ML17262B056: Difference between revisions
StriderTol (talk | contribs) (Created page by program invented by StriderTol) |
StriderTol (talk | contribs) (Created page by program invented by StriderTol) |
||
Line 19: | Line 19: | ||
=Text= | =Text= | ||
{{#Wiki_filter:ROCHESTERGASANDELECTRICCORPORATIONe89EASTAVENUE,'ROCHESTERN.Y.14649.0001ROBERTCMECREOYVicePresidentclnnaNuclearproductionSeptember30,1992TELEPHONEnstEa,cooETis546-2700U.S.NuclearRegulatoryCommissionDocumentControlDeskAttn:AllenR.JohnsonPWRProjectDirectorateI-3Washington,D.C.20555Subject:StatusofActionsinResponsetoSWSOPXViolations,Deficiencies,andUnresolvedItemsXnspectionReport50-244/91-201R.E.GinnaNuclearPowerPlantDocketNo.50-244DearMr.Johnson,InReference(a)RG&Ecommitted,bytheendofthethirdquarter1992,toprovideanupdatedstatusofRG&EactionstakenorplannedirnresponsetotheitemsidentifiedinAppendixAofReference(b).AppendixAofReference(b)identifiedatotalof15items;4wereidentifiedasDeficiencies,5wereidentifiedasUnresolveditems,and6wereidentifiedasObservations.Three,of.theseresultedinViolationsasdocumentedinReference(c).Since.theissuanceofReference(b)andthesubsequentNoticeofViolations,Reference(c),RG&EhasexpendedasignificantefforttowardresolutionoftheopenissuesidentifiedduringtheSWSOPITeamXnspection.AsacknowledgedbytheNRCinReference(c),allidentifieditems,weaknesses,andobservationsrelatedtotheSWSOPI'rebeingtrackedinourCommitmentandActionTrackingSystemto.assureformalresolutionofthesematters.Sincethecompletionoftheteaminspection,RG&Ehasbeentrackingtheprogressof62COmrtlitmentSOiaCticnitesssSreSultingdireCtjfrOmtaheSWSOPXOrrelatedtoit.Currently,35ofthesehavebeenclosedbyRG&Eand27remainopenin,variousstagesofcompletion.Inaddition,duringtheweekofAugust17,1992,NRCstaffperformedafollow-upinspectionduringwhichRG&EprovidedinformationandstatusofRG&Eactionsforthethreeviolations(91-201Ž01,91-201-11,and91-201-14)andtwooftheunresolveditems(91-201-04and91-201-15).SinceNRCdocumentationoftheresultsof.thatinspection(designated50-244/92-012)hasnotasyet,beenreceived,thisletterprovidesthestatusofallthe15deficiencies,unresolveditems,andobservationsidentifiedinAppendixAofReference(a).('Tt210210045921016PDRADOCK050002448,'PDR | {{#Wiki_filter:ROCHESTERGASANDELECTRICCORPORATIONe89EASTAVENUE,'ROCHESTERN.Y.14649.0001ROBERTCMECREOYVicePresidentclnnaNuclearproductionSeptember30,1992TELEPHONEnstEa,cooETis546-2700U.S.NuclearRegulatoryCommissionDocumentControlDeskAttn:AllenR.JohnsonPWRProjectDirectorateI-3Washington,D.C.20555Subject:StatusofActionsinResponsetoSWSOPXViolations,Deficiencies,andUnresolvedItemsXnspectionReport50-244/91-201R.E.GinnaNuclearPowerPlantDocketNo.50-244DearMr.Johnson,InReference(a)RG&Ecommitted,bytheendofthethirdquarter1992,toprovideanupdatedstatusofRG&EactionstakenorplannedirnresponsetotheitemsidentifiedinAppendixAofReference(b).AppendixAofReference(b)identifiedatotalof15items;4wereidentifiedasDeficiencies,5wereidentifiedasUnresolveditems,and6wereidentifiedasObservations.Three,of.theseresultedinViolationsasdocumentedinReference(c).Since.theissuanceofReference(b)andthesubsequentNoticeofViolations,Reference(c),RG&EhasexpendedasignificantefforttowardresolutionoftheopenissuesidentifiedduringtheSWSOPITeamXnspection.AsacknowledgedbytheNRCinReference(c),allidentifieditems,weaknesses,andobservationsrelatedtotheSWSOPI'rebeingtrackedinourCommitmentandActionTrackingSystemto.assureformalresolutionofthesematters.Sincethecompletionoftheteaminspection,RG&Ehasbeentrackingtheprogressof62COmrtlitmentSOiaCticnitesssSreSultingdireCtjfrOmtaheSWSOPXOrrelatedtoit.Currently,35ofthesehavebeenclosedbyRG&Eand27remainopenin,variousstagesofcompletion.Inaddition,duringtheweekofAugust17,1992,NRCstaffperformedafollow-upinspectionduringwhichRG&EprovidedinformationandstatusofRG&Eactionsforthethreeviolations(91-201Ž01,91-201-11,and91-201-14)andtwooftheunresolveditems(91-201-04and91-201-15).SinceNRCdocumentationoftheresultsof.thatinspection(designated50-244/92-012)hasnotasyet,beenreceived,thisletterprovidesthestatusofallthe15deficiencies,unresolveditems,andobservationsidentifiedinAppendixAofReference(a).('Tt210210045921016PDRADOCK050002448,'PDR | ||
ATTACHMENTAInresponseRG&Ecommittedto1)evaluate/test,thedieselgeneratorcoolerperformanceanddeterminetheoptimumflow[R01958];2)enhancetheanalyticalmodelingandcapabilityoftheexistinghydraulicmodelsothatananalyticalbasisandtestspecificationforthere-balanceoftheSWSisavailablepriortothe1993refuelingoutage[R01959];and3)conducttestingasrequiredduringthe1993outagetoconfirmtheanalyticalresultsoftheenhancedmodelandtosetoptimalflows"foreachSWcoolersothat.theSWSflowbalancewillbeoptimizedwhentheplantreturnstopowerfollowing"the1993outage.[R01960]Inalett~~,Reference,(d),RG&Eindicatedthattheexistingservicewaters'st:emflowbalancetotheemergencydieselgeneratorcoolerswassatisfactoryandthatnochangewaswarrantedatthistime,however,theoverallSWSflowbalancecontinues;.tobeplannedforthe1993outage.Inaddition,byReference(e)RG&Ecommittedtoperformpilotthermalperformancetestingofthedieselgeneratorcoolersduringthesummerof1992basedupontheexistingsysteminstrumentation[R02438],evaluatetheseresults[R02440],andcommenceperiodicthermalperformancetestingduringthesummerof1993tocoincidewiththehighestlakewatertemperatures[R02439].The'pilottestinghasbeencompletedandtheresultsarebeingreviewedbyengineeringandplantstaff.Page-7 | ATTACHMENTAInresponseRG&Ecommittedto1)evaluate/test,thedieselgeneratorcoolerperformanceanddeterminetheoptimumflow[R01958];2)enhancetheanalyticalmodelingandcapabilityoftheexistinghydraulicmodelsothatananalyticalbasisandtestspecificationforthere-balanceoftheSWSisavailablepriortothe1993refuelingoutage[R01959];and3)conducttestingasrequiredduringthe1993outagetoconfirmtheanalyticalresultsoftheenhancedmodelandtosetoptimalflows"foreachSWcoolersothat.theSWSflowbalancewillbeoptimizedwhentheplantreturnstopowerfollowing"the1993outage.[R01960]Inalett~~,Reference,(d),RG&Eindicatedthattheexistingservicewaters'st:emflowbalancetotheemergencydieselgeneratorcoolerswassatisfactoryandthatnochangewaswarrantedatthistime,however,theoverallSWSflowbalancecontinues;.tobeplannedforthe1993outage.Inaddition,byReference(e)RG&Ecommittedtoperformpilotthermalperformancetestingofthedieselgeneratorcoolersduringthesummerof1992basedupontheexistingsysteminstrumentation[R02438],evaluatetheseresults[R02440],andcommenceperiodicthermalperformancetestingduringthesummerof1993tocoincidewiththehighestlakewatertemperatures[R02439].The'pilottestinghasbeencompletedandtheresultsarebeingreviewedbyengineeringandplantstaff.Page-7 | ||
}} | }} |
Revision as of 13:38, 18 May 2018
ML17262B056 | |
Person / Time | |
---|---|
Site: | Ginna |
Issue date: | 09/30/1992 |
From: | ROCHESTER GAS & ELECTRIC CORP. |
To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM), Office of Nuclear Reactor Regulation |
Shared Package | |
ML17262B055 | List: |
References | |
NUDOCS 9210210045 | |
Download: ML17262B056 (2) | |
See also: IR 05000244/1991201
Text
ROCHESTERGASANDELECTRICCORPORATIONe89EASTAVENUE,'ROCHESTERN.Y.14649.0001ROBERTCMECREOYVicePresidentclnnaNuclearproductionSeptember30,1992TELEPHONEnstEa,cooETis546-2700U.S.NuclearRegulatoryCommissionDocumentControlDeskAttn:AllenR.JohnsonPWRProjectDirectorateI-3Washington,D.C.20555Subject:StatusofActionsinResponsetoSWSOPXViolations,Deficiencies,andUnresolvedItemsXnspectionReport50-244/91-201R.E.GinnaNuclearPowerPlantDocketNo.50-244DearMr.Johnson,InReference(a)RG&Ecommitted,bytheendofthethirdquarter1992,toprovideanupdatedstatusofRG&EactionstakenorplannedirnresponsetotheitemsidentifiedinAppendixAofReference(b).AppendixAofReference(b)identifiedatotalof15items;4wereidentifiedasDeficiencies,5wereidentifiedasUnresolveditems,and6wereidentifiedasObservations.Three,of.theseresultedinViolationsasdocumentedinReference(c).Since.theissuanceofReference(b)andthesubsequentNoticeofViolations,Reference(c),RG&EhasexpendedasignificantefforttowardresolutionoftheopenissuesidentifiedduringtheSWSOPITeamXnspection.AsacknowledgedbytheNRCinReference(c),allidentifieditems,weaknesses,andobservationsrelatedtotheSWSOPI'rebeingtrackedinourCommitmentandActionTrackingSystemto.assureformalresolutionofthesematters.Sincethecompletionoftheteaminspection,RG&Ehasbeentrackingtheprogressof62COmrtlitmentSOiaCticnitesssSreSultingdireCtjfrOmtaheSWSOPXOrrelatedtoit.Currently,35ofthesehavebeenclosedbyRG&Eand27remainopenin,variousstagesofcompletion.Inaddition,duringtheweekofAugust17,1992,NRCstaffperformedafollow-upinspectionduringwhichRG&EprovidedinformationandstatusofRG&Eactionsforthethreeviolations(91-201Ž01,91-201-11,and91-201-14)andtwooftheunresolveditems(91-201-04and91-201-15).SinceNRCdocumentationoftheresultsof.thatinspection(designated50-244/92-012)hasnotasyet,beenreceived,thisletterprovidesthestatusofallthe15deficiencies,unresolveditems,andobservationsidentifiedinAppendixAofReference(a).('Tt210210045921016PDRADOCK050002448,'PDR
ATTACHMENTAInresponseRG&Ecommittedto1)evaluate/test,thedieselgeneratorcoolerperformanceanddeterminetheoptimumflow[R01958];2)enhancetheanalyticalmodelingandcapabilityoftheexistinghydraulicmodelsothatananalyticalbasisandtestspecificationforthere-balanceoftheSWSisavailablepriortothe1993refuelingoutage[R01959];and3)conducttestingasrequiredduringthe1993outagetoconfirmtheanalyticalresultsoftheenhancedmodelandtosetoptimalflows"foreachSWcoolersothat.theSWSflowbalancewillbeoptimizedwhentheplantreturnstopowerfollowing"the1993outage.[R01960]Inalett~~,Reference,(d),RG&Eindicatedthattheexistingservicewaters'st:emflowbalancetotheemergencydieselgeneratorcoolerswassatisfactoryandthatnochangewaswarrantedatthistime,however,theoverallSWSflowbalancecontinues;.tobeplannedforthe1993outage.Inaddition,byReference(e)RG&Ecommittedtoperformpilotthermalperformancetestingofthedieselgeneratorcoolersduringthesummerof1992basedupontheexistingsysteminstrumentation[R02438],evaluatetheseresults[R02440],andcommenceperiodicthermalperformancetestingduringthesummerof1993tocoincidewiththehighestlakewatertemperatures[R02439].The'pilottestinghasbeencompletedandtheresultsarebeingreviewedbyengineeringandplantstaff.Page-7