ML19337A252: Difference between revisions
StriderTol (talk | contribs) (Created page by program invented by StriderTol) |
StriderTol (talk | contribs) (Created page by program invented by StriderTol) |
||
Line 17: | Line 17: | ||
=Text= | =Text= | ||
{{#Wiki_filter:}} | {{#Wiki_filter:. | ||
4 w | |||
3 U. S. NUCLEA3 CEGULATO2Y COMMIS$10N ,. | |||
NAC FORM 366 ' . | |||
47 771-LICENSEE EVENT REPO. | |||
;- | |||
O' ; | |||
, G I (PLEASE PRINT C, lYPE ALL REQUIRED INFORMATION) $' | |||
CONTROL SLCCK: ! | |||
i | |||
} I l ! | |||
lh 5 | |||
ill@ | |||
l J o &J 3i ) l N I J LICENSEE 000E l 0 l C t4 l ?:S l 1 l@l 0 l 0 l- l 010 UCENSE NUM8ER l 010 l0 IS l--10 26 l 0 | |||
.ACENSE l@l *v'E Al Jo 1l57 11car 54 1l@l COWT 1 lolil se ig l L gl 0 l 5 l 0 l 0 l 0 l 2 l 1 l 589 )@l 69 017 l 2 'l91810 EVENT QATE 74 | |||
)@l019 75 | |||
{0 l2181080l@ | |||
REPORT D ATE - : | |||
8 60 on DOCKET NUV8ER EVENT OESCRIPTTCN ANO PRC8ABLE CONSEQUENCES h i o ! 21_ l On July 29, 1980 during a routine surveillance test of the standbv gas 1 Io isl l treatment system #1 (SGTS #1), an overload trip was experienced on SGTS I l344; l exhaus e fan 1-8. Automatic circuitry started SGTS 12 which perfor: led I ioistl satisf acto rily. he safety significance of the event is considered I i;is ; l minimal since SGTS 42-vas available and oper'able if the need for its i jo;7i l operation had occurred. I I | |||
10 i a l I SO 7 5 3 SYSTEW OAUSE OALSE COMP. valve 000E 000E SL9 CODE COMPCNENT 000E SLOC00E SL8 CODE loIal l S l C l@ y@ l zl@ l a l E j L l A l y l S 18- l@ l 3 l@ [z_,J @ | |||
19 .0 r 4 4 10 11 12 13 OCOURRENCE RE8CRT REVisrCN , | |||
SECUENTIAL EV ENT VE A R misoRT NC. CODE TYPE No. | |||
@ ,"tE a. aC,5g 18 10 l 1-1 ! O I 3l 41 1/l 1013I IL I l-1 10I 2i 22 23 24 26 27 M 29 30 31 02 IPPECT - SpVTOCwN ATTACHMENT NP 4 0-4 'mVE COMP. COMPCNENT ACTICN suttat sCRM 368. SLP8U E R VANL F ACTL p E R TAKEN ACT:CN . ON ot.AN WETwCO aCbRS ** SU6MITTEC IAl@lxl@ | |||
.a 4 | |||
I: l@ | |||
25 - | |||
L.;j@ | |||
a. | |||
l 010I oI oI40 (2J@ | |||
si ai LvJ 42 | |||
@ L2J@ | |||
43 lcIoIaiol@ | |||
a 47 CAUSE CESCRIPT?CN AND CCRRECrtVE ACrIONS h It 13i } The accarent cause of the overlead trio was unusuntiv high | |||
=~M e w e- ~. I lt it I I erature around the motor control cubiele for fan 1-8. ''h e nve- b d --n- 1 I,t2i i cective device was reolaced and SGTS 41 was tested satisfactortiv. An I , | |||
1 !s t i engineering investiration is in oretress to dete =ine what sters can he l l 141 l taken to avoid recuirence of tries due to hizh a ibient conditions . I f | |||
* 80 5 9 s Acrit*v .* ' vtT)*CO 08 | |||
* 5?ATLS % 80VvEn ; ruga $74.gs d OiSCOVERY OISCOVEnv OEsCniP''CN 37 I' t !I l 0! 3I 6I NA | |||
= | |||
l las3 @l* Surveillance Test l . | |||
, .0 . | |||
*Av,.y a.Est ': . | |||
agggasE3 saggE23g aggyq7 ;p AC':VITY OCATICN 08 RELEASE . | |||
It t3)12l l NA l l NA 50 | |||
*ERSONNE t ocsN ES | |||
. NUM8Em *v8E O ESCR l **' C N i, m 10 i o 10 Gi 2 t@i Ni i IO " | |||
- ' #En3CNNE.\N RiE5 Nbv3Em O E 50miPT'CN fITlIo!OIO!@l | |||
, , , :2 NA l | |||
.053 Os Om O AVACE O sacti.*v | |||
*ssE Ofsemier oN . | |||
I'I3! NA l s3 13 - . | |||
30 ag g g;C;yv . | |||
C USE CNLv SSL E OtsCo.eycN $ , | |||
I2 !Ol IT I 7eeklv Neve Re *;e a g e l Il l 3 [ll lll ll l@ | |||
.. t , .. ,, ,0. ; . | |||
e NAVE CF **E8 ARE, Donald A. Ross , 201-455-3784 | |||
**090903 73 [ | |||
m . ~ . _ , . . . ~ | |||
.u m | |||
. ; | |||
'A \ | |||
II | |||
, (9 l | |||
^ | |||
} | |||
.7 . | |||
r Jersey Central Power & Ught Company ' | |||
s. | |||
,k 7 1 b.7 ff y' Madison Avenue at Punch Scwt Road Momstown, New Jersey 07960 (201)455-8200 | |||
.2 : | |||
OYSTER CREEK NUCLEAR GENERATING STATION '. | |||
Forked River, New Jersey 08731 ' ,, | |||
1 Licensee Event Report Reportable Occurrence No. 50-219/80-34/ 3L Repor: Date September 2, 1980 , | |||
Occurrence Date July 29, 1980 , | |||
Identifi_ation of Occurrence Operation of the Standby Gas Treatment System in a degraded mode as allowed by Technical Specification, paragraph 3.5.B.3 when standby gas treatment system #1 was found :o be inoperable during a scheduled surveillance test. - . | |||
31s event is considered to be a reportable occurrence in :he Technical Specifi-cations, paragraph 6.9.2.b.2. | |||
Conditions Prior to Occurrence The plant was operating at steady state power. | |||
Power: Reactor,1660 We Electrical, 542 W e Flow: Recirculation 13 x 10'' 3pm Feedwater, 6.00 x 10* lb/hr Pressure: 1020 psig Stack Gas Activity: 4.085 x 103 aci/sec Description of Occurrence On Tuesday, July 29,1980 at 2346 hourt, during a routine surveillance :est of | |||
:he s:andby gas :reatment system I (3GTS !), an overload trip was experienced 1 on SGTS exhaus: fan 1-8. Automatic circuitry started SG''S 92 which perforned satis f acto rily. | |||
Apparent Cause of Occurrence A subsequen investigation revealed that an overload trip on the "3" phase of E? l-3 had occurred. S e apparen: cause for the overload trip was an unusually high x2 bien: :*mperature around the noter control cubicle (106*y) . | |||
Arssy Oscir31 0:wer 'a ~. Wt Ocf*:ary S 1 VG'"C9r Of Te 00rG'ai OuCuC ' tliI;GS 3fSt6m | |||
r . | |||
, .y~. . , | |||
_;# - .g | |||
....pe ~p s., p J . | |||
( | |||
a lb | |||
. s t | |||
( 3 Reportable Occurrence No. 50-219'/80-34/3L Page 2- .tg | |||
[-'' L September 2,~;i980 - | |||
Analvsis of Occurrence | |||
',2 l | |||
Standby gas treatment system is 'used to process the reactor building atmosphere should conditions be' present which require its operation ~ Although SGTS ~ fl | |||
. s-- | |||
p ,became~1noperable. SGTS 12 did' initiate and performed as designed. | |||
^ | |||
The . safety ' significance of this event is considered minimmi since SGTS #2 was ' | |||
available and operable if the need for'its operation had occurred. | |||
Corrective Action | |||
'SGTS 11 (Fan 1-8) was. removed from service and the overload protective device- a replaced. An operability test was performed to prove the' system operable. | |||
.y | |||
' As part of the investigation of the overload trip, the =otor control center breakers for SGTS 11~ (I71-8) and SGTS , d2 (IF 1-9) and their related fusos. | |||
. breakers and overloads were checked and found to be satisfactory. | |||
-In addition,;the amperage of the motor was found to be in compliance with its design. The full load name place current rating is 12.8 amps. The full lead . | |||
current was measured at 13.2 amps which is well within the 1.15 rated service s fac to r. | |||
An Engineering investigation is in progress to determine what steps can be taken m to" avoid recurrence of trips due to high ambient conditions as experienced. , ; | |||
-Failure Data . | |||
General ~Ilectric - | |||
.Model CR124-C028 | |||
-Mocor Overload Relay. | |||
s j | |||
. ,i 1 | |||
a = | |||
i | |||
' ~ " '' ' ' ' ' - ' ' _______-______._e. | |||
_}} |
Revision as of 13:43, 31 January 2020
ML19337A252 | |
Person / Time | |
---|---|
Site: | Oyster Creek |
Issue date: | 09/02/1980 |
From: | Ross D JERSEY CENTRAL POWER & LIGHT CO. |
To: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
Shared Package | |
ML19337A236 | List: |
References | |
LER-80-034-03L, LER-80-34-3L, NUDOCS 8009090373 | |
Download: ML19337A252 (3) | |
Text
.
4 w
3 U. S. NUCLEA3 CEGULATO2Y COMMIS$10N ,.
NAC FORM 366 ' .
47 771-LICENSEE EVENT REPO.
- -
O' ;
, G I (PLEASE PRINT C, lYPE ALL REQUIRED INFORMATION) $'
CONTROL SLCCK: !
i
} I l !
lh 5
ill@
l J o &J 3i ) l N I J LICENSEE 000E l 0 l C t4 l ?:S l 1 l@l 0 l 0 l- l 010 UCENSE NUM8ER l 010 l0 IS l--10 26 l 0
.ACENSE l@l *v'E Al Jo 1l57 11car 54 1l@l COWT 1 lolil se ig l L gl 0 l 5 l 0 l 0 l 0 l 2 l 1 l 589 )@l 69 017 l 2 'l91810 EVENT QATE 74
)@l019 75
{0 l2181080l@
REPORT D ATE - :
8 60 on DOCKET NUV8ER EVENT OESCRIPTTCN ANO PRC8ABLE CONSEQUENCES h i o ! 21_ l On July 29, 1980 during a routine surveillance test of the standbv gas 1 Io isl l treatment system #1 (SGTS #1), an overload trip was experienced on SGTS I l344; l exhaus e fan 1-8. Automatic circuitry started SGTS 12 which perfor: led I ioistl satisf acto rily. he safety significance of the event is considered I i;is ; l minimal since SGTS 42-vas available and oper'able if the need for its i jo;7i l operation had occurred. I I
10 i a l I SO 7 5 3 SYSTEW OAUSE OALSE COMP. valve 000E 000E SL9 CODE COMPCNENT 000E SLOC00E SL8 CODE loIal l S l C l@ y@ l zl@ l a l E j L l A l y l S 18- l@ l 3 l@ [z_,J @
19 .0 r 4 4 10 11 12 13 OCOURRENCE RE8CRT REVisrCN ,
SECUENTIAL EV ENT VE A R misoRT NC. CODE TYPE No.
@ ,"tE a. aC,5g 18 10 l 1-1 ! O I 3l 41 1/l 1013I IL I l-1 10I 2i 22 23 24 26 27 M 29 30 31 02 IPPECT - SpVTOCwN ATTACHMENT NP 4 0-4 'mVE COMP. COMPCNENT ACTICN suttat sCRM 368. SLP8U E R VANL F ACTL p E R TAKEN ACT:CN . ON ot.AN WETwCO aCbRS ** SU6MITTEC IAl@lxl@
.a 4
I: l@
25 -
L.;j@
a.
l 010I oI oI40 (2J@
si ai LvJ 42
@ L2J@
43 lcIoIaiol@
a 47 CAUSE CESCRIPT?CN AND CCRRECrtVE ACrIONS h It 13i } The accarent cause of the overlead trio was unusuntiv high
=~M e w e- ~. I lt it I I erature around the motor control cubiele for fan 1-8. h e nve- b d --n- 1 I,t2i i cective device was reolaced and SGTS 41 was tested satisfactortiv. An I ,
1 !s t i engineering investiration is in oretress to dete =ine what sters can he l l 141 l taken to avoid recuirence of tries due to hizh a ibient conditions . I f
- 80 5 9 s Acrit*v .* ' vtT)*CO 08
=
l las3 @l* Surveillance Test l .
, .0 .
- Av,.y a.Est ': .
agggasE3 saggE23g aggyq7 ;p AC':VITY OCATICN 08 RELEASE .
It t3)12l l NA l l NA 50
- ERSONNE t ocsN ES
. NUM8Em *v8E O ESCR l **' C N i, m 10 i o 10 Gi 2 t@i Ni i IO "
- ' #En3CNNE.\N RiE5 Nbv3Em O E 50miPT'CN fITlIo!OIO!@l
, , , :2 NA l
.053 Os Om O AVACE O sacti.*v
- ssE Ofsemier oN .
I'I3! NA l s3 13 - .
30 ag g g;C;yv .
C USE CNLv SSL E OtsCo.eycN $ ,
I2 !Ol IT I 7eeklv Neve Re *;e a g e l Il l 3 [ll lll ll l@
.. t , .. ,, ,0. ; .
e NAVE CF **E8 ARE, Donald A. Ross , 201-455-3784
- 090903 73 [
m . ~ . _ , . . . ~
.u m
. ;
'A \
II
, (9 l
^
}
.7 .
r Jersey Central Power & Ught Company '
s.
,k 7 1 b.7 ff y' Madison Avenue at Punch Scwt Road Momstown, New Jersey 07960 (201)455-8200
.2 :
OYSTER CREEK NUCLEAR GENERATING STATION '.
Forked River, New Jersey 08731 ' ,,
1 Licensee Event Report Reportable Occurrence No. 50-219/80-34/ 3L Repor: Date September 2, 1980 ,
Occurrence Date July 29, 1980 ,
Identifi_ation of Occurrence Operation of the Standby Gas Treatment System in a degraded mode as allowed by Technical Specification, paragraph 3.5.B.3 when standby gas treatment system #1 was found :o be inoperable during a scheduled surveillance test. - .
31s event is considered to be a reportable occurrence in :he Technical Specifi-cations, paragraph 6.9.2.b.2.
Conditions Prior to Occurrence The plant was operating at steady state power.
Power: Reactor,1660 We Electrical, 542 W e Flow: Recirculation 13 x 10 3pm Feedwater, 6.00 x 10* lb/hr Pressure: 1020 psig Stack Gas Activity: 4.085 x 103 aci/sec Description of Occurrence On Tuesday, July 29,1980 at 2346 hourt, during a routine surveillance :est of
- he s:andby gas :reatment system I (3GTS !), an overload trip was experienced 1 on SGTS exhaus: fan 1-8. Automatic circuitry started SGS 92 which perforned satis f acto rily.
Apparent Cause of Occurrence A subsequen investigation revealed that an overload trip on the "3" phase of E? l-3 had occurred. S e apparen: cause for the overload trip was an unusually high x2 bien: :*mperature around the noter control cubicle (106*y) .
Arssy Oscir31 0:wer 'a ~. Wt Ocf*:ary S 1 VG'"C9r Of Te 00rG'ai OuCuC ' tliI;GS 3fSt6m
r .
, .y~. . ,
_;# - .g
....pe ~p s., p J .
(
a lb
. s t
( 3 Reportable Occurrence No. 50-219'/80-34/3L Page 2- .tg
[- L September 2,~;i980 -
Analvsis of Occurrence
',2 l
Standby gas treatment system is 'used to process the reactor building atmosphere should conditions be' present which require its operation ~ Although SGTS ~ fl
. s--
p ,became~1noperable. SGTS 12 did' initiate and performed as designed.
^
The . safety ' significance of this event is considered minimmi since SGTS #2 was '
available and operable if the need for'its operation had occurred.
Corrective Action
'SGTS 11 (Fan 1-8) was. removed from service and the overload protective device- a replaced. An operability test was performed to prove the' system operable.
.y
' As part of the investigation of the overload trip, the =otor control center breakers for SGTS 11~ (I71-8) and SGTS , d2 (IF 1-9) and their related fusos.
. breakers and overloads were checked and found to be satisfactory.
-In addition,;the amperage of the motor was found to be in compliance with its design. The full load name place current rating is 12.8 amps. The full lead .
current was measured at 13.2 amps which is well within the 1.15 rated service s fac to r.
An Engineering investigation is in progress to determine what steps can be taken m to" avoid recurrence of trips due to high ambient conditions as experienced. , ;
-Failure Data .
General ~Ilectric -
.Model CR124-C028
-Mocor Overload Relay.
s j
. ,i 1
a =
i
' ~ " ' ' ' ' - ' ' _______-______._e.
_