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| ==DearMr.O'ReillyIThislettertransmitsthesubjectreportwhichsupplementsPLA-71,== | | ==DearMr.O'ReillyIThislettertransmitsthesubjectreportwhichsupplementsPLA-71,== |
| 1datedJuly25,1975andisintendedtocompletePPKL'sresponsibilityinreportingthedeficienciesinfabricatedstructuralsteelmembers(BoxColumnSupports)whichhad'beenlocatedinpositionforinstalla-tioninSusquehannaUnit18c2structures.Asindicatedintheattachedreport,thedecisionhas'beenmadetoredesignthestructuresand,toreplacealleightunits,includingthosefoundnottocontaindefects.Thereplacementunitsemploymaterialchangesandweld)ointconfigurationsvhichvillfacilitatefabricationandshouldprecludetherecurrenceofthelamellartearingphenomenonexperiencedinoriginalunits.XnadditiontothosecorrectivemeasuresidentifiedinPLA-74andtheattachedBechteldetailed.report,,PPkLhasconcurredinanincreaseinBechtelsurveillanceactivitiesatthevendor'sfabricationfacility(BeMhlehemSteelCompany'sPottstown,PAplant,).Additionally,receivingandpreinstallationactivitiesattheSSESsitewillbealignedtoperformafinalvisualexaminationbeforethenewunitsarepermanentlycommittedtotheplantstructure.Weawaityouradviceshouldyouhaveanyfurtherquestionsorconcernsonthismatter.VerytrulyyoursN.W.CurtisVicePresident-Engineering5ConstructionCJQQQARS:bPENNSYLVANIAPOWER8LIGHTCOMPANY 0)J/ | | 1datedJuly25,1975andisintendedtocompletePPKL'sresponsibilityinreportingthedeficienciesinfabricatedstructuralsteelmembers(BoxColumnSupports)whichhad'beenlocatedinpositionforinstalla-tioninSusquehannaUnit18c2structures.Asindicatedintheattachedreport,thedecisionhas'beenmadetoredesignthestructuresand,toreplacealleightunits,includingthosefoundnottocontaindefects.Thereplacementunitsemploymaterialchangesandweld)ointconfigurationsvhichvillfacilitatefabricationandshouldprecludetherecurrenceofthelamellartearingphenomenonexperiencedinoriginalunits.XnadditiontothosecorrectivemeasuresidentifiedinPLA-74andtheattachedBechteldetailed.report,,PPkLhasconcurredinanincreaseinBechtelsurveillanceactivitiesatthevendor'sfabricationfacility(BeMhlehemSteelCompany'sPottstown,PAplant,).Additionally,receivingandpreinstallationactivitiesattheSSESsitewillbealignedtoperformafinalvisualexaminationbeforethenewunitsarepermanentlycommittedtotheplantstructure.Weawaityouradviceshouldyouhaveanyfurtherquestionsorconcernsonthismatter.VerytrulyyoursN.W.CurtisVicePresident-Engineering5ConstructionCJQQQARS:bPENNSYLVANIAPOWER8LIGHTCOMPANY 0)J/}} |
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Revision as of 01:18, 18 May 2018
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Category:Deficiency Correspondence (per 10CFR50.55e and Part 21)
MONTHYEARML24302A2772024-10-28028 October 2024 57243-EN 57243_5 - Rssc Dba Marmon - Update 20241030 ML17223A1982017-07-21021 July 2017 Part 21 Notification - Eaton/Cutler Hammer A200 Series Starter PLA-7613, Interim Report of a Deviation, Units 1 & 2 - (PLA-7613)2017-06-0909 June 2017 Interim Report of a Deviation, Units 1 & 2 - (PLA-7613) ML17081A4532017-03-20020 March 2017 Part 21 - Plastic Jar Dedication Sampling ML16313A0622016-10-18018 October 2016 C&D Technologies, Inc. - 10 CFR Part 21 Evaluation Regarding Terminal Welding Failure in 3DCU-9 Batteries ML14204A7072014-07-23023 July 2014 Completed Evaluation of Part 21 Potentially Reportable Condition Notification: Unseating of Valve Spring on SSPV ML14210A0102014-07-23023 July 2014 Part 21 - Unseating of Valve Spring on Scram Solenoid Pilot Valve ML13165A3422013-06-12012 June 2013 60-Day Interim Report Involving an Evaluation of a Design Change to Magne-Blast Circuit Breakers ML13044A0752013-02-0808 February 2013 Part 21 - Completed Evaluation for Potential Error in Main Steam Line High Flow Calculational Methodology ML12347A3082012-12-12012 December 2012 Part 21 60-Day Interim Report Notification: Error in Main Steam Line High Flow Calculational Methodology ML12319A0122012-09-27027 September 2012 Error in Main Steam Line High Flow Calculational Methodology ML12158A4472012-06-0606 June 2012 Part 21 60-Day Interim Report Notification - Closufailure of CRD Collet Retainer Tube/Outer Tube Weld ML1127000672011-09-26026 September 2011 GE-Hitachi Part 21 Reportable Condition Notification: Failure to Include Seismic Input in Channel-Control Blade Interference Customer Guidance ML11115A0392011-04-14014 April 2011 Notice of Deviation Pursuant to 10 CFR 21, NPKC-7-21A(N) Splice Kit with Possible Compromised Jacket Seal ML1025202192010-09-0303 September 2010 Part 21 - Failure to Include Seismic Input in Reactor Control Blade Customer Guidance ML1018907392010-07-0101 July 2010 Part 21 Report Concerning Failure of Turbine Overspeed Reset Control Valve Diaphragm ML1015305642010-05-28028 May 2010 Part 21 Notification from C & D Technologies, Inc., Post Corrosion on Dcu Batteries ML1009604492010-04-0202 April 2010 Part 21 Report by Tyco Valves and Controls, LP Possible Failure of Solenoid Valves with Dual Function Main Steam Safety Valves ML0934301402009-12-0202 December 2009 10CFR21 Reporting of Defects and Non-Compliance - Engine Systems, Inc. Report No. 1OCFR21-0098, Rev. 0, Amot Thermostatic Valve Element, P/N: 9760X ML0232901622002-11-18018 November 2002 Final Report, Stability Option III: Possible Successive Confirmation Count Resets - Not Reportable ML18024A0581978-09-18018 September 1978 Letter Attaching a Final Report of a Deficiency in Carriage Bolt Fasteners Used on 480 Volt Motor Control Center Bus Splices ML18024A1011978-07-19019 July 1978 Letter Attaching a Report of Defects Discovered During Qualification and Manufacturing of Control Room Systems ML18024A0661978-07-14014 July 1978 Letter Referring to the April 17, 1978 Letter and Regarding an Update of Interim Report of Reportable Deficiency Regarding Potential Transformers on 4.16K Switchgear ML18024A0681978-07-0505 July 1978 Letter Referring to the April 26, 1978 Letter and Advising the Commission That a Definitive Report Will Be Submitted by September 29, 1978 ML18024A0771978-06-23023 June 1978 Letter Referring to the June 22, 1977 Letter and Relating to the Definitive Report, Prepared by Bechtel Power Corp., of a Reportable Deficiency Regarding Unsatisfactory Field Welding and Inspection of Shear Suds ML18024A0691978-05-31031 May 1978 Letter Referring to the December 1, 1977 Letter Providing an Interim Report of a Deficiency in Physical Separation of Electrical Circuits and Advising the Commission That the Definitive Report Will Be Submitted by September ML18024A0711978-04-26026 April 1978 Letter Attaching Bechtel Engineering'S Interim Report on Spot Welding of Struts for SSES Units 1 and 2 and Advising the Commission That the Definitive Report Will Be Submitted by July 31, 1978 ML18025A4791976-11-0505 November 1976 Interim Report of Reportable Deficiency Defect in RPV Susquehanna Unit 2 Bottom Head Side Plate ML18025A4901975-08-29029 August 1975 Letter Regarding the Definitive Report of Deficiencies in Box Column Supports Which Supplements PLA-74 ML18025A4921975-04-0404 April 1975 Letter Attaching an Interim Report on Potential Deficiency Which Was Discussed with Mr. Heishman on March 6, 1975 2024-10-28
[Table view] Category:Letter
MONTHYEARML24289A1252024-10-22022 October 2024 – Authorized Alternative to Requirements of the ASME OM Code PLA-8145, Biennial 10 CFR 50.59 and 72.48 Summary Report and Changes to Regulatory Commitments - PLA-81452024-10-21021 October 2024 Biennial 10 CFR 50.59 and 72.48 Summary Report and Changes to Regulatory Commitments - PLA-8145 ML24291A1562024-10-16016 October 2024 Missed Annual Inventory Required by 40 CFR 266, Subpart in PLE 0026645 PLA-8148, Registration for the Use of Spent Fuel Storage Casks 311, 308, and 3102024-10-15015 October 2024 Registration for the Use of Spent Fuel Storage Casks 311, 308, and 310 PLA-8141, Response to Request for Additional Information Regarding Relief Request 1RR06, PLA-81412024-09-18018 September 2024 Response to Request for Additional Information Regarding Relief Request 1RR06, PLA-8141 PLA-8142, Registration for the Use of Spent Fuel Storage Casks 306, 309, and 307 - PLA-81422024-09-18018 September 2024 Registration for the Use of Spent Fuel Storage Casks 306, 309, and 307 - PLA-8142 ML24260A2312024-09-17017 September 2024 Senior Reactor and Reactor Operator Initial License Examinations 05000387/LER-2024-002, B Diesel Generator Inoperable Due to Failed Excitation System Linear Reactor2024-09-16016 September 2024 B Diesel Generator Inoperable Due to Failed Excitation System Linear Reactor ML24255A8642024-09-0606 September 2024 Rscc Wire & Cable LLC Dba Marmon Industrial Energy & Infrastructure - Part 21 Retraction of Final Notification ML24249A1362024-09-0404 September 2024 EN 57304 - Westinghouse Electric Company, LLC, Final Report - No Embedded Files. Notification of the Potential Existence of Defects Pursuant to 10 CFR Part 21 ML24233A2192024-09-0303 September 2024 – Authorized Alternative to Requirements of the American Society of Mechanical Engineers Boiler and Pressure Vessel Code IR 05000387/20240052024-08-29029 August 2024 Updated Inspection Plan for Susquehanna Steam Electric Station, Units 1 and 2 (Report 05000387/2024005 and 05000388/2024005) 05000387/LER-2023-004-01, Manual Reactor Scram Due to Degraded Main Condenser Vacuum2024-08-26026 August 2024 Manual Reactor Scram Due to Degraded Main Condenser Vacuum 05000387/LER-2024-001-01, Main Steam Isolation Valve Leakage Due to Valve Body Seat Wear2024-08-21021 August 2024 Main Steam Isolation Valve Leakage Due to Valve Body Seat Wear IR 05000387/20240022024-08-12012 August 2024 Integrated Inspection Report 05000387/2024002 and 05000388/2024002 ML24208A0962024-07-25025 July 2024 57243-EN 57243 - Rssc Wire & Cable LLC, Dba Marmon - Part 21 Notification PLA-8117, 23rd Refueling Outage Owners Activity Report (PLA-8117)2024-07-23023 July 2024 23rd Refueling Outage Owners Activity Report (PLA-8117) ML24197A0982024-07-15015 July 2024 Request for Information for a Biennial Problem Identification and Resolution Inspection; Inspection Report 05000387/2024010 and 05000388/2024010 PLA-8126, Response to Request for Confirmation of Information Regarding Relief Request 1RR062024-05-29029 May 2024 Response to Request for Confirmation of Information Regarding Relief Request 1RR06 ML24127A2262024-05-29029 May 2024 Issuance of Amendment Nos. 288 and 272 Adoption of TSTF-563 PLA-8122, Annual Radiological Environmental Operating Report (PLA-8122)2024-05-28028 May 2024 Annual Radiological Environmental Operating Report (PLA-8122) 05000387/LER-2024-001, Main Steam Isolation Valve Leakage2024-05-23023 May 2024 Main Steam Isolation Valve Leakage PLA-8115, Relief Request IRR06 One Time Extension to the Fourth 10-Year Inservice Testing Program Interval (PLA-8115)2024-05-23023 May 2024 Relief Request IRR06 One Time Extension to the Fourth 10-Year Inservice Testing Program Interval (PLA-8115) IR 05000387/20240012024-05-13013 May 2024 Integrated Inspection Report 05000387/2024001 and 05000388/2024001 IR 05000387/20244042024-05-0707 May 2024 Information Request for the Cybersecurity Baseline Inspection, Notification to Perform Inspection 05000387/2024404 and 05000388/2024404 PLA-8095, 2023 Annual Radiological Environmental Operating Report (PLA-8095)2024-04-22022 April 2024 2023 Annual Radiological Environmental Operating Report (PLA-8095) PLA-8094, Radioactive Effluent Release Report and Offsite Dose Calculation Manual PLA-80942024-04-22022 April 2024 Radioactive Effluent Release Report and Offsite Dose Calculation Manual PLA-8094 PLA-8101, Re 2023 Annual Report of Radiation Exposure2024-04-22022 April 2024 Re 2023 Annual Report of Radiation Exposure ML24082A1372024-04-22022 April 2024 Issuance of Amendment Nos. 287 and 271 Adoption of TSTF-568, Revision 2 and Associated Technical Specification Changes PLA-8102, Annual Environmental Operating Report (Nonradiological) PLA-81022024-04-11011 April 2024 Annual Environmental Operating Report (Nonradiological) PLA-8102 PLA-8113, Response to Request for Additional Information Regarding Relief Request 4RR-11 (PLA-8113)2024-04-11011 April 2024 Response to Request for Additional Information Regarding Relief Request 4RR-11 (PLA-8113) PLA-8112, Relief Request 4RR-11 Relief from End of Interval Boundary Leakage Test PLA-81122024-04-0909 April 2024 Relief Request 4RR-11 Relief from End of Interval Boundary Leakage Test PLA-8112 PLA-8110, Submittal of Unit 1 Cycle 24 Core Operating License Report (Pla 8110)2024-04-0404 April 2024 Submittal of Unit 1 Cycle 24 Core Operating License Report (Pla 8110) PLA-8100, Property Insurance Program (PLA-8100)2024-04-0101 April 2024 Property Insurance Program (PLA-8100) ML24092A4022024-04-0101 April 2024 Annual Financial Report (PLA-8098) PLA-8109, Supplement to Request for Exemption from Certain Requirements of 10 CR 72.212 and 10 CFR 72.214 Resulting from Fuel Basket Design Control Compliance (PLA-8109)2024-03-21021 March 2024 Supplement to Request for Exemption from Certain Requirements of 10 CR 72.212 and 10 CFR 72.214 Resulting from Fuel Basket Design Control Compliance (PLA-8109) PLA-8107, Request for Exemption from Certain Requirements of 10 CFR 72.212 and 10 CFR 72.214 Resulting from Fuel Basket Design Control Compliance2024-03-19019 March 2024 Request for Exemption from Certain Requirements of 10 CFR 72.212 and 10 CFR 72.214 Resulting from Fuel Basket Design Control Compliance ML24067A2512024-03-19019 March 2024 Authorized Alternative to Requirements of the ASME Code ML24044A2532024-03-14014 March 2024 Associated Independent Spent Fuel Storage Installation – Exemption from Select Requirements of 10 CFR Part 73 (EPID L-2023-LLE-0077 (Security Notifications, Reports, and Recordkeeping & Suspicious Activity Reporting)) IR 05000387/20240112024-02-29029 February 2024 Commercial Grade Dedication Inspection Report 05000387/2024011 and 05000388/2024011 IR 05000387/20230062024-02-28028 February 2024 Annual Assessment Letter for Susquehanna Steam Electric Station, Units 1 and 2 (Reports 05000387/2023006 and 05000388/2023006) ML24039A1882024-02-27027 February 2024 Issuance of Amendment Nos. 286 and 270 Changes to Technical Specifications for Control Rods ML24037A3072024-02-22022 February 2024 Summary of Regulatory Audit in Support of Relief Request 5RR-02 PLA-8099, Proof of Financial Protection and Guarantee of Payment of Deferred Premiums (PLA-8099)2024-02-13013 February 2024 Proof of Financial Protection and Guarantee of Payment of Deferred Premiums (PLA-8099) IR 05000387/20230042024-02-0707 February 2024 Integrated Inspection Report 05000387/2023004 and 05000388/2023004 05000387/LER-2023-004, Manual Reactor Scram Due to Degraded Main Condenser Vacuum2024-01-0909 January 2024 Manual Reactor Scram Due to Degraded Main Condenser Vacuum PLA-8096, Response to Request for Additional Information Regarding Proposed Relief Request for the Fifth 10-Year Inservice Test Program Interval2024-01-0404 January 2024 Response to Request for Additional Information Regarding Proposed Relief Request for the Fifth 10-Year Inservice Test Program Interval PLA-8077, Emergency Plan Revision 67 (PLA-8077)2023-12-27027 December 2023 Emergency Plan Revision 67 (PLA-8077) IR 05000387/20230102023-12-11011 December 2023 Fire Protection Team Inspection Report 05000387/2023010 and 05000388/2023010 PLA-8088, Request for Exemption from Enhanced Weapons, Firearms Background Checks and Security Event Notifications Implementation (PLA-8088)2023-12-0505 December 2023 Request for Exemption from Enhanced Weapons, Firearms Background Checks and Security Event Notifications Implementation (PLA-8088) 2024-09-06
[Table view] |
Text
NR-ISTRIBUTIONFORPART50DOCTMATERIAL(TEMPORARYFORM)CONTRQLNO:FILE:FROM.PennsylvaniaPower6LigCo.Allentown,PaN.WCurtistDATEOFDOC'ATEREC'DLTRTW5RPTOTHERTO:'rJ,P,O'ei1lyORIGnot..ignedCCOTHERSENTNRCPDRSENTLOCALPDRCLASS//CLASS"'(xxxPROPINFOINPUTNOCYSREC'DDOCKETNO:"0-38aii6888)DESCRIPTION:Ltrnotarized9-3-75~~,.~transthefollowingDistPerH;RushbrookPLANTNAME:Susquehana16c2(15cysenc'1rec'd)I,~i8l)$7~~~Ev.t-tuENCLOSURES:i'I~'i-~ReportOnDeficiencyInBoxColumnforTheSusquehannaNuclearPlantSupportsFORACTION/INFORMATION9-8-75JGBTLER(L)W/CopiesCLARK(L)W/CopiesPARR(L)W/CopiesKNIEL,(L)W/CopiesSCHWENCER(L)W/CopiesSTOLZ(L)W/CopiesVASSALLO(L)W/CopiesPURPLE(L)W/CopiesZIEMANN(L)W/CopiesiDICKER(E)W/CopiesKNIGHTON(E)W/CopiesYOUNGBLOOD(E)W/CopiesBEGAN(E)W/CopiesLEAR(L)W/CopiesSBICSW/CopiesW/(oplesREID(L)W/COPIESINTERNALDISTRIBUTIONDENTON~RIMESR.gAMMILLH.GKASTNERBALLARDP.SPANGLER.RENVIROS.MULLERM.SDICKERS.SKNIGHTONM.SYOUNGBLOODH.SBEGANS.PROJECTLDRLICASSTDIGGS(L)EARIN(L)GOULBOURNE(L)KREUTZER(E)EE(L)U3:iBROOQL)+REED(E)'RVICE(L)HEPPARD(L)LATER(E)MITH(L)TEETS(L)~G.WILLIAMS(E)V,WILSON(L)R.INGRAM(L)'CANHARLESSH.DUEEXTERNALDISTRIBUTIONECHREVIEYifSCHROEOER"MGC,ROOMP-SOBA%IACCARY>~GOSSICK/STAFF~NI'GHTCASEPAWLICKIGIAMBUSSO'HAOBOYDSTELLOMOORE(L)HOUSTON~YOUNG(L)M~NOVAKSKOVHOLT(L)ROSSGOLLER(L)(Ltr)IPPOLITOP.COLIINS~~DESCO+~~DENISEJ.COLLINS~GOPRAAPItLAIHASFILESiREGION(2IBENAROYAMIPCVOLLMER.1A/TIND~BRAITMANSALTZMANMELTZPLANSMCDONALDCHAPMANDUBE(Ltr)E.COUPEPETERSONHARTFIELD.(2)KLECKEREISENHUTWIGGINTON~~1-1-1-LOCALPDRWilksBarre,PaTIC(ABERNATHY)(1)(2)(10)-NATIONALLABSNSIC(BUCHANAN)1-W.PENNINGTON,RmE-20'IGTASLB1-CONSULTANlSNewtonAndersonNEWMARK/0LUME/AGBADIANACRS.ENTfo1-PDR-SAN/LA/NY1-BROOKI1AVENNATLAB1-G.ULBII<SONORNL
~lf TWONORTHNINTHSTREET,ALLENTOWN,PA.18101PHONEMEt215)8215151August29,1975'rCj.-,&W<).WQ'/(0<YiMr.Z.P.O'ReillyDirector-RegionISUSQUEHANNASDEFINITIVEREPORTOFDEFICIENCIESIN<BOXCOLUMNSUPPORTSDOCKETNOS.:50-387and50-388LICENSENOS.:CPPR-101andCPPR-102ERs100450/100508FILE840-4PLA-82U.S.NuclearRegulatoryCommission931ParkAvenueKingofPrussia,Pennsylvania19406~i<<,,";~gjTEAMELECTRXCSTATIONi/'re,+>>
DearMr.O'ReillyIThislettertransmitsthesubjectreportwhichsupplementsPLA-71,
1datedJuly25,1975andisintendedtocompletePPKL'sresponsibilityinreportingthedeficienciesinfabricatedstructuralsteelmembers(BoxColumnSupports)whichhad'beenlocatedinpositionforinstalla-tioninSusquehannaUnit18c2structures.Asindicatedintheattachedreport,thedecisionhas'beenmadetoredesignthestructuresand,toreplacealleightunits,includingthosefoundnottocontaindefects.Thereplacementunitsemploymaterialchangesandweld)ointconfigurationsvhichvillfacilitatefabricationandshouldprecludetherecurrenceofthelamellartearingphenomenonexperiencedinoriginalunits.XnadditiontothosecorrectivemeasuresidentifiedinPLA-74andtheattachedBechteldetailed.report,,PPkLhasconcurredinanincreaseinBechtelsurveillanceactivitiesatthevendor'sfabricationfacility(BeMhlehemSteelCompany'sPottstown,PAplant,).Additionally,receivingandpreinstallationactivitiesattheSSESsitewillbealignedtoperformafinalvisualexaminationbeforethenewunitsarepermanentlycommittedtotheplantstructure.Weawaityouradviceshouldyouhaveanyfurtherquestionsorconcernsonthismatter.VerytrulyyoursN.W.CurtisVicePresident-Engineering5ConstructionCJQQQARS:bPENNSYLVANIAPOWER8LIGHTCOMPANY 0)J/