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| issue date = 07/19/1993
| issue date = 07/19/1993
| title = LER 93-009-00:on 930629,automatic Start of Motor Driven Auxiliary Feedwater Pumps Occurred Due to Mgt/Qa Deficiency. Troubleshooting Procedures developed.W/930719 Ltr
| title = LER 93-009-00:on 930629,automatic Start of Motor Driven Auxiliary Feedwater Pumps Occurred Due to Mgt/Qa Deficiency. Troubleshooting Procedures developed.W/930719 Ltr
| author name = POLLACK M J, VONDRA C A
| author name = Pollack M, Vondra C
| author affiliation = PUBLIC SERVICE ELECTRIC & GAS CO. OF NEW JERSEY
| author affiliation = PUBLIC SERVICE ELECTRIC & GAS CO. OF NEW JERSEY
| addressee name =  
| addressee name =  
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=Text=
=Text=
{{#Wiki_filter:. e Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038 Salem Generating Station u. s. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555  
{{#Wiki_filter:. e OPS~G Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038 Salem Generating Station July 19, 1993
: u. s.     Nuclear Regulatory Commission Document Control Desk Washington, DC               20555


==Dear Sir:==
==Dear Sir:==
SALEM GENERATING STATION LICENSE NO. DPR-75 DOCKET NO. 50-311 UNIT NO. 2 LICENSEE EVENT REPORT 93-009-00 July 19, 1993 This Licensee Event Report is being submitted pursuant to the requirements of the Code of Federal Regulations 10CFR 50.73(a) (2) (iv). This report is required to be issued within thirty (30) days of event discovery.
 
MP:pc Distribution 9307280092 930719 ADDCK 05000311 PDR The power is in your hanas. Sincerely yours, c. A Vondra General Manager -Salem Operations 95-2189 REV 7-92 NRC FORM366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED OMB NO. 3150-0104
SALEM GENERATING STATION LICENSE NO. DPR-75 DOCKET NO. 50-311 UNIT NO. 2 LICENSEE EVENT REPORT 93-009-00 This Licensee Event Report is being submitted pursuant to the requirements of the Code of Federal Regulations 10CFR 50.73(a) (2) (iv).           This report is required to be issued within thirty (30) days of event discovery.
* (6-89) LICENSEE EVENT REPORT (LER) FACILITY NAME 11> Salem Generating Station -Unit 2 TITLE (4) EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (P-530)0 U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON.
Sincerely yours,
DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET. WASHINGTON, DC 20503. !DOCKET NUMBER (2) I PAGE (3) o 1 s Io Io Io I 31 i 1i I 1 loFI 016 ESF Actuation:
: c. A Vondra General Manager -
Automatic Start of Motor Driven Auxiliary Feedwater Pumps. EVENT DATE (5) LER NUMBER (61 REPORT DATE (71 OTHER FACILITIES INVOLVED (Bl MONTH DAY YEAR YEAR JJ:
Salem Operations MP:pc Distribution 9307280092 930719
tt MONTH DAY YEAR FACILITY NAMES DO<;:KET NUMBER(SI o 1 6 2 I 2 9 1 3 9l3-olol9 ol o o I 1 1 119 OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE RkoQUIREMENTS DF 10 CFR &sect;: (Chock ono or moro of th* following)
~DR ADDCK 05000311 PDR The power is in your hanas.
(11) 50.73(*ll2lM
95-2189 REV 7-92
...__ ...__ 50.73(*ll2lMil 50.73(*ll2)1viiil(A)
 
-50.73(*1(2l(vlill(BI
NRC FORM366                                                                       U.S. NUCLEAR REGULATORY COMMISSION
-50.731*H2ll*I MODE (9) 3 t-----.--....&...:.-+---1 20.402(bl 20.405(c) 50.73(*ll2llivl POWER I 0 I 0 10 -
*   (6-89)                                                                                                                                         APPROVED OMB NO. 3150-0104 EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD LICENSEE EVENT REPORT (LER)                                                            COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (P-530) 0 U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON. DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET. WASHINGTON, DC 20503.
.........  
FACILITY NAME      11>                                                                                                                    DOCKET NUMBER (2)                   I       PAGE (3)
""'"' ...... --1 20.405(*1!111iil 111!4ll= :::::::::
Salem Generating Station - Unit 2 TITLE (4)
20.405(*111 llil LICENSEE CONTACT FOR THIS LER (12) NAME M. J. Pollack -LER Coordinator AREA CODE ---73.71(b) 73.71(c) OTHER ($pacify in Abstract below end in NRC Form 366Ai TELEPHONE NUMBER COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13) CAUSE SYSTEM COMPONENT I I I I I I I I TURER I I I I I I SUPPLEMENTAL REPORT EXPECTED (141 I YES (If Y61, compl*t* EXPECTED SUBMISSION DATE) ABSTRACT (Limit to 1400 spact1s, i.e .* approximately fifttJtJn sing/tJ-spactJ typt1writtt1n lines} 116) SYSTEM COMPONENT I 1* I I I I I I MANUFAC-TUR ER I I I I I I -MONTH DAY YEAR . EXPECTED SUBMISSION DATE 1151 I I I On June 22, 1993, at 0326 hours, 21 and 22 motor driven Auxiliary Feedwater (MDAFW) Pumps automatically started due to 21 and 22 Steam Generator Feed Pumps (SGFPs) tripping on low suction pressure (an Engineered Safety Feature).
                                                                                                                                            !o 1s Io Io Io I 31 i 1i I               1 loFI   016 ESF Actuation: Automatic Start of Motor Driven Auxiliary Feedwater Pumps.
Both SGFPs had been running in support of Condensate System cleanup. At the time, Condensate Polishing System 24 demineralizer (DM) vessel was being restored to service. The SGFPs tripped during the tagging release of the 24 DM vessel. Investigation revealed that the reduced SGFP suction pressure was a direct result of a pressure transient induced during the 24 DM vessel tagging release. The root cause of this event is "Management/QA Deficiency".
EVENT DATE (5)                           LER NUMBER (61                             REPORT DATE (71                       OTHER FACILITIES INVOLVED (Bl MONTH       DAY       YEAR         YEAR   JJ: SE~~~~~~AL tt ~~~~~~              MONTH         DAY   YEAR             FACILITY NAMES                     DO<;:KET NUMBER(SI o   16 2 I 2 9 3 1
Adequate control was not maintained over concurrent testing performed during the 24 DM vessel maintenance work such that the 24CP2 arming controls remained "OPEN" and was not considered when restoring the vessel to service. A Chemistry Department troubleshooting procedure is being developed.
9l3-olol9                           ol o o I 1 119      1 OPERATING                   THIS REPORT IS SUBMITTED PURSUANT TO THE RkoQUIREMENTS DF 10 CFR               &sect;: (Chock ono or moro of th* following) (11)
In the _interim, a temporary revision to an existing procedure was completed.
MODE (9)           3 I                                                                                                ~
This procedure provides an automatic sequence that refills the vessel and details specific valve manipulation.
t-----.--....&...:.-+---1 20.402(bl                                                   20.405(c)                           50.73(*ll2llivl                           73.71(b)
The circumstances surrounding the cause of this event and the ways in which it could have been prevented will be reviewed with applicable Chemistry Department personnel.
POWER L~~~L 0 .........
Also, the requirement to employ plans in support of testing/troubleshooting activities will be stressed.
  ~,.,,,,.,,.,,,~.;;.... I 0""'"'
This event will be reviewed by the Nuclear Training Center for lessons learned. NRC Form 366 (6-891 LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station Unit 2 DOCKET NUMBER 5000311 PLANT AND SYSTEM IDENTIFICATION:
20.405(*111 llil 10......- --1 20.405(*1!111iil 50.73(*ll2lM 50.73(*ll2lMil
Westinghouse  
                                                                                                                                                                --    73.71(c)
-Pressurized Water Reactor LER NUMBER 93-009-00 PAGE 2 of 6 Energy Industry Identification System (EIIS) codes are identified in the text as {xx} IDENTIFICATION OF OCCURRENCE:
OTHER ($pacify in Abstract below end in Text~ NRC Form 111!4ll= :::::::::                                                                                               --      50.73(*ll2)1viiil(A)                      366Ai 50.73(*1(2l(vlill(BI 50.731*H2ll*I LICENSEE CONTACT FOR THIS LER (12)
Engineered Safety Feature Actuation:
NAME                                                                                                                                                         TELEPHONE NUMBER AREA CODE M. J. Pollack - LER Coordinator COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
Automatic Start of Motor Driven Auxiliary Feedwater Event Date: 6/22/93 Report Date: 7/19/93 This report was initiated by Incident Report No. 93-277. CONDITIONS PRIOR TO OCCURRENCE:
MANUFAC-                                                                                      MANUFAC-CAUSE     SYSTEM       COMPONENT                                                                           SYSTEM      COMPONENT TURER                                                                                        TUR ER I          I  I      I          I    I I                                                    I          1*    I    I         I   I   I I         I   I       I         I    I I                                                    I          I     I   I         I   I   I SUPPLEMENTAL REPORT EXPECTED (141                                                                               -MONTH      DAY    YEAR
Mode 3 Reactor Power 0% Unit Load -o-MWe DESCRIPTION OF OCCURRENCE:
                                                                                                                                                    . EXPECTED
                                                                                              ~NO SUBMISSION I     YES (If Y61, compl*t* EXPECTED SUBMISSION DATE)
DATE 1151 I          I        I ABSTRACT (Limit to 1400 spact1s, i.e.* approximately fifttJtJn sing/tJ-spactJ typt1writtt1n lines} 116)
On June 22, 1993, at 0326 hours, 21 and 22 motor driven Auxiliary Feedwater (MDAFW) Pumps automatically started due to 21 and 22 Steam Generator Feed Pumps (SGFPs) tripping on low suction pressure (an Engineered Safety Feature). Both SGFPs had been running in support of Condensate System cleanup. At the time, Condensate Polishing System 24 demineralizer (DM) vessel was being restored to service. The SGFPs tripped during the tagging release of the 24 DM vessel.                                                                                         Investigation revealed that the reduced SGFP suction pressure was a direct result of a pressure transient induced during the 24 DM vessel tagging release. The root cause of this event is "Management/QA Deficiency". Adequate control was not maintained over concurrent testing performed during the 24 DM vessel maintenance work such that the 24CP2 arming controls remained "OPEN" and was not considered when restoring the vessel to service. A Chemistry Department troubleshooting procedure is being developed.                                                                                                           In the _interim, a temporary revision to an existing procedure was completed. This procedure provides an automatic sequence that refills the vessel and details specific valve manipulation. The circumstances surrounding the cause of this event and the ways in which it could have been prevented will be reviewed with applicable Chemistry Department personnel. Also, the requirement to employ plans in support of testing/troubleshooting activities will be stressed. This event will be reviewed by the Nuclear Training Center for lessons learned.
NRC Form 366 (6-891
 
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station       DOCKET NUMBER      LER NUMBER        PAGE Unit 2                             5000311         93-009-00        2 of 6 PLANT AND SYSTEM IDENTIFICATION:
Westinghouse   - Pressurized Water Reactor Energy Industry Identification System (EIIS) codes are identified in the text as {xx}
IDENTIFICATION OF OCCURRENCE:
Engineered Safety Feature Actuation:   Automatic Start of Motor Driven Auxiliary Feedwater P~mps Event Date:   6/22/93 Report Date:   7/19/93 This report was initiated by Incident Report No. 93-277.
CONDITIONS PRIOR TO OCCURRENCE:
Mode 3   Reactor Power 0%     Unit Load -o- MWe DESCRIPTION OF OCCURRENCE:
On June 22, 1993, at 0326 hours, 21 and 22 motor driven Auxiliary Feedwater (MDAFW) Pumps {BA} automatically started due to 21 and 22 Steam Generator Feed Pumps (SGFPs) tripping on low suction pressure.
On June 22, 1993, at 0326 hours, 21 and 22 motor driven Auxiliary Feedwater (MDAFW) Pumps {BA} automatically started due to 21 and 22 Steam Generator Feed Pumps (SGFPs) tripping on low suction pressure.
The unit was maintained in MODE 3 (Hot Standby) . Both SGFPs had been running in support of Condensate System cleanup prior to Unit restart. At the time of the event, Condensate Polishing System (CPS) {SF} 21, 22, and 23 demineralizer (DM) vessels were in stand-by with the 25 and 26 DM vessels in service. 24 DM vessel, which had been out of service in support of maintenance, was being restored to service (for standby operation) at the time of the event. The SGFPs tripped during the tagging release of the 24 DM vessel. Investigation revealed that the reduced SGFP suction pressure was a direct result of a pressure transient induced during the 24 DM vessel tagging release. The automatic start of the MDAFW Pumps is an Engineered Safety Feature {ESF) {JE} actuation, which was reported to the Nuclear Regulatory Commission in accordance with Code of Federal Regulations lOCFR 50.72(b) (2) (ii), at 0724 hours (same day). ANALYSIS OF OCCURRENCE:
The unit was maintained in MODE 3 (Hot Standby) . Both SGFPs had been running in support of Condensate System cleanup prior to Unit restart.
At the time of the event, Condensate Polishing System (CPS) {SF} 21, 22, and 23 demineralizer (DM) vessels were in stand-by with the 25 and 26 DM vessels in service. 24 DM vessel, which had been out of service in support of maintenance, was being restored to service (for standby operation) at the time of the event. The SGFPs tripped during the tagging release of the 24 DM vessel. Investigation revealed that the reduced SGFP suction pressure was a direct result of a pressure transient induced during the 24 DM vessel tagging release.
The automatic start of the MDAFW Pumps is an Engineered Safety Feature {ESF) {JE} actuation, which was reported to the Nuclear Regulatory Commission in accordance with Code of Federal Regulations 10CFR 50.72(b) (2) (ii), at 0724 hours (same day).
ANALYSIS OF OCCURRENCE:
The Auxiliary Feedwater system consists of two (2) MDAFW pumps, one (1) steam driven auxiliary feedwater pump and associated valves and piping. It is required to be operable in Modes 1 (Power Operation),
The Auxiliary Feedwater system consists of two (2) MDAFW pumps, one (1) steam driven auxiliary feedwater pump and associated valves and piping. It is required to be operable in Modes 1 (Power Operation),
* LICENSEE EVENT REPORT {LER) TEXT CONTINUATION Salem Generating Station Unit 2 DOCKET NUMBER 5000311 ANALYSIS OF OCCURRENCE: (cont'd) LER NUMBER 93-009-00 PAGE 3 of 6 2 {Startup), and 3 {Hot Standby).
 
The system is designed to cooldown the Reactor Coolant system {RCS) {AB} to less than 350&deg;F from normal operating conditions in the event of a total loss of off-site power. At less than 350&deg;F, the Residual Heat Removal {RHR) System {BP} is used to remove excess RCS heat. As stated, this event involved the automatic start of the MDAFW Pumps upon loss of both SGFPs, which is an ESF function.
LICENSEE EVENT REPORT {LER) TEXT CONTINUATION Salem Generating Station       DOCKET NUMBER    LER NUMBER        PAGE Unit 2                           5000311         93-009-00        3 of 6 ANALYSIS OF OCCURRENCE:   (cont'd) 2 {Startup), and 3 {Hot Standby). The system   is designed to cooldown the Reactor Coolant system {RCS) {AB} to less than 350&deg;F from normal operating conditions in the event of a total loss of off-site power. At less than 350&deg;F, the Residual Heat   Removal {RHR) System
Therefore, this event is reportable to the Nuclear Regulatory conunission in accordance with Code of Federal Regulations 10CFR50.73{a)
{BP} is used to remove excess RCS heat.
{2) {iv). Prior to this event, the CPS 24 DM vessel had been cleared and tagged in support of maintenance.
As stated, this event involved the automatic start of the MDAFW Pumps upon loss of both SGFPs, which is an ESF function. Therefore, this event is reportable to the Nuclear Regulatory conunission in accordance with Code of Federal Regulations 10CFR50.73{a) {2) {iv).
Tagging included the DM vessel inlet manual isolation valve, 24CP1 {Posi-Seal Butterfly Valve). Concurrent to the vessel maintenance, air leakage testing of the 24 DM vessel automatic inlet isolation valve actuator, 24CP2 was conducted.
Prior to this event, the CPS 24 DM vessel had been cleared and tagged in support of maintenance. Tagging included the DM vessel inlet manual isolation valve, 24CP1 {Posi-Seal Butterfly Valve).
This manipulation generated an "OPEN" signal to the valve actuator from the valve OPEN/CLOSE control switch. Per design, the 24 DM vessel pressurizing bypass valve, 24CP4, opened and 24CP2 controls received an "OPEN" arming signal, which would cause 24CP2 to automatically open with less than 8 psid across the valve. Control air to 24CP2 was tagged closed preventing automatic valve operation.
Concurrent to the vessel maintenance, air leakage testing of the 24 DM vessel automatic inlet isolation valve actuator, 24CP2 was conducted. This manipulation generated an "OPEN" signal to the valve actuator from the valve OPEN/CLOSE control switch. Per design, the 24 DM vessel pressurizing bypass valve, 24CP4, opened and 24CP2 controls received an "OPEN" arming signal, which would cause 24CP2 to automatically open with less than 8 psid across the valve. Control air to 24CP2 was tagged closed preventing automatic valve operation.
The 24CP2 valve "OPEN" signal remained armed {per design). There is no positive indication when the valve is armed. {reference Attachment 1, schematic of system) On June 21 maintenance on 24 DM vessel was completed and a flange, which had been removed to allow the vessel to drain, was reinstalled.
The 24CP2 valve "OPEN" signal remained armed {per design). There is no positive indication when the valve is armed.   {reference Attachment 1, schematic of system)
Prior to this event, it was not recognized that 24CP1, which although closed, was leaking past its valve seat. Consequently, leakage occurred through the open 24CP4 via 24CP1. This leakage initiated 24 DM vessel fill despite the fact that the 24CP1 valve was tagged closed. On June 22, a tagging release of 24 DM vessel was completed.
On June 21 maintenance on 24 DM vessel was completed and a flange, which had been removed to allow the vessel to drain, was reinstalled. Prior to this event, it was not recognized that 24CP1, which although closed, was leaking past its valve seat.
When the 24CP1 was opened, the rate of vessel fill increased.
Consequently, leakage occurred through the open 24CP4 via 24CP1.
With the 24 DM vessel vent valve closed, an air bubble formed in the vessel. Condensate System pressure {610 psi) caused the vessel to pressurize.
This leakage initiated 24 DM vessel fill despite the fact that the 24CP1 valve was tagged closed.
Once the differential pressure decreased to 8 psid across 24CP2, the valve automatically opened due to the armed OPEN signal. Pressurizing of the 24 DM vessel caused the air bubble to compress.
On June 22, a tagging release of 24 DM vessel was completed. When the 24CP1 was opened, the rate of vessel fill increased. With the 24 DM vessel vent valve closed, an air bubble formed in the vessel.
Condensate System pressure {610 psi) caused the vessel to pressurize. Once the differential pressure decreased to 8 psid across 24CP2, the valve automatically opened due to the armed OPEN signal.
Pressurizing of the 24 DM vessel caused the air bubble to compress.
Once the 24CP2 opened, the air bubble released into the Condensate System piping causing a pressure transient which resulted in momentary low suction pressure to the SGFPs inlet piping and the subsequent trip of the SGFPs.
Once the 24CP2 opened, the air bubble released into the Condensate System piping causing a pressure transient which resulted in momentary low suction pressure to the SGFPs inlet piping and the subsequent trip of the SGFPs.
* LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station Unit 2 APPARENT CAUSE OF OCCURRENCE:
 
DOCKET NUMBER 5000311 LER NUMBER 93-009-00 PAGE 4 of 6 The root cause of this event is "Management/QA Deficiency" (per NUREG 1022). Adequate control was not maintained over concurrent testing performed during the 24 DM vessel maintenance work such that the 24CP2 arming controls remained "OPEN" and was not considered when restoring the vessel to service. In this event, the vent valve was cleared and tagged in support of the 24 DM vessel planned maintenance.
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station       DOCKET NUMBER     LER NUMBER       PAGE Unit 2                          5000311        93-009-00       4 of 6 APPARENT CAUSE OF OCCURRENCE:
When the vesse.l was to be returned to service, it was one of the first tags to be released.
The root cause of this event is "Management/QA Deficiency" (per NUREG 1022). Adequate control was not maintained over concurrent testing performed during the 24 DM vessel maintenance work such that the 24CP2 arming controls remained "OPEN" and was not considered when restoring the vessel to service.
Operational considerations were not taken as to the potential that the vessel was filling via the 24CP1 and 24CP4 valves and that the 24CP2 valve controls had an armed "OPEN" signal from the concurrent work. A contributing factor to the cause of this event is the lack of positive indication of the status of the 24CP2 "OPEN" signal. PRIOR SIMILAR OCCURRENCES:
In this event, the vent valve was cleared and tagged in support of the 24 DM vessel planned maintenance. When the vesse.l was to be returned to service, it was one of the first tags to be released.
On March 16, 1993, Salem Unit 2 experienced a reactor trip (reference LER 311/93-005-00) which was initiated by a pressure transient from the Condensate Polishing System which tripped a SGFP. Although the results are comparable to the event addressed in this LER, the specific causal factors differ. The March 16 event was initiated by the failure of a differential pressure switch which had failed due to water intrusion from a leaking valve. SAFETY SIGNIFICANCE:
Operational considerations were not taken as to the potential that the vessel was filling via the 24CP1 and 24CP4 valves and that the 24CP2 valve controls had an armed "OPEN" signal from the concurrent work.
Steam Generator level was maintained during this event. The automatic start of the MDAFW Pumps although inadvertent, functioned per design upon the trip of both SGFPs. The health and safety of the public was not affected by this event. CORRECTIVE ACTION: The circumstances surrounding the cause of this event and the ways in which it could have been prevented will be reviewed with applicable Chemistry Department personnel.
A contributing factor to the cause of this event is the lack of positive indication of the status of the 24CP2 "OPEN" signal.
Included in the review will be the need to apply a blocking tag to the CP2 valve switch when a DM vessel is to be cleared and tagged for maintenance.
PRIOR SIMILAR OCCURRENCES:
Also, the requirement to employ plans in support of testing/troubleshooting activities will be stressed.
On March 16, 1993, Salem Unit 2 experienced a reactor trip (reference LER 311/93-005-00) which was initiated by a pressure transient from the Condensate Polishing System which tripped a SGFP. Although the results are comparable to the event addressed in this LER, the specific causal factors differ. The March 16 event was initiated by the failure of a differential pressure switch which had failed due to water intrusion from a leaking valve.
SAFETY SIGNIFICANCE:
Steam Generator level was maintained during this event. The automatic start of the MDAFW Pumps although inadvertent, functioned per design upon the trip of both SGFPs. The health and safety of the public was not affected by this event.
CORRECTIVE ACTION:
The circumstances surrounding the cause of this event and the ways in which it could have been prevented will be reviewed with applicable Chemistry Department personnel. Included in the review will be the need to apply a blocking tag to the CP2 valve switch when a DM vessel is to be cleared and tagged for maintenance. Also, the requirement to employ plans in support of testing/troubleshooting activities will be stressed.
A Chemistry Department troubleshooting procedure is being developed.
A Chemistry Department troubleshooting procedure is being developed.
In the interim, a temporary revision to Chemistry Procedure SC.CH-SO.CP-0842(A), "Condensate Polisher Resin Transfer" was completed.
In the interim, a temporary revision to Chemistry Procedure SC.CH-SO.CP-0842(A), "Condensate Polisher Resin Transfer" was completed. This procedure provides an automatic sequence that refills the vessel and opens the CP2 valve. The temporary revision
This procedure provides an automatic sequence that refills the vessel and opens the CP2 valve. The temporary revision
 
* LICENSEE EVENT REPORT {LER) TEXT CONTINUATION Salem Generating Station Unit 2 CORRECTIVE ACTION: (cont'd) DOCKET NUMBER 5000311 LER NUMBER 93-009-00 PAGE 5 of 6 provides manual intervention to ensure the vessel is full* of water and has no air prior to the CP2 valve opening. This event will be reviewed by the Nuclear Training Center for lessons learned. Revisions to existing programs will be made as appropriate.
LICENSEE EVENT REPORT {LER) TEXT CONTINUATION Salem Generating Station     DOCKET NUMBER     LER NUMBER       PAGE Unit 2                          5000311        93-009-00       5 of 6 CORRECTIVE ACTION:  (cont'd) provides manual intervention to ensure the vessel is full* of water and has no air prior to the CP2 valve opening.
Considerations include reviewing the Chemistry Department training programs to ensure that system operational consequences are adequately addressed.
This event will be reviewed by the Nuclear Training Center for lessons learned. Revisions to existing programs will be made as appropriate. Considerations include reviewing the Chemistry Department training programs to ensure that system operational consequences are adequately addressed.
The need to provide positive indication of the status of the CP2 valve "OPEN" signal indication is being assessed.
The need to provide positive indication of the status of the CP2 valve "OPEN" signal indication is being assessed. Action will be taken based on the results of this assessment.
Action will be taken based on the results of this assessment.
(L~
MP:pc SORC Mtg. 93-067 eneral Manager -Salem Operations
eneral Manager -
* LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station Unit 2 26 25 1< 24 DM -VESSEL DOCKET NUMBER 5000311 ATTACHMENT 1 DISTRIBUTION MANIFOLD --< >---< >-LER NUMBER 93-009-00 FROM COND. PUMP CP4 CP2 CPl 21 >-+,...-------<-
Salem Operations MP:pc SORC Mtg. 93-067
TO SGFPs PAGE 6 of 6}}
 
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station       DOCKET NUMBER    LER NUMBER    PAGE Unit 2                           5000311      93-009-00    6 of 6 ATTACHMENT 1 DISTRIBUTION MANIFOLD 26 25 1--~~<-~  FROM COND. PUMP CP4 1<  c~~,--+-1--Cf~>
CP2     CPl 24 DM
              -  VESSEL                              21
                          >-+,...-------<-
TO SGFPs}}

Latest revision as of 06:09, 3 February 2020

LER 93-009-00:on 930629,automatic Start of Motor Driven Auxiliary Feedwater Pumps Occurred Due to Mgt/Qa Deficiency. Troubleshooting Procedures developed.W/930719 Ltr
ML18100A493
Person / Time
Site: Salem PSEG icon.png
Issue date: 07/19/1993
From: Pollack M, Vondra C
Public Service Enterprise Group
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
LER-93-009-01, LER-93-9-1, NUDOCS 9307280092
Download: ML18100A493 (7)


Text

. e OPS~G Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038 Salem Generating Station July 19, 1993

u. s. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555

Dear Sir:

SALEM GENERATING STATION LICENSE NO. DPR-75 DOCKET NO. 50-311 UNIT NO. 2 LICENSEE EVENT REPORT 93-009-00 This Licensee Event Report is being submitted pursuant to the requirements of the Code of Federal Regulations 10CFR 50.73(a) (2) (iv). This report is required to be issued within thirty (30) days of event discovery.

Sincerely yours,

c. A Vondra General Manager -

Salem Operations MP:pc Distribution 9307280092 930719

~DR ADDCK 05000311 PDR The power is in your hanas.

95-2189 REV 7-92

NRC FORM366 U.S. NUCLEAR REGULATORY COMMISSION

  • (6-89) APPROVED OMB NO. 3150-0104 EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD LICENSEE EVENT REPORT (LER) COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (P-530) 0 U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON. DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET. WASHINGTON, DC 20503.

FACILITY NAME 11> DOCKET NUMBER (2) I PAGE (3)

Salem Generating Station - Unit 2 TITLE (4)

!o 1s Io Io Io I 31 i 1i I 1 loFI 016 ESF Actuation: Automatic Start of Motor Driven Auxiliary Feedwater Pumps.

EVENT DATE (5) LER NUMBER (61 REPORT DATE (71 OTHER FACILITIES INVOLVED (Bl MONTH DAY YEAR YEAR JJ: SE~~~~~~AL tt ~~~~~~ MONTH DAY YEAR FACILITY NAMES DO<;:KET NUMBER(SI o 16 2 I 2 9 3 1

9l3-olol9 ol o o I 1 119 1 OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE RkoQUIREMENTS DF 10 CFR §: (Chock ono or moro of th* following) (11)

MODE (9) 3 I ~

t-----.--....&...:.-+---1 20.402(bl 20.405(c) 50.73(*ll2llivl 73.71(b)

POWER L~~~L 0 .........

~,.,,,,.,,.,,,~.;;.... I 0""'"'

20.405(*111 llil 10......- --1 20.405(*1!111iil 50.73(*ll2lM 50.73(*ll2lMil

-- 73.71(c)

OTHER ($pacify in Abstract below end in Text~ NRC Form 111!4ll= ::::::::: -- 50.73(*ll2)1viiil(A) 366Ai 50.73(*1(2l(vlill(BI 50.731*H2ll*I LICENSEE CONTACT FOR THIS LER (12)

NAME TELEPHONE NUMBER AREA CODE M. J. Pollack - LER Coordinator COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)

MANUFAC- MANUFAC-CAUSE SYSTEM COMPONENT SYSTEM COMPONENT TURER TUR ER I I I I I I I I 1* I I I I I I I I I I I I I I I I I I I SUPPLEMENTAL REPORT EXPECTED (141 -MONTH DAY YEAR

. EXPECTED

~NO SUBMISSION I YES (If Y61, compl*t* EXPECTED SUBMISSION DATE)

DATE 1151 I I I ABSTRACT (Limit to 1400 spact1s, i.e.* approximately fifttJtJn sing/tJ-spactJ typt1writtt1n lines} 116)

On June 22, 1993, at 0326 hours0.00377 days <br />0.0906 hours <br />5.390212e-4 weeks <br />1.24043e-4 months <br />, 21 and 22 motor driven Auxiliary Feedwater (MDAFW) Pumps automatically started due to 21 and 22 Steam Generator Feed Pumps (SGFPs) tripping on low suction pressure (an Engineered Safety Feature). Both SGFPs had been running in support of Condensate System cleanup. At the time, Condensate Polishing System 24 demineralizer (DM) vessel was being restored to service. The SGFPs tripped during the tagging release of the 24 DM vessel. Investigation revealed that the reduced SGFP suction pressure was a direct result of a pressure transient induced during the 24 DM vessel tagging release. The root cause of this event is "Management/QA Deficiency". Adequate control was not maintained over concurrent testing performed during the 24 DM vessel maintenance work such that the 24CP2 arming controls remained "OPEN" and was not considered when restoring the vessel to service. A Chemistry Department troubleshooting procedure is being developed. In the _interim, a temporary revision to an existing procedure was completed. This procedure provides an automatic sequence that refills the vessel and details specific valve manipulation. The circumstances surrounding the cause of this event and the ways in which it could have been prevented will be reviewed with applicable Chemistry Department personnel. Also, the requirement to employ plans in support of testing/troubleshooting activities will be stressed. This event will be reviewed by the Nuclear Training Center for lessons learned.

NRC Form 366 (6-891

LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 2 5000311 93-009-00 2 of 6 PLANT AND SYSTEM IDENTIFICATION:

Westinghouse - Pressurized Water Reactor Energy Industry Identification System (EIIS) codes are identified in the text as {xx}

IDENTIFICATION OF OCCURRENCE:

Engineered Safety Feature Actuation: Automatic Start of Motor Driven Auxiliary Feedwater P~mps Event Date: 6/22/93 Report Date: 7/19/93 This report was initiated by Incident Report No.93-277.

CONDITIONS PRIOR TO OCCURRENCE:

Mode 3 Reactor Power 0% Unit Load -o- MWe DESCRIPTION OF OCCURRENCE:

On June 22, 1993, at 0326 hours0.00377 days <br />0.0906 hours <br />5.390212e-4 weeks <br />1.24043e-4 months <br />, 21 and 22 motor driven Auxiliary Feedwater (MDAFW) Pumps {BA} automatically started due to 21 and 22 Steam Generator Feed Pumps (SGFPs) tripping on low suction pressure.

The unit was maintained in MODE 3 (Hot Standby) . Both SGFPs had been running in support of Condensate System cleanup prior to Unit restart.

At the time of the event, Condensate Polishing System (CPS) {SF} 21, 22, and 23 demineralizer (DM) vessels were in stand-by with the 25 and 26 DM vessels in service. 24 DM vessel, which had been out of service in support of maintenance, was being restored to service (for standby operation) at the time of the event. The SGFPs tripped during the tagging release of the 24 DM vessel. Investigation revealed that the reduced SGFP suction pressure was a direct result of a pressure transient induced during the 24 DM vessel tagging release.

The automatic start of the MDAFW Pumps is an Engineered Safety Feature {ESF) {JE} actuation, which was reported to the Nuclear Regulatory Commission in accordance with Code of Federal Regulations 10CFR 50.72(b) (2) (ii), at 0724 hours0.00838 days <br />0.201 hours <br />0.0012 weeks <br />2.75482e-4 months <br /> (same day).

ANALYSIS OF OCCURRENCE:

The Auxiliary Feedwater system consists of two (2) MDAFW pumps, one (1) steam driven auxiliary feedwater pump and associated valves and piping. It is required to be operable in Modes 1 (Power Operation),

LICENSEE EVENT REPORT {LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 2 5000311 93-009-00 3 of 6 ANALYSIS OF OCCURRENCE: (cont'd) 2 {Startup), and 3 {Hot Standby). The system is designed to cooldown the Reactor Coolant system {RCS) {AB} to less than 350°F from normal operating conditions in the event of a total loss of off-site power. At less than 350°F, the Residual Heat Removal {RHR) System

{BP} is used to remove excess RCS heat.

As stated, this event involved the automatic start of the MDAFW Pumps upon loss of both SGFPs, which is an ESF function. Therefore, this event is reportable to the Nuclear Regulatory conunission in accordance with Code of Federal Regulations 10CFR50.73{a) {2) {iv).

Prior to this event, the CPS 24 DM vessel had been cleared and tagged in support of maintenance. Tagging included the DM vessel inlet manual isolation valve, 24CP1 {Posi-Seal Butterfly Valve).

Concurrent to the vessel maintenance, air leakage testing of the 24 DM vessel automatic inlet isolation valve actuator, 24CP2 was conducted. This manipulation generated an "OPEN" signal to the valve actuator from the valve OPEN/CLOSE control switch. Per design, the 24 DM vessel pressurizing bypass valve, 24CP4, opened and 24CP2 controls received an "OPEN" arming signal, which would cause 24CP2 to automatically open with less than 8 psid across the valve. Control air to 24CP2 was tagged closed preventing automatic valve operation.

The 24CP2 valve "OPEN" signal remained armed {per design). There is no positive indication when the valve is armed. {reference Attachment 1, schematic of system)

On June 21 maintenance on 24 DM vessel was completed and a flange, which had been removed to allow the vessel to drain, was reinstalled. Prior to this event, it was not recognized that 24CP1, which although closed, was leaking past its valve seat.

Consequently, leakage occurred through the open 24CP4 via 24CP1.

This leakage initiated 24 DM vessel fill despite the fact that the 24CP1 valve was tagged closed.

On June 22, a tagging release of 24 DM vessel was completed. When the 24CP1 was opened, the rate of vessel fill increased. With the 24 DM vessel vent valve closed, an air bubble formed in the vessel.

Condensate System pressure {610 psi) caused the vessel to pressurize. Once the differential pressure decreased to 8 psid across 24CP2, the valve automatically opened due to the armed OPEN signal.

Pressurizing of the 24 DM vessel caused the air bubble to compress.

Once the 24CP2 opened, the air bubble released into the Condensate System piping causing a pressure transient which resulted in momentary low suction pressure to the SGFPs inlet piping and the subsequent trip of the SGFPs.

LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 2 5000311 93-009-00 4 of 6 APPARENT CAUSE OF OCCURRENCE:

The root cause of this event is "Management/QA Deficiency" (per NUREG 1022). Adequate control was not maintained over concurrent testing performed during the 24 DM vessel maintenance work such that the 24CP2 arming controls remained "OPEN" and was not considered when restoring the vessel to service.

In this event, the vent valve was cleared and tagged in support of the 24 DM vessel planned maintenance. When the vesse.l was to be returned to service, it was one of the first tags to be released.

Operational considerations were not taken as to the potential that the vessel was filling via the 24CP1 and 24CP4 valves and that the 24CP2 valve controls had an armed "OPEN" signal from the concurrent work.

A contributing factor to the cause of this event is the lack of positive indication of the status of the 24CP2 "OPEN" signal.

PRIOR SIMILAR OCCURRENCES:

On March 16, 1993, Salem Unit 2 experienced a reactor trip (reference LER 311/93-005-00) which was initiated by a pressure transient from the Condensate Polishing System which tripped a SGFP. Although the results are comparable to the event addressed in this LER, the specific causal factors differ. The March 16 event was initiated by the failure of a differential pressure switch which had failed due to water intrusion from a leaking valve.

SAFETY SIGNIFICANCE:

Steam Generator level was maintained during this event. The automatic start of the MDAFW Pumps although inadvertent, functioned per design upon the trip of both SGFPs. The health and safety of the public was not affected by this event.

CORRECTIVE ACTION:

The circumstances surrounding the cause of this event and the ways in which it could have been prevented will be reviewed with applicable Chemistry Department personnel. Included in the review will be the need to apply a blocking tag to the CP2 valve switch when a DM vessel is to be cleared and tagged for maintenance. Also, the requirement to employ plans in support of testing/troubleshooting activities will be stressed.

A Chemistry Department troubleshooting procedure is being developed.

In the interim, a temporary revision to Chemistry Procedure SC.CH-SO.CP-0842(A), "Condensate Polisher Resin Transfer" was completed. This procedure provides an automatic sequence that refills the vessel and opens the CP2 valve. The temporary revision

LICENSEE EVENT REPORT {LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 2 5000311 93-009-00 5 of 6 CORRECTIVE ACTION: (cont'd) provides manual intervention to ensure the vessel is full* of water and has no air prior to the CP2 valve opening.

This event will be reviewed by the Nuclear Training Center for lessons learned. Revisions to existing programs will be made as appropriate. Considerations include reviewing the Chemistry Department training programs to ensure that system operational consequences are adequately addressed.

The need to provide positive indication of the status of the CP2 valve "OPEN" signal indication is being assessed. Action will be taken based on the results of this assessment.

(L~

eneral Manager -

Salem Operations MP:pc SORC Mtg.93-067

LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 2 5000311 93-009-00 6 of 6 ATTACHMENT 1 DISTRIBUTION MANIFOLD 26 25 1--~~<-~ FROM COND. PUMP CP4 1< c~~,--+-1--Cf~>

CP2 CPl 24 DM

- VESSEL 21

>-+,...-------<-

TO SGFPs