ML19324C317: Difference between revisions
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{{#Wiki_filter:^^ ' | {{#Wiki_filter:^^ ' | ||
: f. y- 7J. , l< | : f. y- 7J. , l< | ||
( , | ( , | ||
) ' .. , | ) ' .. , | ||
p . ;e3 e' , | p . ;e3 e' , | ||
i' Carolina Power & Light Crsmpany ' : | i' Carolina Power & Light Crsmpany ' : | ||
' Brunswick Nuclear Project P. O. Box 10429. | ' Brunswick Nuclear Project P. O. Box 10429. | ||
Scuthport. NC 28461-0429 | Scuthport. NC 28461-0429 i, | ||
i, | |||
November'7, 1989 t t y | November'7, 1989 t t y | ||
7 | 7 | ||
( / | ( / | ||
i | i FILE: B09,135100- 10CFR50.73 : | ||
FILE: B09,135100- 10CFR50.73 : | |||
SERIAL: BSEP/89-1002 U.S.' Nuclear Regulatory Commission ; | SERIAL: BSEP/89-1002 U.S.' Nuclear Regulatory Commission ; | ||
. ATTN: Document' Control Desk | . ATTN: Document' Control Desk Washington, DC 20555 { | ||
Washington, DC 20555 { | |||
BRUNSWICK STEAM ELECTRIC PLANT UNIT 1 SOCKET NO. 50-325 y LICENSE NO. DPR-71 LICENSEE EVENT REPORT 1-89-020 , | BRUNSWICK STEAM ELECTRIC PLANT UNIT 1 SOCKET NO. 50-325 y LICENSE NO. DPR-71 LICENSEE EVENT REPORT 1-89-020 , | ||
Gentlemen: I In accordance with Title 10 to the Code of. Federal Regulations, the enclosed , | Gentlemen: I In accordance with Title 10 to the Code of. Federal Regulations, the enclosed , | ||
Line 54: | Line 37: | ||
4 a, | 4 a, | ||
s.' u-, - - | s.' u-, - - | ||
I J. L. Harness, General Manager Brunswick Nuclear Project 1 TH/mcg 1 | |||
I J. L. Harness, General Manager | 1' ' Enclosure I~ | ||
Brunswick Nuclear Project 1 | |||
TH/mcg | |||
cc: 'Ir. S. D. Ebneter Hr. E. G. Tourigny , | cc: 'Ir. S. D. Ebneter Hr. E. G. Tourigny , | ||
53EP NRC Recident Office i. | |||
53EP NRC Recident Office | |||
i. | |||
/i 8911160126 891107 f7T k' . | /i 8911160126 891107 f7T k' . | ||
PDR ADOCK 05000325 | PDR ADOCK 05000325 | ||
, .S PNU | , .S PNU | ||
l c: ' . | l c: ' . | ||
; . c j u s. Nuctsta 5.e oute. tony coenMiessoN gears see . APPA!vlD Ohnt 800 31400164 . 3 "a'a"''"'" | ; . c j u s. Nuctsta 5.e oute. tony coenMiessoN gears see . APPA!vlD Ohnt 800 31400164 . 3 "a'a"''"'" | ||
LICENSEE EVENT REPORT (LER) pocaat Nuuria m ' " " * | LICENSEE EVENT REPORT (LER) pocaat Nuuria m ' " " * | ||
, A. ,u , , ,, A.,i, m | , A. ,u , , ,, A.,i, m Brunswick Steam Electric Plant Unit 1 0 l 6101010 l312 15 1 l0Fl d 4 | ||
Brunswick Steam Electric Plant Unit 1 0 l 6101010 l312 15 1 l0Fl d 4 | |||
? TIT L' i*' Loss'of Control Power and Operability of the 1-E41-F006 Valve While Removing the i Indicator Light Bulb from the MCC Breaker Cormartment tytNt Datt all Lim NUMein 141 mePomt DAtt spi OTHlR $ ACILltll$ 04v0Lvl0101 pay 3 gam e aput * **Mts DOCLIt NUMSIMisi MONTH DAv vtAm vlam 8 8,0M '*, 6 **AiSgp McNin 0ICIO1010 1 t l | ? TIT L' i*' Loss'of Control Power and Operability of the 1-E41-F006 Valve While Removing the i Indicator Light Bulb from the MCC Breaker Cormartment tytNt Datt all Lim NUMein 141 mePomt DAtt spi OTHlR $ ACILltll$ 04v0Lvl0101 pay 3 gam e aput * **Mts DOCLIt NUMSIMisi MONTH DAv vtAm vlam 8 8,0M '*, 6 **AiSgp McNin 0ICIO1010 1 t l | ||
~ - | ~ - | ||
Line 91: | Line 54: | ||
* 1 to actioi to miei u niensHio n vim unmm x n ntenan.1 nmw | * 1 to actioi to miei u niensHio n vim unmm x n ntenan.1 nmw | ||
:y so doommm so menti u ni nsavai gt,we g ja g g nei 110 10 to enemmm _ _ _ , | :y so doommm so menti u ni nsavai gt,we g ja g g nei 110 10 to enemmm _ _ _ , | ||
s to mmmem u.timmm u nemi.inuai use | s to mmmem u.timmm u nemi.inuai use 30 delleit1Hivi u v3isniiW 60 tSteH3HvinH91 to 408taH1Het l 6413isHineal to.13deimial LICEN8tl CONTACf POR YMia LER isti q;yg tittPMQNb NvM08m AmleGQ05 Tony liarris, Regulatory Compliance Specialist 911 l 9 415 17 l- l 2101 318 i i | ||
30 delleit1Hivi u v3isniiW 60 tSteH3HvinH91 to 408taH1Het l 6413isHineal to.13deimial LICEN8tl CONTACf POR YMia LER isti q;yg tittPMQNb NvM08m AmleGQ05 Tony liarris, Regulatory Compliance Specialist 911 l 9 415 17 l- l 2101 318 i i | |||
COMPLitt ONI LINE FOR B ACM COMPONENT F Aitums otSC#iORD IN TMis aspont Ital l | COMPLitt ONI LINE FOR B ACM COMPONENT F Aitums otSC#iORD IN TMis aspont Ital l | ||
civ e systaM COMPONENT **lWl^8 "I'o0 ",','!!' cAun :vst M eoMeoNeNt "'lWl^C' "l',0",''j}' , | civ e systaM COMPONENT **lWl^8 "I'o0 ",','!!' cAun :vst M eoMeoNeNt "'lWl^C' "l',0",''j}' , | ||
j i | j i | ||
I X IgU l l *i | I X IgU l l *i | ||
* Gt 0 8l 0 1 Yes 1 i 1 1 I i ; j | * Gt 0 8l 0 1 Yes 1 i 1 1 I i ; j l i I I I I i 1 l l I I l- I MONtw Day vtAm SvPPLEMINTAL Altont ExPECito nee Sv0 Mission [ | ||
l i I I I I i 1 l l I I l- I MONtw Day vtAm SvPPLEMINTAL Altont ExPECito nee Sv0 Mission [ | |||
1 | 1 | ||
~} vis in r. <omm avserio suswssioW e4 rre I~] No l l AntaCt ev.,n w ,a mno e. m -wP rsw e o e an w ~ ~esi oo l | ~} vis in r. <omm avserio suswssioW e4 rre I~] No l l AntaCt ev.,n w ,a mno e. m -wP rsw e o e an w ~ ~esi oo l | ||
Line 108: | Line 66: | ||
The event was caused by movement of the negat.ive socket coil into contact with ! | The event was caused by movement of the negat.ive socket coil into contact with ! | ||
the positive scchet tab during bulb removal. The coil movement during removal l" 1s attributed to inward force applied to the bulb during removal. When the coil came into contact with the tab the resulting short caused the loss of i control power to the F006 valvo. 1 | the positive scchet tab during bulb removal. The coil movement during removal l" 1s attributed to inward force applied to the bulb during removal. When the coil came into contact with the tab the resulting short caused the loss of i control power to the F006 valvo. 1 | ||
- Corrective actions include replacement of the lamp, socket and fuse and a | - Corrective actions include replacement of the lamp, socket and fuse and a sampling of various plant MCCs for similar coil distortion. As a result of this inspection, additional corrective actions were identified, including a review of the event wit.h appropriate operating personnel, evaluation of the feasibility of replacing the current socket with a different type socket, and . | ||
sampling of various plant MCCs for similar coil distortion. As a result of this inspection, additional corrective actions were identified, including a review of the event wit.h appropriate operating personnel, evaluation of the feasibility of replacing the current socket with a different type socket, and . | |||
development of an inspection plan for safety related MCCs and Transformer l sockets in the switchyard area. This event would not be considered more l significant under reasonabic and credible alternative conditions. | development of an inspection plan for safety related MCCs and Transformer l sockets in the switchyard area. This event would not be considered more l significant under reasonabic and credible alternative conditions. | ||
**No E1IS component identifier availabic l | **No E1IS component identifier availabic l | ||
Line 116: | Line 72: | ||
m , | m , | ||
; | ; | ||
.' g' p assa . - | .' g' p assa . - | ||
e, vs =vessia uevero.1co . o=l , | e, vs =vessia uevero.1co . o=l , | ||
[ | [ | ||
Line 127: | Line 79: | ||
. . .* >,- e * | . . .* >,- e * | ||
-LICENSEE EVENT REPORT (LER) TEXT CONTINUATICN *= wooous=oso.oiod s==nes emo , | -LICENSEE EVENT REPORT (LER) TEXT CONTINUATICN *= wooous=oso.oiod s==nes emo , | ||
raustrTT nasse gy @ocalf Numeth $ tem munssta tel pace tas | raustrTT nasse gy @ocalf Numeth $ tem munssta tel pace tas | ||
" " ~ " . ." ". -,*. | " " ~ " . ." ". -,*. | ||
i | i | ||
, ' Brunswick Steam Electric Plant | , ' Brunswick Steam Electric Plant | ||
,' 0 ll l 0 l 0 l 0 l 3l215 819 - | ,' 0 ll l 0 l 0 l 0 l 3l215 819 - | ||
Ol2l0 - | Ol2l0 - | ||
0l0 01 2 or 0 14 | 0l0 01 2 or 0 14 L . eammeeseemowas eseeasmwmetasmasawim | ||
L . eammeeseemowas eseeasmwmetasmasawim | |||
?! | ?! | ||
Event i | Event i | ||
Loss of control power and operability of 1-E41-F006 valve while removing the | Loss of control power and operability of 1-E41-F006 valve while removing the | ||
Line 147: | Line 92: | ||
Initial Conditions Unit 1 Reactor was at 100*; powe r . The Residual llent Removal / Low Pressure Coo'lant Injection (RllR/LPCI) System (EIIS/110), Core Spray System. (Ells /BM), | Initial Conditions Unit 1 Reactor was at 100*; powe r . The Residual llent Removal / Low Pressure Coo'lant Injection (RllR/LPCI) System (EIIS/110), Core Spray System. (Ells /BM), | ||
Reactor Core Isolation Cooling (RCIC) System (EIIS/BN) and the Automatic Depressurir.ation System (EIIS/*) were in standby readiness. | Reactor Core Isolation Cooling (RCIC) System (EIIS/BN) and the Automatic Depressurir.ation System (EIIS/*) were in standby readiness. | ||
Event Description At 1035 on 10/11/89, the llPCI (E41)-F006 valve Motor Control Center (MCC) indicating light sock'et (Ells /BJ/INV/IL/**), General Electric Model CR2940 shorted and blew the control power fuse to the F006 valve au the blown bulb was being removed from the socket by an Auxiliary Operator (AO). This resulted in a loss of control power to the 1-E41-F006 IIPCI irijection valve | Event Description At 1035 on 10/11/89, the llPCI (E41)-F006 valve Motor Control Center (MCC) indicating light sock'et (Ells /BJ/INV/IL/**), General Electric Model CR2940 shorted and blew the control power fuse to the F006 valve au the blown bulb was being removed from the socket by an Auxiliary Operator (AO). This resulted in a loss of control power to the 1-E41-F006 IIPCI irijection valve (EIIS/BJ/INV). This loss of control power would have prevented the valve from automatically opening if the HPCI System was needed. An LCO was initiated on the system due to this condition, and the fuse and lamp sccket were replaced. | ||
(EIIS/BJ/INV). This loss of control power would have prevented the valve from automatically opening if the HPCI System was needed. An LCO was initiated on the system due to this condition, and the fuse and lamp sccket were replaced. | |||
The system was returned to r;ervice on 10/11/89 at 2036. | The system was returned to r;ervice on 10/11/89 at 2036. | ||
Event Investigation The cause of this event was the positive tab of the light bulb socket coming int.o contact with the negative coil of the socket, causing a short which resulted in the blown fuse. The negative coil is used as the thread for the light in the socket. The exact cause of the tab coming into contact with the coil is not known; however, during the investigation into possibic mechanisms for the contact between the coil and the t.ab, it was noted that numerous sockets for indicating lights in various MCOs had coils that were closer to the j tab than in a new socket. The reason for this closeness is possibly due to I | Event Investigation The cause of this event was the positive tab of the light bulb socket coming int.o contact with the negative coil of the socket, causing a short which resulted in the blown fuse. The negative coil is used as the thread for the light in the socket. The exact cause of the tab coming into contact with the coil is not known; however, during the investigation into possibic mechanisms for the contact between the coil and the t.ab, it was noted that numerous sockets for indicating lights in various MCOs had coils that were closer to the j tab than in a new socket. The reason for this closeness is possibly due to I | ||
Line 157: | Line 100: | ||
may be distorted inward, closer to the positive tab. It was also noted during | may be distorted inward, closer to the positive tab. It was also noted during | ||
*No EIIS system code available | *No EIIS system code available | ||
**No EIIS component identifier available | **No EIIS component identifier available e y . 0p0.l000 0 424 636,4M g,. , | ||
e y . 0p0.l000 0 424 636,4M g,. , | |||
y men . v s avca:.x e.vmoa, co wa.o= ; | y men . v s avca:.x e.vmoa, co wa.o= ; | ||
Line 165: | Line 106: | ||
* _' | * _' | ||
* UCENSEE EVENT REPORT (LERI TEXT CONTINUATISN . mioveo o w o s e .o m spins w a | * UCENSEE EVENT REPORT (LERI TEXT CONTINUATISN . mioveo o w o s e .o m spins w a | ||
.- .e n, .n ava a = u. . ...e . l | .- .e n, .n ava a = u. . ...e . l | ||
,'.. "'-^" ~ ~ ~. , " . | ,'.. "'-^" ~ ~ ~. , " . | ||
Brunswick Steam Electric Plant ' | Brunswick Steam Electric Plant ' | ||
Line 175: | Line 113: | ||
01 0 0l3 OP Ol4 y rur aam amm e ame= == amm= *t amimpw nn i | 01 0 0l3 OP Ol4 y rur aam amm e ame= == amm= *t amimpw nn i | ||
1 field inspection of in-service sockets that the presence of corrosion on the socket coll / tab areas or the lamp base makes removal of the bulb difficult, often requiring inward force to be applied to the lamp during removal. + | 1 field inspection of in-service sockets that the presence of corrosion on the socket coll / tab areas or the lamp base makes removal of the bulb difficult, often requiring inward force to be applied to the lamp during removal. + | ||
The coil in the type socket involved in this failure is secured only at one | The coil in the type socket involved in this failure is secured only at one side of the socket. This allows inward movement of the coil toward the tab when inward pressure is applied during removal. | ||
side of the socket. This allows inward movement of the coil toward the tab when inward pressure is applied during removal. | |||
The vendor (GE) has been contacted to find out if similar occurrences of shorted sockets have been experienced by other facilities. No other similar socket failures were identified by the vendor. | The vendor (GE) has been contacted to find out if similar occurrences of shorted sockets have been experienced by other facilities. No other similar socket failures were identified by the vendor. | ||
Exact determination of the root cause of the mechanism for the shortin's has been hampered by the fact that the original faulted socket, fuse and bulb were l discarded prior to an in-depth analysis. The conclusion documented herein is a result of field inspections of in-service sockets, detailed breakdown, inspection and testing of a new socket and discussions with the A0 and Instrumentation and Control (16C) technicians involved with the incident. | Exact determination of the root cause of the mechanism for the shortin's has been hampered by the fact that the original faulted socket, fuse and bulb were l discarded prior to an in-depth analysis. The conclusion documented herein is a result of field inspections of in-service sockets, detailed breakdown, inspection and testing of a new socket and discussions with the A0 and Instrumentation and Control (16C) technicians involved with the incident. | ||
Line 183: | Line 119: | ||
The lamp, socket and fuse have been replaced. Technical Support engineers i have performed a random sampling of HCC indicating light sockets in order to i determing if the distortion of the coil could be a generic problem. s Preliminary results from this investigation (approximately 70 sockets were inspected in the Reactor Building, Turbine Bui? ding, Radwaste Building, and main transformer area) support the conclusion that coil distortion is a i potential generic effect from bulb removal, especially where corrosion is involved. | The lamp, socket and fuse have been replaced. Technical Support engineers i have performed a random sampling of HCC indicating light sockets in order to i determing if the distortion of the coil could be a generic problem. s Preliminary results from this investigation (approximately 70 sockets were inspected in the Reactor Building, Turbine Bui? ding, Radwaste Building, and main transformer area) support the conclusion that coil distortion is a i potential generic effect from bulb removal, especially where corrosion is involved. | ||
A memorandum has been issued to the Plant Management group, using this event l | A memorandum has been issued to the Plant Management group, using this event l | ||
as an example, defining the responsibility of site personnel in preserving physical evidence for investigations until the completion of the , | as an example, defining the responsibility of site personnel in preserving physical evidence for investigations until the completion of the , | ||
l | l investigation, per the direction of Regulatory Complience Instruction ; | ||
investigation, per the direction of Regulatory Complience Instruction ; | |||
(RCI)-06.6, Site Event Investigation Process. | (RCI)-06.6, Site Event Investigation Process. | ||
Corrective Actions to be Taken to Prevent Recurrence The following corrective actions will be taken: | Corrective Actions to be Taken to Prevent Recurrence The following corrective actions will be taken: | ||
: 1. Review of this event with appropriate Operations personnel. This item 1 will be completed by the end of the first quarter of 1990. | : 1. Review of this event with appropriate Operations personnel. This item 1 will be completed by the end of the first quarter of 1990. | ||
: 2. Technical Support will investigate the feasibility of replacement of the currently stocked General Einctric Model CR2940 socket with a Westinghouse bayonet type socket. | : 2. Technical Support will investigate the feasibility of replacement of the currently stocked General Einctric Model CR2940 socket with a Westinghouse bayonet type socket. | ||
Line 199: | Line 130: | ||
: y. - . _ . | : y. - . _ . | ||
U S KVCLl3 CloW4Atolv CowwiLUoV 8.Mt M '. | U S KVCLl3 CloW4Atolv CowwiLUoV 8.Mt M '. | ||
,; .._ L' * | ,; .._ L' | ||
* LICENSEE EVENT CEPORT (LER) TEXT CONTINUATION unoveo ow. =o me.oio. | |||
LICENSEE EVENT CEPORT (LER) TEXT CONTINUATION unoveo ow. =o me.oio. | |||
:=>*se ema f pm staus tu . DOC"4I"V"'88" | :=>*se ema f pm staus tu . DOC"4I"V"'88" | ||
* L 4 A NV'aD8 8 8 8 '688 'P | * L 4 A NV'aD8 8 8 8 '688 'P Brunswick Steam Electric Plant | ||
;. Unit 1 ofn 0l 4 0F 0 l4 0 5 o l o l 01 31215 ' 8!9 - | ;. Unit 1 ofn 0l 4 0F 0 l4 0 5 o l o l 01 31215 ' 8!9 - | ||
Ol 2 l0 - | Ol 2 l0 - | ||
wee mm . a mm wme w maawon | wee mm . a mm wme w maawon | ||
: 3. An inspection plan will be developed and implemented for safety related MCCs for socket degradation. This inapection will be limited to MCCs | : 3. An inspection plan will be developed and implemented for safety related MCCs for socket degradation. This inapection will be limited to MCCs which could produce a system failure due to a single socket failure. | ||
which could produce a system failure due to a single socket failure. | |||
Development of this plan will be completed by the end of the first quarter of 1990. | Development of this plan will be completed by the end of the first quarter of 1990. | ||
: 4. Transformer sockets in the plant switchyard area have been identified to be more susceptible to corrosion due to tha outside environment. | : 4. Transformer sockets in the plant switchyard area have been identified to be more susceptible to corrosion due to tha outside environment. | ||
Technical Support will coordinate with the Wilmington Transmission | Technical Support will coordinate with the Wilmington Transmission | ||
. Department the-inspection / replacement of the sockets in the plant switchyard transformers as necessary. | . Department the-inspection / replacement of the sockets in the plant switchyard transformers as necessary. | ||
Event Assessment As a result of this event, the IIPCI F006 valve would not have been able to 1 | Event Assessment As a result of this event, the IIPCI F006 valve would not have been able to 1 automatically open u} ion receipt of an initiation signal due to the loss of control power, which would have prevented the system from automatically injecting into the vessel. This is mitigated by three factors: | ||
automatically open u} ion receipt of an initiation signal due to the loss of control power, which would have prevented the system from automatically injecting into the vessel. This is mitigated by three factors: | |||
: 1. The valve is accessible and could have been manually operated if required. | : 1. The valve is accessible and could have been manually operated if required. | ||
: 2. The ADS /LPCI systems combination serves as a backup to !!PCI for safe shutdown and accident conditions. These systems were operable for the i duration of this event. | : 2. The ADS /LPCI systems combination serves as a backup to !!PCI for safe shutdown and accident conditions. These systems were operable for the i duration of this event. | ||
L 3. The plant is analyzed for a llPCI failure. | L 3. The plant is analyzed for a llPCI failure. | ||
l l As a result of the above, this event would not be considered more significant l under reasonable and credible alternative conditions. | l l As a result of the above, this event would not be considered more significant l under reasonable and credible alternative conditions. | ||
Line 233: | Line 152: | ||
l l | l l | ||
1 | 1 | ||
.v . .... ... . . w ... | .v . .... ... . . w ... | ||
, - - _ _ _ _ _ - -}} | , - - _ _ _ _ _ - -}} |
Revision as of 01:11, 1 February 2020
ML19324C317 | |
Person / Time | |
---|---|
Site: | Brunswick |
Issue date: | 11/07/1989 |
From: | Harness J, Harris T CAROLINA POWER & LIGHT CO. |
To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
References | |
BSEP-89-1002, LER-89-020, LER-89-20, NUDOCS 8911160126 | |
Download: ML19324C317 (5) | |
Text
^^ '
- f. y- 7J. , l<
( ,
) ' .. ,
p . ;e3 e' ,
i' Carolina Power & Light Crsmpany ' :
' Brunswick Nuclear Project P. O. Box 10429.
Scuthport. NC 28461-0429 i,
November'7, 1989 t t y
7
( /
i FILE: B09,135100- 10CFR50.73 :
SERIAL: BSEP/89-1002 U.S.' Nuclear Regulatory Commission ;
. ATTN: Document' Control Desk Washington, DC 20555 {
BRUNSWICK STEAM ELECTRIC PLANT UNIT 1 SOCKET NO. 50-325 y LICENSE NO. DPR-71 LICENSEE EVENT REPORT 1-89-020 ,
Gentlemen: I In accordance with Title 10 to the Code of. Federal Regulations, the enclosed ,
- Licensee Event Report is submitted. This report fulfills the requirement for
.t a-written report within thirty (30) days of a reportable occurrence and is in l, accordance with the' format set forth in NUREG-1022, September 1983.
J Very truly yours, >
4 a,
s.' u-, - -
I J. L. Harness, General Manager Brunswick Nuclear Project 1 TH/mcg 1
1' ' Enclosure I~
cc: 'Ir. S. D. Ebneter Hr. E. G. Tourigny ,
53EP NRC Recident Office i.
/i 8911160126 891107 f7T k' .
PDR ADOCK 05000325
, .S PNU
l c: ' .
- . c j u s. Nuctsta 5.e oute. tony coenMiessoN gears see . APPA!vlD Ohnt 800 31400164 . 3 "a'a""'"
LICENSEE EVENT REPORT (LER) pocaat Nuuria m ' " " *
, A. ,u , , ,, A.,i, m Brunswick Steam Electric Plant Unit 1 0 l 6101010 l312 15 1 l0Fl d 4
? TIT L' i*' Loss'of Control Power and Operability of the 1-E41-F006 Valve While Removing the i Indicator Light Bulb from the MCC Breaker Cormartment tytNt Datt all Lim NUMein 141 mePomt DAtt spi OTHlR $ ACILltll$ 04v0Lvl0101 pay 3 gam e aput * **Mts DOCLIt NUMSIMisi MONTH DAv vtAm vlam 8 8,0M '*, 6 **AiSgp McNin 0ICIO1010 1 t l
~ -
1l0 1l 1 8 9 8l9 0 l 2l0 0l 0 1l 1 0l7 8l9 inis mePont is sveMitteo Punsv&N1 to two meovinsMsNYs Os to cea i tea.ca eas e, ene, et tae fe"en asi atti 0 isto l0 ioi l l opanatiNo "008
- 1 to actioi to miei u niensHio n vim unmm x n ntenan.1 nmw
- y so doommm so menti u ni nsavai gt,we g ja g g nei 110 10 to enemmm _ _ _ ,
s to mmmem u.timmm u nemi.inuai use 30 delleit1Hivi u v3isniiW 60 tSteH3HvinH91 to 408taH1Het l 6413isHineal to.13deimial LICEN8tl CONTACf POR YMia LER isti q;yg tittPMQNb NvM08m AmleGQ05 Tony liarris, Regulatory Compliance Specialist 911 l 9 415 17 l- l 2101 318 i i
COMPLitt ONI LINE FOR B ACM COMPONENT F Aitums otSC#iORD IN TMis aspont Ital l
civ e systaM COMPONENT **lWl^8 "I'o0 ",','!!' cAun :vst M eoMeoNeNt "'lWl^C' "l',0",j}' ,
j i
I X IgU l l *i
- Gt 0 8l 0 1 Yes 1 i 1 1 I i ; j l i I I I I i 1 l l I I l- I MONtw Day vtAm SvPPLEMINTAL Altont ExPECito nee Sv0 Mission [
1
~} vis in r. <omm avserio suswssioW e4 rre I~] No l l AntaCt ev.,n w ,a mno e. m -wP rsw e o e an w ~ ~esi oo l
At 1035 on 10/11/89, with Unit 1 at 100'. power, the HPCI F006 injection value Motor Control Center indicating light socket shorted and blew the control power fuse for the F006 valve as the bulb was being removed. This resulted in j a loss of centrol power to the F006 valve, which would have prevented the valve i from automatienlly opening if the HPCI system was needed.
}
The event was caused by movement of the negat.ive socket coil into contact with !
the positive scchet tab during bulb removal. The coil movement during removal l" 1s attributed to inward force applied to the bulb during removal. When the coil came into contact with the tab the resulting short caused the loss of i control power to the F006 valvo. 1
- Corrective actions include replacement of the lamp, socket and fuse and a sampling of various plant MCCs for similar coil distortion. As a result of this inspection, additional corrective actions were identified, including a review of the event wit.h appropriate operating personnel, evaluation of the feasibility of replacing the current socket with a different type socket, and .
development of an inspection plan for safety related MCCs and Transformer l sockets in the switchyard area. This event would not be considered more l significant under reasonabic and credible alternative conditions.
- No E1IS component identifier availabic l
$M
m ,
.' g' p assa . -
e, vs =vessia uevero.1co . o=l ,
[
e
. . .* >,- e *
-LICENSEE EVENT REPORT (LER) TEXT CONTINUATICN *= wooous=oso.oiod s==nes emo ,
raustrTT nasse gy @ocalf Numeth $ tem munssta tel pace tas
" " ~ " . ." ". -,*.
i
, ' Brunswick Steam Electric Plant
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Event i
Loss of control power and operability of 1-E41-F006 valve while removing the
, indicator light bulb from the MCC breaker compartment.
Initial Conditions Unit 1 Reactor was at 100*; powe r . The Residual llent Removal / Low Pressure Coo'lant Injection (RllR/LPCI) System (EIIS/110), Core Spray System. (Ells /BM),
Reactor Core Isolation Cooling (RCIC) System (EIIS/BN) and the Automatic Depressurir.ation System (EIIS/*) were in standby readiness.
Event Description At 1035 on 10/11/89, the llPCI (E41)-F006 valve Motor Control Center (MCC) indicating light sock'et (Ells /BJ/INV/IL/**), General Electric Model CR2940 shorted and blew the control power fuse to the F006 valve au the blown bulb was being removed from the socket by an Auxiliary Operator (AO). This resulted in a loss of control power to the 1-E41-F006 IIPCI irijection valve (EIIS/BJ/INV). This loss of control power would have prevented the valve from automatically opening if the HPCI System was needed. An LCO was initiated on the system due to this condition, and the fuse and lamp sccket were replaced.
The system was returned to r;ervice on 10/11/89 at 2036.
Event Investigation The cause of this event was the positive tab of the light bulb socket coming int.o contact with the negative coil of the socket, causing a short which resulted in the blown fuse. The negative coil is used as the thread for the light in the socket. The exact cause of the tab coming into contact with the coil is not known; however, during the investigation into possibic mechanisms for the contact between the coil and the t.ab, it was noted that numerous sockets for indicating lights in various MCOs had coils that were closer to the j tab than in a new socket. The reason for this closeness is possibly due to I
inward force being exerted on the coil during removal of bulbs. It is speculated that the coil moved closer to the tab as a result of this inward force, and as I the A0 was removing tha bulb, the coil came into contact with the tab, fusing i the two together, j
The investigating engineer for this event noted that if an inward pressure was i applied and maintained while removing a bulb from a typical socket, the coil '
may be distorted inward, closer to the positive tab. It was also noted during
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1 field inspection of in-service sockets that the presence of corrosion on the socket coll / tab areas or the lamp base makes removal of the bulb difficult, often requiring inward force to be applied to the lamp during removal. +
The coil in the type socket involved in this failure is secured only at one side of the socket. This allows inward movement of the coil toward the tab when inward pressure is applied during removal.
The vendor (GE) has been contacted to find out if similar occurrences of shorted sockets have been experienced by other facilities. No other similar socket failures were identified by the vendor.
Exact determination of the root cause of the mechanism for the shortin's has been hampered by the fact that the original faulted socket, fuse and bulb were l discarded prior to an in-depth analysis. The conclusion documented herein is a result of field inspections of in-service sockets, detailed breakdown, inspection and testing of a new socket and discussions with the A0 and Instrumentation and Control (16C) technicians involved with the incident.
Corrective Actions Which llave Been Taken i i
The lamp, socket and fuse have been replaced. Technical Support engineers i have performed a random sampling of HCC indicating light sockets in order to i determing if the distortion of the coil could be a generic problem. s Preliminary results from this investigation (approximately 70 sockets were inspected in the Reactor Building, Turbine Bui? ding, Radwaste Building, and main transformer area) support the conclusion that coil distortion is a i potential generic effect from bulb removal, especially where corrosion is involved.
A memorandum has been issued to the Plant Management group, using this event l
as an example, defining the responsibility of site personnel in preserving physical evidence for investigations until the completion of the ,
l investigation, per the direction of Regulatory Complience Instruction ;
(RCI)-06.6, Site Event Investigation Process.
Corrective Actions to be Taken to Prevent Recurrence The following corrective actions will be taken:
- 1. Review of this event with appropriate Operations personnel. This item 1 will be completed by the end of the first quarter of 1990.
- 2. Technical Support will investigate the feasibility of replacement of the currently stocked General Einctric Model CR2940 socket with a Westinghouse bayonet type socket.
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- 3. An inspection plan will be developed and implemented for safety related MCCs for socket degradation. This inapection will be limited to MCCs which could produce a system failure due to a single socket failure.
Development of this plan will be completed by the end of the first quarter of 1990.
- 4. Transformer sockets in the plant switchyard area have been identified to be more susceptible to corrosion due to tha outside environment.
Technical Support will coordinate with the Wilmington Transmission
. Department the-inspection / replacement of the sockets in the plant switchyard transformers as necessary.
Event Assessment As a result of this event, the IIPCI F006 valve would not have been able to 1 automatically open u} ion receipt of an initiation signal due to the loss of control power, which would have prevented the system from automatically injecting into the vessel. This is mitigated by three factors:
- 1. The valve is accessible and could have been manually operated if required.
- 2. The ADS /LPCI systems combination serves as a backup to !!PCI for safe shutdown and accident conditions. These systems were operable for the i duration of this event.
L 3. The plant is analyzed for a llPCI failure.
l l As a result of the above, this event would not be considered more significant l under reasonable and credible alternative conditions.
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