IR 05000387/2018003: Difference between revisions

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| issue date = 11/08/2018
| issue date = 11/08/2018
| title = Integrated Inspection Report 05000387/2018003 and 05000388/2018003
| title = Integrated Inspection Report 05000387/2018003 and 05000388/2018003
| author name = Greives J E
| author name = Greives J
| author affiliation = NRC/RGN-I/DRP/PB4
| author affiliation = NRC/RGN-I/DRP/PB4
| addressee name = Berryman B
| addressee name = Berryman B
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| docket = 05000387, 05000388
| docket = 05000387, 05000388
| license number = NPF-014, NPF-022
| license number = NPF-014, NPF-022
| contact person = Greives J E
| contact person = Greives J
| document report number = IR 2018003
| document report number = IR 2018003
| document type = Inspection Report, Letter
| document type = Inspection Report, Letter
Line 18: Line 18:


=Text=
=Text=
{{#Wiki_filter:
{{#Wiki_filter:November 8, 2018
[[Issue date::November 8, 2018]]


Mr. Brad Berryman President and Chief Nuclear Officer Susquehanna Nuclear, LLC 769 Salem Blvd., NUCSB3
==SUBJECT:==
 
SUSQUEHANNA STEAM ELECTRIC STATION - INTEGRATED INSPECTION REPORT 05000387/2018003 AND 05000388/2018003
Berwick, PA 18603
 
SUBJECT: SUSQUEHANNA STEAM ELECTRIC STATION - INTEGRATED INSPECTION REPORT 05000387/2018003 AND 05000388/2018003


==Dear Mr. Berryman:==
==Dear Mr. Berryman:==
Line 32: Line 28:
The NRC inspectors did not identify any findings or violations of more than minor significance.
The NRC inspectors did not identify any findings or violations of more than minor significance.


This letter, its enclosure, and your response (if any) will be made available for public inspection  
This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations (10 CFR), Part 2.390, Public Inspections, Exemptions, Requests for Withholding.


and copying at http://www.nrc.gov/reading-rm/adams.html and the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations (10 CFR), Part 2.390, "Public Inspections, Exemptions, Requests for Withholding."
Sincerely,
/RA/  


Sincerely,/RA/ Jonathan E. Greives, Chief Reactor Projects Branch 4  
Jonathan E. Greives, Chief Reactor Projects Branch 4 Division of Reactor Projects


Division of Reactor Projects Docket Numbers: 50-387 and 50-388 License Numbers: NPF-14 and NPF-22  
Docket Numbers: 50-387 and 50-388 License Numbers: NPF-14 and NPF-22  


===Enclosure:===
===Enclosure:===
Inspection Report 05000387/2018003 and 05000388/2018003  
Inspection Report 05000387/2018003 and 05000388/2018003  


cc w/encl: Distribution via ListServ
==Inspection Report==
Docket Numbers:
50-387 and 50-388
 
License Numbers:
NPF-14 and NPF-22


ML18313A025 SUNSI Review Non-Sensitive Sensitive Publicly Available Non-Publicly Available OFFICE RI/DRP RI/DRP RI/DRP NAME LMicewski via email SBarber JGreives DATE 11/8/18 11/7/18 11/8/18
Report Numbers:
05000387/2018003 and 05000388/2018003


1 Enclosure U.S. NUCLEAR REGULATORY COMMISSION Inspection Report
Enterprise Identifier: I-2018-003-0069


Docket Numbers: 50-387 and 50-388 License Numbers: NPF-14 and NPF-22
Licensee:
Susquehanna Nuclear, LLC (Susquehanna)


Report Numbers: 05000387/2018003 and 05000388/2018003
Facility:
Susquehanna Steam Electric Station, Units 1 and 2


Enterprise Identifier: I-2018-003-0069
Location:
Berwick, Pennsylvania


Licensee: Susquehanna Nuclear, LLC (Susquehanna)
Inspection Dates:
July 1, 2018 to September 30, 2018


Facility: Susquehanna Steam Electric Station, Units 1 and 2
Inspectors:  


Location: Berwick, Pennsylvania
L. Micewski, Senior Resident Inspector


Inspection Dates: July 1, 2018 to September 30, 2018
T. Daun, Resident Inspector
N. Floyd, Senior Reactor Inspector
M. Orr, Reactor Inspector
J. Furia, Senior Health Physicist


Inspectors: L. Micewski, Senior Resident Inspector T. Daun, Resident Inspector N. Floyd, Senior Reactor Inspector M. Orr, Reactor Inspector J. Furia, Senior Health Physicist
Approved By:
Jonathan E. Greives, Chief


Approved By: Jonathan E. Greives, Chief Reactor Projects Branch 4 Division of Reactor Projects
Reactor Projects Branch 4  


2
Division of Reactor Projects


=SUMMARY=
=SUMMARY=
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring Susquehanna's performance at Susquehanna Steam Electric Station, Units 1 and 2 by conducting the baseline inspections described in this report in accordance with the Reactor Oversight Process. The  
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring Susquehannas performance at Susquehanna Steam Electric Station, Units 1 and 2 by conducting the baseline inspections described in this report in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.
 
Reactor Oversight Process is the NRC's program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.


No findings or more-than-minor violations were identified.
No findings or more-than-minor violations were identified.


Additional Tracking Items Type Issue number Title Inspection Results Section Status LER 05000388;387/2016-006-00 Loss of Secondary Containment Due to Damper Controller Sticking 71153 Closed LER 05000388;387/2017-005-00 Secondary Containment Declared Inoperable Due to Trip of Zone III Filtered  
===Additional Tracking Items===
 
Type Issue number Title Inspection Results Section Status LER 05000388;387/2016-006-00 Loss of Secondary Containment Due to Damper Controller Sticking 71153 Closed LER 05000388;387/2017-005-00 Secondary Containment Declared Inoperable Due to Trip of Zone III Filtered Exhaust Fan 71153 Closed LER 05000388;387/2017-006-00 Secondary Containment Declared Inoperable Due to Trip of Zone II Exhaust Fan 71153 Closed
Exhaust Fan 71153 Closed LER 05000388;387/2017-006-00 Secondary Containment Declared Inoperable Due to Trip of Zone II Exhaust Fan 71153 Closed  
 
3


=PLANT STATUS=
=PLANT STATUS=
Line 89: Line 95:


==INSPECTION SCOPES==
==INSPECTION SCOPES==
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, "Light-Water Reactor Inspection Program - Operations Phase.The inspectors performed plant status activities described in IMC 2515, Appendix D, "Plant Status," and conducted routine reviews using IP 71152, "Problem Identification and Resolution.The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess Susquehanna's performance and compliance with Commission rules and regulations, license conditions, site procedures, and  
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515, Appendix D, Plant Status, and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess Susquehannas performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.
 
standards.


==REACTOR SAFETY==
==REACTOR SAFETY==
==71111.01 - Adverse Weather Protection==
==71111.01 - Adverse Weather Protection==
 
===External Flooding (1 Sample)===
External Flooding (1 Sample)
The inspectors evaluated readiness to cope with external flooding.
The inspectors evaluated readiness to cope with external flooding.


==71111.04 - Equipment Alignment==
==71111.04 - Equipment Alignment==
 
===Partial Walkdown (3 Samples)===
Partial Walkdown (3 Samples)
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:
: (1) Unit 1, division 2 core spray during work on a division 1 'C' core spray room cooler on July 2, 2018
: (1) Unit 1, division 2 core spray during work on a division 1 C core spray room cooler on July 2, 2018
: (2) Unit 1, division 2 residual heat removal (RHR) during 'A' RHR system outage window on August 8, 2018
: (2) Unit 1, division 2 residual heat removal (RHR) during A RHR system outage window on August 8, 2018
: (3) Unit 2, division 2 RHR service water (RHRSW) during work on division 1 RHRSW pump discharge valves on September 11, 2018 Complete Walkdown (1 Sample)
: (3) Unit 2, division 2 RHR service water (RHRSW) during work on division 1 RHRSW pump discharge valves on September 11, 2018  


The inspectors evaluated system configurations during a complete walkdown of the Unit Common, 'E' emergency diesel generator (EDG) and support systems following 5 year diesel overhaul.
===Complete Walkdown (1 Sample)===
The inspectors evaluated system configurations during a complete walkdown of the Unit Common, E emergency diesel generator (EDG) and support systems following 5 year diesel overhaul.


==71111.05A/Q - Fire Protection Annual/Quarterly==
==71111.05A/Q - Fire Protection Annual/Quarterly==
===Quarterly Inspection (5 Samples)===
The inspectors evaluated fire protection program implementation in the following selected areas:
: (1) Unit Common, A EDG (fire zone 0-41A) on July 16, 2018
: (2) Unit 2, A RHR pump room (fire zone 2-1F) on September 12, 2018
: (3) Unit 1, A core spray pump room (fire zone 1-1A) on September 14, 2018
: (4) Unit Common, C EDG (fire zone 0-41C) on September 26, 2018
: (5) Unit Common, engineered safeguard service water pump house (fire zones 0-51 and 0-52) on September 27, 2018


Quarterly Inspection (5 Samples)
===Annual Inspection (1 Sample)===
 
The inspectors evaluated fire protection program implementation in the following selected
 
areas:
: (1) Unit Common, 'A' EDG (fire zone 0-41A) on July 16, 2018
: (2) Unit 2, 'A' RHR pump room (fire zone 2-1F) on September 12, 2018
: (3) Unit 1, 'A' core spray pump room (fire zone 1-1A) on September 14, 2018
: (4) Unit Common, 'C' EDG (fire zone 0-41C) on September 26, 2018
: (5) Unit Common, engineered safeguard service water pump house (fire zones 0-51 and 0-52) on September 27, 2018 Annual Inspection (1 Sample)  
 
The inspectors evaluated fire brigade performance on August 16, 2018.
The inspectors evaluated fire brigade performance on August 16, 2018.


==71111.07 - Heat Sink Performance==
==71111.07 - Heat Sink Performance==
 
===Heat Sink (1 Sample)===
Heat Sink (1 Sample)  
The inspectors evaluated Susquehannas monitoring and maintenance of Unit Common E EDG lube oil cooler performance.
 
The inspectors evaluated Susquehanna's monitoring and maintenance of Unit Common 'E' EDG lube oil cooler performance.


==71111.11 - Licensed Operator Requalification Program and Licensed Operator Performance==
==71111.11 - Licensed Operator Requalification Program and Licensed Operator Performance==
 
===Operator Requalification (1 Sample)===
Operator Requalification (1 Sample)  
 
The inspectors observed and evaluated licensed operator simulator training, which included a loss of all instrument air, a small break loss of coolant accident, trip of the high pressure coolant injection pump due to loss of lubrication oil cooling, and the failure of select components to automatically start as required on August 13, 2018.
The inspectors observed and evaluated licensed operator simulator training, which included a loss of all instrument air, a small break loss of coolant accident, trip of the high pressure coolant injection pump due to loss of lubrication oil cooling, and the failure of select components to automatically start as required on August 13, 2018.


Operator Performance (1 Sample)
===Operator Performance (1 Sample)===
The inspectors observed reactivity manipulations to reduce power to approximately 63 percent, and a subsequent rod sequence exchange at Unit 1 on August 3 and 4, 2018. The inspectors also observed reactor shutdown activities for a planned maintenance outage at Unit 1 on August 18, 2018.
The inspectors observed reactivity manipulations to reduce power to approximately 63 percent, and a subsequent rod sequence exchange at Unit 1 on August 3 and 4, 2018. The inspectors also observed reactor shutdown activities for a planned maintenance outage at Unit 1 on August 18, 2018.


==71111.12 - Maintenance Effectiveness==
==71111.12 - Maintenance Effectiveness==
 
===Routine Maintenance Effectiveness (2 Samples)===
Routine Maintenance Effectiveness (2 Samples)
The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:
The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:
: (1) Unit Common, scram discharge volume vent and drain valve stroke timing and coordination
: (1) Unit Common, scram discharge volume vent and drain valve stroke timing and coordination
Line 152: Line 146:
The inspectors evaluated the risk assessments for the following planned and emergent work activities:
The inspectors evaluated the risk assessments for the following planned and emergent work activities:
: (1) Unit 1, emergent work control associated with half scram resulting from failure of K14A reactor protection system (RPS) relay on July 18, 2018
: (1) Unit 1, emergent work control associated with half scram resulting from failure of K14A reactor protection system (RPS) relay on July 18, 2018
: (2) Unit 2, 'D' RHR pump protected during 'B' RHR pump maintenance on July 31, 2018
: (2) Unit 2, D RHR pump protected during B RHR pump maintenance on July 31, 2018
: (3) Unit 1, 'A' reactor recirculation pump #2 seal failure on August 7, 2018
: (3) Unit 1, A reactor recirculation pump #2 seal failure on August 7, 2018
: (4) Unit 1, risk management activities during 'A' standby liquid control pressure sensing valve replacement on September 28, 2018
: (4) Unit 1, risk management activities during A standby liquid control pressure sensing valve replacement on September 28, 2018


==71111.15 - Operability Determinations and Functionality Assessments==
==71111.15 - Operability Determinations and Functionality Assessments==
Line 162: Line 156:
: (1) Unit 2, failure of relay 44A in 4kV bus 2C prevented 2C RHR and 2C core spray pumps from starting on July 24, 2018
: (1) Unit 2, failure of relay 44A in 4kV bus 2C prevented 2C RHR and 2C core spray pumps from starting on July 24, 2018
: (2) Unit Common, control structure chillers following T-20 electrical transient on July 30, 2018
: (2) Unit Common, control structure chillers following T-20 electrical transient on July 30, 2018
: (3) Unit Common, ESW through wall leak in Unit 1 reactor core isolation cooling (RCIC) room on August 28, 2018
: (3) Unit Common, ESW through wall leak in Unit 1 reactor core isolation cooling (RCIC)room on August 28, 2018
: (4) Unit 1, ladder stored adjacent to RCIC division 2 isolation panel on August 29, 2018
: (4) Unit 1, ladder stored adjacent to RCIC division 2 isolation panel on August 29, 2018
: (5) Unit Common, water leaking from conduit into engineered safeguard service water pump house basement on September 25, 2018  
: (5) Unit Common, water leaking from conduit into engineered safeguard service water pump house basement on September 25, 2018  


71111.17T - Evaluations of Changes, Tests, and Experiments (25 Samples)
===71111.17T - Evaluations of Changes, Tests, and Experiments===
{{IP sample|IP=IP 71111.17|count=25}}
 
The inspectors evaluated the following changes which were implemented from August 2015 to August 2018:  
The inspectors evaluated the following changes which were implemented from August 2015 to August 2018:  


10 CFR 50.59 Evaluations
10 CFR 50.59 Evaluations
: (1) SE 00028, Unit 1 and 2 Online Noble Chemistry System Installation, Revision 0
: (1) SE 00028, Unit 1 and 2 Online Noble Chemistry System Installation, Revision 0
: (2) SE 00015, Vent Effluent Radiation Monitoring System Replacement, Revision 0 10 CFR 50.59 Screening/Applicability Determinations
: (2) SE 00015, Vent Effluent Radiation Monitoring System Replacement, Revision 0  
 
10 CFR 50.59 Screening/Applicability Determinations
: (1) SD 01381, EC 1684212, Control Structure Chiller Time Delay Control Changes, Revision 1
: (1) SD 01381, EC 1684212, Control Structure Chiller Time Delay Control Changes, Revision 1
: (2) SD 01502, EC 1544685, Install Higher Head Pumps in Place of Fire Pumps 0P511, 0P512, and 0P592, Revision 8
: (2) SD 01502, EC 1544685, Install Higher Head Pumps in Place of Fire Pumps 0P511, 0P512, and 0P592, Revision 8
Line 182: Line 180:
: (9) SD 01786, EC 1805589, Remove CIG Compressor Inlet Check Valves, Revision 0
: (9) SD 01786, EC 1805589, Remove CIG Compressor Inlet Check Valves, Revision 0
: (10) SD 01793, Removal of LIS25348 per PCWO 1935310 greater than 90 days at power, Revision 0
: (10) SD 01793, Removal of LIS25348 per PCWO 1935310 greater than 90 days at power, Revision 0
: (11) SD 01795, ZWO 1959855, Compensatory Meas ure for 'A' CST Heat Trace Inoperable, Revision 0
: (11) SD 01795, ZWO 1959855, Compensatory Measure for A CST Heat Trace Inoperable, Revision 0
: (12) SD 01819, Change Shutdown Cooling Startup Sequence to Crack Open F017 Valves Prior to Starting Residual Heat Removal Pump, Revision 0
: (12) SD 01819, Change Shutdown Cooling Startup Sequence to Crack Open F017 Valves Prior to Starting Residual Heat Removal Pump, Revision 0
: (13) SD 01828, LDCN 5269, Isolation of ESW from 'E' DG Fuel Oil Heat Exchanger 0E526E, Revision 0
: (13) SD 01828, LDCN 5269, Isolation of ESW from E DG Fuel Oil Heat Exchanger 0E526E, Revision 0
: (14) SD 01840, Temporary Alteration Applied Under PCWO 1912777 in Place Greater than 90 Days, Revision 0
: (14) SD 01840, Temporary Alteration Applied Under PCWO 1912777 in Place Greater than 90 Days, Revision 0
: (15) SD 01871, EC 1948468, Repair of Service Water Lines Using External Composite Pipe Wrap Material, Revision 0
: (15) SD 01871, EC 1948468, Repair of Service Water Lines Using External Composite Pipe Wrap Material, Revision 0
Line 200: Line 198:


The inspectors evaluated post maintenance testing for the following maintenance/repair activities:
The inspectors evaluated post maintenance testing for the following maintenance/repair activities:
: (1) Unit 1, 'C' core spray room cooler following relay replacement on July 2, 2018
: (1) Unit 1, C core spray room cooler following relay replacement on July 2, 2018
: (2) Unit 1, replacement of auxiliary contact kit on K14A RPS relay on July 18, 2018
: (2) Unit 1, replacement of auxiliary contact kit on K14A RPS relay on July 18, 2018
: (3) Unit Common, 'C' ESW pump following lift check maintenance on July 23, 2018
: (3) Unit Common, C ESW pump following lift check maintenance on July 23, 2018
: (4) Unit Common, 'D' EDG following mechanical governor replacement on August 2, 2018
: (4) Unit Common, D EDG following mechanical governor replacement on August 2, 2018
: (5) Unit Common, 'E' EDG following overhaul, on August 17, 2018
: (5) Unit Common, E EDG following overhaul, on August 17, 2018
: (6) Unit 1, 'A' reactor recirculation pump following seal replacement on September 14, 2018
: (6) Unit 1, A reactor recirculation pump following seal replacement on September 14, 2018


==71111.20 - Refueling and Other Outage Activities==
==71111.20 - Refueling and Other Outage Activities==
Line 213: Line 211:


==71111.22 - Surveillance Testing==
==71111.22 - Surveillance Testing==
The inspectors evaluated the following surveillance tests:


The inspectors evaluated the following surveillance tests:
===Inservice===
Inservice (2 Samples)
{{IP sample|IP=IP 71111.22|count=2}}
: (1) Unit 1, Division 1 core spray valve exercising on July 3, 2018
: (1) Unit 1, Division 1 core spray valve exercising on July 3, 2018
: (2) Unit Common, 'C' ESW pump inservice test re-baseline on September 19, 2018 Reactor Coolant System Leak Detection (1 Sample)
: (2) Unit Common, C ESW pump inservice test re-baseline on September 19, 2018  
: (1) Unit 1, unidentified/identified leakage calculations following seal failure, on August 16, 2018
 
===Reactor Coolant System Leak Detection (1 Sample)===
: (1) Unit 1, unidentified/identified leakage calculations following seal failure, on August 16, 2018


==71114.06 - Drill Evaluation==
==71114.06 - Drill Evaluation==
 
===Emergency Planning Drill (1 Sample)===
Emergency Planning Drill (1 Sample)  
The inspectors evaluated the emergency director, dose assessment personnel, and communicators emergency preparedness implementation during three tabletop training exercises between July 19, 2018 and August 2, 2018. The inspectors observed three different emergency response organization crews responding to a scenario that involved a loss of offsite power and a simulated radiological release due to fuel cladding damage.
 
The inspectors evaluated the emergency director, dose assessment personnel, and communicators' emergency preparedness implementation during three tabletop training exercises between July 19, 2018 and August 2, 2018. The inspectors observed three different emergency response organization crews responding to a scenario that involved a loss of offsite power and a simulated radiological release due to fuel cladding damage.


==RADIATION SAFETY==
==RADIATION SAFETY==
==71124.06 - Radioactive Gaseous and Liquid Effluent Treatment==
==71124.06 - Radioactive Gaseous and Liquid Effluent Treatment==
 
===Walkdowns and Observations (1 sample)===
Walkdowns and Observations (1 sample)
The inspectors walked down the gaseous and liquid radioactive effluent monitoring and filtered ventilation systems to assess the material condition and verify proper alignment according to plant design.
The inspectors walked down the gaseous and liquid radioactive effluent monitoring and filtered ventilation systems to assess the material condition and verify proper alignment according to plant design.


Calibration and Testing Program (1 sample)
===Calibration and Testing Program (1 sample)===
The inspectors reviewed gaseous and liquid effluent monitor instrument calibration, functional test results, and alarm set-points based on National Institute of Standards and Technology calibration traceability and offsite dose calculation manual (ODCM)specifications.
The inspectors reviewed gaseous and liquid effluent monitor instrument calibration, functional test results, and alarm set-points based on National Institute of Standards and Technology calibration traceability and offsite dose calculation manual (ODCM)specifications.


Sampling and Analyses (1 sample) The inspectors reviewed radioactive effluent sampling activities, representative sampling requirements, compensatory measures taken during effluent discharges with inoperable effluent radiation monitoring instrumentation, the use of compensatory radioactive effluent sampling, and the results of the inter-laboratory and intra-laboratory comparison program including scaling of hard-to-detect isotopes.
===Sampling and Analyses (1 sample)===
The inspectors reviewed radioactive effluent sampling activities, representative sampling requirements, compensatory measures taken during effluent discharges with inoperable effluent radiation monitoring instrumentation, the use of compensatory radioactive effluent sampling, and the results of the inter-laboratory and intra-laboratory comparison program including scaling of hard-to-detect isotopes.


Instrumentation and Equipment (1 sample) The inspectors reviewed the methodology used to determine the radioactive effluent stack and vent flow rates to verify that the flow rates were consistent with technical specification/ODCM and updated final safety analysis report values. The inspectors reviewed radioactive effluent discharge system surveillance test results based on technical specification acceptance criteria.
===Instrumentation and Equipment (1 sample)===
The inspectors reviewed the methodology used to determine the radioactive effluent stack and vent flow rates to verify that the flow rates were consistent with technical specification/ODCM and updated final safety analysis report values. The inspectors reviewed radioactive effluent discharge system surveillance test results based on technical specification acceptance criteria.


Dose Calculations (1 sample) The inspectors reviewed changes in reported dose values from the previous annual radioactive effluent release reports, several liquid and gaseous radioactive waste discharge permits, the scaling method for hard-to-detect radionuclides, ODCM changes, land use census changes, public dose calculations (monthly, quarterly, annual), and records of abnormal gaseous or liquid radioactive releases.
===Dose Calculations (1 sample)===
The inspectors reviewed changes in reported dose values from the previous annual radioactive effluent release reports, several liquid and gaseous radioactive waste discharge permits, the scaling method for hard-to-detect radionuclides, ODCM changes, land use census changes, public dose calculations (monthly, quarterly, annual), and records of abnormal gaseous or liquid radioactive releases.


==71124.08 - Radioactive Solid Waste Processing and Radioactive Material Handling, Storage, and Transportation==
==71124.08 - Radioactive Solid Waste Processing and Radioactive Material Handling, Storage,==
and Transportation  


Radioactive Material Storage (1 sample)
===Radioactive Material Storage===
{{IP sample|IP=IP 71124.08|count=1}}


The inspectors observed radioactive waste container storage areas and verified the postings and controls and that Susquehanna had established a process for monitoring the impact of long-term storage of the waste.
The inspectors observed radioactive waste container storage areas and verified the postings and controls and that Susquehanna had established a process for monitoring the impact of long-term storage of the waste.


Radioactive Waste System Walkdown (1 sample)  
===Radioactive Waste System Walkdown (1 sample)===
 
The inspectors walked down accessible portions of liquid and solid radioactive waste processing systems, abandoned in place radioactive waste processing equipment, and current methods and procedures for dewatering waste.
The inspectors walked down accessible portions of liquid and solid radioactive waste processing systems, abandoned in place radioactive waste processing equipment, and current methods and procedures for dewatering waste.


Waste Characterization and Classification (1 sample)  
===Waste Characterization and Classification (1 sample)===
 
The inspectors identified radioactive waste streams and reviewed radiochemical sample analysis results to support radioactive waste characterization. The inspectors reviewed the use of scaling factors and calculations to account for difficult-to-measure radionuclides.
The inspectors identified radioactive waste streams and reviewed radiochemical sample analysis results to support radioactive waste characterization. The inspectors reviewed the use of scaling factors and calculations to account for difficult-to-measure radionuclides.


Shipment Preparation (1 sample)
===Shipment Preparation (1 sample)===
The inspectors reviewed the records of shipment packaging, surveying, labeling, marking, placarding, vehicle checks, emergency instructions, disposal manifest, shipping papers provided to the driver, and licensee verification of shipment readiness.
The inspectors reviewed the records of shipment packaging, surveying, labeling, marking, placarding, vehicle checks, emergency instructions, disposal manifest, shipping papers provided to the driver, and licensee verification of shipment readiness.


Shipping Records (1 sample)  
===Shipping Records (1 sample)===
 
The inspectors reviewed selected non-excepted package shipment records.
The inspectors reviewed selected non-excepted package shipment records.


==OTHER ACTIVITIES - BASELINE==
==OTHER ACTIVITIES - BASELINE==
71151 - Performance Indicator Verification The inspectors verified Susquehanna's performance indicator submittals listed below (8 Samples)
===71151 - Performance Indicator Verification The inspectors verified Susquehannas performance indicator submittals listed below  
: (1) Unit 1 and Unit 2, MS05 Safety System Functional Failures, July 1, 2017 through June 30, 2018
 
===
{{IP sample|IP=IP 71151|count=8}}
: (1) Unit 1 and Unit 2, MS05 Safety System Functional Failures, July 1, 2017 through June 30, 2018
: (2) Unit 1 and Unit 2, MS06 MSPI Emergency AC Power Systems (EDG), July 1, 2017 through June 30, 2018
: (2) Unit 1 and Unit 2, MS06 MSPI Emergency AC Power Systems (EDG), July 1, 2017 through June 30, 2018
: (3) Unit 1 and Unit 2, MS07 MSPI High Pressure Injection (HPCI), July 1, 2017 through June 30, 2018
: (3) Unit 1 and Unit 2, MS07 MSPI High Pressure Injection (HPCI), July 1, 2017 through June 30, 2018
Line 271: Line 273:


==71152 - Problem Identification and Resolution==
==71152 - Problem Identification and Resolution==
 
===Annual Follow-up of Selected Issues (3 Samples)===
Annual Follow-up of Selected Issues (3 Samples)
The inspectors reviewed the Susquehannas implementation of its corrective action program related to the following issues:
The inspectors reviewed the Susquehanna's implementation of its corrective action program related to the following issues:
: (1) Ineffective risk management actions during emergent work
: (1) Ineffective risk management actions during emergent work
: (2) Unit 2 fuel leaker identified in the 2017 refueling outage
: (2) Unit 2 fuel leaker identified in the 2017 refueling outage
: (3) EDG slow start times 71153 - Follow-up of Events and Notices of Enforcement Discretion Licensee Event Reports (3 Samples)
: (3) EDG slow start times  
 
===71153 - Follow-up of Events and Notices of Enforcement Discretion Licensee Event Reports===
{{IP sample|IP=IP 71153|count=3}}
 
The inspectors evaluated the following licensee event reports (LERs):
The inspectors evaluated the following licensee event reports (LERs):
: (1) LER 05000388;387/2016-006-00, Loss of Secondary Containment Due to Damper Controller Sticking (ADAMS Accession No. ML16323A007). The inspectors determined that it was not reasonable to foresee or correct the cause discussed in the LER therefore no performance deficiency was identified. Thus, the inspectors also concluded that no violation of NRC requirements occurred.
: (1) LER 05000388;387/2016-006-00, Loss of Secondary Containment Due to Damper Controller Sticking (ADAMS Accession No. ML16323A007). The inspectors determined that it was not reasonable to foresee or correct the cause discussed in the LER therefore no performance deficiency was identified. Thus, the inspectors also concluded that no violation of NRC requirements occurred.
: (2) LER 05000388;387/2017-005-00, Secondary Containment Declared Inoperable Due to Trip of Zone III Filtered Exhaust Fan (ADAMS Accession No. ML17230A248). The inspectors determined that it was not reasonable to foresee or correct the cause discussed in the LER therefore no performance deficiency was identified. Thus, the inspectors also concluded that no violation of NRC requirements occurred.
: (2) LER 05000388;387/2017-005-00, Secondary Containment Declared Inoperable Due to Trip of Zone III Filtered Exhaust Fan (ADAMS Accession No. ML17230A248). The inspectors determined that it was not reasonable to foresee or correct the cause discussed in the LER therefore no performance deficiency was identified. Thus, the inspectors also concluded that no violation of NRC requirements occurred.
: (3) LER 05000388;387/2017-006-00, Secondary Containment Declared Inoperable Due to Trip of Zone II Exhaust Fan (ADAMS Accession No. ML17249A538). The inspectors determined that it was not reasonable to foresee or correct the cause discussed in the LER therefore no performance deficiency was identified. Thus, the inspectors also concluded that no violation of NRC requirements occurred.
: (3) LER 05000388;387/2017-006-00, Secondary Containment Declared Inoperable Due to Trip of Zone II Exhaust Fan (ADAMS Accession No. ML17249A538). The inspectors determined that it was not reasonable to foresee or correct the cause discussed in the LER therefore no performance deficiency was identified. Thus, the inspectors also concluded that no violation of NRC requirements occurred.


==OTHER ACTIVITIES==
==OTHER ACTIVITIES==
- TEMPORARY INSTRUCTIONS, INFREQUENT, AND ABNORMAL IP 92709 - Contingency Plans for Licensee Strikes or Lockouts Susquehanna developed a Business Continuity Plan to ensure a sufficient number of qualified personnel were available to continue operations in the event that Local 1600 International Brotherhood of Electrical Workers (IBEW) personal engaged in a job action upon the expiration of their contract on August 26, 2018. Using guidance contained in NRC IP 92709, "Contingency Plants for Licensee Strikes or Lockouts," the inspectors reviewed Susquehanna's plans to address a potential job action at the site. On August 24, 2018, Susquehanna and IBEW, Local 1600, tentatively agreed to a new contract and union members subsequently approved the new contract. No job action was taken.
- TEMPORARY INSTRUCTIONS, INFREQUENT, AND ABNORMAL  
 
IP 92709 - Contingency Plans for Licensee Strikes or Lockouts  
 
Susquehanna developed a Business Continuity Plan to ensure a sufficient number of qualified personnel were available to continue operations in the event that Local 1600 International Brotherhood of Electrical Workers (IBEW) personal engaged in a job action upon the expiration of their contract on August 26, 2018. Using guidance contained in NRC IP 92709, Contingency Plants for Licensee Strikes or Lockouts, the inspectors reviewed Susquehannas plans to address a potential job action at the site. On August 24, 2018, Susquehanna and IBEW, Local 1600, tentatively agreed to a new contract and union members subsequently approved the new contract. No job action was taken.


==INSPECTION RESULTS==
==INSPECTION RESULTS==
Observations 71152 Annual Follow-up of Selected Issues Condition Report CR-2017-17228, Cognitive trend of not effectively utilizing risk mitigation actions during emergent work  
Observations 71152 Annual Follow-up of Selected Issues Condition Report CR-2017-17228, Cognitive trend of not effectively utilizing risk mitigation actions during emergent work  


During 2016 and 2017, several examples of inadequate assessment and management of risk were identified, including an unplanned change to station risk that resulted in a Green non-cited violation (05000387/2017002-02), an inadvertent break of a daisy chained neutral while changing a light socket that resulted in single loop operations and a significant power transient, and an inadvertent electrical short during maintenance that resulted in a reactor scram.
During 2016 and 2017, several examples of inadequate assessment and management of risk were identified, including an unplanned change to station risk that resulted in a Green non-cited violation (05000387/2017002-02), an inadvertent break of a daisy chained neutral while changing a light socket that resulted in single loop operations and a significant power transient, and an inadvertent electrical short during maintenance that resulted in a reactor scram.


Susquehanna performed a cause analysis on the events under CR-2017-17228. In all cases the cause was related to issues with human performance, communications, and not challenging assumptions. Corrective actions taken by Susquehanna included revision of the Emergent Work Checklist and the High Risk Challenge Board procedural guidance to include a requirement to consider the consequences prior to performing work. The station also revised procedure NDAP-QA-1902, "Integrated Risk Management," to add a requirement for development of risk mitigation actions for a Yellow probabilistic risk assessment risk.
Susquehanna performed a cause analysis on the events under CR-2017-17228. In all cases the cause was related to issues with human performance, communications, and not challenging assumptions. Corrective actions taken by Susquehanna included revision of the Emergent Work Checklist and the High Risk Challenge Board procedural guidance to include a requirement to consider the consequences prior to performing work. The station also revised procedure NDAP-QA-1902, Integrated Risk Management, to add a requirement for development of risk mitigation actions for a Yellow probabilistic risk assessment risk.


The inspectors reviewed the technical adequacy and depth of evaluations performed by the licensee for these issues. The inspectors also evaluated the licensee's development and implementation of corrective actions in this area and concluded that they were reasonable.
The inspectors reviewed the technical adequacy and depth of evaluations performed by the licensee for these issues. The inspectors also evaluated the licensees development and implementation of corrective actions in this area and concluded that they were reasonable.


Observations 71152 Annual Follow-up of Selected Issues Condition Report CR-2016-25721, Indications of fuel defect for Unit 2; CR-2017-10852, Debris failure identified for rod in fuel bundle V27452; and CR-2017-13888, Adverse trend of foreign material intrusion into fuel assemblies in Unit 2 reactor In conjunction with Susquehanna's fuel vendor, Susquehanna determined that the most probable cause of the fuel defect identified in fuel bundle V27452 in 2017 was debris fret caused by foreign material.
Observations 71152 Annual Follow-up of Selected Issues Condition Report CR-2016-25721, Indications of fuel defect for Unit 2; CR-2017-10852, Debris failure identified for rod in fuel bundle V27452; and CR-2017-13888, Adverse trend of foreign material intrusion into fuel assemblies in Unit 2 reactor  


Susquehanna conducted a thorough technical review of their foreign material exclusion (FME) program under CR-2017-13888. Susquehanna determined that there was a lack of program ownership for the FME program combined with a lack of oversight by the line organizations in regards to FME controls. Corrective actions included assigning an FME coordinator to fill the vacant role at the station, assign individuals within each line organization to become the FME lead within that organization, and to reinstate monthly FME steering committee meetings.
In conjunction with Susquehannas fuel vendor, Susquehanna determined that the most probable cause of the fuel defect identified in fuel bundle V27452 in 2017 was debris fret caused by foreign material.


The inspectors reviewed the corrective actions and determined Susquehanna's overall response to the issues were commensurate with the safety significance, were timely, and were generally effective. The inspectors noted a high number of FME-related condition reports were generated during the previous refueling outage but acknowledge this is most likely the result of the increased focus and oversight on FME controls.
Susquehanna conducted a thorough technical review of their foreign material exclusion (FME)program under CR-2017-13888. Susquehanna determined that there was a lack of program ownership for the FME program combined with a lack of oversight by the line organizations in regards to FME controls. Corrective actions included assigning an FME coordinator to fill the vacant role at the station, assign individuals within each line organization to become the FME lead within that organization, and to reinstate monthly FME steering committee meetings.
 
The inspectors reviewed the corrective actions and determined Susquehannas overall response to the issues were commensurate with the safety significance, were timely, and were generally effective. The inspectors noted a high number of FME-related condition reports were generated during the previous refueling outage but acknowledge this is most likely the result of the increased focus and oversight on FME controls.


The inspectors reviewed the condition reports and determined they were being entered at an appropriately low threshold and were being addressed commensurate with their safety significance.
The inspectors reviewed the condition reports and determined they were being entered at an appropriately low threshold and were being addressed commensurate with their safety significance.


Observations 71152 Annual Follow-up of Selected Issues Condition Report CR-2017-00530, MRC requested further evaluation on trend "slower than typical DG starts"; CR-2017-11996, A DG start for SO-024-001A 10.1 seconds to frequency The inspectors reviewed corrective action CR-2017-00530, which was initiated by Susquehanna staff on January 6, 2017, to evaluate a trend in slower EDG start times that still met technical specification requirements. Additionally, the inspectors reviewed CR-2017-11996 to evaluate and correct the 'A' EDG not meeting starting time requirements.
Observations 71152 Annual Follow-up of Selected Issues Condition Report CR-2017-00530, MRC requested further evaluation on trend slower than typical DG starts; CR-2017-11996, A DG start for SO-024-001A 10.1 seconds to frequency  


The inspectors' review of CR-2017-00530 determined that Susquehanna engineering staff concluded there was not an adverse trend because a review of records since January 2009 documented normal operating start times from 7 to 8.9 seconds. The review also determined Susquehanna staff were generating condition reports at a lower threshold which resulted in an increased number of condition reports. The inspectors concluded the evaluation was conducted with sufficient technical rigor to support the conclusions.
The inspectors reviewed corrective action CR-2017-00530, which was initiated by Susquehanna staff on January 6, 2017, to evaluate a trend in slower EDG start times that still met technical specification requirements. Additionally, the inspectors reviewed CR-2017-11996 to evaluate and correct the A EDG not meeting starting time requirements.


CR-2017-11996 indicated that the 'A' EDG reached frequency in 10.16 seconds versus the required 10 seconds during testing on June 19, 2017. The inspectors determined that Susquehanna staff implemented the applicable technical specification requirements, evaluated the problem in sufficient detail to identify that pneumatic valves USY-9 and/or USCV-9 actuated slowly resulting in a pneumatic delay, and that other causes were reasonably ruled out. Susquehanna staff replaced these valves and planned actions to revise maintenance activities and schedules for the pneumatic shuttle valves. The evaluation further noted the pneumatic starting circuit is only present in test mode and is locked out during an emergency mode start. The inspectors concluded the evaluation was of sufficient detail to identify the likely cause of not meeting the required start time and provided for corrective actions that addressed the cause.
The inspectors review of CR-2017-00530 determined that Susquehanna engineering staff concluded there was not an adverse trend because a review of records since January 2009 documented normal operating start times from 7 to 8.9 seconds. The review also determined Susquehanna staff were generating condition reports at a lower threshold which resulted in an increased number of condition reports. The inspectors concluded the evaluation was conducted with sufficient technical rigor to support the conclusions.
 
CR-2017-11996 indicated that the A EDG reached frequency in 10.16 seconds versus the required 10 seconds during testing on June 19, 2017. The inspectors determined that Susquehanna staff implemented the applicable technical specification requirements, evaluated the problem in sufficient detail to identify that pneumatic valves USY-9 and/or USCV-9 actuated slowly resulting in a pneumatic delay, and that other causes were reasonably ruled out. Susquehanna staff replaced these valves and planned actions to revise maintenance activities and schedules for the pneumatic shuttle valves. The evaluation further noted the pneumatic starting circuit is only present in test mode and is locked out during an emergency mode start. The inspectors concluded the evaluation was of sufficient detail to identify the likely cause of not meeting the required start time and provided for corrective actions that addressed the cause.


==EXIT MEETINGS AND DEBRIEFS==
==EXIT MEETINGS AND DEBRIEFS==
Line 315: Line 328:
=DOCUMENTS REVIEWED=
=DOCUMENTS REVIEWED=


71111.01 Drawings SSES Units 1 & 2 FSAR, Figure 2.5-22, Plot Plan, Revision 47
71111.01
SSES Units 1 & 2 FSAR, Figure 2.5-17A, Extent of Rock and Soil Foundations, Revision 55 SSES Units 1 & 2 FSAR, Figure 2.5-40, Spray Pond Measured & Projected Water Levels, Revision 47 SSES Units 1 & 2 FSAR, Figure 2.5-56, Profile of Slope North of Spray Pond, Revision 47
Drawings
Miscellaneous SSES-FSAR, 2.4 Hydrologic Engineering, Revision 66
SSES Units 1 & 2 FSAR, Figure 2.5-22, Plot Plan, Revision 47
SSES Units 1 & 2 FSAR, Figure 2.5-17A, Extent of Rock and Soil Foundations, Revision 55
SSES Units 1 & 2 FSAR, Figure 2.5-40, Spray Pond Measured & Projected Water Levels,
Revision 47
SSES Units 1 & 2 FSAR, Figure 2.5-56, Profile of Slope North of Spray Pond, Revision 47
Miscellaneous
SSES-FSAR, 2.4 Hydrologic Engineering, Revision 66
71111.04
71111.04
Drawings M-151, Unit 1 P&ID RHR, Sheet 1, Revision 72 M-151ABD, Unit 1 Analysis Boundary Diagram RHR Div. 1, Sheet 2, Revision 7 M-112, Unit 1 P&ID RHR Service Water System, Sheet 1, Revision 2
Drawings
M-151, Unit 1 P&ID RHR, Sheet 1, Revision 72
M-151ABD, Unit 1 Analysis Boundary Diagram RHR Div. 1, Sheet 2, Revision 7
M-112, Unit 1 P&ID RHR Service Water System, Sheet 1, Revision 2
M-151, Unit 1 P&ID RHR, Sheet 2, Revision 53
M-151, Unit 1 P&ID RHR, Sheet 2, Revision 53
M-151ABD, Unit 1 Analysis Boundary Diagram RHR Div. 2, Sheet 4, Revision 5
M-151ABD, Unit 1 Analysis Boundary Diagram RHR Div. 2, Sheet 4, Revision 5
M-151ABD, Unit 1 Analysis Boundary Diagram RHR, Sheet 3, Revision 5
M-151ABD, Unit 1 Analysis Boundary Diagram RHR, Sheet 3, Revision 5
M-112ABD, Common Analysis Boundary Diagram RHR Service Water System, Sheet 2, Revision 5 M-134, Common P&ID 'E' Diesel Auxiliaries (Fuel Oil System, Lube Oil System and Air Intake & Exhaust System), Sheet 7, Revision 22 M-134, Common P&ID 'E' Diesel Auxiliaries (Starting Air and Jacket Water Systems), Sheet 5, Revision 23 M-134, Common P&ID Diesel 'E' Auxiliaries (Starting Air System), Sheet 6, Revision 7
M-112ABD, Common Analysis Boundary Diagram RHR Service Water System, Sheet 2,
71111.05  Procedures TQ-171, Susquehanna Fire Training Program, Revision 8
ON-013-001, Response to Fire, Revision 49 NDAP-QA-0445, Fire Brigade, Revision 21
Condition Reports CR-2018-12060 CR-2018-12074
Miscellaneous FP-013-189, Diesel Generator Bay 'A' Fire Zone 0-41A, Elevations 677', 660' and 710',
Revision 4 Fire Brigade Quarterly Drill, Transient Combustibles Fire, Scenario #36
FP-013-140, Computer Room (C-202) Fire Zone 0-24E Elevation 698'-0", Revision 7
FP-213-241, RHR Pump Room "A" (II-14) Fire Zone 2-1F Elevation 645'-0 Revision 6 FP-113-101, Core Spray Pump Room 'A' (I-17) Fire Zone 1-1A Elevation 645'-0", Revision 5 FP-013-195, Diesel Generator Bay 'C' Fire Zone 0-41C Elevations 677', 660' and 710',
Revision 5
Revision 5
FP-013-200, ESSW Pump House Loop 'A' Pump Room (E-1) Fire Zone 0-51 Elevation 685'-6,"
M-134, Common P&ID E Diesel Auxiliaries (Fuel Oil System, Lube Oil System and Air Intake &
Revision 4 FP-013-201, ESSW Pump House Loop 'B' Pump Room (E-2) Fire Zone 0-52 Elevation 685'-6,"
Exhaust System), Sheet 7, Revision 22
M-134, Common P&ID E Diesel Auxiliaries (Starting Air and Jacket Water Systems), Sheet 5,
Revision 23
M-134, Common P&ID Diesel E Auxiliaries (Starting Air System), Sheet 6, Revision 7
71111.05
Procedures
TQ-171, Susquehanna Fire Training Program, Revision 8
ON-013-001, Response to Fire, Revision 49
NDAP-QA-0445, Fire Brigade, Revision 21
Condition Reports
CR-2018-12060
CR-2018-12074
Miscellaneous
FP-013-189, Diesel Generator Bay A Fire Zone 0-41A, Elevations 677, 660 and 710,
Revision 4
Revision 4
71111.07  Procedures MT-GM-031, Immersed Component/Heat Exchanger Internals Epoxy Lining/Cladding,
Fire Brigade Quarterly Drill, Transient Combustibles Fire, Scenario #36
Revision 22 MT-GM-025, Heat Exchanger-Cleaning and Inspection, Revision 22
FP-013-140, Computer Room (C-202) Fire Zone 0-24E Elevation 698-0, Revision 7
FP-213-241, RHR Pump Room A (II-14) Fire Zone 2-1F Elevation 645-0 Revision 6
FP-113-101, Core Spray Pump Room A (I-17) Fire Zone 1-1A Elevation 645-0, Revision 5
FP-013-195, Diesel Generator Bay C Fire Zone 0-41C Elevations 677, 660 and 710,
Revision 5


Work Orders 2093734 2112486 2133022 G0104-05
FP-013-200, ESSW Pump House Loop A Pump Room (E-1) Fire Zone 0-51 Elevation 685-6,
Drawings M-111, Common P&ID Emergency Service Water System, Sheet 4, Revision 5
Revision 4
M-134, Common P&ID 'E' Diesel Auxiliaries (Fuel Oil System, Lube Oil System and Air Intake & Exhaust System), Sheet 7, Revision 22
FP-013-201, ESSW Pump House Loop B Pump Room (E-2) Fire Zone 0-52 Elevation 685-6,
71111.11 Procedures GO-100-012, Power Maneuvers, Revision 53 OP-131-001, Rod Worth Minimizer RWM, Revision 17 NDAP-QA-0338, Reactivity Management and Controls Program, Revision 27
Revision 4
Condition Reports CR-2018-11865
71111.07
71111.12 Procedures NDAP-QA-0413, Implementation of the Maintenance Rule, Revision 15
Procedures
MT-GM-031, Immersed Component/Heat Exchanger Internals Epoxy Lining/Cladding,
Revision 22
MT-GM-025, Heat Exchanger-Cleaning and Inspection, Revision 22
Work Orders
2093734
2112486
2133022
G0104-05
Drawings
M-111, Common P&ID Emergency Service Water System, Sheet 4, Revision 5
M-134, Common P&ID E Diesel Auxiliaries (Fuel Oil System, Lube Oil System and Air Intake &
Exhaust System), Sheet 7, Revision 22
71111.11
Procedures
GO-100-012, Power Maneuvers, Revision 53
OP-131-001, Rod Worth Minimizer RWM, Revision 17
NDAP-QA-0338, Reactivity Management and Controls Program, Revision 27
Condition Reports
CR-2018-11865
71111.12
Procedures
NDAP-QA-0413, Implementation of the Maintenance Rule, Revision 15
NDAP-QA-0483, Underground Piping and Tanks Program, Revision 6
NDAP-QA-0483, Underground Piping and Tanks Program, Revision 6
Condition Reports CR-2017-10847 CR-2017-18437 CR-2018-08960 CR-2018-12816 CR-2018-11207 CR-2018-11231 CR-2018-12238 CR-2018-12271
Condition Reports
CR-2018-12276 CR-2018-12440 CR-2018-12564 CR-2018-12566
CR-2017-10847
CR-2018-12817 CR-2018-12892 CR-2018-13215 CR-2018-13388
CR-2017-18437
Action Requests AR-2018-09858 AR-2018-12461 AR-2018-13434 AR-2018-13623
CR-2018-08960
AR-2018-13830 AR-2018-14040 DI-2018-09779  
CR-2018-12816
 
CR-2018-11207
Miscellaneous General Electric Spec 22A7468, Sheet 10, Revision 3
CR-2018-11231
CR-2018-12238
CR-2018-12271
CR-2018-12276
CR-2018-12440
CR-2018-12564
CR-2018-12566
CR-2018-12817
CR-2018-12892
CR-2018-13215
CR-2018-13388
Action Requests
AR-2018-09858
AR-2018-12461
AR-2018-13434
AR-2018-13623
AR-2018-13830
AR-2018-14040
DI-2018-09779
Miscellaneous
General Electric Spec 22A7468, Sheet 10, Revision 3
Underground Vault Inspections 2013 to 2017  
Underground Vault Inspections 2013 to 2017  


71111.13 Condition Reports CR-2018-10666 CR-2018-11180 CR-2018-11762 CR-2018-11979  
71111.13
 
Condition Reports
Drawings M-142, Unit 1 P&ID Nuclear Boiler Vessel Instrumentation, Sheet 1, Revision 55  
CR-2018-10666
 
CR-2018-11180
Miscellaneous DLAP dated July 31, 2018
CR-2018-11762
CR-2018-11979
Drawings
M-142, Unit 1 P&ID Nuclear Boiler Vessel Instrumentation, Sheet 1, Revision 55
Miscellaneous
DLAP dated July 31, 2018
IOM 311-1, Tab 8 Vendor Supplied Instruments, Volume 1, Revision 15
IOM 311-1, Tab 8 Vendor Supplied Instruments, Volume 1, Revision 15
NP-2-1, Control Room Panel, MPL H12-P609, Seismic Qualification Review, Revision 1
NP-2-1, Control Room Panel, MPL H12-P609, Seismic Qualification Review, Revision 1
Protected Equipment list dated September 28, 2018
Protected Equipment list dated September 28, 2018
064C, Reactor Recirculation Systems and Motor Generator Set, Revision 12  
064C, Reactor Recirculation Systems and Motor Generator Set, Revision 12
 
71111.15
71111.15
Procedures NDAP-QA-0703, Operability Determinations and Functionality Assessments, Revision 31
Procedures
Condition Reports CR-2018-08841 CR-2018-09365 CR-2018-09496 CR-2018-11157
NDAP-QA-0703, Operability Determinations and Functionality Assessments, Revision 31
CR-2018-11159 CR-2018-12440
Condition Reports
Action Requests AR-2018-09929 AR-2018-12461
CR-2018-08841
CR-2018-09365
CR-2018-09496
CR-2018-11157
CR-2018-11159
CR-2018-12440
Action Requests
AR-2018-09929
AR-2018-12461
Work Orders
Work Orders
2181881 Drawings E-214, Common Schematic Diagram HVAC Control Structure Chilled Water System Chilled 'B' Comp Motor, Sheet 2, Revision 28 E-214, Common Schematic Diagram HVAC Control Structure Chilled Water System Chilled Cond Water Circ PP 0P170A&B, Sheet 5, Revision 17 E-214, Common Schematic Diagram Control Structure HVAC Chilled Water System Chilled Water Circ Pump 0P162B, Sheet 19, Revision 10 M310-244, Common Schematic Diagram Control Structure Chilled Water System Chiller 0K112B, Sheet 2, Revision 7 E-214, Common Schematic Diagram Control Structure HVAC Chilled Water System Chilled Water Circ PPS, Sheet 4, Revision 29 E-16, Unit 1 Circuit Breaker Interruption, Impact Drawing, DC Panel 1D614, Sheet 3,
2181881
Drawings
E-214, Common Schematic Diagram HVAC Control Structure Chilled Water System Chilled B
Comp Motor, Sheet 2, Revision 28
E-214, Common Schematic Diagram HVAC Control Structure Chilled Water System Chilled
Cond Water Circ PP 0P170A&B, Sheet 5, Revision 17
E-214, Common Schematic Diagram Control Structure HVAC Chilled Water System Chilled
Water Circ Pump 0P162B, Sheet 19, Revision 10
M310-244, Common Schematic Diagram Control Structure Chilled Water System Chiller
0K112B, Sheet 2, Revision 7
E-214, Common Schematic Diagram Control Structure HVAC Chilled Water System Chilled
Water Circ PPS, Sheet 4, Revision 29
E-16, Unit 1 Circuit Breaker Interruption, Impact Drawing, DC Panel 1D614, Sheet 3,
Revision 23
Revision 23
Miscellaneous Control Structure Chiller Response following Electrical Transient
Miscellaneous
Cases of ASME Boiler and Pressure Vessel Code, Case N-513-3 EP-115  
Control Structure Chiller Response following Electrical Transient
Cases of ASME Boiler and Pressure Vessel Code, Case N-513-3
EP-115  


71111.17
71111.17
Procedures GO-100-009, Single Recirculation Loop Operation, Revision 23
Procedures
GO-100-009, Single Recirculation Loop Operation, Revision 23
MT-GE-024, Installation and Removal of Oscillographic Recorder for Diesel Generator
MT-GE-024, Installation and Removal of Oscillographic Recorder for Diesel Generator
Surveillances, Revision 28 MT-GM-092, Temporary Repair of Minor Pipe Leaks, Revision 0
Surveillances, Revision 28
MT-GM-092, Temporary Repair of Minor Pipe Leaks, Revision 0
NDAP-QA-0726, 10 CFR 50.59 and 10 CFR 72.48 Implementation, Revision 20
NDAP-QA-0726, 10 CFR 50.59 and 10 CFR 72.48 Implementation, Revision 20
NDAP-QA-1218, Temporary Changes, Revision 17 OP-149-002, Residual Heat Removal Shutdown Cooling, Revision 58
NDAP-QA-1218, Temporary Changes, Revision 17
Susquehanna 50.59 Resource Manual, Revision 8  
OP-149-002, Residual Heat Removal Shutdown Cooling, Revision 58
 
Susquehanna 50.59 Resource Manual, Revision 8
Condition Reports (*initiated in response to inspection) CR-2015-09176 CR-2015-22586 CR-2015-22822 CR-2015-26472 CR-2016-06540 CR-2016-07955 CR-2016-22888 CR-2018-10783 CR-2018-12308* CR-2018-12310* CR-2018-12337*  
Condition Reports (*initiated in response to inspection)
 
CR-2015-09176
Work Orders PCWO 1935310
CR-2015-22586
Drawings E-214, Sheet 12, Schematic Diagram Control Structure HVAC Chilled Water System Chilled
CR-2015-22822
Water Circulating Pumps, Revision 16 M-151, Unit 1 Piping and Instrumentation Drawing (P&ID) Residual Heat Removal, Revision 72
CR-2015-26472
CR-2016-06540
CR-2016-07955
CR-2016-22888
CR-2018-10783
CR-2018-12308*
CR-2018-12310*
CR-2018-12337*
Work Orders
PCWO 1935310
Drawings
E-214, Sheet 12, Schematic Diagram Control Structure HVAC Chilled Water System Chilled
Water Circulating Pumps, Revision 16
M-151, Unit 1 Piping and Instrumentation Drawing (P&ID) Residual Heat Removal, Revision 72
M-157, Unit 1 Containment Atmos. Control Hardened Containment Vent System, Revision 0
M-157, Unit 1 Containment Atmos. Control Hardened Containment Vent System, Revision 0
Engineering Evaluations EC-013-0022, Fire Protection Piping Pressure Losses, Revision 11
Engineering Evaluations
EC-013-1438, Examination of Appendix R Safe Shutdown Components with Regard to Fire Suppression Activities, Revision 3 EC-FLOD-0001, Internal Flooding Evaluations for Moderate Energy Pipe Cracks and Sprinkler System Actuation, Revision 3
EC-013-0022, Fire Protection Piping Pressure Losses, Revision 11
Miscellaneous Check-In Self-Assessment of the SSES 10 CFR 50.59 Program, dated April 20, 2018
EC-013-1438, Examination of Appendix R Safe Shutdown Components with Regard to Fire
Design Basis Document (DBD) 002, Control Structure HVAC and Chilled Water Systems, Revision 2 DBD 043, Reactor Water Cleanup System, Revision 5
Suppression Activities, Revision 3
EC-FLOD-0001, Internal Flooding Evaluations for Moderate Energy Pipe Cracks and Sprinkler
System Actuation, Revision 3
Miscellaneous
Check-In Self-Assessment of the SSES 10 CFR 50.59 Program, dated April 20, 2018
Design Basis Document (DBD) 002, Control Structure HVAC and Chilled Water Systems,
Revision 2
DBD 043, Reactor Water Cleanup System, Revision 5
DBD 019, Fire Protection, Revision 7
DBD 019, Fire Protection, Revision 7
Fire Protection Review Report, Revision 13
Fire Protection Review Report, Revision 13
PLA-7321, Susquehanna Steam Electric Station Completion of Actions Required by NRC Order EA-12-051, "Reliable Spent Fuel Pool Instrumentation," dated July 2, 2015 PLA-7542, Susquehanna Steam Electric Station 10 CFR 50.59 Summary Report and Changes to Regulatory Commitments, dated October 24, 2016 PLA-7711, Report of Full Compliance with June 6, 2013, Commission Order Modifying Licenses with Regard to Reliable Hardened Containment Vents Capable of Operation Under Severe
PLA-7321, Susquehanna Steam Electric Station Completion of Actions Required by NRC Order
Accident Conditions, June 26, 2018 Technical Specifications - Susquehanna Steam Electric Station Unit 1, Revised June 28, 2018 Technical Specifications - Susquehanna Steam Electric Station Unit 2, Revised June 28, 2018
EA-12-051, "Reliable Spent Fuel Pool Instrumentation," dated July 2, 2015
PLA-7542, Susquehanna Steam Electric Station 10 CFR 50.59 Summary Report and Changes
to Regulatory Commitments, dated October 24, 2016
PLA-7711, Report of Full Compliance with June 6, 2013, Commission Order Modifying Licenses
with Regard to Reliable Hardened Containment Vents Capable of Operation Under Severe
Accident Conditions, June 26, 2018
Technical Specifications - Susquehanna Steam Electric Station Unit 1, Revised June 28, 2018
Technical Specifications - Susquehanna Steam Electric Station Unit 2, Revised June 28, 2018
Updated Final Safety Analysis Report for Susquehanna Steam Electric Station, Revision 66  
Updated Final Safety Analysis Report for Susquehanna Steam Electric Station, Revision 66  


71111.19 Procedures SO-054-A03, 92DY-ESW Flow Verif 'A' Loop, Revision 18 SO-024-001D, Monthly Diesel Generator 'D' Operability Test, Revision 27
71111.19
SO-024-D01, Diesel Generator 'D' Integrated Surveillance Test, Revision 1
Procedures
OT-02-149, Diesel Generator 'E' Restoration, Revision 2
SO-054-A03, 92DY-ESW Flow Verif A Loop, Revision 18
SO-024-001D, Monthly Diesel Generator D Operability Test, Revision 27
SO-024-D01, Diesel Generator D Integrated Surveillance Test, Revision 1
OT-02-149, Diesel Generator E Restoration, Revision 2
MT-064-014, N-7500 Reactor Recirculating Pump Seal Rebuilding and Test, Revision 42
MT-064-014, N-7500 Reactor Recirculating Pump Seal Rebuilding and Test, Revision 42
TP-164-045, Local System Leakage Test of Reactor Recirculation Loops A & B, Revision 10
TP-164-045, Local System Leakage Test of Reactor Recirculation Loops A & B, Revision 10
Condition Reports CR-2018-10666 CR-2018-10080 CR-2018-12055
Condition Reports
CR-2018-10666
CR-2018-10080
CR-2018-12055
Work Orders
Work Orders
1961035 2107565 2181918 2183442 2188571 2191979
1961035
2191984 2195198 2195226
2107565
71111.20 Condition Reports CR-2018-12041 CR-2018-12048 CR-2018-12053 CR-2018-12054 CR-2018-12055 CR-2018-12056 CR-2018-12064 CR-2018-12078
2181918
CR-2018-12081 CR-2018-12092 CR-2018-12093 CR-2018-12097
2183442
CR-2018-12124 CR-2018-12134 CR-2018-12135 CR-2018-12146
2188571
CR-2018-12225 CR-2018-12250 CR-2018-12280
2191979
71111.22  Procedures SO-151-A04, Quarterly Core Spray Valve Exercising Division 1, Revision 13 SO-100-106, Shiftly Surveillance Operating Log, Revision 118 SO-054-A03, Quarterly ESW Flow Verification Loop 'A', Revision 18
2191984
2195198
2195226
71111.20
Condition Reports
CR-2018-12041
CR-2018-12048
CR-2018-12053
CR-2018-12054
CR-2018-12055
CR-2018-12056
CR-2018-12064
CR-2018-12078
CR-2018-12081
CR-2018-12092
CR-2018-12093
CR-2018-12097
CR-2018-12124
CR-2018-12134
CR-2018-12135
CR-2018-12146
CR-2018-12225
CR-2018-12250
CR-2018-12280  


Condition Reports CR-2018-10080
71111.22
Action Requests AR-2018-13417
Procedures
71114.06 Miscellaneous EP-PS-001, Emergency Planning Forms and Supplementary Instructions, Revision 14 Susquehanna Steam Electric Station Dose Assessment Summary
SO-151-A04, Quarterly Core Spray Valve Exercising Division 1, Revision 13
Final Timeline for Tabletop PI- New to be Conducted July 5, 2018
SO-100-106, Shiftly Surveillance Operating Log, Revision 118
SO-054-A03, Quarterly ESW Flow Verification Loop A, Revision 18
Condition Reports
CR-2018-10080
Action Requests
AR-2018-13417
71114.06
Miscellaneous
EP-PS-001, Emergency Planning Forms and Supplementary Instructions, Revision 14
Susquehanna Steam Electric Station Dose Assessment Summary
Final Timeline for Tabletop PI-New to be Conducted July 5, 2018
Drill Data Set, Unit 1
Drill Data Set, Unit 1
71124.08 Shipments 17-046; 17-047; 18-043; 18-047; 18-057
71124.08
71151 Condition Reports CR-2018-10876 CR-2018-10985 DI-2016-25418 DI-2016-25423
Shipments
DI-2017-00413 DI-2017-00588 DI-2017-19298 DI-2017-19309
17-046; 17-047; 18-043; 18-047; 18-057  
DI-2018-01291 DI-2018-01143
 
71152 Equipment Apparent Cause Evaluation CR-2017-11996
71151
Condition Reports CR-2016-18464 CR-2016-26216 CR-2016-27120 CR-2017-00530 CR-2017-17228 CR-2018-10285 CR-2018-11166 CR-2018-12195
Condition Reports
Completed Surveillance, Performance, and Functional Tests SO-024-001A, Monthly Diesel Generator 'A' Operability Test, performed 3/24/18, 4/25/18 and
CR-2018-10876
5/20/18 SO-024-001B, Monthly Diesel Generator 'B' Operability Test, performed 3/25/18, 4/27/18 and
CR-2018-10985
5/28/18 SO-024-001C, Monthly Diesel Generator 'C' Operability Test, performed 4/4/18, 5/7/18 and
DI-2016-25418
6/4/18 SO-024-001D, Monthly Diesel Generator 'D' Operability Test, performed 4/13/18, 5/14/18 and
DI-2016-25423
6/11/18 SO-024-001E, Monthly Diesel Generator 'E' Test While Substituting for Another Diesel Generator, performed 2/1/18, 3/5/18 and 3/28/18
DI-2017-00413
Drawings FF105801, Sh. 1, Common Standby Generator Set Control Diagram, Revision 9 FF105801, Sh. 2, Cooper Bessemer Control Diagram KSV-36-10, Revision 5
DI-2017-00588
71153 Condition Reports CR-2015-32449 CR-2015-32451 CR-2016-21657 CR-2017-12327
DI-2017-19298
DI-2017-19309
DI-2018-01291
DI-2018-01143
71152
Equipment Apparent Cause Evaluation
CR-2017-11996
Condition Reports
CR-2016-18464
CR-2016-26216
CR-2016-27120
CR-2017-00530
CR-2017-17228
CR-2018-10285
CR-2018-11166
CR-2018-12195
Completed Surveillance, Performance, and Functional Tests
SO-024-001A, Monthly Diesel Generator A Operability Test, performed 3/24/18, 4/25/18 and
5/20/18
SO-024-001B, Monthly Diesel Generator B Operability Test, performed 3/25/18, 4/27/18 and
5/28/18
SO-024-001C, Monthly Diesel Generator C Operability Test, performed 4/4/18, 5/7/18 and
6/4/18
SO-024-001D, Monthly Diesel Generator D Operability Test, performed 4/13/18, 5/14/18 and
6/11/18
SO-024-001E, Monthly Diesel Generator E Test While Substituting for Another Diesel
Generator, performed 2/1/18, 3/5/18 and 3/28/18
Drawings
FF105801, Sh. 1, Common Standby Generator Set Control Diagram, Revision 9
FF105801, Sh. 2, Cooper Bessemer Control Diagram KSV-36-10, Revision 5
71153
Condition Reports
CR-2015-32449
CR-2015-32451
CR-2016-21657
CR-2017-12327
CR-2017-13014
CR-2017-13014
Action Requests AR-2017-14031
Action Requests
AR-2017-14031
Miscellaneous
Miscellaneous
LER 50-388(387)/2017-006-00
LER 50-388(387)/2017-006-00
}}
}}

Latest revision as of 09:46, 5 January 2025

Integrated Inspection Report 05000387/2018003 and 05000388/2018003
ML18313A025
Person / Time
Site: Susquehanna  
Issue date: 11/08/2018
From: Jon Greives
Reactor Projects Region 1 Branch 4
To: Berryman B
Susquehanna
Greives J
References
IR 2018003
Download: ML18313A025 (20)


Text

November 8, 2018

SUBJECT:

SUSQUEHANNA STEAM ELECTRIC STATION - INTEGRATED INSPECTION REPORT 05000387/2018003 AND 05000388/2018003

Dear Mr. Berryman:

On September 30, 2018, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Susquehanna Steam Electric Station, Units 1 and 2. On October 18, 2018, the NRC inspectors discussed the results of this inspection with Mr. Kevin Cimorelli, Site Vice President, and other members of your staff. The results of this inspection are documented in the enclosed report.

The NRC inspectors did not identify any findings or violations of more than minor significance.

This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations (10 CFR), Part 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Jonathan E. Greives, Chief Reactor Projects Branch 4 Division of Reactor Projects

Docket Numbers: 50-387 and 50-388 License Numbers: NPF-14 and NPF-22

Enclosure:

Inspection Report 05000387/2018003 and 05000388/2018003

Inspection Report

Docket Numbers:

50-387 and 50-388

License Numbers:

NPF-14 and NPF-22

Report Numbers:

05000387/2018003 and 05000388/2018003

Enterprise Identifier: I-2018-003-0069

Licensee:

Susquehanna Nuclear, LLC (Susquehanna)

Facility:

Susquehanna Steam Electric Station, Units 1 and 2

Location:

Berwick, Pennsylvania

Inspection Dates:

July 1, 2018 to September 30, 2018

Inspectors:

L. Micewski, Senior Resident Inspector

T. Daun, Resident Inspector

N. Floyd, Senior Reactor Inspector

M. Orr, Reactor Inspector

J. Furia, Senior Health Physicist

Approved By:

Jonathan E. Greives, Chief

Reactor Projects Branch 4

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring Susquehannas performance at Susquehanna Steam Electric Station, Units 1 and 2 by conducting the baseline inspections described in this report in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

No findings or more-than-minor violations were identified.

Additional Tracking Items

Type Issue number Title Inspection Results Section Status LER 05000388;387/2016-006-00 Loss of Secondary Containment Due to Damper Controller Sticking 71153 Closed LER 05000388;387/2017-005-00 Secondary Containment Declared Inoperable Due to Trip of Zone III Filtered Exhaust Fan 71153 Closed LER 05000388;387/2017-006-00 Secondary Containment Declared Inoperable Due to Trip of Zone II Exhaust Fan 71153 Closed

PLANT STATUS

Unit 1 began the inspection period at 100 percent power. On August 3, 2018, operators reduced power to approximately 57 percent to perform a rod sequence exchange. Full power was achieved again on August 5, 2018. On August 18, 2018, operators shut down the unit for a planned maintenance outage to replace a reactor recirculation pump seal. Following seal replacement, operators commenced a reactor startup on August 23, 2018, and commenced a ramp towards full power, achieving 96 percent power on August 30, 2018. On August 30, 2018, operators lowered power to 59 percent following an electrical disturbance that caused a loss of drywell cooling. Following restoration of drywell cooling, operators restored power to 96 percent and continued the ramp, achieving full power on the same day. Unit 1 remained at or near 100 percent power for the remainder of the inspection period.

Unit 2 began the inspection period at 100 percent power. On August 30, 2018, operators lowered power to 60 percent following an electrical disturbance that caused a loss of drywell cooling. Following restoration of drywell cooling, operators restored power to 100 percent that same day. On August 31, 2018, operators reduced power to approximately 62 percent to perform a rod pattern adjustment. Operators returned the unit to 100 percent on September 2, 2018, and remained at or near 100 percent power for the remainder of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515, Appendix D, Plant Status, and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess Susquehannas performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

External Flooding (1 Sample)

The inspectors evaluated readiness to cope with external flooding.

71111.04 - Equipment Alignment

Partial Walkdown (3 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) Unit 1, division 2 core spray during work on a division 1 C core spray room cooler on July 2, 2018
(2) Unit 1, division 2 residual heat removal (RHR) during A RHR system outage window on August 8, 2018
(3) Unit 2, division 2 RHR service water (RHRSW) during work on division 1 RHRSW pump discharge valves on September 11, 2018

Complete Walkdown (1 Sample)

The inspectors evaluated system configurations during a complete walkdown of the Unit Common, E emergency diesel generator (EDG) and support systems following 5 year diesel overhaul.

71111.05A/Q - Fire Protection Annual/Quarterly

Quarterly Inspection (5 Samples)

The inspectors evaluated fire protection program implementation in the following selected areas:

(1) Unit Common, A EDG (fire zone 0-41A) on July 16, 2018
(2) Unit 2, A RHR pump room (fire zone 2-1F) on September 12, 2018
(3) Unit 1, A core spray pump room (fire zone 1-1A) on September 14, 2018
(4) Unit Common, C EDG (fire zone 0-41C) on September 26, 2018
(5) Unit Common, engineered safeguard service water pump house (fire zones 0-51 and 0-52) on September 27, 2018

Annual Inspection (1 Sample)

The inspectors evaluated fire brigade performance on August 16, 2018.

71111.07 - Heat Sink Performance

Heat Sink (1 Sample)

The inspectors evaluated Susquehannas monitoring and maintenance of Unit Common E EDG lube oil cooler performance.

71111.11 - Licensed Operator Requalification Program and Licensed Operator Performance

Operator Requalification (1 Sample)

The inspectors observed and evaluated licensed operator simulator training, which included a loss of all instrument air, a small break loss of coolant accident, trip of the high pressure coolant injection pump due to loss of lubrication oil cooling, and the failure of select components to automatically start as required on August 13, 2018.

Operator Performance (1 Sample)

The inspectors observed reactivity manipulations to reduce power to approximately 63 percent, and a subsequent rod sequence exchange at Unit 1 on August 3 and 4, 2018. The inspectors also observed reactor shutdown activities for a planned maintenance outage at Unit 1 on August 18, 2018.

71111.12 - Maintenance Effectiveness

Routine Maintenance Effectiveness (2 Samples)

The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:

(1) Unit Common, scram discharge volume vent and drain valve stroke timing and coordination
(2) Unit Common, emergency service water (ESW) piping corrosion and preservation in vaults

71111.13 - Maintenance Risk Assessments and Emergent Work Control

The inspectors evaluated the risk assessments for the following planned and emergent work activities:

(1) Unit 1, emergent work control associated with half scram resulting from failure of K14A reactor protection system (RPS) relay on July 18, 2018
(2) Unit 2, D RHR pump protected during B RHR pump maintenance on July 31, 2018
(3) Unit 1, A reactor recirculation pump #2 seal failure on August 7, 2018
(4) Unit 1, risk management activities during A standby liquid control pressure sensing valve replacement on September 28, 2018

71111.15 - Operability Determinations and Functionality Assessments

The inspectors evaluated the following operability determinations and functionality assessments:

(1) Unit 2, failure of relay 44A in 4kV bus 2C prevented 2C RHR and 2C core spray pumps from starting on July 24, 2018
(2) Unit Common, control structure chillers following T-20 electrical transient on July 30, 2018
(3) Unit Common, ESW through wall leak in Unit 1 reactor core isolation cooling (RCIC)room on August 28, 2018
(4) Unit 1, ladder stored adjacent to RCIC division 2 isolation panel on August 29, 2018
(5) Unit Common, water leaking from conduit into engineered safeguard service water pump house basement on September 25, 2018

71111.17T - Evaluations of Changes, Tests, and Experiments

The inspectors evaluated the following changes which were implemented from August 2015 to August 2018:

10 CFR 50.59 Evaluations

(1) SE 00028, Unit 1 and 2 Online Noble Chemistry System Installation, Revision 0
(2) SE 00015, Vent Effluent Radiation Monitoring System Replacement, Revision 0

10 CFR 50.59 Screening/Applicability Determinations

(1) SD 01381, EC 1684212, Control Structure Chiller Time Delay Control Changes, Revision 1
(2) SD 01502, EC 1544685, Install Higher Head Pumps in Place of Fire Pumps 0P511, 0P512, and 0P592, Revision 8
(3) SD 01694, EC 1846732, Ensure Positive Seating of Residual Heat Removal Injection Check Valves HV151F050A&B, Revision 0
(4) SD 01708, Temporary Repairs of Minor Pipe Leaks, Revision 0
(5) SD 01750, Depressurize Reactor Vessel to <40 psig Prior to Initiating Shutdown Cooling, Revision 0
(6) SD 01751, Reliable Hardened Containment Vent System, Revision 3
(7) SD 01757, Pre-engineered Replacement of PSA Mechanical Snubbers and Compensating Struts with Lisega Hydraulic Units, Revision 0
(8) SD 01785, Installation and Removal of Oscillographic Recorder for Diesel Generator Surveillances in Accordance with MT-GE-024, Revision 0
(9) SD 01786, EC 1805589, Remove CIG Compressor Inlet Check Valves, Revision 0
(10) SD 01793, Removal of LIS25348 per PCWO 1935310 greater than 90 days at power, Revision 0
(11) SD 01795, ZWO 1959855, Compensatory Measure for A CST Heat Trace Inoperable, Revision 0
(12) SD 01819, Change Shutdown Cooling Startup Sequence to Crack Open F017 Valves Prior to Starting Residual Heat Removal Pump, Revision 0
(13) SD 01828, LDCN 5269, Isolation of ESW from E DG Fuel Oil Heat Exchanger 0E526E, Revision 0
(14) SD 01840, Temporary Alteration Applied Under PCWO 1912777 in Place Greater than 90 Days, Revision 0
(15) SD 01871, EC 1948468, Repair of Service Water Lines Using External Composite Pipe Wrap Material, Revision 0
(16) SD 01928, EC 2002457, Increase the Design Pressure for Instrument Air Piping, Revision 0
(17) SD 01934, On-Line Functional Test of Residual Heat Removal Loop B at 2 C201B, Revision 0
(18) SD 01937, LDCN 5295, Change to Design Basis Hydrogen Generation, Revision 0
(19) SD 01944, LDCN 5301, Impact of AREVA Computer Code Version Changes Used for U2C19 Analysis, Revision 0
(20) SD 01960, LDCN 5311, Fuel Handling Accident Analysis Update, Revision 0
(21) SD 02104, EC 2132596, Yokogawa CX112 Replacement with DX1012N for Reactor Core Isolation Cooling Steam Leak Detection System, Revision 0
(22) SD 02122, EC 2033998, Replace the Compressors and Air Dryers in DG Air Start System, Revision 0
(23) SD 02128, Use of Core Flow Versus Core Pressure Drop Relationship for Core Flow Validation in Single Loop Operation, Revision 0

71111.19 - Post Maintenance Testing

The inspectors evaluated post maintenance testing for the following maintenance/repair activities:

(1) Unit 1, C core spray room cooler following relay replacement on July 2, 2018
(2) Unit 1, replacement of auxiliary contact kit on K14A RPS relay on July 18, 2018
(3) Unit Common, C ESW pump following lift check maintenance on July 23, 2018
(4) Unit Common, D EDG following mechanical governor replacement on August 2, 2018
(5) Unit Common, E EDG following overhaul, on August 17, 2018
(6) Unit 1, A reactor recirculation pump following seal replacement on September 14, 2018

71111.20 - Refueling and Other Outage Activities

The inspectors evaluated Unit 1 forced outage SD01-18-02 activities from August 17, 2018 to August 23, 2018.

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance tests:

Inservice

(1) Unit 1, Division 1 core spray valve exercising on July 3, 2018
(2) Unit Common, C ESW pump inservice test re-baseline on September 19, 2018

Reactor Coolant System Leak Detection (1 Sample)

(1) Unit 1, unidentified/identified leakage calculations following seal failure, on August 16, 2018

71114.06 - Drill Evaluation

Emergency Planning Drill (1 Sample)

The inspectors evaluated the emergency director, dose assessment personnel, and communicators emergency preparedness implementation during three tabletop training exercises between July 19, 2018 and August 2, 2018. The inspectors observed three different emergency response organization crews responding to a scenario that involved a loss of offsite power and a simulated radiological release due to fuel cladding damage.

RADIATION SAFETY

71124.06 - Radioactive Gaseous and Liquid Effluent Treatment

Walkdowns and Observations (1 sample)

The inspectors walked down the gaseous and liquid radioactive effluent monitoring and filtered ventilation systems to assess the material condition and verify proper alignment according to plant design.

Calibration and Testing Program (1 sample)

The inspectors reviewed gaseous and liquid effluent monitor instrument calibration, functional test results, and alarm set-points based on National Institute of Standards and Technology calibration traceability and offsite dose calculation manual (ODCM)specifications.

Sampling and Analyses (1 sample)

The inspectors reviewed radioactive effluent sampling activities, representative sampling requirements, compensatory measures taken during effluent discharges with inoperable effluent radiation monitoring instrumentation, the use of compensatory radioactive effluent sampling, and the results of the inter-laboratory and intra-laboratory comparison program including scaling of hard-to-detect isotopes.

Instrumentation and Equipment (1 sample)

The inspectors reviewed the methodology used to determine the radioactive effluent stack and vent flow rates to verify that the flow rates were consistent with technical specification/ODCM and updated final safety analysis report values. The inspectors reviewed radioactive effluent discharge system surveillance test results based on technical specification acceptance criteria.

Dose Calculations (1 sample)

The inspectors reviewed changes in reported dose values from the previous annual radioactive effluent release reports, several liquid and gaseous radioactive waste discharge permits, the scaling method for hard-to-detect radionuclides, ODCM changes, land use census changes, public dose calculations (monthly, quarterly, annual), and records of abnormal gaseous or liquid radioactive releases.

71124.08 - Radioactive Solid Waste Processing and Radioactive Material Handling, Storage,

and Transportation

Radioactive Material Storage

The inspectors observed radioactive waste container storage areas and verified the postings and controls and that Susquehanna had established a process for monitoring the impact of long-term storage of the waste.

Radioactive Waste System Walkdown (1 sample)

The inspectors walked down accessible portions of liquid and solid radioactive waste processing systems, abandoned in place radioactive waste processing equipment, and current methods and procedures for dewatering waste.

Waste Characterization and Classification (1 sample)

The inspectors identified radioactive waste streams and reviewed radiochemical sample analysis results to support radioactive waste characterization. The inspectors reviewed the use of scaling factors and calculations to account for difficult-to-measure radionuclides.

Shipment Preparation (1 sample)

The inspectors reviewed the records of shipment packaging, surveying, labeling, marking, placarding, vehicle checks, emergency instructions, disposal manifest, shipping papers provided to the driver, and licensee verification of shipment readiness.

Shipping Records (1 sample)

The inspectors reviewed selected non-excepted package shipment records.

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification The inspectors verified Susquehannas performance indicator submittals listed below

=

(1) Unit 1 and Unit 2, MS05 Safety System Functional Failures, July 1, 2017 through June 30, 2018
(2) Unit 1 and Unit 2, MS06 MSPI Emergency AC Power Systems (EDG), July 1, 2017 through June 30, 2018
(3) Unit 1 and Unit 2, MS07 MSPI High Pressure Injection (HPCI), July 1, 2017 through June 30, 2018
(4) Unit 1 and Unit 2, MS08 Heat Removal Systems (RCIC), July 1, 2017 through June 30, 2018

71152 - Problem Identification and Resolution

Annual Follow-up of Selected Issues (3 Samples)

The inspectors reviewed the Susquehannas implementation of its corrective action program related to the following issues:

(1) Ineffective risk management actions during emergent work
(2) Unit 2 fuel leaker identified in the 2017 refueling outage
(3) EDG slow start times

71153 - Follow-up of Events and Notices of Enforcement Discretion Licensee Event Reports

The inspectors evaluated the following licensee event reports (LERs):

(1) LER 05000388;387/2016-006-00, Loss of Secondary Containment Due to Damper Controller Sticking (ADAMS Accession No. ML16323A007). The inspectors determined that it was not reasonable to foresee or correct the cause discussed in the LER therefore no performance deficiency was identified. Thus, the inspectors also concluded that no violation of NRC requirements occurred.
(2) LER 05000388;387/2017-005-00, Secondary Containment Declared Inoperable Due to Trip of Zone III Filtered Exhaust Fan (ADAMS Accession No. ML17230A248). The inspectors determined that it was not reasonable to foresee or correct the cause discussed in the LER therefore no performance deficiency was identified. Thus, the inspectors also concluded that no violation of NRC requirements occurred.
(3) LER 05000388;387/2017-006-00, Secondary Containment Declared Inoperable Due to Trip of Zone II Exhaust Fan (ADAMS Accession No. ML17249A538). The inspectors determined that it was not reasonable to foresee or correct the cause discussed in the LER therefore no performance deficiency was identified. Thus, the inspectors also concluded that no violation of NRC requirements occurred.

OTHER ACTIVITIES

- TEMPORARY INSTRUCTIONS, INFREQUENT, AND ABNORMAL

IP 92709 - Contingency Plans for Licensee Strikes or Lockouts

Susquehanna developed a Business Continuity Plan to ensure a sufficient number of qualified personnel were available to continue operations in the event that Local 1600 International Brotherhood of Electrical Workers (IBEW) personal engaged in a job action upon the expiration of their contract on August 26, 2018. Using guidance contained in NRC IP 92709, Contingency Plants for Licensee Strikes or Lockouts, the inspectors reviewed Susquehannas plans to address a potential job action at the site. On August 24, 2018, Susquehanna and IBEW, Local 1600, tentatively agreed to a new contract and union members subsequently approved the new contract. No job action was taken.

INSPECTION RESULTS

Observations 71152 Annual Follow-up of Selected Issues Condition Report CR-2017-17228, Cognitive trend of not effectively utilizing risk mitigation actions during emergent work

During 2016 and 2017, several examples of inadequate assessment and management of risk were identified, including an unplanned change to station risk that resulted in a Green non-cited violation (05000387/2017002-02), an inadvertent break of a daisy chained neutral while changing a light socket that resulted in single loop operations and a significant power transient, and an inadvertent electrical short during maintenance that resulted in a reactor scram.

Susquehanna performed a cause analysis on the events under CR-2017-17228. In all cases the cause was related to issues with human performance, communications, and not challenging assumptions. Corrective actions taken by Susquehanna included revision of the Emergent Work Checklist and the High Risk Challenge Board procedural guidance to include a requirement to consider the consequences prior to performing work. The station also revised procedure NDAP-QA-1902, Integrated Risk Management, to add a requirement for development of risk mitigation actions for a Yellow probabilistic risk assessment risk.

The inspectors reviewed the technical adequacy and depth of evaluations performed by the licensee for these issues. The inspectors also evaluated the licensees development and implementation of corrective actions in this area and concluded that they were reasonable.

Observations 71152 Annual Follow-up of Selected Issues Condition Report CR-2016-25721, Indications of fuel defect for Unit 2; CR-2017-10852, Debris failure identified for rod in fuel bundle V27452; and CR-2017-13888, Adverse trend of foreign material intrusion into fuel assemblies in Unit 2 reactor

In conjunction with Susquehannas fuel vendor, Susquehanna determined that the most probable cause of the fuel defect identified in fuel bundle V27452 in 2017 was debris fret caused by foreign material.

Susquehanna conducted a thorough technical review of their foreign material exclusion (FME)program under CR-2017-13888. Susquehanna determined that there was a lack of program ownership for the FME program combined with a lack of oversight by the line organizations in regards to FME controls. Corrective actions included assigning an FME coordinator to fill the vacant role at the station, assign individuals within each line organization to become the FME lead within that organization, and to reinstate monthly FME steering committee meetings.

The inspectors reviewed the corrective actions and determined Susquehannas overall response to the issues were commensurate with the safety significance, were timely, and were generally effective. The inspectors noted a high number of FME-related condition reports were generated during the previous refueling outage but acknowledge this is most likely the result of the increased focus and oversight on FME controls.

The inspectors reviewed the condition reports and determined they were being entered at an appropriately low threshold and were being addressed commensurate with their safety significance.

Observations 71152 Annual Follow-up of Selected Issues Condition Report CR-2017-00530, MRC requested further evaluation on trend slower than typical DG starts; CR-2017-11996, A DG start for SO-024-001A 10.1 seconds to frequency

The inspectors reviewed corrective action CR-2017-00530, which was initiated by Susquehanna staff on January 6, 2017, to evaluate a trend in slower EDG start times that still met technical specification requirements. Additionally, the inspectors reviewed CR-2017-11996 to evaluate and correct the A EDG not meeting starting time requirements.

The inspectors review of CR-2017-00530 determined that Susquehanna engineering staff concluded there was not an adverse trend because a review of records since January 2009 documented normal operating start times from 7 to 8.9 seconds. The review also determined Susquehanna staff were generating condition reports at a lower threshold which resulted in an increased number of condition reports. The inspectors concluded the evaluation was conducted with sufficient technical rigor to support the conclusions.

CR-2017-11996 indicated that the A EDG reached frequency in 10.16 seconds versus the required 10 seconds during testing on June 19, 2017. The inspectors determined that Susquehanna staff implemented the applicable technical specification requirements, evaluated the problem in sufficient detail to identify that pneumatic valves USY-9 and/or USCV-9 actuated slowly resulting in a pneumatic delay, and that other causes were reasonably ruled out. Susquehanna staff replaced these valves and planned actions to revise maintenance activities and schedules for the pneumatic shuttle valves. The evaluation further noted the pneumatic starting circuit is only present in test mode and is locked out during an emergency mode start. The inspectors concluded the evaluation was of sufficient detail to identify the likely cause of not meeting the required start time and provided for corrective actions that addressed the cause.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

On October 18, 2018, the inspectors presented the quarterly resident inspector inspection results to Mr. Kevin Cimorelli, Site Vice President, and other members of the Susquehanna staff.

DOCUMENTS REVIEWED

71111.01

Drawings

SSES Units 1 & 2 FSAR, Figure 2.5-22, Plot Plan, Revision 47

SSES Units 1 & 2 FSAR, Figure 2.5-17A, Extent of Rock and Soil Foundations, Revision 55

SSES Units 1 & 2 FSAR, Figure 2.5-40, Spray Pond Measured & Projected Water Levels,

Revision 47

SSES Units 1 & 2 FSAR, Figure 2.5-56, Profile of Slope North of Spray Pond, Revision 47

Miscellaneous

SSES-FSAR, 2.4 Hydrologic Engineering, Revision 66

71111.04

Drawings

M-151, Unit 1 P&ID RHR, Sheet 1, Revision 72

M-151ABD, Unit 1 Analysis Boundary Diagram RHR Div. 1, Sheet 2, Revision 7

M-112, Unit 1 P&ID RHR Service Water System, Sheet 1, Revision 2

M-151, Unit 1 P&ID RHR, Sheet 2, Revision 53

M-151ABD, Unit 1 Analysis Boundary Diagram RHR Div. 2, Sheet 4, Revision 5

M-151ABD, Unit 1 Analysis Boundary Diagram RHR, Sheet 3, Revision 5

M-112ABD, Common Analysis Boundary Diagram RHR Service Water System, Sheet 2,

Revision 5

M-134, Common P&ID E Diesel Auxiliaries (Fuel Oil System, Lube Oil System and Air Intake &

Exhaust System), Sheet 7, Revision 22

M-134, Common P&ID E Diesel Auxiliaries (Starting Air and Jacket Water Systems), Sheet 5,

Revision 23

M-134, Common P&ID Diesel E Auxiliaries (Starting Air System), Sheet 6, Revision 7

71111.05

Procedures

TQ-171, Susquehanna Fire Training Program, Revision 8

ON-013-001, Response to Fire, Revision 49

NDAP-QA-0445, Fire Brigade, Revision 21

Condition Reports

CR-2018-12060

CR-2018-12074

Miscellaneous

FP-013-189, Diesel Generator Bay A Fire Zone 0-41A, Elevations 677, 660 and 710,

Revision 4

Fire Brigade Quarterly Drill, Transient Combustibles Fire, Scenario #36

FP-013-140, Computer Room (C-202) Fire Zone 0-24E Elevation 698-0, Revision 7

FP-213-241, RHR Pump Room A (II-14) Fire Zone 2-1F Elevation 645-0 Revision 6

FP-113-101, Core Spray Pump Room A (I-17) Fire Zone 1-1A Elevation 645-0, Revision 5

FP-013-195, Diesel Generator Bay C Fire Zone 0-41C Elevations 677, 660 and 710,

Revision 5

FP-013-200, ESSW Pump House Loop A Pump Room (E-1) Fire Zone 0-51 Elevation 685-6,

Revision 4

FP-013-201, ESSW Pump House Loop B Pump Room (E-2) Fire Zone 0-52 Elevation 685-6,

Revision 4

71111.07

Procedures

MT-GM-031, Immersed Component/Heat Exchanger Internals Epoxy Lining/Cladding,

Revision 22

MT-GM-025, Heat Exchanger-Cleaning and Inspection, Revision 22

Work Orders

2093734

2112486

2133022

G0104-05

Drawings

M-111, Common P&ID Emergency Service Water System, Sheet 4, Revision 5

M-134, Common P&ID E Diesel Auxiliaries (Fuel Oil System, Lube Oil System and Air Intake &

Exhaust System), Sheet 7, Revision 22

71111.11

Procedures

GO-100-012, Power Maneuvers, Revision 53

OP-131-001, Rod Worth Minimizer RWM, Revision 17

NDAP-QA-0338, Reactivity Management and Controls Program, Revision 27

Condition Reports

CR-2018-11865

71111.12

Procedures

NDAP-QA-0413, Implementation of the Maintenance Rule, Revision 15

NDAP-QA-0483, Underground Piping and Tanks Program, Revision 6

Condition Reports

CR-2017-10847

CR-2017-18437

CR-2018-08960

CR-2018-12816

CR-2018-11207

CR-2018-11231

CR-2018-12238

CR-2018-12271

CR-2018-12276

CR-2018-12440

CR-2018-12564

CR-2018-12566

CR-2018-12817

CR-2018-12892

CR-2018-13215

CR-2018-13388

Action Requests

AR-2018-09858

AR-2018-12461

AR-2018-13434

AR-2018-13623

AR-2018-13830

AR-2018-14040

DI-2018-09779

Miscellaneous

General Electric Spec 22A7468, Sheet 10, Revision 3

Underground Vault Inspections 2013 to 2017

71111.13

Condition Reports

CR-2018-10666

CR-2018-11180

CR-2018-11762

CR-2018-11979

Drawings

M-142, Unit 1 P&ID Nuclear Boiler Vessel Instrumentation, Sheet 1, Revision 55

Miscellaneous

DLAP dated July 31, 2018

IOM 311-1, Tab 8 Vendor Supplied Instruments, Volume 1, Revision 15

NP-2-1, Control Room Panel, MPL H12-P609, Seismic Qualification Review, Revision 1

Protected Equipment list dated September 28, 2018

064C, Reactor Recirculation Systems and Motor Generator Set, Revision 12

71111.15

Procedures

NDAP-QA-0703, Operability Determinations and Functionality Assessments, Revision 31

Condition Reports

CR-2018-08841

CR-2018-09365

CR-2018-09496

CR-2018-11157

CR-2018-11159

CR-2018-12440

Action Requests

AR-2018-09929

AR-2018-12461

Work Orders

2181881

Drawings

E-214, Common Schematic Diagram HVAC Control Structure Chilled Water System Chilled B

Comp Motor, Sheet 2, Revision 28

E-214, Common Schematic Diagram HVAC Control Structure Chilled Water System Chilled

Cond Water Circ PP 0P170A&B, Sheet 5, Revision 17

E-214, Common Schematic Diagram Control Structure HVAC Chilled Water System Chilled

Water Circ Pump 0P162B, Sheet 19, Revision 10

M310-244, Common Schematic Diagram Control Structure Chilled Water System Chiller

0K112B, Sheet 2, Revision 7

E-214, Common Schematic Diagram Control Structure HVAC Chilled Water System Chilled

Water Circ PPS, Sheet 4, Revision 29

E-16, Unit 1 Circuit Breaker Interruption, Impact Drawing, DC Panel 1D614, Sheet 3,

Revision 23

Miscellaneous

Control Structure Chiller Response following Electrical Transient

Cases of ASME Boiler and Pressure Vessel Code, Case N-513-3

EP-115

71111.17

Procedures

GO-100-009, Single Recirculation Loop Operation, Revision 23

MT-GE-024, Installation and Removal of Oscillographic Recorder for Diesel Generator

Surveillances, Revision 28

MT-GM-092, Temporary Repair of Minor Pipe Leaks, Revision 0

NDAP-QA-0726, 10 CFR 50.59 and 10 CFR 72.48 Implementation, Revision 20

NDAP-QA-1218, Temporary Changes, Revision 17

OP-149-002, Residual Heat Removal Shutdown Cooling, Revision 58

Susquehanna 50.59 Resource Manual, Revision 8

Condition Reports (*initiated in response to inspection)

CR-2015-09176

CR-2015-22586

CR-2015-22822

CR-2015-26472

CR-2016-06540

CR-2016-07955

CR-2016-22888

CR-2018-10783

CR-2018-12308*

CR-2018-12310*

CR-2018-12337*

Work Orders

PCWO 1935310

Drawings

E-214, Sheet 12, Schematic Diagram Control Structure HVAC Chilled Water System Chilled

Water Circulating Pumps, Revision 16

M-151, Unit 1 Piping and Instrumentation Drawing (P&ID) Residual Heat Removal, Revision 72

M-157, Unit 1 Containment Atmos. Control Hardened Containment Vent System, Revision 0

Engineering Evaluations

EC-013-0022, Fire Protection Piping Pressure Losses, Revision 11

EC-013-1438, Examination of Appendix R Safe Shutdown Components with Regard to Fire

Suppression Activities, Revision 3

EC-FLOD-0001, Internal Flooding Evaluations for Moderate Energy Pipe Cracks and Sprinkler

System Actuation, Revision 3

Miscellaneous

Check-In Self-Assessment of the SSES 10 CFR 50.59 Program, dated April 20, 2018

Design Basis Document (DBD) 002, Control Structure HVAC and Chilled Water Systems,

Revision 2

DBD 043, Reactor Water Cleanup System, Revision 5

DBD 019, Fire Protection, Revision 7

Fire Protection Review Report, Revision 13

PLA-7321, Susquehanna Steam Electric Station Completion of Actions Required by NRC Order

EA-12-051, "Reliable Spent Fuel Pool Instrumentation," dated July 2, 2015

PLA-7542, Susquehanna Steam Electric Station 10 CFR 50.59 Summary Report and Changes

to Regulatory Commitments, dated October 24, 2016

PLA-7711, Report of Full Compliance with June 6, 2013, Commission Order Modifying Licenses

with Regard to Reliable Hardened Containment Vents Capable of Operation Under Severe

Accident Conditions, June 26, 2018

Technical Specifications - Susquehanna Steam Electric Station Unit 1, Revised June 28, 2018

Technical Specifications - Susquehanna Steam Electric Station Unit 2, Revised June 28, 2018

Updated Final Safety Analysis Report for Susquehanna Steam Electric Station, Revision 66

71111.19

Procedures

SO-054-A03, 92DY-ESW Flow Verif A Loop, Revision 18

SO-024-001D, Monthly Diesel Generator D Operability Test, Revision 27

SO-024-D01, Diesel Generator D Integrated Surveillance Test, Revision 1

OT-02-149, Diesel Generator E Restoration, Revision 2

MT-064-014, N-7500 Reactor Recirculating Pump Seal Rebuilding and Test, Revision 42

TP-164-045, Local System Leakage Test of Reactor Recirculation Loops A & B, Revision 10

Condition Reports

CR-2018-10666

CR-2018-10080

CR-2018-12055

Work Orders

1961035

2107565

2181918

2183442

2188571

2191979

2191984

2195198

2195226

71111.20

Condition Reports

CR-2018-12041

CR-2018-12048

CR-2018-12053

CR-2018-12054

CR-2018-12055

CR-2018-12056

CR-2018-12064

CR-2018-12078

CR-2018-12081

CR-2018-12092

CR-2018-12093

CR-2018-12097

CR-2018-12124

CR-2018-12134

CR-2018-12135

CR-2018-12146

CR-2018-12225

CR-2018-12250

CR-2018-12280

71111.22

Procedures

SO-151-A04, Quarterly Core Spray Valve Exercising Division 1, Revision 13

SO-100-106, Shiftly Surveillance Operating Log, Revision 118

SO-054-A03, Quarterly ESW Flow Verification Loop A, Revision 18

Condition Reports

CR-2018-10080

Action Requests

AR-2018-13417

71114.06

Miscellaneous

EP-PS-001, Emergency Planning Forms and Supplementary Instructions, Revision 14

Susquehanna Steam Electric Station Dose Assessment Summary

Final Timeline for Tabletop PI-New to be Conducted July 5, 2018

Drill Data Set, Unit 1

71124.08

Shipments17-046; 17-047;18-043; 18-047;18-057

71151

Condition Reports

CR-2018-10876

CR-2018-10985

DI-2016-25418

DI-2016-25423

DI-2017-00413

DI-2017-00588

DI-2017-19298

DI-2017-19309

DI-2018-01291

DI-2018-01143

71152

Equipment Apparent Cause Evaluation

CR-2017-11996

Condition Reports

CR-2016-18464

CR-2016-26216

CR-2016-27120

CR-2017-00530

CR-2017-17228

CR-2018-10285

CR-2018-11166

CR-2018-12195

Completed Surveillance, Performance, and Functional Tests

SO-024-001A, Monthly Diesel Generator A Operability Test, performed 3/24/18, 4/25/18 and

5/20/18

SO-024-001B, Monthly Diesel Generator B Operability Test, performed 3/25/18, 4/27/18 and

5/28/18

SO-024-001C, Monthly Diesel Generator C Operability Test, performed 4/4/18, 5/7/18 and

6/4/18

SO-024-001D, Monthly Diesel Generator D Operability Test, performed 4/13/18, 5/14/18 and

6/11/18

SO-024-001E, Monthly Diesel Generator E Test While Substituting for Another Diesel

Generator, performed 2/1/18, 3/5/18 and 3/28/18

Drawings

FF105801, Sh. 1, Common Standby Generator Set Control Diagram, Revision 9

FF105801, Sh. 2, Cooper Bessemer Control Diagram KSV-36-10, Revision 5

71153

Condition Reports

CR-2015-32449

CR-2015-32451

CR-2016-21657

CR-2017-12327

CR-2017-13014

Action Requests

AR-2017-14031

Miscellaneous

LER 50-388(387)/2017-006-00