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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20046C0661993-07-30030 July 1993 LER 92-009-01:on 920910,deficiencies Discovered During Dynamic Testing of Motor Operated Valves in Response to Generic Ltr 89-10.MOVs W/Deficiencies Modified or Repaired. W/930730 Ltr ML20046B6011993-07-26026 July 1993 LER 93-004-00:on 930428,plant Entered Mode 2 W/Afw Pump Turbine Main Steam Line Crossover Check Valve MS735 in Open Position.Caused by Inappropriate Use of Engineering Judgement.Valve MS735 closed.W/930726 Ltr ML20045D2451993-06-17017 June 1993 LER 93-003-00:on 930520,plant Experienced Trip from Approx & Continuity Between Fuse & Fuseholder Lost,Resulting in Loss of Selected RCS Average Temp Input to Ics.Faulty Fuse Cap & Fuse replaced.W/930617 Ltr ML20044B1681990-07-10010 July 1990 LER 90-002-01:on 900126,reactor Coolant Pump Current Monitor Inputs to Sfrcs ACH1 & Reactor Pressure Sys Channel 1 Experienced Reactor Trip.Probably Caused by Inadequate Test Switches & Isolation plug.W/900710 Ltr ML20043H3201990-06-18018 June 1990 LER 90-010-00:on 900518,station Experienced Inadvertent Safety Features Actuation Signal Level 1-4 Actuation W/Injection of 1,000 Gallons of Borated Water.Caused by Loss of 120-volt Ac Bus Y3.W/900618 Ltr ML20043B5711990-05-25025 May 1990 LER 90-008-00:on 900425,safety Features Actuation Sys Level 1 Actuation Occurred,Resulting in Trip of Containment Radiation Monitors.Caused by High Radiation Fields While Lifting Core Support Assembly.Mod initiated.W/900525 Ltr ML20043B8051990-05-25025 May 1990 LER 90-009-00:on 900426,source-check of Station Vent Radiation Monitors Not Performed Per Tech Spec 3.3.3.10. Caused by Use of Outmoded Light Emitting Dioide as Check Source.Source Check Procedures revised.W/900525 Ltr ML20042F2811990-05-0303 May 1990 LER 90-007-00:on 900403,inadvertent,inconsequential Safety Features Actuation Signal Occured While Defueled.Caused by Incidental Contact W/Monitor in Containment.Temporary Barriers Built Around monitors.W/900503 Ltr ML20042F2791990-05-0303 May 1990 LER 90-006-00:on 900403,station Experienced Safety Features Actuation Sys Levels 1 Through 5 Actuation.Caused by Contact W/Breaker Switch HAAE2 in High Voltage Switchgear Room 2. Meetings Held W/Craft personnel.W/900503 Ltr ML20042E4891990-04-16016 April 1990 LER 90-005-00:on 900314,determined That Some Class 1E Circuits That Pass Through Containment Electrical Penetrations Do Not Have Adequate Backup Fault Protection. Caused by Inadequate Design control.W/900416 Ltr ML20012D0341990-03-19019 March 1990 LER 90-004-00:on 900217,fuel Assembly Moved in Spent Fuel Pool While Emergency Ventilation Inoperable.Caused by Personnel Error.Personnel Involved Counseled & Subj LER Part of Required reading.W/900319 Ltr ML20012C7151990-03-14014 March 1990 LER 90-003-00:on 900212,station Entered Mode 6,refueling,w/o Operable Audible Source Range Indication.Caused by Personnel Error.Individual counseled.W/900314 Ltr ML20012B4851990-03-0606 March 1990 LER 83-039/03X-2:on 830726,discovered That Handwheel for Inner Door of Personnel Airlock in Shut Position & Partially Opened.Caused by Excessive Use of Door During Outages.Door Repaired & Returned to Operable status.W/900306 Ltr ML20011F3831990-02-26026 February 1990 LER 90-002-00:on 900126,reactor Tripped from 73% Power. Caused by Spurious Reactor Coolant Pump Monitor Signal Indicating Only One Pump Running in Each Loop.Pump Seal to Be Replaced During Sixth Refueling outage.W/900226 Ltr ML20006E6861990-02-20020 February 1990 LER 90-001-00:on 900118,reactor Protection Sys Channel 2 Bypassed Temporarily During Performance of DB-MI-03207. Caused by Inadequate Procedure Re Inoperable Channel Removal.Procedure SP1105.02 revised.W/900220 Ltr ML20011E2251990-01-30030 January 1990 LER 86-032-01:on 860802,inadvertent Start of High Pressure Injection Pump 1-2 Occurred.Caused by Open Relay Coil. Failed Relay Replaced & Procedure Change Initiated. W/900130 Ltr ML20005G1091990-01-0909 January 1990 LER 89-015-01:on 891026,concluded That Transmitter Was Out of Tolerance When Reactor Protection Sys Channel 2 Returned to Operable Status on 890924.Caused by leak-by in Instrument Manifold.Transmitter Recalibr successfully.W/900109 Ltr ML20042D4011990-01-0202 January 1990 LER 89-010-01:on 890612,control Room Ventilation Sys Declared Inoperable Due to Compressor High Pressure Trips. Caused by Tripping of Refrigerant Pressure Switch on High Pressure.Switch Reset & Sys retested.W/900102 Ltr ML19354D7361989-12-22022 December 1989 LER 89-018-00:on 891123,hydrogen Dilution Blower 1-1 Casing Drain Line Broke Off at Casing,Declaring Blower Inoperable. Caused by Drain Line Being Accidentally Stepped On.Drain Removed & Pipe Plug installed.W/891222 Ltr ML19332F8951989-12-13013 December 1989 LER 89-017-00:on 891113,containment Spray Pump 1-1 Inadvertently Started During Monthly Functional Test in Safety Features Actuation Sys (Sfas) Channel 1.Caused by Failed Relay in Sfas Channel 3.Relay replaced.W/891213 Ltr ML19332E7521989-12-0404 December 1989 LER 89-016-00:on 890917,unplanned Release of Radioactive Resin to Onsite Settling Basin Occurred.Caused by Personnel Error.Standing Order 89-051 Generated on 890920 to Direct Use of Working Copy of procedures.W/891204 Ltr ML19332D3111989-11-27027 November 1989 LER 89-015-00:on 890924,RCS Flow Transmitter Out of Tolerance When Reactor Protection Sys Channel 2 Returned to Operable Status.Caused by leak-by in Instrument Manifold Seen as Zero Shift.Transmitter recalibr.W/891127 Ltr ML19324C2081989-11-10010 November 1989 LER 89-014-00:on 891011,plastic Sheeting Blocked Off Fire Detectors in Auxiliary Feedwater Pump 1-1 Room & High Voltage Switchgear Room B,Making Fire Detectors Inoperable. Caused by Personnel Oversight.Event reviewed.W/891110 Ltr ML19325D4671989-10-16016 October 1989 LER 89-004-01:on 890411,determined That Circulating Water Line Break Would Result in Loss of Svc Water as Result of Concerns Raised on 890206.Cause Unknown.Standing Order 89-026 in Place to Plug Floor drains.W/891016 Ltr ML19325C8531989-10-13013 October 1989 LER 89-013-00:on 890913,hourly Fire Watch Patrol Exceeded Allowed Interval,Violating Tech Spec 3.7.10,Action a.2. Caused by Personnel Error.Individual Counseled & Event Info Distributed to Fire Watch personnel.W/891013 Ltr ML20024E2591983-08-0101 August 1983 LER 83-033/03L-0:on 830620,fire Detection Zone Reactor Coolant Pump 1-2,containment Level 603 Ft Alarmed & Could Not Be Reset.Caused by Faulty Detector String.Zone Will Be Restored During Next Refueling outage.W/830801 Ltr ML20024B8351983-07-0101 July 1983 LER 83-028/03L-0:on 830603 & 17,fuel Handling Area Radiation Monitors RE8446 & 7 Found Deenergized.Caused by Blown Radiation Monitoring Cabinet Fuse.Fuse replaced.W/830701 Ltr ML20024B0471983-06-21021 June 1983 LER 83-026/03L-0:on 830524,one Half Channel Trip in Steam & Feedwater Rupture Control Sys (Sfrcs) Channel 2 Received. Caused by Component Failure.Input Buffer replaced.W/830621 Ltr ML20024A3621983-06-0909 June 1983 LER 83-024/03L-0:on 830511,while Starting Up from 830510 Reactor Trip,Quadrant Power Tilt in Quadrant Yz Exceeded Tech Spec steady-state Limit.Caused by Inherent Design of B&W NSSS & Negative Moderator Temp coefficient.W/830609 Ltr ML20024A5341983-06-0808 June 1983 LER 83-023/03L-0:on 830510,120-volt Ac Essential Bus Y4 Lost,Resulting in Deenergizing Reactor Protection & Safety Features Actuation Sys Channel 4.Caused by Blown Fuse in Inverter YV4.Power Restored to bus.W/830608 Ltr ML20024A5481983-06-0707 June 1983 Revised LER 83-002/03X-2:on 830115,18,0409,10 & 0510,RCS Dose Equivalent I-131 Exceeded Tech Spec Limit.Caused by Slight Fission Product Leakage Through Fuel Cladding.Level of I-131 monitored.W/830607 Ltr ML20023D9051983-05-26026 May 1983 LER 83-027/03L-0:on 830428,valve RC240B Would Not Close W/O Repeated Signals from Control Room.Caused by Valve Operator Torquing Out Due to Dirty & Improperly Lubricated Stem.Stem Cleaned & Torque Switch reset.W/830526 Ltr ML20023C3241983-05-0505 May 1983 LER 83-016/03L-0:on 830407,determined That Amplifier of Startup Level Transmitter LT-SP9A3 for Steam Generator 1-2 Failed.Caused by Component Failure within Amplifier. Amplifier Replaced ML20023C3021983-05-0505 May 1983 Revised LER 83-002/03X-1:on 830115,RCS Dose Equivalent I-131 Exceeded Tech Spec Limit of 1.0 Uci/Gm.Caused by Leakage of Fission Products Through Fuel cladding.I-131 Monitored Until Level Dropped ML20028E9581983-01-19019 January 1983 LER 82-068/03L-0:on 821220,core Imbalance Vs Core Power Limit Computer Alarm C963 Inoperable.Caused by Mistake in Alarm Subroutine.Alarm Statement Corrected So Limits & Value for Imbalance Scaled Same ML20028D2291983-01-0707 January 1983 Revised LER 81-045/03X-1:on 810730,after Unit Trip,Three Action Statements Entered.Auxiliary Feedwater Pump 1-2 Did Not Operate Properly.Shield Bldg Integrity Lost When Panel Blown Out.Main Steam Safety Valve Lifted at Low Setpoint ML20028C1231983-01-0303 January 1983 LER 82-064/03L-0:on 821129,decay Heat Cooler Component Cooling Water Outlet Valve on CCW Train 1 Would Not Open. Caused by Mfg Error.Flanged Bearing Missing from Actuator Mounting Plate.Flanged Bearing Installed on 821215 ML20028C3111982-12-30030 December 1982 Revised LER 81-031/03X-6:on 810512,following Reactor Trip, RCS Sample Level Peaked Above Microcurie Limit.Other Iodine Spikes Occurred 810730,0902,1016 & 23 & 1228.Caused by Slight Leakage of Fission Products Through Fuel Cladding ML20028C1971982-12-30030 December 1982 Revised LER 82-045/03X-1:on 820904 & 1203,auxiliary Feedwater Pump 1-1 Suction Valve FW786 Closed for No Apparent Reason W/O Operator Touching Close Button.Cause Unknown.Valve FW786 Reopened Upon Discovery ML20028C2591982-12-30030 December 1982 LER 82-065/03L-0:on 821201,discovered That Control Room Not Placed in Recirculation Mode within 1 H of Ventilation Sys Chlorine Detector Being Taken Out of Svc.On 821203,chlorine Detector Failed.Caused by Personnel Error ML20028B0291982-11-19019 November 1982 LER 82-054/03L-0:on 821021,Door 107 to Radiation Equipment Found Partially Open & Blocked by Hose When Personnel Attempted to Perform Routine Flush on RE-1878.Caused by Personnel Error.Personnel Counseled ML20028B2281982-11-16016 November 1982 LER 82-053/03L-0:on 821018,half Trip Alarm on Steam & Feedwater Rupture Control Sys Channel 2 Received Due to Failure of Steam Generator Level Instrument Cabinet Channel 2,24-volt Dc Power Supply.Caused by Component Failure ML20027E7891982-11-0404 November 1982 Revised LER 82-052/03X-1:on 820928,reactor Quadrant Power Tilt in Wx Quadrant Exceeded Tech Specs.Caused by Xenon Oscillation Producing Large Negative Imbalance.Control Rod Group 7 Borated Out to Reduce Negative Imbalance ML20027C9551982-10-19019 October 1982 LER 82-049/03L-0:on 820920 & 22,Channels 2 & 3 on Containment post-accident Radiation Monitor Re 4597BA Were Reading High.Caused by Problem in Microprocessor Software. New Set of Software Installed & Faulty Actuator Replaced ML20027C5381982-10-0404 October 1982 LER 82-045/03L-0:on 820904,auxiliary Feedwater Pump 1-1, Suction Valve FW786 Observed Closed for No Apparent Reason W/O Operator Touching Close Button.Cause Unknown. Valve Reopened ML20027A9471982-09-0707 September 1982 LER 82-036/03L-0:on 820808,hole Discovered in Fire Barrier Wall Above Door 309.Caused by Snubber EBD125R43 Penetrating Wall Through Pipe Shell.Hole Left by Workers After Work on Snubbers.Fire Watch Established & Hole Filled ML20052G6651982-05-0707 May 1982 LER 82-020/03L-0:on 820409,while in Mode 6,station Experienced Loss of 120-volt Ac Distribution Panel Y2.Caused by Blown YV2 Inverter Fuse When Short to Ground Occurred During Maint on Control Room Emergency Ventilation Sys ML20052E6231982-04-30030 April 1982 LER 82-019/01T-0:on 820426,some Steam Generator Tubes Adjacent to Auxiliary Feedwater Header Showed Potential Interaction W/Header Support Sys.Header Found Insecurely Fastened & Damaged.Cause & Corrections Being Investigated ML20052E8761982-04-29029 April 1982 LER 82-016/03X-1:on 820312,door 108 Found W/Both Door Closure Mechanisms Broken.Caused by Improper Operation of Door Closure Mechanisms by Personnel.Mechanisms Temporarily Repaired & New Parts Ordered ML20052C4151982-04-23023 April 1982 LER 82-018/03L-0:on 820326,electrician Cut High Voltage Cable on Source Range Detector NI-2,while Working in Containment Penetration Box P1L1L1.Caused by Problem in Coordination of Work Performed.Cut Cable Reconnected 1993-07-30
[Table view] Category:RO)
MONTHYEARML20046C0661993-07-30030 July 1993 LER 92-009-01:on 920910,deficiencies Discovered During Dynamic Testing of Motor Operated Valves in Response to Generic Ltr 89-10.MOVs W/Deficiencies Modified or Repaired. W/930730 Ltr ML20046B6011993-07-26026 July 1993 LER 93-004-00:on 930428,plant Entered Mode 2 W/Afw Pump Turbine Main Steam Line Crossover Check Valve MS735 in Open Position.Caused by Inappropriate Use of Engineering Judgement.Valve MS735 closed.W/930726 Ltr ML20045D2451993-06-17017 June 1993 LER 93-003-00:on 930520,plant Experienced Trip from Approx & Continuity Between Fuse & Fuseholder Lost,Resulting in Loss of Selected RCS Average Temp Input to Ics.Faulty Fuse Cap & Fuse replaced.W/930617 Ltr ML20044B1681990-07-10010 July 1990 LER 90-002-01:on 900126,reactor Coolant Pump Current Monitor Inputs to Sfrcs ACH1 & Reactor Pressure Sys Channel 1 Experienced Reactor Trip.Probably Caused by Inadequate Test Switches & Isolation plug.W/900710 Ltr ML20043H3201990-06-18018 June 1990 LER 90-010-00:on 900518,station Experienced Inadvertent Safety Features Actuation Signal Level 1-4 Actuation W/Injection of 1,000 Gallons of Borated Water.Caused by Loss of 120-volt Ac Bus Y3.W/900618 Ltr ML20043B5711990-05-25025 May 1990 LER 90-008-00:on 900425,safety Features Actuation Sys Level 1 Actuation Occurred,Resulting in Trip of Containment Radiation Monitors.Caused by High Radiation Fields While Lifting Core Support Assembly.Mod initiated.W/900525 Ltr ML20043B8051990-05-25025 May 1990 LER 90-009-00:on 900426,source-check of Station Vent Radiation Monitors Not Performed Per Tech Spec 3.3.3.10. Caused by Use of Outmoded Light Emitting Dioide as Check Source.Source Check Procedures revised.W/900525 Ltr ML20042F2811990-05-0303 May 1990 LER 90-007-00:on 900403,inadvertent,inconsequential Safety Features Actuation Signal Occured While Defueled.Caused by Incidental Contact W/Monitor in Containment.Temporary Barriers Built Around monitors.W/900503 Ltr ML20042F2791990-05-0303 May 1990 LER 90-006-00:on 900403,station Experienced Safety Features Actuation Sys Levels 1 Through 5 Actuation.Caused by Contact W/Breaker Switch HAAE2 in High Voltage Switchgear Room 2. Meetings Held W/Craft personnel.W/900503 Ltr ML20042E4891990-04-16016 April 1990 LER 90-005-00:on 900314,determined That Some Class 1E Circuits That Pass Through Containment Electrical Penetrations Do Not Have Adequate Backup Fault Protection. Caused by Inadequate Design control.W/900416 Ltr ML20012D0341990-03-19019 March 1990 LER 90-004-00:on 900217,fuel Assembly Moved in Spent Fuel Pool While Emergency Ventilation Inoperable.Caused by Personnel Error.Personnel Involved Counseled & Subj LER Part of Required reading.W/900319 Ltr ML20012C7151990-03-14014 March 1990 LER 90-003-00:on 900212,station Entered Mode 6,refueling,w/o Operable Audible Source Range Indication.Caused by Personnel Error.Individual counseled.W/900314 Ltr ML20012B4851990-03-0606 March 1990 LER 83-039/03X-2:on 830726,discovered That Handwheel for Inner Door of Personnel Airlock in Shut Position & Partially Opened.Caused by Excessive Use of Door During Outages.Door Repaired & Returned to Operable status.W/900306 Ltr ML20011F3831990-02-26026 February 1990 LER 90-002-00:on 900126,reactor Tripped from 73% Power. Caused by Spurious Reactor Coolant Pump Monitor Signal Indicating Only One Pump Running in Each Loop.Pump Seal to Be Replaced During Sixth Refueling outage.W/900226 Ltr ML20006E6861990-02-20020 February 1990 LER 90-001-00:on 900118,reactor Protection Sys Channel 2 Bypassed Temporarily During Performance of DB-MI-03207. Caused by Inadequate Procedure Re Inoperable Channel Removal.Procedure SP1105.02 revised.W/900220 Ltr ML20011E2251990-01-30030 January 1990 LER 86-032-01:on 860802,inadvertent Start of High Pressure Injection Pump 1-2 Occurred.Caused by Open Relay Coil. Failed Relay Replaced & Procedure Change Initiated. W/900130 Ltr ML20005G1091990-01-0909 January 1990 LER 89-015-01:on 891026,concluded That Transmitter Was Out of Tolerance When Reactor Protection Sys Channel 2 Returned to Operable Status on 890924.Caused by leak-by in Instrument Manifold.Transmitter Recalibr successfully.W/900109 Ltr ML20042D4011990-01-0202 January 1990 LER 89-010-01:on 890612,control Room Ventilation Sys Declared Inoperable Due to Compressor High Pressure Trips. Caused by Tripping of Refrigerant Pressure Switch on High Pressure.Switch Reset & Sys retested.W/900102 Ltr ML19354D7361989-12-22022 December 1989 LER 89-018-00:on 891123,hydrogen Dilution Blower 1-1 Casing Drain Line Broke Off at Casing,Declaring Blower Inoperable. Caused by Drain Line Being Accidentally Stepped On.Drain Removed & Pipe Plug installed.W/891222 Ltr ML19332F8951989-12-13013 December 1989 LER 89-017-00:on 891113,containment Spray Pump 1-1 Inadvertently Started During Monthly Functional Test in Safety Features Actuation Sys (Sfas) Channel 1.Caused by Failed Relay in Sfas Channel 3.Relay replaced.W/891213 Ltr ML19332E7521989-12-0404 December 1989 LER 89-016-00:on 890917,unplanned Release of Radioactive Resin to Onsite Settling Basin Occurred.Caused by Personnel Error.Standing Order 89-051 Generated on 890920 to Direct Use of Working Copy of procedures.W/891204 Ltr ML19332D3111989-11-27027 November 1989 LER 89-015-00:on 890924,RCS Flow Transmitter Out of Tolerance When Reactor Protection Sys Channel 2 Returned to Operable Status.Caused by leak-by in Instrument Manifold Seen as Zero Shift.Transmitter recalibr.W/891127 Ltr ML19324C2081989-11-10010 November 1989 LER 89-014-00:on 891011,plastic Sheeting Blocked Off Fire Detectors in Auxiliary Feedwater Pump 1-1 Room & High Voltage Switchgear Room B,Making Fire Detectors Inoperable. Caused by Personnel Oversight.Event reviewed.W/891110 Ltr ML19325D4671989-10-16016 October 1989 LER 89-004-01:on 890411,determined That Circulating Water Line Break Would Result in Loss of Svc Water as Result of Concerns Raised on 890206.Cause Unknown.Standing Order 89-026 in Place to Plug Floor drains.W/891016 Ltr ML19325C8531989-10-13013 October 1989 LER 89-013-00:on 890913,hourly Fire Watch Patrol Exceeded Allowed Interval,Violating Tech Spec 3.7.10,Action a.2. Caused by Personnel Error.Individual Counseled & Event Info Distributed to Fire Watch personnel.W/891013 Ltr ML20024E2591983-08-0101 August 1983 LER 83-033/03L-0:on 830620,fire Detection Zone Reactor Coolant Pump 1-2,containment Level 603 Ft Alarmed & Could Not Be Reset.Caused by Faulty Detector String.Zone Will Be Restored During Next Refueling outage.W/830801 Ltr ML20024B8351983-07-0101 July 1983 LER 83-028/03L-0:on 830603 & 17,fuel Handling Area Radiation Monitors RE8446 & 7 Found Deenergized.Caused by Blown Radiation Monitoring Cabinet Fuse.Fuse replaced.W/830701 Ltr ML20024B0471983-06-21021 June 1983 LER 83-026/03L-0:on 830524,one Half Channel Trip in Steam & Feedwater Rupture Control Sys (Sfrcs) Channel 2 Received. Caused by Component Failure.Input Buffer replaced.W/830621 Ltr ML20024A3621983-06-0909 June 1983 LER 83-024/03L-0:on 830511,while Starting Up from 830510 Reactor Trip,Quadrant Power Tilt in Quadrant Yz Exceeded Tech Spec steady-state Limit.Caused by Inherent Design of B&W NSSS & Negative Moderator Temp coefficient.W/830609 Ltr ML20024A5341983-06-0808 June 1983 LER 83-023/03L-0:on 830510,120-volt Ac Essential Bus Y4 Lost,Resulting in Deenergizing Reactor Protection & Safety Features Actuation Sys Channel 4.Caused by Blown Fuse in Inverter YV4.Power Restored to bus.W/830608 Ltr ML20024A5481983-06-0707 June 1983 Revised LER 83-002/03X-2:on 830115,18,0409,10 & 0510,RCS Dose Equivalent I-131 Exceeded Tech Spec Limit.Caused by Slight Fission Product Leakage Through Fuel Cladding.Level of I-131 monitored.W/830607 Ltr ML20023D9051983-05-26026 May 1983 LER 83-027/03L-0:on 830428,valve RC240B Would Not Close W/O Repeated Signals from Control Room.Caused by Valve Operator Torquing Out Due to Dirty & Improperly Lubricated Stem.Stem Cleaned & Torque Switch reset.W/830526 Ltr ML20023C3241983-05-0505 May 1983 LER 83-016/03L-0:on 830407,determined That Amplifier of Startup Level Transmitter LT-SP9A3 for Steam Generator 1-2 Failed.Caused by Component Failure within Amplifier. Amplifier Replaced ML20023C3021983-05-0505 May 1983 Revised LER 83-002/03X-1:on 830115,RCS Dose Equivalent I-131 Exceeded Tech Spec Limit of 1.0 Uci/Gm.Caused by Leakage of Fission Products Through Fuel cladding.I-131 Monitored Until Level Dropped ML20028E9581983-01-19019 January 1983 LER 82-068/03L-0:on 821220,core Imbalance Vs Core Power Limit Computer Alarm C963 Inoperable.Caused by Mistake in Alarm Subroutine.Alarm Statement Corrected So Limits & Value for Imbalance Scaled Same ML20028D2291983-01-0707 January 1983 Revised LER 81-045/03X-1:on 810730,after Unit Trip,Three Action Statements Entered.Auxiliary Feedwater Pump 1-2 Did Not Operate Properly.Shield Bldg Integrity Lost When Panel Blown Out.Main Steam Safety Valve Lifted at Low Setpoint ML20028C1231983-01-0303 January 1983 LER 82-064/03L-0:on 821129,decay Heat Cooler Component Cooling Water Outlet Valve on CCW Train 1 Would Not Open. Caused by Mfg Error.Flanged Bearing Missing from Actuator Mounting Plate.Flanged Bearing Installed on 821215 ML20028C3111982-12-30030 December 1982 Revised LER 81-031/03X-6:on 810512,following Reactor Trip, RCS Sample Level Peaked Above Microcurie Limit.Other Iodine Spikes Occurred 810730,0902,1016 & 23 & 1228.Caused by Slight Leakage of Fission Products Through Fuel Cladding ML20028C1971982-12-30030 December 1982 Revised LER 82-045/03X-1:on 820904 & 1203,auxiliary Feedwater Pump 1-1 Suction Valve FW786 Closed for No Apparent Reason W/O Operator Touching Close Button.Cause Unknown.Valve FW786 Reopened Upon Discovery ML20028C2591982-12-30030 December 1982 LER 82-065/03L-0:on 821201,discovered That Control Room Not Placed in Recirculation Mode within 1 H of Ventilation Sys Chlorine Detector Being Taken Out of Svc.On 821203,chlorine Detector Failed.Caused by Personnel Error ML20028B0291982-11-19019 November 1982 LER 82-054/03L-0:on 821021,Door 107 to Radiation Equipment Found Partially Open & Blocked by Hose When Personnel Attempted to Perform Routine Flush on RE-1878.Caused by Personnel Error.Personnel Counseled ML20028B2281982-11-16016 November 1982 LER 82-053/03L-0:on 821018,half Trip Alarm on Steam & Feedwater Rupture Control Sys Channel 2 Received Due to Failure of Steam Generator Level Instrument Cabinet Channel 2,24-volt Dc Power Supply.Caused by Component Failure ML20027E7891982-11-0404 November 1982 Revised LER 82-052/03X-1:on 820928,reactor Quadrant Power Tilt in Wx Quadrant Exceeded Tech Specs.Caused by Xenon Oscillation Producing Large Negative Imbalance.Control Rod Group 7 Borated Out to Reduce Negative Imbalance ML20027C9551982-10-19019 October 1982 LER 82-049/03L-0:on 820920 & 22,Channels 2 & 3 on Containment post-accident Radiation Monitor Re 4597BA Were Reading High.Caused by Problem in Microprocessor Software. New Set of Software Installed & Faulty Actuator Replaced ML20027C5381982-10-0404 October 1982 LER 82-045/03L-0:on 820904,auxiliary Feedwater Pump 1-1, Suction Valve FW786 Observed Closed for No Apparent Reason W/O Operator Touching Close Button.Cause Unknown. Valve Reopened ML20027A9471982-09-0707 September 1982 LER 82-036/03L-0:on 820808,hole Discovered in Fire Barrier Wall Above Door 309.Caused by Snubber EBD125R43 Penetrating Wall Through Pipe Shell.Hole Left by Workers After Work on Snubbers.Fire Watch Established & Hole Filled ML20052G6651982-05-0707 May 1982 LER 82-020/03L-0:on 820409,while in Mode 6,station Experienced Loss of 120-volt Ac Distribution Panel Y2.Caused by Blown YV2 Inverter Fuse When Short to Ground Occurred During Maint on Control Room Emergency Ventilation Sys ML20052E6231982-04-30030 April 1982 LER 82-019/01T-0:on 820426,some Steam Generator Tubes Adjacent to Auxiliary Feedwater Header Showed Potential Interaction W/Header Support Sys.Header Found Insecurely Fastened & Damaged.Cause & Corrections Being Investigated ML20052E8761982-04-29029 April 1982 LER 82-016/03X-1:on 820312,door 108 Found W/Both Door Closure Mechanisms Broken.Caused by Improper Operation of Door Closure Mechanisms by Personnel.Mechanisms Temporarily Repaired & New Parts Ordered ML20052C4151982-04-23023 April 1982 LER 82-018/03L-0:on 820326,electrician Cut High Voltage Cable on Source Range Detector NI-2,while Working in Containment Penetration Box P1L1L1.Caused by Problem in Coordination of Work Performed.Cut Cable Reconnected 1993-07-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K1231999-10-14014 October 1999 Revised Positions for DBNPS & Pnpp QA Program ML20217D5441999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Davis-Besse Nuclear Power Station.With ML20211R0811999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20211B0271999-08-13013 August 1999 SER Accepting Second 10-year Interval Inservice Insp Requests for Relief RR-A16,RR-A17 & RR-B9 for Plant, Unit 1 ML20210Q8541999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20209E6231999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20195K2871999-06-16016 June 1999 Safety Evaluation Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20195F4871999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20207E8011999-05-19019 May 1999 Non-proprietary Rev 2 to HI-981933, Design & Licensing Rept DBNPS Unit 1 Cask Pit Rack Installation Project ML20207F4351999-05-0404 May 1999 Rev 1 to DBNPS Emergency Preparedness Evaluated Exercise Manual 990504 ML20206M6341999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Davis-Besse Nuclear Station,Unit 1.With ML20205M2931999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Davis-Besse Nuclear Power Station.With ML20207J1461999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20199H5931999-01-20020 January 1999 Safety Evaluation Accepting Thermo-Lag Re Ampacity Derating Issues for Plant ML20204J6751998-12-31031 December 1998 1998 Annual Rept for Dbnps,Unit 1,PNPP,Unit 1 & BVPS Units 1 & 2 ML20199E2501998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20206B0101998-12-31031 December 1998 1998 Annual Rept for Firstenergy Corp, for Perry Nuclear Power Plant & Davis-Besse Nuclear Power Station.Form 10-K Annual Rept to Us Securities & Exchange Commission for Fiscal Yr Ending 981231,encl ML20205K5781998-12-31031 December 1998 Waterhammer Phenomena in Containment Air Cooler Swss ML20197J3441998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20195D0001998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20155B6781998-10-28028 October 1998 Safety Evaluation Accepting Proposed Reduction in Commitment Changes in QA Program Matl Receipt Insp Process ML20154H5801998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20151W1611998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Dbnps.With ML20237E3171998-08-21021 August 1998 ISI Summary Rept of Eleventh Refueling Outage Activities for Davis-Besse Nuclear Power Station ML20237B1681998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20236U5011998-07-23023 July 1998 Special Rept:On 980624,Unit 1 Site Damaged by Tornado & High Winds.Alert Declared by DBNPS Staff,Dbnps Emergency Response Facilities Activiated & Special Insp Team Deployed to Site by Nrc,As Result of Event ML20236R1441998-07-15015 July 1998 SER Related to Quality Assurance Program Description Changes for Davis-Besse Nuclear Power Station,Unit 1 ML20236N7451998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20236K3981998-06-30030 June 1998 SER Accepting in Part & Denying in Part Relief Requests from Some of ASME Section XI Requirements as Endorsed by 10CFR50.55a for Containment Insp for Davis-Besse Nuclear Power Station,Unit 1 ML20236K5131998-06-29029 June 1998 Safety Evaluation Accepting Proposed Alternate Emergency Operations Facility Location for Davis-Besse Nuclear Power Station,Unit 1 ML20248F7441998-05-31031 May 1998 Reactor Vessel Working Group,Response to RAI Regarding Reactor Pressure Vessel Integrity ML20249A4121998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20196B5221998-05-23023 May 1998 10CFR50.59 Summary Rept of Facility Changes,Tests & Experiments Dbnps,Unit 1 for 960602-980523 ML20236E7581998-05-19019 May 1998 Rev 0 to Davis-Besse Unit 1 Cycle 12 Colr ML20236N7501998-04-30030 April 1998 Rev 2 to Monthly Operating Rept for Apr 1998 for Davis-Besse Nuclear Power Station,Unit ML20247F6721998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Davis-Bess Nuclear Power Station,Unit 1 ML20249A4141998-04-30030 April 1998 Revised Monthly Operating Rept for Apr 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20217P8041998-04-0707 April 1998 11RFO OTSG ECT Insp Scope ML20216B4041998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20216C5131998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20202D3721998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20199G6321998-01-26026 January 1998 Rev 1 to Davis-Besse Unit 1,Cycle 11,COLR ML20198R4771998-01-13013 January 1998 SER Approving Second 10-year Interval Inservice Inspection Program Plan Requests for Relief for Davis-Besse Nuclear Power Station,Unit 1 ML20198K7931997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Davis-Besse Nuclear Power Station,Unit 1 ML20217K6401997-12-31031 December 1997 1997 Annual Rept First Energy ML20203A3931997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Davis-Besse Nuclear Power Plant,Unit 1 ML20198S5371997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Davis-Besse Nuclear Power Station ML20217H7701997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Davis-Besse Nuclear Power Station,Unit 1 ML20216H3261997-08-31031 August 1997 Monthly Operating Rept for August 1997 for DBNPS ML20217K0241997-07-31031 July 1997 Monthly Operating Rept for Jul 1997 for Davis Besse Nuclear Power Station,Unit 1 1999-09-30
[Table view] |
Text
NRd FORM 3'66 U. S. NUCLEAR REGULATORY COMMISSION (7 77)
LICENSEE EVENT REPORT (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)
CONTROL BLOCK: l t
l l l l l lh 6
lo l 18 l9 l 0 l H 7
l D l B l S l141 l@l LICENSEE CODE 15 0 l 0 l - l 0LICENSE l 0 l 0NUMBER l 0 l 0 l - l 0 l 025l@l26 4 l 1 l 1 l 1 l 1 l@l57 CAT LICENSE TYPE JO l l@
58 CON'T lolil 7 6 SC"Ce60 l L l@l 61 0 l 5 DOCKET l 0 l 0NUMBERl 0 l 3 l 4 l686 @l 69 0 lEVENT 1 l 115 DATE l 8 l 743 l@l0 75 l REPORT 6 l0 lDATE 7 l 8 l380l@
EVENT DESCRIPTION AND PROBABLE CONSEQUENCES O'o 2lg l (NP-33-83-03) On 1/15/83, 1/18/83, 4/9/83, 4/10/83, and 5/10/83, the Reactor Coolant ]
io ;3 ; ] System (RCS) Dose Equivalent I-131 exceeded the Technical Specification 3.4.8 limit ofl
[ o ,4 j l1.0 uCi/gm. The peak levels measured were: 2.67 uCi/gm on 1/15/83, 1.39 uCi/gm on l 2 Jg l 1/18/83 and 4/9/83, 1.95 uCi/gm on 4/10/83, and 1.16 uCi/gm on 5/10/83. There was no l l 016 l l danger to the health and safety of the public or station personnel. At no time did l
[ o l 7 l l the specific activity exceed the allowable limit of Tech Spec 3.4.8 which accommodates l io,g, lpossible iodine spiking phenomenon that may occur following a change in thermal power.l DE CODE S SC E COMPONENT CODE SUSCODE S E g
l Rl ' Cl@" W@ lC l@ l Fl Ul El Ll El X[@ ]@ ]@
,_ SEQUENTIAL OCCURRENCE REPORT R EVISION EVENT YE AR REPORT NO. CODE TYPE NO.
@ ~"LE u'M _R21I 81 RO3l22 L--j l 0l 01 21 l-l l 0l 3l [xj [_j l2 ;
23 24 26 27 28 M 30 31 32 KN AC O ON PL NT ME HOURS 22 SB ITT FOR 8. SUPPLI MANUFAC RER lZl@ b @ lZl@
33 34 35 l36 Zl@ lN lN IN I T l 37 40 b@ d@
43 42 l Nl g 43 lB l0 l1 l5 l g 44 47 CAUSE OESCRIPTION AND CORRECTIVE ACTIONS h l i l O l l The cause was a slight leakage of fission products through the fuel cladding. Some l li;il l leakage is normal following a reactor trip due to RCS temperature and pressure l
, , l changes. The I-131 level was monitored until it dropped below the Technical Specifi- l g l cation limit. l i 4 l l 7 8 9 80 STA S % POWER oTHER STATUS IS O RY DISCOVERY DESCRIPTION 32 R (,,,XJ@ @ l 0 l 0 l@l NA l l A l@l Per Table 4.4-4 of Tech Spec .4.8 l A TIVITY C TENT RELEASED 06 PELEASE AVOUNT OF ACTivlTY LOCATION OF RELEASE R [Zj 7 8 9
@ (3_jglNA 10 11 44 l l NA 45 80 l
PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION l 1 l 7 l l 0 l O l 0 l@l Z [@l' NA l so PERSONN E L INJU IEs 8306170429 830607 i a NUMBER l 0l 0 l 0 l@l NA DESCRIPTION @ PDR ADOCK 05000346 S PDR ,p $ l
'0S,5,OF 7y m OR 0 hAGE TO FACILITY
\
i 9 (_Zj@l NA l 7 18 9 to 80 NRC USE ONLY ,
tSSUE 1,2,,[p,,j [Nf@lDESCRIPTION NA l l((;[gl;;;;;lg 88 88 805 dVRs*83-006,'007,008,037,056 NAME OF PREPARER Lynn Richter PHONE: 419-259-5000. Ext. %4{
d TOLEDO
%ms EDISON June 7, 1983 Log No. K83-829 File: RR 2 (NP-33-83-03)
Docket No. 50-346 License No. NPF-3 Mr. James G. Keppler Regional Director, Region III Office of Inspection and Enforcement U. S. Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, Illinois 60137
Dear Mr. Keppler:
Enclosed are three copies of Revision 2 to Licensee Event Report 83-002, including revised supplemental information pages. The revisions to the report are indicated by a "2" in the left margin of each page.
Please destroy your previous copies of this report and replace with the attached revision.
Yours truly, f0 Terry D. Murray Station Superintendent Davis-Besse Nuclear Power Station TDM/ljk i
Enclosure l
l cc: Mr. Richard DeYoung, Director Orfice of Inspection and Enforcement Encl: 30 copies Mr. Norman Haller, Director l
l Office of Management and Program Analysis Encl: 3 copies
, Mr. Tom Peebles l NRC Resident Inspector Encl: 1 copy l
l JUN 131983 I
THE TOLEDO EDISON COMPANY EOISON PLAZA 300 MADISON AVENUE TOLEDO. OHIO 43652
TOLEDO EDISON COMPANY DAVIS-BESSE NUCLEAR POWER STATION UNIT ONE SUPPLEMENTAL INFORMATION FOR LER NP-33-83-03 2
DATE OF EVENT: January 15 and 18, 1983; April 9 and 10, 1983;
' May 10, 1983 FACILITY: Davis-Besse Unit 1 IDENTIFICATION OF OCCURRENCE: Reactor Coolant System (RCS) Dose Equiva-lent I-131 Exceeded Technical Specification Limits Conditions Prior to Occurrence: The unit was in Mode 3, with Power (MWT) = 0 and Load (Gross.MWE) = 0 Description of Occurrence: On January 15, 1983 after a reactor trip, the specific activity of the primary coolant exceeded the Technical Specifica-tion 3.4.8 limit of 1.0 pCi/gm Dose Equivalent I-131. The level peaked at 2.67 pCi/gm at 2004 hours0.0232 days <br />0.557 hours <br />0.00331 weeks <br />7.62522e-4 months <br /> on January 15, 1983.
A similar event occurred after a reactor trip on January 18, 1983 with the dose equivalent level peaking at 1.39 pCi/gm at 2301 hours0.0266 days <br />0.639 hours <br />0.0038 weeks <br />8.755305e-4 months <br />.
On April 9, 1983, at 0420 hours0.00486 days <br />0.117 hours <br />6.944444e-4 weeks <br />1.5981e-4 months <br />, following a power reduction to repair a
~
failed steam generator level transmitter, the Dose Equivalent I-131 exceeded the limit of Technical Specification 3.4.8. The level peaked at 1.39 pCi/gm at 0620 hours0.00718 days <br />0.172 hours <br />0.00103 weeks <br />2.3591e-4 months <br /> oa April 10, 1983.
I On May 10, 1983, following a reactor / turbine trip, the Dose Equivalent 2 I-131 exceeded the limit of Technical Specification 3.4.8. The level i peaked at 1.16 pCi/gm at 1323 hours0.0153 days <br />0.368 hours <br />0.00219 weeks <br />5.034015e-4 months <br /> on May 10, 1983.
The following information is supplied per reporting requirements:
Power History On January 15, 1983, reactor power was approximately 100% until a reactor / turbine trip at 1700 hours0.0197 days <br />0.472 hours <br />0.00281 weeks <br />6.4685e-4 months <br />.
Date Time Reactor Power 1/14/83 0000 hours0 days <br />0 hours <br />0 weeks <br />0 months <br /> 99.4%
1600 hours0.0185 days <br />0.444 hours <br />0.00265 weeks <br />6.088e-4 months <br /> 99.5%
1/15/83 1600 hours0.0185 days <br />0.444 hours <br />0.00265 weeks <br />6.088e-4 months <br /> 98.7%
1700 hours0.0197 days <br />0.472 hours <br />0.00281 weeks <br />6.4685e-4 months <br /> TRIP 4 r- -- - -- -. , ,, . . ~ ,
TOLEDO EDISON COMPANY DAVIS-BESSE NUCLEAR POWER STATION UNIT ONE .
SUPPLEMENTAL INFORMATION FOR LER NP-33-83-03 PAGE 2 On January 18, 1983, reactor power was approximately 100% until a reactor / turbine trip at 1925 hours0.0223 days <br />0.535 hours <br />0.00318 weeks <br />7.324625e-4 months <br />.
Date Time Reactor Power 1/16/83 1600 hours0.0185 days <br />0.444 hours <br />0.00265 weeks <br />6.088e-4 months <br /> 84.3%
1/17/83 0000 hours0 days <br />0 hours <br />0 weeks <br />0 months <br /> 87.3%
0800 hours0.00926 days <br />0.222 hours <br />0.00132 weeks <br />3.044e-4 months <br /> 97.9%
1600 hours0.0185 days <br />0.444 hours <br />0.00265 weeks <br />6.088e-4 months <br /> 99.2%
lfi8/83 0000 hours0 days <br />0 hours <br />0 weeks <br />0 months <br /> 99.3%
0800 hours0.00926 days <br />0.222 hours <br />0.00132 weeks <br />3.044e-4 months <br /> 99.4%
1600 hours0.0185 days <br />0.444 hours <br />0.00265 weeks <br />6.088e-4 months <br /> 99.6%
1925 hours0.0223 days <br />0.535 hours <br />0.00318 weeks <br />7.324625e-4 months <br /> TRIP On April 8, 1983, a power reduction from approximately 100% was initiated for a short maintenance outage.
Date Time Reactor Power 4/8/83 2000 99.1%
4/9/83 0100 48.5%
0700 6.4%
1600 21.7%
2400 42.0%
4/10/83 0300 79.8%
0345 TRIP On May 10, 1983, reactor power was approximately 90% until a reactor /
turbine trip at 1028 hours0.0119 days <br />0.286 hours <br />0.0017 weeks <br />3.91154e-4 months <br />.
2 Date Time Reactor Power 5/9/83 1200 90%
i 5/10/83 0000 90%
0800 90%
1028 TRIP Fuel Burnup By Core Region: See attached computer printout.
Cleanup Flow History 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> prior to the first limiting exceeding
, sample, the average letdown flow during this time was:
January 13, 1983 - 60 gpm January 14, 1983 - 61 gpm January 15, 1983 - 86 gpm
e TOLEDO EDISON COMPANY DAVIS-BESSE NUCLEAR POWER STATION UNIT ONE .
SUPPLEMENTAL INFORMATION FOR LER NP-33-83-03 PAGE 3 January 16, 1983 - 109 gpm January 17, 1983 - 101 gpm January 18, 1983 - 60 gpm April 7, 1983 - 60 gpm April 8, 1983 - 69 gpm April 9, 1983 - 93 gpm April.10, 1983 - 95 gpm May 8, 1983 - 72 gpm .
2 May 9, 1983 - 72 gpm May 10, 1983 - 72 gpm There was no degassing operation.
Table 1 lists the specific activity analysis, the time duration the specific activity exceeded the Technical Specification, and the maximum level reached for each occurrence.
Designation of Apparent Cause of Occurrence: The cause was a slight leakage of fission products through the fuel cladding. Some leakage is normal following a reactor trip due to RCS temperature and pressure changes.
Analysis of Occurrence: There was no danger to the health and safety of the public or station personnel.
At no time did the specific activity exceed the allowable limit of Techni-cal Specification 3.4.8, which accommodates possible iodine spiking phenomenon that may occur following a change in thermal power as shown in Figure 3.4-1.
Corrective Action: Per the action statement requirements of Technical Specification 3.4.8, sampling of the primary coolant was performed at least once every four hours. Monitoring of the I-131 level continued until it dropped below the Technical Specification limit of 1.0 pCi/gm.
Since icdine spikes are typical following a power change, no additional corrective. action is applicable.
Failure Data: Previous occurrences of the RCS dose equivalent I-131 exceeding the Technical Specification limit have been reported in Licensee Event Reports NP-33-80-114 (80-088), NP-33-81-15 (81-016), NP-33-81-37 (81-031).
LER #83-002
TABLE 1 sEE
- O5dE Approximate # % T' 8 i Specific Activity Analysis - Time Duration Maximum #Em Date of Occurrence Date Time Activity (pCi/gm) Tech Spec Level Level h$$
Dose Equivalent 1-131 Exceeded pCi/gm "8 January 15, 1983
@E*
1/15/83 0810- 0.17 21 hours2.430556e-4 days <br />0.00583 hours <br />3.472222e-5 weeks <br />7.9905e-6 months <br /> 2.67 g n g_
2004 2.67 p i6 1
2155 2.54 g-1/16/83 0102 2.33 @g 0400 2.40 ,,,
0730 1.59 . @ %l 0930 1,58 e4 1330 1.14 N5*
1730 0.73 2 7E January 18, 1983 1/18/83 1354 0.14 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> 1.39 Oy 2301 1.39- So o
. YM 1/19/83 0256 1.11 8 ,
0645 0.81 April 9, 1983 4/8/83 1207- 0.09 11 hours1.273148e-4 days <br />0.00306 hours <br />1.818783e-5 weeks <br />4.1855e-6 months <br /> 1.39 4/9/83 0420 1.06 0806 1.37 1145 1.39 1531 0.96 April 10, 1983 4/10/83 0130 0.41 15 hours1.736111e-4 days <br />0.00417 hours <br />2.480159e-5 weeks <br />5.7075e-6 months <br /> 1.95 0620 1.95 -
1002 1.82 1341- 1.31 1710 1.30 2110 0.89
- May 10, 1983 5/10/83 0811 0.06 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> 1.16 1323 1.16 2 .
1600 0.95.
2000 0.85 ,
$/11/83 0820 0.33 1 -
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1
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TOY EDISON-COMPANY DA L -BESSE. NUCLEAR POWR STATION UNIT ONE s SUP21.EMENTAL INFORMATFON FOR LER NP-33-83 J PAGE 5 s t ,
.g i ,
1 FUEL BURNTIP BY CORE REGION FOR JANUARY 15, 1983 AND JANUARY 18, 1983 EVENTS m
The f'uel burnup is given for each fuel assembly as designated by the computer assigned assembly number.
For the location of the assemblies, see the attached core map. Units are given in Megawatt Days *
~ x 10 Metric Ton
's w%
' I' FUEL ASSEMBLIES *
- x .
e lt n A .
. t9'42L+t1 f 5 51' 4 t' + 01 37P6?L 41 c u t;p r + e l 21*57(+01 2917?f+31 3905?t+01 1 through 7
- s. l'119 4l + 0 2 T 2 218E + 02 17n t TE + L'2 E U3 0E + C 2' 1119 3T
- 0? 38hS.*t+01 2P741L+01 8 through 14 s N 1:4 '2 0 f + L P 4!13SE+C1 247,1)+0? '> 4 0. ? f , 't ? 1" 1?t+t? 153370+3? IG'?Of+0? 15 through 21 23s79E+b2 D G rvt + 02 444thb+01 13409f+0? Jy 4 H /th01 45411E+01 ?6106t+0? 22 through 28 14 3 7 7 t: + 0 ? 15 4 7t C + 02 16%34f*0? 5 11141 e fil ae5360*L?\19474E*02 14 3 4 9 '. + 0 2 29 through 35 auun91+02 442990+t1 26539L+01 39tL0E+L1 2.,14 4 t + G P '14 4 9'": + t8 2 244Utf+02 36 through 42 I ? 3 0 eif
- 0 2 .t t 0 81 F + 02 ? !11rL + 0? 2109HF+0p 1, ? ? 9 6 t +Y 2 2 4 3 ( 'a r + r:2 14431t+02 s 43 through 49
\ E4681l+b? aP4 ? At + 01. ? ?9a 7t +01 1104sC + tr ? %67f +0? 1 5 t.9 1 E + ' ? 12185f+02 50 through 56 s ' I$6 Y3 fs+1? T Jr 3 6t +0? 15' 41 t + 0 2 26736t+02 13 8 4 4 t ,+ 0 TA 12157E+0? 15551F+02 57 through 63 t
e34T7 Nud 10 Hit +0.* 2 7 e4 L + 01 '5FSIf+01 22635t+0? 1519-E+y? 16 319 5. + 0 ? 64 through 70 PM590+02 269t> 7E + b2 13061E+02 22297E+b2 1.8 5 6 6 f + 0 2 '2 6 9P G E + 0 2 27494f+0? 71 through 77 I t. '. 52/ + t ? IS143E+0? ??!64F+02 ? q H '4 n E + 61 37b67f+di 17P17E'+0F 1530?r+0? 78 through 84 N'5 91 H ot + 01 T8004f+02 13 pat'+0? ? ?2 7 ? E + ti? 15665E+0? ???'44E+n? 13'!17 t + 0 ? 85 through 91
'4170t+L2 L D 4 tA L + C 1 1 % 2 '> G F + 0 ? 1776%F+0? 371490+01 3533?#+01 22574'.+0? 92 through 98 1.> t 2 4 t' + a .' I t.2 a5E + S2 2 7 4 '.8 f + 0 ? ?6941t+n 13'20E+C2 22?47f+3? 13530F+0? 99 through 105 P ro t' l L + 0 ? 27bd6E+02 It310t+02 15137t.+ h 22563E+02 34t42E+31 27244:+01 106 through 112 1 *'9 2 % + 0 ? P 3 4.? 3 L + 0 ? 1 % 3 H t' + 0 ? 1 J r. 8 a E + f, P 13/6EF+09 P 617 /F + n; 13P 7F t + 0? 113 through 119 Pe ISoL +02 13790E+02 12141E+02 15548F + 0? ?34760+02 10917E+0? 269t,1 f + 01 120 through 126 3Pa67t+ul ?5 ??*iE + 02 19377L+0? ?4304L+02 I??3?E+02 ?70?^f+0? 29 0 3 5 t '* 0 ? 127 through 133
.eM3HE*UP 1219Pr+02 2 '+ a f t, t + 0 2 14 4 01E + r r ? % 0 9t + 0 2 3F 22 .f + 31 2Pt431+01 134 through 140 4 ,0 7 t.t + 01 ." 6 031t + 02 1439d+L? 15 4 4 ? E + r.? t*,491L+0? 9015"L+01 I t 4t. 0 L + 02 141 through 147 l 'ue ? 3 L + 2 14 29 /E +0? 2e>0?3E + 0? 4 4 0 s, l t te) ?n479F=01 13 89H + u? 44?601.+01 148 through 154 s
24797L+02 3930E +02 l ') 4 8 4 L + 0 2 l o!,L U + Q -1 ! 4 61 C + 0 2 2 3 92 9 E + 0.2 2f>181E+02 155 through 161 9 4 2 0 2 L + f.1 13 39PE + 02 2 870 SE
- 01 Th6'ti+Pf 11172E+0? 22?C7E+02 17 7'/ 3 t + 02 162 through 168
- ? 21 's 6 f + 0 2 111m3f+02 3860HE+01 28E7pr+dl.27*b7E+01 3534*E+31 37675t+01 169 through 175 176 through 177 SS331E + 01 273?4E+01 S *AS READ IR9M LEFT TO RIGHT s i i '
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DAVIS-BESSE NUCLEAR POWER STATION UNIT ONE SUPPLEMENTAL INFORMATION FOR LER NP-33-83-03 PAGE 6 FUEL BURNUP BY CORE REGION FOR APRIL 9, 1983 AND APRIL 10, 1983 EVENTS The fuel burnup is given for each fuel assembly as designated by the computer assigned assembly number.
For the location of the assemblies, see the attached core map. Units ar.e given in Megawatt Days- -3 10 Metric Ton FUEL ASSEMBLIES * .
44936E+01 57712E+01 61204E+01 57816E+01 44983E+01 47002E+01 62491L+01 1 through 7 jf 15825E+02 24556E+02 20118E+02 24577E+02 130460+02 62568C+91 e. 6 7 7 2 E + 01 8 through 14 ' ,
14713E+02 72375E+01 26855E+02 26354E+02 18153E402 17396E+92 18151E+02 15 through 21 26274E*02 27256E+02 71974E+01 14675E+02 47347E+01 72681E+11.28439E+02 22 through 28 1705HE+02 17350E+02 18727E+02 82091E+01 187360+02 17362E+02'170480+02 29 through 35 28404E+02 71681E+01 46475E+01 63162E+01 27311L+02 17281E+02 26992E+02 36 through 42 -
15293E+02 29397E+02 '30291E+02 29426E+02.15294E+02 26988E*02 17246E+02 43 thro' ugh 49 ,
26851E+02 61934E+01 45356E+01 13502E+02 26025E+02 17535E+0? 150600+02 50 through 56 16763E+02 28583E+02 16523L+02 28587E+02 If>764r+02 15046Et02 17502F+02 57 through,63 25777C+02 13386E+02 44434E+01 57979E+01'24898E+02 17628E+02 18349L+02 64 through 70 ,
29679E+02 29402E+02 16332C+02 25019E+02 16342E+02 29431E+02 29779E+02 71 through 77 18341E+02 17580E+02 24849E+02 56999E+01 61106E*01 20082E+02 17341F+02 78 through 84 ,
80721E+01 30159E + 02 16454 E+0 2 24963E +02 1833 6E +0 2 ,25 018 E+ 02 16495E+02 85 through 91
^,
3 023 9E +0 2 81254 E + 01 17337E+02 20037E+02 60362E+01 57401E+01 24829E+02 92 through 98 17527E+02 18289E+02 29756E+02 29373E+02 16?871+02 24966E+02 16304F+02 99 through 105' '
29412E*02 29815E+02 18349E+02 17571E+02 24823E+02 56923E+01 44577E+01 106 through 112 13373E+02 25665E+02 17444E+02 14955E+02 16671E+02 28517E+02 16454E+02 113 through 119 28498E+02 16730E+02 15031E+02 17518E+02 25773f+02 13367E+02 49283E+01 120 through 126 61737E+01 27403E+02 17149E+02 26882E+02 15190E+02 29310E+02 30204E+02 127 through 133 29186E+02 151H7E+02~ 26919E+02 17183E+02 27172E+02 61634F+01 463531+01 134 through 140 71281L+01 28340E+02 16992E.+02 17318E+02 18659E+02 81061E+01 18628E+02 141 through 147 17278E+02 16983E+02 28363E+02 71310E+01 46315E+01 19663E+02 71529E+01 148 through 154 26980E+02 26271E+02 18128E+02-17356E+02 18105E+02 26259E+02 27341E+02 155 through 161 71503E+01 14641E+02 46628E+01 62239E+01 13791E+02 2455JE+02 20071E+02 162 through 168 24538E*02 13803E+02 62159E+01 46581C+01 44822E+01 57618E+01 61114E+01 169 through 175 57592E*01 4 4 7 76E +01 176 through 177 l
- AS READ FROM LEFT TO RIGilT
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TOLEDO EDISON COMPANY ,,
DAVIS-BESSE NUCLEAR POWER STATION UNIT ONE ,
SUPPLEMENTAL INFORMATION FOR LER NP-33-83-03 PAGE 7 '
~ '
FUEL BURNUP BY CORE REGION FOR; ~Y# '
MAY 10, 1983 EVENT ' *
. r.
The fuel burnup-is given for each fuel assembly as designated by the computer assigned assembly number.
For the location of the assemblies, see the attached core map. Units are given in Megawatt Days ~
x 10 Metric Ton f
. FUEL ASSEMBLIES
- SGR07i+01 6515CE+01 69C43E+C1 65292E+01 509 0 0 E + 01 t 30 4S E+ 01 70320E+01 1 through 7 14626E+C2 253J2E+C': 2CL91E+C2 S S 3 f. 8 E + ' ' 14716C+C2 7C'ESE+11 52878E+G1 8 through 14 IS145E+02 F1454E+C1 27E74E+02 27139E+02 1'f 035 ;4 0 2 18099E+02 19338F+02 15 through 21 27Jf2E+02 2 79hE +G2 81135 E+01 151C91+C2 534 04 f + 01 F.17 7 2 E + J 1 20218E+0? 22 through 28 17 % " E <- 0 2 IE018E+G2 194 74 E+02 924 74E + 21 lo486E + S2 1803CE+32 17967E+02 29 through 35 29157E*r2 SC214E+01 Sr54?,E+01 710102+C1 23037E+02 1 8 2 1 ': E + 3 2 27872E+0? 36 through 42 lo 0GE+G2 J017]E+32 31018F+02 3 0 0 0 0 E + ::P 16206E+32 27871E+32 18186.+0" 43 through 49 2 2 7f 7t E+C 2 e ? 787/+c1 51227e+01 14315E+62 2 'i B 21 '~ 4 0 2 16263E+02 16026?+0? 50 through 56 177T7t HT '93 E+!? 17J 85E + 22 2925'E+0P 17733_C 2 16C1'd+c2 18213-:+0? 57 through 63 aut:E+02 111 % E + n 5 0C'2 3E + C 1 653"1E+31 2 5 6 4 4 , + J:2 1P.4'7E+02 19038E+02 64 through 70 2 C + ! i c. + l T 2021]E+0F 172PC E + 0 2 2590'C+J2 1723 6 L +0 2 3 0?t 2 E + 02 3 0 550 +0 2 71 through 77 l'034L+bP 18 3 01 E + :,2 2 0 5 $5 E + :* 2 642 7F+;1 (: H F 8 4 ~. + 01 2084"E+02 18n36 M12 78 through 84 9 t. 9 5 7 E + 01 20873E+"? 17339E+02 25P4"E+j2 19122E+02 25907C+02 17356E+02 85 through 91 3 0"t i t'+ 9 2 '215. 74 E + .1 18.3 3 5 E +0 2 23804E+12 6a l 2 6.'+ G 1 5 4 7 43 E + 91 25573;+02 92 through 98 1 334L+0; 1297"En2 3T927E+C2 32162f+92 17176:+02 25F54E+02 17196F+02 99 through 105 '
51J~HEa c 'T _s' EEL +~" 19L4cC+/I 163 elf +02 25566'+02 a4307E+01 50423"+C1 106 through 112 141Elc+C2 3.4 2 ': E + M. If149E+C2 15919E+32 1763 2 E +0 2 P 92P '.E+ 3 ? 17 % 14 :. + 0 2 113 through 119 2026Ev4J2 17 ( 9 7 0 - r. 2 15 0 0 3 : + t. 2 18729C+?" 26f452+D2 1417GE+32 50117?i01 120 through 126 6 ;" 44 r
- J1 761 1E+22 13 'J 8 4 F.+ 0 2 27761E+ 2 15194E+: S 3C081E+12 30c27;+0? 127 through 133 2 - 9 4 4 t. 4 42 l al'? b E + 32 21H02E+02 18122E+52 27P?bi+J2 65-44?C+01 52594E+01 134 through 140 t- C J 5 F E . r.1 2 911 t c + L ,' ;7994r+02 17967E+ 1 9 4 9 5 ,+ '; 71411E+01 19374E+0? 141 through 147 I M 4Fi+G2 178 %i + C 2 2 '3141 E + 0 2 803EJE+!1 52?S5'+~1 15094E+32 80626t+01 148 through 154 2 7 7 0 ". :. + 4 " 7 3 7- 1 E
- C 2 19011E+02 18058E+G2 la?8PC+22 2704aE+32 2 S 0 6 3 + 0 ? 155 through 161 80SS4E+,1 15072E+02 6259hI+01 7 010 7 E + e,1 14557E+02 25327E+02 2C844E+02 162 through 168 2531M.+02 19 6i.V_+f? 70015E+01 52644E+01 50712E+01 65073E+01 CA952E+01 169 through 175 6E041:+31 ' C 62 "E +t 1 176 through 177
- AS READ FROM LEFT TO RIGHT
n TOLEDO EDISOM COMPANY DAVIS-BESSE NUCLEAR POWER STATION UNIT ONE SUPPLEMENTAL INH)RMATION FOR LER NP-33-83-03 PAGE 8
- f. j March 18. 1982 '
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1 2 3 4 5 6 7 8 9 10 11 12 13 14 15 Incore Detector Z O = Total Core Monitor Fuel Assembly Batch ID. (No. in Core)
X = Symmetry Monitor yoet Asee biy zD 1 (25) For=er sacch A - once burn =4
@ = Total Core and Symmetry proceeded 3 (60) Former Batch C - twice burned bY NO 4 (44) Formar Batch D - once burned Monitor AllID'sd 5A (8) New Fuel - 3.04% cariched Incore Detector String Number h 5B (40) New Fuel - 2.99% enriched gig g 1
Regenerative Sources at P4 and 812 C001 Control Component / Source ID and Type Q31 1 89 A = APSRA a - Regenerative Neutron Source C = CRA Computer Aseigned Assembly Number _ j Control Component Group / Rod l Prepared By _. , / /b2[>> Approved By ! M y 1
__--_____.-__m_ _ . _ _ _ _ _