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=Text=
=Text=
{{#Wiki_filter:.
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                                                                                                                    .
                                                                                                                          -        -                        - - - - - -              ---
                                                                      ,
              '                                                                              '
        '
contact stock: 1                    I      I      I      I    I    l                      tetEAsE PRiuTcR TYPE Att nEcuinto inecRuATisNi i                                      .@
contact stock: 1                    I      I      I      I    I    l                      tetEAsE PRiuTcR TYPE Att nEcuinto inecRuATisNi i                                      .@
Io lilsl eN l JuCENset l0 lCCoot      lP l1 lglis              0l O! -l 0 ]uCENst      O l 0Nvusan  l0 l0 l- l0 l0 as@l          l                                                  ]      ]g 7                                                  24                                                                                  a 4uCENss  l 1 l mE        1 ll']a 1-    l@l se car      se cort                                                                  ~
Io lilsl eN l JuCENset l0 lCCoot      lP l1 lglis              0l O! -l 0 ]uCENst      O l 0Nvusan  l0 l0 l- l0 l0 as@l          l                                                  ]      ]g 7                                                  24                                                                                  a 4uCENss  l 1 l mE        1 ll']a 1-    l@l se car      se cort                                                                  ~
                                                                                                                                    '
l o I8 i IhEu#C lL)@l0151010l01211 I                              60              si              DOCKET NUM3ER 9 @ l 01 2l 64    SS        EVENT 1lDATE 3l 81 0 l @ l 01 3I 01 61 8) O 74      75            MEPORT DATE 80 EVENT CESCRIPTloN AND PROBABLE CONSEQUENCES h
l o I8 i IhEu#C lL)@l0151010l01211 I                              60              si              DOCKET NUM3ER 9 @ l 01 2l 64    SS        EVENT 1lDATE 3l 81 0 l @ l 01 3I 01 61 8) O 74      75            MEPORT DATE
                                                                                                                                                                        ***
80
* EVENT CESCRIPTloN AND PROBABLE CONSEQUENCES h
   ;  I O I 21 i          On February 13, 1980, while cerforming a 10 hour test on Standbv Gas                                                                                                                I r5 ry] l            Treatment
   ;  I O I 21 i          On February 13, 1980, while cerforming a 10 hour test on Standbv Gas                                                                                                                I r5 ry] l            Treatment
* System (SGTS) #1, the system flow was observed to be less'tha'n                                                                                                        1-i o i,i i          that prescribed in the Technical Specifications. The flow observed was                                                                                                              1
* System (SGTS) #1, the system flow was observed to be less'tha'n                                                                                                        1-i o i,i i          that prescribed in the Technical Specifications. The flow observed was                                                                                                              1
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bility.
bility.
io 6a1 i 7    t 9 E                CE          5 BC E                    CCMPCNENT CCC E                        SUSC NE                $      E lotel 7      8 lS IC l@ lE l@ l X l@ l Bl Ll 0 l W l E lR i@ l Z l@ lZ 9          to            11                12            13                                    18          19                    20 l@
io 6a1 i 7    t 9 E                CE          5 BC E                    CCMPCNENT CCC E                        SUSC NE                $      E lotel 7      8 lS IC l@ lE l@ l X l@ l Bl Ll 0 l W l E lR i@ l Z l@ lZ 9          to            11                12            13                                    18          19                    20 l@
SE QUENTI Al.                          OCCURRENCf            MEPORT                          REvtslON
SE QUENTI Al.                          OCCURRENCf            MEPORT                          REvtslON EVENT YE AR                                    REPORT NO,                                  COCE                TYPE                                  NO.
                                      ,,,
EVENT YE AR                                    REPORT NO,                                  COCE                TYPE                                  NO.
t
t
                   @ ,a,.E  EgR,RO        I 810 l                l-l              l 0 JO l7 l                l/l            10 13 l                lL l                l-l            l 0l 21          22          23              24            2s          27              28          29          30                    31            32 N A        C              0 P NT                M                                                                    POR      B.      SU U                    MANUF            RER Iss Al@l34 zl@                    121@
                   @ ,a,.E  EgR,RO        I 810 l                l-l              l 0 JO l7 l                l/l            10 13 l                lL l                l-l            l 0l 21          22          23              24            2s          27              28          29          30                    31            32 N A        C              0 P NT                M                                                                    POR      B.      SU U                    MANUF            RER Iss Al@l34 zl@                    121@
Line 50: Line 37:
       ,,,,,j              EF1-8 were replaced. Operability tests and filter tests were acain
       ,,,,,j              EF1-8 were replaced. Operability tests and filter tests were acain
       ,,,,,,              performed to prove system operabil,ity.
       ,,,,,,              performed to prove system operabil,ity.
                                                                                                                      '
                 * *'EY A                sPOwEn                            OTufnsTATUS @    '
                 * *'EY A                sPOwEn                            OTufnsTATUS @    '
50        Y                            OtSCOVERY DESCRIPTION @
50        Y                            OtSCOVERY DESCRIPTION @
liI5llHl@ l0l0l0l@l                                                        NA                  l      [,3 j@l                  Surveillance Test 7                                              12        is                                44        as                                                                                                s s 4 ,,, ,i g aELEASE                                                                                                                              LOCATION OF RELEASE @
liI5llHl@ l0l0l0l@l                                                        NA                  l      [,3 j@l                  Surveillance Test 7                                              12        is                                44        as                                                                                                s s 4 ,,, ,i g aELEASE                                                                                                                              LOCATION OF RELEASE @
AMOUNT                        OF" ACTIVITY                            @l i
AMOUNT                        OF" ACTIVITY                            @l i
l    li I s l l Z l @D OF REl.EASEWgl                                    NA                                      [                                  NA
l    li I s l l Z l @D OF REl.EASEWgl                                    NA                                      [                                  NA nasONNE$.ExecstIAEs Nu..E .                Tvn            oE CainiON @
'    '    * *                  '                                                                                **
* nasONNE$.ExecstIAEs Nu..E .                Tvn            oE CainiON @
NA I t 171 l 0 l 0 l 0 l@l Z l@l                                                                                                                                                                          s
NA I t 171 l 0 l 0 l 0 l@l Z l@l                                                                                                                                                                          s
     '      ' '                                            is rEnsONNEI'auu' lies l
     '      ' '                                            is rEnsONNEI'auu' lies l
Line 64: Line 48:
7      8 9                    13 LOSS OF 04 OAMAGE TO FACIUTY Q -
7      8 9                    13 LOSS OF 04 OAMAGE TO FACIUTY Q -
TYPE        DESCRtPTION                        v NA                      80031906g6 ggj y @l 7      8 9          . 10 "U                                                                                                                                                    ._
TYPE        DESCRtPTION                        v NA                      80031906g6 ggj y @l 7      8 9          . 10 "U                                                                                                                                                    ._
NRC t%E ONLY
NRC t%E ONLY l
,
l
'
     @ b,@[l                10
     @ b,@[l                10
                                 ,gg,y,o Weekly News Release - 3/13/80 SS l    IIIII1111III 49,,          , . . , , , ,      Il
                                 ,gg,y,o Weekly News Release - 3/13/80 SS l    IIIII1111III 49,,          , . . , , , ,      Il
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455-8784 NAME OF PREPARER
455-8784 NAME OF PREPARER


    .
        .
      ,
            ,
Jersey Central Power & Ught Company
Jersey Central Power & Ught Company
                 . kh              ('                                                    Madison Avenue at Punen Bowt Road Mornstown, New Jersey o7960 (201)455-8200 OYSTER CREEK NUCLEAR GENERATING STATION Forked River, New Jersey 08731 Licensee Event Report Reportable Occurrence No. 50-219/80-7/3L
                 . kh              ('                                                    Madison Avenue at Punen Bowt Road Mornstown, New Jersey o7960 (201)455-8200 OYSTER CREEK NUCLEAR GENERATING STATION Forked River, New Jersey 08731 Licensee Event Report Reportable Occurrence No. 50-219/80-7/3L Report Date March 7, 1980 Occurrence Date                  .
                                                                                                                    .
Report Date March 7, 1980 Occurrence Date                  .
February 13, 1980 Identification of Occurrence Standby Gas Treatment System (SGTS) #1 was found to be operating with a flow less than that prescribed in the Technical Specifications.
February 13, 1980 Identification of Occurrence Standby Gas Treatment System (SGTS) #1 was found to be operating with a flow less than that prescribed in the Technical Specifications.
This event is considered to be a reportable occurrence as defined in the Techni-cal Specifications, paragraph 6.9.2,(b),(2).
This event is considered to be a reportable occurrence as defined in the Techni-cal Specifications, paragraph 6.9.2,(b),(2).
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Analysis of Occurrence                                                                              .
Analysis of Occurrence                                                                              .
Standby Gas Treatment System is used to process the reactor building atmosphere, should conditions develop which require its functioning, and exhaust it through the plant stack. Despite its degraded condition, SGTS #1 was considered oper-able since only the process rate of the system was affected and not its ability to process. SGTS #2 was available to perform its function at rated system capa-bility. The safety significance of this event is considered minimal, since the                                      {
Standby Gas Treatment System is used to process the reactor building atmosphere, should conditions develop which require its functioning, and exhaust it through the plant stack. Despite its degraded condition, SGTS #1 was considered oper-able since only the process rate of the system was affected and not its ability to process. SGTS #2 was available to perform its function at rated system capa-bility. The safety significance of this event is considered minimal, since the                                      {
                                                                                                                              ;
only concern was a loss of SGTS redundancy at rated system flow.                                                    1 l
only concern was a loss of SGTS redundancy at rated system flow.                                                    1 l
l
l
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. s ..
. s ..
                                                                                        .
Reportable Occurrence No. 50-219/80-7/3L                                  Page 2 March 7, 1980 Corrective Action SGTS #1 was taken out of service after SGTS #2 was confirmed to be functional at rated system flow, and the subject exhaust fan drive belts were replaced.
Reportable Occurrence No. 50-219/80-7/3L                                  Page 2 March 7, 1980 Corrective Action SGTS #1 was taken out of service after SGTS #2 was confirmed to be functional at rated system flow, and the subject exhaust fan drive belts were replaced.
Operability tests and filter aP tests were again perfonned to prove the system operable.
Operability tests and filter aP tests were again perfonned to prove the system operable.
Failure Data Not Applicable.}}
Failure Data Not Applicable.}}

Latest revision as of 23:15, 21 February 2020

LER 80-007/03L-0:on 800213,while Performing 10-h Test on Standby Gas Treatment Sys 1,flow Was Less than Tech Spec Limit.Caused by Slipping Drive Belts on Exhaust Fan EF1-8. Drive Belts Replaced
ML19305B366
Person / Time
Site: Oyster Creek
Issue date: 03/06/1980
From: Ross D
JERSEY CENTRAL POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19305B337 List:
References
LER-80-007-03L, LER-80-7-3L, NUDOCS 8003190586
Download: ML19305B366 (3)


Text

.

contact stock: 1 I I I I I l tetEAsE PRiuTcR TYPE Att nEcuinto inecRuATisNi i .@

Io lilsl eN l JuCENset l0 lCCoot lP l1 lglis 0l O! -l 0 ]uCENst O l 0Nvusan l0 l0 l- l0 l0 as@l l ] ]g 7 24 a 4uCENss l 1 l mE 1 ll']a 1- l@l se car se cort ~

l o I8 i IhEu#C lL)@l0151010l01211 I 60 si DOCKET NUM3ER 9 @ l 01 2l 64 SS EVENT 1lDATE 3l 81 0 l @ l 01 3I 01 61 8) O 74 75 MEPORT DATE 80 EVENT CESCRIPTloN AND PROBABLE CONSEQUENCES h

I O I 21 i On February 13, 1980, while cerforming a 10 hour1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br /> test on Standbv Gas I r5 ry] l Treatment
  • System (SGTS) #1, the system flow was observed to be less'tha'n 1-i o i,i i that prescribed in the Technical Specifications. The flow observed was 1

,ois,g 1350 CFM, which is less than rated capacity of 2600 CFM. Only the pro-  ;

i o ,, i i ces's rate of SGTS #1 was affected and not its ability to process. Also r SGTS #2 was available to perform its function at rated system capa- p

, o 3,; ;

bility.

io 6a1 i 7 t 9 E CE 5 BC E CCMPCNENT CCC E SUSC NE $ E lotel 7 8 lS IC l@ lE l@ l X l@ l Bl Ll 0 l W l E lR i@ l Z l@ lZ 9 to 11 12 13 18 19 20 l@

SE QUENTI Al. OCCURRENCf MEPORT REvtslON EVENT YE AR REPORT NO, COCE TYPE NO.

t

@ ,a,.E EgR,RO I 810 l l-l l 0 JO l7 l l/l 10 13 l lL l l-l l 0l 21 22 23 24 2s 27 28 29 30 31 32 N A C 0 P NT M POR B. SU U MANUF RER Iss Al@l34 zl@ 121@

ss lsozi@- 3710101010 NOURShlS$sYsN 4o l43Y !@ d@ 42 lNl@

42 l-l-l-l-44 4 CAusE DESCRtPTION AND CORRECTIVE ACTIONS 27 Iitol l The cause of this occurrence was sliaoina drive belts nn avhwet %

ii,ii l EF1-8. SGTS #1 was taken out of service after SGTS 42 was confi-ad % l

,,,,, i be. functional at rated system flow, and the drive belts on exhaust fan

,,,,,j EF1-8 were replaced. Operability tests and filter tests were acain

,,,,,, performed to prove system operabil,ity.

  • *'EY A sPOwEn OTufnsTATUS @ '

50 Y OtSCOVERY DESCRIPTION @

liI5llHl@ l0l0l0l@l NA l [,3 j@l Surveillance Test 7 12 is 44 as s s 4 ,,, ,i g aELEASE LOCATION OF RELEASE @

AMOUNT OF" ACTIVITY @l i

l li I s l l Z l @D OF REl.EASEWgl NA [ NA nasONNE$.ExecstIAEs Nu..E . Tvn oE CainiON @

NA I t 171 l 0 l 0 l 0 l@l Z l@l s

' ' ' is rEnsONNEI'auu' lies l

NuweEn oEscairriON@

l g l 0 l 0 l 0 [@l 12 NA i

7 8 9 13 LOSS OF 04 OAMAGE TO FACIUTY Q -

TYPE DESCRtPTION v NA 80031906g6 ggj y @l 7 8 9 . 10 "U ._

NRC t%E ONLY l

@ b,@[l 10

,gg,y,o Weekly News Release - 3/13/80 SS l IIIII1111III 49,, , . . , , , , Il

~7 8 9 .

" * $$ PHONE.

455-8784 NAME OF PREPARER

Jersey Central Power & Ught Company

. kh (' Madison Avenue at Punen Bowt Road Mornstown, New Jersey o7960 (201)455-8200 OYSTER CREEK NUCLEAR GENERATING STATION Forked River, New Jersey 08731 Licensee Event Report Reportable Occurrence No. 50-219/80-7/3L Report Date March 7, 1980 Occurrence Date .

February 13, 1980 Identification of Occurrence Standby Gas Treatment System (SGTS) #1 was found to be operating with a flow less than that prescribed in the Technical Specifications.

This event is considered to be a reportable occurrence as defined in the Techni-cal Specifications, paragraph 6.9.2,(b),(2).

Conditions Prior to Occurrence The plant was shutdown for a refueling / maintenance outage.

The reactor mode switch was locked in refuel.

The reactor cavity was flooded and less than 212*F.

Description of Occurrence On Wednesday, February 13, 1980, at approximately 2130 hours0.0247 days <br />0.592 hours <br />0.00352 weeks <br />8.10465e-4 months <br />, while performing a 10 hour1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br /> test on SGTS #1, the system flow was observed to be 1350 CFM, which is less than rated capacity of 2600 CFM.

Apparent Cause of Occurrence The reduced system flow was caused by slipping drive belts on exhaust fan EF1-8.

Analysis of Occurrence .

Standby Gas Treatment System is used to process the reactor building atmosphere, should conditions develop which require its functioning, and exhaust it through the plant stack. Despite its degraded condition, SGTS #1 was considered oper-able since only the process rate of the system was affected and not its ability to process. SGTS #2 was available to perform its function at rated system capa-bility. The safety significance of this event is considered minimal, since the {

only concern was a loss of SGTS redundancy at rated system flow. 1 l

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Reportable Occurrence No. 50-219/80-7/3L Page 2 March 7, 1980 Corrective Action SGTS #1 was taken out of service after SGTS #2 was confirmed to be functional at rated system flow, and the subject exhaust fan drive belts were replaced.

Operability tests and filter aP tests were again perfonned to prove the system operable.

Failure Data Not Applicable.