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{{#Wiki_filter:UNITED STATES
{{#Wiki_filter:UNITED STATES  
                                        NUCLEAR REGULATORY COMMISSION
NUCLEAR REGULATORY COMMISSION  
                                                      REGION II
REGION II  
                                    245 PEACHTREE CENTER AVENUE NE, SUITE 1200
245 PEACHTREE CENTER AVENUE NE, SUITE 1200  
                                              ATLANTA, GEORGIA 30303-1257
ATLANTA, GEORGIA 30303-1257  
                                          November 7, 2012
Mr. Michael J. Annacone
Vice President
Brunswick Steam Electric Plant
November 7, 2012  
P.O. Box 10429
Southport, NC 28461-0429
SUBJECT:       BRUNSWICK STEAM ELECTRIC PLANT - NRC INTEGRATED INSPECTION
Mr. Michael J. Annacone  
                REPORT NOS.: 05000325/2012004 AND 05000324/2012004
Vice President  
Dear Mr. Annacone:
Brunswick Steam Electric Plant  
On September 30, 2012, the U.S. Nuclear Regulatory Commission (NRC) completed an
P.O. Box 10429  
inspection at your Brunswick Unit 1 and 2 facilities. The enclosed integrated inspection report
Southport, NC 28461-0429  
documents the inspection findings, which were discussed on October 11, 2012, with you and
other members of your staff.
SUBJECT:  
The inspection examined activities conducted under your license as they relate to safety and
BRUNSWICK STEAM ELECTRIC PLANT - NRC INTEGRATED INSPECTION  
compliance with the Commissions rules and regulations and with the conditions of your license.
REPORT NOS.: 05000325/2012004 AND 05000324/2012004  
The inspectors reviewed selected procedures and records, observed activities, and interviewed
personnel.
Dear Mr. Annacone:  
One NRC-identified and one self-revealing finding of very low safety significance (Green) were
identified during this inspection. These findings were determined to involve a violation of NRC
On September 30, 2012, the U.S. Nuclear Regulatory Commission (NRC) completed an  
requirements. Further, two licensee-identified violations were determined to be of very low
inspection at your Brunswick Unit 1 and 2 facilities. The enclosed integrated inspection report  
safety significance and are listed in this report. The NRC is treating these findings as non-cited
documents the inspection findings, which were discussed on October 11, 2012, with you and  
violations (NCVs) consistent with Section 2.3.2 of the Enforcement Policy.
other members of your staff.  
If you contest the violations or the significance of these NCVs, you should provide a response
within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear
The inspection examined activities conducted under your license as they relate to safety and  
Regulatory Commission, ATTN.: Document Control Desk, Washington DC 20555-0001; with
compliance with the Commissions rules and regulations and with the conditions of your license.  
copies to the Regional Administrator Region II; the Director, Office of Enforcement, United
The inspectors reviewed selected procedures and records, observed activities, and interviewed  
States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident
personnel.  
Inspector at the Brunswick Steam Electric Plant.
If you disagree with the cross-cutting aspect assignment in this report, you should provide a
One NRC-identified and one self-revealing finding of very low safety significance (Green) were  
response within 30 days of the date of this inspection report, with the basis for your
identified during this inspection. These findings were determined to involve a violation of NRC  
disagreement, to the Regional Administrator, Region II, and the NRC Resident Inspector at the
requirements. Further, two licensee-identified violations were determined to be of very low  
safety significance and are listed in this report. The NRC is treating these findings as non-cited  
violations (NCVs) consistent with Section 2.3.2 of the Enforcement Policy.  
If you contest the violations or the significance of these NCVs, you should provide a response  
within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear  
Regulatory Commission, ATTN.: Document Control Desk, Washington DC 20555-0001; with  
copies to the Regional Administrator Region II; the Director, Office of Enforcement, United  
States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident  
Inspector at the Brunswick Steam Electric Plant.  
If you disagree with the cross-cutting aspect assignment in this report, you should provide a  
response within 30 days of the date of this inspection report, with the basis for your  
disagreement, to the Regional Administrator, Region II, and the NRC Resident Inspector at the  
Brunswick Steam Electric Plant.
Brunswick Steam Electric Plant.


M. Annacone                                     2
M. Annacone  
In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter, its
2  
enclosure, and your response (if any) will be available electronically for public inspection in the
NRC Public Document Room or from the Publicly Available Records (PARS) component of
NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter, its  
                                            Sincerely,
enclosure, and your response (if any) will be available electronically for public inspection in the  
                                            /RA/
NRC Public Document Room or from the Publicly Available Records (PARS) component of  
                                            Randall A. Musser, Chief
NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at  
                                            Reactor Projects Branch 4
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).  
                                            Division of Reactor Projects
Docket Nos.: 50-325, 50-324
Sincerely,  
License Nos.: DPR-71, DPR-62
Enclosure:     Inspection Report 05000325, 324/2012004
/RA/  
              w/Attachment: Supplemental Information
cc w/encl:     (See page 3)
Randall A. Musser, Chief  
Reactor Projects Branch 4  
Division of Reactor Projects  
Docket Nos.: 50-325, 50-324  
License Nos.: DPR-71, DPR-62  
Enclosure:  
Inspection Report 05000325, 324/2012004  
w/Attachment: Supplemental Information  
cc w/encl:  
(See page 3)


M. Annacone
2
In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter, its
enclosure, and your response (if any) will be available electronically for public inspection in the
NRC Public Document Room or from the Publicly Available Records (PARS) component of
NRCs document system (ADAMS).  ADAMS is accessible from the NRC Web site at
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,
/RA/
Randall A. Musser, Chief
Reactor Projects Branch 4
Division of Reactor Projects
Docket Nos.: 50-325, 50-324
License Nos.: DPR-71, DPR-62
Enclosure:
Inspection Report 05000325, 324/2012004
w/Attachment:  Supplemental Information
cc w/encl:
(See page 3)
x PUBLICLY AVAILABLE
G NON-PUBLICLY AVAILABLE
G SENSITIVE
x NON-SENSITIVE
ADAMS: x Yes
ACCESSION NUMBER:ML12312A082_________________ 
x SUNSI REVIEW COMPLETE x FORM 665 ATTACHED
OFFICE
RII:DRP
RII:DRP
RII:DRP
RII:DRP
RII:DRP
RII:DRP
RII:DRP
SIGNATURE
JSD: /RA/
RAM RA for
MPS
Via e-mail
Via e-mail
Via e-mail
Via e-mail
JGW: /RA/
NAME
JDodson
MCatts
MSchwieg
PNiebaum
LLake
MEndress
JWorosilo
DATE
10/24/2012
11/07/2012
10/24/2012
10/29/2012
10/26/2012
10/25/2012
10/15/2012
E-MAIL COPY?
    YES
NO   
  YES
NO      YES
NO   
  YES
NO   
  YES
NO      YES
NO   
  YES
NO   
OFFICE
RII:DRP
RII:DRS
SIGNATURE
RAM: /RA/
Via e-mail
NAME
RMusser
MSpeck
DATE
11/7/2012
11/06/2012
E-MAIL COPY?
    YES
NO   
  YES
NO   
OFFICIAL
RECORD
COPY          DOCUMENT
NAME:
G:\\DRPII\\RPB4\\BRUNSWICK\\REPORTS\\2012
REPORTS\\12-
04\\BRUNSWICK IIR 2012004.DOCX


ML12312A082_________________                x SUNSI REVIEW COMPLETE x FORM 665 ATTACHED
M. Annacone
  OFFICE            RII:DRP        RII:DRP      RII:DRP          RII:DRP          RII:DRP          RII:DRP        RII:DRP
3
  SIGNATURE        JSD: /RA/      RAM RA for    Via e-mail      Via e-mail      Via e-mail      Via e-mail      JGW: /RA/
                                  MPS
   
  NAME              JDodson        MCatts        MSchwieg        PNiebaum        LLake            MEndress        JWorosilo
   
  DATE                10/24/2012      11/07/2012    10/24/2012      10/29/2012      10/26/2012      10/25/2012      10/15/2012
cc w/encl:  
  E-MAIL COPY?        YES    NO    YES      NO YES      NO      YES      NO    YES      NO    YES      NO    YES      NO
Plant General Manager
  OFFICE            RII:DRP        RII:DRS
Brunswick Steam Electric Plant
  SIGNATURE        RAM: /RA/      Via e-mail
Progress Energy
  NAME              RMusser        MSpeck
Electronic Mail Distribution
  DATE                  11/7/2012      11/06/2012
   
E-MAIL COPY?        YES    NO    YES      NO
Edward L. Wills, Jr.
       
Director Site Operations
M. Annacone                          3
Brunswick Steam Electric Plant
cc w/encl:                            Lee Grzeck
Electronic Mail Distribution
Plant General Manager                  Regulatory Affairs Manager
   
Brunswick Steam Electric Plant        Brunswick Steam Electric Plant
J. W. (Bill) Pitesa
Progress Energy                        Progress Energy Carolinas, Inc.
Senior Vice President
Electronic Mail Distribution           Electronic Mail Distribution
Nuclear Operations
Edward L. Wills, Jr.                  Randy C. Ivey
Duke Energy Corporation
Director Site Operations              Manager, Nuclear Oversight
Electronic Mail Distribution
Brunswick Steam Electric Plant        Brunswick Steam Electric Plant
   
Electronic Mail Distribution          Progress Energy Carolinas, Inc.
John A. Krakuszeski
                                      Electronic Mail Distribution
Plant Manager
J. W. (Bill) Pitesa
Brunswick Steam Electric Plant  
Senior Vice President                  Paul E. Dubrouillet
Electronic Mail Distribution
Nuclear Operations                    Manager, Training
   
Duke Energy Corporation                Brunswick Steam Electric Plant
Lara S. Nichols
Electronic Mail Distribution           Electronic Mail Distribution
Deputy General Counsel
John A. Krakuszeski                    Joseph W. Donahue
Duke Energy Corporation
Plant Manager                          Vice President
Electronic Mail Distribution
Brunswick Steam Electric Plant        Nuclear Oversight
   
Electronic Mail Distribution          Progress Energy
M. Christopher Nolan
                                      Electronic Mail Distribution
Director - Regulatory Affairs
Lara S. Nichols
General Office
Deputy General Counsel                Senior Resident Inspector
Duke Energy Corporation
Duke Energy Corporation                U.S. Nuclear Regulatory Commission
Electronic Mail Distribution
Electronic Mail Distribution          Brunswick Steam Electric Plant
   
                                      U.S. NRC
Michael J. Annacone
M. Christopher Nolan                  8470 River Road, SE
Vice President
Director - Regulatory Affairs          Southport, NC 28461
Brunswick Steam Electric Plant
General Office
Electronic Mail Distribution
Duke Energy Corporation                John H. O'Neill, Jr.
   
Electronic Mail Distribution          Shaw, Pittman, Potts & Trowbridge
Annette H. Pope
                                      2300 N. Street, NW
Manager-Organizational Effectiveness
Michael J. Annacone                    Washington, DC 20037-1128
Brunswick Steam Electric Plant
Vice President
Electronic Mail Distribution
Brunswick Steam Electric Plant        Peggy Force
Electronic Mail Distribution          Assistant Attorney General
Lee Grzeck  
                                      State of North Carolina
Regulatory Affairs Manager  
Annette H. Pope                        P.O. Box 629
Brunswick Steam Electric Plant  
Manager-Organizational Effectiveness  Raleigh, NC 27602
Progress Energy Carolinas, Inc.  
Brunswick Steam Electric Plant
Electronic Mail Distribution  
Electronic Mail Distribution          (cc w/encl - continued)
Randy C. Ivey  
Manager, Nuclear Oversight  
Brunswick Steam Electric Plant  
Progress Energy Carolinas, Inc.  
Electronic Mail Distribution  
Paul E. Dubrouillet  
Manager, Training  
Brunswick Steam Electric Plant  
Electronic Mail Distribution  
Joseph W. Donahue  
Vice President  
Nuclear Oversight  
Progress Energy  
Electronic Mail Distribution  
Senior Resident Inspector  
U.S. Nuclear Regulatory Commission  
Brunswick Steam Electric Plant  
U.S. NRC  
8470 River Road, SE  
Southport, NC   28461  
John H. O'Neill, Jr.  
Shaw, Pittman, Potts & Trowbridge  
2300 N. Street, NW  
Washington, DC   20037-1128  
Peggy Force  
Assistant Attorney General  
State of North Carolina  
P.O. Box 629  
Raleigh, NC   27602  
(cc w/encl - continued)


M. Annacone                               4
M. Annacone  
cc w/encl contd:
4  
Chairman
North Carolina Utilities Commission
Electronic Mail Distribution
Robert P. Gruber
cc w/encl contd:  
Executive Director
Chairman  
Public Staff - NCUC
North Carolina Utilities Commission  
4326 Mail Service Center
Electronic Mail Distribution  
Raleigh, NC 27699-4326
Anthony Marzano
Robert P. Gruber  
Director
Executive Director  
Brunswick County Emergency Services
Public Staff - NCUC  
Electronic Mail Distribution
4326 Mail Service Center  
Public Service Commission
Raleigh, NC   27699-4326  
State of South Carolina
P.O. Box 11649
Anthony Marzano  
Columbia, SC 29211
Director  
W. Lee Cox, III
Brunswick County Emergency Services  
Section Chief
Electronic Mail Distribution  
Radiation Protection Section
N.C. Department of Environmental Commerce & Natural Resources
Public Service Commission  
Electronic Mail Distribution
State of South Carolina  
Warren Lee
P.O. Box 11649  
Emergency Management Director
Columbia, SC   29211  
New Hanover County
Department of Emergency Management
W. Lee Cox, III  
230 Government Center Drive
Section Chief  
Suite 115
Radiation Protection Section  
Wilmington, NC 28403
N.C. Department of Environmental Commerce & Natural Resources  
Electronic Mail Distribution  
Warren Lee  
Emergency Management Director  
New Hanover County
Department of Emergency Management  
230 Government Center Drive  
Suite 115  
Wilmington, NC   28403  


M. Annacone                                   5
M. Annacone  
Letter to Michael J. Annacone from Randall A. Musser dated November 7, 2012
5  
SUBJECT:       BRUNSWICK STEAM ELECTRIC PLANT - NRC INTEGRATED INSPECTION
                REPORT NOS.: 05000325/2012004 AND 05000324/2012004
Distribution w/encl:
J. Baptist, RII EICS
Letter to Michael J. Annacone from Randall A. Musser dated November 7, 2012
L. Douglas, RII EICS
OE Mail (email address if applicable)
SUBJECT:  
RIDSNRRDIRS
BRUNSWICK STEAM ELECTRIC PLANT - NRC INTEGRATED INSPECTION  
PUBLIC
REPORT NOS.: 05000325/2012004 AND 05000324/2012004  
R. Pascarelli, NRR ((Regulatory Conferences Only))
Distribution w/encl:  
J. Baptist, RII EICS
L. Douglas, RII EICS
OE Mail (email address if applicable)  
RIDSNRRDIRS  
PUBLIC  
R. Pascarelli, NRR ((Regulatory Conferences Only))  
RidsNrrPMBrunswick Resource
RidsNrrPMBrunswick Resource


              U. S. NUCLEAR REGULATORY COMMISSION
                                  REGION II
Docket Nos.: 50-325, 50-324
Enclosure
License Nos.: DPR-71, DPR-62
U. S. NUCLEAR REGULATORY COMMISSION  
Report Nos.: 05000325/2012004, 05000324/2012004
Licensee:     Carolina Power and Light (CP&L)
REGION II  
Facility:     Brunswick Steam Electric Plant, Units 1 & 2
Location:     8470 River Road, SE
              Southport, NC 28461
Docket Nos.:  
Dates:       July 1, 2012 through September 30, 2012
50-325, 50-324  
Inspectors:   M. Catts, Senior Resident Inspector
              M. Schwieg, Resident Inspector
              P. Niebaum, Acting Senior Resident Inspector
              J. Dodson, Senior Project Engineer (1R04, 1R05, 4OA2)
License Nos.:  
              L. Lake, Senior Reactor Inspector (4OA5)
DPR-71, DPR-62  
              M. Endress, Reactor Inspector (1R07)
Approved by: Randall A. Musser, Chief
              Reactor Projects Branch 4
              Division of Reactor Projects
Report Nos.:  
                                                                    Enclosure
05000325/2012004, 05000324/2012004  
Licensee:  
Carolina Power and Light (CP&L)  
Facility:  
Brunswick Steam Electric Plant, Units 1 & 2  
Location:  
8470 River Road, SE  
Southport, NC 28461  
Dates:  
July 1, 2012 through September 30, 2012  
Inspectors:  
M. Catts, Senior Resident Inspector  
M. Schwieg, Resident Inspector  
P. Niebaum, Acting Senior Resident Inspector  
J. Dodson, Senior Project Engineer (1R04, 1R05, 4OA2)  
L. Lake, Senior Reactor Inspector (4OA5)  
M. Endress, Reactor Inspector (1R07)  
Approved by:  
Randall A. Musser, Chief  
Reactor Projects Branch 4  
Division of Reactor Projects  


                                    SUMMARY OF FINDINGS
IR 05000325/2012004, 05000324/2012004; 07/01/12 - 09/30/12; Brunswick Steam Electric
Plant, Units 1 & 2; Refueling and Other Outage Activities, Identification and Resolution of
SUMMARY OF FINDINGS  
Problems
This report covers a three-month period of inspection by resident inspectors and announced
baseline inspections by regional inspectors. Two Green findings were identified by the
IR 05000325/2012004, 05000324/2012004; 07/01/12 - 09/30/12; Brunswick Steam Electric  
inspectors. The significance of most findings is indicated by their color (Green, White, Yellow,
Plant, Units 1 & 2; Refueling and Other Outage Activities, Identification and Resolution of  
Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process
Problems  
(SDP). The cross-cutting aspects were determined using IMC 0310, Components Within the
Cross-Cutting Areas. Findings for which the SDP does not apply may be Green or be assigned
This report covers a three-month period of inspection by resident inspectors and announced  
a severity level after NRC management review.
baseline inspections by regional inspectors. Two Green findings were identified by the  
A.     NRC-Identified and Self-Revealing Findings
inspectors. The significance of most findings is indicated by their color (Green, White, Yellow,  
        Cornerstone: Barrier Integrity
Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process  
        Green: The inspectors identified a Green non-cited violation (NCV) of TS 3.6.4.1,
(SDP). The cross-cutting aspects were determined using IMC 0310, Components Within the  
        Secondary Containment because the licensee did not maintain secondary containment
Cross-Cutting Areas. Findings for which the SDP does not apply may be Green or be assigned  
        operable as required during a maintenance activity considered an operation with a
a severity level after NRC management review.  
        potential for draining the reactor vessel (OPDRV). Once questioned by the inspectors,
        the licensee restored secondary containment, developed an Operation standing
A.  
        instruction (12-052) to treat the activity as an OPDRV and placed this issue into its
NRC-Identified and Self-Revealing Findings  
        corrective action program (CAP) as AR 562188.
        The failure to maintain secondary containment operable while Unit 1 was in Mode 4 with
Cornerstone: Barrier Integrity  
        an OPDRV in progress was a performance deficiency. The finding was more than minor
        because it was associated with the configuration control attribute of the Barrier Integrity
Green: The inspectors identified a Green non-cited violation (NCV) of TS 3.6.4.1,  
        Cornerstone, and adversely affected the cornerstone objective to provide reasonable
Secondary Containment because the licensee did not maintain secondary containment  
        assurance that physical design barriers (fuel cladding, reactor coolant system, and
operable as required during a maintenance activity considered an operation with a  
        containment) protect the public from radionuclide releases caused by accidents or
potential for draining the reactor vessel (OPDRV). Once questioned by the inspectors,  
        events because the Unit 1 secondary containment boundary was not preserved or
the licensee restored secondary containment, developed an Operation standing  
        maintained. The inspectors evaluated the finding using Inspection Manual Chapter
instruction (12-052) to treat the activity as an OPDRV and placed this issue into its  
        (IMC) 0609, Attachment 4, Phase 1 - Initial Screening and Characterization of Findings,
corrective action program (CAP) as AR 562188.  
        which required an analysis using IMC 0609 Appendix G since the reactor was in Mode 4
The failure to maintain secondary containment operable while Unit 1 was in Mode 4 with  
        (cold shutdown). The finding was determined to be of very low safety significance
an OPDRV in progress was a performance deficiency. The finding was more than minor  
        (Green) according to IMC 0609 Appendix G, Attachment 1, Checklist 6, since a
because it was associated with the configuration control attribute of the Barrier Integrity  
        quantitative assessment (Phase 2 or Phase 3 evaluation) was not required. Specifically,
Cornerstone, and adversely affected the cornerstone objective to provide reasonable  
        the inspectors determined that the licensee maintained adequate mitigation capability for
assurance that physical design barriers (fuel cladding, reactor coolant system, and  
        reactor vessel water level inventory and an event did not occur that could be
containment) protect the public from radionuclide releases caused by accidents or  
        characterized as a loss of control. The cause of this finding was directly related to the
events because the Unit 1 secondary containment boundary was not preserved or  
        cross-cutting aspect of Accurate Procedures in the Resources component of the Human
maintained. The inspectors evaluated the finding using Inspection Manual Chapter  
        Performance area, because the licensee did not consider the recirculation pump seal
(IMC) 0609, Attachment 4, Phase 1 - Initial Screening and Characterization of Findings,  
        replacement activity to be OPDRV based on procedural guidance that contains
which required an analysis using IMC 0609 Appendix G since the reactor was in Mode 4  
        exclusions to what are considered OPDRV activities. [H.2(c)] (Section 1R20)
(cold shutdown). The finding was determined to be of very low safety significance  
(Green) according to IMC 0609 Appendix G, Attachment 1, Checklist 6, since a  
quantitative assessment (Phase 2 or Phase 3 evaluation) was not required. Specifically,  
the inspectors determined that the licensee maintained adequate mitigation capability for  
reactor vessel water level inventory and an event did not occur that could be  
characterized as a loss of control. The cause of this finding was directly related to the  
cross-cutting aspect of Accurate Procedures in the Resources component of the Human  
Performance area, because the licensee did not consider the recirculation pump seal  
replacement activity to be OPDRV based on procedural guidance that contains  
exclusions to what are considered OPDRV activities. [H.2(c)] (Section 1R20)  


                                              3
  Cornerstone: Emergency Preparedness
3  
  Green: A self-revealing Green NCV of 10 CFR 50.54(q)(2) was identified for the
  licensees failure to properly evaluate or consider the impact to emergency response
Cornerstone: Emergency Preparedness  
  facilities of design change ESR98-00436 which was implemented in 1999. This resulted
  in the loss of Emergency Response Facility Information System (ERFIS), Emergency
Green: A self-revealing Green NCV of 10 CFR 50.54(q)(2) was identified for the  
  Response Data System (ERDS), Safety Parameter Display System (SPDS), and all
licensees failure to properly evaluate or consider the impact to emergency response  
  displays including radiation monitors for the emergency response facilities. Specifically,
facilities of design change ESR98-00436 which was implemented in 1999. This resulted  
  the licensee failed to ensure that adequate emergency response facilities and equipment
in the loss of Emergency Response Facility Information System (ERFIS), Emergency  
  were available as required by the Brunswick Nuclear Plant Radiological Emergency
Response Data System (ERDS), Safety Parameter Display System (SPDS), and all  
  Plan, Section 1.3.1.3 revision 80 and 10 CFR 50.47(b)(8). This issue was captured in the
displays including radiation monitors for the emergency response facilities. Specifically,  
  licensees CAP as AR 542704.
the licensee failed to ensure that adequate emergency response facilities and equipment  
  The licensees failure to properly evaluate or consider the impact to emergency
were available as required by the Brunswick Nuclear Plant Radiological Emergency  
  response facilities of design change ESR98-00436 which was implemented in 1999 was
Plan, Section 1.3.1.3 revision 80 and 10 CFR 50.47(b)(8). This issue was captured in the  
  a performance deficiency. Specifically, the licensee introduced a single point failure
licensees CAP as AR 542704.  
  mode which did not meet the design requirements specified in their Design Basis
  Document (DBD 60) sections 3.6.7.2 and 3.6.7.3. This resulted in the licensees failure
The licensees failure to properly evaluate or consider the impact to emergency  
  to ensure that adequate emergency response facilities and equipment were available as
response facilities of design change ESR98-00436 which was implemented in 1999 was  
  delineated in the Updated Final Safety Analysis Report (UFSAR) Section 7.7.1.9, and
a performance deficiency. Specifically, the licensee introduced a single point failure  
  required by the Brunswick Nuclear Plant Radiological Emergency Plan, Section 1.3.1.3,
mode which did not meet the design requirements specified in their Design Basis  
  revision 80, and 10 CFR 50.47(b)(8). The finding was more than minor because it
Document (DBD 60) sections 3.6.7.2 and 3.6.7.3. This resulted in the licensees failure  
  adversely affected the Emergency Preparedness Cornerstone objective of ensuring that
to ensure that adequate emergency response facilities and equipment were available as  
  the licensee was capable of implementing adequate measures to protect the health and
delineated in the Updated Final Safety Analysis Report (UFSAR) Section 7.7.1.9, and  
  safety of the public in the event of a radiological emergency. Specifically, the Facilities
required by the Brunswick Nuclear Plant Radiological Emergency Plan, Section 1.3.1.3,  
  and Equipment attribute was affected during the time when the ERFIS, ERDS, SPDS,
revision 80, and 10 CFR 50.47(b)(8). The finding was more than minor because it  
  and all displays including radiation monitors for the emergency response facilities were
adversely affected the Emergency Preparedness Cornerstone objective of ensuring that  
  degraded, and as a result did not meet 10 CFR 50.47(b)(8) Planning Standard program
the licensee was capable of implementing adequate measures to protect the health and  
  element, adequate emergency facilities and equipment to support the emergency
safety of the public in the event of a radiological emergency. Specifically, the Facilities  
  response are provided and maintained. The finding was assessed for significance in
and Equipment attribute was affected during the time when the ERFIS, ERDS, SPDS,  
  accordance with NRC IMC 0609, Appendix B Emergency Preparedness Significance
and all displays including radiation monitors for the emergency response facilities were  
  Determination Process. Attachment 2 of Appendix B, Failure to Comply Significance
degraded, and as a result did not meet 10 CFR 50.47(b)(8) Planning Standard program  
  Logic is as follows: Failure to comply; Loss of Risk Significant Planning Standard
element, adequate emergency facilities and equipment to support the emergency  
  Function (RSPS), No; RSPS Degraded Function, No; Loss of Planning Standard
response are provided and maintained. The finding was assessed for significance in  
  Function, No; the result is a Green finding. The inspectors determined that this resulted
accordance with NRC IMC 0609, Appendix B Emergency Preparedness Significance  
  in a very low safety significance finding (Green). No cross-cutting aspect was assigned
Determination Process. Attachment 2 of Appendix B, Failure to Comply Significance  
  to this finding because the performance deficiency occurred more than three years ago
Logic is as follows: Failure to comply; Loss of Risk Significant Planning Standard  
  and is not reflective of current plant performance. (Section 4OA2.2)
Function (RSPS), No; RSPS Degraded Function, No; Loss of Planning Standard  
B. Licensee-Identified Violations
Function, No; the result is a Green finding. The inspectors determined that this resulted  
  Violations of very low safety significance that were identified by the licensee have been
in a very low safety significance finding (Green). No cross-cutting aspect was assigned  
  reviewed by inspectors. Corrective actions taken or planned by the licensee have been
to this finding because the performance deficiency occurred more than three years ago  
  entered into the licensees CAP. These violations and corrective action tracking
and is not reflective of current plant performance. (Section 4OA2.2)  
  numbers are listed in Section 4OA7 of this report.
B.  
Licensee-Identified Violations  
Violations of very low safety significance that were identified by the licensee have been  
reviewed by inspectors. Corrective actions taken or planned by the licensee have been  
entered into the licensees CAP. These violations and corrective action tracking  
numbers are listed in Section 4OA7 of this report.  


                                        REPORT DETAILS
Summary of Plant Status
Unit 1 began the inspection period at rated thermal power (RTP), and operated at or near full
REPORT DETAILS  
power until July 22, 2012 when reactor power was lowered to 52 percent to clear a fouled
circulating water debris filter and power was returned to RTP on July 23, 2012. On August 3,
Summary of Plant Status  
2012, power was reduced to 70 percent for a rod sequence exchange and power was returned
to RTP on August 5, 2012. On August 5, 2012, power was reduced to 90 percent for control rod
Unit 1 began the inspection period at rated thermal power (RTP), and operated at or near full  
improvement and power was returned to RTP on the same day. On August 8, 2012, power was
power until July 22, 2012 when reactor power was lowered to 52 percent to clear a fouled  
reduced to 65 percent for offsite transmission line work and power was returned to RTP on the
circulating water debris filter and power was returned to RTP on July 23, 2012. On August 3,  
same day. On September 16, 2012, the reactor was shut down for forced outage to replace the
2012, power was reduced to 70 percent for a rod sequence exchange and power was returned  
1A and 1B recirculation pump seal assemblies. Reactor startup commenced on September 27,
to RTP on August 5, 2012. On August 5, 2012, power was reduced to 90 percent for control rod  
2012 and the main generator was synchronized to the grid on September 28, 2012. Reactor
improvement and power was returned to RTP on the same day. On August 8, 2012, power was  
power was raised to RTP on September 29, 2012. On September 30, 2012 reactor power was
reduced to 65 percent for offsite transmission line work and power was returned to RTP on the  
reduced to 75 percent for a scheduled control rod improvement. Power ascension continued to
same day. On September 16, 2012, the reactor was shut down for forced outage to replace the  
RTP for the remainder of the inspection period.
1A and 1B recirculation pump seal assemblies. Reactor startup commenced on September 27,  
Unit 2 began the inspection period at RTP, and operated at or near full power until August 18,
2012 and the main generator was synchronized to the grid on September 28, 2012. Reactor  
2012, when power was reduced to 70 percent for a rod sequence exchange and power was
power was raised to RTP on September 29, 2012. On September 30, 2012 reactor power was  
returned to RTP on August 19, 2012. On August 20, 2012, power was reduced to 86 percent
reduced to 75 percent for a scheduled control rod improvement. Power ascension continued to  
for control rod improvement and power was returned to RTP on August 21, 2012. On August
RTP for the remainder of the inspection period.  
21, 2012, power was reduced to 94 percent for control rod improvement and power was
returned to RTP on August 21, 2012. On September 29, 2012, reactor power was reduced to
Unit 2 began the inspection period at RTP, and operated at or near full power until August 18,  
94 percent to support a scheduled rod improvement and returned to RTP later that day and
2012, when power was reduced to 70 percent for a rod sequence exchange and power was  
maintained RTP for the remainder of the inspection period.
returned to RTP on August 19, 2012. On August 20, 2012, power was reduced to 86 percent  
1.     REACTOR SAFETY
for control rod improvement and power was returned to RTP on August 21, 2012.   On August  
        Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
21, 2012, power was reduced to 94 percent for control rod improvement and power was  
1R01 Adverse Weather Protection (71111.01 - 1 sample)
returned to RTP on August 21, 2012. On September 29, 2012, reactor power was reduced to  
        External Flooding
94 percent to support a scheduled rod improvement and returned to RTP later that day and  
   a.   Inspection Scope
maintained RTP for the remainder of the inspection period.  
        The inspectors evaluated the design, material condition, and procedures for coping with
        the design basis probable maximum flood. The inspectors reviewed the Updated Final
1.  
        Safety Analysis Report (UFSAR), which depicted the design flood levels and protection
REACTOR SAFETY  
        areas containing safety-related equipment, to identify areas that may be affected by
        external flooding. The inspectors conducted a site walk-down of the service water
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity  
        building, to ensure that erected flood protection measures were in accordance with
        design specifications. The inspectors reviewed the sealing of equipment below the flood
1R01 Adverse Weather Protection (71111.01 - 1 sample)  
        line, adequacy of watertight doors, drain systems and sumps including check valves,
        and maintenance and calibration of flood protection equipment. The inspectors also
        reviewed operating procedures for mitigating external flooding during severe weather to
External Flooding  
   a.  
Inspection Scope
The inspectors evaluated the design, material condition, and procedures for coping with  
the design basis probable maximum flood. The inspectors reviewed the Updated Final  
Safety Analysis Report (UFSAR), which depicted the design flood levels and protection  
areas containing safety-related equipment, to identify areas that may be affected by  
external flooding. The inspectors conducted a site walk-down of the service water  
building, to ensure that erected flood protection measures were in accordance with  
design specifications. The inspectors reviewed the sealing of equipment below the flood  
line, adequacy of watertight doors, drain systems and sumps including check valves,  
and maintenance and calibration of flood protection equipment. The inspectors also  
reviewed operating procedures for mitigating external flooding during severe weather to


                                                5
      determine if the licensee planned or established adequate measures to protect against
5  
      external flooding events.
   b. Findings
determine if the licensee planned or established adequate measures to protect against  
      No findings were identified.
external flooding events.  
1R04 Equipment Alignment
.1   Quarterly Partial System Walk-downs (71111.04Q - 3 samples)
   b.  
   a. Inspection Scope
Findings  
      The inspectors performed partial system walk-downs of the following risk-significant
      systems:
No findings were identified.  
      *   Unit 2 A train Core Spray (CS) system while B residual heat removal/service
          (RHR/SW) was inoperable for a system outage on July 11, 2012;
1R04 Equipment Alignment  
      *   Unit 1 Reactor Building Closed Cooling Water (RBCCW) on July 27, 2012; and
      *   Unit 1 B Standby Gas Treatment (SBGT) while the A SBGT was inoperable for a
.1  
          maintenance outage on September 19, 2012.
Quarterly Partial System Walk-downs (71111.04Q - 3 samples)  
      The inspectors selected these systems based on their risk-significance relative to the
      reactor safety cornerstones at the time they were inspected. The inspectors attempted
   a.  
      to identify any discrepancies that could impact the function of the system, and, therefore,
Inspection Scope  
      potentially increase risk. The inspectors reviewed applicable operating procedures,
      system diagrams, UFSAR, Technical Specification (TS) requirements, outstanding work
The inspectors performed partial system walk-downs of the following risk-significant  
      orders, condition reports, and the impact of ongoing work activities on redundant trains
systems:  
      of equipment in order to identify conditions that could have rendered the systems
      incapable of performing their intended functions. The inspectors also walked down
*  
      accessible portions of the systems to verify that system components and support
Unit 2 A train Core Spray (CS) system while B residual heat removal/service  
      equipment were aligned correctly and were operable. The inspectors examined the
(RHR/SW) was inoperable for a system outage on July 11, 2012;  
      material condition of the components and observed operating parameters of equipment
*  
      to verify that there were no obvious deficiencies. The inspectors also verified that the
Unit 1 Reactor Building Closed Cooling Water (RBCCW) on July 27, 2012; and  
      licensee had properly identified and resolved equipment alignment problems that could
*  
      cause initiating events or impact the capability of mitigating systems or barriers and
Unit 1 B Standby Gas Treatment (SBGT) while the A SBGT was inoperable for a  
      entered them into the CAP with the appropriate significance characterization.
maintenance outage on September 19, 2012.  
   b. Findings
      No findings were identified.
The inspectors selected these systems based on their risk-significance relative to the  
.2   Semi-Annual Complete System Walk-down (71111.04S - 1 sample)
reactor safety cornerstones at the time they were inspected. The inspectors attempted  
   a. Inspection Scope
to identify any discrepancies that could impact the function of the system, and, therefore,  
      On September 5, 2012 the inspectors performed a complete system alignment
potentially increase risk. The inspectors reviewed applicable operating procedures,  
      inspection of the Unit 1 RHR system to verify the functional capability of the system.
system diagrams, UFSAR, Technical Specification (TS) requirements, outstanding work  
      This system was selected because it was considered both safety-significant and risk-
orders, condition reports, and the impact of ongoing work activities on redundant trains  
of equipment in order to identify conditions that could have rendered the systems  
incapable of performing their intended functions. The inspectors also walked down  
accessible portions of the systems to verify that system components and support  
equipment were aligned correctly and were operable. The inspectors examined the  
material condition of the components and observed operating parameters of equipment  
to verify that there were no obvious deficiencies. The inspectors also verified that the  
licensee had properly identified and resolved equipment alignment problems that could  
cause initiating events or impact the capability of mitigating systems or barriers and  
entered them into the CAP with the appropriate significance characterization.  
   b.  
Findings  
No findings were identified.  
.2  
Semi-Annual Complete System Walk-down (71111.04S - 1 sample)  
   a.  
Inspection Scope  
On September 5, 2012 the inspectors performed a complete system alignment  
inspection of the Unit 1 RHR system to verify the functional capability of the system.
This system was selected because it was considered both safety-significant and risk-


                                                6
    significant in the licensees probabilistic risk assessment. The inspectors walked down
6  
    the system to review mechanical and electrical equipment line-ups, electrical power
    availability, system pressure and temperature indications, as appropriate, component
significant in the licensees probabilistic risk assessment. The inspectors walked down  
    labeling, component lubrication, component and equipment cooling, hangers and
the system to review mechanical and electrical equipment line-ups, electrical power  
    supports, operability of support systems, and to ensure that ancillary equipment or
availability, system pressure and temperature indications, as appropriate, component  
    debris did not interfere with equipment operation. A review of a sample of past and
labeling, component lubrication, component and equipment cooling, hangers and  
    outstanding work orders (WOs) was performed to determine whether any deficiencies
supports, operability of support systems, and to ensure that ancillary equipment or  
    significantly affected the system function. In addition, the inspectors reviewed the CAP
debris did not interfere with equipment operation. A review of a sample of past and  
    to ensure that system equipment alignment problems were being identified and
outstanding work orders (WOs) was performed to determine whether any deficiencies  
    appropriately resolved.
significantly affected the system function. In addition, the inspectors reviewed the CAP  
  b.  Findings
to ensure that system equipment alignment problems were being identified and  
    No findings were identified.
appropriately resolved.
1R05 Fire Protection (71111.05Q - 5 samples)
   
    Quarterly Resident Inspector Tours
  b.  
  a. Inspection Scope
Findings
    The inspectors conducted fire protection walk-downs which were focused on availability,
    accessibility, and the condition of firefighting equipment in the following risk-significant
   
    plant areas:
No findings were identified.  
    *   Unit 1 and 2 Control Buildings 23' Elevation 1PFP-CB-7;
    *   Unit 1 Reactor Building East 50 Elevation 1PFP-RB1-1h;
1R05 Fire Protection (71111.05Q - 5 samples)  
    *   Unit 1 Turbine Building South Area 38 Elevation 1PFP-TB1-1k;
    *   Unit 2 Reactor Building 50 Elevation 2PFP-RB2-1h; and
    *   Unit 2 Reactor Building North 2A Core Spray Room 2-PFP-RB2-1b.
Quarterly Resident Inspector Tours  
    The inspectors reviewed areas to assess if the licensee had implemented a fire
   
    protection program that adequately controlled combustibles and ignition sources within
  a.  
    the plant, effectively maintained fire detection and suppression capability, maintained
Inspection Scope  
    passive fire protection features in good material condition, and had implemented
    adequate compensatory measures for out-of-service, degraded or inoperable fire
The inspectors conducted fire protection walk-downs which were focused on availability,  
    protection equipment, systems, or features in accordance with the licensees fire plan.
accessibility, and the condition of firefighting equipment in the following risk-significant  
    The inspectors selected fire areas based on their overall contribution to internal fire risk
plant areas:
    as documented in the plants Individual Plant Examination of External Events with later
    additional insights, their potential to impact equipment which could initiate or mitigate a
*  
    plant transient, or their impact on the plants ability to respond to a security event. Using
Unit 1 and 2 Control Buildings 23' Elevation 1PFP-CB-7;  
    the documents listed in the attachment, the inspectors verified that fire hoses and
*  
    extinguishers were in their designated locations and available for immediate use; that
Unit 1 Reactor Building East 50 Elevation 1PFP-RB1-1h;  
    fire detectors and sprinklers were unobstructed, that transient material loading was
*  
    within the analyzed limits; and fire doors, dampers, and penetration seals appeared to
Unit 1 Turbine Building South Area 38 Elevation 1PFP-TB1-1k;  
    be in satisfactory condition. The inspectors also verified that minor issues identified
*  
    during the inspection were entered into the licensees CAP.
Unit 2 Reactor Building 50 Elevation 2PFP-RB2-1h; and  
*  
Unit 2 Reactor Building North 2A Core Spray Room 2-PFP-RB2-1b.  
The inspectors reviewed areas to assess if the licensee had implemented a fire  
protection program that adequately controlled combustibles and ignition sources within  
the plant, effectively maintained fire detection and suppression capability, maintained  
passive fire protection features in good material condition, and had implemented  
adequate compensatory measures for out-of-service, degraded or inoperable fire  
protection equipment, systems, or features in accordance with the licensees fire plan.
The inspectors selected fire areas based on their overall contribution to internal fire risk  
as documented in the plants Individual Plant Examination of External Events with later  
additional insights, their potential to impact equipment which could initiate or mitigate a  
plant transient, or their impact on the plants ability to respond to a security event. Using  
the documents listed in the attachment, the inspectors verified that fire hoses and  
extinguishers were in their designated locations and available for immediate use; that  
fire detectors and sprinklers were unobstructed, that transient material loading was  
within the analyzed limits; and fire doors, dampers, and penetration seals appeared to  
be in satisfactory condition. The inspectors also verified that minor issues identified  
during the inspection were entered into the licensees CAP.  


                                                7
  b.  Findings
7  
    No findings were identified.
   
1R06 Flood Protection Measures (71111.06 - 1 sample)
  b.  
    Annual Review of Cables Located in Underground Bunkers/Manholes
Findings
  a. Inspection Scope
   
    The inspectors conducted an inspection of underground bunkers/manholes subject to
No findings were identified.  
    flooding that contain cables whose failure could disable risk-significant equipment. The
    inspectors performed walk-downs of risk-significant areas, including manhole 2-MH-
1R06 Flood Protection Measures (71111.06 - 1 sample)  
    7SW, to verify that the cables were not submerged in water, that cables and/or splices
    appear intact and to observe the condition of cable support structures. When applicable,
    the inspectors verified proper dewatering device (sump pump) operation and verified
Annual Review of Cables Located in Underground Bunkers/Manholes
    level alarm circuits are set appropriately to ensure that the cables will not be submerged.
   
    Where dewatering devices were not installed; the inspectors ensured that drainage was
  a.  
    provided and was functioning properly.
Inspection Scope  
  b.  Findings
    No findings were identified.
The inspectors conducted an inspection of underground bunkers/manholes subject to  
1R07 Heat Sink Performance (71111.07T - 3 samples)
flooding that contain cables whose failure could disable risk-significant equipment. The  
    Triennial Review of Heat Sink Performance
inspectors performed walk-downs of risk-significant areas, including manhole 2-MH-
  a. Inspection Scope
7SW, to verify that the cables were not submerged in water, that cables and/or splices  
    The inspectors selected the Residual Heat Removal (RHR) Heat Exchanger 2A, Diesel
appear intact and to observe the condition of cable support structures. When applicable,  
    Generator (DG) 3 Jacket Water Cooler and the Core Spray (CS) Room Cooler 1A,
the inspectors verified proper dewatering device (sump pump) operation and verified  
    based on their risk-significance in the licensees probabilistic safety analysis and their
level alarm circuits are set appropriately to ensure that the cables will not be submerged.  
    importance to safety-related mitigating system support functions in the NRCs model for
Where dewatering devices were not installed; the inspectors ensured that drainage was  
    Brunswick Nuclear Power Plant, Units 1 and 2.
provided and was functioning properly.
    For the RHR Heat Exchanger 2A, DG 3 Jacket Water Cooler and the CS Room Cooler
   
    1A, the inspectors reviewed the licensees inspection, maintenance, and monitoring of
  b.  
    biotic fouling and macro-fouling programs, to determine if they were adequate to ensure
Findings
    proper heat transfer. This was accomplished by determining whether the methods used
   
    were consistent with accepted industry practices. The inspectors also reviewed the
No findings were identified.  
    licensees inspection and cleaning activities had established acceptance criteria
    consistent with industry standards, and the as-found results were recorded, evaluated,
1R07 Heat Sink Performance (71111.07T - 3 samples)  
    and appropriately dispositioned to maintain structural integrity.
    For the RHR Heat Exchanger 2A, DG 3 Jacket Water Cooler and the CS Room Cooler
    1A, the inspectors reviewed the methods and results of heat exchanger performance
Triennial Review of Heat Sink Performance  
    inspections. In addition, the inspectors reviewed the condition and operation of the RHR
   
    Heat Exchanger 2A, DG 3 Jacket Water Cooler and the CS Room Cooler 1A to
  a.  
Inspection Scope  
The inspectors selected the Residual Heat Removal (RHR) Heat Exchanger 2A, Diesel  
Generator (DG) 3 Jacket Water Cooler and the Core Spray (CS) Room Cooler 1A,  
based on their risk-significance in the licensees probabilistic safety analysis and their  
importance to safety-related mitigating system support functions in the NRCs model for  
Brunswick Nuclear Power Plant, Units 1 and 2.  
For the RHR Heat Exchanger 2A, DG 3 Jacket Water Cooler and the CS Room Cooler  
1A, the inspectors reviewed the licensees inspection, maintenance, and monitoring of  
biotic fouling and macro-fouling programs, to determine if they were adequate to ensure  
proper heat transfer. This was accomplished by determining whether the methods used  
were consistent with accepted industry practices. The inspectors also reviewed the  
licensees inspection and cleaning activities had established acceptance criteria  
consistent with industry standards, and the as-found results were recorded, evaluated,  
and appropriately dispositioned to maintain structural integrity.  
For the RHR Heat Exchanger 2A, DG 3 Jacket Water Cooler and the CS Room Cooler  
1A, the inspectors reviewed the methods and results of heat exchanger performance  
inspections. In addition, the inspectors reviewed the condition and operation of the RHR  
Heat Exchanger 2A, DG 3 Jacket Water Cooler and the CS Room Cooler 1A to  


                                              8
  determine if they were consistent with design assumptions in heat transfer calculations
8  
  and as described in the USFAR. This included determining whether the number of
  plugged tubes was within pre-established limits based on capacity and heat transfer
determine if they were consistent with design assumptions in heat transfer calculations  
  assumptions. The inspectors also determined whether the licensee evaluated the
and as described in the USFAR. This included determining whether the number of  
  potential for water hammer and established adequate controls and operational limits to
plugged tubes was within pre-established limits based on capacity and heat transfer  
  prevent heat exchanger degradation due to excessive flow-induced vibration during
assumptions. The inspectors also determined whether the licensee evaluated the  
  operation.
potential for water hammer and established adequate controls and operational limits to  
  The inspectors determined whether the performance of the ultimate heat sink (UHS)-
prevent heat exchanger degradation due to excessive flow-induced vibration during  
  Cape Fear River and its subcomponents such as piping, intake screens, pumps, valves,
operation.  
  etc. was appropriately evaluated by tests or other equivalent methods to ensure
  availability and accessibility to the in-plant cooling water systems. The inspectors also
The inspectors determined whether the performance of the ultimate heat sink (UHS)-
  reviewed design changes to the service water system and the UHS.
Cape Fear River and its subcomponents such as piping, intake screens, pumps, valves,  
  The inspectors reviewed the licensees operation of the service water system and UHS.
etc. was appropriately evaluated by tests or other equivalent methods to ensure  
  This included a review of licensees procedures for a loss of the service water system or
availability and accessibility to the in-plant cooling water systems. The inspectors also  
  UHS and the verification that instrumentation, which is relied upon for decision-making,
reviewed design changes to the service water system and the UHS.  
  was available and functional. The inspectors also performed a system walk-down on the
  service water system to determine whether the licensees assessment on structural
The inspectors reviewed the licensees operation of the service water system and UHS.
  integrity was adequate and interviewed the respective system engineer. For buried or
This included a review of licensees procedures for a loss of the service water system or  
  inaccessible piping, the inspectors reviewed the licensees pipe testing, inspection, and
UHS and the verification that instrumentation, which is relied upon for decision-making,  
  monitoring program to determine whether structural integrity was ensured and that any
was available and functional. The inspectors also performed a system walk-down on the  
  leakage or degradation was appropriately identified and dispositioned by the licensee.
service water system to determine whether the licensees assessment on structural  
  The inspectors performed a system walk-down of the service water intake structure to
integrity was adequate and interviewed the respective system engineer. For buried or  
  determine whether the licensees assessment on structural integrity and component
inaccessible piping, the inspectors reviewed the licensees pipe testing, inspection, and  
  functionality was adequate. The inspectors also determined whether service water
monitoring program to determine whether structural integrity was ensured and that any  
  pump bay silt accumulation was monitored, trended, and maintained at an acceptable
leakage or degradation was appropriately identified and dispositioned by the licensee.  
  level by the licensee, and that water level instruments were functional and routinely
  monitored. The inspectors also determined whether the licensees ability to ensure
The inspectors performed a system walk-down of the service water intake structure to  
  functionality during adverse weather conditions was adequate.
determine whether the licensees assessment on structural integrity and component  
  The inspectors reviewed condition reports related to the heat exchangers and heat sink
functionality was adequate. The inspectors also determined whether service water  
  performance issues to determine whether the licensee had an appropriate threshold for
pump bay silt accumulation was monitored, trended, and maintained at an acceptable  
  identifying issues and to evaluate the effectiveness of the corrective actions. Records
level by the licensee, and that water level instruments were functional and routinely  
  were also reviewed to verify that the licensee actions were consistent with Generic Letter
monitored. The inspectors also determined whether the licensees ability to ensure  
  (GL) 89-13 licensee commitments, Electric Power Research Institute (EPRI) and other
functionality during adverse weather conditions was adequate.  
  industry guidelines. These inspection activities constituted three heat sink inspection
  samples as defined in IP 71111.07-05.
The inspectors reviewed condition reports related to the heat exchangers and heat sink  
b. Findings
performance issues to determine whether the licensee had an appropriate threshold for  
  No findings were identified.
identifying issues and to evaluate the effectiveness of the corrective actions. Records  
were also reviewed to verify that the licensee actions were consistent with Generic Letter  
(GL) 89-13 licensee commitments, Electric Power Research Institute (EPRI) and other  
industry guidelines. These inspection activities constituted three heat sink inspection  
samples as defined in IP 71111.07-05.  
  b.  
Findings  
No findings were identified.  


                                                  9
1R11 Licensed Operator Requalification Program (71111.11Q - 2 samples)
9  
.1   Quarterly Review of Licensed Operator Requalification Testing and Training
   a. Inspection Scope
1R11 Licensed Operator Requalification Program (71111.11Q - 2 samples)  
      On August 13, 2012, the inspectors observed a crew of licensed operators in the plants
      simulator during licensed operator requalification examinations to verify that operator
.1  
      performance was adequate, evaluators were identifying and documenting crew
Quarterly Review of Licensed Operator Requalification Testing and Training  
      performance problems, and to ensure that training was being conducted in accordance
      with licensee procedures. The inspectors evaluated the following areas:
   a.  
      *   licensed operator performance;
Inspection Scope  
      *   crews clarity and formality of communications;
      *   ability to take timely actions in the conservative direction;
On August 13, 2012, the inspectors observed a crew of licensed operators in the plants  
      *   prioritization, interpretation, and verification of annunciator alarms;
simulator during licensed operator requalification examinations to verify that operator  
      *   correct use and implementation of abnormal and emergency procedures;
performance was adequate, evaluators were identifying and documenting crew  
      *   control board manipulations;
performance problems, and to ensure that training was being conducted in accordance  
      *   oversight and direction from supervisors; and
with licensee procedures. The inspectors evaluated the following areas:  
      *   ability to identify and implement appropriate TS actions and Emergency Plan actions
          and notifications.
*  
      The crews performance in these areas was compared to pre-established operator action
licensed operator performance;  
      expectations and successful critical task completion requirements.
*  
   b. Findings
crews clarity and formality of communications;  
      No findings were identified.
*  
.2   Quarterly Review of Licensed Operator Performance in the Main Control Room
ability to take timely actions in the conservative direction;  
   a. Inspection Scope
*  
      Inspectors observed and assessed licensed operator performance in the plant and main
prioritization, interpretation, and verification of annunciator alarms;  
      control room, particularly during periods of heightened activity or risk and where the
*  
      activities could affect plant safety. Specifically, on September 16th, the inspectors
correct use and implementation of abnormal and emergency procedures;  
      observed the Unit 1 shutdown and cooldown evolutions leading up to the forced outage
*  
      to repair the recirculation pump seals. The inspectors reviewed various licensee policies
control board manipulations;  
      and procedures listed in the Attachment.
*  
      *   Operator compliance and use of procedures.
oversight and direction from supervisors; and  
      *   Control board manipulations.
*  
      *   Communication between crew members.
ability to identify and implement appropriate TS actions and Emergency Plan actions  
      *   Use and interpretation of plant instruments, indications and alarms.
and notifications.  
      *   Use of human error prevention techniques.
      *   Documentation of activities, including initials and sign-offs in procedures.
The crews performance in these areas was compared to pre-established operator action  
      *   Supervision of activities, including risk and reactivity management.
expectations and successful critical task completion requirements.  
      *   Pre-job briefs and crew briefs
   b.  
Findings  
No findings were identified.  
.2  
Quarterly Review of Licensed Operator Performance in the Main Control Room  
   a.  
Inspection Scope  
Inspectors observed and assessed licensed operator performance in the plant and main  
control room, particularly during periods of heightened activity or risk and where the  
activities could affect plant safety. Specifically, on September 16th, the inspectors  
observed the Unit 1 shutdown and cooldown evolutions leading up to the forced outage  
to repair the recirculation pump seals. The inspectors reviewed various licensee policies  
and procedures listed in the Attachment.  
*  
Operator compliance and use of procedures.  
*  
Control board manipulations.  
*  
Communication between crew members.  
*  
Use and interpretation of plant instruments, indications and alarms.  
*  
Use of human error prevention techniques.  
*  
Documentation of activities, including initials and sign-offs in procedures.  
*  
Supervision of activities, including risk and reactivity management.  
*  
Pre-job briefs and crew briefs  


                                              10
    This activity constituted one License Operator Requalification inspection sample and one
10  
    Control Room Observation inspection sample.
  b.  Findings
This activity constituted one License Operator Requalification inspection sample and one  
    No findings were identified.
Control Room Observation inspection sample.  
1R12 Maintenance Effectiveness (71111.12Q - 3 samples)
   
  a. Inspection Scope
  b.  
    The inspectors evaluated degraded performance issues involving the following risk-
Findings
    significant systems:
   
    *   1B Nuclear Service Water Pump smoking with vibration and strainer leakage on
No findings were identified.  
        pump start on June 26, 2012;
    *   2A Standby Liquid Cooling accumulator failure before operability run on September
1R12 Maintenance Effectiveness (71111.12Q - 3 samples)  
        10, 2012 (AR560026); and
   
    *   Performance (unavailability and unreliability) history of the Severe Accident
  a.  
        Mitigation Alternatives (SAMA) diesels
Inspection Scope  
    The inspectors reviewed events where ineffective equipment maintenance may have
    resulted in equipment failure or invalid automatic actuations of Engineered Safeguards
The inspectors evaluated degraded performance issues involving the following risk-
    Systems and independently verified the licensee's actions to address system
significant systems:  
    performance or condition problems in terms of the following:
    *   implementing appropriate work practices;
*  
    *   identifying and addressing common cause failures;
1B Nuclear Service Water Pump smoking with vibration and strainer leakage on  
    *   scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;
pump start on June 26, 2012;  
    *   characterizing system reliability issues for performance;
*  
    *   charging unavailability for performance;
2A Standby Liquid Cooling accumulator failure before operability run on September  
    *   trending key parameters for condition monitoring; and
10, 2012 (AR560026); and  
    *   ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or re-classification; and verifying
*  
        appropriate performance criteria for structures, systems and components
Performance (unavailability and unreliability) history of the Severe Accident  
        (SSCs)/functions classified as (a)(2) or appropriate and adequate goals and
Mitigation Alternatives (SAMA) diesels  
        corrective actions for systems classified as (a)(1).
    The inspectors assessed performance issues with respect to the reliability, availability,
The inspectors reviewed events where ineffective equipment maintenance may have  
    and condition monitoring of the system. In addition, the inspectors verified maintenance
resulted in equipment failure or invalid automatic actuations of Engineered Safeguards  
    effectiveness issues were entered into the corrective action program with the appropriate
Systems and independently verified the licensee's actions to address system  
    significance characterization.
performance or condition problems in terms of the following:  
  b.  Findings
    No findings were identified.
*  
implementing appropriate work practices;  
*  
identifying and addressing common cause failures;  
*  
scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;  
*  
characterizing system reliability issues for performance;  
*  
charging unavailability for performance;  
*  
trending key parameters for condition monitoring; and  
*  
ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or re-classification; and verifying  
appropriate performance criteria for structures, systems and components  
(SSCs)/functions classified as (a)(2) or appropriate and adequate goals and  
corrective actions for systems classified as (a)(1).  
The inspectors assessed performance issues with respect to the reliability, availability,  
and condition monitoring of the system. In addition, the inspectors verified maintenance  
effectiveness issues were entered into the corrective action program with the appropriate  
significance characterization.  
   
  b.  
Findings
   
No findings were identified.  


                                                11
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13 - 4 samples)
11  
  a. Inspection Scope
    The inspectors reviewed the licensee's evaluation and management of plant risk for the
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13 - 4 samples)  
    maintenance and emergent work activities affecting risk-significant equipment listed
   
    below to verify that the appropriate risk assessments were performed prior to removing
  a.  
    equipment for work:
Inspection Scope  
    *   Unit 2 yellow risk during emergent work on 2-E21-F015A, 2A Core Spray Full Flow
        Test Bypass Valve, and scheduled maintenance on 2B RHR/residual heat removal
The inspectors reviewed the licensee's evaluation and management of plant risk for the  
        service water (RHRSW) on July 11, 2012;
maintenance and emergent work activities affecting risk-significant equipment listed  
    *   Unit 1 yellow risk during 1B Recirculation Pump Variable Frequency Drive power
below to verify that the appropriate risk assessments were performed prior to removing  
        recovery, and planned maintenance on 1A RHR/RHRSW on July 26, 2012;
equipment for work:  
    *   Unit 1 yellow risk during planned maintenance on 1B RHR/RHRSW September 4 to
        September 6, 2012;
*  
    *   Unit 1 integrated risk during repair of 1B recirculation pump seal September 17 to
Unit 2 yellow risk during emergent work on 2-E21-F015A, 2A Core Spray Full Flow  
        September 25, 2012;
Test Bypass Valve, and scheduled maintenance on 2B RHR/residual heat removal  
    These activities were selected based on their potential risk-significance relative to the
service water (RHRSW) on July 11, 2012;  
    reactor safety cornerstones. As applicable for each activity, the inspectors verified that
*  
    risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate
Unit 1 yellow risk during 1B Recirculation Pump Variable Frequency Drive power  
    and complete. When emergent work was performed, the inspectors verified that the
recovery, and planned maintenance on 1A RHR/RHRSW on July 26, 2012;  
    plant risk was promptly reassessed and managed. The inspectors reviewed the scope
*  
    of maintenance work, discussed the results of the assessment with the licensee's
Unit 1 yellow risk during planned maintenance on 1B RHR/RHRSW September 4 to  
    probabilistic risk analyst or shift technical advisor, and verified plant conditions were
September 6, 2012;  
    consistent with the risk assessment. The inspectors also reviewed TS requirements and
*  
    walked down portions of redundant safety systems, when applicable, to verify risk
Unit 1 integrated risk during repair of 1B recirculation pump seal September 17 to  
    analysis assumptions were valid and applicable requirements were met.
September 25, 2012;  
  b.  Findings
    No findings were identified.
These activities were selected based on their potential risk-significance relative to the  
1R15 Operability Evaluations (71111.15 - 5 samples)
reactor safety cornerstones. As applicable for each activity, the inspectors verified that  
  a. Inspection Scope
risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate  
    The inspectors reviewed the following five issues:
and complete. When emergent work was performed, the inspectors verified that the  
    *   Unit 2 High Pressure Coolant Injection (HPCI) elevated thrust bearing temperature
plant risk was promptly reassessed and managed. The inspectors reviewed the scope  
        on July 6, 2012 (AR548370);
of maintenance work, discussed the results of the assessment with the licensee's  
    *   2D RHRSW Booster pump coupling grease specification evaluation on July 12, 2012
probabilistic risk analyst or shift technical advisor, and verified plant conditions were  
        (AR542025);
consistent with the risk assessment. The inspectors also reviewed TS requirements and  
    *   Emergency Diesel Generator (EDG) #3 debris in bearing oil site glass on July 15,
walked down portions of redundant safety systems, when applicable, to verify risk  
        2012 (AR549420);
analysis assumptions were valid and applicable requirements were met.  
    *   Reactor Building Close Cooling Water (RBCCW) piping corrosion in rattle space on
   
        August 21, 2012 (AR557151); and
  b.  
Findings
   
No findings were identified.  
1R15 Operability Evaluations (71111.15 - 5 samples)  
   
  a.  
Inspection Scope  
The inspectors reviewed the following five issues:  
*  
Unit 2 High Pressure Coolant Injection (HPCI) elevated thrust bearing temperature  
on July 6, 2012 (AR548370);  
*  
2D RHRSW Booster pump coupling grease specification evaluation on July 12, 2012  
(AR542025);  
*  
Emergency Diesel Generator (EDG) #3 debris in bearing oil site glass on July 15,  
2012 (AR549420);  
*  
Reactor Building Close Cooling Water (RBCCW) piping corrosion in rattle space on  
August 21, 2012 (AR557151); and  


                                              12
    *   EDG #4 alternate safe shutdown switch contact continuity indications on August 27,
12  
        2012 (AR558810)
    The inspectors selected these potential operability issues based on the risk-significance
*  
    of the associated components and systems. The inspectors evaluated the technical
EDG #4 alternate safe shutdown switch contact continuity indications on August 27,  
    adequacy of the evaluations to ensure that TS operability was properly justified and the
2012 (AR558810)  
    subject component or system remained available such that no unrecognized increase in
    risk occurred. The inspectors compared the operability and design criteria in the
The inspectors selected these potential operability issues based on the risk-significance  
    appropriate sections of the UFSAR and TS to the licensees evaluations, to determine
of the associated components and systems. The inspectors evaluated the technical  
    whether the components or systems were operable. Where compensatory measures
adequacy of the evaluations to ensure that TS operability was properly justified and the  
    were required to maintain operability, the inspectors determined whether the measures
subject component or system remained available such that no unrecognized increase in  
    in place would function as intended and were properly controlled. The inspectors
risk occurred. The inspectors compared the operability and design criteria in the  
    determined, where appropriate, compliance with bounding limitations associated with the
appropriate sections of the UFSAR and TS to the licensees evaluations, to determine  
    evaluations. Additionally, the inspectors also reviewed a sampling of corrective action
whether the components or systems were operable. Where compensatory measures  
    documents to verify that the licensee was identifying and correcting any deficiencies
were required to maintain operability, the inspectors determined whether the measures  
    associated with operability evaluations.
in place would function as intended and were properly controlled. The inspectors  
  b.  Findings
determined, where appropriate, compliance with bounding limitations associated with the  
    No findings were identified.
evaluations. Additionally, the inspectors also reviewed a sampling of corrective action  
1R18 Plant Modifications (71111.18 - 2 samples)
documents to verify that the licensee was identifying and correcting any deficiencies  
  a. Inspection Scope
associated with operability evaluations.  
    The inspectors reviewed the two modifications listed below to determine whether the
   
    modifications affected the safety functions of systems that are important to safety. The
  b.  
    inspectors reviewed 10 CFR 50.59 documentation and post-modification testing results
Findings
    and conducted field walk-downs of the modifications to verify that the modifications did
   
    not degrade the design bases, licensing bases, and performance capability of the
No findings were identified.  
    affected systems.
    *   Design leak tight barriers at reactor building rattle spaces (EC86304);
1R18 Plant Modifications (71111.18 - 2 samples)  
    *   Service water building drain hub baffle plate installation (EC 88431)
   
  b.  Findings
  a.  
    No findings were identified.
Inspection Scope  
1R19 Post Maintenance Testing (71111.19 - 7 samples)
  a. Inspection Scope
The inspectors reviewed the two modifications listed below to determine whether the  
    The inspectors reviewed the following seven post-maintenance activities to verify that
modifications affected the safety functions of systems that are important to safety. The  
    procedures and test activities were adequate to ensure system operability and functional
inspectors reviewed 10 CFR 50.59 documentation and post-modification testing results  
    capability:
and conducted field walk-downs of the modifications to verify that the modifications did  
    *   0PT-12.2D, No. 4 Diesel Generator Monthly Load Test after replacement of the 60X
not degrade the design bases, licensing bases, and performance capability of the  
        relay on July 23, 2012;
affected systems.  
*  
Design leak tight barriers at reactor building rattle spaces (EC86304);  
*  
Service water building drain hub baffle plate installation (EC 88431)  
   
  b.  
Findings
   
No findings were identified.  
1R19 Post Maintenance Testing (71111.19 - 7 samples)
   
  a.  
Inspection Scope  
The inspectors reviewed the following seven post-maintenance activities to verify that  
procedures and test activities were adequate to ensure system operability and functional  
capability:  
*  
0PT-12.2D, No. 4 Diesel Generator Monthly Load Test after replacement of the 60X  
relay on July 23, 2012;  


                                              13
    *   0PT-08.1.4B, Residual Heat Removal (RHR) Service Water (SW) System Operability
13  
          Test - Unit 2 RHRSW Loop B after the maintenance outage on July 12, 2012;
    *   0PT-08.2.2c, Low Pressure Coolant Injection/RHR System Operability Test - Unit 1
*  
          RHR Loop A after the maintenance outage on July 27, 2012;
0PT-08.1.4B, Residual Heat Removal (RHR) Service Water (SW) System Operability  
    *   0PT-12.2C, EDG #3 Operability Test - Unit 2 after repair of jacket water pump on
Test - Unit 2 RHRSW Loop B after the maintenance outage on July 12, 2012;
          August 16, 2012;
*  
    *   0PT-15.6, Standby Gas Treatment Operability Test, Unit 1 B after relay replacement
0PT-08.2.2c, Low Pressure Coolant Injection/RHR System Operability Test - Unit 1  
          on August 15, 2012;
RHR Loop A after the maintenance outage on July 27, 2012;  
    *   0PT-10.1.1, Reactor Core Isolation Cooling System Operability Test, Unit 2 after
*  
          replacement of Electronic Governor - Magnetic (EGM) on August 23, 2012; and
0PT-12.2C, EDG #3 Operability Test - Unit 2 after repair of jacket water pump on  
    *   0PT-80.5, Reactor Pressure Vessel Pressure Test - Unit 1 after repair of 1B
August 16, 2012;  
          recirculation pump seal on September 26, 2012
*  
    These activities were selected based upon the structure, system, or component's ability
0PT-15.6, Standby Gas Treatment Operability Test, Unit 1 B after relay replacement  
    to impact risk. The inspectors evaluated these activities for the following, as applicable:
on August 15, 2012;  
    the effect of testing on the plant had been adequately addressed; testing was adequate
*  
    for the maintenance performed; acceptance criteria were clear and demonstrated
0PT-10.1.1, Reactor Core Isolation Cooling System Operability Test, Unit 2 after  
    operational readiness; test instrumentation was appropriate; tests were performed as
replacement of Electronic Governor - Magnetic (EGM) on August 23, 2012; and  
    written in accordance with properly reviewed and approved procedures; equipment was
*  
    returned to its operational status following testing, and test documentation was properly
0PT-80.5, Reactor Pressure Vessel Pressure Test - Unit 1 after repair of 1B  
    evaluated. The inspectors evaluated the activities against the UFSAR and TS to ensure
recirculation pump seal on September 26, 2012  
    that the test results adequately ensured that the equipment met the licensing basis and
    design requirements. In addition, the inspectors reviewed corrective action documents
These activities were selected based upon the structure, system, or component's ability  
    associated with post-maintenance tests to determine whether the licensee was
to impact risk. The inspectors evaluated these activities for the following, as applicable:  
    identifying problems and entering them in the CAP and that the problems were being
the effect of testing on the plant had been adequately addressed; testing was adequate  
    corrected commensurate with their importance to safety.
for the maintenance performed; acceptance criteria were clear and demonstrated  
  b.  Findings
operational readiness; test instrumentation was appropriate; tests were performed as  
    No findings were identified.
written in accordance with properly reviewed and approved procedures; equipment was  
1R20 Refueling and Other Outage Activities (71111.20 - 1 sample)
returned to its operational status following testing, and test documentation was properly  
    Other Outage Activities
evaluated. The inspectors evaluated the activities against the UFSAR and TS to ensure  
  a. Inspection Scope
that the test results adequately ensured that the equipment met the licensing basis and  
    The inspectors evaluated licensee outage activities for an unscheduled forced outage to
design requirements. In addition, the inspectors reviewed corrective action documents  
    replace the 1B recirculation pump seal assembly. During the outage, the licensee made
associated with post-maintenance tests to determine whether the licensee was  
    the decision to replace the 1A recirculation pump seal assembly to address the potential
identifying problems and entering them in the CAP and that the problems were being  
    extent of cause/condition. The outage began on September 16, 2012 and concluded on
corrected commensurate with their importance to safety.  
    September 28, 2012. The inspectors reviewed activities to ensure that the licensee
   
    considered risk in developing, planning, and implementing the outage schedule.
  b.  
    Additionally, the inspectors observed or reviewed the reactor shutdown and cool down,
Findings
    outage equipment configuration and risk management, electrical lineups, control and
   
    monitoring of decay heat removal, control of containment activities, performed a drywell
No findings were identified.  
    close out inspection, observed reactor startup and heat up activities, and identification
    and resolution of problems associated with the outage. Documents reviewed are listed
1R20 Refueling and Other Outage Activities (71111.20 - 1 sample)  
    in the Attachment.
Other Outage Activities  
  a.  
Inspection Scope  
The inspectors evaluated licensee outage activities for an unscheduled forced outage to  
replace the 1B recirculation pump seal assembly. During the outage, the licensee made  
the decision to replace the 1A recirculation pump seal assembly to address the potential  
extent of cause/condition. The outage began on September 16, 2012 and concluded on  
September 28, 2012. The inspectors reviewed activities to ensure that the licensee  
considered risk in developing, planning, and implementing the outage schedule.
Additionally, the inspectors observed or reviewed the reactor shutdown and cool down,  
outage equipment configuration and risk management, electrical lineups, control and  
monitoring of decay heat removal, control of containment activities, performed a drywell  
close out inspection, observed reactor startup and heat up activities, and identification  
and resolution of problems associated with the outage. Documents reviewed are listed  
in the Attachment.  


                                            14
b. Findings
14  
  Introduction: The inspectors identified a Green NCV of TS 3.6.4.1, Secondary
  Containment because the licensee did not maintain secondary containment operable as
  b.  
  required during an activity considered an operation with a potential for draining the
Findings  
  reactor vessel (OPDRV).
  Description: On September 19, 2012, the licensee was replacing the 1B recirculation
Introduction: The inspectors identified a Green NCV of TS 3.6.4.1, Secondary  
  pump seal assembly while Unit 1 was in Mode 4 (cold shutdown). In an effort to properly
Containment because the licensee did not maintain secondary containment operable as  
  isolate the work area, the recirculation suction and discharge isolation valves were
required during an activity considered an operation with a potential for draining the  
  tagged closed. Due to seat leakage across the isolation valves, the 1B recirculation
reactor vessel (OPDRV).  
  pump drain valve was uncapped and opened to maintain the pump body partially empty
Description: On September 19, 2012, the licensee was replacing the 1B recirculation  
  to prevent water from impacting the work area while the pump seal was removed. The
pump seal assembly while Unit 1 was in Mode 4 (cold shutdown). In an effort to properly  
  pump drain leakage was sent to the drywell floor drain system. The 1B recirculation
isolate the work area, the recirculation suction and discharge isolation valves were  
  pump seal replacement activity had the potential to drain the reactor vessel below the
tagged closed. Due to seat leakage across the isolation valves, the 1B recirculation  
  top of the fuel because the recirculation loops penetrate the reactor vessel below the top
pump drain valve was uncapped and opened to maintain the pump body partially empty  
  of active fuel. An OPDRV is described in the licensees technical specifications as an
to prevent water from impacting the work area while the pump seal was removed. The  
  operation with a potential for draining the reactor vessel. However, the licensee did not
pump drain leakage was sent to the drywell floor drain system. The 1B recirculation  
  recognize or consider this activity as an OPDRV due to inadequate procedural guidance
pump seal replacement activity had the potential to drain the reactor vessel below the  
  that was used to exclude this activity as an OPDRV. Specifically, the licensee adopted
top of the fuel because the recirculation loops penetrate the reactor vessel below the top  
  the definition of an OPDRV in procedure 0OI-01.01 as provided in Enforcement
of active fuel. An OPDRV is described in the licensees technical specifications as an  
  Guidance Memorandum (EGM) 11-003 as any activity that could potentially result in
operation with a potential for draining the reactor vessel. However, the licensee did not  
  draining or siphoning the RPV water level below the top of the fuel, without taking credit
recognize or consider this activity as an OPDRV due to inadequate procedural guidance  
  for mitigating measures. However, section 9.16.15.b.(2) of licensee procedure 0OI-
that was used to exclude this activity as an OPDRV. Specifically, the licensee adopted  
  01.01, BNP Conduct of Operations Supplement, stated leakage through mechanical
the definition of an OPDRV in procedure 0OI-01.01 as provided in Enforcement  
  joints (for example valve or flange packing leaks, seat leakage through an isolation
Guidance Memorandum (EGM) 11-003 as any activity that could potentially result in  
  valve, flange leakage, etc) is not considered an OPDRV. On September 19, 2012, the
draining or siphoning the RPV water level below the top of the fuel, without taking credit  
  licensee relaxed Unit 1 secondary containment from 03:30 a.m. until 09:20 p.m. by
for mitigating measures. However, section 9.16.15.b.(2) of licensee procedure 0OI-
  opening the reactor building air lock doors on the 20-foot elevation to increase ventilation
01.01, BNP Conduct of Operations Supplement, stated leakage through mechanical  
  to the recirculation pump seal replacement work area in the Unit 1 drywell. This resulted
joints (for example valve or flange packing leaks, seat leakage through an isolation  
  in Secondary Containment inoperability while Unit 1 was in Mode 4 during an OPRDV
valve, flange leakage, etc) is not considered an OPDRV. On September 19, 2012, the  
  activity. The inspectors questioned the licensees Operations staff on the decision to
licensee relaxed Unit 1 secondary containment from 03:30 a.m. until 09:20 p.m. by  
  make secondary containment inoperable during an OPDRV activity. Following this, the
opening the reactor building air lock doors on the 20-foot elevation to increase ventilation  
  licensee restored secondary containment, developed an Operation standing instruction
to the recirculation pump seal replacement work area in the Unit 1 drywell. This resulted  
  12-052 to treat this activity as an OPDRV and placed this issue into its CAP as AR
in Secondary Containment inoperability while Unit 1 was in Mode 4 during an OPRDV  
  562188.
activity. The inspectors questioned the licensees Operations staff on the decision to  
  Analysis: The inspectors determined that the failure to maintain secondary containment
make secondary containment inoperable during an OPDRV activity. Following this, the  
  operable while Unit 1 was in Mode 4 with an OPDRV in progress was a performance
licensee restored secondary containment, developed an Operation standing instruction  
  deficiency. The performance deficiency was more than minor because it was associated
12-052 to treat this activity as an OPDRV and placed this issue into its CAP as AR  
  with the configuration control attribute of the Barrier Integrity Cornerstone, and adversely
562188.  
  affected the cornerstone objective to provide reasonable assurance that physical design
Analysis: The inspectors determined that the failure to maintain secondary containment  
  barriers (fuel cladding, reactor coolant system, and containment) protect the public from
operable while Unit 1 was in Mode 4 with an OPDRV in progress was a performance  
  radionuclide releases caused by accidents or events because the Unit 1 secondary
deficiency. The performance deficiency was more than minor because it was associated  
  containment boundary was not preserved or maintained. The inspectors evaluated the
with the configuration control attribute of the Barrier Integrity Cornerstone, and adversely  
  finding using Inspection Manual Chapter (IMC) 0609, Attachment 4, Phase 1 - Initial
affected the cornerstone objective to provide reasonable assurance that physical design  
  Screening and Characterization of Findings, which required an analysis using IMC 0609
barriers (fuel cladding, reactor coolant system, and containment) protect the public from  
  Appendix G since the reactor was in Mode 4 (cold shutdown). The finding was
radionuclide releases caused by accidents or events because the Unit 1 secondary  
  determined to be of very low safety significance (Green) according to IMC 0609
containment boundary was not preserved or maintained. The inspectors evaluated the  
finding using Inspection Manual Chapter (IMC) 0609, Attachment 4, Phase 1 - Initial  
Screening and Characterization of Findings, which required an analysis using IMC 0609  
Appendix G since the reactor was in Mode 4 (cold shutdown). The finding was  
determined to be of very low safety significance (Green) according to IMC 0609  


                                                15
      Appendix G, Attachment 1, Checklist 6, since a quantitative assessment (Phase 2 or
15  
      Phase 3 evaluation) was not required. Specifically, the inspectors determined that the
      licensee maintained adequate mitigation capability for reactor vessel water level
Appendix G, Attachment 1, Checklist 6, since a quantitative assessment (Phase 2 or  
      inventory and an event did not occur that could be characterized as a loss of control.
Phase 3 evaluation) was not required. Specifically, the inspectors determined that the  
      The cause of this finding was directly related to the cross-cutting aspect of Accurate
licensee maintained adequate mitigation capability for reactor vessel water level  
      Procedures in the Resources component of the Human Performance area, because the
inventory and an event did not occur that could be characterized as a loss of control.
      licensee did not consider the recirculation pump seal replacement activity to be OPDRV
The cause of this finding was directly related to the cross-cutting aspect of Accurate  
      based on procedural guidance that contains exclusions to what are considered OPDRV
Procedures in the Resources component of the Human Performance area, because the  
      activities. [H.2(c)]
licensee did not consider the recirculation pump seal replacement activity to be OPDRV  
      Enforcement: Unit 1 TS 3.6.4.1, Secondary Containment, required secondary
based on procedural guidance that contains exclusions to what are considered OPDRV  
      containment to be operable during modes one, two, three, during movement of recently
activities. [H.2(c)]  
      irradiated fuel assemblies in the secondary containment and during operations with a
      potential for draining the reactor vessel (OPDRVs). Contrary to the above, on
Enforcement: Unit 1 TS 3.6.4.1, Secondary Containment, required secondary  
      September 19, 2012, Unit 1 secondary containment was not maintained operable during
containment to be operable during modes one, two, three, during movement of recently  
      an OPDRV activity. The licensee entered this issue in its CAP as AR 562188, and
irradiated fuel assemblies in the secondary containment and during operations with a  
      restored secondary containment during the OPDRV activity. Because the licensee
potential for draining the reactor vessel (OPDRVs). Contrary to the above, on  
      entered the issue into its CAP and the finding is of very low safety significance (Green),
September 19, 2012, Unit 1 secondary containment was not maintained operable during  
      this violation is being treated as an NCV, consistent with Section 2.3.2 of the NRCs
an OPDRV activity. The licensee entered this issue in its CAP as AR 562188, and  
      Enforcement Policy: NCV 05000325/2012004-01, Failure to Maintain Secondary
restored secondary containment during the OPDRV activity. Because the licensee  
      Containment Operable during an OPDRV activity.
entered the issue into its CAP and the finding is of very low safety significance (Green),  
1R22 Surveillance Testing
this violation is being treated as an NCV, consistent with Section 2.3.2 of the NRCs  
.1   Routine Surveillance Testing (71111.22 - 4 samples)
Enforcement Policy: NCV 05000325/2012004-01, Failure to Maintain Secondary  
   a. Inspection Scope
Containment Operable during an OPDRV activity.  
      The inspectors either observed surveillance tests or reviewed the test results for the
1R22 Surveillance Testing
      following activities to verify the tests met TS surveillance requirements, UFSAR
      commitments, in-service testing requirements, and licensee procedural requirements.
.1  
      The inspectors assessed the effectiveness of the tests in demonstrating that the SSCs
Routine Surveillance Testing (71111.22 - 4 samples)  
      were operationally capable of performing their intended safety functions.
      *   0PT-07.2.4A, Core Spray System Operability Test - Loop A on July 5, 2012;
   a.  
      *   0MST-RHR21Q, RHR-LPCI, CSS and HPCI Hi Drywell Pressure Trip Unit Inst Chan
Inspection Scope  
          Cal on July 10, 2012;
      *   0MST-RCIC42R, RCIC Auto-actuation and Isolation Logic Sys Functional on July 24,
The inspectors either observed surveillance tests or reviewed the test results for the  
          2012; and
following activities to verify the tests met TS surveillance requirements, UFSAR  
      *   0PT-12.12D, No. 4 Diesel Generator Monthly Load Test on August 17, 2012;
commitments, in-service testing requirements, and licensee procedural requirements.
   b. Findings
The inspectors assessed the effectiveness of the tests in demonstrating that the SSCs  
      No findings were identified.
were operationally capable of performing their intended safety functions.  
*  
0PT-07.2.4A, Core Spray System Operability Test - Loop A on July 5, 2012;  
*  
0MST-RHR21Q, RHR-LPCI, CSS and HPCI Hi Drywell Pressure Trip Unit Inst Chan  
Cal on July 10, 2012;  
*  
0MST-RCIC42R, RCIC Auto-actuation and Isolation Logic Sys Functional on July 24,  
2012; and  
*  
0PT-12.12D, No. 4 Diesel Generator Monthly Load Test on August 17, 2012;  
 
   b.  
Findings  
No findings were identified.  


                                                16
.2   In-Service Testing (IST) Surveillance (71111.22 - 1 sample)
16  
   a. Inspection Scope
      The inspectors reviewed the performance of Unit 1 LPCI/RHR System Operability Test -
.2  
      Loop B on August 9, 2012 to evaluate the effectiveness of the licensees American
In-Service Testing (IST) Surveillance (71111.22 - 1 sample)  
      Society of Mechanical Engineers (ASME) Section XI testing program for determining
      equipment availability and reliability. The inspectors evaluated selected portions of the
   a.  
      following areas: 1) testing procedures, 2) acceptance criteria, 3) testing methods, 4)
Inspection Scope  
      compliance with the licensees IST program, TS, selected licensee commitments, and
      code requirements, 5) range and accuracy of test instruments, and 6) required corrective
The inspectors reviewed the performance of Unit 1 LPCI/RHR System Operability Test -  
      actions.
Loop B on August 9, 2012 to evaluate the effectiveness of the licensees American  
   b. Findings
Society of Mechanical Engineers (ASME) Section XI testing program for determining  
      No findings were identified.
equipment availability and reliability. The inspectors evaluated selected portions of the  
.3   Reactor Coolant System Leak Detection Inspection Surveillance (71111.22 - 1 sample)
following areas: 1) testing procedures, 2) acceptance criteria, 3) testing methods, 4)  
   a. Inspection Scope
compliance with the licensees IST program, TS, selected licensee commitments, and  
      The inspectors observed and reviewed the test results for a reactor coolant system leak
code requirements, 5) range and accuracy of test instruments, and 6) required corrective  
      detection surveillance, 0PT-80.5, Mid-Cycle Maintenance Outage Reactor Pressure
actions.  
      Vessel Pressure Test, on September 28, 2012. The inspectors observed in-plant
      activities and reviewed procedures and associated records to determine whether:
   b.  
      effects of the testing were adequately addressed by control room personnel or engineers
Findings  
      prior to the commencement of the testing; acceptance criteria were clearly stated,
      demonstrated operational readiness, and were consistent with the system design basis;
No findings were identified.  
      plant equipment calibration was correct, accurate, and properly documented; and the
      calibration frequency was in accordance with TSs, the UFSAR, procedures, and
.3  
      applicable commitments; applicable prerequisites described in the test procedures were
Reactor Coolant System Leak Detection Inspection Surveillance (71111.22 - 1 sample)  
      satisfied; test frequencies met TS requirements to demonstrate operability and reliability;
      tests were performed in accordance with the test procedures and other applicable
   a.  
      procedures; and test data and results were accurate, complete, within limits, and valid.
Inspection Scope  
      Inspectors verified that test results not meeting acceptance criteria were addressed with
      an adequate operability evaluation or the system or component was declared
The inspectors observed and reviewed the test results for a reactor coolant system leak  
      inoperable; equipment was returned to a position or status required to support the
detection surveillance, 0PT-80.5, Mid-Cycle Maintenance Outage Reactor Pressure  
      performance of its safety functions; and all problems identified during the testing were
Vessel Pressure Test, on September 28, 2012. The inspectors observed in-plant  
      appropriately documented and dispositioned in the corrective action program.
activities and reviewed procedures and associated records to determine whether:
   b. Findings
effects of the testing were adequately addressed by control room personnel or engineers  
      No findings were identified.
prior to the commencement of the testing; acceptance criteria were clearly stated,  
demonstrated operational readiness, and were consistent with the system design basis;  
plant equipment calibration was correct, accurate, and properly documented; and the  
calibration frequency was in accordance with TSs, the UFSAR, procedures, and  
applicable commitments; applicable prerequisites described in the test procedures were  
satisfied; test frequencies met TS requirements to demonstrate operability and reliability;  
tests were performed in accordance with the test procedures and other applicable  
procedures; and test data and results were accurate, complete, within limits, and valid.
Inspectors verified that test results not meeting acceptance criteria were addressed with  
an adequate operability evaluation or the system or component was declared  
inoperable; equipment was returned to a position or status required to support the  
performance of its safety functions; and all problems identified during the testing were  
appropriately documented and dispositioned in the corrective action program.  
   b.  
Findings  
No findings were identified.  


                                                17
1EP6 Emergency Planning Drill Evaluation (71114.06 - 2 samples)
17  
   a. Inspection Scope
      The inspectors observed site emergency preparedness training drill/simulator scenarios
1EP6 Emergency Planning Drill Evaluation (71114.06 - 2 samples)  
      conducted on July 9, 2012 and July 25, 2012. The inspectors reviewed the drill scenario
      narrative to identify the timing and location of classifications, notifications, and protective
   a.  
      action recommendations development activities. During the drill, the inspectors
Inspection Scope  
      assessed the adequacy of event classification and notification activities. The inspectors
      observed portions of the licensees post-drill. The inspectors verified that the licensee
The inspectors observed site emergency preparedness training drill/simulator scenarios  
      properly evaluated the drills performance with respect to performance indicators and
conducted on July 9, 2012 and July 25, 2012. The inspectors reviewed the drill scenario  
      assessed drill performance with respect to drill objectives.
narrative to identify the timing and location of classifications, notifications, and protective  
   b. Findings
action recommendations development activities. During the drill, the inspectors  
      No findings were identified.
assessed the adequacy of event classification and notification activities. The inspectors  
4.   OTHER ACTIVITIES
observed portions of the licensees post-drill. The inspectors verified that the licensee  
4OA1 Performance Indicator (PI) Verification (71151 - 6 samples)
properly evaluated the drills performance with respect to performance indicators and  
.1   Mitigating Systems Cornerstone
assessed drill performance with respect to drill objectives.  
   a. Inspection Scope
      *   Mitigating Systems Performance Index, Residual Heat Removal - Unit 1
   b.  
      *   Mitigating Systems Performance Index, Residual Heat Removal - Unit 2
Findings  
      The inspectors sampled licensee submittals for the Mitigating Systems Performance
      Index (MSPI) performance indicators listed above for the period from the third (3rd)
No findings were identified.  
      quarter 2011 through the second (2nd) quarter 2012. The inspectors reviewed the
      licensees operator narrative logs, issue reports, MSPI derivation reports, event reports
4.  
      and NRC Integrated Inspection reports for the period to validate the accuracy of the
OTHER ACTIVITIES  
      submittals.
   b.  Findings
4OA1 Performance Indicator (PI) Verification (71151 - 6 samples)  
      No findings were identified.
.2   Barrier Integrity Cornerstone
.1  
   a. Inspection Scope
Mitigating Systems Cornerstone  
      *   Reactor Coolant System (RCS) Specific Activity - Unit 1
      *   Reactor Coolant System (RCS) Specific Activity - Unit 2
   a.  
      The inspectors reviewed licensee submittals for the Reactor Coolant System Specific
Inspection Scope  
      Activity performance indicator for the period from the third (3rd) quarter 2011 through the
      second (2nd) quarter 2012. The inspectors reviewed the licensees RCS chemistry
*  
Mitigating Systems Performance Index, Residual Heat Removal - Unit 1  
*  
Mitigating Systems Performance Index, Residual Heat Removal - Unit 2  
The inspectors sampled licensee submittals for the Mitigating Systems Performance  
Index (MSPI) performance indicators listed above for the period from the third (3rd)  
quarter 2011 through the second (2nd) quarter 2012. The inspectors reviewed the  
licensees operator narrative logs, issue reports, MSPI derivation reports, event reports  
and NRC Integrated Inspection reports for the period to validate the accuracy of the  
submittals.  
   b.  
  Findings  
No findings were identified.  
.2  
Barrier Integrity Cornerstone  
   a.  
Inspection Scope  
*  
Reactor Coolant System (RCS) Specific Activity - Unit 1  
*  
Reactor Coolant System (RCS) Specific Activity - Unit 2  
The inspectors reviewed licensee submittals for the Reactor Coolant System Specific  
Activity performance indicator for the period from the third (3rd) quarter 2011 through the  
second (2nd) quarter 2012. The inspectors reviewed the licensees RCS chemistry  


                                                  18
      samples, TS requirements, issue reports, and event reports for the period to validate the
18  
      accuracy of the submittals. In addition to record reviews, the inspectors observed a
      chemistry technician obtain and analyze a reactor coolant system sample.
samples, TS requirements, issue reports, and event reports for the period to validate the  
      *   Reactor Coolant System Leakage - Unit 1
accuracy of the submittals. In addition to record reviews, the inspectors observed a  
      *   Reactor Coolant System Leakage - Unit 2
chemistry technician obtain and analyze a reactor coolant system sample.  
      The inspectors sampled licensee submittals for the Reactor Coolant System Leakage
      performance indicator for the period from the third (3rd) quarter 2011 through the second
*  
      (2nd) quarter 2012. The inspectors reviewed the licensees operator logs, RCS leakage
Reactor Coolant System Leakage - Unit 1  
      tracking data, issue reports, and event reports for the period to validate the accuracy of
*  
      the submittals.
Reactor Coolant System Leakage - Unit 2  
   b. Findings
      No findings were identified.
The inspectors sampled licensee submittals for the Reactor Coolant System Leakage  
4OA2 Identification and Resolution of Problems (71152 - 2 samples)
performance indicator for the period from the third (3rd) quarter 2011 through the second  
.1   Routine Review of Items Entered Into the Corrective Action Program
(2nd) quarter 2012. The inspectors reviewed the licensees operator logs, RCS leakage  
   a. Inspection Scope
tracking data, issue reports, and event reports for the period to validate the accuracy of  
      To aid in the identification of repetitive equipment failures or specific human performance
the submittals.  
      issues for follow-up, the inspectors performed frequent screenings of items entered into
      the licensees corrective action program. The review was accomplished by reviewing
   b.  
      daily action request reports.
Findings  
   b. Findings
      No findings were identified.
No findings were identified.  
.2   Assessments and Observations
      Selected Issue Follow-up Inspection: UPS-A Failure and Loss of Emergency Response
4OA2 Identification and Resolution of Problems (71152 - 2 samples)  
      Facility Information System (ERFIS), Plant Process Computer (PPC), Business Network
   a. Inspection Scope
.1  
      The inspectors selected AR 542704, UPS-A Failure and Loss of ERFIS, PPC, Business
Routine Review of Items Entered Into the Corrective Action Program  
      Network, for detailed review. This AR identified that a single failure caused the loss of
      ERFIS and Safety Parameter Display System (SPDS) on both units. The inspectors
   a.  
      reviewed the licensees CAP for ERFIS and SPDS failures in the past. The inspectors
Inspection Scope  
      reviewed these reports to verify that the licensee identified the full extent of the issue,
      performed an appropriate evaluation, and specified and prioritized appropriate corrective
To aid in the identification of repetitive equipment failures or specific human performance  
      actions. The inspectors evaluated the reports against the requirements of the licensees
issues for follow-up, the inspectors performed frequent screenings of items entered into  
      CAP as delineated in corporate procedure CAP-NGGC-0200, Corrective Action
the licensees corrective action program. The review was accomplished by reviewing  
      Program, 10 CFR 50.47, and 10 CFR 50 Appendix E.
daily action request reports.  
   b.  
Findings  
No findings were identified.  
.2  
Assessments and Observations  
Selected Issue Follow-up Inspection: UPS-A Failure and Loss of Emergency Response  
Facility Information System (ERFIS), Plant Process Computer (PPC), Business Network  
   a.  
Inspection Scope  
The inspectors selected AR 542704, UPS-A Failure and Loss of ERFIS, PPC, Business  
Network, for detailed review. This AR identified that a single failure caused the loss of  
ERFIS and Safety Parameter Display System (SPDS) on both units. The inspectors  
reviewed the licensees CAP for ERFIS and SPDS failures in the past. The inspectors  
reviewed these reports to verify that the licensee identified the full extent of the issue,  
performed an appropriate evaluation, and specified and prioritized appropriate corrective  
actions. The inspectors evaluated the reports against the requirements of the licensees  
CAP as delineated in corporate procedure CAP-NGGC-0200, Corrective Action  
Program, 10 CFR 50.47, and 10 CFR 50 Appendix E.  


                                            19
b. Findings
19  
  No findings were identified
a. Inspection Scope
  b.  
  The inspectors selected AR 542704, UPS-A Failure and Loss of ERFIS, PPC, Business
Findings  
  Network, for detailed review. This AR identified that a single failure caused the loss of
  ERFIS and Safety Parameter Display System (SPDS) on both units. The inspectors
No findings were identified  
  reviewed the licensees CAP for ERFIS and SPDS failures in the past. The inspectors
  reviewed these reports to verify that the licensee identified the full extent of the issue,
  a.  
  performed an appropriate evaluation, and specified and prioritized appropriate corrective
Inspection Scope  
  actions. The inspectors evaluated the reports against the requirements of the licensees
  CAP as delineated in corporate procedure CAP-NGGC-0200, Corrective Action
The inspectors selected AR 542704, UPS-A Failure and Loss of ERFIS, PPC, Business  
  Program, 10 CFR 50.47, and 10 CFR 50 Appendix E.
Network, for detailed review. This AR identified that a single failure caused the loss of  
b. Findings
ERFIS and Safety Parameter Display System (SPDS) on both units. The inspectors  
  Introduction: A self-revealing Green NCV of 10 CFR 50.54(q)(2) was identified for the
reviewed the licensees CAP for ERFIS and SPDS failures in the past. The inspectors  
  licensees failure to properly evaluate or consider the impact to emergency response
reviewed these reports to verify that the licensee identified the full extent of the issue,  
  facilities of design change ESR98-00436 which was implemented in 1999. As a result,
performed an appropriate evaluation, and specified and prioritized appropriate corrective  
  a number of temporary losses of ERFIS, Emergency Response Data System (ERDS),
actions. The inspectors evaluated the reports against the requirements of the licensees  
  SPDS, and all displays including radiation monitors for the emergency response facilities
CAP as delineated in corporate procedure CAP-NGGC-0200, Corrective Action  
  occurred. Specifically, the licensee failed to ensure that adequate emergency response
Program, 10 CFR 50.47, and 10 CFR 50 Appendix E.  
  facilities and equipment were available as required by the Brunswick Nuclear Plant
  Radiological Emergency Plan, Section 1.3.1.3, revision 80, and 10 CFR 50.47(b)(8).
  This issue was captured in the licensees CAP as AR 542704.
  Description: In 1999, the licensee implemented design change ESR98-00436 for the
  power supply to the ERFIS, ERDS, SPDS, and all displays including RMS for the
  emergency response facilities. The licensee did not properly evaluate or consider the
  b.  
  impact to emergency response facilities and equipment prior to implementation of this
Findings  
  design change. As a result, the ERFIS, ERDS, and SPDS systems, and all radiation
  monitoring system (RMS) displays were susceptible to a single point power failure mode.
Introduction: A self-revealing Green NCV of 10 CFR 50.54(q)(2) was identified for the  
  The implementation of the design change introduced a single point failure mode which
licensees failure to properly evaluate or consider the impact to emergency response  
  did not meet the design requirements specified in their Design Basis Document (DBD
facilities of design change ESR98-00436 which was implemented in 1999. As a result,
  60) sections 3.6.7.2 and 3.6.7.3. Prior to the licensees implementation of design
a number of temporary losses of ERFIS, Emergency Response Data System (ERDS),  
  change ESR98-00436 in 1999, this single point vulnerability did not exist as the power
SPDS, and all displays including radiation monitors for the emergency response facilities  
  supply system had automatic switching capability on loss of one power source. When
occurred. Specifically, the licensee failed to ensure that adequate emergency response  
  the design change was implemented, the ERFIS, ERDS, and SPDS systems and RMS
facilities and equipment were available as required by the Brunswick Nuclear Plant  
  displays were degraded as demonstrated by the resulting failures of those systems on
Radiological Emergency Plan, Section 1.3.1.3, revision 80, and 10 CFR 50.47(b)(8).
  multiple occasions including July 17, 2004 and June 12, 2012. Additionally, all displays
This issue was captured in the licensees CAP as AR 542704.  
  for those systems were lost in all of the emergency facilities including the radiation
  monitoring system.
Description: In 1999, the licensee implemented design change ESR98-00436 for the  
power supply to the ERFIS, ERDS, SPDS, and all displays including RMS for the  
emergency response facilities. The licensee did not properly evaluate or consider the  
impact to emergency response facilities and equipment prior to implementation of this  
design change. As a result, the ERFIS, ERDS, and SPDS systems, and all radiation  
monitoring system (RMS) displays were susceptible to a single point power failure mode.
The implementation of the design change introduced a single point failure mode which  
did not meet the design requirements specified in their Design Basis Document (DBD  
60) sections 3.6.7.2 and 3.6.7.3. Prior to the licensees implementation of design  
change ESR98-00436 in 1999, this single point vulnerability did not exist as the power  
supply system had automatic switching capability on loss of one power source. When  
the design change was implemented, the ERFIS, ERDS, and SPDS systems and RMS  
displays were degraded as demonstrated by the resulting failures of those systems on  
multiple occasions including July 17, 2004 and June 12, 2012. Additionally, all displays  
for those systems were lost in all of the emergency facilities including the radiation  
monitoring system.  


                                        20
On June 13, 2012, the licensee made an event notification to the NRC Operations
20  
Center, 50.72(b)(3)(xiii) Loss of Emergency Assessment Capability, Offsite Response
Capability, or Offsite Communications Capability for the emergency response facilities.
On June 13, 2012, the licensee made an event notification to the NRC Operations  
The report delineated that at 5:57 p.m. EDT on June 12, 2012, Brunswick Nuclear Plant
Center, 50.72(b)(3)(xiii) Loss of Emergency Assessment Capability, Offsite Response  
experienced a fault on the Emergency Response Facility Information System (ERFIS)
Capability, or Offsite Communications Capability for the emergency response facilities.  
uninterruptible power supply (UPS) electrical bus A. This resulted in a loss of site
The report delineated that at 5:57 p.m. EDT on June 12, 2012, Brunswick Nuclear Plant  
Safety Parameter Display System (SPDS), Emergency Response Data System (ERDS)
experienced a fault on the Emergency Response Facility Information System (ERFIS)  
and Plant Process Computer (PPC) for both Unit 1 and Unit 2.
uninterruptible power supply (UPS) electrical bus A. This resulted in a loss of site  
During the loss of SPDS, the emergency response capability of that system was lost to
Safety Parameter Display System (SPDS), Emergency Response Data System (ERDS)  
the site. During the loss of ERDS, the automatic data transfer feature of that system
and Plant Process Computer (PPC) for both Unit 1 and Unit 2.
was lost for transmissions to the NRC, however manual data transfer was still available.
During the loss of the PPC, automatic core thermal power averaging and automatic core
During the loss of SPDS, the emergency response capability of that system was lost to  
thermal limit monitoring was lost. Manual calculations were available for these functions.
the site. During the loss of ERDS, the automatic data transfer feature of that system  
Unit 1 SPDS was restored to the Emergency Operations Facility (EOF) at 7:49 p.m. on
was lost for transmissions to the NRC, however manual data transfer was still available.  
June 12, 2012. Unit 2 SPDS was restored to the EOF at 8:30 p.m. on June 12, 2012.
During the loss of the PPC, automatic core thermal power averaging and automatic core  
The inverter was restored to service on June 17, 2012 at 12:00 noon.
thermal limit monitoring was lost. Manual calculations were available for these functions.  
Inspectors determined that the licensee did not properly evaluate or consider the impact
Unit 1 SPDS was restored to the Emergency Operations Facility (EOF) at 7:49 p.m. on  
to all emergency response facilities and equipment prior to implementation of the
June 12, 2012. Unit 2 SPDS was restored to the EOF at 8:30 p.m. on June 12, 2012.
ESR98-00436 design change. The inspectors concluded that the ERFIS, ERDS, and
The inverter was restored to service on June 17, 2012 at 12:00 noon.  
SPDS systems required by the Brunswick Nuclear Plant Radiological Emergency Plan
were degraded from 1999 when the design change was installed to present.
Compensatory measures were put in place during the June 2012 event to manually
Inspectors determined that the licensee did not properly evaluate or consider the impact  
obtain and log the required data from the instrumentation in the control room and
to all emergency response facilities and equipment prior to implementation of the  
transmit to the emergency response facilities, and after the June 2012 event, the
ESR98-00436 design change. The inspectors concluded that the ERFIS, ERDS, and  
licensee initiated a design change to restore the power configuration to those systems
SPDS systems required by the Brunswick Nuclear Plant Radiological Emergency Plan  
back to the original design which would remove this failure mechanism.
were degraded from 1999 when the design change was installed to present.
Analysis: The licensees failure to properly evaluate or consider the impact to
Compensatory measures were put in place during the June 2012 event to manually  
emergency response facilities of design change ESR98-00436 which was implemented
obtain and log the required data from the instrumentation in the control room and  
in 1999 was a performance deficiency. Specifically, the licensee introduced a single
transmit to the emergency response facilities, and after the June 2012 event, the  
point failure mode which did not meet the design requirements specified in their Design
licensee initiated a design change to restore the power configuration to those systems  
Basis Document (DBD 60) sections 3.6.7.2 and 3.6.7.3. This resulted in the licensees
back to the original design which would remove this failure mechanism.  
failure to ensure that adequate emergency response facilities and equipment were
available as delineated in the Updated Final Safety Analysis Report (UFSAR) Section
Analysis: The licensees failure to properly evaluate or consider the impact to  
7.7.1.9, and required by the Brunswick Nuclear Plant Radiological Emergency Plan,
emergency response facilities of design change ESR98-00436 which was implemented  
Section 1.3.1.3, revision 80, and 10 CFR 50.47(b)(8).
in 1999 was a performance deficiency. Specifically, the licensee introduced a single  
The finding was more than minor because it adversely affected the Emergency
point failure mode which did not meet the design requirements specified in their Design  
Preparedness Cornerstone objective of ensuring that the licensee was capable of
Basis Document (DBD 60) sections 3.6.7.2 and 3.6.7.3. This resulted in the licensees  
implementing adequate measures to protect the health and safety of the public in the
failure to ensure that adequate emergency response facilities and equipment were  
event of a radiological emergency. Specifically, the Facilities and Equipment attribute
available as delineated in the Updated Final Safety Analysis Report (UFSAR) Section  
was affected during the time when the ERFIS, ERDS, SPDS, and all displays including
7.7.1.9, and required by the Brunswick Nuclear Plant Radiological Emergency Plan,  
radiation monitors for the emergency response facilities were degraded, and as a result
Section 1.3.1.3, revision 80, and 10 CFR 50.47(b)(8).  
did not meet 10 CFR 50.47(b)(8) Planning Standard program element, adequate
emergency facilities and equipment to support the emergency response are provided
The finding was more than minor because it adversely affected the Emergency  
and maintained. The finding was assessed for significance in accordance with NRC IMC
Preparedness Cornerstone objective of ensuring that the licensee was capable of  
0609, Appendix B Emergency Preparedness Significance Determination Process.
implementing adequate measures to protect the health and safety of the public in the  
event of a radiological emergency. Specifically, the Facilities and Equipment attribute  
was affected during the time when the ERFIS, ERDS, SPDS, and all displays including  
radiation monitors for the emergency response facilities were degraded, and as a result  
did not meet 10 CFR 50.47(b)(8) Planning Standard program element, adequate  
emergency facilities and equipment to support the emergency response are provided  
and maintained. The finding was assessed for significance in accordance with NRC IMC  
0609, Appendix B Emergency Preparedness Significance Determination Process.


                                                21
      Attachment 2 of Appendix B, Failure to Comply Significance Logic is as follows: Failure
21  
      to comply; Loss of Risk Significant Planning Standard Function (RSPS), No; RSPS
      Degraded Function, No; Loss of Planning Standard Function, No; the result is a Green
Attachment 2 of Appendix B, Failure to Comply Significance Logic is as follows: Failure  
      finding. The inspectors determined that this resulted in a low safety significance finding
to comply; Loss of Risk Significant Planning Standard Function (RSPS), No; RSPS  
      (Green). No cross-cutting aspect was assigned to this finding because the performance
Degraded Function, No; Loss of Planning Standard Function, No; the result is a Green  
      deficiency occurred more than three years ago and is not reflective of current plant
finding. The inspectors determined that this resulted in a low safety significance finding  
      performance.
(Green). No cross-cutting aspect was assigned to this finding because the performance  
      Enforcement: 10 CFR 50.54(q)(2) requires, in part, a licensee to follow and maintain the
deficiency occurred more than three years ago and is not reflective of current plant  
      effectiveness of an emergency plan that meets the requirements in Appendix E to this
performance.  
      part and, for nuclear power reactor licensee, the planning standards of 10 CFR 50.47(b).
      The Brunswick Nuclear Plant Radiological Emergency Plan, Section 1.3.1.3, revision 80,
Enforcement: 10 CFR 50.54(q)(2) requires, in part, a licensee to follow and maintain the  
      states in part that special provisions have been made to assure that ample space and
effectiveness of an emergency plan that meets the requirements in Appendix E to this  
      proper equipment are available to effectively respond to a full range of possible
part and, for nuclear power reactor licensee, the planning standards of 10 CFR 50.47(b).  
      emergencies. Contrary to the above, from 1999, when design change ESR98-00436
The Brunswick Nuclear Plant Radiological Emergency Plan, Section 1.3.1.3, revision 80,  
      was installed, until the compensatory measures were put in place in June 2012, the
states in part that special provisions have been made to assure that ample space and  
      licensee failed to maintain adequate emergency facilities and equipment to support
proper equipment are available to effectively respond to a full range of possible  
      emergency response when the ERFIS, ERDS, SPDS, and all displays including radiation
emergencies.   Contrary to the above, from 1999, when design change ESR98-00436  
      monitors for the emergency response facilities were degraded due to the implementation
was installed, until the compensatory measures were put in place in June 2012, the  
      of the design change. This resulted in failures of those systems on July 17, 2004 and
licensee failed to maintain adequate emergency facilities and equipment to support  
      June 12, 2012. The licensee has compensatory measures in place, entered this issue
emergency response when the ERFIS, ERDS, SPDS, and all displays including radiation  
      their CAP as AR 542704, and initiated a design change to restore the power
monitors for the emergency response facilities were degraded due to the implementation  
      configuration back to the original design. Because the licensee entered the issue into its
of the design change. This resulted in failures of those systems on July 17, 2004 and  
      CAP and the finding is of very low safety significance (Green), this violation is being
June 12, 2012. The licensee has compensatory measures in place, entered this issue  
      treated as an NCV, consistent with Section 2.3.2 of the NRCs Enforcement Policy: NCV
their CAP as AR 542704, and initiated a design change to restore the power  
      05000325; 324/2012004-02, Failure to Maintain Reliability and Availability of Emergency
configuration back to the original design. Because the licensee entered the issue into its  
      Response Equipment for Emergency Response Facilities.
CAP and the finding is of very low safety significance (Green), this violation is being  
.3   Assessments and Observations
treated as an NCV, consistent with Section 2.3.2 of the NRCs Enforcement Policy: NCV  
      Selected Issue Follow-up Inspection: EDG 2 wiring associated with Alternate Safe
05000325; 324/2012004-02, Failure to Maintain Reliability and Availability of Emergency  
      Shutdown (ASSD) Switch 2-DG-SS-A1
Response Equipment for Emergency Response Facilities.  
   a. Inspection Scope
      The inspectors performed a detailed review of AR 557897 associated with the wiring for
.3  
      the EDG 2 Alternate Safe Shutdown (ASSD) Switch 2-DG-SS-A1. The issue was
Assessments and Observations  
      discovered during a planned system outage for EDG2 during the week of August 26.
      The inspectors verified that the issue was captured completely and accurately in the
Selected Issue Follow-up Inspection: EDG 2 wiring associated with Alternate Safe  
      CAP. The inspectors evaluated the licensees operability determinations and performed
Shutdown (ASSD) Switch 2-DG-SS-A1  
      walk-downs with licensee staff of applicable fire areas as needed. The inspectors
      followed the licensees actions to restore the wiring to its proper configuration and also
   a.  
      verified the extent of condition inspections for the remaining EDGs 1, 3 and 4 were
Inspection Scope  
      completed in a timely manner. The inspectors reviewed the licensees reportability
      evaluation and subsequent 8-hour report made to the NRC in accordance with 10 CFR
The inspectors performed a detailed review of AR 557897 associated with the wiring for  
      50.72(b)(3)(ii)(B). Additional documents reviewed are listed in the Attachment.
the EDG 2 Alternate Safe Shutdown (ASSD) Switch 2-DG-SS-A1. The issue was  
   b. Findings
discovered during a planned system outage for EDG2 during the week of August 26.
The inspectors verified that the issue was captured completely and accurately in the  
CAP. The inspectors evaluated the licensees operability determinations and performed  
walk-downs with licensee staff of applicable fire areas as needed. The inspectors  
followed the licensees actions to restore the wiring to its proper configuration and also  
verified the extent of condition inspections for the remaining EDGs 1, 3 and 4 were  
completed in a timely manner. The inspectors reviewed the licensees reportability  
evaluation and subsequent 8-hour report made to the NRC in accordance with 10 CFR  
50.72(b)(3)(ii)(B). Additional documents reviewed are listed in the Attachment.  
   b.  
Findings  


                                                22
      Introduction: The inspectors opened an unresolved item (URI) for this issue of concern
22  
      to determine if a performance deficiency existed.
      Description: A wiring discrepancy was identified during inspection of the EDG 2 ASSD
Introduction: The inspectors opened an unresolved item (URI) for this issue of concern  
      switch 2-DG-SS-A1. A contact in the circuit was determined to be bypassed that would
to determine if a performance deficiency existed.  
      have the potential to prevent proper isolation of the EDG2 control circuits from the Main
      Control Room (MCR) during an Appendix R fire event. The inspectors plan to review the
Description: A wiring discrepancy was identified during inspection of the EDG 2 ASSD  
      licensees cause evaluation for this event and determine if a performance deficiency
switch 2-DG-SS-A1. A contact in the circuit was determined to be bypassed that would  
      existed. This issue is being tracked as URI 05000325; 324/2012004-03, EDG2 wiring on
have the potential to prevent proper isolation of the EDG2 control circuits from the Main  
      ASSD switch.
Control Room (MCR) during an Appendix R fire event. The inspectors plan to review the  
4OA3 Follow-up of Events (71153 - 2 samples)
licensees cause evaluation for this event and determine if a performance deficiency  
.1   Notice of Unusual Event for Fire in the Protected Area
existed. This issue is being tracked as URI 05000325; 324/2012004-03, EDG2 wiring on  
   a. Inspection Scope
ASSD switch.  
      For the plant event listed below, the inspectors reviewed plant parameters, reviewed
      personnel performance, and evaluated performance of mitigating systems. The
4OA3 Follow-up of Events (71153 - 2 samples)  
      inspectors communicated the plant events to appropriate regional NRC personnel, and
      compared the event details with criteria contained in IMC 0309, Reactive Inspection
.1  
      Decision Basis for Reactors, for consideration of potential reactive inspection activities.
Notice of Unusual Event for Fire in the Protected Area  
      As applicable, the inspectors verified that the licensee made appropriate emergency
      classification assessments and properly reported the event in accordance with 10 CFR
   a.  
      50.72. The inspectors reviewed the licensees follow-up actions related to the events to
Inspection Scope  
      assure that the licensee implemented appropriate corrective actions commensurate with
      their safety significance.
For the plant event listed below, the inspectors reviewed plant parameters, reviewed  
      *   On August 2, 2012, a fire existed in the protected area on the Units 1 and 2 turbine
personnel performance, and evaluated performance of mitigating systems. The  
          building roof for approximately two hours, meeting the criteria for a Notice of Unusual
inspectors communicated the plant events to appropriate regional NRC personnel, and  
          Event declaration.
compared the event details with criteria contained in IMC 0309, Reactive Inspection  
   b. Findings
Decision Basis for Reactors, for consideration of potential reactive inspection activities.
      One licensee identified violation is documented in Section 4OA7 of this report.
As applicable, the inspectors verified that the licensee made appropriate emergency  
.2   (Closed) LER 05000325/2012-004-00, High Pressure Coolant Injection (HPCI)
classification assessments and properly reported the event in accordance with 10 CFR  
      Inoperable Due to Erratic Governor Operation
50.72. The inspectors reviewed the licensees follow-up actions related to the events to  
   a. Inspection Scope
assure that the licensee implemented appropriate corrective actions commensurate with  
      On May 2, 2012, Unit 1 HPCI was declared inoperable due to erratic governor operation
their safety significance.  
      during Surveillance Test 0PT-09.2, HPCI System Operability Test. The erratic governor
      operation was due to the failure of the Ramp Generator Signal Convertor (RGSC). The
*  
      licensee determined that the root cause of the RGSC failure was due to a lack of a
On August 2, 2012, a fire existed in the protected area on the Units 1 and 2 turbine  
      replacement preventative maintenance (PM) for the RGSC, which had been installed for
building roof for approximately two hours, meeting the criteria for a Notice of Unusual  
      at least 22 years. The corrective actions included replacing the RGSC and creating a
Event declaration.  
      PM task to replace the RGSCs. The licensee documented the root cause evaluation in
   b.  
Findings  
One licensee identified violation is documented in Section 4OA7 of this report.  
.2
(Closed) LER 05000325/2012-004-00, High Pressure Coolant Injection (HPCI)  
Inoperable Due to Erratic Governor Operation  
   a.  
Inspection Scope  
On May 2, 2012, Unit 1 HPCI was declared inoperable due to erratic governor operation  
during Surveillance Test 0PT-09.2, HPCI System Operability Test. The erratic governor  
operation was due to the failure of the Ramp Generator Signal Convertor (RGSC). The  
licensee determined that the root cause of the RGSC failure was due to a lack of a  
replacement preventative maintenance (PM) for the RGSC, which had been installed for  
at least 22 years. The corrective actions included replacing the RGSC and creating a  
PM task to replace the RGSCs. The licensee documented the root cause evaluation in  


                                                23
      NCR 534364. The inspectors reviewed the LER, the NCR, and corrective actions to
23  
      determine whether the station adequately evaluated the condition.
   b. Findings
NCR 534364. The inspectors reviewed the LER, the NCR, and corrective actions to  
      One licensee identified violation is documented in Section 4OA7 of this report. This LER
determine whether the station adequately evaluated the condition.  
      is closed.
4OA5 Other Activities
.1   (Discussed) NRC Temporary Instruction (TI) 2515/187, Inspection of Near-Term Task
   b.  
      Force Recommendation 2.3 Flooding Walk-downs, and NRC TI 2515/188, Inspection of
Findings  
      Near-Term Task Force Recommendation 2.3 Seismic Walk-downs
   a. Inspection Scope
One licensee identified violation is documented in Section 4OA7 of this report. This LER  
      Inspectors accompanied the licensee on a sampling basis, during their flooding and
is closed.  
      seismic walk-downs, to verify that the licensees walk-down activities were conducted
      using the methodology endorsed by the NRC. These walk-downs are being performed at
4OA5 Other Activities  
      all sites in response to a letter from the NRC to licensees, entitled Request for
      Information Pursuant to Title 10 of the Code of Federal Regulations 50.54(f) Regarding
.1  
      Recommendations 2.1, 2.3, and 9.3, of the Near-Term Task Force Review of Insights
(Discussed) NRC Temporary Instruction (TI) 2515/187, Inspection of Near-Term Task  
      from the Fukushima Dai-Ichi Accident, dated March 12, 2012 (ADAMS Accession No.
Force Recommendation 2.3 Flooding Walk-downs, and NRC TI 2515/188, Inspection of  
      ML12053A340).
Near-Term Task Force Recommendation 2.3 Seismic Walk-downs
      Enclosure 3 of the March 12, 2012, letter requested licensees to perform seismic walk-
      downs using an NRC-endorsed walk-down methodology. Electric Power Research
   a.  
      Institute (EPRI) document 1025286 titled, Seismic Walk-down Guidance, (ADAMS
Inspection Scope  
      Accession No. ML12188A031) provided the NRC-endorsed methodology for performing
      seismic walk-downs to verify that plant features, credited in the current licensing basis
Inspectors accompanied the licensee on a sampling basis, during their flooding and  
      (CLB) for seismic events, are available, functional, and properly maintained.
seismic walk-downs, to verify that the licensees walk-down activities were conducted  
      Enclosure 4 of the letter requested licensees to perform external flooding walk-downs
using the methodology endorsed by the NRC. These walk-downs are being performed at  
      using an NRC-endorsed walk-down methodology (ADAMS Accession No.
all sites in response to a letter from the NRC to licensees, entitled Request for  
      ML12056A050). Nuclear Energy Industry (NEI) document 12-07 titled, Guidelines for
Information Pursuant to Title 10 of the Code of Federal Regulations 50.54(f) Regarding  
      Performing Verification Walk-downs of Plant Protection Features, (ADAMS Accession
Recommendations 2.1, 2.3, and 9.3, of the Near-Term Task Force Review of Insights  
      No. ML12173A215) provided the NRC-endorsed methodology for assessing external
from the Fukushima Dai-Ichi Accident, dated March 12, 2012 (ADAMS Accession No.  
      flood protection and mitigation capabilities to verify that plant features, credited in the
ML12053A340).  
      CLB for protection and mitigation from external flood events, are available, functional,
      and properly maintained.
Enclosure 3 of the March 12, 2012, letter requested licensees to perform seismic walk-
   b. Findings
downs using an NRC-endorsed walk-down methodology. Electric Power Research  
      Findings or violations associated with the flooding and seismic walk-downs, if any, will
Institute (EPRI) document 1025286 titled, Seismic Walk-down Guidance, (ADAMS  
      be documented in future reports.
Accession No. ML12188A031) provided the NRC-endorsed methodology for performing  
seismic walk-downs to verify that plant features, credited in the current licensing basis  
(CLB) for seismic events, are available, functional, and properly maintained.  
Enclosure 4 of the letter requested licensees to perform external flooding walk-downs  
using an NRC-endorsed walk-down methodology (ADAMS Accession No.  
ML12056A050). Nuclear Energy Industry (NEI) document 12-07 titled, Guidelines for  
Performing Verification Walk-downs of Plant Protection Features, (ADAMS Accession  
No. ML12173A215) provided the NRC-endorsed methodology for assessing external  
flood protection and mitigation capabilities to verify that plant features, credited in the  
CLB for protection and mitigation from external flood events, are available, functional,  
and properly maintained.  
   b.  
Findings  
Findings or violations associated with the flooding and seismic walk-downs, if any, will  
be documented in future reports.  


                                              24
.2   (Discussed) Temporary Instruction (TI) 2515/182 - Review of the Implementation of the
24  
      Industry Initiative to Control Degradation of Underground Piping and Tanks, Phase 1
   a. Inspection Scope
      Leakage from buried and underground pipes has resulted in ground water contamination
      incidents with associated heightened NRC and public interest. The industry issued a
      guidance document, Nuclear Energy Institute (NEI) 09-14, Guideline for the
.2  
      Management of Buried Piping Integrity, (ADAMS Accession No. ML 1030901420), to
(Discussed) Temporary Instruction (TI) 2515/182 - Review of the Implementation of the  
      describe the goals and required actions (commitments made by the licensee) resulting
Industry Initiative to Control Degradation of Underground Piping and Tanks, Phase 1  
      from this underground piping and tank initiative. On December 31, 2010, NEI issued
      Revision 1 to NEI 09-14, Guidance for the Management of Underground Piping and
   a.  
      Tank Integrity, (ADAMS Accession No. ML 110700122), with an expanded scope of
Inspection Scope  
      components which included underground piping that was not in direct contact with the
      soil and underground tanks. On November 17, 2011, the NRC issued TI-2515/182,
      Review of the Industry Initiative to Control Degradation of Underground Piping and
Leakage from buried and underground pipes has resulted in ground water contamination  
      Tanks, to gather information related to the industrys implementation of this initiative.
incidents with associated heightened NRC and public interest. The industry issued a  
      The instructors reviewed the licensees programs for buried pipe and underground piping
guidance document, Nuclear Energy Institute (NEI) 09-14, Guideline for the  
      and tanks in accordance with TI-2515/182 to determine if the program attributes and
Management of Buried Piping Integrity, (ADAMS Accession No. ML 1030901420), to  
      completion dates identified in Section 3.3 A and 3.3 B of NEI 09-14, Revision 1, were
describe the goals and required actions (commitments made by the licensee) resulting  
      contained in the licensees program and implementing procedures. For the buried pipe
from this underground piping and tank initiative. On December 31, 2010, NEI issued  
      and underground piping program attributes, with completion dates that had passed, the
Revision 1 to NEI 09-14, Guidance for the Management of Underground Piping and  
      inspectors reviewed records to determine if the attribute was in fact complete and to
Tank Integrity, (ADAMS Accession No. ML 110700122), with an expanded scope of  
      determine if the attribute was accomplished in a manner which reflected good or poor
components which included underground piping that was not in direct contact with the  
      practices in management.
soil and underground tanks. On November 17, 2011, the NRC issued TI-2515/182,  
   b. Observations
Review of the Industry Initiative to Control Degradation of Underground Piping and  
      The licensees buried piping and underground piping and tanks program was inspected
Tanks, to gather information related to the industrys implementation of this initiative.
      in accordance with paragraphs 03.01.a through 03.01.c of TI-2515/182 and was found to
The instructors reviewed the licensees programs for buried pipe and underground piping  
      meet all applicable aspects of NEI 09-14 Revision 1, as set forth in Table 1 of the TI.
and tanks in accordance with TI-2515/182 to determine if the program attributes and  
      Based upon the scope of the review described above, Phase I of TI-2515/182 was
completion dates identified in Section 3.3 A and 3.3 B of NEI 09-14, Revision 1, were  
      completed.
contained in the licensees program and implementing procedures. For the buried pipe  
   c. Findings
and underground piping program attributes, with completion dates that had passed, the  
      No findings were identified.
inspectors reviewed records to determine if the attribute was in fact complete and to  
4OA6 Management Meetings
determine if the attribute was accomplished in a manner which reflected good or poor  
      Exit Meeting Summary
practices in management.  
      On July 19, 2012, the inspectors presented inspection results of the triennial heat sink
      inspection to Mr. Michael Annacone and other members of the licensee staff. The
   b.  
Observations  
The licensees buried piping and underground piping and tanks program was inspected  
in accordance with paragraphs 03.01.a through 03.01.c of TI-2515/182 and was found to  
meet all applicable aspects of NEI 09-14 Revision 1, as set forth in Table 1 of the TI.  
Based upon the scope of the review described above, Phase I of TI-2515/182 was  
completed.  
   c.  
Findings  
No findings were identified.  
4OA6 Management Meetings  
Exit Meeting Summary  
On July 19, 2012, the inspectors presented inspection results of the triennial heat sink  
inspection to Mr. Michael Annacone and other members of the licensee staff. The  


                                                25
    inspectors confirmed that none of the potential report input discussed was considered
25  
    proprietary.
    On September 18, 2012, the inspector presented inspection results of the TI-182, Phase
inspectors confirmed that none of the potential report input discussed was considered  
    1 of the Underground Piping and Tanks Inspection by conference call to Mr. James
proprietary.  
    Burke, Site Director of Engineering, and other members of the licensee staff. The
    inspector verified that all proprietary information was returned to the licensee.
On September 18, 2012, the inspector presented inspection results of the TI-182, Phase  
    On October 11, 2012, the inspectors presented inspection results from the quarterly
1 of the Underground Piping and Tanks Inspection by conference call to Mr. James  
    inspection to Mr. Annacone and other members of the licensee staff. The inspectors
Burke, Site Director of Engineering, and other members of the licensee staff. The  
    confirmed that any proprietary information received during the inspection period were
inspector verified that all proprietary information was returned to the licensee.  
    properly controlled or returned to licensee staff.
4OA7 Licensee-Identified Violations
On October 11, 2012, the inspectors presented inspection results from the quarterly  
    The following violations of very low significance (Green) were identified by the licensee
inspection to Mr. Annacone and other members of the licensee staff. The inspectors  
    and are violations of NRC requirements which meet the criteria of the NRC Enforcement
confirmed that any proprietary information received during the inspection period were  
    Policy, for being dispositioned as NCVs.
properly controlled or returned to licensee staff.  
    *       10 CFR 50.54(q) requires, in part, a licensee authorized to possess and operate
            a nuclear power reactor shall follow and maintain in effect emergency plans
4OA7 Licensee-Identified Violations
            which meet the standards of 10 CFR 50.47(b). Title 10 CFR 50.47(b)(4)
            requires, in part, a standard emergency classification and action level scheme be
The following violations of very low significance (Green) were identified by the licensee  
            used by the licensee. Procedure 0PEP-02.1.1, Emergency Control - Notification
and are violations of NRC requirements which meet the criteria of the NRC Enforcement  
            of Unusual Event, Alert, Site Area Emergency, and General Emergency, Step
Policy, for being dispositioned as NCVs.  
            5.7.2 states, that the emergency declaration will be made within 15 minutes after
            the availability of indications to plant operators that an emergency action level
*  
            has been exceeded. Procedure 0PEP-02.1, Initial Emergency Actions, HU2.1,
10 CFR 50.54(q) requires, in part, a licensee authorized to possess and operate  
            requires the declaration of an Unusual Event when a fire is not extinguished
a nuclear power reactor shall follow and maintain in effect emergency plans  
            within 15 minutes of control room notification or verification of a control room fire
which meet the standards of 10 CFR 50.47(b). Title 10 CFR 50.47(b)(4)  
            alarm in any Table H-1 or Table H-3 areas. Table H-1 includes the turbine
requires, in part, a standard emergency classification and action level scheme be  
            building. Contrary to the above, on August 2, 2012, a Notice of Unusual Event
used by the licensee. Procedure 0PEP-02.1.1, Emergency Control - Notification  
            (NOUE) was not classified within 15 minutes of a fire within the protected area
of Unusual Event, Alert, Site Area Emergency, and General Emergency, Step  
            not being extinguished within 15 minutes of detection. Specifically, when a fire
5.7.2 states, that the emergency declaration will be made within 15 minutes after  
            was reported on the Turbine Building roof to the Control Room and was not
the availability of indications to plant operators that an emergency action level  
            extinguished within 15 minutes, conditions were met for classification of EAL
has been exceeded. Procedure 0PEP-02.1, Initial Emergency Actions, HU2.1,  
            HU2.1 in accordance with Procedure 0PEP-02.1; however, the EAL was not
requires the declaration of an Unusual Event when a fire is not extinguished  
            classified until approximately eight hours after the fire started. This issue was
within 15 minutes of control room notification or verification of a control room fire  
            entered into the licensees CAP as NCR 552984 and the licensee is performing a
alarm in any Table H-1 or Table H-3 areas. Table H-1 includes the turbine  
            root cause evaluation. Corrective actions included making a one hour report to
building. Contrary to the above, on August 2, 2012, a Notice of Unusual Event  
            the NRC for discovery of a condition that met the EAL classification for an NOUE
(NOUE) was not classified within 15 minutes of a fire within the protected area  
            after the fact. The inspectors determined the finding was associated with an
not being extinguished within 15 minutes of detection. Specifically, when a fire  
            actual event implementation problem, and assessed the significance using IMC
was reported on the Turbine Building roof to the Control Room and was not  
            0609, Appendix B, "Emergency Preparedness Significance Determination
extinguished within 15 minutes, conditions were met for classification of EAL  
            Process." Using the Emergency Preparedness SDP, Sheet 1, "Failure to
HU2.1 in accordance with Procedure 0PEP-02.1; however, the EAL was not  
            Implement (Actual Event) Significance Logic" the inspectors determined the
classified until approximately eight hours after the fire started. This issue was  
            finding was of very low safety significance (Green) because the licensee failed to
entered into the licensees CAP as NCR 552984 and the licensee is performing a  
            implement a risk significant planning standard (10 CFR 50.47(b)(4)) during an
root cause evaluation. Corrective actions included making a one hour report to  
            actual Notice of Unusual Event.
the NRC for discovery of a condition that met the EAL classification for an NOUE  
after the fact. The inspectors determined the finding was associated with an  
actual event implementation problem, and assessed the significance using IMC  
0609, Appendix B, "Emergency Preparedness Significance Determination  
Process." Using the Emergency Preparedness SDP, Sheet 1, "Failure to  
Implement (Actual Event) Significance Logic" the inspectors determined the  
finding was of very low safety significance (Green) because the licensee failed to  
implement a risk significant planning standard (10 CFR 50.47(b)(4)) during an  
actual Notice of Unusual Event.


                                            26
    *   10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings,"
26  
          requires that activities affecting quality shall be prescribed by documented
          instructions, procedures, or drawings, of a type appropriate to the circumstances
          and shall be accomplished in accordance with these instructions, procedures, or
*  
          drawings. Licensee procedure ADM-NGGC-0107, Equipment Reliability Process
10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings,"  
          Guideline, steps 9.4.9 and 9.4.10 required component experts and preventive
requires that activities affecting quality shall be prescribed by documented  
          maintenance (PM) optimization to determine if there was a cost effective PM to
instructions, procedures, or drawings, of a type appropriate to the circumstances  
          prevent failure and then to develop the PM model. Contrary to the above, the
and shall be accomplished in accordance with these instructions, procedures, or  
          Unit 1 high pressure coolant injection (HPCI) ramp generator signal converter
drawings. Licensee procedure ADM-NGGC-0107, Equipment Reliability Process  
          (RGSC) did not have the appropriate preventive maintenance to prevent failure.
Guideline, steps 9.4.9 and 9.4.10 required component experts and preventive  
          As a result, the Unit 1 high pressure coolant injection (HPCI) system failed the
maintenance (PM) optimization to determine if there was a cost effective PM to  
          HPCI System Operability Test performed on April 30, 2012 and was declared
prevent failure and then to develop the PM model. Contrary to the above, the  
          inoperable. The licensee entered this issue into the CAP as NCR 534364.
Unit 1 high pressure coolant injection (HPCI) ramp generator signal converter  
          Corrective actions included replacing the RGSC and creating a PM task to
(RGSC) did not have the appropriate preventive maintenance to prevent failure.
          replace the RGSCs on a specified frequency. Using IMC 0609, Appendix A,
As a result, the Unit 1 high pressure coolant injection (HPCI) system failed the  
          "Phase 1 Initial Screening and Characterization of Findings," the inspectors
HPCI System Operability Test performed on April 30, 2012 and was declared  
          determined this finding required a Phase 2 analysis. The Phase 1 screened this
inoperable. The licensee entered this issue into the CAP as NCR 534364.
          Mitigating Systems Cornerstone finding to Phase 2 because the finding
Corrective actions included replacing the RGSC and creating a PM task to  
          represented a loss of HPCI system and/or function. The inspectors, with the
replace the RGSCs on a specified frequency. Using IMC 0609, Appendix A,  
          assistance of the regional Senior Risk Analyst, performed a Phase 2 analysis
"Phase 1 Initial Screening and Characterization of Findings," the inspectors  
          using the Saphire 8 Model. 109 hours of unavailability time was used for the
determined this finding required a Phase 2 analysis. The Phase 1 screened this  
          analysis since HPCI was not required during the refueling outage from February
Mitigating Systems Cornerstone finding to Phase 2 because the finding  
          23, 2012 through April 29, 2012. Based on the results of the Phase 2 analysis,
represented a loss of HPCI system and/or function. The inspectors, with the  
          the inspectors determined the finding was of very low safety significance (Green).
assistance of the regional Senior Risk Analyst, performed a Phase 2 analysis  
ATTACHMENT: SUPPLEMENTAL INFORMATION
using the Saphire 8 Model. 109 hours of unavailability time was used for the  
analysis since HPCI was not required during the refueling outage from February  
23, 2012 through April 29, 2012. Based on the results of the Phase 2 analysis,  
the inspectors determined the finding was of very low safety significance (Green).  
ATTACHMENT: SUPPLEMENTAL INFORMATION  


                                SUPPLEMENTAL INFORMATION
                                  KEY POINTS OF CONTACT
Attachment
Licensee Personnel
SUPPLEMENTAL INFORMATION  
M. Annacone, Site Vice President
A. Brittain, Manager - Security
KEY POINTS OF CONTACT  
J. Burke, Director - Site Engineering
K. Croker, Supervisor - Emergency Preparedness
Licensee Personnel  
C. Dunsmore, Manager - Shift Operations
P. Dubrouillet, Manager - Training
M. Annacone, Site Vice President  
G. Galloway, Acting Manager, Nuclear Oversight
A. Brittain, Manager - Security  
C. George, Manager - BOP Systems
J. Burke, Director - Site Engineering  
S. Gordy, Manager - Maintenance
K. Croker, Supervisor - Emergency Preparedness
L. Grzeck, Manager - Regulatory Affairs
C. Dunsmore, Manager - Shift Operations  
M. Hamm, Superintendent - Mechanical Maintenance
P. Dubrouillet, Manager - Training  
F. Jefferson, Manager - Reactor Systems Engineering
G. Galloway, Acting Manager, Nuclear Oversight  
J. Kalamaja, Manager - Operations
C. George, Manager - BOP Systems  
J. Krakuszeski, Plant General Manager
S. Gordy, Manager - Maintenance
R. Mosier, Communication Specialist
L. Grzeck, Manager - Regulatory Affairs  
A. Padleckas, Superintendent - Nuclear Operations Performance
M. Hamm, Superintendent - Mechanical Maintenance  
D. Petrusic, Superintendent - Environmental and Chemistry
F. Jefferson, Manager - Reactor Systems Engineering  
A. Pope, Manager - Nuclear Support Services
J. Kalamaja, Manager - Operations  
J. Price, Manager- Design Engineering
J. Krakuszeski, Plant General Manager  
W. Richardson, Engineering
R. Mosier, Communication Specialist  
T. Roeder, Supervisor - Chemistry
A. Padleckas, Superintendent - Nuclear Operations Performance  
T. Sherrill, Licensing Senior Technical Specialist
D. Petrusic, Superintendent - Environmental and Chemistry  
P. Smith, Superintendent - Electrical, Instrumentation, and Controls Maintenance
A. Pope, Manager - Nuclear Support Services  
M. Talon, Buried Piping Program Manager
J. Price, Manager- Design Engineering  
J. Terrell, Corporate Buried Piping Program Manager
W. Richardson, Engineering  
M. Turkal, Lead Engineer - Technical Support
T. Roeder, Supervisor - Chemistry  
J. Vincelli, Manager - Environmental and Radiological Controls
T. Sherrill, Licensing Senior Technical Specialist  
B. Wilder, Engineering
P. Smith, Superintendent - Electrical, Instrumentation, and Controls Maintenance  
E. Wills, Director - Site Operations
M. Talon, Buried Piping Program Manager  
NRC Personnel
J. Terrell, Corporate Buried Piping Program Manager  
R. Musser, Chief, Reactor Projects Branch 4, Division of Reactor Projects Region II
M. Turkal, Lead Engineer - Technical Support  
                                                                                    Attachment
J. Vincelli, Manager - Environmental and Radiological Controls  
B. Wilder, Engineering  
E. Wills, Director - Site Operations  
NRC Personnel  
R. Musser, Chief, Reactor Projects Branch 4, Division of Reactor Projects Region II  


                  LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Opened and Closed
Attachment
05000325/2012004-01         NCV   Failure to Maintain Secondary Containment Operable
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED  
                                  During an OPDRV Activity. (Section 1R20)
05000325;324/2012004-02      NCV  Failure to Maintain Reliability and Availability of
                                  Emergency Response Equipment for Emergency
Opened and Closed  
                                  Response Facilities. (Section 4OA2.2)
Opened
05000325/2012004-01  
05000325;324/2012004-03       URI  EDG2 Wiring on ASSD Switch (Section 4OA2.3)
Closed
05000325/2012-004-00         LER  High Pressure Coolant Injection (HPCI) Inoperable
05000325;324/2012004-02
                                  Due to Erratic Governor Operation (Section 4OA3.2)
NCV  
Discussed
Temporary Instruction         TI Inspection of Near-Term Task Force Recommendation
2515/187                          2.3 Flooding Walk-downs (Section 4OA5.1)
NCV
Temporary Instruction         TI Inspection of Near-Term Task Force Recommendation
Failure to Maintain Secondary Containment Operable  
2515/188                          2.3 Seismic Walk-downs (Section 4OA5.1)
During an OPDRV Activity. (Section 1R20)
Temporary Instruction         TI Review of the Implementation of the Industry Initiative
2515/182                          to Control Degradation of Underground Piping and
Failure to Maintain Reliability and Availability of  
                                  Tanks, Phase 1 (Section 4OA5.2)
Emergency Response Equipment for Emergency  
                                                                                    Attachment
Response Facilities. (Section 4OA2.2)  
Opened  
05000325;324/2012004-03  
URI  
   
EDG2 Wiring on ASSD Switch (Section 4OA2.3)  
Closed  
05000325/2012-004-00  
LER  
   
High Pressure Coolant Injection (HPCI) Inoperable  
Due to Erratic Governor Operation (Section 4OA3.2)  
Discussed  
Temporary Instruction  
2515/187
TI  
Inspection of Near-Term Task Force Recommendation  
2.3 Flooding Walk-downs (Section 4OA5.1)  
Temporary Instruction  
2515/188
TI  
Inspection of Near-Term Task Force Recommendation  
2.3 Seismic Walk-downs (Section 4OA5.1)  
Temporary Instruction  
2515/182
TI  
Review of the Implementation of the Industry Initiative  
to Control Degradation of Underground Piping and  
Tanks, Phase 1 (Section 4OA5.2)  


                              LIST OF DOCUMENTS REVIEWED
Section 1R01: Adverse Weather Protection
Attachment
Procedures
LIST OF DOCUMENTS REVIEWED  
0AOP-13.0, Operation During Hurricane, Flood Conditions, Tornado, or Earthquake
0PEP-02.6, Severe Weather
Section 1R01: Adverse Weather Protection  
  2APP-UA-01, Annunciator Procedure for Panel UA-01
2APP-UA-28, Annunciator Procedure for Panel UA-28
Procedures  
2OP-43, Service Water System Operating Procedure
0AOP-13.0, Operation During Hurricane, Flood Conditions, Tornado, or Earthquake  
OPS-NGGC-1305, Operability Determinations
0PEP-02.6, Severe Weather  
Nuclear Condition Reports
  2APP-UA-01, Annunciator Procedure for Panel UA-01  
556860         556861         556862       556863         556864       556865
2APP-UA-28, Annunciator Procedure for Panel UA-28  
556866         556867         556868       556869         556870       557375
2OP-43, Service Water System Operating Procedure  
555023         545354         553946
OPS-NGGC-1305, Operability Determinations  
Work Orders
550098         550100         550102       550015         545859       545861
Nuclear Condition Reports  
1828825       1828826       1643223       1775054
556860  
Drawings
556861  
D-02778, Reactor Building Floor and Wall Sleeves Tabulation - Sheet No 1 Unit No 2
556862  
D-02779, Reactor Building Floor and Wall Sleeves Tabulation and Details - Sheet No 2
556863  
D-11597, Backdraft Damper with Extra Deep Frame
556864  
F-0424, Service Water Intake Structure Units 1 & 2 Ventilation System & Drainage Piping
556865  
LL-FB-02103, Reactor Building, Elevation -170, Fire Barrier Penetrations, RHR-HPCI Room
556866  
        North Wall
556867  
Miscellaneous
556868  
0PIC-LS001, Omnitrol (Valrec) Level Control Switch Model 613, Single Actuator
556869  
DBD-106, Hazards Analysis
556870  
Engineering Change 80408R0, Flooding Design Basis Update
557375  
Individual Plant Examination for External Events Submittal, June 1995
555023  
Link Seal Vendor Manual
545354  
Quick Hit Self-Assessment 541666-15, Emergency Action Level Functionality
553946  
SD-43, Service Water System
URS List of Flood Features Inspected
Work Orders  
URS Near Term Force Recommendations 2.3: Flooding, Project Number 30703-007
550098  
Section 1R04: Equipment Alignment
550100  
Procedures
550102  
Procedure 2OP-18, Core Spray System Operating Procedure
550015  
1OP-17, RHR System Operating Procedure
545859  
2OP-10, Standby Gas Treatment System Operating Procedure
545861  
                                                                                  Attachment
1828825  
1828826  
1643223  
1775054  
Drawings  
D-02778, Reactor Building Floor and Wall Sleeves Tabulation - Sheet No 1 Unit No 2  
D-02779, Reactor Building Floor and Wall Sleeves Tabulation and Details - Sheet No 2  
D-11597, Backdraft Damper with Extra Deep Frame  
F-0424, Service Water Intake Structure Units 1 & 2 Ventilation System & Drainage Piping  
LL-FB-02103, Reactor Building, Elevation -170, Fire Barrier Penetrations, RHR-HPCI Room  
North Wall  
Miscellaneous
0PIC-LS001, Omnitrol (Valrec) Level Control Switch Model 613, Single Actuator
DBD-106, Hazards Analysis  
Engineering Change 80408R0, Flooding Design Basis Update  
Individual Plant Examination for External Events Submittal, June 1995  
Link Seal Vendor Manual
Quick Hit Self-Assessment 541666-15, Emergency Action Level Functionality
SD-43, Service Water System  
URS List of Flood Features Inspected
URS Near Term Force Recommendations 2.3: Flooding, Project Number 30703-007  
Section 1R04: Equipment Alignment  
Procedures  
Procedure 2OP-18, Core Spray System Operating Procedure  
1OP-17, RHR System Operating Procedure  
2OP-10, Standby Gas Treatment System Operating Procedure  


                                              4
4  
Drawings
D-25024, Reactor Building Core Spray System Piping Diagram
Attachment
9527-D-2025, sheets 1A and 1B, RHR System, Unit 1
Drawings  
F-04073, Reactor Building Standby Gas Treatment Piping Diagram
D-25024, Reactor Building Core Spray System Piping Diagram  
Miscellaneous
9527-D-2025, sheets 1A and 1B, RHR System, Unit 1  
DBD-10, Design Basis Document Standby Gas Treatment System
F-04073, Reactor Building Standby Gas Treatment Piping Diagram  
SD-10, System Description Standby Gas Treatment System
Section 1R05: Fire Protection
Miscellaneous
Procedures
DBD-10, Design Basis Document Standby Gas Treatment System  
0FPP-014, Control of Combustible, Transient Fire Loads, and Ignition Sources
SD-10, System Description Standby Gas Treatment System  
0PFP-CB, Control Building Pre-Fire Plans
OPLP-01, Fire Protection Program Document
Section 1R05: Fire Protection  
OPLP-01.2, Fire Protection System Operability, Action, and Surveillance Requirements
0PFP-013, General Fire Plan
Procedures  
1PFP-RB, Reactor Building Pre-Fire Plans Unit 1
0FPP-014, Control of Combustible, Transient Fire Loads, and Ignition Sources  
2PFP-RB, Reactor Building Prefire Plans Unit 2
0PFP-CB, Control Building Pre-Fire Plans  
OPT-34.11.2.0, Portable Fire Extinguisher Inspection
OPLP-01, Fire Protection Program Document  
1PFP-TB, Turbine Building Prefire plans
OPLP-01.2, Fire Protection System Operability, Action, and Surveillance Requirements  
Section 1R06: Flood Protection
0PFP-013, General Fire Plan  
Nuclear Condition Reports
1PFP-RB, Reactor Building Pre-Fire Plans Unit 1  
490292
2PFP-RB, Reactor Building Prefire Plans Unit 2  
Drawings
OPT-34.11.2.0, Portable Fire Extinguisher Inspection  
F-03347, East Yard Area - Units No. 1 & 2 Electrical Underground Duct Runs Manholes
1PFP-TB, Turbine Building Prefire plans  
F-03343, East Yard Area - Units No. 1 & 2 Electrical Underground Duct Runs Plan
Section 1R07: Heat Sink Performance
Section 1R06: Flood Protection  
Procedures
0ENP-2704, Administrative Control of NRC Generic Letter 89-13 Requirements
Nuclear Condition Reports  
0ENP-2705, Service Water Heat Exchanger Thermal Performance Testing
490292  
0PM-ACU500, Inspection and Cleaning of the RHR/Core Spray Room Aerofin Cooler Air Filters
      and Coolers
Drawings  
0PM-STU500, Service Water Intake Structure Inspection and Cleaning
F-03347, East Yard Area - Units No. 1 & 2 Electrical Underground Duct Runs Manholes  
0CM-ENG521, Perfex Cooler Inspection and Repair
F-03343, East Yard Area - Units No. 1 & 2 Electrical Underground Duct Runs Plan  
0E&RC-3212, Service/Circulating Water Chlorine Sampling
1PM-MEC502, Nuclear Service Water Header Inspection
Section 1R07: Heat Sink Performance  
1PM-MEC506, Conventional Service Water Header Inspection
2PM-MEC501, Nuclear Service Water Header Inspection
Procedures  
2PM-MEC505, Conventional Service Water Header Inspection
0ENP-2704, Administrative Control of NRC Generic Letter 89-13 Requirements  
0PT-08.1.4a, RHR Service Water System Operability Test - Loop A
0ENP-2705, Service Water Heat Exchanger Thermal Performance Testing  
0AOP-18.0, Nuclear Service Water system Failure
0PM-ACU500, Inspection and Cleaning of the RHR/Core Spray Room Aerofin Cooler Air Filters  
0AOP-19-0, Conventional Service Water System Failure
and Coolers  
                                                                                  Attachment
0PM-STU500, Service Water Intake Structure Inspection and Cleaning  
0CM-ENG521, Perfex Cooler Inspection and Repair  
0E&RC-3212, Service/Circulating Water Chlorine Sampling  
1PM-MEC502, Nuclear Service Water Header Inspection  
1PM-MEC506, Conventional Service Water Header Inspection  
2PM-MEC501, Nuclear Service Water Header Inspection  
2PM-MEC505, Conventional Service Water Header Inspection  
0PT-08.1.4a, RHR Service Water System Operability Test - Loop A  
0AOP-18.0, Nuclear Service Water system Failure  
0AOP-19-0, Conventional Service Water System Failure  


                                              5
5  
0AOP-37.1, Intake System Blockages
0O1-03.4, Unit 0 Outside Auxiliary Operator Daily Check Sheets
Attachment
IPT-24.1-1, Service Water Pump and Discharge Valve Operability Test
0AOP-37.1, Intake System Blockages  
0AI-81, Water Chemistry Guidelines
0O1-03.4, Unit 0 Outside Auxiliary Operator Daily Check Sheets  
0A1-86, Service/Circulating Water Treatment Strategic Plan
IPT-24.1-1, Service Water Pump and Discharge Valve Operability Test  
0SMP-SW1500, Sodium Hypochlorite Injection to the SW System
0AI-81, Water Chemistry Guidelines  
Nuclear Condition Reports
0A1-86, Service/Circulating Water Treatment Strategic Plan  
392541       507589         339272         539775       497132         542399
0SMP-SW1500, Sodium Hypochlorite Injection to the SW System  
Work Orders
01582632     01324149
Nuclear Condition Reports  
Drawings
392541  
BN 43.0.01, Service Water System
507589  
Calculations
339272  
OSW-0096, Calculation for Tube Plugging and Fouling of Service Water Safety Related Heat
539775  
      Exchangers
497132  
OSW-0097, RHR and Core Spray Room Cooler Performance
542399  
G0050C-04, Design Basis Heat Loads from Vital Heat Exchangers
Miscellaneous
Work Orders  
LTAM-BNP-12-0009, Formal Water Hammer Analysis for Service Water
01582632  
DBD-43, Service Water System
01324149  
DBD-17, Residual Heat Removal System
System Health Report, Q1-2012, RBCCW Unit 1
Drawings  
System Health Report, Q1-2012, Service Water
BN 43.0.01, Service Water System  
System Health Report, Q1-2012, Emergency Diesel Generators
Program Health Report, Q1-2012, GL 89-13 Program
Calculations  
EC-84365, Temporary Removal of Degraded Coating on Internal Surfaces of Service Water
OSW-0096, Calculation for Tube Plugging and Fouling of Service Water Safety Related Heat
      Pump Discharge Pipe Spools and Elbows
Exchangers  
EC-85258, Replace Nuclear and Conventional Service Water Pump Discharge Elbow
OSW-0097, RHR and Core Spray Room Cooler Performance  
2-E11-B002A, Final Eddy Current Inspection Report for RHR Heat Exchanger 2A,
G0050C-04, Design Basis Heat Loads from Vital Heat Exchangers  
      March 15, 2011
EDG-3-JWC-2010, Final Eddy Current Inspection Report for EDG-3 Jacket Water Cooler
Miscellaneous
      May 18, 2010
LTAM-BNP-12-0009, Formal Water Hammer Analysis for Service Water  
SD-63, Sodium Hypochlorite Injection System
DBD-43, Service Water System  
Procedure Revision Requests
DBD-17, Residual Heat Removal System  
00549906     00549915       00549919       00549920     00549923       00549924
System Health Report, Q1-2012, RBCCW Unit 1  
00550041     00550333
System Health Report, Q1-2012, Service Water  
Section 1R11: Licensed Operator Requalification
System Health Report, Q1-2012, Emergency Diesel Generators  
Procedures
Program Health Report, Q1-2012, GL 89-13 Program  
0PEP-2.1.1, Emergency Control - Notification of Unusual Event, Alert, Site Area Emergency, or
EC-84365, Temporary Removal of Degraded Coating on Internal Surfaces of Service Water  
General Emergency
Pump Discharge Pipe Spools and Elbows  
                                                                                  Attachment
EC-85258, Replace Nuclear and Conventional Service Water Pump Discharge Elbow  
2-E11-B002A, Final Eddy Current Inspection Report for RHR Heat Exchanger 2A,  
March 15, 2011  
EDG-3-JWC-2010, Final Eddy Current Inspection Report for EDG-3 Jacket Water Cooler  
May 18, 2010  
SD-63, Sodium Hypochlorite Injection System  
Procedure Revision Requests  
00549906  
00549915  
00549919  
00549920  
00549923  
00549924  
00550041  
00550333  
Section 1R11: Licensed Operator Requalification  
Procedures  
0PEP-2.1.1, Emergency Control - Notification of Unusual Event, Alert, Site Area Emergency, or  
General Emergency  


                                              6
6  
0PEP-02.1, Initial Emergency Actions
AOP-17, Turbine Building Closed Cooling Water System
Attachment
AOP-19, Conventional Service Water System Failure
0PEP-02.1, Initial Emergency Actions  
EM-78, Nuclear Power Facility Emergency Notification Form
AOP-17, Turbine Building Closed Cooling Water System
ENP-24.5, Reactivity Control Planning
AOP-19, Conventional Service Water System Failure  
2EOP-01-LPC, Level/Power Control
EM-78, Nuclear Power Facility Emergency Notification Form  
2EOP-01-RSP, Reactor Scram Procedure
ENP-24.5, Reactivity Control Planning  
OPS-NGGC-1000, Fleet Conduct of Operations
2EOP-01-LPC, Level/Power Control  
TRN-NGGC-0420, Conduct of Simulator Training and Evaluation
2EOP-01-RSP, Reactor Scram Procedure  
Miscellaneous
OPS-NGGC-1000, Fleet Conduct of Operations  
LORX-IPO-003 Scenario
TRN-NGGC-0420, Conduct of Simulator Training and Evaluation  
Technical Specifications 3.7.1, Residual Heat Removal Service Water System
Technical Specifications 3.7.2.E, Service Water System and Ultimate Heat Sink
Miscellaneous
Section 1R12: Maintenance Effectiveness
LORX-IPO-003 Scenario  
Procedures
Technical Specifications 3.7.1, Residual Heat Removal Service Water System  
1OP-43, Service Water System Operating Procedure
Technical Specifications 3.7.2.E, Service Water System and Ultimate Heat Sink  
MNT-NGGC-0001, Maintenance Rework Program
0PT-06.1, SLC System Operability Test
Section 1R12: Maintenance Effectiveness  
0AOP-36.2, Station Blackout
0PT-12.22, Load Test for SAMA Diesels
Procedures  
ADM-NGGC-0101, Maintenance Rule Program
1OP-43, Service Water System Operating Procedure  
Nuclear Condition Reports
MNT-NGGC-0001, Maintenance Rework Program  
546346       554488         549265       519703       477622         436705
0PT-06.1, SLC System Operability Test  
436703       409663         408997       401149       477561         477622
0AOP-36.2, Station Blackout  
401149
0PT-12.22, Load Test for SAMA Diesels  
Work Orders
ADM-NGGC-0101, Maintenance Rule Program  
1802757       2104000         1868030       1746181
Drawings
Nuclear Condition Reports  
Miscellaneous
546346  
FP-20234, R.P Adams CO, Inc, Strainers, Poro-Edge Automatic
554488  
Technical Specification 3.7.2, Service Water System and Ultimate Heat Sink
549265  
SD-05, Standby Liquid Control System
519703  
Maintenance Rule Unavailability Reports, January 2012 through August 2012
477622  
SAMA Diesels System Health Report, Q2-2012
436705  
Section 1R13: Maintenance Risk Assessment and Emergent Work Control
436703  
Procedures
409663  
0AI-144, Risk Management
408997  
0AP-022, BNP Outage Risk Management
401149  
0AP-025, BNP Integrated Scheduling
477561  
                                                                              Attachment
477622  
401149  
Work Orders  
1802757  
2104000  
1868030  
1746181  
Drawings  
Miscellaneous
FP-20234, R.P Adams CO, Inc, Strainers, Poro-Edge Automatic  
Technical Specification 3.7.2, Service Water System and Ultimate Heat Sink  
SD-05, Standby Liquid Control System
Maintenance Rule Unavailability Reports, January 2012 through August 2012  
SAMA Diesels System Health Report, Q2-2012  
Section 1R13: Maintenance Risk Assessment and Emergent Work Control  
Procedures  
0AI-144, Risk Management  
0AP-022, BNP Outage Risk Management  
0AP-025, BNP Integrated Scheduling  


                                              7
7  
ADM-NGGC-0006, Online EOOS Model
ADM-NGGC-0104, Work Management Process
Attachment
WCP-NGGC-0500, Work Activity Integrated Risk Management Program
ADM-NGGC-0006, Online EOOS Model  
OPS-NGGC-1311, Protected Equipment
ADM-NGGC-0104, Work Management Process  
Nuclear Condition Reports
WCP-NGGC-0500, Work Activity Integrated Risk Management Program  
559242
OPS-NGGC-1311, Protected Equipment  
Miscellaneous
BNP EOOS Risk Assessment
Nuclear Condition Reports  
BNP EOOS Risk Assessment Report for Work Week 36
559242  
Section 1R15: Operability Evaluations
Procedures
0PT-12.2C, No. 3 Diesel Generator Monthly Load Test
Miscellaneous
FP-20322, Diesel Generator Instruction Manual
BNP EOOS Risk Assessment  
OPS-NGGC-1305, Operability Determinations
BNP EOOS Risk Assessment Report for Work Week 36  
OPS-NGGC-1307, Operational Decision making
Nuclear Condition Reports
Section 1R15: Operability Evaluations  
250203       310500       318607         548370         549420     558810
Work Orders
Procedures  
542970
0PT-12.2C, No. 3 Diesel Generator Monthly Load Test  
Drawings
FP-20322, Diesel Generator Instruction Manual  
D-25028, Reactor Building Closed Cooling Water System
OPS-NGGC-1305, Operability Determinations  
F-09348, Diesel Generator No. 4 Circuits Control Wiring Diagram
OPS-NGGC-1307, Operational Decision making  
Miscellaneous
EDG 1-4 Generator Bearing Oil Analysis
Nuclear Condition Reports  
SD-39, Emergency Diesel Generators
250203  
Section 1R18: Plant Modifications
310500  
Procedures
318607  
EGR-NGGC-0028 Engineering Evaluation
548370  
0AI-68 Brunswick Nuclear Plant Response to Severe Weather Warnings
549420
Engineering Changes
558810  
EC 88431, Service Water Building Drain Hub Baffle Plate Installation
EC 86304, Design Leak Tight Barriers at Reactor Bldg Rattle Spaces
Work Orders  
Nuclear Condition Reports
542970  
559173       490292
                                                                            Attachment
Drawings  
D-25028, Reactor Building Closed Cooling Water System  
F-09348, Diesel Generator No. 4 Circuits Control Wiring Diagram  
Miscellaneous
EDG 1-4 Generator Bearing Oil Analysis  
SD-39, Emergency Diesel Generators  
Section 1R18: Plant Modifications  
Procedures  
EGR-NGGC-0028 Engineering Evaluation  
0AI-68 Brunswick Nuclear Plant Response to Severe Weather Warnings  
Engineering Changes  
EC 88431, Service Water Building Drain Hub Baffle Plate Installation  
EC 86304, Design Leak Tight Barriers at Reactor Bldg Rattle Spaces  
Nuclear Condition Reports  
559173  
490292  


                                              8
8  
Drawings
D-02041, Service Water System Piping Diagram
Attachment
F-04024, Service Water Intake Structure Ventilation System & Draining Piping
Drawings  
F-01027, Seismic Isolation Space
D-02041, Service Water System Piping Diagram  
Miscellaneous
F-04024, Service Water Intake Structure Ventilation System & Draining Piping  
UFSAR Updated Final Safety Analysis Report
F-01027, Seismic Isolation Space  
Section 1R19: Post Maintenance Testing
Procedures
Miscellaneous
0PT-08.2.2C, LPCI/RHR System Operability Test
UFSAR Updated Final Safety Analysis Report  
0PT-80.5, Mid-Cycle Maintenance Outage Reactor Pressure Vessel Pressure Test
Nuclear Condition Reports
Section 1R19: Post Maintenance Testing  
551048
Work Orders
Procedures  
1951825       2028895         2034614       2112268
0PT-08.2.2C, LPCI/RHR System Operability Test  
Drawings
0PT-80.5, Mid-Cycle Maintenance Outage Reactor Pressure Vessel Pressure Test  
D-25026, Sheet 2A, Residual Heat Removal System, Unit 1
Miscellaneous
Nuclear Condition Reports  
Technical Specifications 3.5.1, Emergency Core Cooling System - Operating
551048  
Section 1R20: Outage Activities
Procedures
Work Orders  
0GP-01, Prestartup Checklist
1951825  
0GP-02, Approach to Criticality and Pressurization of the Reactor
2028895  
0GP-03, Unit Startup and Synchronization
2034614  
0GP-05, Unit Shutdown
2112268  
0GP-10, Rod Sequence Checkoff Sheets
0AI-127, Primary Containment Inspection and Closeout
Drawings  
0AP-22, BNP Outage Risk Management
D-25026, Sheet 2A, Residual Heat Removal System, Unit 1  
0OI-01-01, BNP Conduct of Operations Supplement
0SP-12-001, EGM 11-003 OPDRV Activities
Miscellaneous  
Nuclear Condition Reports
Technical Specifications 3.5.1, Emergency Core Cooling System - Operating
561831       561899         561173       562188
Drawings
Section 1R20: Outage Activities  
D-20022 Sheet 1, Piping Diagram Extraction Steam System, Unit 1
Miscellaneous
Procedures  
Main Control Room (MCR) Logs
0GP-01, Prestartup Checklist  
Outage Control Center (OCC) Logs
0GP-02, Approach to Criticality and Pressurization of the Reactor  
                                                                            Attachment
0GP-03, Unit Startup and Synchronization  
0GP-05, Unit Shutdown  
0GP-10, Rod Sequence Checkoff Sheets  
0AI-127, Primary Containment Inspection and Closeout  
0AP-22, BNP Outage Risk Management  
0OI-01-01, BNP Conduct of Operations Supplement  
0SP-12-001, EGM 11-003 OPDRV Activities  
Nuclear Condition Reports  
561831  
561899  
561173  
562188  
Drawings  
D-20022 Sheet 1, Piping Diagram Extraction Steam System, Unit 1  
Miscellaneous  
Main Control Room (MCR) Logs  
Outage Control Center (OCC) Logs  


                                              9
9  
Unit 1 Key Safety Function Component Status Sheets
Operations Standing Instruction 12-052
Attachment
Section 1R22: Surveillance Testing
Unit 1 Key Safety Function Component Status Sheets  
Procedures
Operations Standing Instruction 12-052  
0PT-07.2.4a, Core Spray System Operability Test - Loop A
0MST-RHR21Q, CSS and HPCI Hi Drywell Pressure Trip Unit Chan Cal
Section 1R22: Surveillance Testing  
0MST-RCIC42R, RCIC Auto-actuation and Isolation Logic Sys Functional
0PT-12.12D, No. 4 Diesel Generator Monthly Load Test
Procedures  
0PT-08.2.2B, LPCI/RHR System Operability Test - Loop B
0PT-07.2.4a, Core Spray System Operability Test - Loop A  
0PT-80.5, Mid-Cycle Maintenance Outage Reactor Pressure Vessel Pressure Test
0MST-RHR21Q, CSS and HPCI Hi Drywell Pressure Trip Unit Chan Cal  
Nuclear Condition Reports
0MST-RCIC42R, RCIC Auto-actuation and Isolation Logic Sys Functional  
547945
0PT-12.12D, No. 4 Diesel Generator Monthly Load Test  
Work Orders
0PT-08.2.2B, LPCI/RHR System Operability Test - Loop B  
2107649
0PT-80.5, Mid-Cycle Maintenance Outage Reactor Pressure Vessel Pressure Test  
Drawings
D-25024, Reactor Building Core Spray System Piping Diagram
Nuclear Condition Reports  
Miscellaneous
547945  
Technical Specification 3.5.1, Emergency Core Cooling System - Operating
UFSAR Section 6.3.3.7, Lag Times
Work Orders  
Section 1EP6: Drill Evaluation
2107649  
Procedures
0PEP-2.1.1, Emergency Control - Notification of Unusual Event, Alert, Site Area Emergency, or
Drawings  
General Emergency
D-25024, Reactor Building Core Spray System Piping Diagram
0PEP-02.1, Initial Emergency Actions
0PEP-02.6.20, Dose Projection Coordinator
Miscellaneous
0PEP-03.4.8, Offsite Dose Projections for Monitored Releases
Technical Specification 3.5.1, Emergency Core Cooling System - Operating  
2EOP-01-RSP, Reactor Scram Procedure
UFSAR Section 6.3.3.7, Lag Times  
EM-78, Nuclear Power Facility Emergency Notification Form
EMG-NGGC-0002, Offsite-Dose Assessment
Section 1EP6: Drill Evaluation  
OPS-NGGC-1000, Fleet Conduct of Operations
Nuclear Condition Reports
Procedures  
551255       551620         551698       552439
0PEP-2.1.1, Emergency Control - Notification of Unusual Event, Alert, Site Area Emergency, or  
Section 4OA1: Performance Indicator Verification
General Emergency  
Procedures
0PEP-02.1, Initial Emergency Actions  
0E&RC-1006, Operation of the Reactor Building Sample Stations
0PEP-02.6.20, Dose Projection Coordinator  
0E&RC-2212, Calibration/Operation of Genie Gamma Spectroscopy System
0PEP-03.4.8, Offsite Dose Projections for Monitored Releases  
REG-NGGC-0009, NRC Performance Indicators and Monthly Operating Report Data
2EOP-01-RSP, Reactor Scram Procedure  
                                                                                  Attachment
EM-78, Nuclear Power Facility Emergency Notification Form  
EMG-NGGC-0002, Offsite-Dose Assessment  
OPS-NGGC-1000, Fleet Conduct of Operations  
Nuclear Condition Reports  
551255  
551620  
551698  
552439  
Section 4OA1: Performance Indicator Verification  
Procedures  
0E&RC-1006, Operation of the Reactor Building Sample Stations  
0E&RC-2212, Calibration/Operation of Genie Gamma Spectroscopy System  
REG-NGGC-0009, NRC Performance Indicators and Monthly Operating Report Data  


                                            10
10  
Miscellaneous
BNP-PSA-069, NRC Mitigating System Performance Index (MSPI) Basis Document
Attachment
Unit 1 RHR MSPI Margin Reports, July 2011 to June 2012
Unit 2 RHR MSPI Margin Reports, July 2011 to June 2012
Miscellaneous
Unit 1 RHR MSPI Derivation Reports, July 2011 to June 2012
BNP-PSA-069, NRC Mitigating System Performance Index (MSPI) Basis Document  
Unit 2 RHR MSPI Derivation Reports, July 2011 to June 2012
Unit 1 RHR MSPI Margin Reports, July 2011 to June 2012  
REG-NGGC-0009, Attachment 4 - MSPI Unavailability Data Sheets, July 2011 to June 2012
Unit 2 RHR MSPI Margin Reports, July 2011 to June 2012  
REG-NGGC-0009, Attachment 6 - MSPI Unreliability Data Sheets, July 2011 to June 2012
Unit 1 RHR MSPI Derivation Reports, July 2011 to June 2012  
Section 4OA2: Identification and Resolution of Problems
Unit 2 RHR MSPI Derivation Reports, July 2011 to June 2012  
Procedures
REG-NGGC-0009, Attachment 4 - MSPI Unavailability Data Sheets, July 2011 to June 2012  
CAP-NGGC-0200, Condition Identification and Screening Process
REG-NGGC-0009, Attachment 6 - MSPI Unreliability Data Sheets, July 2011 to June 2012  
CAP-NGGC-0205, Condition Evaluation and Corrective Action Process
CAP-NGGC-0206, Performance Assessment and Trending
Section 4OA2: Identification and Resolution of Problems  
OERP, Radiological Emergency Response Plan
OPLP-37, Equipment Important to Emergency Preparedness and ERO Response
Procedures  
OPEP-02.6.21, Emergency Communicator
CAP-NGGC-0200, Condition Identification and Screening Process  
OPEP-04.2, Emergency Facilities and Equipment
CAP-NGGC-0205, Condition Evaluation and Corrective Action Process  
ADM-NGGC-0119, Nuclear Safety Culture Program, Revision 01
CAP-NGGC-0206, Performance Assessment and Trending  
Nuclear Condition Reports
OERP, Radiological Emergency Response Plan  
AR 00201153, Adverse Trend - Failed ERFIS Multiplexer Modules
OPLP-37, Equipment Important to Emergency Preparedness and ERO Response  
ACE CR 542704, UPS-A Failure and Loss of ERFIS, PPC, Business Network
OPEP-02.6.21, Emergency Communicator  
Miscellaneous
OPEP-04.2, Emergency Facilities and Equipment  
Down Time by Computer System Log
ADM-NGGC-0119, Nuclear Safety Culture Program, Revision 01  
NIT Key performance indicators
ESR 98-00436, RAINS 99-0045, 50.59 Evaluation
Nuclear Condition Reports  
ESR 98-00436, RAINS 99-0045, 50.54q Evaluation
AR 00201153, Adverse Trend - Failed ERFIS Multiplexer Modules  
Section 4OA3: Event Followup
ACE CR 542704, UPS-A Failure and Loss of ERFIS, PPC, Business Network  
Procedures
0PT-09.2, HPCI System Operability Test
Miscellaneous
0PT-09.3, HPCI System - 165 PSIG Flow Test
Down Time by Computer System Log  
ADM-NGGC-0107, Equipment Reliability Process Guideline
NIT Key performance indicators  
0PEP-02.1, Initial Emergency Actions
ESR 98-00436, RAINS 99-0045, 50.59 Evaluation  
0PEP-02.1.1, Emergency Control - Notification of Unusual Event, Alert, Site Area Emergency,
ESR 98-00436, RAINS 99-0045, 50.54q Evaluation  
        and General Emergency
0PEP-02.2.1, Emergency Action Level Bases
Section 4OA3: Event Followup  
Nuclear Condition Reports
534364       552815       552984
Procedures  
Work Orders
0PT-09.2, HPCI System Operability Test  
2107224       2107264       2107271       2107313
0PT-09.3, HPCI System - 165 PSIG Flow Test  
                                                                                  Attachment
ADM-NGGC-0107, Equipment Reliability Process Guideline  
0PEP-02.1, Initial Emergency Actions  
0PEP-02.1.1, Emergency Control - Notification of Unusual Event, Alert, Site Area Emergency,  
and General Emergency  
0PEP-02.2.1, Emergency Action Level Bases  
Nuclear Condition Reports  
534364  
552815  
552984  
Work Orders  
2107224  
2107264  
2107271  
2107313  


                                                11
11  
Drawings
1-FP-02039, General Electric Gas Control Piping Diagram
Attachment
D-02055, Piping Diagram, Carbon Dioxide & Hydrogen Systems, Units 1 & 2
Miscellaneous
Drawings  
10 CFR 50.72 Event Report 47893, High Pressure Coolant Injection Inoperable due to Erratic
1-FP-02039, General Electric Gas Control Piping Diagram  
      Governor Operation, May 2, 2012
D-02055, Piping Diagram, Carbon Dioxide & Hydrogen Systems, Units 1 & 2  
LER 1-2012-004-00, High Pressure Coolant Injection Inoperable due to Erratic Governor
      Operation, June 29, 2012
Miscellaneous
System Description 19, High Pressure Coolant Injection System
10 CFR 50.72 Event Report 47893, High Pressure Coolant Injection Inoperable due to Erratic  
Technical Specification 3.5.1, Emergency Core Cooling Systems and Reactor Core Isolation
Governor Operation, May 2, 2012  
      Cooling
LER 1-2012-004-00, High Pressure Coolant Injection Inoperable due to Erratic Governor  
Event Notification, Discovery of a Condition that Met the EAL Classification of an Unusual Event
Operation, June 29, 2012  
      (After-the-Fact), August 2, 2012
System Description 19, High Pressure Coolant Injection System  
NUREG-1022, Event Reporting Guidelines
Technical Specification 3.5.1, Emergency Core Cooling Systems and Reactor Core Isolation  
Operator Logs, August 2, 2012
Cooling  
SD-59, Hydrogen Water Chemistry System
Event Notification, Discovery of a Condition that Met the EAL Classification of an Unusual Event  
Section 4OA5: Other Activities
(After-the-Fact), August 2, 2012  
Procedures
NUREG-1022, Event Reporting Guidelines  
EGR-NGGC-0209, Buried Piping Program, Rev. 3
Operator Logs, August 2, 2012  
EGR-NGGC-0513, License Renewal Buried Piping and Tanks Inspection Program, Rev. 3
SD-59, Hydrogen Water Chemistry System  
0AOP-13.0, Operation During Hurricane, Flood Conditions, Tornado, or Earthquake
0PEP-02.6, Severe Weather
Section 4OA5: Other Activities  
2APP-UA-01, Annunciator Procedure for Panel UA-01
2APP-UA-28, Annunciator Procedure for Panel UA-28
Procedures  
2OP-43, Service Water System Operating Procedure
EGR-NGGC-0209, Buried Piping Program, Rev. 3  
OPS-NGGC-1305, Operability Determinations
EGR-NGGC-0513, License Renewal Buried Piping and Tanks Inspection Program, Rev. 3  
MNT-NGGC-004, Scaffolding Control
0AOP-13.0, Operation During Hurricane, Flood Conditions, Tornado, or Earthquake  
0PT-34.2.2.1, Fire Door, Pressure Boundary Door, ASSD Access/Egress Door, and Severe
0PEP-02.6, Severe Weather  
      Weather/Flood Control Door Inspections
2APP-UA-01, Annunciator Procedure for Panel UA-01  
0AI-68, Brunswick Nuclear Plant Response to Severe Weather Warnings
2APP-UA-28, Annunciator Procedure for Panel UA-28  
0PEP-02.1.1, Emergency Control-Notification of Unusual Event, Alert, Site Area Emergency,
2OP-43, Service Water System Operating Procedure  
      and General Emergency
OPS-NGGC-1305, Operability Determinations  
0PEP-02.6, Severe Weather
MNT-NGGC-004, Scaffolding Control  
0AOP-13.0, Operation During Hurricane, Flood Conditions, Tornado, or Earthquake
0PT-34.2.2.1, Fire Door, Pressure Boundary Door, ASSD Access/Egress Door, and Severe  
Nuclear Condition Reports
Weather/Flood Control Door Inspections  
551646         551838         551964         550469       559173         556860
0AI-68, Brunswick Nuclear Plant Response to Severe Weather Warnings  
556861         556862         556863         556864       556865         556866
0PEP-02.1.1, Emergency Control-Notification of Unusual Event, Alert, Site Area Emergency,  
556867         556868         556869         556870       557375         555023
and General Emergency  
545354         553946
0PEP-02.6, Severe Weather  
Work Orders
0AOP-13.0, Operation During Hurricane, Flood Conditions, Tornado, or Earthquake  
550098         550100         550102         550015       545859         545861
1828825               11828826     1643223       1775054       2113607
Nuclear Condition Reports  
                                                                                      Attachment
551646  
551838  
551964  
550469  
559173  
556860  
556861  
556862  
556863  
556864  
556865  
556866  
556867  
556868  
556869  
556870  
557375  
555023  
545354  
553946  
Work Orders  
550098  
550100  
550102  
550015  
545859  
545861  
1828825  
11828826  
1643223  
1775054  
2113607  


                                              12
12  
Work Requests
546632         546540         546541       546543         544971       546174
Attachment
546823         546824         546203       546274         546278
Drawings
Work Requests  
D-11099, Reactor Building Miscellaneous Steel Pool Liners
546632  
D-2274, Diesel Cooling Water
546540  
D-25049, Reactor Building Piping Diagram Fuel Pool Cooling & Filtering System, Unit 1
546541  
D-26007, Reactor Building Fuel Pool Cooling & Filter System Plan EL 80-0 & Sections
546543  
D-26009, Reactor Building Fuel Pool Cooling & Filter System Miscellaneous Plans & Sections
544971  
D-27010, Supplemental Spent Fuel Pool Cooling System
546174  
F-25008, Reactor Building Arrangement & Details, Fuel Pool
546823  
D-02778, Reactor Building Floor and Wall Sleeves Tabulation - Sheet No 1 Unit No 2
546824  
D-02779, Reactor Building Floor and Wall Sleeves Tabulation and Details - Sheet No 2
546203  
D-11597, Backdraft Damper with Extra Deep Frame
546274  
F-0424, Service Water Intake Structure Units 1 & 2 Ventilation System & Drainage Piping
546278  
LL-FB-02103, Reactor Building, Elevation -170, Fire Barrier Penetrations, RHR-HPCI Room
        North Wall
Drawings  
1-FP-09319, Reactor Building Railroad Doors
D-11099, Reactor Building Miscellaneous Steel Pool Liners  
Corrective Action Document
D-2274, Diesel Cooling Water  
PRR 562261, Revise EGR-NGGC-0209 to strengthen the tie to the License Renewal Program
D-25049, Reactor Building Piping Diagram Fuel Pool Cooling & Filtering System, Unit 1  
Miscellaneous
D-26007, Reactor Building Fuel Pool Cooling & Filter System Plan EL 80-0 & Sections  
Calculation 2RB2-0012, Analysis for Spent Fuel Pool - Elevation of Top of Active Fuel
D-26009, Reactor Building Fuel Pool Cooling & Filter System Miscellaneous Plans & Sections  
Engineering Change 80408R0, Flooding Design Basis Update
D-27010, Supplemental Spent Fuel Pool Cooling System  
EPRI Report 1025286, Seismic Walk-down Guidance for Resolution of Fukushima Near-Term
F-25008, Reactor Building Arrangement & Details, Fuel Pool  
        Task Force Recommendation 2.3: Seismic
D-02778, Reactor Building Floor and Wall Sleeves Tabulation - Sheet No 1 Unit No 2  
FP-75090, International Instruments INC, Instruments, Switchboard, Edgewise
D-02779, Reactor Building Floor and Wall Sleeves Tabulation and Details - Sheet No 2  
System Description SD-43, Service Water System
D-11597, Backdraft Damper with Extra Deep Frame  
UFSAR Section 9.1.3.3, Fuel Pool Cooling and Cleanup System, Safety Evaluation
F-0424, Service Water Intake Structure Units 1 & 2 Ventilation System & Drainage Piping  
Units 1 and 2, Flood Protection Feature 6BL, Service Water Building, 4 Elevation, Pipe
LL-FB-02103, Reactor Building, Elevation -170, Fire Barrier Penetrations, RHR-HPCI Room  
        Penetration Seal\20-8 Pipe Sleeves
North Wall  
Unit 1, SWEL 1 List
1-FP-09319, Reactor Building Railroad Doors  
Unit 1, SWEL 2 List
Unit 2, SWEL 1 List
Corrective Action Document  
Unit 2, SWEL 2 List
PRR 562261, Revise EGR-NGGC-0209 to strengthen the tie to the License Renewal Program  
URS Post Fukushima Project, NTTF Recommendation 2.3 Seismic Walk-down Training Record
Miscellaneous
Calculation 2RB2-0012, Analysis for Spent Fuel Pool - Elevation of Top of Active Fuel  
Engineering Change 80408R0, Flooding Design Basis Update  
EPRI Report 1025286, Seismic Walk-down Guidance for Resolution of Fukushima Near-Term  
Task Force Recommendation 2.3: Seismic  
FP-75090, International Instruments INC, Instruments, Switchboard, Edgewise  
System Description SD-43, Service Water System  
UFSAR Section 9.1.3.3, Fuel Pool Cooling and Cleanup System, Safety Evaluation  
Units 1 and 2, Flood Protection Feature 6BL, Service Water Building, 4 Elevation, Pipe  
Penetration Seal\\20-8 Pipe Sleeves  
Unit 1, SWEL 1 List  
Unit 1, SWEL 2 List  
Unit 2, SWEL 1 List  
Unit 2, SWEL 2 List  
URS Post Fukushima Project, NTTF Recommendation 2.3 Seismic Walk-down Training Record  
URS Project Number 30703-007, Near Term Task Force Recommendation 2.3 Seismic Walk-
URS Project Number 30703-007, Near Term Task Force Recommendation 2.3 Seismic Walk-
down Procedure
down Procedure  
0PIC-LS001, Omnitrol (Valrec) Level Control Switch Model 613, Single Actuator
0PIC-LS001, Omnitrol (Valrec) Level Control Switch Model 613, Single Actuator
DBD-106, Hazards Analysis
DBD-106, Hazards Analysis  
Engineering Change 80408R0, Flooding Design Basis Update
Engineering Change 80408R0, Flooding Design Basis Update  
Individual Plant Examination for External Events Submittal, June 1995
Individual Plant Examination for External Events Submittal, June 1995  
Link Seal Vendor Manual
Link Seal Vendor Manual
Quick Hit Self-Assessment 541666-15, Emergency Action Level Functionality
Quick Hit Self-Assessment 541666-15, Emergency Action Level Functionality
SD-43, Service Water System
SD-43, Service Water System  
                                                                                    Attachment


                                                13
13  
URS List of Flood Features Inspected
URS Near Term Force Recommendations 2.3: Flooding, Project Number 30703-007
Attachment
Report Number 110311.401, Summary of Progress Energy Fleet Underground Piping and
URS List of Flood Features Inspected
        Tanks with the Scope of NEI 09-14 (Rev. 1), prepared by Structural Integrity Associates,
URS Near Term Force Recommendations 2.3: Flooding, Project Number 30703-007  
        Inc., dated 12/07/2011
Report Number 110311.401, Summary of Progress Energy Fleet Underground Piping and  
Assessment Number 531636, Quick Hit Self Assessment for HNP and BNP Buried Piping
Tanks with the Scope of NEI 09-14 (Rev. 1), prepared by Structural Integrity Associates,  
        Program and the NRC TI-2515/182 Inspection, 08/15/2012
Inc., dated 12/07/2011  
Specification 024-001 for Special Doors
Assessment Number 531636, Quick Hit Self Assessment for HNP and BNP Buried Piping  
Section 4OA7: Licensee-Identified Violations
Program and the NRC TI-2515/182 Inspection, 08/15/2012  
Procedures
Specification 024-001 for Special Doors  
0PEP-02.1, Initial Emergency Actions
0PEP-02.1.1, Emergency Control - Notification of Unusual Event, Alert, Site Area Emergency,
Section 4OA7: Licensee-Identified Violations  
        and General Emergency
0PEP-02.2.1, Emergency Action Level Bases
Procedures  
Nuclear Condition Reports
0PEP-02.1, Initial Emergency Actions  
552815         552984
0PEP-02.1.1, Emergency Control - Notification of Unusual Event, Alert, Site Area Emergency,  
Drawings
and General Emergency  
1-FP-02039, General Electric Gas Control Piping Diagram
0PEP-02.2.1, Emergency Action Level Bases  
D-02055, Piping Diagram, Carbon Dioxide & Hydrogen Systems, Units 1 & 2
Miscellaneous
Nuclear Condition Reports  
Event Notification, Discovery of a Condition that Met the EAL Classification of an Unusual Event
552815  
        (After-the-Fact), August 2, 2012
552984  
NUREG-1022, Event Reporting Guidelines
Operator Logs, August 2, 2012
Drawings  
1-FP-02039, General Electric Gas Control Piping Diagram  
D-02055, Piping Diagram, Carbon Dioxide & Hydrogen Systems, Units 1 & 2  
Miscellaneous
Event Notification, Discovery of a Condition that Met the EAL Classification of an Unusual Event  
(After-the-Fact), August 2, 2012  
NUREG-1022, Event Reporting Guidelines  
Operator Logs, August 2, 2012  
SD-59, Hydrogen Water Chemistry System
SD-59, Hydrogen Water Chemistry System
                                                                                      Attachment
}}
}}

Latest revision as of 21:15, 11 January 2025

IR 05000325-12-004, 05000324-12-004; 07/01/12 - 09/30/12; Brunswick Steam Electric Plant, Units 1 & 2; Refueling and Other Outage Activities, Identification and Resolution of Problems
ML12312A082
Person / Time
Site: Brunswick  
Issue date: 11/07/2012
From: Randy Musser
NRC/RGN-II/DRP/RPB4
To: Annacone M
Carolina Power & Light Co
Shared Package
ML12325A266 List:
References
IR-12-004
Download: ML12312A082 (45)


See also: IR 05000324/2012004

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

245 PEACHTREE CENTER AVENUE NE, SUITE 1200

ATLANTA, GEORGIA 30303-1257

November 7, 2012

Mr. Michael J. Annacone

Vice President

Brunswick Steam Electric Plant

P.O. Box 10429

Southport, NC 28461-0429

SUBJECT:

BRUNSWICK STEAM ELECTRIC PLANT - NRC INTEGRATED INSPECTION

REPORT NOS.: 05000325/2012004 AND 05000324/2012004

Dear Mr. Annacone:

On September 30, 2012, the U.S. Nuclear Regulatory Commission (NRC) completed an

inspection at your Brunswick Unit 1 and 2 facilities. The enclosed integrated inspection report

documents the inspection findings, which were discussed on October 11, 2012, with you and

other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

One NRC-identified and one self-revealing finding of very low safety significance (Green) were

identified during this inspection. These findings were determined to involve a violation of NRC

requirements. Further, two licensee-identified violations were determined to be of very low

safety significance and are listed in this report. The NRC is treating these findings as non-cited

violations (NCVs) consistent with Section 2.3.2 of the Enforcement Policy.

If you contest the violations or the significance of these NCVs, you should provide a response

within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear

Regulatory Commission, ATTN.: Document Control Desk, Washington DC 20555-0001; with

copies to the Regional Administrator Region II; the Director, Office of Enforcement, United

States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident

Inspector at the Brunswick Steam Electric Plant.

If you disagree with the cross-cutting aspect assignment in this report, you should provide a

response within 30 days of the date of this inspection report, with the basis for your

disagreement, to the Regional Administrator, Region II, and the NRC Resident Inspector at the

Brunswick Steam Electric Plant.

M. Annacone

2

In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter, its

enclosure, and your response (if any) will be available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records (PARS) component of

NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Randall A. Musser, Chief

Reactor Projects Branch 4

Division of Reactor Projects

Docket Nos.: 50-325, 50-324

License Nos.: DPR-71, DPR-62

Enclosure:

Inspection Report 05000325, 324/2012004

w/Attachment: Supplemental Information

cc w/encl:

(See page 3)

M. Annacone

2

In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter, its

enclosure, and your response (if any) will be available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records (PARS) component of

NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Randall A. Musser, Chief

Reactor Projects Branch 4

Division of Reactor Projects

Docket Nos.: 50-325, 50-324

License Nos.: DPR-71, DPR-62

Enclosure:

Inspection Report 05000325, 324/2012004

w/Attachment: Supplemental Information

cc w/encl:

(See page 3)

x PUBLICLY AVAILABLE

G NON-PUBLICLY AVAILABLE

G SENSITIVE

x NON-SENSITIVE

ADAMS: x Yes

ACCESSION NUMBER:ML12312A082_________________

x SUNSI REVIEW COMPLETE x FORM 665 ATTACHED

OFFICE

RII:DRP

RII:DRP

RII:DRP

RII:DRP

RII:DRP

RII:DRP

RII:DRP

SIGNATURE

JSD: /RA/

RAM RA for

MPS

Via e-mail

Via e-mail

Via e-mail

Via e-mail

JGW: /RA/

NAME

JDodson

MCatts

MSchwieg

PNiebaum

LLake

MEndress

JWorosilo

DATE

10/24/2012

11/07/2012

10/24/2012

10/29/2012

10/26/2012

10/25/2012

10/15/2012

E-MAIL COPY?

YES

NO

YES

NO YES

NO

YES

NO

YES

NO YES

NO

YES

NO

OFFICE

RII:DRP

RII:DRS

SIGNATURE

RAM: /RA/

Via e-mail

NAME

RMusser

MSpeck

DATE

11/7/2012

11/06/2012

E-MAIL COPY?

YES

NO

YES

NO

OFFICIAL

RECORD

COPY DOCUMENT

NAME:

G:\\DRPII\\RPB4\\BRUNSWICK\\REPORTS\\2012

REPORTS\\12-

04\\BRUNSWICK IIR 2012004.DOCX

M. Annacone

3

cc w/encl:

Plant General Manager

Brunswick Steam Electric Plant

Progress Energy

Electronic Mail Distribution

Edward L. Wills, Jr.

Director Site Operations

Brunswick Steam Electric Plant

Electronic Mail Distribution

J. W. (Bill) Pitesa

Senior Vice President

Nuclear Operations

Duke Energy Corporation

Electronic Mail Distribution

John A. Krakuszeski

Plant Manager

Brunswick Steam Electric Plant

Electronic Mail Distribution

Lara S. Nichols

Deputy General Counsel

Duke Energy Corporation

Electronic Mail Distribution

M. Christopher Nolan

Director - Regulatory Affairs

General Office

Duke Energy Corporation

Electronic Mail Distribution

Michael J. Annacone

Vice President

Brunswick Steam Electric Plant

Electronic Mail Distribution

Annette H. Pope

Manager-Organizational Effectiveness

Brunswick Steam Electric Plant

Electronic Mail Distribution

Lee Grzeck

Regulatory Affairs Manager

Brunswick Steam Electric Plant

Progress Energy Carolinas, Inc.

Electronic Mail Distribution

Randy C. Ivey

Manager, Nuclear Oversight

Brunswick Steam Electric Plant

Progress Energy Carolinas, Inc.

Electronic Mail Distribution

Paul E. Dubrouillet

Manager, Training

Brunswick Steam Electric Plant

Electronic Mail Distribution

Joseph W. Donahue

Vice President

Nuclear Oversight

Progress Energy

Electronic Mail Distribution

Senior Resident Inspector

U.S. Nuclear Regulatory Commission

Brunswick Steam Electric Plant

U.S. NRC

8470 River Road, SE

Southport, NC 28461

John H. O'Neill, Jr.

Shaw, Pittman, Potts & Trowbridge

2300 N. Street, NW

Washington, DC 20037-1128

Peggy Force

Assistant Attorney General

State of North Carolina

P.O. Box 629

Raleigh, NC 27602

(cc w/encl - continued)

M. Annacone

4

cc w/encl contd:

Chairman

North Carolina Utilities Commission

Electronic Mail Distribution

Robert P. Gruber

Executive Director

Public Staff - NCUC

4326 Mail Service Center

Raleigh, NC 27699-4326

Anthony Marzano

Director

Brunswick County Emergency Services

Electronic Mail Distribution

Public Service Commission

State of South Carolina

P.O. Box 11649

Columbia, SC 29211

W. Lee Cox, III

Section Chief

Radiation Protection Section

N.C. Department of Environmental Commerce & Natural Resources

Electronic Mail Distribution

Warren Lee

Emergency Management Director

New Hanover County

Department of Emergency Management

230 Government Center Drive

Suite 115

Wilmington, NC 28403

M. Annacone

5

Letter to Michael J. Annacone from Randall A. Musser dated November 7, 2012

SUBJECT:

BRUNSWICK STEAM ELECTRIC PLANT - NRC INTEGRATED INSPECTION

REPORT NOS.: 05000325/2012004 AND 05000324/2012004

Distribution w/encl:

J. Baptist, RII EICS

L. Douglas, RII EICS

OE Mail (email address if applicable)

RIDSNRRDIRS

PUBLIC

R. Pascarelli, NRR ((Regulatory Conferences Only))

RidsNrrPMBrunswick Resource

Enclosure

U. S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos.:

50-325, 50-324

License Nos.:

DPR-71, DPR-62

Report Nos.:

05000325/2012004, 05000324/2012004

Licensee:

Carolina Power and Light (CP&L)

Facility:

Brunswick Steam Electric Plant, Units 1 & 2

Location:

8470 River Road, SE

Southport, NC 28461

Dates:

July 1, 2012 through September 30, 2012

Inspectors:

M. Catts, Senior Resident Inspector

M. Schwieg, Resident Inspector

P. Niebaum, Acting Senior Resident Inspector

J. Dodson, Senior Project Engineer (1R04, 1R05, 4OA2)

L. Lake, Senior Reactor Inspector (4OA5)

M. Endress, Reactor Inspector (1R07)

Approved by:

Randall A. Musser, Chief

Reactor Projects Branch 4

Division of Reactor Projects

SUMMARY OF FINDINGS

IR 05000325/2012004, 05000324/2012004; 07/01/12 - 09/30/12; Brunswick Steam Electric

Plant, Units 1 & 2; Refueling and Other Outage Activities, Identification and Resolution of

Problems

This report covers a three-month period of inspection by resident inspectors and announced

baseline inspections by regional inspectors. Two Green findings were identified by the

inspectors. The significance of most findings is indicated by their color (Green, White, Yellow,

Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process

(SDP). The cross-cutting aspects were determined using IMC 0310, Components Within the

Cross-Cutting Areas. Findings for which the SDP does not apply may be Green or be assigned

a severity level after NRC management review.

A.

NRC-Identified and Self-Revealing Findings

Cornerstone: Barrier Integrity

Green: The inspectors identified a Green non-cited violation (NCV) of TS 3.6.4.1,

Secondary Containment because the licensee did not maintain secondary containment

operable as required during a maintenance activity considered an operation with a

potential for draining the reactor vessel (OPDRV). Once questioned by the inspectors,

the licensee restored secondary containment, developed an Operation standing

instruction (12-052) to treat the activity as an OPDRV and placed this issue into its

corrective action program (CAP) as AR 562188562188

The failure to maintain secondary containment operable while Unit 1 was in Mode 4 with

an OPDRV in progress was a performance deficiency. The finding was more than minor

because it was associated with the configuration control attribute of the Barrier Integrity

Cornerstone, and adversely affected the cornerstone objective to provide reasonable

assurance that physical design barriers (fuel cladding, reactor coolant system, and

containment) protect the public from radionuclide releases caused by accidents or

events because the Unit 1 secondary containment boundary was not preserved or

maintained. The inspectors evaluated the finding using Inspection Manual Chapter

(IMC) 0609, Attachment 4, Phase 1 - Initial Screening and Characterization of Findings,

which required an analysis using IMC 0609 Appendix G since the reactor was in Mode 4

(cold shutdown). The finding was determined to be of very low safety significance

(Green) according to IMC 0609 Appendix G, Attachment 1, Checklist 6, since a

quantitative assessment (Phase 2 or Phase 3 evaluation) was not required. Specifically,

the inspectors determined that the licensee maintained adequate mitigation capability for

reactor vessel water level inventory and an event did not occur that could be

characterized as a loss of control. The cause of this finding was directly related to the

cross-cutting aspect of Accurate Procedures in the Resources component of the Human

Performance area, because the licensee did not consider the recirculation pump seal

replacement activity to be OPDRV based on procedural guidance that contains

exclusions to what are considered OPDRV activities. H.2(c) (Section 1R20)

3

Cornerstone: Emergency Preparedness

Green: A self-revealing Green NCV of 10 CFR 50.54(q)(2) was identified for the

licensees failure to properly evaluate or consider the impact to emergency response

facilities of design change ESR98-00436 which was implemented in 1999. This resulted

in the loss of Emergency Response Facility Information System (ERFIS), Emergency

Response Data System (ERDS), Safety Parameter Display System (SPDS), and all

displays including radiation monitors for the emergency response facilities. Specifically,

the licensee failed to ensure that adequate emergency response facilities and equipment

were available as required by the Brunswick Nuclear Plant Radiological Emergency

Plan, Section 1.3.1.3 revision 80 and 10 CFR 50.47(b)(8). This issue was captured in the

licensees CAP as AR 542704542704

The licensees failure to properly evaluate or consider the impact to emergency

response facilities of design change ESR98-00436 which was implemented in 1999 was

a performance deficiency. Specifically, the licensee introduced a single point failure

mode which did not meet the design requirements specified in their Design Basis

Document (DBD 60) sections 3.6.7.2 and 3.6.7.3. This resulted in the licensees failure

to ensure that adequate emergency response facilities and equipment were available as

delineated in the Updated Final Safety Analysis Report (UFSAR) Section 7.7.1.9, and

required by the Brunswick Nuclear Plant Radiological Emergency Plan, Section 1.3.1.3,

revision 80, and 10 CFR 50.47(b)(8). The finding was more than minor because it

adversely affected the Emergency Preparedness Cornerstone objective of ensuring that

the licensee was capable of implementing adequate measures to protect the health and

safety of the public in the event of a radiological emergency. Specifically, the Facilities

and Equipment attribute was affected during the time when the ERFIS, ERDS, SPDS,

and all displays including radiation monitors for the emergency response facilities were

degraded, and as a result did not meet 10 CFR 50.47(b)(8) Planning Standard program

element, adequate emergency facilities and equipment to support the emergency

response are provided and maintained. The finding was assessed for significance in

accordance with NRC IMC 0609, Appendix B Emergency Preparedness Significance

Determination Process. Attachment 2 of Appendix B, Failure to Comply Significance

Logic is as follows: Failure to comply; Loss of Risk Significant Planning Standard

Function (RSPS), No; RSPS Degraded Function, No; Loss of Planning Standard

Function, No; the result is a Green finding. The inspectors determined that this resulted

in a very low safety significance finding (Green). No cross-cutting aspect was assigned

to this finding because the performance deficiency occurred more than three years ago

and is not reflective of current plant performance. (Section 4OA2.2)

B.

Licensee-Identified Violations

Violations of very low safety significance that were identified by the licensee have been

reviewed by inspectors. Corrective actions taken or planned by the licensee have been

entered into the licensees CAP. These violations and corrective action tracking

numbers are listed in Section 4OA7 of this report.

REPORT DETAILS

Summary of Plant Status

Unit 1 began the inspection period at rated thermal power (RTP), and operated at or near full

power until July 22, 2012 when reactor power was lowered to 52 percent to clear a fouled

circulating water debris filter and power was returned to RTP on July 23, 2012. On August 3,

2012, power was reduced to 70 percent for a rod sequence exchange and power was returned

to RTP on August 5, 2012. On August 5, 2012, power was reduced to 90 percent for control rod

improvement and power was returned to RTP on the same day. On August 8, 2012, power was

reduced to 65 percent for offsite transmission line work and power was returned to RTP on the

same day. On September 16, 2012, the reactor was shut down for forced outage to replace the

1A and 1B recirculation pump seal assemblies. Reactor startup commenced on September 27,

2012 and the main generator was synchronized to the grid on September 28, 2012. Reactor

power was raised to RTP on September 29, 2012. On September 30, 2012 reactor power was

reduced to 75 percent for a scheduled control rod improvement. Power ascension continued to

RTP for the remainder of the inspection period.

Unit 2 began the inspection period at RTP, and operated at or near full power until August 18,

2012, when power was reduced to 70 percent for a rod sequence exchange and power was

returned to RTP on August 19, 2012. On August 20, 2012, power was reduced to 86 percent

for control rod improvement and power was returned to RTP on August 21, 2012. On August

21, 2012, power was reduced to 94 percent for control rod improvement and power was

returned to RTP on August 21, 2012. On September 29, 2012, reactor power was reduced to

94 percent to support a scheduled rod improvement and returned to RTP later that day and

maintained RTP for the remainder of the inspection period.

1.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection (71111.01 - 1 sample)

External Flooding

a.

Inspection Scope

The inspectors evaluated the design, material condition, and procedures for coping with

the design basis probable maximum flood. The inspectors reviewed the Updated Final

Safety Analysis Report (UFSAR), which depicted the design flood levels and protection

areas containing safety-related equipment, to identify areas that may be affected by

external flooding. The inspectors conducted a site walk-down of the service water

building, to ensure that erected flood protection measures were in accordance with

design specifications. The inspectors reviewed the sealing of equipment below the flood

line, adequacy of watertight doors, drain systems and sumps including check valves,

and maintenance and calibration of flood protection equipment. The inspectors also

reviewed operating procedures for mitigating external flooding during severe weather to

5

determine if the licensee planned or established adequate measures to protect against

external flooding events.

b.

Findings

No findings were identified.

1R04 Equipment Alignment

.1

Quarterly Partial System Walk-downs (71111.04Q - 3 samples)

a.

Inspection Scope

The inspectors performed partial system walk-downs of the following risk-significant

systems:

Unit 2 A train Core Spray (CS) system while B residual heat removal/service

(RHR/SW) was inoperable for a system outage on July 11, 2012;

Unit 1 Reactor Building Closed Cooling Water (RBCCW) on July 27, 2012; and

Unit 1 B Standby Gas Treatment (SBGT) while the A SBGT was inoperable for a

maintenance outage on September 19, 2012.

The inspectors selected these systems based on their risk-significance relative to the

reactor safety cornerstones at the time they were inspected. The inspectors attempted

to identify any discrepancies that could impact the function of the system, and, therefore,

potentially increase risk. The inspectors reviewed applicable operating procedures,

system diagrams, UFSAR, Technical Specification (TS) requirements, outstanding work

orders, condition reports, and the impact of ongoing work activities on redundant trains

of equipment in order to identify conditions that could have rendered the systems

incapable of performing their intended functions. The inspectors also walked down

accessible portions of the systems to verify that system components and support

equipment were aligned correctly and were operable. The inspectors examined the

material condition of the components and observed operating parameters of equipment

to verify that there were no obvious deficiencies. The inspectors also verified that the

licensee had properly identified and resolved equipment alignment problems that could

cause initiating events or impact the capability of mitigating systems or barriers and

entered them into the CAP with the appropriate significance characterization.

b.

Findings

No findings were identified.

.2

Semi-Annual Complete System Walk-down (71111.04S - 1 sample)

a.

Inspection Scope

On September 5, 2012 the inspectors performed a complete system alignment

inspection of the Unit 1 RHR system to verify the functional capability of the system.

This system was selected because it was considered both safety-significant and risk-

6

significant in the licensees probabilistic risk assessment. The inspectors walked down

the system to review mechanical and electrical equipment line-ups, electrical power

availability, system pressure and temperature indications, as appropriate, component

labeling, component lubrication, component and equipment cooling, hangers and

supports, operability of support systems, and to ensure that ancillary equipment or

debris did not interfere with equipment operation. A review of a sample of past and

outstanding work orders (WOs) was performed to determine whether any deficiencies

significantly affected the system function. In addition, the inspectors reviewed the CAP

to ensure that system equipment alignment problems were being identified and

appropriately resolved.

b.

Findings

No findings were identified.

1R05 Fire Protection (71111.05Q - 5 samples)

Quarterly Resident Inspector Tours

a.

Inspection Scope

The inspectors conducted fire protection walk-downs which were focused on availability,

accessibility, and the condition of firefighting equipment in the following risk-significant

plant areas:

Unit 1 and 2 Control Buildings 23' Elevation 1PFP-CB-7;

Unit 1 Reactor Building East 50 Elevation 1PFP-RB1-1h;

Unit 1 Turbine Building South Area 38 Elevation 1PFP-TB1-1k;

Unit 2 Reactor Building 50 Elevation 2PFP-RB2-1h; and

Unit 2 Reactor Building North 2A Core Spray Room 2-PFP-RB2-1b.

The inspectors reviewed areas to assess if the licensee had implemented a fire

protection program that adequately controlled combustibles and ignition sources within

the plant, effectively maintained fire detection and suppression capability, maintained

passive fire protection features in good material condition, and had implemented

adequate compensatory measures for out-of-service, degraded or inoperable fire

protection equipment, systems, or features in accordance with the licensees fire plan.

The inspectors selected fire areas based on their overall contribution to internal fire risk

as documented in the plants Individual Plant Examination of External Events with later

additional insights, their potential to impact equipment which could initiate or mitigate a

plant transient, or their impact on the plants ability to respond to a security event. Using

the documents listed in the attachment, the inspectors verified that fire hoses and

extinguishers were in their designated locations and available for immediate use; that

fire detectors and sprinklers were unobstructed, that transient material loading was

within the analyzed limits; and fire doors, dampers, and penetration seals appeared to

be in satisfactory condition. The inspectors also verified that minor issues identified

during the inspection were entered into the licensees CAP.

7

b.

Findings

No findings were identified.

1R06 Flood Protection Measures (71111.06 - 1 sample)

Annual Review of Cables Located in Underground Bunkers/Manholes

a.

Inspection Scope

The inspectors conducted an inspection of underground bunkers/manholes subject to

flooding that contain cables whose failure could disable risk-significant equipment. The

inspectors performed walk-downs of risk-significant areas, including manhole 2-MH-

7SW, to verify that the cables were not submerged in water, that cables and/or splices

appear intact and to observe the condition of cable support structures. When applicable,

the inspectors verified proper dewatering device (sump pump) operation and verified

level alarm circuits are set appropriately to ensure that the cables will not be submerged.

Where dewatering devices were not installed; the inspectors ensured that drainage was

provided and was functioning properly.

b.

Findings

No findings were identified.

1R07 Heat Sink Performance (71111.07T - 3 samples)

Triennial Review of Heat Sink Performance

a.

Inspection Scope

The inspectors selected the Residual Heat Removal (RHR) Heat Exchanger 2A, Diesel

Generator (DG) 3 Jacket Water Cooler and the Core Spray (CS) Room Cooler 1A,

based on their risk-significance in the licensees probabilistic safety analysis and their

importance to safety-related mitigating system support functions in the NRCs model for

Brunswick Nuclear Power Plant, Units 1 and 2.

For the RHR Heat Exchanger 2A, DG 3 Jacket Water Cooler and the CS Room Cooler

1A, the inspectors reviewed the licensees inspection, maintenance, and monitoring of

biotic fouling and macro-fouling programs, to determine if they were adequate to ensure

proper heat transfer. This was accomplished by determining whether the methods used

were consistent with accepted industry practices. The inspectors also reviewed the

licensees inspection and cleaning activities had established acceptance criteria

consistent with industry standards, and the as-found results were recorded, evaluated,

and appropriately dispositioned to maintain structural integrity.

For the RHR Heat Exchanger 2A, DG 3 Jacket Water Cooler and the CS Room Cooler

1A, the inspectors reviewed the methods and results of heat exchanger performance

inspections. In addition, the inspectors reviewed the condition and operation of the RHR

Heat Exchanger 2A, DG 3 Jacket Water Cooler and the CS Room Cooler 1A to

8

determine if they were consistent with design assumptions in heat transfer calculations

and as described in the USFAR. This included determining whether the number of

plugged tubes was within pre-established limits based on capacity and heat transfer

assumptions. The inspectors also determined whether the licensee evaluated the

potential for water hammer and established adequate controls and operational limits to

prevent heat exchanger degradation due to excessive flow-induced vibration during

operation.

The inspectors determined whether the performance of the ultimate heat sink (UHS)-

Cape Fear River and its subcomponents such as piping, intake screens, pumps, valves,

etc. was appropriately evaluated by tests or other equivalent methods to ensure

availability and accessibility to the in-plant cooling water systems. The inspectors also

reviewed design changes to the service water system and the UHS.

The inspectors reviewed the licensees operation of the service water system and UHS.

This included a review of licensees procedures for a loss of the service water system or

UHS and the verification that instrumentation, which is relied upon for decision-making,

was available and functional. The inspectors also performed a system walk-down on the

service water system to determine whether the licensees assessment on structural

integrity was adequate and interviewed the respective system engineer. For buried or

inaccessible piping, the inspectors reviewed the licensees pipe testing, inspection, and

monitoring program to determine whether structural integrity was ensured and that any

leakage or degradation was appropriately identified and dispositioned by the licensee.

The inspectors performed a system walk-down of the service water intake structure to

determine whether the licensees assessment on structural integrity and component

functionality was adequate. The inspectors also determined whether service water

pump bay silt accumulation was monitored, trended, and maintained at an acceptable

level by the licensee, and that water level instruments were functional and routinely

monitored. The inspectors also determined whether the licensees ability to ensure

functionality during adverse weather conditions was adequate.

The inspectors reviewed condition reports related to the heat exchangers and heat sink

performance issues to determine whether the licensee had an appropriate threshold for

identifying issues and to evaluate the effectiveness of the corrective actions. Records

were also reviewed to verify that the licensee actions were consistent with Generic Letter

(GL) 89-13 licensee commitments, Electric Power Research Institute (EPRI) and other

industry guidelines. These inspection activities constituted three heat sink inspection

samples as defined in IP 71111.07-05.

b.

Findings

No findings were identified.

9

1R11 Licensed Operator Requalification Program (71111.11Q - 2 samples)

.1

Quarterly Review of Licensed Operator Requalification Testing and Training

a.

Inspection Scope

On August 13, 2012, the inspectors observed a crew of licensed operators in the plants

simulator during licensed operator requalification examinations to verify that operator

performance was adequate, evaluators were identifying and documenting crew

performance problems, and to ensure that training was being conducted in accordance

with licensee procedures. The inspectors evaluated the following areas:

licensed operator performance;

crews clarity and formality of communications;

ability to take timely actions in the conservative direction;

prioritization, interpretation, and verification of annunciator alarms;

correct use and implementation of abnormal and emergency procedures;

control board manipulations;

oversight and direction from supervisors; and

ability to identify and implement appropriate TS actions and Emergency Plan actions

and notifications.

The crews performance in these areas was compared to pre-established operator action

expectations and successful critical task completion requirements.

b.

Findings

No findings were identified.

.2

Quarterly Review of Licensed Operator Performance in the Main Control Room

a.

Inspection Scope

Inspectors observed and assessed licensed operator performance in the plant and main

control room, particularly during periods of heightened activity or risk and where the

activities could affect plant safety. Specifically, on September 16th, the inspectors

observed the Unit 1 shutdown and cooldown evolutions leading up to the forced outage

to repair the recirculation pump seals. The inspectors reviewed various licensee policies

and procedures listed in the Attachment.

Operator compliance and use of procedures.

Control board manipulations.

Communication between crew members.

Use and interpretation of plant instruments, indications and alarms.

Use of human error prevention techniques.

Documentation of activities, including initials and sign-offs in procedures.

Supervision of activities, including risk and reactivity management.

Pre-job briefs and crew briefs

10

This activity constituted one License Operator Requalification inspection sample and one

Control Room Observation inspection sample.

b.

Findings

No findings were identified.

1R12 Maintenance Effectiveness (71111.12Q - 3 samples)

a.

Inspection Scope

The inspectors evaluated degraded performance issues involving the following risk-

significant systems:

1B Nuclear Service Water Pump smoking with vibration and strainer leakage on

pump start on June 26, 2012;

2A Standby Liquid Cooling accumulator failure before operability run on September

10, 2012 (AR560026560026; and

Performance (unavailability and unreliability) history of the Severe Accident

Mitigation Alternatives (SAMA) diesels

The inspectors reviewed events where ineffective equipment maintenance may have

resulted in equipment failure or invalid automatic actuations of Engineered Safeguards

Systems and independently verified the licensee's actions to address system

performance or condition problems in terms of the following:

implementing appropriate work practices;

identifying and addressing common cause failures;

scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;

characterizing system reliability issues for performance;

charging unavailability for performance;

trending key parameters for condition monitoring; and

ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or re-classification; and verifying

appropriate performance criteria for structures, systems and components

(SSCs)/functions classified as (a)(2) or appropriate and adequate goals and

corrective actions for systems classified as (a)(1).

The inspectors assessed performance issues with respect to the reliability, availability,

and condition monitoring of the system. In addition, the inspectors verified maintenance

effectiveness issues were entered into the corrective action program with the appropriate

significance characterization.

b.

Findings

No findings were identified.

11

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13 - 4 samples)

a.

Inspection Scope

The inspectors reviewed the licensee's evaluation and management of plant risk for the

maintenance and emergent work activities affecting risk-significant equipment listed

below to verify that the appropriate risk assessments were performed prior to removing

equipment for work:

Unit 2 yellow risk during emergent work on 2-E21-F015A, 2A Core Spray Full Flow

Test Bypass Valve, and scheduled maintenance on 2B RHR/residual heat removal

service water (RHRSW) on July 11, 2012;

Unit 1 yellow risk during 1B Recirculation Pump Variable Frequency Drive power

recovery, and planned maintenance on 1A RHR/RHRSW on July 26, 2012;

Unit 1 yellow risk during planned maintenance on 1B RHR/RHRSW September 4 to

September 6, 2012;

Unit 1 integrated risk during repair of 1B recirculation pump seal September 17 to

September 25, 2012;

These activities were selected based on their potential risk-significance relative to the

reactor safety cornerstones. As applicable for each activity, the inspectors verified that

risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate

and complete. When emergent work was performed, the inspectors verified that the

plant risk was promptly reassessed and managed. The inspectors reviewed the scope

of maintenance work, discussed the results of the assessment with the licensee's

probabilistic risk analyst or shift technical advisor, and verified plant conditions were

consistent with the risk assessment. The inspectors also reviewed TS requirements and

walked down portions of redundant safety systems, when applicable, to verify risk

analysis assumptions were valid and applicable requirements were met.

b.

Findings

No findings were identified.

1R15 Operability Evaluations (71111.15 - 5 samples)

a.

Inspection Scope

The inspectors reviewed the following five issues:

Unit 2 High Pressure Coolant Injection (HPCI) elevated thrust bearing temperature

on July 6, 2012 (AR548370548370;

2D RHRSW Booster pump coupling grease specification evaluation on July 12, 2012

(AR542025542025;

Emergency Diesel Generator (EDG) #3 debris in bearing oil site glass on July 15,

2012 (AR549420549420;

Reactor Building Close Cooling Water (RBCCW) piping corrosion in rattle space on

August 21, 2012 (AR557151557151; and

12

EDG #4 alternate safe shutdown switch contact continuity indications on August 27,

2012 (AR558810558810

The inspectors selected these potential operability issues based on the risk-significance

of the associated components and systems. The inspectors evaluated the technical

adequacy of the evaluations to ensure that TS operability was properly justified and the

subject component or system remained available such that no unrecognized increase in

risk occurred. The inspectors compared the operability and design criteria in the

appropriate sections of the UFSAR and TS to the licensees evaluations, to determine

whether the components or systems were operable. Where compensatory measures

were required to maintain operability, the inspectors determined whether the measures

in place would function as intended and were properly controlled. The inspectors

determined, where appropriate, compliance with bounding limitations associated with the

evaluations. Additionally, the inspectors also reviewed a sampling of corrective action

documents to verify that the licensee was identifying and correcting any deficiencies

associated with operability evaluations.

b.

Findings

No findings were identified.

1R18 Plant Modifications (71111.18 - 2 samples)

a.

Inspection Scope

The inspectors reviewed the two modifications listed below to determine whether the

modifications affected the safety functions of systems that are important to safety. The

inspectors reviewed 10 CFR 50.59 documentation and post-modification testing results

and conducted field walk-downs of the modifications to verify that the modifications did

not degrade the design bases, licensing bases, and performance capability of the

affected systems.

Design leak tight barriers at reactor building rattle spaces (EC86304);

Service water building drain hub baffle plate installation (EC 88431)

b.

Findings

No findings were identified.

1R19 Post Maintenance Testing (71111.19 - 7 samples)

a.

Inspection Scope

The inspectors reviewed the following seven post-maintenance activities to verify that

procedures and test activities were adequate to ensure system operability and functional

capability:

0PT-12.2D, No. 4 Diesel Generator Monthly Load Test after replacement of the 60X

relay on July 23, 2012;

13

0PT-08.1.4B, Residual Heat Removal (RHR) Service Water (SW) System Operability

Test - Unit 2 RHRSW Loop B after the maintenance outage on July 12, 2012;

0PT-08.2.2c, Low Pressure Coolant Injection/RHR System Operability Test - Unit 1

RHR Loop A after the maintenance outage on July 27, 2012;

0PT-12.2C, EDG #3 Operability Test - Unit 2 after repair of jacket water pump on

August 16, 2012;

0PT-15.6, Standby Gas Treatment Operability Test, Unit 1 B after relay replacement

on August 15, 2012;

0PT-10.1.1, Reactor Core Isolation Cooling System Operability Test, Unit 2 after

replacement of Electronic Governor - Magnetic (EGM) on August 23, 2012; and

0PT-80.5, Reactor Pressure Vessel Pressure Test - Unit 1 after repair of 1B

recirculation pump seal on September 26, 2012

These activities were selected based upon the structure, system, or component's ability

to impact risk. The inspectors evaluated these activities for the following, as applicable:

the effect of testing on the plant had been adequately addressed; testing was adequate

for the maintenance performed; acceptance criteria were clear and demonstrated

operational readiness; test instrumentation was appropriate; tests were performed as

written in accordance with properly reviewed and approved procedures; equipment was

returned to its operational status following testing, and test documentation was properly

evaluated. The inspectors evaluated the activities against the UFSAR and TS to ensure

that the test results adequately ensured that the equipment met the licensing basis and

design requirements. In addition, the inspectors reviewed corrective action documents

associated with post-maintenance tests to determine whether the licensee was

identifying problems and entering them in the CAP and that the problems were being

corrected commensurate with their importance to safety.

b.

Findings

No findings were identified.

1R20 Refueling and Other Outage Activities (71111.20 - 1 sample)

Other Outage Activities

a.

Inspection Scope

The inspectors evaluated licensee outage activities for an unscheduled forced outage to

replace the 1B recirculation pump seal assembly. During the outage, the licensee made

the decision to replace the 1A recirculation pump seal assembly to address the potential

extent of cause/condition. The outage began on September 16, 2012 and concluded on

September 28, 2012. The inspectors reviewed activities to ensure that the licensee

considered risk in developing, planning, and implementing the outage schedule.

Additionally, the inspectors observed or reviewed the reactor shutdown and cool down,

outage equipment configuration and risk management, electrical lineups, control and

monitoring of decay heat removal, control of containment activities, performed a drywell

close out inspection, observed reactor startup and heat up activities, and identification

and resolution of problems associated with the outage. Documents reviewed are listed

in the Attachment.

14

b.

Findings

Introduction: The inspectors identified a Green NCV of TS 3.6.4.1, Secondary

Containment because the licensee did not maintain secondary containment operable as

required during an activity considered an operation with a potential for draining the

reactor vessel (OPDRV).

Description: On September 19, 2012, the licensee was replacing the 1B recirculation

pump seal assembly while Unit 1 was in Mode 4 (cold shutdown). In an effort to properly

isolate the work area, the recirculation suction and discharge isolation valves were

tagged closed. Due to seat leakage across the isolation valves, the 1B recirculation

pump drain valve was uncapped and opened to maintain the pump body partially empty

to prevent water from impacting the work area while the pump seal was removed. The

pump drain leakage was sent to the drywell floor drain system. The 1B recirculation

pump seal replacement activity had the potential to drain the reactor vessel below the

top of the fuel because the recirculation loops penetrate the reactor vessel below the top

of active fuel. An OPDRV is described in the licensees technical specifications as an

operation with a potential for draining the reactor vessel. However, the licensee did not

recognize or consider this activity as an OPDRV due to inadequate procedural guidance

that was used to exclude this activity as an OPDRV. Specifically, the licensee adopted

the definition of an OPDRV in procedure 0OI-01.01 as provided in Enforcement

Guidance Memorandum (EGM)11-003 as any activity that could potentially result in

draining or siphoning the RPV water level below the top of the fuel, without taking credit

for mitigating measures. However, section 9.16.15.b.(2) of licensee procedure 0OI-

01.01, BNP Conduct of Operations Supplement, stated leakage through mechanical

joints (for example valve or flange packing leaks, seat leakage through an isolation

valve, flange leakage, etc) is not considered an OPDRV. On September 19, 2012, the

licensee relaxed Unit 1 secondary containment from 03:30 a.m. until 09:20 p.m. by

opening the reactor building air lock doors on the 20-foot elevation to increase ventilation

to the recirculation pump seal replacement work area in the Unit 1 drywell. This resulted

in Secondary Containment inoperability while Unit 1 was in Mode 4 during an OPRDV

activity. The inspectors questioned the licensees Operations staff on the decision to

make secondary containment inoperable during an OPDRV activity. Following this, the

licensee restored secondary containment, developed an Operation standing instruction 12-052 to treat this activity as an OPDRV and placed this issue into its CAP as AR

562188.

Analysis: The inspectors determined that the failure to maintain secondary containment

operable while Unit 1 was in Mode 4 with an OPDRV in progress was a performance

deficiency. The performance deficiency was more than minor because it was associated

with the configuration control attribute of the Barrier Integrity Cornerstone, and adversely

affected the cornerstone objective to provide reasonable assurance that physical design

barriers (fuel cladding, reactor coolant system, and containment) protect the public from

radionuclide releases caused by accidents or events because the Unit 1 secondary

containment boundary was not preserved or maintained. The inspectors evaluated the

finding using Inspection Manual Chapter (IMC) 0609, Attachment 4, Phase 1 - Initial

Screening and Characterization of Findings, which required an analysis using IMC 0609

Appendix G since the reactor was in Mode 4 (cold shutdown). The finding was

determined to be of very low safety significance (Green) according to IMC 0609

15

Appendix G, Attachment 1, Checklist 6, since a quantitative assessment (Phase 2 or

Phase 3 evaluation) was not required. Specifically, the inspectors determined that the

licensee maintained adequate mitigation capability for reactor vessel water level

inventory and an event did not occur that could be characterized as a loss of control.

The cause of this finding was directly related to the cross-cutting aspect of Accurate

Procedures in the Resources component of the Human Performance area, because the

licensee did not consider the recirculation pump seal replacement activity to be OPDRV

based on procedural guidance that contains exclusions to what are considered OPDRV

activities. H.2(c)

Enforcement: Unit 1 TS 3.6.4.1, Secondary Containment, required secondary

containment to be operable during modes one, two, three, during movement of recently

irradiated fuel assemblies in the secondary containment and during operations with a

potential for draining the reactor vessel (OPDRVs). Contrary to the above, on

September 19, 2012, Unit 1 secondary containment was not maintained operable during

an OPDRV activity. The licensee entered this issue in its CAP as AR 562188562188 and

restored secondary containment during the OPDRV activity. Because the licensee

entered the issue into its CAP and the finding is of very low safety significance (Green),

this violation is being treated as an NCV, consistent with Section 2.3.2 of the NRCs

Enforcement Policy: NCV 05000325/2012004-01, Failure to Maintain Secondary

Containment Operable during an OPDRV activity.

1R22 Surveillance Testing

.1

Routine Surveillance Testing (71111.22 - 4 samples)

a.

Inspection Scope

The inspectors either observed surveillance tests or reviewed the test results for the

following activities to verify the tests met TS surveillance requirements, UFSAR

commitments, in-service testing requirements, and licensee procedural requirements.

The inspectors assessed the effectiveness of the tests in demonstrating that the SSCs

were operationally capable of performing their intended safety functions.

0PT-07.2.4A, Core Spray System Operability Test - Loop A on July 5, 2012;

0MST-RHR21Q, RHR-LPCI, CSS and HPCI Hi Drywell Pressure Trip Unit Inst Chan

Cal on July 10, 2012;

0MST-RCIC42R, RCIC Auto-actuation and Isolation Logic Sys Functional on July 24,

2012; and

0PT-12.12D, No. 4 Diesel Generator Monthly Load Test on August 17, 2012;

b.

Findings

No findings were identified.

16

.2

In-Service Testing (IST) Surveillance (71111.22 - 1 sample)

a.

Inspection Scope

The inspectors reviewed the performance of Unit 1 LPCI/RHR System Operability Test -

Loop B on August 9, 2012 to evaluate the effectiveness of the licensees American

Society of Mechanical Engineers (ASME)Section XI testing program for determining

equipment availability and reliability. The inspectors evaluated selected portions of the

following areas: 1) testing procedures, 2) acceptance criteria, 3) testing methods, 4)

compliance with the licensees IST program, TS, selected licensee commitments, and

code requirements, 5) range and accuracy of test instruments, and 6) required corrective

actions.

b.

Findings

No findings were identified.

.3

Reactor Coolant System Leak Detection Inspection Surveillance (71111.22 - 1 sample)

a.

Inspection Scope

The inspectors observed and reviewed the test results for a reactor coolant system leak

detection surveillance, 0PT-80.5, Mid-Cycle Maintenance Outage Reactor Pressure

Vessel Pressure Test, on September 28, 2012. The inspectors observed in-plant

activities and reviewed procedures and associated records to determine whether:

effects of the testing were adequately addressed by control room personnel or engineers

prior to the commencement of the testing; acceptance criteria were clearly stated,

demonstrated operational readiness, and were consistent with the system design basis;

plant equipment calibration was correct, accurate, and properly documented; and the

calibration frequency was in accordance with TSs, the UFSAR, procedures, and

applicable commitments; applicable prerequisites described in the test procedures were

satisfied; test frequencies met TS requirements to demonstrate operability and reliability;

tests were performed in accordance with the test procedures and other applicable

procedures; and test data and results were accurate, complete, within limits, and valid.

Inspectors verified that test results not meeting acceptance criteria were addressed with

an adequate operability evaluation or the system or component was declared

inoperable; equipment was returned to a position or status required to support the

performance of its safety functions; and all problems identified during the testing were

appropriately documented and dispositioned in the corrective action program.

b.

Findings

No findings were identified.

17

1EP6 Emergency Planning Drill Evaluation (71114.06 - 2 samples)

a.

Inspection Scope

The inspectors observed site emergency preparedness training drill/simulator scenarios

conducted on July 9, 2012 and July 25, 2012. The inspectors reviewed the drill scenario

narrative to identify the timing and location of classifications, notifications, and protective

action recommendations development activities. During the drill, the inspectors

assessed the adequacy of event classification and notification activities. The inspectors

observed portions of the licensees post-drill. The inspectors verified that the licensee

properly evaluated the drills performance with respect to performance indicators and

assessed drill performance with respect to drill objectives.

b.

Findings

No findings were identified.

4.

OTHER ACTIVITIES

4OA1 Performance Indicator (PI) Verification (71151 - 6 samples)

.1

Mitigating Systems Cornerstone

a.

Inspection Scope

Mitigating Systems Performance Index, Residual Heat Removal - Unit 1

Mitigating Systems Performance Index, Residual Heat Removal - Unit 2

The inspectors sampled licensee submittals for the Mitigating Systems Performance

Index (MSPI) performance indicators listed above for the period from the third (3rd)

quarter 2011 through the second (2nd) quarter 2012. The inspectors reviewed the

licensees operator narrative logs, issue reports, MSPI derivation reports, event reports

and NRC Integrated Inspection reports for the period to validate the accuracy of the

submittals.

b.

Findings

No findings were identified.

.2

Barrier Integrity Cornerstone

a.

Inspection Scope

Reactor Coolant System (RCS) Specific Activity - Unit 1

Reactor Coolant System (RCS) Specific Activity - Unit 2

The inspectors reviewed licensee submittals for the Reactor Coolant System Specific

Activity performance indicator for the period from the third (3rd) quarter 2011 through the

second (2nd) quarter 2012. The inspectors reviewed the licensees RCS chemistry

18

samples, TS requirements, issue reports, and event reports for the period to validate the

accuracy of the submittals. In addition to record reviews, the inspectors observed a

chemistry technician obtain and analyze a reactor coolant system sample.

Reactor Coolant System Leakage - Unit 1

Reactor Coolant System Leakage - Unit 2

The inspectors sampled licensee submittals for the Reactor Coolant System Leakage

performance indicator for the period from the third (3rd) quarter 2011 through the second

(2nd) quarter 2012. The inspectors reviewed the licensees operator logs, RCS leakage

tracking data, issue reports, and event reports for the period to validate the accuracy of

the submittals.

b.

Findings

No findings were identified.

4OA2 Identification and Resolution of Problems (71152 - 2 samples)

.1

Routine Review of Items Entered Into the Corrective Action Program

a.

Inspection Scope

To aid in the identification of repetitive equipment failures or specific human performance

issues for follow-up, the inspectors performed frequent screenings of items entered into

the licensees corrective action program. The review was accomplished by reviewing

daily action request reports.

b.

Findings

No findings were identified.

.2

Assessments and Observations

Selected Issue Follow-up Inspection: UPS-A Failure and Loss of Emergency Response

Facility Information System (ERFIS), Plant Process Computer (PPC), Business Network

a.

Inspection Scope

The inspectors selected AR 542704542704 UPS-A Failure and Loss of ERFIS, PPC, Business

Network, for detailed review. This AR identified that a single failure caused the loss of

ERFIS and Safety Parameter Display System (SPDS) on both units. The inspectors

reviewed the licensees CAP for ERFIS and SPDS failures in the past. The inspectors

reviewed these reports to verify that the licensee identified the full extent of the issue,

performed an appropriate evaluation, and specified and prioritized appropriate corrective

actions. The inspectors evaluated the reports against the requirements of the licensees

CAP as delineated in corporate procedure CAP-NGGC-0200, Corrective Action

Program, 10 CFR 50.47, and 10 CFR 50 Appendix E.

19

b.

Findings

No findings were identified

a.

Inspection Scope

The inspectors selected AR 542704542704 UPS-A Failure and Loss of ERFIS, PPC, Business

Network, for detailed review. This AR identified that a single failure caused the loss of

ERFIS and Safety Parameter Display System (SPDS) on both units. The inspectors

reviewed the licensees CAP for ERFIS and SPDS failures in the past. The inspectors

reviewed these reports to verify that the licensee identified the full extent of the issue,

performed an appropriate evaluation, and specified and prioritized appropriate corrective

actions. The inspectors evaluated the reports against the requirements of the licensees

CAP as delineated in corporate procedure CAP-NGGC-0200, Corrective Action

Program, 10 CFR 50.47, and 10 CFR 50 Appendix E.

b.

Findings

Introduction: A self-revealing Green NCV of 10 CFR 50.54(q)(2) was identified for the

licensees failure to properly evaluate or consider the impact to emergency response

facilities of design change ESR98-00436 which was implemented in 1999. As a result,

a number of temporary losses of ERFIS, Emergency Response Data System (ERDS),

SPDS, and all displays including radiation monitors for the emergency response facilities

occurred. Specifically, the licensee failed to ensure that adequate emergency response

facilities and equipment were available as required by the Brunswick Nuclear Plant

Radiological Emergency Plan, Section 1.3.1.3, revision 80, and 10 CFR 50.47(b)(8).

This issue was captured in the licensees CAP as AR 542704542704

Description: In 1999, the licensee implemented design change ESR98-00436 for the

power supply to the ERFIS, ERDS, SPDS, and all displays including RMS for the

emergency response facilities. The licensee did not properly evaluate or consider the

impact to emergency response facilities and equipment prior to implementation of this

design change. As a result, the ERFIS, ERDS, and SPDS systems, and all radiation

monitoring system (RMS) displays were susceptible to a single point power failure mode.

The implementation of the design change introduced a single point failure mode which

did not meet the design requirements specified in their Design Basis Document (DBD

60) sections 3.6.7.2 and 3.6.7.3. Prior to the licensees implementation of design

change ESR98-00436 in 1999, this single point vulnerability did not exist as the power

supply system had automatic switching capability on loss of one power source. When

the design change was implemented, the ERFIS, ERDS, and SPDS systems and RMS

displays were degraded as demonstrated by the resulting failures of those systems on

multiple occasions including July 17, 2004 and June 12, 2012. Additionally, all displays

for those systems were lost in all of the emergency facilities including the radiation

monitoring system.

20

On June 13, 2012, the licensee made an event notification to the NRC Operations

Center, 50.72(b)(3)(xiii) Loss of Emergency Assessment Capability, Offsite Response

Capability, or Offsite Communications Capability for the emergency response facilities.

The report delineated that at 5:57 p.m. EDT on June 12, 2012, Brunswick Nuclear Plant

experienced a fault on the Emergency Response Facility Information System (ERFIS)

uninterruptible power supply (UPS) electrical bus A. This resulted in a loss of site

Safety Parameter Display System (SPDS), Emergency Response Data System (ERDS)

and Plant Process Computer (PPC) for both Unit 1 and Unit 2.

During the loss of SPDS, the emergency response capability of that system was lost to

the site. During the loss of ERDS, the automatic data transfer feature of that system

was lost for transmissions to the NRC, however manual data transfer was still available.

During the loss of the PPC, automatic core thermal power averaging and automatic core

thermal limit monitoring was lost. Manual calculations were available for these functions.

Unit 1 SPDS was restored to the Emergency Operations Facility (EOF) at 7:49 p.m. on

June 12, 2012. Unit 2 SPDS was restored to the EOF at 8:30 p.m. on June 12, 2012.

The inverter was restored to service on June 17, 2012 at 12:00 noon.

Inspectors determined that the licensee did not properly evaluate or consider the impact

to all emergency response facilities and equipment prior to implementation of the

ESR98-00436 design change. The inspectors concluded that the ERFIS, ERDS, and

SPDS systems required by the Brunswick Nuclear Plant Radiological Emergency Plan

were degraded from 1999 when the design change was installed to present.

Compensatory measures were put in place during the June 2012 event to manually

obtain and log the required data from the instrumentation in the control room and

transmit to the emergency response facilities, and after the June 2012 event, the

licensee initiated a design change to restore the power configuration to those systems

back to the original design which would remove this failure mechanism.

Analysis: The licensees failure to properly evaluate or consider the impact to

emergency response facilities of design change ESR98-00436 which was implemented

in 1999 was a performance deficiency. Specifically, the licensee introduced a single

point failure mode which did not meet the design requirements specified in their Design

Basis Document (DBD 60) sections 3.6.7.2 and 3.6.7.3. This resulted in the licensees

failure to ensure that adequate emergency response facilities and equipment were

available as delineated in the Updated Final Safety Analysis Report (UFSAR) Section

7.7.1.9, and required by the Brunswick Nuclear Plant Radiological Emergency Plan,

Section 1.3.1.3, revision 80, and 10 CFR 50.47(b)(8).

The finding was more than minor because it adversely affected the Emergency

Preparedness Cornerstone objective of ensuring that the licensee was capable of

implementing adequate measures to protect the health and safety of the public in the

event of a radiological emergency. Specifically, the Facilities and Equipment attribute

was affected during the time when the ERFIS, ERDS, SPDS, and all displays including

radiation monitors for the emergency response facilities were degraded, and as a result

did not meet 10 CFR 50.47(b)(8) Planning Standard program element, adequate

emergency facilities and equipment to support the emergency response are provided

and maintained. The finding was assessed for significance in accordance with NRC IMC 0609, Appendix B Emergency Preparedness Significance Determination Process.

21

Attachment 2 of Appendix B, Failure to Comply Significance Logic is as follows: Failure

to comply; Loss of Risk Significant Planning Standard Function (RSPS), No; RSPS

Degraded Function, No; Loss of Planning Standard Function, No; the result is a Green

finding. The inspectors determined that this resulted in a low safety significance finding

(Green). No cross-cutting aspect was assigned to this finding because the performance

deficiency occurred more than three years ago and is not reflective of current plant

performance.

Enforcement: 10 CFR 50.54(q)(2) requires, in part, a licensee to follow and maintain the

effectiveness of an emergency plan that meets the requirements in Appendix E to this

part and, for nuclear power reactor licensee, the planning standards of 10 CFR 50.47(b).

The Brunswick Nuclear Plant Radiological Emergency Plan, Section 1.3.1.3, revision 80,

states in part that special provisions have been made to assure that ample space and

proper equipment are available to effectively respond to a full range of possible

emergencies. Contrary to the above, from 1999, when design change ESR98-00436

was installed, until the compensatory measures were put in place in June 2012, the

licensee failed to maintain adequate emergency facilities and equipment to support

emergency response when the ERFIS, ERDS, SPDS, and all displays including radiation

monitors for the emergency response facilities were degraded due to the implementation

of the design change. This resulted in failures of those systems on July 17, 2004 and

June 12, 2012. The licensee has compensatory measures in place, entered this issue

their CAP as AR 542704542704 and initiated a design change to restore the power

configuration back to the original design. Because the licensee entered the issue into its

CAP and the finding is of very low safety significance (Green), this violation is being

treated as an NCV, consistent with Section 2.3.2 of the NRCs Enforcement Policy: NCV

05000325; 324/2012004-02, Failure to Maintain Reliability and Availability of Emergency

Response Equipment for Emergency Response Facilities.

.3

Assessments and Observations

Selected Issue Follow-up Inspection: EDG 2 wiring associated with Alternate Safe

Shutdown (ASSD) Switch 2-DG-SS-A1

a.

Inspection Scope

The inspectors performed a detailed review of AR 557897557897associated with the wiring for

the EDG 2 Alternate Safe Shutdown (ASSD) Switch 2-DG-SS-A1. The issue was

discovered during a planned system outage for EDG2 during the week of August 26.

The inspectors verified that the issue was captured completely and accurately in the

CAP. The inspectors evaluated the licensees operability determinations and performed

walk-downs with licensee staff of applicable fire areas as needed. The inspectors

followed the licensees actions to restore the wiring to its proper configuration and also

verified the extent of condition inspections for the remaining EDGs 1, 3 and 4 were

completed in a timely manner. The inspectors reviewed the licensees reportability

evaluation and subsequent 8-hour report made to the NRC in accordance with 10 CFR

50.72(b)(3)(ii)(B). Additional documents reviewed are listed in the Attachment.

b.

Findings

22

Introduction: The inspectors opened an unresolved item (URI) for this issue of concern

to determine if a performance deficiency existed.

Description: A wiring discrepancy was identified during inspection of the EDG 2 ASSD

switch 2-DG-SS-A1. A contact in the circuit was determined to be bypassed that would

have the potential to prevent proper isolation of the EDG2 control circuits from the Main

Control Room (MCR) during an Appendix R fire event. The inspectors plan to review the

licensees cause evaluation for this event and determine if a performance deficiency

existed. This issue is being tracked as URI 05000325; 324/2012004-03, EDG2 wiring on

ASSD switch.

4OA3 Follow-up of Events (71153 - 2 samples)

.1

Notice of Unusual Event for Fire in the Protected Area

a.

Inspection Scope

For the plant event listed below, the inspectors reviewed plant parameters, reviewed

personnel performance, and evaluated performance of mitigating systems. The

inspectors communicated the plant events to appropriate regional NRC personnel, and

compared the event details with criteria contained in IMC 0309, Reactive Inspection

Decision Basis for Reactors, for consideration of potential reactive inspection activities.

As applicable, the inspectors verified that the licensee made appropriate emergency

classification assessments and properly reported the event in accordance with 10 CFR

50.72. The inspectors reviewed the licensees follow-up actions related to the events to

assure that the licensee implemented appropriate corrective actions commensurate with

their safety significance.

On August 2, 2012, a fire existed in the protected area on the Units 1 and 2 turbine

building roof for approximately two hours, meeting the criteria for a Notice of Unusual

Event declaration.

b.

Findings

One licensee identified violation is documented in Section 4OA7 of this report.

.2

(Closed) LER 05000325/2012-004-00, High Pressure Coolant Injection (HPCI)

Inoperable Due to Erratic Governor Operation

a.

Inspection Scope

On May 2, 2012, Unit 1 HPCI was declared inoperable due to erratic governor operation

during Surveillance Test 0PT-09.2, HPCI System Operability Test. The erratic governor

operation was due to the failure of the Ramp Generator Signal Convertor (RGSC). The

licensee determined that the root cause of the RGSC failure was due to a lack of a

replacement preventative maintenance (PM) for the RGSC, which had been installed for

at least 22 years. The corrective actions included replacing the RGSC and creating a

PM task to replace the RGSCs. The licensee documented the root cause evaluation in

23

NCR 534364. The inspectors reviewed the LER, the NCR, and corrective actions to

determine whether the station adequately evaluated the condition.

b.

Findings

One licensee identified violation is documented in Section 4OA7 of this report. This LER

is closed.

4OA5 Other Activities

.1

(Discussed) NRC Temporary Instruction (TI) 2515/187, Inspection of Near-Term Task

Force Recommendation 2.3 Flooding Walk-downs, and NRC TI 2515/188, Inspection of

Near-Term Task Force Recommendation 2.3 Seismic Walk-downs

a.

Inspection Scope

Inspectors accompanied the licensee on a sampling basis, during their flooding and

seismic walk-downs, to verify that the licensees walk-down activities were conducted

using the methodology endorsed by the NRC. These walk-downs are being performed at

all sites in response to a letter from the NRC to licensees, entitled Request for

Information Pursuant to Title 10 of the Code of Federal Regulations 50.54(f) Regarding

Recommendations 2.1, 2.3, and 9.3, of the Near-Term Task Force Review of Insights

from the Fukushima Dai-Ichi Accident, dated March 12, 2012 (ADAMS Accession No.

ML12053A340).

Enclosure 3 of the March 12, 2012, letter requested licensees to perform seismic walk-

downs using an NRC-endorsed walk-down methodology. Electric Power Research

Institute (EPRI) document 1025286 titled, Seismic Walk-down Guidance, (ADAMS

Accession No. ML12188A031) provided the NRC-endorsed methodology for performing

seismic walk-downs to verify that plant features, credited in the current licensing basis

(CLB) for seismic events, are available, functional, and properly maintained.

Enclosure 4 of the letter requested licensees to perform external flooding walk-downs

using an NRC-endorsed walk-down methodology (ADAMS Accession No.

ML12056A050). Nuclear Energy Industry (NEI) document 12-07 titled, Guidelines for

Performing Verification Walk-downs of Plant Protection Features, (ADAMS Accession

No. ML12173A215) provided the NRC-endorsed methodology for assessing external

flood protection and mitigation capabilities to verify that plant features, credited in the

CLB for protection and mitigation from external flood events, are available, functional,

and properly maintained.

b.

Findings

Findings or violations associated with the flooding and seismic walk-downs, if any, will

be documented in future reports.

24

.2

(Discussed) Temporary Instruction (TI) 2515/182 - Review of the Implementation of the

Industry Initiative to Control Degradation of Underground Piping and Tanks, Phase 1

a.

Inspection Scope

Leakage from buried and underground pipes has resulted in ground water contamination

incidents with associated heightened NRC and public interest. The industry issued a

guidance document, Nuclear Energy Institute (NEI) 09-14, Guideline for the

Management of Buried Piping Integrity, (ADAMS Accession No. ML 1030901420), to

describe the goals and required actions (commitments made by the licensee) resulting

from this underground piping and tank initiative. On December 31, 2010, NEI issued

Revision 1 to NEI 09-14, Guidance for the Management of Underground Piping and

Tank Integrity, (ADAMS Accession No. ML 110700122), with an expanded scope of

components which included underground piping that was not in direct contact with the

soil and underground tanks. On November 17, 2011, the NRC issued TI-2515/182,

Review of the Industry Initiative to Control Degradation of Underground Piping and

Tanks, to gather information related to the industrys implementation of this initiative.

The instructors reviewed the licensees programs for buried pipe and underground piping

and tanks in accordance with TI-2515/182 to determine if the program attributes and

completion dates identified in Section 3.3 A and 3.3 B of NEI 09-14, Revision 1, were

contained in the licensees program and implementing procedures. For the buried pipe

and underground piping program attributes, with completion dates that had passed, the

inspectors reviewed records to determine if the attribute was in fact complete and to

determine if the attribute was accomplished in a manner which reflected good or poor

practices in management.

b.

Observations

The licensees buried piping and underground piping and tanks program was inspected

in accordance with paragraphs 03.01.a through 03.01.c of TI-2515/182 and was found to

meet all applicable aspects of NEI 09-14 Revision 1, as set forth in Table 1 of the TI.

Based upon the scope of the review described above, Phase I of TI-2515/182 was

completed.

c.

Findings

No findings were identified.

4OA6 Management Meetings

Exit Meeting Summary

On July 19, 2012, the inspectors presented inspection results of the triennial heat sink

inspection to Mr. Michael Annacone and other members of the licensee staff. The

25

inspectors confirmed that none of the potential report input discussed was considered

proprietary.

On September 18, 2012, the inspector presented inspection results of the TI-182, Phase

1 of the Underground Piping and Tanks Inspection by conference call to Mr. James

Burke, Site Director of Engineering, and other members of the licensee staff. The

inspector verified that all proprietary information was returned to the licensee.

On October 11, 2012, the inspectors presented inspection results from the quarterly

inspection to Mr. Annacone and other members of the licensee staff. The inspectors

confirmed that any proprietary information received during the inspection period were

properly controlled or returned to licensee staff.

4OA7 Licensee-Identified Violations

The following violations of very low significance (Green) were identified by the licensee

and are violations of NRC requirements which meet the criteria of the NRC Enforcement

Policy, for being dispositioned as NCVs.

10 CFR 50.54(q) requires, in part, a licensee authorized to possess and operate

a nuclear power reactor shall follow and maintain in effect emergency plans

which meet the standards of 10 CFR 50.47(b). Title 10 CFR 50.47(b)(4)

requires, in part, a standard emergency classification and action level scheme be

used by the licensee. Procedure 0PEP-02.1.1, Emergency Control - Notification

of Unusual Event, Alert, Site Area Emergency, and General Emergency, Step

5.7.2 states, that the emergency declaration will be made within 15 minutes after

the availability of indications to plant operators that an emergency action level

has been exceeded. Procedure 0PEP-02.1, Initial Emergency Actions, HU2.1,

requires the declaration of an Unusual Event when a fire is not extinguished

within 15 minutes of control room notification or verification of a control room fire

alarm in any Table H-1 or Table H-3 areas. Table H-1 includes the turbine

building. Contrary to the above, on August 2, 2012, a Notice of Unusual Event

(NOUE) was not classified within 15 minutes of a fire within the protected area

not being extinguished within 15 minutes of detection. Specifically, when a fire

was reported on the Turbine Building roof to the Control Room and was not

extinguished within 15 minutes, conditions were met for classification of EAL

HU2.1 in accordance with Procedure 0PEP-02.1; however, the EAL was not

classified until approximately eight hours after the fire started. This issue was

entered into the licensees CAP as NCR 552984 and the licensee is performing a

root cause evaluation. Corrective actions included making a one hour report to

the NRC for discovery of a condition that met the EAL classification for an NOUE

after the fact. The inspectors determined the finding was associated with an

actual event implementation problem, and assessed the significance using IMC 0609, Appendix B, "Emergency Preparedness Significance Determination

Process." Using the Emergency Preparedness SDP, Sheet 1, "Failure to

Implement (Actual Event) Significance Logic" the inspectors determined the

finding was of very low safety significance (Green) because the licensee failed to

implement a risk significant planning standard (10 CFR 50.47(b)(4)) during an

actual Notice of Unusual Event.

26

10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings,"

requires that activities affecting quality shall be prescribed by documented

instructions, procedures, or drawings, of a type appropriate to the circumstances

and shall be accomplished in accordance with these instructions, procedures, or

drawings. Licensee procedure ADM-NGGC-0107, Equipment Reliability Process

Guideline, steps 9.4.9 and 9.4.10 required component experts and preventive

maintenance (PM) optimization to determine if there was a cost effective PM to

prevent failure and then to develop the PM model. Contrary to the above, the

Unit 1 high pressure coolant injection (HPCI) ramp generator signal converter

(RGSC) did not have the appropriate preventive maintenance to prevent failure.

As a result, the Unit 1 high pressure coolant injection (HPCI) system failed the

HPCI System Operability Test performed on April 30, 2012 and was declared

inoperable. The licensee entered this issue into the CAP as NCR 534364.

Corrective actions included replacing the RGSC and creating a PM task to

replace the RGSCs on a specified frequency. Using IMC 0609, Appendix A,

"Phase 1 Initial Screening and Characterization of Findings," the inspectors

determined this finding required a Phase 2 analysis. The Phase 1 screened this

Mitigating Systems Cornerstone finding to Phase 2 because the finding

represented a loss of HPCI system and/or function. The inspectors, with the

assistance of the regional Senior Risk Analyst, performed a Phase 2 analysis

using the Saphire 8 Model. 109 hours0.00126 days <br />0.0303 hours <br />1.802249e-4 weeks <br />4.14745e-5 months <br /> of unavailability time was used for the

analysis since HPCI was not required during the refueling outage from February

23, 2012 through April 29, 2012. Based on the results of the Phase 2 analysis,

the inspectors determined the finding was of very low safety significance (Green).

ATTACHMENT: SUPPLEMENTAL INFORMATION

Attachment

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

M. Annacone, Site Vice President

A. Brittain, Manager - Security

J. Burke, Director - Site Engineering

K. Croker, Supervisor - Emergency Preparedness

C. Dunsmore, Manager - Shift Operations

P. Dubrouillet, Manager - Training

G. Galloway, Acting Manager, Nuclear Oversight

C. George, Manager - BOP Systems

S. Gordy, Manager - Maintenance

L. Grzeck, Manager - Regulatory Affairs

M. Hamm, Superintendent - Mechanical Maintenance

F. Jefferson, Manager - Reactor Systems Engineering

J. Kalamaja, Manager - Operations

J. Krakuszeski, Plant General Manager

R. Mosier, Communication Specialist

A. Padleckas, Superintendent - Nuclear Operations Performance

D. Petrusic, Superintendent - Environmental and Chemistry

A. Pope, Manager - Nuclear Support Services

J. Price, Manager- Design Engineering

W. Richardson, Engineering

T. Roeder, Supervisor - Chemistry

T. Sherrill, Licensing Senior Technical Specialist

P. Smith, Superintendent - Electrical, Instrumentation, and Controls Maintenance

M. Talon, Buried Piping Program Manager

J. Terrell, Corporate Buried Piping Program Manager

M. Turkal, Lead Engineer - Technical Support

J. Vincelli, Manager - Environmental and Radiological Controls

B. Wilder, Engineering

E. Wills, Director - Site Operations

NRC Personnel

R. Musser, Chief, Reactor Projects Branch 4, Division of Reactor Projects Region II

Attachment

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed 05000325/2012004-01

05000325;324/2012004-02

NCV

NCV

Failure to Maintain Secondary Containment Operable

During an OPDRV Activity. (Section 1R20)

Failure to Maintain Reliability and Availability of

Emergency Response Equipment for Emergency

Response Facilities. (Section 4OA2.2)

Opened

05000325;324/2012004-03

URI

EDG2 Wiring on ASSD Switch (Section 4OA2.3)

Closed

05000325/2012-004-00

LER

High Pressure Coolant Injection (HPCI) Inoperable

Due to Erratic Governor Operation (Section 4OA3.2)

Discussed

Temporary Instruction

2515/187

TI

Inspection of Near-Term Task Force Recommendation

2.3 Flooding Walk-downs (Section 4OA5.1)

Temporary Instruction

2515/188

TI

Inspection of Near-Term Task Force Recommendation

2.3 Seismic Walk-downs (Section 4OA5.1)

Temporary Instruction

2515/182

TI

Review of the Implementation of the Industry Initiative

to Control Degradation of Underground Piping and

Tanks, Phase 1 (Section 4OA5.2)

Attachment

LIST OF DOCUMENTS REVIEWED

Section 1R01: Adverse Weather Protection

Procedures

0AOP-13.0, Operation During Hurricane, Flood Conditions, Tornado, or Earthquake

0PEP-02.6, Severe Weather

2APP-UA-01, Annunciator Procedure for Panel UA-01

2APP-UA-28, Annunciator Procedure for Panel UA-28

2OP-43, Service Water System Operating Procedure

OPS-NGGC-1305, Operability Determinations

Nuclear Condition Reports

556860

556861

556862

556863

556864

556865

556866

556867

556868

556869

556870

557375

555023

545354

553946

Work Orders

550098

550100

550102

550015

545859

545861

1828825

1828826

1643223

1775054

Drawings

D-02778, Reactor Building Floor and Wall Sleeves Tabulation - Sheet No 1 Unit No 2

D-02779, Reactor Building Floor and Wall Sleeves Tabulation and Details - Sheet No 2

D-11597, Backdraft Damper with Extra Deep Frame

F-0424, Service Water Intake Structure Units 1 & 2 Ventilation System & Drainage Piping

LL-FB-02103, Reactor Building, Elevation -170, Fire Barrier Penetrations, RHR-HPCI Room

North Wall

Miscellaneous

0PIC-LS001, Omnitrol (Valrec) Level Control Switch Model 613, Single Actuator

DBD-106, Hazards Analysis

Engineering Change 80408R0, Flooding Design Basis Update

Individual Plant Examination for External Events Submittal, June 1995

Link Seal Vendor Manual

Quick Hit Self-Assessment 541666-15, Emergency Action Level Functionality

SD-43, Service Water System

URS List of Flood Features Inspected

URS Near Term Force Recommendations 2.3: Flooding, Project Number 30703-007

Section 1R04: Equipment Alignment

Procedures

Procedure 2OP-18, Core Spray System Operating Procedure

1OP-17, RHR System Operating Procedure

2OP-10, Standby Gas Treatment System Operating Procedure

4

Attachment

Drawings

D-25024, Reactor Building Core Spray System Piping Diagram

9527-D-2025, sheets 1A and 1B, RHR System, Unit 1

F-04073, Reactor Building Standby Gas Treatment Piping Diagram

Miscellaneous

DBD-10, Design Basis Document Standby Gas Treatment System

SD-10, System Description Standby Gas Treatment System

Section 1R05: Fire Protection

Procedures

0FPP-014, Control of Combustible, Transient Fire Loads, and Ignition Sources

0PFP-CB, Control Building Pre-Fire Plans

OPLP-01, Fire Protection Program Document

OPLP-01.2, Fire Protection System Operability, Action, and Surveillance Requirements

0PFP-013, General Fire Plan

1PFP-RB, Reactor Building Pre-Fire Plans Unit 1

2PFP-RB, Reactor Building Prefire Plans Unit 2

OPT-34.11.2.0, Portable Fire Extinguisher Inspection

1PFP-TB, Turbine Building Prefire plans

Section 1R06: Flood Protection

Nuclear Condition Reports

490292

Drawings

F-03347, East Yard Area - Units No. 1 & 2 Electrical Underground Duct Runs Manholes

F-03343, East Yard Area - Units No. 1 & 2 Electrical Underground Duct Runs Plan

Section 1R07: Heat Sink Performance

Procedures

0ENP-2704, Administrative Control of NRC Generic Letter 89-13 Requirements

0ENP-2705, Service Water Heat Exchanger Thermal Performance Testing

0PM-ACU500, Inspection and Cleaning of the RHR/Core Spray Room Aerofin Cooler Air Filters

and Coolers

0PM-STU500, Service Water Intake Structure Inspection and Cleaning

0CM-ENG521, Perfex Cooler Inspection and Repair

0E&RC-3212, Service/Circulating Water Chlorine Sampling

1PM-MEC502, Nuclear Service Water Header Inspection

1PM-MEC506, Conventional Service Water Header Inspection

2PM-MEC501, Nuclear Service Water Header Inspection

2PM-MEC505, Conventional Service Water Header Inspection

0PT-08.1.4a, RHR Service Water System Operability Test - Loop A

0AOP-18.0, Nuclear Service Water system Failure

0AOP-19-0, Conventional Service Water System Failure

5

Attachment

0AOP-37.1, Intake System Blockages

0O1-03.4, Unit 0 Outside Auxiliary Operator Daily Check Sheets

IPT-24.1-1, Service Water Pump and Discharge Valve Operability Test

0AI-81, Water Chemistry Guidelines

0A1-86, Service/Circulating Water Treatment Strategic Plan

0SMP-SW1500, Sodium Hypochlorite Injection to the SW System

Nuclear Condition Reports

392541

507589

339272

539775

497132

542399

Work Orders

01582632

01324149

Drawings

BN 43.0.01, Service Water System

Calculations

OSW-0096, Calculation for Tube Plugging and Fouling of Service Water Safety Related Heat

Exchangers

OSW-0097, RHR and Core Spray Room Cooler Performance

G0050C-04, Design Basis Heat Loads from Vital Heat Exchangers

Miscellaneous

LTAM-BNP-12-0009, Formal Water Hammer Analysis for Service Water

DBD-43, Service Water System

DBD-17, Residual Heat Removal System

System Health Report, Q1-2012, RBCCW Unit 1

System Health Report, Q1-2012, Service Water

System Health Report, Q1-2012, Emergency Diesel Generators

Program Health Report, Q1-2012, GL 89-13 Program

EC-84365, Temporary Removal of Degraded Coating on Internal Surfaces of Service Water

Pump Discharge Pipe Spools and Elbows

EC-85258, Replace Nuclear and Conventional Service Water Pump Discharge Elbow

2-E11-B002A, Final Eddy Current Inspection Report for RHR Heat Exchanger 2A,

March 15, 2011

EDG-3-JWC-2010, Final Eddy Current Inspection Report for EDG-3 Jacket Water Cooler

May 18, 2010

SD-63, Sodium Hypochlorite Injection System

Procedure Revision Requests

00549906

00549915

00549919

00549920

00549923

00549924

00550041

00550333

Section 1R11: Licensed Operator Requalification

Procedures

0PEP-2.1.1, Emergency Control - Notification of Unusual Event, Alert, Site Area Emergency, or

General Emergency

6

Attachment

0PEP-02.1, Initial Emergency Actions

AOP-17, Turbine Building Closed Cooling Water System

AOP-19, Conventional Service Water System Failure

EM-78, Nuclear Power Facility Emergency Notification Form

ENP-24.5, Reactivity Control Planning

2EOP-01-LPC, Level/Power Control

2EOP-01-RSP, Reactor Scram Procedure

OPS-NGGC-1000, Fleet Conduct of Operations

TRN-NGGC-0420, Conduct of Simulator Training and Evaluation

Miscellaneous

LORX-IPO-003 Scenario

Technical Specifications 3.7.1, Residual Heat Removal Service Water System

Technical Specifications 3.7.2.E, Service Water System and Ultimate Heat Sink

Section 1R12: Maintenance Effectiveness

Procedures

1OP-43, Service Water System Operating Procedure

MNT-NGGC-0001, Maintenance Rework Program

0PT-06.1, SLC System Operability Test

0AOP-36.2, Station Blackout

0PT-12.22, Load Test for SAMA Diesels

ADM-NGGC-0101, Maintenance Rule Program

Nuclear Condition Reports

546346

554488

549265

519703

477622

436705

436703

409663

408997

401149

477561

477622

401149

Work Orders

1802757

2104000

1868030

1746181

Drawings

Miscellaneous

FP-20234, R.P Adams CO, Inc, Strainers, Poro-Edge Automatic

Technical Specification 3.7.2, Service Water System and Ultimate Heat Sink

SD-05, Standby Liquid Control System

Maintenance Rule Unavailability Reports, January 2012 through August 2012

SAMA Diesels System Health Report, Q2-2012

Section 1R13: Maintenance Risk Assessment and Emergent Work Control

Procedures

0AI-144, Risk Management

0AP-022, BNP Outage Risk Management

0AP-025, BNP Integrated Scheduling

7

Attachment

ADM-NGGC-0006, Online EOOS Model

ADM-NGGC-0104, Work Management Process

WCP-NGGC-0500, Work Activity Integrated Risk Management Program

OPS-NGGC-1311, Protected Equipment

Nuclear Condition Reports

559242

Miscellaneous

BNP EOOS Risk Assessment

BNP EOOS Risk Assessment Report for Work Week 36

Section 1R15: Operability Evaluations

Procedures

0PT-12.2C, No. 3 Diesel Generator Monthly Load Test

FP-20322, Diesel Generator Instruction Manual

OPS-NGGC-1305, Operability Determinations

OPS-NGGC-1307, Operational Decision making

Nuclear Condition Reports

250203

310500

318607

548370

549420

558810

Work Orders

542970

Drawings

D-25028, Reactor Building Closed Cooling Water System

F-09348, Diesel Generator No. 4 Circuits Control Wiring Diagram

Miscellaneous

EDG 1-4 Generator Bearing Oil Analysis

SD-39, Emergency Diesel Generators

Section 1R18: Plant Modifications

Procedures

EGR-NGGC-0028 Engineering Evaluation

0AI-68 Brunswick Nuclear Plant Response to Severe Weather Warnings

Engineering Changes

EC 88431, Service Water Building Drain Hub Baffle Plate Installation

EC 86304, Design Leak Tight Barriers at Reactor Bldg Rattle Spaces

Nuclear Condition Reports

559173

490292

8

Attachment

Drawings

D-02041, Service Water System Piping Diagram

F-04024, Service Water Intake Structure Ventilation System & Draining Piping

F-01027, Seismic Isolation Space

Miscellaneous

UFSAR Updated Final Safety Analysis Report

Section 1R19: Post Maintenance Testing

Procedures

0PT-08.2.2C, LPCI/RHR System Operability Test

0PT-80.5, Mid-Cycle Maintenance Outage Reactor Pressure Vessel Pressure Test

Nuclear Condition Reports

551048

Work Orders

1951825

2028895

2034614

2112268

Drawings

D-25026, Sheet 2A, Residual Heat Removal System, Unit 1

Miscellaneous

Technical Specifications 3.5.1, Emergency Core Cooling System - Operating

Section 1R20: Outage Activities

Procedures

0GP-01, Prestartup Checklist

0GP-02, Approach to Criticality and Pressurization of the Reactor

0GP-03, Unit Startup and Synchronization

0GP-05, Unit Shutdown

0GP-10, Rod Sequence Checkoff Sheets

0AI-127, Primary Containment Inspection and Closeout

0AP-22, BNP Outage Risk Management

0OI-01-01, BNP Conduct of Operations Supplement

0SP-12-001, EGM 11-003 OPDRV Activities

Nuclear Condition Reports

561831

561899

561173

562188

Drawings

D-20022 Sheet 1, Piping Diagram Extraction Steam System, Unit 1

Miscellaneous

Main Control Room (MCR) Logs

Outage Control Center (OCC) Logs

9

Attachment

Unit 1 Key Safety Function Component Status Sheets

Operations Standing Instruction 12-052

Section 1R22: Surveillance Testing

Procedures

0PT-07.2.4a, Core Spray System Operability Test - Loop A

0MST-RHR21Q, CSS and HPCI Hi Drywell Pressure Trip Unit Chan Cal

0MST-RCIC42R, RCIC Auto-actuation and Isolation Logic Sys Functional

0PT-12.12D, No. 4 Diesel Generator Monthly Load Test

0PT-08.2.2B, LPCI/RHR System Operability Test - Loop B

0PT-80.5, Mid-Cycle Maintenance Outage Reactor Pressure Vessel Pressure Test

Nuclear Condition Reports

547945

Work Orders

2107649

Drawings

D-25024, Reactor Building Core Spray System Piping Diagram

Miscellaneous

Technical Specification 3.5.1, Emergency Core Cooling System - Operating

UFSAR Section 6.3.3.7, Lag Times

Section 1EP6: Drill Evaluation

Procedures

0PEP-2.1.1, Emergency Control - Notification of Unusual Event, Alert, Site Area Emergency, or

General Emergency

0PEP-02.1, Initial Emergency Actions

0PEP-02.6.20, Dose Projection Coordinator

0PEP-03.4.8, Offsite Dose Projections for Monitored Releases

2EOP-01-RSP, Reactor Scram Procedure

EM-78, Nuclear Power Facility Emergency Notification Form

EMG-NGGC-0002, Offsite-Dose Assessment

OPS-NGGC-1000, Fleet Conduct of Operations

Nuclear Condition Reports

551255

551620

551698

552439

Section 4OA1: Performance Indicator Verification

Procedures

0E&RC-1006, Operation of the Reactor Building Sample Stations

0E&RC-2212, Calibration/Operation of Genie Gamma Spectroscopy System

REG-NGGC-0009, NRC Performance Indicators and Monthly Operating Report Data

10

Attachment

Miscellaneous

BNP-PSA-069, NRC Mitigating System Performance Index (MSPI) Basis Document

Unit 1 RHR MSPI Margin Reports, July 2011 to June 2012

Unit 2 RHR MSPI Margin Reports, July 2011 to June 2012

Unit 1 RHR MSPI Derivation Reports, July 2011 to June 2012

Unit 2 RHR MSPI Derivation Reports, July 2011 to June 2012

REG-NGGC-0009, Attachment 4 - MSPI Unavailability Data Sheets, July 2011 to June 2012

REG-NGGC-0009, Attachment 6 - MSPI Unreliability Data Sheets, July 2011 to June 2012

Section 4OA2: Identification and Resolution of Problems

Procedures

CAP-NGGC-0200, Condition Identification and Screening Process

CAP-NGGC-0205, Condition Evaluation and Corrective Action Process

CAP-NGGC-0206, Performance Assessment and Trending

OERP, Radiological Emergency Response Plan

OPLP-37, Equipment Important to Emergency Preparedness and ERO Response

OPEP-02.6.21, Emergency Communicator

OPEP-04.2, Emergency Facilities and Equipment

ADM-NGGC-0119, Nuclear Safety Culture Program, Revision 01

Nuclear Condition Reports

AR 00201153, Adverse Trend - Failed ERFIS Multiplexer Modules

ACE CR 542704, UPS-A Failure and Loss of ERFIS, PPC, Business Network

Miscellaneous

Down Time by Computer System Log

NIT Key performance indicators

ESR 98-00436, RAINS 99-0045, 50.59 Evaluation

ESR 98-00436, RAINS 99-0045, 50.54q Evaluation

Section 4OA3: Event Followup

Procedures

0PT-09.2, HPCI System Operability Test

0PT-09.3, HPCI System - 165 PSIG Flow Test

ADM-NGGC-0107, Equipment Reliability Process Guideline

0PEP-02.1, Initial Emergency Actions

0PEP-02.1.1, Emergency Control - Notification of Unusual Event, Alert, Site Area Emergency,

and General Emergency

0PEP-02.2.1, Emergency Action Level Bases

Nuclear Condition Reports

534364

552815

552984

Work Orders

2107224

2107264

2107271

2107313

11

Attachment

Drawings

1-FP-02039, General Electric Gas Control Piping Diagram

D-02055, Piping Diagram, Carbon Dioxide & Hydrogen Systems, Units 1 & 2

Miscellaneous

10 CFR 50.72 Event Report 47893, High Pressure Coolant Injection Inoperable due to Erratic

Governor Operation, May 2, 2012

LER 1-2012-004-00, High Pressure Coolant Injection Inoperable due to Erratic Governor

Operation, June 29, 2012

System Description 19, High Pressure Coolant Injection System

Technical Specification 3.5.1, Emergency Core Cooling Systems and Reactor Core Isolation

Cooling

Event Notification, Discovery of a Condition that Met the EAL Classification of an Unusual Event

(After-the-Fact), August 2, 2012

NUREG-1022, Event Reporting Guidelines

Operator Logs, August 2, 2012

SD-59, Hydrogen Water Chemistry System

Section 4OA5: Other Activities

Procedures

EGR-NGGC-0209, Buried Piping Program, Rev. 3

EGR-NGGC-0513, License Renewal Buried Piping and Tanks Inspection Program, Rev. 3

0AOP-13.0, Operation During Hurricane, Flood Conditions, Tornado, or Earthquake

0PEP-02.6, Severe Weather

2APP-UA-01, Annunciator Procedure for Panel UA-01

2APP-UA-28, Annunciator Procedure for Panel UA-28

2OP-43, Service Water System Operating Procedure

OPS-NGGC-1305, Operability Determinations

MNT-NGGC-004, Scaffolding Control

0PT-34.2.2.1, Fire Door, Pressure Boundary Door, ASSD Access/Egress Door, and Severe

Weather/Flood Control Door Inspections

0AI-68, Brunswick Nuclear Plant Response to Severe Weather Warnings

0PEP-02.1.1, Emergency Control-Notification of Unusual Event, Alert, Site Area Emergency,

and General Emergency

0PEP-02.6, Severe Weather

0AOP-13.0, Operation During Hurricane, Flood Conditions, Tornado, or Earthquake

Nuclear Condition Reports

551646

551838

551964

550469

559173

556860

556861

556862

556863

556864

556865

556866

556867

556868

556869

556870

557375

555023

545354

553946

Work Orders

550098

550100

550102

550015

545859

545861

1828825

11828826

1643223

1775054

2113607

12

Attachment

Work Requests

546632

546540

546541

546543

544971

546174

546823

546824

546203

546274

546278

Drawings

D-11099, Reactor Building Miscellaneous Steel Pool Liners

D-2274, Diesel Cooling Water

D-25049, Reactor Building Piping Diagram Fuel Pool Cooling & Filtering System, Unit 1

D-26007, Reactor Building Fuel Pool Cooling & Filter System Plan EL 80-0 & Sections

D-26009, Reactor Building Fuel Pool Cooling & Filter System Miscellaneous Plans & Sections

D-27010, Supplemental Spent Fuel Pool Cooling System

F-25008, Reactor Building Arrangement & Details, Fuel Pool

D-02778, Reactor Building Floor and Wall Sleeves Tabulation - Sheet No 1 Unit No 2

D-02779, Reactor Building Floor and Wall Sleeves Tabulation and Details - Sheet No 2

D-11597, Backdraft Damper with Extra Deep Frame

F-0424, Service Water Intake Structure Units 1 & 2 Ventilation System & Drainage Piping

LL-FB-02103, Reactor Building, Elevation -170, Fire Barrier Penetrations, RHR-HPCI Room

North Wall

1-FP-09319, Reactor Building Railroad Doors

Corrective Action Document

PRR 562261, Revise EGR-NGGC-0209 to strengthen the tie to the License Renewal Program

Miscellaneous

Calculation 2RB2-0012, Analysis for Spent Fuel Pool - Elevation of Top of Active Fuel

Engineering Change 80408R0, Flooding Design Basis Update

EPRI Report 1025286, Seismic Walk-down Guidance for Resolution of Fukushima Near-Term

Task Force Recommendation 2.3: Seismic

FP-75090, International Instruments INC, Instruments, Switchboard, Edgewise

System Description SD-43, Service Water System

UFSAR Section 9.1.3.3, Fuel Pool Cooling and Cleanup System, Safety Evaluation

Units 1 and 2, Flood Protection Feature 6BL, Service Water Building, 4 Elevation, Pipe

Penetration Seal\\20-8 Pipe Sleeves

Unit 1, SWEL 1 List

Unit 1, SWEL 2 List

Unit 2, SWEL 1 List

Unit 2, SWEL 2 List

URS Post Fukushima Project, NTTF Recommendation 2.3 Seismic Walk-down Training Record

URS Project Number 30703-007, Near Term Task Force Recommendation 2.3 Seismic Walk-

down Procedure

0PIC-LS001, Omnitrol (Valrec) Level Control Switch Model 613, Single Actuator

DBD-106, Hazards Analysis

Engineering Change 80408R0, Flooding Design Basis Update

Individual Plant Examination for External Events Submittal, June 1995

Link Seal Vendor Manual

Quick Hit Self-Assessment 541666-15, Emergency Action Level Functionality

SD-43, Service Water System

13

Attachment

URS List of Flood Features Inspected

URS Near Term Force Recommendations 2.3: Flooding, Project Number 30703-007

Report Number 110311.401, Summary of Progress Energy Fleet Underground Piping and

Tanks with the Scope of NEI 09-14 (Rev. 1), prepared by Structural Integrity Associates,

Inc., dated 12/07/2011

Assessment Number 531636, Quick Hit Self Assessment for HNP and BNP Buried Piping

Program and the NRC TI-2515/182 Inspection, 08/15/2012

Specification 024-001 for Special Doors

Section 4OA7: Licensee-Identified Violations

Procedures

0PEP-02.1, Initial Emergency Actions

0PEP-02.1.1, Emergency Control - Notification of Unusual Event, Alert, Site Area Emergency,

and General Emergency

0PEP-02.2.1, Emergency Action Level Bases

Nuclear Condition Reports

552815

552984

Drawings

1-FP-02039, General Electric Gas Control Piping Diagram

D-02055, Piping Diagram, Carbon Dioxide & Hydrogen Systems, Units 1 & 2

Miscellaneous

Event Notification, Discovery of a Condition that Met the EAL Classification of an Unusual Event

(After-the-Fact), August 2, 2012

NUREG-1022, Event Reporting Guidelines

Operator Logs, August 2, 2012

SD-59, Hydrogen Water Chemistry System