment No. 211, Unit 2 - Amendment No. 216

- WO Package 40118739-01; Verify Operators Respiratory Qualifications

- 0-SOP-G02-001; Maintenance Operation For EDG G-02; Completed April 26, 2012

4OA3 Follow-Up of Events and Notices of Enforcement Discretion

- 1ICP 10.046; Check Of Rod Control System Redundant Power Supplies; Revision 1

- 2F3201 Forced Outage Critical Path; June 27, 2012

- 2F32HS Forced Outage Issues And Actions

- 2-SOP-19KV-001; Transformers 2X-01/2X-02 Outages And Electrical Operations; Completed

April 11, 2012

- ACE 01640098-01; AFI In The Area Of Equipment Reliability During January 2011 INPO E&A;

Revision 3

- Agenda For Operations Burden Review Meeting; May 30, 2012

- AR01640098; 2011 INPO Eval AFI ER.2-1: PMS Of Some Electrical Components

- AR01724425; Controller Not Controlling At Set Flow Rate

- AR01743615; Increase In Operations Requested Emergent PCRS

- AR01752251; Control Room Deficiencies Changed From White To Yellow

- AR01757638; Unanticipated Axial Flux Response During Load Swing

- CE For AR01750489; Progress On INPO AFI ER.2-1; April 12, 2012

- Daily Status Report; June 29, 2012

- EC 274720; 2F52-142; A And C Phase Grid Side Jumpers

13

Attachment

- EN48053; Unit 2 Manual Reactor Actuated Due To Indications Of 100% Load Rejection;

June 27, 2012

- EN47896; Licensed Operating Supervisor Tested Positive For A For-Cause Test For Alcohol;

May 3, 2012

- ER.2-1 Strength Plan

- Incident Investigation And Post-Trip Reviews; Completed June 27, 2012

- NARS Forms; April 25, 2012

- Nextera Energy Life Cycle Management Plan; November 26, 2012

- NP 2.1.4; Operator Burdens; Revision 14

- NPM 2012-0111; Internal Correspondence From D. Weber; Subject: Operator Burden Review

Board Meeting Minutes; April 4, 2012

- OI 38; Circulating Water System Operation; Revision 56

- OP 1C; Startup To Power Operation Unit 2; Revision 24

- OP 3A Unit 1; Power Operation To Hot Standby Unit 1; Revision 9

- OP 3B; Reactor Shutdown; Revision 43

- OP-AA-108; Oversight And Control Of Operator Burdens; Revision 0

- Open POD List; Indicator OX-14; April 2012

- PBNP Outage Status Report; June 29, 2012

- PBNP Shutdown Safety Assessment And Fire Condition; Unit 2; June 29, 2012

- PBNP Subcomponent PM Optimization Charter; April 10, 2012

- PBNP Unit 2 Forced Outage List; As Of April 17, April 19, 2012

- PBNP Unit 2; Forced Outage List; As Of June 29, 2012

- PFNP U2 cycle 32 F52-142 Repair Mode; April 13, April 17, 2012

- POD; May 2, 2012

- Response to NRC Questions Received; Dated June 11, 2012

- Safety Monitor, Unit 1; June 27 To 28, 2012

- Safety Monitor, Unit 2; June 27, 2012

- Station Log; April 19 To April 21, 2012

- Station Log; June 27 To June 29, 2012

- Station Log; Various Dates From April 8 To April 27, 2012

- Unit 2 Planned Outage Shift Coverage; Begins April 19, 2012

- Westinghouse Simulator Handbook; Summary Of Protection Grade Interlocks; Revision 1107

- WO 40106974-01; Unit 2 345 KV Output Breaker; April 12, 2012

- AR01380059; NEI Buried Piping Initiative; January 11, 2010

4OA5 Other Activities

- AR01660378; 2N-31 SRNI HVPS Failed High

- AR01687256; June 13 Unit 2 Rx Trip LER/PI Data Needs Revision

- AR01762573 Buried And Underground Piping And Tanks Inspection; May 2, 2012

- ENG-ER-AA-102; Buried Piping Program Manager Qualification Guide; Revision 1

- ER-AA-102; Buried Piping Program; Revision 3

- ER-AA-102-1000; Buried Piping Examination Procedure; Revision 1

- LER 05000301/2011-004-00; Automatic Reactor Trip During Startup Physics Testing Due To

Source Range Detector Failure; July 25, 2011

- LER 05000301/2011-004-01; Automatic Reactor Trip During Startup Physics Testing Due To

Source Range Detector Failure; October 13, 2011

- LR-AMP-018-BSMON; Buried Services Monitoring Program Basis Document For License

Renewal; Revision 0

- PBNP Buried Piping Inspection Plan; Revision 1

- PBSA-12-21; Quick Hit Assessment Report; March 29, 2012

14

Attachment

- Program Health Report; Buried Piping; January 1 To March 31, 2012

- Program Health Report; Cathodic Protection; January 1 To March 31, 2012

- RCA 01660378; Unit 2 Reactor Trip Due To 2N31 High Level Trip; July 26 And July 14, 2011

- SEM 8.0; Buried Services Monitoring Program; Revision 0

15

Attachment

LIST OF ACRONYMS USED

AC

Alternating Current

ADAMS

Agencywide Document Access Management System

AFW

Auxiliary Feedwater

ALARA

As-Low-As-Is-Reasonably-Achievable

AOP

Abnormal Operating Procedure

ASME

American Society of Mechanical Engineers

BOL

Beginning Of Life

CAP

Corrective Action Program

CCW

Component Cooling Water

CFR

Code of Federal Regulations

CR

Condition Report

DRP

Division of Reactor Projects

EDG

Emergency Diesel Generator

EPU

Extended Power Uprate

FP

Fire Protection

FSAR

Final Safety Analysis Report

FW

Feedwater

HEPA

High Efficiency Particulate Air

IP

Inspection Procedure

IR

Inspection Report

kV

Kilovolt

LER

Licensee Event Report

MFIV

Main Feedwater Isolation Valve

MSIV

Main Steam Isolation Valve

NCV

Non-Cited Violation

NEI

Nuclear Energy Institute

NFPA

National Fire Protection Association

NRC

U.S. Nuclear Regulatory Commission

OWA

Operator Workaround

PAB

Primary Auxiliary Building

PARS

Publicly Available Records System

PI

Performance Indicator

PMT

Post-Maintenance Testing

RCS

Reactor Coolant System

RHR

Residual Heat Removal

SDP

Significance Determination Process

SI

Safety Injection

SR

Safety-Related

SRM

Source Range Monitor

SSC

Structure, System, and Component

SW

Service Water

TDAFW

Turbine-Driven Auxiliary Feedwater

TEDE

Total Effective Dose Equivalent

TI

Temporary Instruction

TS

Technical Specification

TSC

Technical Support Center

URI

Unresolved Item

WO

Work Order

L. Meyer

-2-

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its

enclosure, and your response (if any) will be available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records System (PARS)

component of NRC's Agencywide Document Access and Management System (ADAMS).

ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html

(the Public Electronic Reading Room).

Sincerely,

/RA/

Michael A. Kunowski, Branch Chief

Branch 5

Division of Reactor Projects

Docket Nos.: 05000266; 05000301

License Nos.: DPR-24; DPR-27

Enclosure: Inspection Report 05000266/2012003 and 05000301/2012003;

w/Attachment: Supplemental Information

cc w/encl:

Distribution via ListServ

DISTRIBUTION:

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To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" = Copy with attach/encl "N" = No copy

OFFICE

RIII

RIII

RIII

RIII

NAME

MKunowski:rj

DATE

08/03/12

OFFICIAL RECORD COPY

Letter to L. Meyer from M. Kunowski dated August 3, 2012

SUBJECT:

POINT BEACH NUCLEAR PLANT, UNITS 1 AND 2

NRC INTEGRATED INSPECTION REPORT 05000266/2012003 AND

05000301/2012003

DISTRIBUTION:

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