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| | document type = Letter, Request for Additional Information (RAI) | | | document type = Letter, Request for Additional Information (RAI) |
| | page count = 5 | | | page count = 5 |
| | project = TAC:MF2984, TAC:MF2983 | | | project = TAC:MF2983, TAC:MF2984 |
| | stage = RAI | | | stage = RAI |
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| ==Enclosure:== | | ==Enclosure:== |
| Request for Additional Information cc w/encl: Distribution via Listserv G. Edward Miller, Project Manager Plant Licensing Branch 11-1 Division of Operating Reactor Licensing Office of Nuclear Reactor Regulation REQUEST FOR ADDITIONAL INFORMATION MCGUIRE NUCLEAR STATION, UNITS 1 AND 2 RELATED TO A LICENSE AMENDMENT REQUEST SUPPORTING CORRECTION OF A NUCLEAR SERVICE WATER SYSTEM DEGRADED CONDITION DUKE ENERGY CAROLINAS, LLC DOCKET NOS. 50-369 AND 50-370 By letter dated June 30, 2015 (Agencywide Documents Access and Management System (ADAMS) Accession No. ML 15191A025), Duke Energy Carolinas, LLC (Duke Energy) submitted a license amendment request (LAR) to temporarily change McGuire Nuclear Station (MNS), Units 1 and 2, Technical Specifications (TSs) for correction of a degraded condition affecting the 'A' Train of the nuclear service water system (NSWS). The requested amendment would temporarily change the following TSs to allow the inoperability of the 'A' Train of the NSWS for a total of up to 14 days: TS 3.5.2, Emergency Core Cooling System (ECCS) -Operating; TS 3.6.6, Containment Spray System (CSS); TS 3.7.5, Auxiliary Feedwater (AFW) System; TS 3.7.6, Component Cooling Water (CCW) System; TS 3.7.7, Nuclear Service Water System (NSWS); TS 3.7.9, Control Room Area Ventilation System (CRAVS); TS 3.7.11, Auxiliary Building Filtered Ventilation Exhaust System (ABFVES), and TS 3.8.1, AC Operating. The 'A' Train of the shared NSWS would be inoperable while the safety-related supply from the MNS Nuclear Service Water Pond was drained and isolated to correct a degraded condition affecting that line. Based on its review of this amendment request, the NRC staff has determined the following additional information is necessary to support completion of its technical review: SCVB-RAl-001 The license amendment focuses on the temporary alignments and changes requested for the NSWS, however, these changes impact other systems. For the CSS, CRAVS, and the ABFVES: a. Explain the available capabilities of the above systems during the time when the requested temporary TSs would be enacted. b. Discuss the impact of any deviations from standard alignment and operation of the systems. Enclosure SRXB-RAl-001 While the approach taken in the proposed LAR is a qualitative risk approach, please address the need to preclude potentially high-risk plant configurations that could result if additional | | Request for Additional Information cc w/encl: Distribution via Listserv G. Edward Miller, Project Manager Plant Licensing Branch 11-1 Division of Operating Reactor Licensing Office of Nuclear Reactor Regulation REQUEST FOR ADDITIONAL INFORMATION MCGUIRE NUCLEAR STATION, UNITS 1 AND 2 RELATED TO A LICENSE AMENDMENT REQUEST SUPPORTING CORRECTION OF A NUCLEAR SERVICE WATER SYSTEM DEGRADED CONDITION DUKE ENERGY CAROLINAS, LLC DOCKET NOS. 50-369 AND 50-370 By letter dated June 30, 2015 (Agencywide Documents Access and Management System (ADAMS) Accession No. ML 15191A025), Duke Energy Carolinas, LLC (Duke Energy) submitted a license amendment request (LAR) to temporarily change McGuire Nuclear Station (MNS), Units 1 and 2, Technical Specifications (TSs) for correction of a degraded condition affecting the 'A' Train of the nuclear service water system (NSWS). The requested amendment would temporarily change the following TSs to allow the inoperability of the 'A' Train of the NSWS for a total of up to 14 days: TS 3.5.2, Emergency Core Cooling System (ECCS) -Operating; TS 3.6.6, Containment Spray System (CSS); TS 3.7.5, Auxiliary Feedwater (AFW) System; TS 3.7.6, Component Cooling Water (CCW) System; TS 3.7.7, Nuclear Service Water System (NSWS); TS 3.7.9, Control Room Area Ventilation System (CRAVS); TS 3.7.11, Auxiliary Building Filtered Ventilation Exhaust System (ABFVES), and TS 3.8.1, AC Operating. The 'A' Train of the shared NSWS would be inoperable while the safety-related supply from the MNS Nuclear Service Water Pond was drained and isolated to correct a degraded condition affecting that line. Based on its review of this amendment request, the NRC staff has determined the following additional information is necessary to support completion of its technical review: SCVB-RAl-001 The license amendment focuses on the temporary alignments and changes requested for the NSWS, however, these changes impact other systems. For the CSS, CRAVS, and the ABFVES: a. Explain the available capabilities of the above systems during the time when the requested temporary TSs would be enacted. b. Discuss the impact of any deviations from standard alignment and operation of the systems. Enclosure SRXB-RAl-001 While the approach taken in the proposed LAR is a qualitative risk approach, please address the need to preclude potentially high-risk plant configurations that could result if additional |
| * equipment, not associated with the proposed change, is taken out-of-service during the proposed Allowed Outage Time (AOT) extension. Provide a justification to limiting the prohibition of discretionary maintenance to the following systems: a. 1A EOG; b. 2A EOG; c. The 'A' Train of NSWS excluding the activities described in the LAR for the 'A' Train NSWS piping to the SNSWP; d. The 'B' Train of NSWS, ECCS, CSS, AFW, CCW, CRAVS, ABFVES or the EOGs; e. The switchyard and other offsite power sources; and f. The SSF. Specifically, provide a justification for not implementing a broader limitation on discretionary maintenance (e.g., such as that of the cited STPNOC precedent (ML050100291 ), "STPNOC will not perform any planned voluntary maintenance in Unit 1 during the extended AOT (EAOT) that would increase the ICCDP. '?. -SRXB-RAl-002 The LAR lists the following equipment to be protected during the AOT extension of the 'A' train of NSWS: a. 'B' Train NSWS b. 18 EOG c. 28 EOG. d. 18 ECCS. e. 28 ECCS f. 18 css g. 28 css h. 1BAFW i. 2BAFW j. 18 ccw k. 28 ccw I. B CRAVS m. BABFVES n. Auxiliary Building WZ Sump and equipment supporting function of sump Provide a discussion on the criteria used to determine the protected equipment. Include a justification for not including the turbine driven AFW pump, Containment Ventilation Cooling Water (RV) system and the Standby Shutdown Facility (SSF) standby makeup pump, which appear to be important to managing the risk of the proposed AOT extension. | | * equipment, not associated with the proposed change, is taken out-of-service during the proposed Allowed Outage Time (AOT) extension. Provide a justification to limiting the prohibition of discretionary maintenance to the following systems: a. 1A EOG; b. 2A EOG; c. The 'A' Train of NSWS excluding the activities described in the LAR for the 'A' Train NSWS piping to the SNSWP; d. The 'B' Train of NSWS, ECCS, CSS, AFW, CCW, CRAVS, ABFVES or the EOGs; e. The switchyard and other offsite power sources; and f. The SSF. Specifically, provide a justification for not implementing a broader limitation on discretionary maintenance (e.g., such as that of the cited STPNOC precedent (ML050100291 ), "STPNOC will not perform any planned voluntary maintenance in Unit 1 during the extended AOT (EAOT) that would increase the ICCDP. '?. -SRXB-RAl-002 The LAR lists the following equipment to be protected during the AOT extension of the 'A' train of NSWS: a. 'B' Train NSWS b. 18 EOG c. 28 EOG. d. 18 ECCS. e. 28 ECCS f. 18 css g. 28 css h. 1BAFW i. 2BAFW j. 18 ccw k. 28 ccw I. B CRAVS m. BABFVES n. Auxiliary Building WZ Sump and equipment supporting function of sump Provide a discussion on the criteria used to determine the protected equipment. Include a justification for not including the turbine driven AFW pump, Containment Ventilation Cooling Water (RV) system and the Standby Shutdown Facility (SSF) standby makeup pump, which appear to be important to managing the risk of the proposed AOT extension. SRXB-RAl-003 Clarify whether any maintenance will be allowed on the 'A' Train NSWS that would impact the ability of the system to operate taking suction from the Lake Norman Low Level Intake (LU) (even if these activities are within the 72 completion time) during the period that the Standby Nuclear Service Water Pond (SNSWP) suction is not available for the 'A' train of NSWS. Specifically, address what is meant by the following statement .in section 3.5 of the LAR: 2. Any maintenance that is on the remaining portions of the 'A' Train NSWS during the period in which the 'A' NSWS piping from the SNSWP is not available will be limited to a 72 hour completion time. |
| SRXB-RAl-003 Clarify whether any maintenance will be allowed on the 'A' Train NSWS that would impact the ability of the system to operate taking suction from the Lake Norman Low Level Intake (LU) (even if these activities are within the 72 completion time) during the period that the Standby Nuclear Service Water Pond (SNSWP) suction is not available for the 'A' train of NSWS. Specifically, address what is meant by the following statement .in section 3.5 of the LAR: 2. Any maintenance that is on the remaining portions of the 'A' Train NSWS during the period in which the 'A' NSWS piping from the SNSWP is not available will be limited to a 72 hour completion time. | |
| Mr. Steven D. Capps Vice President McGuire Nuclear Station Duke Energy Carolinas, LLC 12700 Hagers Ferry Road Huntersville, NC 28078-8985 September 14, 2015 | | Mr. Steven D. Capps Vice President McGuire Nuclear Station Duke Energy Carolinas, LLC 12700 Hagers Ferry Road Huntersville, NC 28078-8985 September 14, 2015 |
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| ==Enclosure:== | | ==Enclosure:== |
| Request for Additional Information cc w/encl: Distribution via Listserv DISTRIBUTION: PUBLIC RidsAcrsAcnw _MailCTR Resource RidsNrrDeEicb Resource RidsNrrLASFigueroa Resource ADAMS Accession No. ML 15252A276 OFFICE NRR/LPL2-1 /PM N NAME GEMiller SFigueroa LPL2-1 R/F Sincerely, /RA/ G. Edward Miller, Project Manager Plant Licensing Branch 11-1 Division of Operating Reactor Licensing Office of Nuclear Reactor Regulation RidsNrrDorllpl2-1 Resource RidsNrrPMMcGuire Resource (hard copy) RidsRgn2MailCenter Resource *Via E-mail S/SRXB/BC NRR/DSS/SCVB/B NRR/LPL2-1/BC RDennig RPascarelli DATE 09/14/15 09/14/15 08/28/15 08/27/15 09/14/15 OFFICIAL RECORD | | Request for Additional Information cc w/encl: Distribution via Listserv DISTRIBUTION: PUBLIC RidsAcrsAcnw _MailCTR Resource RidsNrrDeEicb Resource RidsNrrLASFigueroa Resource ADAMS Accession No. ML 15252A276 OFFICE NRR/LPL2-1 /PM N NAME GEMiller SFigueroa LPL2-1 R/F Sincerely, /RA/ G. Edward Miller, Project Manager Plant Licensing Branch 11-1 Division of Operating Reactor Licensing Office of Nuclear Reactor Regulation RidsNrrDorllpl2-1 Resource RidsNrrPMMcGuire Resource (hard copy) RidsRgn2MailCenter Resource *Via E-mail S/SRXB/BC NRR/DSS/SCVB/B NRR/LPL2-1/BC RDennig RPascarelli DATE 09/14/15 09/14/15 08/28/15 08/27/15 09/14/15 OFFICIAL RECORD}} |
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MONTHYEARML13304B4452013-10-28028 October 2013 Revised License Amendment Request for One-Time Change to Technical Specification 3.8.4, DC Sources-Operating for Battery Replacement Project stage: Request ML13351A3432013-12-19019 December 2013 Acceptance of Requested Licensing Action License Amendment Request for One-Time Change to Technical Specification 3.8.4, DC Sources-Operating for Battery Replacement Project stage: Acceptance Review ML14127A4622014-05-12012 May 2014 Request for Additional Information Regarding License Amendment Request to Modify Specification 3.8.4 Setpoint Project stage: RAI MNS-14-045, Responses to Request for Additional Information Related to License Amendment Request for One-Time Change to Technical Specification 3.8.4, DC Sources-Operating for Battery Replacement Dated October 28, 20132014-06-0303 June 2014 Responses to Request for Additional Information Related to License Amendment Request for One-Time Change to Technical Specification 3.8.4, DC Sources-Operating for Battery Replacement Dated October 28, 2013 Project stage: Response to RAI ML14178B2322014-07-14014 July 2014 Request for Additional Information Regarding License Amendment Request to Modify Technical Specification 3.3.2 Setpoint Project stage: RAI ML14231A6342014-09-10010 September 2014 Issuance of Amendments Regarding Technical Specification 3.8.4, DC Sources-Operating, Project stage: Approval ML15202A6612015-07-27027 July 2015 Acceptance Review of License Amendment Request Temporary Changes to Technical Specifications for Correction of Nuclear Service Water System Degraded Condition Project stage: Acceptance Review ML15196A3862015-08-0404 August 2015 Notice of Consideration of Issuance of Amendment to Facility Operating License, Proposed No Significant Hazards Consideration Determination, and Opportunity for a Hearing and Order Imposing Procedures for Document Access To.. Project stage: Other MNS-15-062, Response to Request for Additional Information Regarding License Amendment Request (LAR) for Temporary Changes to Technical Specifications for Correction of an 'A' Train Nuclear Service Water System (Nsws) Degraded Condition2015-08-11011 August 2015 Response to Request for Additional Information Regarding License Amendment Request (LAR) for Temporary Changes to Technical Specifications for Correction of an 'A' Train Nuclear Service Water System (Nsws) Degraded Condition Project stage: Response to RAI ML15196A6162015-08-13013 August 2015 Duke Energy Carolinas, LLC, McGuire Nuclear Station, Units 1 and 2 - License Amendment Application; Opportunity to Comment, Request a Hearing, and Petition for Leave to Intervene; Order Project stage: Other ML15243A4082015-08-28028 August 2015 NRR E-mail Capture - Draft RAI for Nsws Temp AOT Extension Project stage: Draft RAI ML15252A2762015-09-14014 September 2015 Request for Additional Information Regarding License Amendment Request Nuclear Service Water System Allowed Outage Time Extension Project stage: RAI MNS-15-073, Response to NRC Letter Dated August 27, 2015, Request for Additional Information Regarding License Amendment Request, Nuclear Service Water System Allowed Outage Time Extension2015-09-24024 September 2015 Response to NRC Letter Dated August 27, 2015, Request for Additional Information Regarding License Amendment Request, Nuclear Service Water System Allowed Outage Time Extension Project stage: Request MNS-15-078, Response to NRC Letter Dated September 14, 2015, Request for Additional Information Regarding License Amendment Request, Nuclear Service Water System Allowed Outage Time Extension2015-10-0808 October 2015 Response to NRC Letter Dated September 14, 2015, Request for Additional Information Regarding License Amendment Request, Nuclear Service Water System Allowed Outage Time Extension Project stage: Request ML15289A5552015-10-26026 October 2015 Request for Additional Information Regarding License Amendment Request Nuclear Service Water System Allowed Outage Time Extension Project stage: RAI ML15343A0122015-12-0707 December 2015 Response to NRC Letter Dated 10/26/2015, Request for Additional Information Regarding License Amendment Request, Nuclear Service Water System Allowed Outage Time Extension. Project stage: Request MNS-16-005, Response to Request for Additional Information (RAI) During January 12, 2016, NRC Teleconference Pertaining to License Amendment Request for Nuclear Service Water System Allowed Outage Time Extension2016-02-10010 February 2016 Response to Request for Additional Information (RAI) During January 12, 2016, NRC Teleconference Pertaining to License Amendment Request for Nuclear Service Water System Allowed Outage Time Extension Project stage: Response to RAI 2015-12-07
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Category:Letter
MONTHYEARIR 05000369/20244022024-10-0808 October 2024 Security Baseline Inspection Report 05000369/2024402 05000370/2024402 IR 05000369/20240052024-08-26026 August 2024 Updated Inspection Plan for McGuire Nuclear Station, Units 1 and 2, (Report 05000369-2024005 and 05000370-2024005) IR 05000369/20244042024-08-0101 August 2024 Cover Letter Security Baseline Inspection Report 05000369/2024404 and 05000370/2024404 IR 05000369/20253012024-07-29029 July 2024 Notification of Licensed Operator Initial Examination 05000369/2025301 and 05000370/2025301 IR 05000369/20244032024-07-25025 July 2024 – Cyber Security Inspection Report 05000369/2024403 and 05000370/2024403 Rev IR 05000369/20240022024-07-24024 July 2024 Integrated Inspection Report 05000369/2024002 and 05000370/2024002 ML24183A0972024-07-12012 July 2024 ISFSI; Catawba 1, 2 & ISFSI; McGuire 1, 2 & ISFSI; Oconee 1, 2, 3 & ISFSI; Shearon Harris 1; H. B. Robinson 2 & ISFSI; and Radioactive Package Shipping Under 10 CFR 71 (71-266 & 71-345) – Review of QA Program Changes EPID L-2024-LLQ-0002 IR 05000369/20244012024-07-0303 July 2024 – Security Baseline Inspection Report 05000369/2024401 and 05000370/2024401 ML24176A2802024-06-26026 June 2024 Notification of Target Set Inspection and Request for Information (NRC Inspection Report 05000369-2024404 and 05000370-2024404) IR 05000369/20240112024-06-0404 June 2024 Biennial Problem Identification and Resolution Inspection Report 05000369/2024011 and 05000370/2024011 ML24149A1772024-05-28028 May 2024 NRC Response to Duke Energy 2025 FOF Schedule Change Request (Catawba and McGuire) IR 05000369/20240012024-05-0808 May 2024 Integrated Inspection Report 05000369-2024001 and 05000370-2024001 and 07200038-2024001 ML24110A0382024-04-30030 April 2024 – Correction to Issuance of Amendment Nos. 330 and 309, Regarding Implementation of Technical Specifications Task Force (TSTF) Traveler TSTF 505, Revision 2, Provide Risk-Informed Extended Completion Times - Ritstf ML24100A8742024-04-10010 April 2024 Information Request for the Cybersecurity Baseline Inspection, Notification to Perform Inspection 05000369/2024403; and 05000370/2024403 ML24052A3062024-04-0808 April 2024 Issuance of Amendment Nos. 331 & 310, Regarding Adoption of Title 10 of Code of Federal Regulations Section 50.69, Risk-Informed Categorization and Treatment of Structures, Systems and Components for Nuclear Power Plants ML24031A5402024-03-26026 March 2024 Issuance of Amendment Nos. 330 and 309 Regarding Implementation of TSTF 505,Rev. 2, Provide Risk-Informed Extended Completion Times - RITSTF Initiative 4B ML24085A2402024-03-21021 March 2024 Requalification Program Inspection - McGuire Nuclear Station IR 05000369/20240102024-03-13013 March 2024 Comprehensive Engineering Team Inspection Report 05000369/2024010 and 05000370/2024010 IR 05000369/20230062024-02-28028 February 2024 Annual Assessment Letter for McGuire Nuclear Station, Units 1 and 2 - NRC Inspection Report 05000369/2023006 and 05000370/2023006 ML24024A2182024-02-0505 February 2024 Exemption from Select Requirements of 10 CFR Part 73 (Security Notifications, Reports, and Recordkeeping and Suspicious Activity Reporting) IR 05000369/20230042024-01-31031 January 2024 Integrated Inspection Report 05000369/2023004 and 05000370/2023004 ML24019A1392024-01-25025 January 2024 TSTF 505 and 50.69 Audit Summary ML24019A2002024-01-24024 January 2024 Notification of Inspection and Request for Information for NRC Problem Identification and Resolution Inspection IR 05000369/20234022023-12-14014 December 2023 – Material Control and Accounting Program Inspection Report 05000369/2023402 and 05000370/2023402 ML23317A2272023-11-17017 November 2023 William B. McGuire Nuclear Station, Units 1 and 2 - Transmittal of Dam Inspection Report - Non-Proprietary ML23317A3462023-11-14014 November 2023 Duke Fleet - Correction Letter to License Amendment Nos. 312 & 340 Issuance of Amendments Regarding the Adoption of Technical Specifications Task Force Traveler TSTF-554, Revision 1 IR 05000369/20230032023-10-24024 October 2023 Integrated Inspection Report 05000369/2023003 and 05000370/2023003; and Inspection Report 07200038/2023001 IR 05000369/20230102023-10-13013 October 2023 Age Related Degradation Inspection Report 05000369/2023010 and 05000370/2023010 ML23256A0882023-09-25025 September 2023 Issuance of Alternative to Steam Generator Welds IR 05000369/20233012023-09-20020 September 2023 William B. McGuire Nuclear Station - NRC Examination Report 05000369/2023301 and 05000370/2023301 ML23230A0652023-08-31031 August 2023 William B. McGuire Nuclear Station, Units 1 and 2 - Relief Request Use of Later Edition of ASME Code ML23195A0782023-08-29029 August 2023 Issuance of Amendments Regarding the Adoption of Technical Specifications Task Force Traveler TSTF-554, Revision 1 IR 05000369/20230052023-08-25025 August 2023 Updated Inspection Plan for McGuire Nuclear Station Units 1 and 2 (Report 05000369/2023005 and 05000370/2023005) IR 05000369/20230022023-07-28028 July 2023 Integrated Inspection Report 05000369/2023002 and 05000370/2023002 IR 05000369/20234202023-07-24024 July 2023 Security Baseline Inspection Report 050003692023420 and 050003702023420 ML23206A0092023-07-24024 July 2023 William B. McGuire Nuclear Station Operator Licensing Written Examination Approval 05000369/2023301 and 05000370/2023301 ML23207A0762023-07-14014 July 2023 EN 56557 - Update to Part 21 Report Re Potential Defect with Trane External Auto/Stop Emergency Stop Relay Card Pn: XI2650728-06 ML23159A2712023-06-20020 June 2023 William B. McGuire Nuclear Station, Unit 1 - Relief Request Impractical Reactor System Welds ML23237A2672023-06-13013 June 2023 June 13, 2002 - Meeting Announcement - McGuire and Catawba Nuclear Stations 50-369, 50-370 and 50-413, 50-414 ML23159A0052023-06-0505 June 2023 56557-EN 56557 - Paragon - Redlined ML23115A2122023-05-0101 May 2023 Review of the Spring 2022 Steam Generator Tube Inspection Report ML23118A0762023-05-0101 May 2023 Approval for Use of Specific Provision of a Later Edition of the American Society of Mechanical Engineers Boiler and Pressure Vessel Code, Section XI IR 05000369/20230012023-05-0101 May 2023 Integrated Inspection Report 05000369/2023001 and 05000370/2023001 ML23094A1832023-04-18018 April 2023 Audit Plan TSTF-505, Rev. 2, RITSTF Initiative 4B & 10 CFR 50.69, Risk-Informed Categorization & Treatment of Structures, Systems & Components for Nuclear Power Reactors (EPIDs L-2023-LLA-0021 & L-2023-LLA-0022) ML22332A4932023-03-10010 March 2023 William States Lee III 1 and 2 - Issuance of Amendments Regarding the Relocation of the Emergency Operations Facility IR 05000369/20220062023-03-0101 March 2023 Annual Assessment Letter for McGuire Nuclear Station Units 1 and 2 (NRC Inspection Report 05000369/2022006 and 05000370 2022006) IR 05000369/20220042023-01-30030 January 2023 Mcguire Nuclear Station - Integrated Inspection Report 05000369/2022004 and 05000370/2022004 IR 05000369/20224202023-01-11011 January 2023 Security Baseline Inspection Report 05000369/2022420 and 05000370/2022420 ML22356A0512022-12-14014 December 2022 Curtiss-Wright Nuclear Division, Letter Regarding Potential Efect in a Configuration of the 11/2 Inch Quick Disconnect Connector Cable Assemblies Supplied to Duke Energy (See Attached Spreadsheet) for a Total of 460 of Connectors Only Suppl ML22347A1512022-12-13013 December 2022 William B. Mcguire Nuclear Station Notification of Licensed Operator Initial Examination 05000369/2023301 and 05000370/2023301 2024-08-26
[Table view] Category:Request for Additional Information (RAI)
MONTHYEARML24197A1702024-07-15015 July 2024 Request for Additional Information Two Proposed Alternatives (RA-23-0242) for the Inspection of Reactor Vessel Closure Head Penetrations ML23151A3482023-05-30030 May 2023 Duke Fleet - Request for Additional Information Proposed Alternative for Pressurizer Welds in Accordance with 10 CFR 50.55a(z)(1) ML23142A2732023-05-22022 May 2023 Duke Fleet - Request for Additional Information Proposed Alternative for Steam Generator Welds in Accordance with 10 CFR 50.55a(z)(1) ML23030B9032023-01-30030 January 2023 Formal Release of RAIs for McGuire Unit 1, Relief Request Impractical RPV Rx Coolant System Welds, Due March 1, 2023 (Email) ML23017A2232023-01-13013 January 2023 Request for Additional Information (RAI) Issuance for McGuire Unit 1 Steam Generator Tube Inspection Report (Email) ML22175A0162022-06-24024 June 2022 Notification of Inspection and Request for Information for NRC Problem Identification and Resolution Inspection ML22115A1412022-04-25025 April 2022 NRR E-mail Capture - Duke Common EOF Relocation - Request for Addition Information ML22102A2962022-04-13013 April 2022 Request for Withholding Information from Public Disclosure Response to Request for Additional Information ML22063B1782022-03-0909 March 2022 Request for Additional Information Regarding LAR for Revision to the Conditional Exemption of the End of Cycle Moderator Temperature Coefficient Measurement Methodology (EPID L-2021-LLA-0198) NON-PROPRIETARY ML22010A0732022-01-0606 January 2022 50.59 Inspection Information Request ML21354A8612021-12-15015 December 2021 NRR E-mail Capture - Request for Additional Information - Duke Fleet Request RA-19-0352 - Alternative for RPV Closure Stud Exams (L-2020-LLR-0156) ML21267A2782021-09-23023 September 2021 50.59 Inspection Information Request ML21252A0532021-09-0808 September 2021 NRR E-mail Capture - Formal Release of Rais, 30 Day Response, Mcguire Relief Request, Ref: Later Edition Addenda ASME Code, Section XI, 50.55a(g)(4)(iv) ML21103A0542021-04-13013 April 2021 NRR E-mail Capture - Extension to Request for Additional Information AMS Topical Report AMS-TR-0720R1 ML21067A6742021-03-0505 March 2021 NRR E-mail Capture - Final Request for Additional Information AMS Topical Report AMS-TR-0720R1 ML21049A2632021-02-0404 February 2021 NRR E-mail Capture - Request for Additional Information - Duke Energy Fleet License Amendment Request to Revise Emergency Plan ML21020A0682021-01-20020 January 2021 Notification of an NRC Fire Protection Team Inspection (FPTI) (NRC Inspection Report 05000369/2021011 and 05000370/2021011) and Request for Information (RFI) ML20346A0212020-12-10010 December 2020 NRR E-mail Capture - Formal Release of RAIs - License Amendment to Change TS 3.8.1 Due Jan. 29, 2021 ML20323A4072020-11-18018 November 2020 NRR E-mail Capture - Request for Additional Information - Brunswick License Exemption Request from 10CFR73 Annual Force on Force Exercise Requirements (EPIC L-2020-LLE-0180) ML20216A3512020-08-0303 August 2020 Mcquire U-1 ISI RFI ML20101L3132020-04-10010 April 2020 Notification of Inspection and Request for Information ML20071D0962020-03-0505 March 2020 NRR E-mail Capture - Request for Additional Information - McGuire Nuclear Station Unit 1 Delay in Update of the Code of Record for in Service Inspections ML20050D3382020-02-21021 February 2020 Letter RAI 1 MAGNASTOR-Catawba and McGuire Exemptions with Enclosure ML19354B6372020-01-0707 January 2020 Exemption Request for NAC Magnastor Cask Loaded to Incorrect Helium Backfill Density Request for Additional Information ML19011A1372019-01-10010 January 2019 NRR E-mail Capture - Duke Energy Fleet RAIs - Relief Request 18-GO-001 - Proposed Alternative for Depth Sizing Qualification Examination of Welds (L-2018-LLR-0117) ML19007A3422018-12-21021 December 2018 NRR E-mail Capture - Duke Energy Fleet Draft RAIs - Relief Request 18-GO-001 - Proposed Alternative for Depth Sizing Qualification Examination of Welds (L-2018-LLR-0117) ML18352A8052018-12-18018 December 2018 NRR E-mail Capture - Request for Additional Information - McGuire Nuclear Station, Units 1 and 2 - MRP-227 Review ML18306A9372018-11-0202 November 2018 NRR E-mail Capture - Request for Additional Information - McGuire Nuclear Station, Units 1 and 2 - Esps LAR ML18285A0812018-10-11011 October 2018 NRR E-mail Capture - Request for Additional Information - McGuire Nuclear Station, Units 1 and 2 - TORMIS LAR RA-18-0011, Response to Request for Supplemental Information Regarding Duke Energy'S Response to GL 2016-01 Monitoring of Neutron-Absorbing Materials in Spent Fuel Pools2018-05-30030 May 2018 Response to Request for Supplemental Information Regarding Duke Energy'S Response to GL 2016-01 Monitoring of Neutron-Absorbing Materials in Spent Fuel Pools ML18138A4662018-05-18018 May 2018 NRR E-mail Capture - Request for Additional Information - McGuire Nuclear Station, Units 1 and 2 - TORMIS LAR ML18088B2822018-03-29029 March 2018 Requalification Program Inspection - McGuire Nuclear Station ML18057A2182018-02-23023 February 2018 Enclosurequest for Additional Information (Letter to A. Zaremba Request for Additional Information for Review of Duke Energy'S Decommissioning Funding Plan Update) ML17331B1492017-11-21021 November 2017 NRR E-mail Capture - Request for Additional Information - McGuire Nuclear Station, Units 1 and 2 - Nsws One-Time LAR (CACs MG0242 and MG0243, EPID L-2017-LLA-0299) ML17317B0932017-11-13013 November 2017 NRR E-mail Capture - Request for Additional Information - McGuire Nuclear Station, Units 1 and 2 - Irlt (CACs MF9020 and MF9021; EPID L-2016-LLA-0032) ML17230A1512017-08-15015 August 2017 Notification of Inspection of Inspection and Request for Information ML17192A4842017-07-11011 July 2017 NRR E-mail Capture - Duke Energy Fleet RAIs Alternative for Reactor Pressure Vessel Flange Threads Examination (MF9513 to MF9521) ML17135A0322017-05-12012 May 2017 NRR E-mail Capture - Request for Additional Information - McGuire TSTF-197 ML17114A4992017-04-17017 April 2017 Emergency Preparedness Inspection and Request for Information ML16302A1122016-11-0404 November 2016 Request for Additional Information Regarding License Amendment Request to Implement a Risk-Informed, Performance-Based Fire Protection Program (CAC Nos. MF2934 and MF2935) MNS-16-077, Responding to Request for Additional Information Related to License Amendment Request to Implement a Risk-informed Performance-Based Fire Protection Program2016-09-29029 September 2016 Responding to Request for Additional Information Related to License Amendment Request to Implement a Risk-informed Performance-Based Fire Protection Program ML16228A2612016-08-15015 August 2016 Email - McGuire Unit No. 1: Request for Additional Informati- Relief Request 16-MN-003 Alternative to Defect Removal Prior to Performing Temporary Repair Activities on Three-Inch-Diameter Nuclear Service Water System Piping. ML16194A2862016-07-12012 July 2016 E-Mail - Mcguirai Ice Condenser Door Position Alternate Verification, (ML16089A228) CAC Nos. MF7526 and MF7527 ML16175A0222016-07-12012 July 2016 Request for Additional Information Regarding License Amendment Request to Implement a Risk-Informed, Performance-Based Fire Protection Program ML16014A6882016-01-20020 January 2016 Request for Additional Information Regarding License Amendment Request to Revise Emergency Action Level Scheme ML15348A2602015-12-17017 December 2015 Request for Additional Information Regarding License Amendment Request to Use an Alternative Fission Gas Gap Release Fraction ML15320A3862015-11-19019 November 2015 RAI LAR to Adopt TSTF-523 ML15314A3592015-11-10010 November 2015 Duke Energy Draft RAIs Request to Adopt TSTF-523 (CAC Nos. MF6413-MF6422) ML15314A3562015-11-10010 November 2015 E-mail from J. Whited to A. Zaremba Duke Energy Draft RAIs License Amendment Request to Adopt TSTF-523 (CAC Nos. MF6413-MF6422) ML15289A5552015-10-26026 October 2015 Request for Additional Information Regarding License Amendment Request Nuclear Service Water System Allowed Outage Time Extension 2024-07-15
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UNITED STATES NUCLEAR REGULATORY COMMISSION WASHINGTON, D.C. 20555-0001 Mr. Steven D. Capps Vice* President . McGuire Nuclear Station Duke Energy Carolinas, LLC 12700 Hagers Ferry Road Huntersville, NC 28078-8985 September 14, 2015
SUBJECT:
MCGUIRE NUCLEAR STATION, UNITS 1AND2: REQUEST FOR ADDITIONAL INFORMATION REGARDING LICENSE AMENDMENT REQUEST NUCLEAR SERVICE WATER SYSTEM ALLOWED OUTAGE TIME . EXTENSION (TAC NOS. MF2983 AND MF2984)
Dear Mr. Capps:
By letter dated June 30, 2015 (Agencywide Documents Access and Management System (ADAMS) Accession No. ML 15191A025), Duke Energy Carolinas, LLC (the licensee) submitted
- a license amendment request, which requested to modify selected Technical Specification Completion Times to support repair activity associated with the Nuclear Service Water System, Train 'A'. The U.S. Nudear Regulatory Commission staff has reviewed the licensee's submittal and determined that additional information is needed in order to complete our review. The enclosed document describes this request for additional information (RAI). On September 4, 2014, the Duke staff indicated that a response to the RAI would be provided within 30 days. If you have any questions, please .call me at 301-415-2481. Docket Nos. 50-369 and 50-370
Enclosure:
Request for Additional Information cc w/encl: Distribution via Listserv G. Edward Miller, Project Manager Plant Licensing Branch 11-1 Division of Operating Reactor Licensing Office of Nuclear Reactor Regulation REQUEST FOR ADDITIONAL INFORMATION MCGUIRE NUCLEAR STATION, UNITS 1 AND 2 RELATED TO A LICENSE AMENDMENT REQUEST SUPPORTING CORRECTION OF A NUCLEAR SERVICE WATER SYSTEM DEGRADED CONDITION DUKE ENERGY CAROLINAS, LLC DOCKET NOS. 50-369 AND 50-370 By letter dated June 30, 2015 (Agencywide Documents Access and Management System (ADAMS) Accession No. ML 15191A025), Duke Energy Carolinas, LLC (Duke Energy) submitted a license amendment request (LAR) to temporarily change McGuire Nuclear Station (MNS), Units 1 and 2, Technical Specifications (TSs) for correction of a degraded condition affecting the 'A' Train of the nuclear service water system (NSWS). The requested amendment would temporarily change the following TSs to allow the inoperability of the 'A' Train of the NSWS for a total of up to 14 days: TS 3.5.2, Emergency Core Cooling System (ECCS) -Operating; TS 3.6.6, Containment Spray System (CSS); TS 3.7.5, Auxiliary Feedwater (AFW) System; TS 3.7.6, Component Cooling Water (CCW) System; TS 3.7.7, Nuclear Service Water System (NSWS); TS 3.7.9, Control Room Area Ventilation System (CRAVS); TS 3.7.11, Auxiliary Building Filtered Ventilation Exhaust System (ABFVES), and TS 3.8.1, AC Operating. The 'A' Train of the shared NSWS would be inoperable while the safety-related supply from the MNS Nuclear Service Water Pond was drained and isolated to correct a degraded condition affecting that line. Based on its review of this amendment request, the NRC staff has determined the following additional information is necessary to support completion of its technical review: SCVB-RAl-001 The license amendment focuses on the temporary alignments and changes requested for the NSWS, however, these changes impact other systems. For the CSS, CRAVS, and the ABFVES: a. Explain the available capabilities of the above systems during the time when the requested temporary TSs would be enacted. b. Discuss the impact of any deviations from standard alignment and operation of the systems. Enclosure SRXB-RAl-001 While the approach taken in the proposed LAR is a qualitative risk approach, please address the need to preclude potentially high-risk plant configurations that could result if additional
- equipment, not associated with the proposed change, is taken out-of-service during the proposed Allowed Outage Time (AOT) extension. Provide a justification to limiting the prohibition of discretionary maintenance to the following systems: a. 1A EOG; b. 2A EOG; c. The 'A' Train of NSWS excluding the activities described in the LAR for the 'A' Train NSWS piping to the SNSWP; d. The 'B' Train of NSWS, ECCS, CSS, AFW, CCW, CRAVS, ABFVES or the EOGs; e. The switchyard and other offsite power sources; and f. The SSF. Specifically, provide a justification for not implementing a broader limitation on discretionary maintenance (e.g., such as that of the cited STPNOC precedent (ML050100291 ), "STPNOC will not perform any planned voluntary maintenance in Unit 1 during the extended AOT (EAOT) that would increase the ICCDP. '?. -SRXB-RAl-002 The LAR lists the following equipment to be protected during the AOT extension of the 'A' train of NSWS: a. 'B' Train NSWS b. 18 EOG c. 28 EOG. d. 18 ECCS. e. 28 ECCS f. 18 css g. 28 css h. 1BAFW i. 2BAFW j. 18 ccw k. 28 ccw I. B CRAVS m. BABFVES n. Auxiliary Building WZ Sump and equipment supporting function of sump Provide a discussion on the criteria used to determine the protected equipment. Include a justification for not including the turbine driven AFW pump, Containment Ventilation Cooling Water (RV) system and the Standby Shutdown Facility (SSF) standby makeup pump, which appear to be important to managing the risk of the proposed AOT extension. SRXB-RAl-003 Clarify whether any maintenance will be allowed on the 'A' Train NSWS that would impact the ability of the system to operate taking suction from the Lake Norman Low Level Intake (LU) (even if these activities are within the 72 completion time) during the period that the Standby Nuclear Service Water Pond (SNSWP) suction is not available for the 'A' train of NSWS. Specifically, address what is meant by the following statement .in section 3.5 of the LAR: 2. Any maintenance that is on the remaining portions of the 'A' Train NSWS during the period in which the 'A' NSWS piping from the SNSWP is not available will be limited to a 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> completion time.
Mr. Steven D. Capps Vice President McGuire Nuclear Station Duke Energy Carolinas, LLC 12700 Hagers Ferry Road Huntersville, NC 28078-8985 September 14, 2015
SUBJECT:
MCGUIRE NUCLEAR STATION, UNITS 1 AND 2: REQUEST FOR ADDITIONAL INFORMATION REGARDING LICENSE AMENDMENT REQUEST NUCLEAR SERVICE WATER SYSTEM ALLOWED OUTAGE TIME EXTENSION (TAC NOS. MF2983 AND MF2984)
Dear Mr. Capps:
By letter dated June 30, 2015 (Agencywide Documents Access and System (ADAMS) Accession No. ML 15191A025), Duke Energy Carolinas, LLC (the licensee) submitted a license amendment request, which requested to modify selected Technical Specification Completion Times to support repair activity associated with the Nuclear Service Water System, Train 'A'. The U.S. Nuclear Regulatory Commission staff has reviewed the licensee's submittal and determined that additional information is needed in order to complete our review. The enclosed document describes this request for additional information (RAI). On September 4, 2014, the Duke staff indicated that a response to the RAI would be provided within 30 days. If you have any questions, please call me at 301-415-2481. / Docket Nos. 50-369 and 50-370
Enclosure:
Request for Additional Information cc w/encl: Distribution via Listserv DISTRIBUTION: PUBLIC RidsAcrsAcnw _MailCTR Resource RidsNrrDeEicb Resource RidsNrrLASFigueroa Resource ADAMS Accession No. ML 15252A276 OFFICE NRR/LPL2-1 /PM N NAME GEMiller SFigueroa LPL2-1 R/F Sincerely, /RA/ G. Edward Miller, Project Manager Plant Licensing Branch 11-1 Division of Operating Reactor Licensing Office of Nuclear Reactor Regulation RidsNrrDorllpl2-1 Resource RidsNrrPMMcGuire Resource (hard copy) RidsRgn2MailCenter Resource *Via E-mail S/SRXB/BC NRR/DSS/SCVB/B NRR/LPL2-1/BC RDennig RPascarelli DATE 09/14/15 09/14/15 08/28/15 08/27/15 09/14/15 OFFICIAL RECORD