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{{#Wiki_filter:dk REGULATORY INFORMATlON DISTRIBUTION SYSTEM (BIDS>DISTRIBUTION FOR INCOMING MATERIAL 50-335 DOCDATE: 08l25/78 DATE RCVD: 09/05/78 REC: OREILLY J P NRC DGCTYPE: LETTER NQTAR IZED: NO COPIES RECEIVED  
{{#Wiki_filter:dk REGULATORY INFORMATlON DISTRIBUTION SYSTEM (BIDS>
DISTRIBUTION FOR INCOMING MATERIAL                                       50-335 REC: OREILLY            J  P                                                              DOCDATE: 08l25/78 NRC                                                                                  DATE RCVD: 09/05/78 DGCTYPE:           LETTER         NQTAR     IZED:   NO                                     COPIES RECEIVED


==SUBJECT:==
==SUBJECT:==
LTR 1 ENCL 1 FORWARD1NG LICENSEE EVENT REPT (RG 50-335/78-029)
LTR 1   ENCL 1 FORWARD1NG LICENSEE EVENT REPT (RG 50-335/78-029) ON 07/28/78 CONCERNING NOTIFICATION BY APPLICANT"S VENDQR OF POTENTIAL PROBLEM WITI-I CERTAIN MOTOR OPERATED VALVES... WlATT.
ON 07/28/78 CONCERNING NOTIFICATION BY APPLICANT"S VENDQR OF POTENTIAL PROBLEM WITI-I CERTAIN MOTOR OPERATED VALVES...WlATT.PLANT NAME: ST LUClE Ni REVIEWER INITIAL: X JM DISTRIBUTOR INITIAL:~4~k<lHt44H~+++4H~~~>H~
PLANT NAME: ST LUClE               Ni                                           REVIEWER INITIAL: X JM 4~k<lHt44H~+++4H~~~>H~         DI TRIBUTION 0,- THIS MAT-RIAL IS AS DISTRIBUTOR FOLLOWS INITIAL:  ~
DI TRIBUTION 0,-THIS MAT-RIAL IS AS FOLLOWS 4+>+>>o>~~+>>>~~~+
4+>+>>o>~~+>>>~~~+
INCIDENT REPORTS (DISTRIBUTION CODE A002)FOR ACTION: INTERNAL: EXTERNAI: BR C<%W/4 ENCL-ILE~'~~W/ENCL-HHa/g I 8c C SYSTEMS BR++W/ENCL NQVAK/CHECK~~4l W/ENCL AD FOR ENG'.~.~W/ENCL I~IANAUER~H~W/ENCL AD FOR SYS Sc PROJ~%W/ENCL ENGINEERING BR+4W/ENCI I'REGER/J.
INCIDENT REPORTS (DISTRIBUTION CODE A002)
CGLL INS~~W/ENCL K SEYFRIT/IE+>W/ENCL LPDR'S FT PIERCEi FL.~<W/ENCL NS I C4F4: W/ENCL ACRS CAT B4".FW/16 ENCL NRC PDRc~~~W/ENCL MIPC+~W/3 ENCL EMERGENCY PLAN BR~<lJ/ENCL EEB~~~W/ENCL PLANT SYSTEMS BR<<lJ/ENCL AD FOR PLANT SYSTEMS>~W/ENCL REACTOR SAFETY BR<4W/ENCL VOLLMER/BUNCH++W/ENCL POIJER SYS BR++W/ENCL DISTRIBUTION:
FOR ACTION:               BR                               C<%W/4 ENCL INTERNAL:                          - ILE~'~~W/ENCL                     NRC PDRc~~~W/ENCL
LTR 44 ENCL 44 SIZE: iP+iP+1P.8$%0H." H 0f CHl%8l%4%6f+%8Hf NHl%Sf SHHF 3HHf)HHf wc Rl%0~THE END CQNTROL NBI a'782480/.33
                                            -HHa /g                           MIPC+~W/3 ENCL I   8c C SYSTEMS BR++W/ENCL                EMERGENCY PLAN BR~<lJ/ENCL NQVAK/CHECK~~4lW/ENCL                        EEB~~~W/ENCL AD FOR ENG'.~.~W/ENCL                        PLANT SYSTEMS BR<<lJ/ENCL I IANAUER~H~W/ENCL
/le't@
                                    ~
I FLORIDA POWER S<<LIGHT QOII<<IPANy August 25, 1978 PRN-LZ-78-2c3>7 Mr.James P.O'Reilly, Director, Region II Office of Inspection and Enforcement U.S.Nuclear Regulatory Commission 230 Peachtree Street, N.N.Suite 1217 Atlanta, Georgia 30303
AD FOR PLANT SYSTEMS>~W/ENCL AD FOR SYS Sc PROJ~%W/ENCL                  REACTOR SAFETY BR<4W/ENCL ENGINEERING BR+4W/ENCI                     VOLLMER/BUNCH++W/ENCL I'REGER/J. CGLL INS~~W/ENCL                  POIJER SYS BR++W/ENCL K   SEYFRIT/IE+>W/ENCL EXTERNAI:                  LPDR'S FT PIERCEi FL.~<W/ENCL NS I C4F4: W/ENCL ACRS       CAT B4".FW/16 ENCL DISTRIBUTION:               LTR 44           ENCL 44                             CQNTROL NBI a'782480/.33 SIZE: iP+iP+1P                                                                                       /le 't@
. 8$ %0H." H 0f CHl%8l %4%6f+%8Hf NHl %Sf SHHF 3HHf )HHf wc Rl % 0   ~
THE END


==Dear Mr.O'Reilly:==
I FLORIDA POWER S<<LIGHT QOII<<IPANy August 25, 1978 PRN-LZ-78-2c3>7 P
REPORTABLE OCCURRENCE 335-78-29 ST.LUCIE UNIT 1 DATE OF OCCURRENCE:
Mr. James P. O'Reilly, Director, Region Office of Inspection and Enforcement II            <<N <<(ie
JULY 28, 1978 P<<(ie~<<N<<>1 Pl C/l TECHNICAL SPECIFICATION 6.9.1.9.C MOTOR OPERATED VALVES The attached Licensee Event Report is being submitted in accordance with Technical Specification 6.9 to provide 30-day notification of the subject occurrence.
                                                                  ~
Very truly yours, RB.D.Schmidt Vice President Power Resources MAS/sn Attachment cc: Harold F.Reis, Esquire Director, Office of Inspection and Enforcement (30)Director, Office of Management Information and Program Control (3)78248QJ33 PEOPLE..SERVING PEOPLE iuFc FQRM X88!7 77!LlCEIXSEE EVE!MT REPORT U.*NUCLSAR RBGULATORY C IIMIS)CION
U.S. Nuclear Regulatory Commission                            <<>1 230 Peachtree Street, N.N. Suite 1217 Atlanta, Georgia 30303                                        Pl C/l
~ol;1 CAN'~OI I 1 3~OI 2 I 1 I I I QI (PLSASB PRINT OR TYPB ALL RBCUIRSD INFORSIATIONI I'C44588 COOK ,.QT, IJCXINSX I'I)44)dail Q, Q 15 5)CS458 TV)4 IU 51 Ai 58 Q":::il"'0'''"''~0~i'5)7 di CCCXXT NVIISSA 67 SVSNT<<ATX 15 A!CAT O*TX 38 BVB)uTOBSCRIPTION
 
'NO PROBABL=CO'ISBCUBNC-S QIQ Our NSSS vendor notified us that we had a potential problem.~o>>with certain motor o crated valves (MOVs).All sus ect.safety-related MOVs outside containment were inspected and, ,"..if'necessary, repaired.;.All suspect safety-related MOVs inside containment will be inspected and, if necessary,~o!1 re aired at the first shutdown of sufficient length, but no later than the next refueling.
==Dear Mr. O'Reilly:==
1 3 SY5TXV CAUSX CAU58 C~P.VALVS C OX CQCS SUSC<<08 C)')PCiiaiiT COOS SUSC<<QX$I'SCQCS~ol 8 IILJIIS iilc 04S'~1>>0 Icc I 0 g I)7 It IZ I7:5 Ig 5 ScCVSNTIAI.
 
CCCJAAXiuCX ASPQRT RSVIS)ON~LSBIFO VSNT V SAR AXPOATNO, COOS TVPS)I Q, OliIII4RI~)~~~3)9~~~03~L~~0'11 I 7 15 11 13 5 18 I 31 ACTION SU~AS SP*SC~SIIV~CCWN AT.ACNMSNT 4PRQ4 PRIAISCCAIP, CQPIPCNI 4T TAXXN AC.IQN CN PLANT 1 STIICQ>>QVIIS i@2 SUSMIT i co PCAV Siia$UPPIJXil IIANUPA<<,UASA QISQ<<S LIS L'JS~0 iic LES II'S I<<JI<<5 36 41 43 44 41 CAUS" OBSCRII'TIOiu AiuOCORRB) iIVB ACilOiuS Qi o Some of these motor o erators have been assembled with the locking nut"staked" improperly.
REPORTABLE OCCURRENCE 335-78-29 ST. LUCIE UNIT 1 DATE OF OCCURRENCE:   JULY 28, 1978 TECHNICAL SPECIFICATION   6.9.1.9.C MOTOR OPERATED VALVES The attached   Licensee Event Report is being submitted     in       accordance with Technical Specification 6.9 to provide 30-day notification of the subject occurrence.
installed valves with improperly staked locking nuts have been or will be staked correctly.
Very   truly yours,
I 6 3 I IC I VI~1 5 ATUS Ri)CVI8 II<<33ISR STATVS E-0 0-NA I:"'JS~I'S~1 IC IX I3 44 ACTIVITV CQNT44T RSLPASSO CP ASLXASS AvovygQP ACTIv)TT QXS I Q22~~QXA 1 3 7 IO If 44!SASC'uiiaL XX)QSVASS ,uvsa, Tvcs QXSCA)p~cNQ.
  .
I~'~~~QS'UQX'~
RB D. Schmidt Vice President Power Resources MAS/sn Attachment cc:   Harold F. Reis, Esquire Director, Office of Inspection and Enforcement (30)
3 7)\ASCNNXL IN7UA)83'iuA eA<<8!CA)P Ti C N, i 0)'))i 0im''IPii N813)CO CP CISCQvSRv OISCQVXR'V CSSCA)STION
Director, Office of Management Information and Program Control (3) 78248QJ33 PEOPLE     .. SERVING PEOPLE
~22 LD'QC: Notified by NSSS veii5or 4$NA LQCAT!ou OP ASL~X Q28 45 58!)7 7 Il$$QP CR QANACX'TO!ICPU~I
 
.)Pc~83C<<R))TICN WQX 7 Io NJSIJC:~~SSVXQ 78iCP)PT:CN GS~f 44 7~iii4$1A 4 PIIss" P-R M.A.SCHOPPMAN 34 I IRC USB CNLT j I)I i I[I 68 30 p>>cuBI 305-552-3802 REPORTABLE OCCURREN 335-78-29 , Licensee Event Repor'a e Two ADDITIONAL EVENT DESCRIPTION and PROBABLE CONSEQUENCES Our NSSS vendor notified us that another plant had experienced a motor operated valve (MOV)failure and that we had some safety-related MOV's with a potential for the same failure.After inves-tigation, other suspect MOV's were indentified in safety-related systems not supplied by the NSSS vendor.All suspect safety-re-lated MOV's outside containment were inspected and repaired if necessary.
iuFc FQRM X88                                                                                                                                   U.*NUCLSAR RBGULATORY C                        IIMIS)CION
All suspect safety-related MOV's inside containment will be inspected and, if necessaiy, repaired at.the first shutdown of sufficient length, but no later than the next refuels:ng (now scheduled'or.-April, 1979)It should be noted that of the 10 such operators insid'e containment, 4 are locked open and de-energized during power.operation (per Technical Specifications), 4 are locked closed and never opened'uri.ng power operation and.two (normally open,and not cycled)'ave no.safety-related function at power.Al-though we have had no failures during 3 years of testing and opera-tions, there is a potential for failure so this report is being made in accordance with Specification 6.9.1.C.'ADDITIONAL CAUSE DESCRIPTION and CORRECTIVE ACTIONS Some of these motor-operators have been assembled by valve vendors with the operator locking nut"staked" improperly.
  !7 77!
The locking nut keeps the stem nut, which connects the motor drive sleeve to the valve stem, from moving axially.Such movement could disengage the stem nut from the valve stem and drive sleeve, thus rendering the valve inoperable.
LlCEIXSEE EVE!MT REPORT
Installed valves with improperly staked locking nuts have been or will be staked correctly as noted in the Event Description.}}
                                                                                                    '~0~i'                                Q, I           I   I     I                     (PLSASB PRINT OR TYPB ALLRBCUIRSD INFORSIATIONI 1
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  ~ol;                                                                                                                                                                            Q                Q 1                          I 'C44588 COOK                   ,.QT,                           IJCXINSX I'I)44)dail                   15       5     ) CS458 TV)4 IU               51   Ai   58 CAN'
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                          ":::il"'0       5)7           di
                                                                                    "
CCCXXT NVIISSA
                                                                                        '
67       SVSNT<<ATX                     15       A   !CAT O*TX             38 BVB)uTOBSCRIPTION 'NO PROBABL= CO'ISBCUBNC-S                                       QIQ
  ~OI    2              Our NSSS vendor                                       notified               us     that         we had a               potential problem                                 .
  ~o   >>                 with certain motor o crated valves (MOVs). All sus ect.
safety-related MOVs outside containment were inspected and,
                  ,"..if 'necessary, repaired.;.All suspect safety-related MOVs inside containment will be inspected and,                                                                                   if       necessary,
  ~o!1                   re aired at the first shutdown of sufficient length, but no later than the next refueling.
IILJIIS iilc 04S'~1>>0 SY5TXV               CAUSX         CAU58                                                           C~P.             VALVS C OX                 CQCS         SUSC<<08                       )')PCiiaiiT COOS Icc C                                  SUSC<<QX         $ I'SCQCS
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                                                                                                ~0 9                                                                                  ~0
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                                                                ~             ~                                         AT.ACNMSNT           4PRQ4       PRIAISCCAIP,                 CQPIPCNI 4T TAXXN         AC. IQN                 CN PLANT             1 STIICQ                   >>QVIIS             SUSMIT i co       PCAV Siia         $ UPPIJXil             IIANUPA<<,UASA LIS L'JS i@2 QISQ<<S I<<JI                                 <<5                   36                                             41 LES II 'S 43                                   44                   41 CAUS" OBSCRII'TIOiu AiuOCORRB) iIVB ACilOiuS                                 Qi o               Some of these motor o erators have been assembled with the locking nut "staked" improperly. installed valves with improperly staked locking nuts have been or                                                                                       will be                 staked correctly.
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                    $ $ QP   CR QANACX'TO!ICPU~I
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REPORTABLE OCCURREN     335-78-29
'aLicensee
,
e Two Event Repor ADDITIONAL EVENT DESCRIPTION and PROBABLE CONSEQUENCES Our NSSS vendor notified us that another plant had experienced a motor operated valve (MOV) failure and that we had some safety-related MOV's with a potential for the same failure. After inves-tigation, other suspect MOV's were indentified in safety-related systems not supplied by the NSSS vendor. All suspect safety-re-lated MOV's outside containment were inspected and repaired necessary.
if All suspect safety-related MOV's inside containment will be inspected and,   if necessaiy, repaired at. the first shutdown of sufficient length, but no later than the next refuels:ng (now scheduled'or.-April, 1979)     It should be noted that of the 10 such operators insid'e containment, 4 are locked open and de-energized during power. operation (per Technical Specifications), 4 are locked closed and never opened'uri.ng power operation and. two (normally open,and not cycled)'ave no. safety-related function at power. Al-though we have had no failures during 3 years of testing and opera-tions, there is a potential for failure so this report is being made in accordance with Specification 6.9.1.C.
  'ADDITIONAL CAUSE DESCRIPTION and CORRECTIVE ACTIONS Some of these motor-operators     have been assembled by valve vendors with the operator locking nut "staked" improperly. The locking nut keeps the stem nut, which connects the motor drive sleeve to the valve stem, from moving axially. Such movement could disengage the stem nut from the valve stem and drive sleeve, thus rendering the valve inoperable. Installed valves with improperly staked locking nuts have been or will be staked correctly as noted in the Event Description.}}

Revision as of 06:29, 21 October 2019

LER 1978-025-00 for St. Lucie Unit 1, on 07/28/78 Concerning Notification by Applicant'S Vendor of Potential Problem with Certain Motor Operated Valves
ML18127A649
Person / Time
Site: Saint Lucie NextEra Energy icon.png
Issue date: 08/25/1978
From: Schmidt A
Florida Power & Light Co
To: O'Reilly J
NRC/RGN-II, NRC/IE
References
PRN-LT-78-237 LER 1978-025-00
Download: ML18127A649 (6)


Text

dk REGULATORY INFORMATlON DISTRIBUTION SYSTEM (BIDS>

DISTRIBUTION FOR INCOMING MATERIAL 50-335 REC: OREILLY J P DOCDATE: 08l25/78 NRC DATE RCVD: 09/05/78 DGCTYPE: LETTER NQTAR IZED: NO COPIES RECEIVED

SUBJECT:

LTR 1 ENCL 1 FORWARD1NG LICENSEE EVENT REPT (RG 50-335/78-029) ON 07/28/78 CONCERNING NOTIFICATION BY APPLICANT"S VENDQR OF POTENTIAL PROBLEM WITI-I CERTAIN MOTOR OPERATED VALVES... WlATT.

PLANT NAME: ST LUClE Ni REVIEWER INITIAL: X JM 4~k<lHt44H~+++4H~~~>H~ DI TRIBUTION 0,- THIS MAT-RIAL IS AS DISTRIBUTOR FOLLOWS INITIAL: ~

4+>+>>o>~~+>>>~~~+

INCIDENT REPORTS (DISTRIBUTION CODE A002)

FOR ACTION: BR C<%W/4 ENCL INTERNAL: - ILE~'~~W/ENCL NRC PDRc~~~W/ENCL

-HHa /g MIPC+~W/3 ENCL I 8c C SYSTEMS BR++W/ENCL EMERGENCY PLAN BR~<lJ/ENCL NQVAK/CHECK~~4lW/ENCL EEB~~~W/ENCL AD FOR ENG'.~.~W/ENCL PLANT SYSTEMS BR<<lJ/ENCL I IANAUER~H~W/ENCL

~

AD FOR PLANT SYSTEMS>~W/ENCL AD FOR SYS Sc PROJ~%W/ENCL REACTOR SAFETY BR<4W/ENCL ENGINEERING BR+4W/ENCI VOLLMER/BUNCH++W/ENCL I'REGER/J. CGLL INS~~W/ENCL POIJER SYS BR++W/ENCL K SEYFRIT/IE+>W/ENCL EXTERNAI: LPDR'S FT PIERCEi FL.~<W/ENCL NS I C4F4: W/ENCL ACRS CAT B4".FW/16 ENCL DISTRIBUTION: LTR 44 ENCL 44 CQNTROL NBI a'782480/.33 SIZE: iP+iP+1P /le 't@

. 8$ %0H." H 0f CHl%8l %4%6f+%8Hf NHl %Sf SHHF 3HHf )HHf wc Rl % 0 ~

THE END

I FLORIDA POWER S<<LIGHT QOII<<IPANy August 25, 1978 PRN-LZ-78-2c3>7 P

Mr. James P. O'Reilly, Director, Region Office of Inspection and Enforcement II <<N <<(ie

~

U.S. Nuclear Regulatory Commission <<>1 230 Peachtree Street, N.N. Suite 1217 Atlanta, Georgia 30303 Pl C/l

Dear Mr. O'Reilly:

REPORTABLE OCCURRENCE 335-78-29 ST. LUCIE UNIT 1 DATE OF OCCURRENCE: JULY 28, 1978 TECHNICAL SPECIFICATION 6.9.1.9.C MOTOR OPERATED VALVES The attached Licensee Event Report is being submitted in accordance with Technical Specification 6.9 to provide 30-day notification of the subject occurrence.

Very truly yours,

.

RB D. Schmidt Vice President Power Resources MAS/sn Attachment cc: Harold F. Reis, Esquire Director, Office of Inspection and Enforcement (30)

Director, Office of Management Information and Program Control (3) 78248QJ33 PEOPLE .. SERVING PEOPLE

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safety-related MOVs outside containment were inspected and,

,"..if 'necessary, repaired.;.All suspect safety-related MOVs inside containment will be inspected and, if necessary,

~o!1 re aired at the first shutdown of sufficient length, but no later than the next refueling.

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REPORTABLE OCCURREN 335-78-29

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e Two Event Repor ADDITIONAL EVENT DESCRIPTION and PROBABLE CONSEQUENCES Our NSSS vendor notified us that another plant had experienced a motor operated valve (MOV) failure and that we had some safety-related MOV's with a potential for the same failure. After inves-tigation, other suspect MOV's were indentified in safety-related systems not supplied by the NSSS vendor. All suspect safety-re-lated MOV's outside containment were inspected and repaired necessary.

if All suspect safety-related MOV's inside containment will be inspected and, if necessaiy, repaired at. the first shutdown of sufficient length, but no later than the next refuels:ng (now scheduled'or.-April, 1979) It should be noted that of the 10 such operators insid'e containment, 4 are locked open and de-energized during power. operation (per Technical Specifications), 4 are locked closed and never opened'uri.ng power operation and. two (normally open,and not cycled)'ave no. safety-related function at power. Al-though we have had no failures during 3 years of testing and opera-tions, there is a potential for failure so this report is being made in accordance with Specification 6.9.1.C.

'ADDITIONAL CAUSE DESCRIPTION and CORRECTIVE ACTIONS Some of these motor-operators have been assembled by valve vendors with the operator locking nut "staked" improperly. The locking nut keeps the stem nut, which connects the motor drive sleeve to the valve stem, from moving axially. Such movement could disengage the stem nut from the valve stem and drive sleeve, thus rendering the valve inoperable. Installed valves with improperly staked locking nuts have been or will be staked correctly as noted in the Event Description.