|
|
(3 intermediate revisions by the same user not shown) |
Line 17: |
Line 17: |
|
| |
|
| =Text= | | =Text= |
| {{#Wiki_filter:Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038 Salem Generating Station U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 | | {{#Wiki_filter:Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038 Salem Generating Station August 20, 1993 U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 |
|
| |
|
| ==Dear Sir:== | | ==Dear Sir:== |
| SALEM GENERATING STATION LICENSE NO. DPR-70 DOCKET NO. 50-272 UNIT NO. 1 LICENSEE EVENT REPORT 93-014-00 August 20, 1993 This Licensee Event Report is being submitted pursuant to the requirements of the Code of Federal Regulations lOCFR 50.73(a) (2) (ii) (B). This report is required to be issued within thirty (30) days of event discovery. | | |
| MJPJ:pc Distribution | | SALEM GENERATING STATION LICENSE NO. DPR-70 DOCKET NO. 50-272 UNIT NO. 1 LICENSEE EVENT REPORT 93-014-00 This Licensee Event Report is being submitted pursuant to the requirements of the Code of Federal Regulations 10CFR 50.73(a) (2) (ii) (B). This report is required to be issued within thirty (30) days of event discovery. |
| ... ) -. 0 Ii r--: "-'"' '-* Ju' The EnerQY People 9308300321 930820 PDR 05000272 S PDR Sincerely yours, C. A Vondra General Manager -Salem Operations 95-2189 ( 10M) 12-89 NRC F0RM 366 (6-89) U.S. NUCLEAR REGULATORY COMMISSION APPROVED OMB NO. 3150-0104 LICENSEE EVENT REPORT (LERI FACILITY NAME 11) Salem Station -Unit 1 TITLE 141 EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH IP-530). U.S. NUCLEAR REGULATORY COMMISSION.
| | Sincerely yours, C. A Vondra General Manager - |
| WASHINGTON. | | Salem Operations MJPJ:pc Distribution |
| DC 20555. AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104). | | . . )~ -. 0 Ii'-* r--Ju'*~ : |
| OFFICE OF MANAGEMENT AND BUDGET. WASHINGTON. | | The EnerQY People 9308300321 930820 95-2189 ( 10M) 12-89 PDR ADOC~ 05000272 S PDR |
| DC 20503. I DOCKET NUMBER 12) I PAGE 13} 01s101010121712 1joFOl5 4KV Vital Bus Second Level Undervoltage Protection Dropout Setpoint Concern (both Units). EVENT OATE (5) LER NUMBER (6) REPORT DATE 17) OTHER FACILITIES INVOLVED IB) MONTH DAY YEAR YEAR rt j( | | |
| MONTH DAY YEAR FACILITY NAMES OOCKET NUMBERISl Salem Unit 2 o 1s1 o Io Io 13 1111 o I 1 2 I 2 9 3 9 I 3 -a I 1 .14 -a I o o I s 21 a 9 I 3 OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE Rl:QUIREMENTS OF 10 CFR §: (Ch*ck on* or mor* of th* following) 111) MODE 19) 1 20.402lb) 20.405lcl 50.731*)12Hiv) | | NRC F0RM 366 U.S. NUCLEAR REGULATORY COMMISSION (6-89) APPROVED OMB NO. 3150-0104 EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD LICENSEE EVENT REPORT (LERI COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH IP-530). U.S. NUCLEAR REGULATORY COMMISSION. WASHINGTON. DC 20555. AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104). OFFICE OF MANAGEMENT AND BUDGET. WASHINGTON. DC 20503. |
| POWER I 0 18 I 0 .....__ --,_ 20.4061*111 Hil 50.3Slcll1) | | FACILITY NAME 11) DOCKET NUMBER 12) I PAGE 13} |
| IX 50.73l*H2llvl
| | Salem TITLE 141 Generatin~ Station - Unit 1 I01s101010121712 1joFOl5 4KV Vital Bus Second Level Undervoltage Protection Dropout Setpoint Concern (both Units). |
| ..__ ,....__ 20.4051aH1lliil 50.38(cll2) 50.731*1121 Mil ..__ -20.40tilall1 Hiiil 50.731*ll2)(i) 50.73l*ll2HvlllHAI
| | EVENT OATE (5) LER NUMBER (6) REPORT DATE 17) OTHER FACILITIES INVOLVED IB) |
| ..__ ....__ 20.4061*>11
| | MONTH DAY YEAR YEAR rt SE~~~~~~AL j( ~~~~~~ MONTH DAY YEAR FACILITY NAMES OOCKET NUMBERISl Salem Unit 2 o 1s1 o Io Io 13 1111 o I1 I 2 2 9 3 9 I3 - a I 1 .14 - a Io oIs 21 a 9 I3 OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE Rl:QUIREMENTS OF 10 CFR §: (Ch*ck on* or mor* of th* following) 111) |
| )(Iv) x 60.73l*ll2llii) 50.73lall2HvlllHBI | | MODE 19) |
| --20.4061*)11 )lvl 50.73l*ll2lliiil 50.73lall2Hxl LICENSEE CONTACT FOR THIS LER 112) NAME M. J. Pastva. Jr. -LER Coordinator AREA CODE .....__ .....__ ....__ 73.71lb) 73.71lc) OTHER (SP1Jcify in Abst,.ct b*low *nd in TDxt. NRC Form 366AJ TELEPHONE NUMBER b 1019* 313*19 1-1511 1615 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT 113) CAUSE SYSTEM COMPONENT I I I I I I I I I I I I I I SUPPLEMENTAL REPORT EXPECTED 114) r:-i YES (If y*s, EXPECTED SUBMISSION DATE) ABSTRACT (Limit to 1400 spaces, i.e .* approKimtJtely fifteen single-space typewritten lines) (16) I I I I I I I I I I I I I I EXPECTED SUBMISSION DATE (151 MONTH DAY YEAR *110 ?1'1 ql':l On 7/22/93, it was determined that the present 91.6% dropout setpoint for second level undervoltage (UV) protection of the 4 kilovolt (KV) vital buses (both Salem Units), may not fully protect motors should the bus voltage degrade to less than 93.2% but greater than 91.6%. This is contrary to Branch Technical Position (BTP)-PSB-1 and the Updated Final Safety Analysis Report (UFSAR). However, engineering calculation shows, given the postulated worst case design basis event, vital bus recovery voltage will not degrade to less than 93.2%. The 91.6% dropout setpoint _was based on the lowest voltage the 4.16 KV motors could be allowed to operate (i.e. 90%) due to voltage drops in the *motors' cables and relay inaccuracy considerations.
| | I |
| The revised recovery voltage of 93.2% will now maintain all motors operable under degraded voltage conditions. | | ---------L-=-i~ 20.402lb) 1 20.4061*111 Hil - |
| During the next refueling outage on each Unit, design changes will be implemented to change the relay setpoint to meet the requirements of BTP-PSB-1. | | 20.405lcl 50.3Slcll1) |
| In the interim, administrative controls are being implemented. | | IX 50.731*)12Hiv) 50.73l*H2llvl 73.71lb) 73.71lc) |
| Technical Specifications and the UFSAR will be reviewed and revised as appropriate. | | POWER L~~~L 0 18 I 0 .....__ 20.4051aH1lliil ..__ 50.38(cll2) 50.731*1121 Mil ....__ OTHER (SP1Jcify in Abst,.ct b*low *nd in TDxt. NRC Form 20.40tilall1 Hiiil 50.731*ll2)(i) 50.73l*ll2HvlllHAI 366AJ 20.4061*>11 )(Iv) 20.4061*)11 )lvl -x 60.73l*ll2llii) 50.73l*ll2lliiil - |
| Conditions necessary for the design concern coincident with a prerequisite plant transient have not occurred. | | LICENSEE CONTACT FOR THIS LER 112) 50.73lall2HvlllHBI 50.73lall2Hxl NAME TELEPHONE NUMBER AREA CODE M. J. Pastva. Jr. - LER Coordinator b 1019* 313*19 1-1511 1615 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT 113) |
| As such, the health and safety of the public has not been affected by this concern. Analysis of this event is continuing. | | CAUSE SYSTEM COMPONENT I I I I I I I I I I I I I I I I I I I I I I I I I I I I SUPPLEMENTAL REPORT EXPECTED 114) MONTH DAY YEAR EXPECTED SUBMISSION r:-i YES (If y*s, com~lot* EXPECTED SUBMISSION DATE) |
| Upon completion of this effort, a supplement to this LER will be submitted. | | DATE (151 |
| | *110 ?1'1 ql':l ABSTRACT (Limit to 1400 spaces, i.e .* approKimtJtely fifteen single-space typewritten lines) (16) |
| | On 7/22/93, it was determined that the present 91.6% dropout setpoint for second level undervoltage (UV) protection of the 4 kilovolt (KV) vital buses (both Salem Units), may not fully protect motors should the bus voltage degrade to less than 93.2% but greater than 91.6%. This is contrary to Branch Technical Position (BTP)-PSB-1 and the Updated Final Safety Analysis Report (UFSAR). However, engineering calculation shows, given the postulated worst case design basis event, vital bus recovery voltage will not degrade to less than 93.2%. The 91.6% dropout setpoint |
| | _was based on the lowest voltage the 4.16 KV motors could be allowed to operate (i.e. 90%) due to voltage drops in the *motors' cables and relay inaccuracy considerations. The revised recovery voltage of 93.2% will now maintain all motors operable under degraded voltage conditions. |
| | During the next refueling outage on each Unit, design changes will be implemented to change the relay setpoint to meet the requirements of BTP-PSB-1. In the interim, administrative controls are being implemented. Technical Specifications and the UFSAR will be reviewed and revised as appropriate. Conditions necessary for the design concern coincident with a prerequisite plant transient have not occurred. As such, the health and safety of the public has not been affected by this concern. Analysis of this event is continuing. Upon completion of this effort, a supplement to this LER will be submitted. |
| NRC Form 366 (6-89) | | NRC Form 366 (6-89) |
| LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station Unit 1 DOCKET NUMBER 5000272 PLANT AND SYSTEM IDENTIFICATION: | | |
| Westinghouse | | LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 1 5000272 93-014-00 |
| -Pressurized Water Reactor LER NUMBER 93-014-00 PAGE | | * 2 of 5 PLANT AND SYSTEM IDENTIFICATION: |
| * 2 of 5 Energy Industry Identification System (EIIS) codes are identified in the text as {xx} IDENTIFICATION OF OCCURRENCE:
| | Westinghouse - Pressurized Water Reactor Energy Industry Identification System (EIIS) codes are identified in the text as {xx} |
| 4 KV Vital Bus Second Level Undervoltage Protection Dropout Setpoint Concern (both Salem Units) Event Discovery Date: 7/22/93 Report Date: 8/20/93 This report was initiated by Incident Report No. 93-320. This event is reportable per 10CFR50.73(a) | | IDENTIFICATION OF OCCURRENCE: |
| (2) (ii) (B) and 10CFR50.73(a) | | 4 KV Vital Bus Second Level Undervoltage Protection Dropout Setpoint Concern (both Salem Units) |
| (2) (v) (D). CONDITIONS PRIOR TO OCCURRENCE: | | Event Discovery Date: 7/22/93 Report Date: 8/20/93 This report was initiated by Incident Report No. 93-320. This event is reportable per 10CFR50.73(a) (2) (ii) (B) and 10CFR50.73(a) (2) (v) (D). |
| Unit 1: Mode 1 Reactor Power 80% -Unit Load 815 MWe Unit 2: Mode 1 Reactor Power 100% -Unit Load 1140 MWe DESCRIPTION OF OCCURRENCE: | | CONDITIONS PRIOR TO OCCURRENCE: |
| On July 22, 1993, it was determined.that the *present 91.6% dropout setpoint for second level undervoltage (UV) protection of the 4 kilovolt (KV) vital buses {VJ} (both Salem Units), will not fully protect motors at the 230 and 460 volt level should the 4KV bus voltage degrade to less than 93.2% but greater than 91.6%. This is contrary to Branch Technical Position (BTP)-PSB-1 and the Updated *.Final Safety Analysis Report (UFSAR). However, engineering calculation shows, given*the postulated worst case design basis event, vital bus recovery voltage will not degrade to less than 93.2%. The Nuclear Regulatory Commission was notified of this event per Code of Federal Regulations lOCFR50.72(b) | | Unit 1: Mode 1 Reactor Power 80% - Unit Load 815 MWe Unit 2: Mode 1 Reactor Power 100% - Unit Load 1140 MWe DESCRIPTION OF OCCURRENCE: |
| (1) (ii) (B). ANALYSIS OF OCCURRENCE: | | On July 22, 1993, it was determined.that the *present 91.6% dropout setpoint for second level undervoltage (UV) protection of the 4 kilovolt (KV) vital buses {VJ} (both Salem Units), will not fully protect motors at the 230 and 460 volt level should the 4KV bus voltage degrade to less than 93.2% but greater than 91.6%. This is contrary to Branch Technical Position (BTP)-PSB-1 and the Updated |
| Availability of minimum redundant alternating current (A.C.) power sources and distribution systems ensures sufficient power will be available to safety-related equipment for safe shutdown of the facility and the mitigation and control of accident conditions.within the facility, as required by General Design Criteria 17 of Appendix "A" to lOCFR Part 50. Per BTP-PSB-1, the plant licensing basis requires a second level of undervoltage protection for 4KV vital buses to ensure minimum motor terminal voltage for all safety-related
| | *.Final Safety Analysis Report (UFSAR). However, engineering calculation shows, given*the postulated worst case design basis event, vital bus recovery voltage will not degrade to less than 93.2%. |
| **, *---*-.,.
| | The Nuclear Regulatory Commission was notified of this event per Code of Federal Regulations 10CFR50.72(b) (1) (ii) (B). |
| -*---*
| | ANALYSIS OF OCCURRENCE: |
| --*----*---*
| |
| r :**** | | r :**** |
| LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station Unit 1 DOCKET NUMBER 5000272 ANALYSIS OF OCCURRENCE: (cont'd) LER NUMBER 93-014-00 PAGE 3 of 5 motors *. At Salem, when vital bus voltage drops below the dropout setpoint for relays providing this protection for greater than 13 seconds, vital bus loads are automatically transferred to their respective emergency diesel generators. | | Availability of minimum redundant alternating current (A.C.) power sources and distribution systems ensures sufficient power will be available to safety-related equipment for safe shutdown of the facility and the mitigation and control of accident conditions.within the facility, as required by General Design Criteria 17 of Appendix "A" to 10CFR Part 50. Per BTP-PSB-1, the plant licensing basis requires a second level of undervoltage protection for 4KV vital buses to ensure minimum motor terminal voltage for all safety-related |
| | **, *---*-.,. -*---* --~..-- --*- -- -*---* ****-----*~*. |
| | |
| | LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 1 5000272 93-014-00 3 of 5 ANALYSIS OF OCCURRENCE: (cont'd) motors *. At Salem, when vital bus voltage drops below the dropout setpoint for relays providing this protection for greater than 13 seconds, vital bus loads are automatically transferred to their respective emergency diesel generators. |
| As part of the self-initiated Electrical Engineering Self-Assessment Program, electrical calculations are being reviewed to ensure guidelines of BTP-PSB-1 are met. On July 1, 1993, review of Revision 1 of ES-15.00S(Q), "Salem Units 1 and 2 Degraded Grid study" identified a potential concern with the 91.6% dropout setpoint of the Units' 4KV vital buses (lA, lB, lC, 2A, 2B, and 2C). On July 22, 1993, further analysis of this concern determined the recovery vital bus voltage is 93.2% of 4.16KV following transfer of the Auxiliary Power Transformers (APTs) to the Station Power Transformers (SPTs). This voltage could result should a group bus transfer to the SPTs occur coincident with a Loss-of-Coolant Accident (LOCA) and the unaffected unit in startup or shutdown. | | As part of the self-initiated Electrical Engineering Self-Assessment Program, electrical calculations are being reviewed to ensure guidelines of BTP-PSB-1 are met. On July 1, 1993, review of Revision 1 of ES-15.00S(Q), "Salem Units 1 and 2 Degraded Grid study" identified a potential concern with the 91.6% dropout setpoint of the Units' 4KV vital buses (lA, lB, lC, 2A, 2B, and 2C). On July 22, 1993, further analysis of this concern determined the recovery vital bus voltage is 93.2% of 4.16KV following transfer of the Auxiliary Power Transformers (APTs) to the Station Power Transformers (SPTs). This voltage could result should a group bus transfer to the SPTs occur coincident with a Loss-of-Coolant Accident (LOCA) and the unaffected unit in startup or shutdown. |
| UFSAR Section 8.3.1.2 describes the setpoint as being determined using the 90% minimum.motor terminal voltage as the starting point. Since 93.2% bus voltage is required to ensure the minimum motor terminal voltage, the existing 91.6% dropout setpoint is not in compliance with the UFSAR or the BTP. However, because ES-15.00S(Q) calculations also show that vital bus recovery voltage will not | | UFSAR Section 8.3.1.2 describes the setpoint as being determined using the 90% minimum.motor terminal voltage as the starting point. |
| * degrade to a level at which actual motor degradation could occur, the intent of the UFSAR and BTP is still met. These calculations take credit for operation, prior to the event, of the load tap changers which are set to* maintain a_ minimum initial bus voltage of 4.3KV. Following event discovery, an evaluation to justify continued operation of both Salem Units, concluded the present dropout setpoint of the relays does not meet the intent of the BTP. However, Revision 1 of Engineering Calculation ES-15.00S(Q) determined there is not a significant safety concern with the present dropout setpoint provided the 4.16KV vital buses are maintained at 4.3KV or greater. Design changes will be implemented during the next refueling outage on each Unit to change the dropout setpoint to meet the intent of the BTP. * * * * * | | Since 93.2% bus voltage is required to ensure the minimum motor terminal voltage, the existing 91.6% dropout setpoint is not in compliance with the UFSAR or the BTP. However, because ES-15.00S(Q) calculations also show that vital bus recovery voltage will not |
| * For the interim, 4.16KV vital bus voltages are being monitored to assure load tap changers are operating properly to maintain a minimum bus voltage of 4. 3KV. In addition, bus voltages below 4. JKV will be. *r:'::* adjusted between 4.JKV and 4.5KV and restrictions concerning vital bus lineup will be in_effect (see "CORRECTIVE ACTIONS:" section). | | * degrade to a level at which actual motor degradation could occur, the intent of the UFSAR and BTP is still met. These calculations take credit for operation, prior to the event, of the load tap changers which are set to* maintain a_ minimum initial bus voltage of 4.3KV. |
| Analysis of this event is continuing. | | Following event discovery, an evaluation to justify continued operation of both Salem Units, concluded the present dropout setpoint of the relays does not meet the intent of the BTP. However, Revision 1 of Engineering Calculation ES-15.00S(Q) determined there is not a significant safety concern with the present dropout setpoint provided the 4.16KV vital buses are maintained at 4.3KV or greater. Design changes will be implemented during the next refueling outage on each Unit to change the dropout setpoint to meet the intent of the BTP. * * * * * |
| Included will be a historical assessment of the effect of the revised assumptions at vital bus levels below 4KV. Upon completion of this effort, a supplement to this LER will be submitted. | | * For the interim, 4.16KV vital bus voltages are being monitored to assure load tap changers are operating properly to maintain a minimum bus voltage of 4. 3KV. In addition, bus voltages below 4. JKV will be. *r:'::* |
| LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating station tinit 1 . --APPARENT CAUSE OF OCCURRENCE: | | adjusted between 4.JKV and 4.5KV and restrictions concerning vital bus lineup will be in_effect (see "CORRECTIVE ACTIONS:" section). |
| DOCKET NUMBER 5000272' LER NUMBER 93:...014-00 PAGE 4 of s The cause of this event is "Design, Manufacturing, Construction/Installation", per NUREG-1022.
| | Analysis of this event is continuing. Included will be a historical assessment of the effect of the revised assumptions at vital bus levels below 4KV. Upon completion of this effort, a supplement to this LER will be submitted. |
| The 91.6% dropout setpoint was based on the lowest voltage the 4.16 KV motors could be allowed to operate (i.e. 90%) due to voltage drops in the motors' cables and relay inaccuracy considerations. | | |
| The revised dropout setpoint, based upon the revised recovery voltage of 93.2%, will now maintain all motors operable under degraded voltage conditions. | | LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating station DOCKET NUMBER LER NUMBER PAGE tinit 1 .- - 5000272' 93:...014-00 4 of s APPARENT CAUSE OF OCCURRENCE: |
| | The cause of this event is "Design, Manufacturing, Construction/Installation", per NUREG-1022. The 91.6% dropout setpoint was based on the lowest voltage the 4.16 KV motors could be allowed to operate (i.e. 90%) due to voltage drops in the motors' cables and relay inaccuracy considerations. The revised dropout setpoint, based upon the revised recovery voltage of 93.2%, will now maintain all motors operable under degraded voltage conditions. |
| PRIOR SIMILAR OCCURRENCES: | | PRIOR SIMILAR OCCURRENCES: |
| No prior. similar.occurrences of this event were identified. | | No prior. similar.occurrences of this event were identified. |
| SAFETY SIGNIFICANCE: | | SAFETY SIGNIFICANCE: |
| Engineering is. currently completing its evaluation of the safety significance of past operation with the non-conservative second level. UV setpoint *. With the current interim controls, the health and safety of the public is not affected by this event. Upon completion of this evaluation this LER will be | | Engineering is. currently completing its evaluation of the safety significance of past operation with the non-conservative second level. |
| * CORRECTIVE ACTION: Design Changes will be implemented to change the relay setpoint on both Units to meet the requirements of BTP-PSB-1 and be in accordance with the plant design basis. This will be done during the upcoming Unit 1 refueling outage and the next Unit 2 refueling outage. A License Change Request will *be implemented to revise Technical Specifications in accordance with the second level UV relay setpoint concern. The UFSAR will be reviewed*and revised as appropriate. | | UV setpoint *. With the current interim controls, the health and safety of the public is not affected by this event. Upon completion of this evaluation this LER will be supplemented~ |
| Administrative controls are being implemented to ensure the following restrictions are employed as interim action until implementation of design changes: 1. 4.i6KV vital bus voltages will be logged hourly to assure a minimum vital bus voltage of 4.3KV. Bus voltages less than 4.3KV will be adjusted to between 4.3KV and 4.SKV. ' 2. '_.,;..:'. | | * CORRECTIVE ACTION: |
| -Only two vital buses may be energized from their operating . , .. transformer if both the-corresponding buses are on -their respective APT. 3a. Three.vital buses may be energized from the operatingtransf armer if one of the corresponding group *** *
| | Design Changes will be implemented to change the relay setpoint on both Units to meet the requirements of BTP-PSB-1 and be in accordance with the plant design basis. This will be done during the upcoming Unit 1 refueling outage and the next Unit 2 refueling outage. |
| * buses is transferred to the operating SPT or LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station Unit 1 CORRECTIVE ACTION: (cont'd) DOCKET NUMBER 5000272 LER NUMBER 93-014-00 PAGE 5 Of 5 3b. Three vital buses may be energized from the operating transformer if the load which can be transferred from the APTs is reduced by 5 mega volt amps. MJPJ:pc SORC Mtg. 93-077 General Manager -Salem Operations | | A License Change Request will *be implemented to revise Technical Specifications in accordance with the second level UV relay setpoint concern. |
| ' . . . ' ,. | | The UFSAR will be reviewed*and revised as appropriate. |
| '.:,'F '-. . .; . . .,:_*' . | | Administrative controls are being implemented to ensure the following restrictions are employed as interim action until implementation of design changes: |
| I}} | | : 1. 4.i6KV vital bus voltages will be logged hourly to assure a ' *~. |
| | minimum vital bus voltage of 4.3KV. Bus voltages less than 4.3KV will be adjusted to between 4.3KV and 4.SKV. |
| | : 2. Only two vital buses may be energized from their operating .,. |
| | transformer if both the-corresponding gro~p buses are on - |
| | their respective APT. |
| | 3a. Three.vital buses may be energized from the operatingtransf armer if one of the corresponding group ** * |
| | * buses is transferred to the operating SPT or |
| | |
| | LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 1 5000272 93-014-00 5 Of 5 CORRECTIVE ACTION: (cont'd) 3b. Three vital buses may be energized from the operating transformer if the load which can be transferred from the APTs is reduced by 5 mega volt amps. |
| | General Manager - |
| | Salem Operations MJPJ:pc SORC Mtg. 93-077 |
| | ' . . '~ |
| | -----*~:.,_;_~I |
| | -~_C: |
| | .; . ;(.~ |
| | '.:,'F |
| | _._-------~"?' I}} |
Similar Documents at Salem |
---|
Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0081998-12-24024 December 1998 LER 97-001-01:on 970215,failure to Perform TS Surveillance of Component Cooling Water Sys Check Valves Occurred.Caused by Inadequate Communication Between EOP Group & IST Reviewers.Procedure Revised.With 981224 Ltr ML18106B0021998-12-17017 December 1998 LER 98-015-01:on 980924,improper Installation of Test Equipment to RPS Occurred.Caused by Inadequate 10CFR50.59 Applicability Reviews During Past Revs.Revised Procedures. with 981217 Ltr ML18106A9551998-11-0303 November 1998 LER 96-013-01:on 960711,concluded That Current Gain & Bias Settings Had Rendered Overtemperature Delta Temp Protection Channels Inoperable.Caused by Scaling Error.Licensee Will Revise Scaling Calculations.With 981105 Ltr ML18106A9451998-10-30030 October 1998 LER 97-004-01:on 970408,failure to Comply with TS Action Statement,Dg Start & Inadequate Surveillance Testing,Was Noted.Caused by Inadequate Tracking of Inoperable Equipment. Discussed Event & Lessons Learned.With 981022 Ltr ML18106A9491998-10-22022 October 1998 LER 98-015-00:on 980924,identified Improper Installation of Test Equipment to Rps.Cause Indeterminate.Procedures for Installation of Test Equipment for Collection of State Point Data Were Placed on Administrative Hold.With 981022 Ltr ML18106A9301998-10-21021 October 1998 LER 98-014-00:on 980725,noted Improper Calibr of Liquid Radwaste Effluent Line Radiation Monitor.Caused by Inattention to Detail by Maint Personnel.Channel Calibr Was Successfully Performed on 1R18 on 980821.With 981019 Ltr ML18106A9071998-10-0101 October 1998 LER 98-014-00:on 980918,discovered That Fire Barrier Matl for HVAC Ducts Does Not Meet Required Level of Fire Resistance.Cause Indeterminate.Established Appropriate Compensatory Actions for Fire Barriers.With 981001 Ltr ML18106A8951998-09-28028 September 1998 LER 98-012-01:on 980725,noted That Afs Was Operated with Less than Required Number of Operable AFW Pumps.Caused by Improper Procedure Implementation.Runout Protection Pressure Device for 22 AFW Pumps Was Returned to Svc.With 980928 Ltr ML18106A8821998-09-21021 September 1998 LER 98-013-00:on 980820,noted Surveillance of Containment Penetration Overcurrent Protection Devices Missed.Caused by Human Error.Satisfactorily Tested Apprpriate Breakers & Disciplined Involved Personnel.With 980921 Ltr ML18106A8791998-09-16016 September 1998 LER 96-006-01:on 960717,determined That non-radioactive Liquid Basin Radwaste Monitor Inoperable During Low Head Conditions.Caused by Inadequate Design Change Package.Design Change 1EC3663-01 Has Been Installed.With 980916 Ltr ML18106A8801998-09-0808 September 1998 LER 98-013-00:on 980806,operation with TS Required Equipment OOS Was Noted.Caused by Human Error.Reviewed Processes & Practices Re Safety Sys Status Control,Procedure Rev & Extra Training.With 980908 Ltr ML18106A8531998-08-27027 August 1998 LER 98-007-00:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Cause of Event Has Not Yet Been Determined.Assembled Root Cause Team & Replaced Affected tubing.W/980827 Ltr ML18106A8521998-08-27027 August 1998 LER 98-011-00:on 980803,ESFA During a 4KV Automatic Transfer Test Was Noted.Caused by Premature Release of Control Console Pushbutton Due to Inadequate Procedural Step.Revised procedure.W/980827 Ltr ML18106A8421998-08-24024 August 1998 LER 98-012-00:on 980725,discovered That Plant Had Operated in Modes 1 & 2 w/twenty-two AFW Pumps Inoperable.Caused by Failure to Restore Pump Runout Protection Pressure Device to Svc.Returned Subject Device to svc.W/980824 Ltr ML18106A8431998-08-24024 August 1998 LER 98-009-00:on 980810,failure to Post Continuous Firewatch as Required by Fire Protection Plan Noted.Caused by Failure to Recognize Concurrent Conditions.Continuous Firewatch Was Posted Immediately & Repaired Smoke detectors.W/980824 Ltr ML18106A8141998-08-13013 August 1998 LER 98-010-00:on 980714,determined That Leakage from Boron Injection Tank Exceeded Max Allowable ECCS Leakage from Sources Outside Containment.Caused by Leaking 2SJ404 Manual Sample valve.2SJ404 Valve repaired.W/980813 Ltr ML18106A8201998-08-13013 August 1998 LER 98-012-00:on 980715,potential to Exceed Rating of Piping Due to Isolation of Overpressure Protection Line Was Noted. Caused by Inadequate Procedural Guidance.Appropriate Operations Dept Procedures Have Been revised.W/980813 Ltr ML18106A6931998-06-29029 June 1998 LER 98-003-00:on 980122,inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2 Sg,Was Performed.Caused by Failure of Qualification,Verification & Validation Process. Tubes Reviewed to Verify No Others Inappropriately Plugged ML18106A6471998-06-0404 June 1998 LER 98-011-00:on 980505,improper Isolation of Single Cell Battery Charger from 125 Vdc Battery Was Noted.Caused by Inadequate 10CFR50.59 Applicability Review.Placed Procedure SC.MD-CM.ZZ-0024(Q) on Administrative hold.W/980604 Ltr ML18106A6421998-06-0101 June 1998 LER 98-010-00:on 931019,reactor Pressure Vessel Insp Plugs Were Out of Configuration,Was Noted.Caused by Personnel Error.Proper Configuration Was Restored Shortly After Discovery Prior to Entering Mode 2.W/980601 Ltr ML18106A6431998-05-29029 May 1998 LER 98-006-01:on 980227,determined Incorrect Scaling Error of First Stage Pressure Transmitter Existed.Caused by Human Error.Revised Setpoint Calculation SC-MS002-01 & Revised Associated Instrument Calibr Database info.W/980529 Ltr ML18106A6141998-05-18018 May 1998 LER 98-008-00:on 970814,failure to Test 21 & 22 AF 40 Valves in Closed Direction as Required by TS 4.0.5 Was Noted.Caused by Inadequate Design Mod Process.Motor Driven 21/22 AF 40 Valves Were Tested IAW Revised procedure.W/980518 Ltr ML18106A5901998-05-0101 May 1998 LER 98-009-00:on 980405,epoxy Missing from Terminals of H Analyzer Was Noted.Caused by Inadequate Development of Procedure.H Analyzers Were Repaired & Review of Other Safety Related Equipment in Containment Was performed.W/980501 Ltr ML18106A5611998-04-20020 April 1998 LER 98-008-00:on 980323,inadequate Testing of Salem Unit 1 Containment Air Locks Resulted in Entering TS 3.0.3.Caused by less-than-adequate Work Practices During Replacement of Equalizing Valve.Salem Unit 2 Airlocks Were Inspected ML18106A6061998-04-0101 April 1998 Corrected LER 98-004-00:on 980302,failure to Comply W/Tss 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Have Been Taken to Correctly Document Safety Factors.Corrects Prior Similar Occurrences ML18106A4451998-04-0101 April 1998 LER 98-004-00:on 980302,failure to Perform TS 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Were Taken to Correctly Document Safety factors.W/980401 Ltr ML18106A4351998-03-30030 March 1998 LER 98-006-00:on 980227,incorrect Scaling of First Stage Turbine Impulse Pressure Transmitters Noted.Cause Indeterminate.Implemented Procedure Changes & re-scaled Affected Turbine Impulse Pressure transmitters.W/980330 Ltr ML18106A3961998-03-20020 March 1998 LER 98-005-00:on 980219,inoperability of Twelve EDG Fuel Oil Transfer Pump (FOTP) Noted.Caused by Installation of Incorrect Control Switch.Installed Correct off-auto-manual Switch & Verified Operability of Twelve FOTP.W/980320 Ltr ML18106A5781998-03-20020 March 1998 Corrected LER 98-005-00:on 980219,inoperability of 12 Fuel Oil Transfer Pump (Fotp),Noted.Caused by Installation of Incorrect Control Switch.Field Insp Performed to Verify Configuration of Switches for 11,21 & 22 FOTPs ML18106A4021998-03-20020 March 1998 LER 98-007-00:on 980218,failure to Establish Containment Integrity (Closure) Prior to Fuel Movement Was Noted.Caused by Failure to Identify & Include Condensate Pot Vent in Appropriate Valve Lineup.Valves identified.W/980320 Ltr ML18106A4031998-03-20020 March 1998 LER 98-006-00:on 980221,ESF Actuation of 11 & 12 Auxiliary Feedwater Pumps Occurred.Caused by Human Error.Operators Promptly Established Feedwater to All SG & Restored Proper Water levels.W/980320 Ltr 1999-08-26
[Table view] Category:RO)
MONTHYEARML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0081998-12-24024 December 1998 LER 97-001-01:on 970215,failure to Perform TS Surveillance of Component Cooling Water Sys Check Valves Occurred.Caused by Inadequate Communication Between EOP Group & IST Reviewers.Procedure Revised.With 981224 Ltr ML18106B0021998-12-17017 December 1998 LER 98-015-01:on 980924,improper Installation of Test Equipment to RPS Occurred.Caused by Inadequate 10CFR50.59 Applicability Reviews During Past Revs.Revised Procedures. with 981217 Ltr ML18106A9551998-11-0303 November 1998 LER 96-013-01:on 960711,concluded That Current Gain & Bias Settings Had Rendered Overtemperature Delta Temp Protection Channels Inoperable.Caused by Scaling Error.Licensee Will Revise Scaling Calculations.With 981105 Ltr ML18106A9451998-10-30030 October 1998 LER 97-004-01:on 970408,failure to Comply with TS Action Statement,Dg Start & Inadequate Surveillance Testing,Was Noted.Caused by Inadequate Tracking of Inoperable Equipment. Discussed Event & Lessons Learned.With 981022 Ltr ML18106A9491998-10-22022 October 1998 LER 98-015-00:on 980924,identified Improper Installation of Test Equipment to Rps.Cause Indeterminate.Procedures for Installation of Test Equipment for Collection of State Point Data Were Placed on Administrative Hold.With 981022 Ltr ML18106A9301998-10-21021 October 1998 LER 98-014-00:on 980725,noted Improper Calibr of Liquid Radwaste Effluent Line Radiation Monitor.Caused by Inattention to Detail by Maint Personnel.Channel Calibr Was Successfully Performed on 1R18 on 980821.With 981019 Ltr ML18106A9071998-10-0101 October 1998 LER 98-014-00:on 980918,discovered That Fire Barrier Matl for HVAC Ducts Does Not Meet Required Level of Fire Resistance.Cause Indeterminate.Established Appropriate Compensatory Actions for Fire Barriers.With 981001 Ltr ML18106A8951998-09-28028 September 1998 LER 98-012-01:on 980725,noted That Afs Was Operated with Less than Required Number of Operable AFW Pumps.Caused by Improper Procedure Implementation.Runout Protection Pressure Device for 22 AFW Pumps Was Returned to Svc.With 980928 Ltr ML18106A8821998-09-21021 September 1998 LER 98-013-00:on 980820,noted Surveillance of Containment Penetration Overcurrent Protection Devices Missed.Caused by Human Error.Satisfactorily Tested Apprpriate Breakers & Disciplined Involved Personnel.With 980921 Ltr ML18106A8791998-09-16016 September 1998 LER 96-006-01:on 960717,determined That non-radioactive Liquid Basin Radwaste Monitor Inoperable During Low Head Conditions.Caused by Inadequate Design Change Package.Design Change 1EC3663-01 Has Been Installed.With 980916 Ltr ML18106A8801998-09-0808 September 1998 LER 98-013-00:on 980806,operation with TS Required Equipment OOS Was Noted.Caused by Human Error.Reviewed Processes & Practices Re Safety Sys Status Control,Procedure Rev & Extra Training.With 980908 Ltr ML18106A8531998-08-27027 August 1998 LER 98-007-00:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Cause of Event Has Not Yet Been Determined.Assembled Root Cause Team & Replaced Affected tubing.W/980827 Ltr ML18106A8521998-08-27027 August 1998 LER 98-011-00:on 980803,ESFA During a 4KV Automatic Transfer Test Was Noted.Caused by Premature Release of Control Console Pushbutton Due to Inadequate Procedural Step.Revised procedure.W/980827 Ltr ML18106A8421998-08-24024 August 1998 LER 98-012-00:on 980725,discovered That Plant Had Operated in Modes 1 & 2 w/twenty-two AFW Pumps Inoperable.Caused by Failure to Restore Pump Runout Protection Pressure Device to Svc.Returned Subject Device to svc.W/980824 Ltr ML18106A8431998-08-24024 August 1998 LER 98-009-00:on 980810,failure to Post Continuous Firewatch as Required by Fire Protection Plan Noted.Caused by Failure to Recognize Concurrent Conditions.Continuous Firewatch Was Posted Immediately & Repaired Smoke detectors.W/980824 Ltr ML18106A8141998-08-13013 August 1998 LER 98-010-00:on 980714,determined That Leakage from Boron Injection Tank Exceeded Max Allowable ECCS Leakage from Sources Outside Containment.Caused by Leaking 2SJ404 Manual Sample valve.2SJ404 Valve repaired.W/980813 Ltr ML18106A8201998-08-13013 August 1998 LER 98-012-00:on 980715,potential to Exceed Rating of Piping Due to Isolation of Overpressure Protection Line Was Noted. Caused by Inadequate Procedural Guidance.Appropriate Operations Dept Procedures Have Been revised.W/980813 Ltr ML18106A6931998-06-29029 June 1998 LER 98-003-00:on 980122,inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2 Sg,Was Performed.Caused by Failure of Qualification,Verification & Validation Process. Tubes Reviewed to Verify No Others Inappropriately Plugged ML18106A6471998-06-0404 June 1998 LER 98-011-00:on 980505,improper Isolation of Single Cell Battery Charger from 125 Vdc Battery Was Noted.Caused by Inadequate 10CFR50.59 Applicability Review.Placed Procedure SC.MD-CM.ZZ-0024(Q) on Administrative hold.W/980604 Ltr ML18106A6421998-06-0101 June 1998 LER 98-010-00:on 931019,reactor Pressure Vessel Insp Plugs Were Out of Configuration,Was Noted.Caused by Personnel Error.Proper Configuration Was Restored Shortly After Discovery Prior to Entering Mode 2.W/980601 Ltr ML18106A6431998-05-29029 May 1998 LER 98-006-01:on 980227,determined Incorrect Scaling Error of First Stage Pressure Transmitter Existed.Caused by Human Error.Revised Setpoint Calculation SC-MS002-01 & Revised Associated Instrument Calibr Database info.W/980529 Ltr ML18106A6141998-05-18018 May 1998 LER 98-008-00:on 970814,failure to Test 21 & 22 AF 40 Valves in Closed Direction as Required by TS 4.0.5 Was Noted.Caused by Inadequate Design Mod Process.Motor Driven 21/22 AF 40 Valves Were Tested IAW Revised procedure.W/980518 Ltr ML18106A5901998-05-0101 May 1998 LER 98-009-00:on 980405,epoxy Missing from Terminals of H Analyzer Was Noted.Caused by Inadequate Development of Procedure.H Analyzers Were Repaired & Review of Other Safety Related Equipment in Containment Was performed.W/980501 Ltr ML18106A5611998-04-20020 April 1998 LER 98-008-00:on 980323,inadequate Testing of Salem Unit 1 Containment Air Locks Resulted in Entering TS 3.0.3.Caused by less-than-adequate Work Practices During Replacement of Equalizing Valve.Salem Unit 2 Airlocks Were Inspected ML18106A6061998-04-0101 April 1998 Corrected LER 98-004-00:on 980302,failure to Comply W/Tss 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Have Been Taken to Correctly Document Safety Factors.Corrects Prior Similar Occurrences ML18106A4451998-04-0101 April 1998 LER 98-004-00:on 980302,failure to Perform TS 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Were Taken to Correctly Document Safety factors.W/980401 Ltr ML18106A4351998-03-30030 March 1998 LER 98-006-00:on 980227,incorrect Scaling of First Stage Turbine Impulse Pressure Transmitters Noted.Cause Indeterminate.Implemented Procedure Changes & re-scaled Affected Turbine Impulse Pressure transmitters.W/980330 Ltr ML18106A3961998-03-20020 March 1998 LER 98-005-00:on 980219,inoperability of Twelve EDG Fuel Oil Transfer Pump (FOTP) Noted.Caused by Installation of Incorrect Control Switch.Installed Correct off-auto-manual Switch & Verified Operability of Twelve FOTP.W/980320 Ltr ML18106A5781998-03-20020 March 1998 Corrected LER 98-005-00:on 980219,inoperability of 12 Fuel Oil Transfer Pump (Fotp),Noted.Caused by Installation of Incorrect Control Switch.Field Insp Performed to Verify Configuration of Switches for 11,21 & 22 FOTPs ML18106A4021998-03-20020 March 1998 LER 98-007-00:on 980218,failure to Establish Containment Integrity (Closure) Prior to Fuel Movement Was Noted.Caused by Failure to Identify & Include Condensate Pot Vent in Appropriate Valve Lineup.Valves identified.W/980320 Ltr ML18106A4031998-03-20020 March 1998 LER 98-006-00:on 980221,ESF Actuation of 11 & 12 Auxiliary Feedwater Pumps Occurred.Caused by Human Error.Operators Promptly Established Feedwater to All SG & Restored Proper Water levels.W/980320 Ltr 1999-08-26
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML18107A5581999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 2.With 991014 Ltr ML18107A5571999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 1.With 991014 Ltr ML18107A5301999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 2.With 990913 Ltr ML18107A5311999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 1.With 990913 ML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A5201999-08-12012 August 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#9) Second Interval,Second Period, First Outage (96RF). ML18107A4811999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 1.With 990813 Ltr ML18107A4821999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 2.With 990813 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A5211999-07-0101 July 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#10) Second Interval,Second Period,Second Outage (99RF). ML18107A4351999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 1.With 990713 Ltr ML18107A4341999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 2.With 990713 Ltr ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3441999-06-0101 June 1999 Interim Part 21 Rept Re Premature Over Voltage Protection Actuation in Circuit Specific Application in Dc Power Supply.Testing & Evaluation Activities Will Be Completed on 990716 ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A3681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 1.With 990611 Ltr ML18107A3721999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 2.With 990611 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A3711999-04-30030 April 1999 Corrected Monthly Operating Rept for Apr 1999 for Salem Generating Station,Unit 1 ML18107A3151999-04-30030 April 1999 Submittal-Only Screening Review of Salem Generating Station Individual Plant Exam for External Events (Seismic Portion), Rev 1 ML18107A2991999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 1.With 990514 Ltr ML18107A2971999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 2.With 990514 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18107A2881999-04-0707 April 1999 Rev 0 to NFS-0174, COLR for Salem Unit 2 Cycle 11. ML18107A1821999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 1.With 990414 Ltr ML18107A1831999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 2.With 990414 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B1021999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 2.With 990315 Ltr ML18106B1011999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 1.With 990315 Ltr ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0561999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 2.With 990212 Ltr ML18106B0571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 1.With 990212 Ltr ML20205P1671999-01-31031 January 1999 a POST-PLUME Phase, Federal Participation Exercise ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0251998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 2.With 990115 Ltr 1999-09-30
[Table view] |
Text
Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038 Salem Generating Station August 20, 1993 U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555
Dear Sir:
SALEM GENERATING STATION LICENSE NO. DPR-70 DOCKET NO. 50-272 UNIT NO. 1 LICENSEE EVENT REPORT 93-014-00 This Licensee Event Report is being submitted pursuant to the requirements of the Code of Federal Regulations 10CFR 50.73(a) (2) (ii) (B). This report is required to be issued within thirty (30) days of event discovery.
Sincerely yours, C. A Vondra General Manager -
Salem Operations MJPJ:pc Distribution
. . )~ -. 0 Ii'-* r--Ju'*~ :
The EnerQY People 9308300321 930820 95-2189 ( 10M) 12-89 PDR ADOC~ 05000272 S PDR
NRC F0RM 366 U.S. NUCLEAR REGULATORY COMMISSION (6-89) APPROVED OMB NO. 3150-0104 EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD LICENSEE EVENT REPORT (LERI COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH IP-530). U.S. NUCLEAR REGULATORY COMMISSION. WASHINGTON. DC 20555. AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104). OFFICE OF MANAGEMENT AND BUDGET. WASHINGTON. DC 20503.
FACILITY NAME 11) DOCKET NUMBER 12) I PAGE 13}
Salem TITLE 141 Generatin~ Station - Unit 1 I01s101010121712 1joFOl5 4KV Vital Bus Second Level Undervoltage Protection Dropout Setpoint Concern (both Units).
EVENT OATE (5) LER NUMBER (6) REPORT DATE 17) OTHER FACILITIES INVOLVED IB)
MONTH DAY YEAR YEAR rt SE~~~~~~AL j( ~~~~~~ MONTH DAY YEAR FACILITY NAMES OOCKET NUMBERISl Salem Unit 2 o 1s1 o Io Io 13 1111 o I1 I 2 2 9 3 9 I3 - a I 1 .14 - a Io oIs 21 a 9 I3 OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE Rl:QUIREMENTS OF 10 CFR §: (Ch*ck on* or mor* of th* following) 111)
MODE 19)
I
L-=-i~ 20.402lb) 1 20.4061*111 Hil -
20.405lcl 50.3Slcll1)
IX 50.731*)12Hiv) 50.73l*H2llvl 73.71lb) 73.71lc)
POWER L~~~L 0 18 I 0 .....__ 20.4051aH1lliil ..__ 50.38(cll2) 50.731*1121 Mil ....__ OTHER (SP1Jcify in Abst,.ct b*low *nd in TDxt. NRC Form 20.40tilall1 Hiiil 50.731*ll2)(i) 50.73l*ll2HvlllHAI 366AJ 20.4061*>11 )(Iv) 20.4061*)11 )lvl -x 60.73l*ll2llii) 50.73l*ll2lliiil -
LICENSEE CONTACT FOR THIS LER 112) 50.73lall2HvlllHBI 50.73lall2Hxl NAME TELEPHONE NUMBER AREA CODE M. J. Pastva. Jr. - LER Coordinator b 1019* 313*19 1-1511 1615 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT 113)
CAUSE SYSTEM COMPONENT I I I I I I I I I I I I I I I I I I I I I I I I I I I I SUPPLEMENTAL REPORT EXPECTED 114) MONTH DAY YEAR EXPECTED SUBMISSION r:-i YES (If y*s, com~lot* EXPECTED SUBMISSION DATE)
DATE (151
- 110 ?1'1 ql':l ABSTRACT (Limit to 1400 spaces, i.e .* approKimtJtely fifteen single-space typewritten lines) (16)
On 7/22/93, it was determined that the present 91.6% dropout setpoint for second level undervoltage (UV) protection of the 4 kilovolt (KV) vital buses (both Salem Units), may not fully protect motors should the bus voltage degrade to less than 93.2% but greater than 91.6%. This is contrary to Branch Technical Position (BTP)-PSB-1 and the Updated Final Safety Analysis Report (UFSAR). However, engineering calculation shows, given the postulated worst case design basis event, vital bus recovery voltage will not degrade to less than 93.2%. The 91.6% dropout setpoint
_was based on the lowest voltage the 4.16 KV motors could be allowed to operate (i.e. 90%) due to voltage drops in the *motors' cables and relay inaccuracy considerations. The revised recovery voltage of 93.2% will now maintain all motors operable under degraded voltage conditions.
During the next refueling outage on each Unit, design changes will be implemented to change the relay setpoint to meet the requirements of BTP-PSB-1. In the interim, administrative controls are being implemented. Technical Specifications and the UFSAR will be reviewed and revised as appropriate. Conditions necessary for the design concern coincident with a prerequisite plant transient have not occurred. As such, the health and safety of the public has not been affected by this concern. Analysis of this event is continuing. Upon completion of this effort, a supplement to this LER will be submitted.
NRC Form 366 (6-89)
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 1 5000272 93-014-00
- 2 of 5 PLANT AND SYSTEM IDENTIFICATION:
Westinghouse - Pressurized Water Reactor Energy Industry Identification System (EIIS) codes are identified in the text as {xx}
IDENTIFICATION OF OCCURRENCE:
4 KV Vital Bus Second Level Undervoltage Protection Dropout Setpoint Concern (both Salem Units)
Event Discovery Date: 7/22/93 Report Date: 8/20/93 This report was initiated by Incident Report No.93-320. This event is reportable per 10CFR50.73(a) (2) (ii) (B) and 10CFR50.73(a) (2) (v) (D).
CONDITIONS PRIOR TO OCCURRENCE:
Unit 1: Mode 1 Reactor Power 80% - Unit Load 815 MWe Unit 2: Mode 1 Reactor Power 100% - Unit Load 1140 MWe DESCRIPTION OF OCCURRENCE:
On July 22, 1993, it was determined.that the *present 91.6% dropout setpoint for second level undervoltage (UV) protection of the 4 kilovolt (KV) vital buses {VJ} (both Salem Units), will not fully protect motors at the 230 and 460 volt level should the 4KV bus voltage degrade to less than 93.2% but greater than 91.6%. This is contrary to Branch Technical Position (BTP)-PSB-1 and the Updated
- .Final Safety Analysis Report (UFSAR). However, engineering calculation shows, given*the postulated worst case design basis event, vital bus recovery voltage will not degrade to less than 93.2%.
The Nuclear Regulatory Commission was notified of this event per Code of Federal Regulations 10CFR50.72(b) (1) (ii) (B).
ANALYSIS OF OCCURRENCE:
r :****
Availability of minimum redundant alternating current (A.C.) power sources and distribution systems ensures sufficient power will be available to safety-related equipment for safe shutdown of the facility and the mitigation and control of accident conditions.within the facility, as required by General Design Criteria 17 of Appendix "A" to 10CFR Part 50. Per BTP-PSB-1, the plant licensing basis requires a second level of undervoltage protection for 4KV vital buses to ensure minimum motor terminal voltage for all safety-related
- , *---*-.,. -*---* --~..-- --*- -- -*---* ****-----*~*.
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 1 5000272 93-014-00 3 of 5 ANALYSIS OF OCCURRENCE: (cont'd) motors *. At Salem, when vital bus voltage drops below the dropout setpoint for relays providing this protection for greater than 13 seconds, vital bus loads are automatically transferred to their respective emergency diesel generators.
As part of the self-initiated Electrical Engineering Self-Assessment Program, electrical calculations are being reviewed to ensure guidelines of BTP-PSB-1 are met. On July 1, 1993, review of Revision 1 of ES-15.00S(Q), "Salem Units 1 and 2 Degraded Grid study" identified a potential concern with the 91.6% dropout setpoint of the Units' 4KV vital buses (lA, lB, lC, 2A, 2B, and 2C). On July 22, 1993, further analysis of this concern determined the recovery vital bus voltage is 93.2% of 4.16KV following transfer of the Auxiliary Power Transformers (APTs) to the Station Power Transformers (SPTs). This voltage could result should a group bus transfer to the SPTs occur coincident with a Loss-of-Coolant Accident (LOCA) and the unaffected unit in startup or shutdown.
UFSAR Section 8.3.1.2 describes the setpoint as being determined using the 90% minimum.motor terminal voltage as the starting point.
Since 93.2% bus voltage is required to ensure the minimum motor terminal voltage, the existing 91.6% dropout setpoint is not in compliance with the UFSAR or the BTP. However, because ES-15.00S(Q) calculations also show that vital bus recovery voltage will not
- degrade to a level at which actual motor degradation could occur, the intent of the UFSAR and BTP is still met. These calculations take credit for operation, prior to the event, of the load tap changers which are set to* maintain a_ minimum initial bus voltage of 4.3KV.
Following event discovery, an evaluation to justify continued operation of both Salem Units, concluded the present dropout setpoint of the relays does not meet the intent of the BTP. However, Revision 1 of Engineering Calculation ES-15.00S(Q) determined there is not a significant safety concern with the present dropout setpoint provided the 4.16KV vital buses are maintained at 4.3KV or greater. Design changes will be implemented during the next refueling outage on each Unit to change the dropout setpoint to meet the intent of the BTP. * * * * *
- For the interim, 4.16KV vital bus voltages are being monitored to assure load tap changers are operating properly to maintain a minimum bus voltage of 4. 3KV. In addition, bus voltages below 4. JKV will be. *r:'::*
adjusted between 4.JKV and 4.5KV and restrictions concerning vital bus lineup will be in_effect (see "CORRECTIVE ACTIONS:" section).
Analysis of this event is continuing. Included will be a historical assessment of the effect of the revised assumptions at vital bus levels below 4KV. Upon completion of this effort, a supplement to this LER will be submitted.
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating station DOCKET NUMBER LER NUMBER PAGE tinit 1 .- - 5000272' 93:...014-00 4 of s APPARENT CAUSE OF OCCURRENCE:
The cause of this event is "Design, Manufacturing, Construction/Installation", per NUREG-1022. The 91.6% dropout setpoint was based on the lowest voltage the 4.16 KV motors could be allowed to operate (i.e. 90%) due to voltage drops in the motors' cables and relay inaccuracy considerations. The revised dropout setpoint, based upon the revised recovery voltage of 93.2%, will now maintain all motors operable under degraded voltage conditions.
PRIOR SIMILAR OCCURRENCES:
No prior. similar.occurrences of this event were identified.
SAFETY SIGNIFICANCE:
Engineering is. currently completing its evaluation of the safety significance of past operation with the non-conservative second level.
UV setpoint *. With the current interim controls, the health and safety of the public is not affected by this event. Upon completion of this evaluation this LER will be supplemented~
Design Changes will be implemented to change the relay setpoint on both Units to meet the requirements of BTP-PSB-1 and be in accordance with the plant design basis. This will be done during the upcoming Unit 1 refueling outage and the next Unit 2 refueling outage.
A License Change Request will *be implemented to revise Technical Specifications in accordance with the second level UV relay setpoint concern.
The UFSAR will be reviewed*and revised as appropriate.
Administrative controls are being implemented to ensure the following restrictions are employed as interim action until implementation of design changes:
- 1. 4.i6KV vital bus voltages will be logged hourly to assure a ' *~.
minimum vital bus voltage of 4.3KV. Bus voltages less than 4.3KV will be adjusted to between 4.3KV and 4.SKV.
- 2. Only two vital buses may be energized from their operating .,.
transformer if both the-corresponding gro~p buses are on -
their respective APT.
3a. Three.vital buses may be energized from the operatingtransf armer if one of the corresponding group ** *
- buses is transferred to the operating SPT or
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 1 5000272 93-014-00 5 Of 5 CORRECTIVE ACTION: (cont'd) 3b. Three vital buses may be energized from the operating transformer if the load which can be transferred from the APTs is reduced by 5 mega volt amps.
General Manager -
Salem Operations MJPJ:pc SORC Mtg.93-077
' . . '~
*~:.,_;_~I
-~_C:
.; . ;(.~
'.:,'F
_._-------~"?' I