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| ==Dear Sir:== | | ==Dear Sir:== |
| SALEM GENERATING STATION LICENSE NO. DPR-75 DOCKET NO. 50-311 UNIT NO. 2 LICENSEE EVENT REPORT 93-014-00 January 27, 1994 This Licensee Event Report is being submitted pursuant to the requirements of Code of Federal Regulation 10CFR50.73(a) | | SALEM GENERATING STATION LICENSE NO. DPR-75 DOCKET NO. 50-311 UNIT NO. 2 LICENSEE EVENT REPORT 93-014-00 January 27, 1994 This Licensee Event Report is being submitted pursuant to the requirements of Code of Federal Regulation 10CFR50.73(a) |
| (2) (iv). Issuance of this report is required within thirty (30) days of event discovery. | | (2) (iv). Issuance of this report is required within thirty (30) days of event discovery. |
| MJPJ:pc Distribution 9402030067 940127 PDR ADOCK 05000311 S PDR The power is in )Our hands. r i ' f* Sincerely yours, // ll/ 1' ndra General Manager -Salem Operations 95-2189 REV 7-92 NRC FORM 366 16-891 U.S. NUCLEAR REGULATORY COMMISSION | | MJPJ:pc Distribution 9402030067 940127 PDR ADOCK 05000311 S PDR The power is in )Our hands. r i ' f* Sincerely yours, // ll/ 1' ndra General Manager -Salem Operations 95-2189 REV 7-92 NRC FORM 366 16-891 U.S. NUCLEAR REGULATORY COMMISSION |
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| DC 20503. I DOCKET NUMBER 12) I PAGE (3) o 15 Io Io Io 13 I l 1 l I , loF 01 S ESF Actuation | | DC 20503. I DOCKET NUMBER 12) I PAGE (3) o 15 Io Io Io 13 I l 1 l I , loF 01 S ESF Actuation |
| & Resultant Pressurizer Overpressure.Protection System Channel I Actuation. | | & Resultant Pressurizer Overpressure.Protection System Channel I Actuation. |
| EVENT DATE ISi LER NUMBER 161 REPORT DATE 17) OTHER FACILITIES INVOLVED (81 MONTH DAY YEAR YEAR | | EVENT DATE ISi LER NUMBER 161 REPORT DATE 17) OTHER FACILITIES INVOLVED (81 MONTH DAY YEAR YEAR |
| :}% | | :}% |
| tt MONTH DAY YEAR FACILITY NAMES DOCKET NUMBERISI OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE OF 10 CFR §:(Chock an* or ma,. of th* fallawlnfl/ | | tt MONTH DAY YEAR FACILITY NAMES DOCKET NUMBERISI OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE OF 10 CFR §:(Chock an* or ma,. of th* fallawlnfl/ |
| (11) MODE (9) 5 20.402lbl 20.405lcl X 60.73(all2llM POWER l 20.4051all1llil 0 I 01 0 I-20.4051*111lliil | | (11) MODE (9) 5 20.402lbl 20.405lcl X 60.73(all2llM POWER l 20.4051all1llil 0 I 01 0 I-20.4051*111lliil |
| .......... | | .......... |
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| However, this review did not identify that SSPS Train "B" Test switch (TS603) would send an open signal to 22SJ54 when placed in the "operate output" position. | | However, this review did not identify that SSPS Train "B" Test switch (TS603) would send an open signal to 22SJ54 when placed in the "operate output" position. |
| As a result, the surveillance test procedure omitted relevant information. | | As a result, the surveillance test procedure omitted relevant information. |
| This procedural inadequacy had not been identified during prior performances of the procedure since the procedure is normally LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station Unit 2 DOCKET NUMBER 5000311 APPARENT CAUSE OF OCCURRENCE: | | This procedural inadequacy had not been identified during prior performances of the procedure since the procedure is normally LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station Unit 2 DOCKET NUMBER 5000311 APPARENT CAUSE OF OCCURRENCE: |
| {cont'd) LER NUMBER 93-014-00 PAGE 4 of 5 performed at RCS pressures above 1000 psig. At RCS pressures above 1000 psig, the accumulator is required to be operable with its discharge valve open. Therefore, the test signal would be applied to an already open valve. Performance of this procedure is required once per 62 days and is applicable in Modes 1-4. This event occurred while performing the procedure in Mode 5 with RCS pressure less than 1000 psig. At the time of this event, the procedure was being performed to allow entry into Mode 4. . . A contributor to this procedural inadequacy resulting in an ESF actuation (during prior Mode 5 performance of the procedure) was a procedural change to Integrated Operating Procedure IOP-6 (Hot Standby to Cold Shutdown) made in November 1991. This change was initiated due to Technical Specification (TS) Amendments 130 and 109, for Units 1 and 2, respectively, which appropriately removed the TS requirement to clear and tag the SJ54 valve breakers when greater than 1000 psig. However, the procedure change also removed a requirement to administratively clear and tag the breaker when less than 1000 psig, which subsequent review following this event showed to be inappropriate. | | {cont'd) LER NUMBER 93-014-00 PAGE 4 of 5 performed at RCS pressures above 1000 psig. At RCS pressures above 1000 psig, the accumulator is required to be operable with its discharge valve open. Therefore, the test signal would be applied to an already open valve. Performance of this procedure is required once per 62 days and is applicable in Modes 1-4. This event occurred while performing the procedure in Mode 5 with RCS pressure less than 1000 psig. At the time of this event, the procedure was being performed to allow entry into Mode 4. . . A contributor to this procedural inadequacy resulting in an ESF actuation (during prior Mode 5 performance of the procedure) was a procedural change to Integrated Operating Procedure IOP-6 (Hot Standby to Cold Shutdown) made in November 1991. This change was initiated due to Technical Specification (TS) Amendments 130 and 109, for Units 1 and 2, respectively, which appropriately removed the TS requirement to clear and tag the SJ54 valve breakers when greater than 1000 psig. However, the procedure change also removed a requirement to administratively clear and tag the breaker when less than 1000 psig, which subsequent review following this event showed to be inappropriate. |
| PREVIOUS SIMILAR OCCURRENCES: | | PREVIOUS SIMILAR OCCURRENCES: |
| LER 311/92-005-00 reported a prior occurrence, caused by procedure inadequacy involving SSPS Procedure S2.0P-ST.SSP-OOOl(Q), Manual Safety Injection, and the concurrent replacement of Rosemount steam flow transmitters. | | LER 311/92-005-00 reported a prior occurrence, caused by procedure inadequacy involving SSPS Procedure S2.0P-ST.SSP-OOOl(Q), Manual Safety Injection, and the concurrent replacement of Rosemount steam flow transmitters. |
| Corrective action to this event consisted of revising the procedure to identify the consequence of moving the Mode Select Switch to TEST as well as the review and appropriate revision of other station procedures involving use of this switch. SAFETY SIGNIFICANCE: | | Corrective action to this event consisted of revising the procedure to identify the consequence of moving the Mode Select Switch to TEST as well as the review and appropriate revision of other station procedures involving use of this switch. SAFETY SIGNIFICANCE: |
| This event did not affect the health and safety of the public.. It is reportable as an Engineered Safety Features Actuation pursuant to lOCFR50.73(a) | | This event did not affect the health and safety of the public.. It is reportable as an Engineered Safety Features Actuation pursuant to lOCFR50.73(a) |
| (2) (iv). In addition, this event is reportable in accordance with Technical Specification (TS) Action Statement 3.4.10.3.c. | | (2) (iv). In addition, this event is reportable in accordance with Technical Specification (TS) Action Statement 3.4.10.3.c. |
| and pursuant to the requirements of TS 6.9.2. Two concerns associated with this event were the possibilities of nitrogen injection into the RCS and pressurized thermal shock (PTS): Nitrogen was not injected into the RCS. A fully charged accumulator will discharge nitrogen into the RCS if pressurizer pressure is less than 162 psig. Since pressurizer pressure was 320 psig, a minimum of 3785 gallons boric acid volume and all nitrogen remained inside the accumulator. | | and pursuant to the requirements of TS 6.9.2. Two concerns associated with this event were the possibilities of nitrogen injection into the RCS and pressurized thermal shock (PTS): Nitrogen was not injected into the RCS. A fully charged accumulator will discharge nitrogen into the RCS if pressurizer pressure is less than 162 psig. Since pressurizer pressure was 320 psig, a minimum of 3785 gallons boric acid volume and all nitrogen remained inside the accumulator. |
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0081998-12-24024 December 1998 LER 97-001-01:on 970215,failure to Perform TS Surveillance of Component Cooling Water Sys Check Valves Occurred.Caused by Inadequate Communication Between EOP Group & IST Reviewers.Procedure Revised.With 981224 Ltr ML18106B0021998-12-17017 December 1998 LER 98-015-01:on 980924,improper Installation of Test Equipment to RPS Occurred.Caused by Inadequate 10CFR50.59 Applicability Reviews During Past Revs.Revised Procedures. with 981217 Ltr ML18106A9551998-11-0303 November 1998 LER 96-013-01:on 960711,concluded That Current Gain & Bias Settings Had Rendered Overtemperature Delta Temp Protection Channels Inoperable.Caused by Scaling Error.Licensee Will Revise Scaling Calculations.With 981105 Ltr ML18106A9451998-10-30030 October 1998 LER 97-004-01:on 970408,failure to Comply with TS Action Statement,Dg Start & Inadequate Surveillance Testing,Was Noted.Caused by Inadequate Tracking of Inoperable Equipment. Discussed Event & Lessons Learned.With 981022 Ltr ML18106A9491998-10-22022 October 1998 LER 98-015-00:on 980924,identified Improper Installation of Test Equipment to Rps.Cause Indeterminate.Procedures for Installation of Test Equipment for Collection of State Point Data Were Placed on Administrative Hold.With 981022 Ltr ML18106A9301998-10-21021 October 1998 LER 98-014-00:on 980725,noted Improper Calibr of Liquid Radwaste Effluent Line Radiation Monitor.Caused by Inattention to Detail by Maint Personnel.Channel Calibr Was Successfully Performed on 1R18 on 980821.With 981019 Ltr ML18106A9071998-10-0101 October 1998 LER 98-014-00:on 980918,discovered That Fire Barrier Matl for HVAC Ducts Does Not Meet Required Level of Fire Resistance.Cause Indeterminate.Established Appropriate Compensatory Actions for Fire Barriers.With 981001 Ltr ML18106A8951998-09-28028 September 1998 LER 98-012-01:on 980725,noted That Afs Was Operated with Less than Required Number of Operable AFW Pumps.Caused by Improper Procedure Implementation.Runout Protection Pressure Device for 22 AFW Pumps Was Returned to Svc.With 980928 Ltr ML18106A8821998-09-21021 September 1998 LER 98-013-00:on 980820,noted Surveillance of Containment Penetration Overcurrent Protection Devices Missed.Caused by Human Error.Satisfactorily Tested Apprpriate Breakers & Disciplined Involved Personnel.With 980921 Ltr ML18106A8791998-09-16016 September 1998 LER 96-006-01:on 960717,determined That non-radioactive Liquid Basin Radwaste Monitor Inoperable During Low Head Conditions.Caused by Inadequate Design Change Package.Design Change 1EC3663-01 Has Been Installed.With 980916 Ltr ML18106A8801998-09-0808 September 1998 LER 98-013-00:on 980806,operation with TS Required Equipment OOS Was Noted.Caused by Human Error.Reviewed Processes & Practices Re Safety Sys Status Control,Procedure Rev & Extra Training.With 980908 Ltr ML18106A8531998-08-27027 August 1998 LER 98-007-00:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Cause of Event Has Not Yet Been Determined.Assembled Root Cause Team & Replaced Affected tubing.W/980827 Ltr ML18106A8521998-08-27027 August 1998 LER 98-011-00:on 980803,ESFA During a 4KV Automatic Transfer Test Was Noted.Caused by Premature Release of Control Console Pushbutton Due to Inadequate Procedural Step.Revised procedure.W/980827 Ltr ML18106A8421998-08-24024 August 1998 LER 98-012-00:on 980725,discovered That Plant Had Operated in Modes 1 & 2 w/twenty-two AFW Pumps Inoperable.Caused by Failure to Restore Pump Runout Protection Pressure Device to Svc.Returned Subject Device to svc.W/980824 Ltr ML18106A8431998-08-24024 August 1998 LER 98-009-00:on 980810,failure to Post Continuous Firewatch as Required by Fire Protection Plan Noted.Caused by Failure to Recognize Concurrent Conditions.Continuous Firewatch Was Posted Immediately & Repaired Smoke detectors.W/980824 Ltr ML18106A8141998-08-13013 August 1998 LER 98-010-00:on 980714,determined That Leakage from Boron Injection Tank Exceeded Max Allowable ECCS Leakage from Sources Outside Containment.Caused by Leaking 2SJ404 Manual Sample valve.2SJ404 Valve repaired.W/980813 Ltr ML18106A8201998-08-13013 August 1998 LER 98-012-00:on 980715,potential to Exceed Rating of Piping Due to Isolation of Overpressure Protection Line Was Noted. Caused by Inadequate Procedural Guidance.Appropriate Operations Dept Procedures Have Been revised.W/980813 Ltr ML18106A6931998-06-29029 June 1998 LER 98-003-00:on 980122,inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2 Sg,Was Performed.Caused by Failure of Qualification,Verification & Validation Process. Tubes Reviewed to Verify No Others Inappropriately Plugged ML18106A6471998-06-0404 June 1998 LER 98-011-00:on 980505,improper Isolation of Single Cell Battery Charger from 125 Vdc Battery Was Noted.Caused by Inadequate 10CFR50.59 Applicability Review.Placed Procedure SC.MD-CM.ZZ-0024(Q) on Administrative hold.W/980604 Ltr ML18106A6421998-06-0101 June 1998 LER 98-010-00:on 931019,reactor Pressure Vessel Insp Plugs Were Out of Configuration,Was Noted.Caused by Personnel Error.Proper Configuration Was Restored Shortly After Discovery Prior to Entering Mode 2.W/980601 Ltr ML18106A6431998-05-29029 May 1998 LER 98-006-01:on 980227,determined Incorrect Scaling Error of First Stage Pressure Transmitter Existed.Caused by Human Error.Revised Setpoint Calculation SC-MS002-01 & Revised Associated Instrument Calibr Database info.W/980529 Ltr ML18106A6141998-05-18018 May 1998 LER 98-008-00:on 970814,failure to Test 21 & 22 AF 40 Valves in Closed Direction as Required by TS 4.0.5 Was Noted.Caused by Inadequate Design Mod Process.Motor Driven 21/22 AF 40 Valves Were Tested IAW Revised procedure.W/980518 Ltr ML18106A5901998-05-0101 May 1998 LER 98-009-00:on 980405,epoxy Missing from Terminals of H Analyzer Was Noted.Caused by Inadequate Development of Procedure.H Analyzers Were Repaired & Review of Other Safety Related Equipment in Containment Was performed.W/980501 Ltr ML18106A5611998-04-20020 April 1998 LER 98-008-00:on 980323,inadequate Testing of Salem Unit 1 Containment Air Locks Resulted in Entering TS 3.0.3.Caused by less-than-adequate Work Practices During Replacement of Equalizing Valve.Salem Unit 2 Airlocks Were Inspected ML18106A6061998-04-0101 April 1998 Corrected LER 98-004-00:on 980302,failure to Comply W/Tss 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Have Been Taken to Correctly Document Safety Factors.Corrects Prior Similar Occurrences ML18106A4451998-04-0101 April 1998 LER 98-004-00:on 980302,failure to Perform TS 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Were Taken to Correctly Document Safety factors.W/980401 Ltr ML18106A4351998-03-30030 March 1998 LER 98-006-00:on 980227,incorrect Scaling of First Stage Turbine Impulse Pressure Transmitters Noted.Cause Indeterminate.Implemented Procedure Changes & re-scaled Affected Turbine Impulse Pressure transmitters.W/980330 Ltr ML18106A3961998-03-20020 March 1998 LER 98-005-00:on 980219,inoperability of Twelve EDG Fuel Oil Transfer Pump (FOTP) Noted.Caused by Installation of Incorrect Control Switch.Installed Correct off-auto-manual Switch & Verified Operability of Twelve FOTP.W/980320 Ltr ML18106A5781998-03-20020 March 1998 Corrected LER 98-005-00:on 980219,inoperability of 12 Fuel Oil Transfer Pump (Fotp),Noted.Caused by Installation of Incorrect Control Switch.Field Insp Performed to Verify Configuration of Switches for 11,21 & 22 FOTPs ML18106A4021998-03-20020 March 1998 LER 98-007-00:on 980218,failure to Establish Containment Integrity (Closure) Prior to Fuel Movement Was Noted.Caused by Failure to Identify & Include Condensate Pot Vent in Appropriate Valve Lineup.Valves identified.W/980320 Ltr ML18106A4031998-03-20020 March 1998 LER 98-006-00:on 980221,ESF Actuation of 11 & 12 Auxiliary Feedwater Pumps Occurred.Caused by Human Error.Operators Promptly Established Feedwater to All SG & Restored Proper Water levels.W/980320 Ltr 1999-08-26
[Table view] Category:RO)
MONTHYEARML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0081998-12-24024 December 1998 LER 97-001-01:on 970215,failure to Perform TS Surveillance of Component Cooling Water Sys Check Valves Occurred.Caused by Inadequate Communication Between EOP Group & IST Reviewers.Procedure Revised.With 981224 Ltr ML18106B0021998-12-17017 December 1998 LER 98-015-01:on 980924,improper Installation of Test Equipment to RPS Occurred.Caused by Inadequate 10CFR50.59 Applicability Reviews During Past Revs.Revised Procedures. with 981217 Ltr ML18106A9551998-11-0303 November 1998 LER 96-013-01:on 960711,concluded That Current Gain & Bias Settings Had Rendered Overtemperature Delta Temp Protection Channels Inoperable.Caused by Scaling Error.Licensee Will Revise Scaling Calculations.With 981105 Ltr ML18106A9451998-10-30030 October 1998 LER 97-004-01:on 970408,failure to Comply with TS Action Statement,Dg Start & Inadequate Surveillance Testing,Was Noted.Caused by Inadequate Tracking of Inoperable Equipment. Discussed Event & Lessons Learned.With 981022 Ltr ML18106A9491998-10-22022 October 1998 LER 98-015-00:on 980924,identified Improper Installation of Test Equipment to Rps.Cause Indeterminate.Procedures for Installation of Test Equipment for Collection of State Point Data Were Placed on Administrative Hold.With 981022 Ltr ML18106A9301998-10-21021 October 1998 LER 98-014-00:on 980725,noted Improper Calibr of Liquid Radwaste Effluent Line Radiation Monitor.Caused by Inattention to Detail by Maint Personnel.Channel Calibr Was Successfully Performed on 1R18 on 980821.With 981019 Ltr ML18106A9071998-10-0101 October 1998 LER 98-014-00:on 980918,discovered That Fire Barrier Matl for HVAC Ducts Does Not Meet Required Level of Fire Resistance.Cause Indeterminate.Established Appropriate Compensatory Actions for Fire Barriers.With 981001 Ltr ML18106A8951998-09-28028 September 1998 LER 98-012-01:on 980725,noted That Afs Was Operated with Less than Required Number of Operable AFW Pumps.Caused by Improper Procedure Implementation.Runout Protection Pressure Device for 22 AFW Pumps Was Returned to Svc.With 980928 Ltr ML18106A8821998-09-21021 September 1998 LER 98-013-00:on 980820,noted Surveillance of Containment Penetration Overcurrent Protection Devices Missed.Caused by Human Error.Satisfactorily Tested Apprpriate Breakers & Disciplined Involved Personnel.With 980921 Ltr ML18106A8791998-09-16016 September 1998 LER 96-006-01:on 960717,determined That non-radioactive Liquid Basin Radwaste Monitor Inoperable During Low Head Conditions.Caused by Inadequate Design Change Package.Design Change 1EC3663-01 Has Been Installed.With 980916 Ltr ML18106A8801998-09-0808 September 1998 LER 98-013-00:on 980806,operation with TS Required Equipment OOS Was Noted.Caused by Human Error.Reviewed Processes & Practices Re Safety Sys Status Control,Procedure Rev & Extra Training.With 980908 Ltr ML18106A8531998-08-27027 August 1998 LER 98-007-00:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Cause of Event Has Not Yet Been Determined.Assembled Root Cause Team & Replaced Affected tubing.W/980827 Ltr ML18106A8521998-08-27027 August 1998 LER 98-011-00:on 980803,ESFA During a 4KV Automatic Transfer Test Was Noted.Caused by Premature Release of Control Console Pushbutton Due to Inadequate Procedural Step.Revised procedure.W/980827 Ltr ML18106A8421998-08-24024 August 1998 LER 98-012-00:on 980725,discovered That Plant Had Operated in Modes 1 & 2 w/twenty-two AFW Pumps Inoperable.Caused by Failure to Restore Pump Runout Protection Pressure Device to Svc.Returned Subject Device to svc.W/980824 Ltr ML18106A8431998-08-24024 August 1998 LER 98-009-00:on 980810,failure to Post Continuous Firewatch as Required by Fire Protection Plan Noted.Caused by Failure to Recognize Concurrent Conditions.Continuous Firewatch Was Posted Immediately & Repaired Smoke detectors.W/980824 Ltr ML18106A8141998-08-13013 August 1998 LER 98-010-00:on 980714,determined That Leakage from Boron Injection Tank Exceeded Max Allowable ECCS Leakage from Sources Outside Containment.Caused by Leaking 2SJ404 Manual Sample valve.2SJ404 Valve repaired.W/980813 Ltr ML18106A8201998-08-13013 August 1998 LER 98-012-00:on 980715,potential to Exceed Rating of Piping Due to Isolation of Overpressure Protection Line Was Noted. Caused by Inadequate Procedural Guidance.Appropriate Operations Dept Procedures Have Been revised.W/980813 Ltr ML18106A6931998-06-29029 June 1998 LER 98-003-00:on 980122,inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2 Sg,Was Performed.Caused by Failure of Qualification,Verification & Validation Process. Tubes Reviewed to Verify No Others Inappropriately Plugged ML18106A6471998-06-0404 June 1998 LER 98-011-00:on 980505,improper Isolation of Single Cell Battery Charger from 125 Vdc Battery Was Noted.Caused by Inadequate 10CFR50.59 Applicability Review.Placed Procedure SC.MD-CM.ZZ-0024(Q) on Administrative hold.W/980604 Ltr ML18106A6421998-06-0101 June 1998 LER 98-010-00:on 931019,reactor Pressure Vessel Insp Plugs Were Out of Configuration,Was Noted.Caused by Personnel Error.Proper Configuration Was Restored Shortly After Discovery Prior to Entering Mode 2.W/980601 Ltr ML18106A6431998-05-29029 May 1998 LER 98-006-01:on 980227,determined Incorrect Scaling Error of First Stage Pressure Transmitter Existed.Caused by Human Error.Revised Setpoint Calculation SC-MS002-01 & Revised Associated Instrument Calibr Database info.W/980529 Ltr ML18106A6141998-05-18018 May 1998 LER 98-008-00:on 970814,failure to Test 21 & 22 AF 40 Valves in Closed Direction as Required by TS 4.0.5 Was Noted.Caused by Inadequate Design Mod Process.Motor Driven 21/22 AF 40 Valves Were Tested IAW Revised procedure.W/980518 Ltr ML18106A5901998-05-0101 May 1998 LER 98-009-00:on 980405,epoxy Missing from Terminals of H Analyzer Was Noted.Caused by Inadequate Development of Procedure.H Analyzers Were Repaired & Review of Other Safety Related Equipment in Containment Was performed.W/980501 Ltr ML18106A5611998-04-20020 April 1998 LER 98-008-00:on 980323,inadequate Testing of Salem Unit 1 Containment Air Locks Resulted in Entering TS 3.0.3.Caused by less-than-adequate Work Practices During Replacement of Equalizing Valve.Salem Unit 2 Airlocks Were Inspected ML18106A6061998-04-0101 April 1998 Corrected LER 98-004-00:on 980302,failure to Comply W/Tss 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Have Been Taken to Correctly Document Safety Factors.Corrects Prior Similar Occurrences ML18106A4451998-04-0101 April 1998 LER 98-004-00:on 980302,failure to Perform TS 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Were Taken to Correctly Document Safety factors.W/980401 Ltr ML18106A4351998-03-30030 March 1998 LER 98-006-00:on 980227,incorrect Scaling of First Stage Turbine Impulse Pressure Transmitters Noted.Cause Indeterminate.Implemented Procedure Changes & re-scaled Affected Turbine Impulse Pressure transmitters.W/980330 Ltr ML18106A3961998-03-20020 March 1998 LER 98-005-00:on 980219,inoperability of Twelve EDG Fuel Oil Transfer Pump (FOTP) Noted.Caused by Installation of Incorrect Control Switch.Installed Correct off-auto-manual Switch & Verified Operability of Twelve FOTP.W/980320 Ltr ML18106A5781998-03-20020 March 1998 Corrected LER 98-005-00:on 980219,inoperability of 12 Fuel Oil Transfer Pump (Fotp),Noted.Caused by Installation of Incorrect Control Switch.Field Insp Performed to Verify Configuration of Switches for 11,21 & 22 FOTPs ML18106A4021998-03-20020 March 1998 LER 98-007-00:on 980218,failure to Establish Containment Integrity (Closure) Prior to Fuel Movement Was Noted.Caused by Failure to Identify & Include Condensate Pot Vent in Appropriate Valve Lineup.Valves identified.W/980320 Ltr ML18106A4031998-03-20020 March 1998 LER 98-006-00:on 980221,ESF Actuation of 11 & 12 Auxiliary Feedwater Pumps Occurred.Caused by Human Error.Operators Promptly Established Feedwater to All SG & Restored Proper Water levels.W/980320 Ltr 1999-08-26
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML18107A5581999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 2.With 991014 Ltr ML18107A5571999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 1.With 991014 Ltr ML18107A5301999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 2.With 990913 Ltr ML18107A5311999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 1.With 990913 ML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A5201999-08-12012 August 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#9) Second Interval,Second Period, First Outage (96RF). ML18107A4811999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 1.With 990813 Ltr ML18107A4821999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 2.With 990813 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A5211999-07-0101 July 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#10) Second Interval,Second Period,Second Outage (99RF). ML18107A4351999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 1.With 990713 Ltr ML18107A4341999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 2.With 990713 Ltr ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3441999-06-0101 June 1999 Interim Part 21 Rept Re Premature Over Voltage Protection Actuation in Circuit Specific Application in Dc Power Supply.Testing & Evaluation Activities Will Be Completed on 990716 ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A3681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 1.With 990611 Ltr ML18107A3721999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 2.With 990611 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A3711999-04-30030 April 1999 Corrected Monthly Operating Rept for Apr 1999 for Salem Generating Station,Unit 1 ML18107A3151999-04-30030 April 1999 Submittal-Only Screening Review of Salem Generating Station Individual Plant Exam for External Events (Seismic Portion), Rev 1 ML18107A2991999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 1.With 990514 Ltr ML18107A2971999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 2.With 990514 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18107A2881999-04-0707 April 1999 Rev 0 to NFS-0174, COLR for Salem Unit 2 Cycle 11. ML18107A1821999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 1.With 990414 Ltr ML18107A1831999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 2.With 990414 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B1021999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 2.With 990315 Ltr ML18106B1011999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 1.With 990315 Ltr ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0561999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 2.With 990212 Ltr ML18106B0571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 1.With 990212 Ltr ML20205P1671999-01-31031 January 1999 a POST-PLUME Phase, Federal Participation Exercise ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0251998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 2.With 990115 Ltr 1999-09-30
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Text
- Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038 Salem Generating Station U. s. Nuclear Regulatory Commission Document Control Desk. Washington, DC 20555
Dear Sir:
SALEM GENERATING STATION LICENSE NO. DPR-75 DOCKET NO. 50-311 UNIT NO. 2 LICENSEE EVENT REPORT 93-014-00 January 27, 1994 This Licensee Event Report is being submitted pursuant to the requirements of Code of Federal Regulation 10CFR50.73(a)
(2) (iv). Issuance of this report is required within thirty (30) days of event discovery.
MJPJ:pc Distribution 9402030067 940127 PDR ADOCK 05000311 S PDR The power is in )Our hands. r i ' f* Sincerely yours, // ll/ 1' ndra General Manager -Salem Operations 95-2189 REV 7-92 NRC FORM 366 16-891 U.S. NUCLEAR REGULATORY COMMISSION
-APPROVED OMB NO. 3150-0104 LICENSEE EVENT REPORT (LERI FACILITY NAME 11) Salem Generating Station -Unit 2 TITLE -EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH IP-530). U.S. NUCLEAR REGULATORY COMMISSION.
WASHINGTON.
DC 20555. AND TO THE PAPERWORK REDUCTION PROJECT 13150-0104).
OFFICE OF MANAGEMENT AND BUDGET. WASHINGTON.
DC 20503. I DOCKET NUMBER 12) I PAGE (3) o 15 Io Io Io 13 I l 1 l I , loF 01 S ESF Actuation
& Resultant Pressurizer Overpressure.Protection System Channel I Actuation.
EVENT DATE ISi LER NUMBER 161 REPORT DATE 17) OTHER FACILITIES INVOLVED (81 MONTH DAY YEAR YEAR
- }%
tt MONTH DAY YEAR FACILITY NAMES DOCKET NUMBERISI OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE OF 10 CFR §:(Chock an* or ma,. of th* fallawlnfl/
(11) MODE (9) 5 20.402lbl 20.405lcl X 60.73(all2llM POWER l 20.4051all1llil 0 I 01 0 I-20.4051*111lliil
..........
..............
___, *&I=::::::::::
NAME '* ,____ I-60.3Slcll11 I-I-50.38lcll21 ,___ 50.7311112llil
-I-60.73(111211iil
,____ I-50.73(1l12lliiil LICENSEE CONTACT FOR THIS LER 1121 M. J. Pastva, Jr. -LER Coordinator 60.731all21M 50.73lall2llviil 50.73111 (2llviil)(AI 60.73111121 lvlilllBI 60.731all211xl AREA CODE -,___ -73.71(b) 73.711cl OTHER {S{Mcify in Abstr*ct b1/ow ind in Ttnct, NRC Form 366AI TELEPHONE NUMBER 6 10 I 9 3 13 f 9 1-1 SI 1 16 I S COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (131 CAUSE SYSTEM COMPONENT I I I I I I I I MANUFAC* TUR ER I I I I I I SUPPLEMENTAL REPORT EXPECTED 1141 n YES (If Y*S. complot* EXPECTED SUBMISSION DATE/ hci NO ABSTRACT (Umir ro 1400 spaces. .. 11ppr0Kimac111v fifrtum sing/e.space rypewritrtJn lintJs} (161 I I I I I I I . I MANUFAC* TUR ER I I I I I I EXPECTED SUBMISSION DATE 1151 MONTH DAY YEAR I I I On 12/28/93, at 0850 hours0.00984 days <br />0.236 hours <br />0.00141 weeks <br />3.23425e-4 months <br />, Reactor Coolant System (RCS) 22 Accumulator . outlet valve 22SJ54 unexpectedly opened and injected an estimated volume of 1735 to 2640 gallons (2200 ppm boric acid) into-the RCS. The resultant RCS pressure transient'actuated Pressurizer Protection System (POPS) Channel I, causing Pressurizer Valve 2PR1 to open at 375 psig. Highest indicated RCS pressure was approximately 372 psig. RCS pressure decreased to approximately 280 psig prior to being rec*overed by the Pressurizer heaters. This event occurred when test switch TS-603 was operated, per procedure S2.0P-ST.SSP-0010(Q), Solid State Protection System .(SSPS) Train B Slave Relays Testing. Plant equipment responded properly to this event and TS-603 was reset to allow reclosure of 22SJ54. The root cause of this event is Defective Procedure, per NUREG-1022.
S2.0P-ST.SSP-0010(Q) did not indicate that operation of TS-603 would result in opening of 22SJ54. Proc"edures have been revised to identify test switches which affect SJ54 valves and require that the appropriate SJ54 breaker be cleared and tagged. Integrated Operating Procedure IOP-6 (Hot Standby to Cold Shutdown) has been revised (both Units) to tag all SJ54 valve breakers when RCS pressure is less than or equal to 1000 psig. A detailed technical review of all SSPS slave relay testing procedures will be performed.
Procedural inadequacy identified with IOP-6 and S2.0P-ST.SSP-0010(Q) and the procedure identified in LER 311/92-005-00, will be examined to determine if any generic implications exist. NRC Form 366 (6-89)
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station Unit 2 DOCKET NUMBER 5000311 PLANT AND SYSTEM IDENTIFICATION:
Westinghouse
-Pressurized Water Reactor LER NUMBER 93-014-00 PAGE 2 of 5 Energy Industry Identification system (EIIS) codes are identified in the text as {xx} IDENTIFICATION OF OCCURRENCE:
., Engineered Safety Featqres Actuation (22 Reactor Coolant System Accumulator Discharge) and Resultant Pressurizer Overpressure Protection System (POPS) Channel I Actuation Event Date: 12/28/93 Report Date: 1/27/94 This report was initiated by Incident Report No.93-529 CONDITIONS PRIOR TO OCCURRENCE:
Mode 5, due to forced outage -Reactor Coolant system (RCS) Pressure approximately 320 psig -RCS Temperature between 170-l80°F Solid State Protection System (SSPS) Train B Slave Relays Testing in progress in accordance with procedure S2.0P-ST.SSP-0010(Q).
DESCRIPTION OF OCCURRENCE:
On December 28, 1993, at 0850 hours0.00984 days <br />0.236 hours <br />0.00141 weeks <br />3.23425e-4 months <br />, Reactor Coolant System {AB} 22 Accumulator outlet valve 22SJ54 unexpectedly opened and injected an estimated volume of 1735 to 2640 gallons (2200 ppm boric acid) into the RCS. The resultant RCS pressure transient actuated POPS Channel I, causing Pressurizer Relief Valve 2PR1 to open at 375 psig. Highest indicated RCS pressure was approximately 372 psig. RCS pressure decreased to approximately 280 psig prior to being recovered by the Pressurizer heaters. This event occurred when test switch TS-603 was operated, per S2.0P-ST.SSP-0010(Q).
Plant equipment responded properly to this event and TS-603 was reset to allow reclosure of 22SJ54. The NRC was notified of this event pursuant to 10 CFR5 0
Availability of RCS accumulators ensures a sufficient volume of borated water will be immediately forced into the reactor core through each reactor cold leg in the event RCS pressure decreases below the pressure of the accumulators.
This initial surge water into the reactor core provides the initial cooling mechanism during postulatedlarge RCS pipe ruptures.
RCS accumulators are required Operable during Modes 1, 2, and 3 when the RCS pressure is greater
- LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station Unit 2 DOCKET NUMBER 5000311 ANALYSIS OF OCCURRENCE: (cont_' d) LER NUMBER 93-014-00 PAGE 3 of 5 than 1000 psig. An operable RCS accumulator requires its discharge valve be opened and its associated power lockout switch be in the "LOCKED OUT" position.
When RCS pressure is less than 1000 psig operating procedures require the RCS discharge valves be closed. This prevents an accumulator from injecting its contents during normal RCS depressurization and cooldown.
Operability of the twq POPSs or an RCS vent opening ensures protection of the RCS pressure*
transients which could exceed the limits of Appendix G to lOCFR Part 50 when one or more the RCS cold legs are less than or equal to 312°F. Either POPS has adequate relieving capability to protect the RCS from overpressurization when the transient is limited to either 1) the start of an idle Reactor Coolant Pump with the secondary water temperature to the steam generator less than or equal to 50°F above the RCS cold leg temperatures, or 2) the start of a safety injection pump and its injection into a water solid RCS. While performing SSPS Train B Slave Relays Testing, RCS 22 Accumulator outlet valve 22SJ54 unexpectedly opened and injected an estimated volume in the range of 1735 to 2640 gallons (2200 ppm boric acid) into the RCS. The resultant RCS pressure transient actuated POPS Channel I, causing Pressurizer Relief Valve 2PR1 to open at 375 psig. 2PR1 open indications included overhead annunciation and Pressurizer Relief Tank (PRT) pressure and temperature indication.
In addition, indications of decreasing accumulator level and pressure were received.
Highest indicated RCS pressure was approximately 372 psig, as recorded by PT-403 (RCS 11 hot leg pressure transmitter).
Accumulator pressure decreased to approximately RCS pressure which terminated the injection.
RCS pressure decreased to approximately 280 psig prior to being recovered by the Pressurizer heaters. This event occurred when test switch TS-603 was operated, as specified by the involved test procedure, S2.0P-ST.SSP-0010(Q).
Plant equipment responded properly to this event and TS-603 was reset to reclose 22SJ54. . APPARENT CAUSE OF OCCURRENCE:
The root cause of this event is Defective Procedure, per NUREG-1022.
S2.0P-ST.SSP-0010(Q) did not indicate that operation of TS-603 would result in opening of 22SJ54. During January 1993, the Procedures Upgrade Program (PUP) completed the technical review of slave relay test procedures, which included S2.0P-ST.SSP-0010(Q).
However, this review did not identify that SSPS Train "B" Test switch (TS603) would send an open signal to 22SJ54 when placed in the "operate output" position.
As a result, the surveillance test procedure omitted relevant information.
This procedural inadequacy had not been identified during prior performances of the procedure since the procedure is normally LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station Unit 2 DOCKET NUMBER 5000311 APPARENT CAUSE OF OCCURRENCE:
{cont'd) LER NUMBER 93-014-00 PAGE 4 of 5 performed at RCS pressures above 1000 psig. At RCS pressures above 1000 psig, the accumulator is required to be operable with its discharge valve open. Therefore, the test signal would be applied to an already open valve. Performance of this procedure is required once per 62 days and is applicable in Modes 1-4. This event occurred while performing the procedure in Mode 5 with RCS pressure less than 1000 psig. At the time of this event, the procedure was being performed to allow entry into Mode 4. . . A contributor to this procedural inadequacy resulting in an ESF actuation (during prior Mode 5 performance of the procedure) was a procedural change to Integrated Operating Procedure IOP-6 (Hot Standby to Cold Shutdown) made in November 1991. This change was initiated due to Technical Specification (TS) Amendments 130 and 109, for Units 1 and 2, respectively, which appropriately removed the TS requirement to clear and tag the SJ54 valve breakers when greater than 1000 psig. However, the procedure change also removed a requirement to administratively clear and tag the breaker when less than 1000 psig, which subsequent review following this event showed to be inappropriate.
PREVIOUS SIMILAR OCCURRENCES:
LER 311/92-005-00 reported a prior occurrence, caused by procedure inadequacy involving SSPS Procedure S2.0P-ST.SSP-OOOl(Q), Manual Safety Injection, and the concurrent replacement of Rosemount steam flow transmitters.
Corrective action to this event consisted of revising the procedure to identify the consequence of moving the Mode Select Switch to TEST as well as the review and appropriate revision of other station procedures involving use of this switch. SAFETY SIGNIFICANCE:
This event did not affect the health and safety of the public.. It is reportable as an Engineered Safety Features Actuation pursuant to lOCFR50.73(a)
(2) (iv). In addition, this event is reportable in accordance with Technical Specification (TS) Action Statement 3.4.10.3.c.
and pursuant to the requirements of TS 6.9.2. Two concerns associated with this event were the possibilities of nitrogen injection into the RCS and pressurized thermal shock (PTS): Nitrogen was not injected into the RCS. A fully charged accumulator will discharge nitrogen into the RCS if pressurizer pressure is less than 162 psig. Since pressurizer pressure was 320 psig, a minimum of 3785 gallons boric acid volume and all nitrogen remained inside the accumulator.
The reactor was not subjected to PTS. The increase in
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- LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station Unit 2 DOCKET NUMBER 5000311 LER NUMBER 93-014-00 PAGE 5 of 5 SAFETY SIGNIFICANCE: (cont'd) pressurizer pressure was maintained at a small value (55 psid) due to relief valve 2PR1 opening and the pressurizer operable with a steam bubble. If the pressurizer had been solid, the relief valve(s) would have passed water instead of steam and a much larger increase in pressure would have occurred.
Also, the reactor was exposed to the water surge for a short time period and in such a manner that the reactor vessel wall temperature change was insign*ificant.
Following this event, Engineering performed calculations to determine the potential consequences of a single accumulator and of all four accumulators discharging into the RCS with a .solid pressurizer.
Results from these calculations show that under worst case conditions (solid pressurizer) operation would not have occurred outside of acceptable temperature/pressure relationships as defined by TS. Due to the recognized significance of this concern, corrective action involving the SJ54 valves, as described below, has been taken to mitigate this concern. CORRECTIVE ACTION: SSPS slave relay surveillance procedures have been revised to identify test switches which affect SJ54 valves and require that the appropriate SJ54 breaker be cleared and tagged. 1(2)-IOP-6 has been revised to tag all SJ54 valve breakers when RCS pressure is less than or equal to 1000 psig. Engineering performed calculations to determine the impact of a single Accumulator and of all four Accumulators discharging into the RCS during a solid plant condition.
A detailed technical review of all SSPS slave relay testing procedures will be performed.
Procedural inadequacy identified with IOP-6 and S2.0P-ST.SSP-0010(Q) and the procedure identified in LER 311/92-005-00, will be examined to determine if any generic neral Manager -Salem Operations MJPJ:pc SORC Mtg.94-008