ML19337A342: Difference between revisions

From kanterella
Jump to navigation Jump to search
(Created page by program invented by StriderTol)
(StriderTol Bot change)
 
Line 20: Line 20:
       "C          ' 3'4                                                                                                                      is ' w:: 84n etEcutATony a.w **wo A y
       "C          ' 3'4                                                                                                                      is ' w:: 84n etEcutATony a.w **wo A y
LICENSEE EVENT REPORT
LICENSEE EVENT REPORT
                   'ccNmot ni ocie i,                            l [[ l            I l@
                   'ccNmot ni ocie i,                            l (( l            I l@
t, (PLEASE PRINT OR TYPE ALL REQUIRED INFORMAT ONI lo li] l A ' LL'LENSEE 8        't    '8 l B lCooE          R l F l 1*5Ql 0 l0 l- lLICENSE L4 0 l0 l0    NuusEn l0 l0 l- l0 l0 l@4  ;6      26 l1    l1 Il l1 l@l57 C lJ@
t, (PLEASE PRINT OR TYPE ALL REQUIRED INFORMAT ONI lo li] l A ' LL'LENSEE 8        't    '8 l B lCooE          R l F l 1*5Ql 0 l0 l- lLICENSE L4 0 l0 l0    NuusEn l0 l0 l- l0 l0 l@4  ;6      26 l1    l1 Il l1 l@l57 C lJ@
UCENSE Tvrt JO                    A T 'a CON.
UCENSE Tvrt JO                    A T 'a CON.
10 l d J
10 l d J
h,2[[lcE                    lL hl0l510101012l5 19 hloIAkVENT              68 11DATEIn 19 In hlnIoInl4 IR In33j@
h,2((lcE                    lL hl0l510101012l5 19 hloIAkVENT              68 11DATEIn 19 In hlnIoInl4 IR In33j@
14      75        HEPoRT O A TE A                                %)              t>            DOCK ET %M8ga                      tv3 f.vf NT DESCRIPTION ANo MCBA8LE CONSEOuENCES h
14      75        HEPoRT O A TE A                                %)              t>            DOCK ET %M8ga                      tv3 f.vf NT DESCRIPTION ANo MCBA8LE CONSEOuENCES h
[o l:] l During normal operation, lightning apparently caused Athens 161 kV line to trip
[o l:] l During normal operation, lightning apparently caused Athens 161 kV line to trip

Latest revision as of 22:37, 15 March 2020

LER 80-059/03L-0:on 800810,during Normal Operation,Lightning Caused Athens 161 Kv Line to Trip Momentarily.Cooling Tower Transformer Tripped,Causing Loss of 4 Kv Tie Board.Cause of Transformer Trip Unknown.Athens Line re-energized
ML19337A342
Person / Time
Site: Browns Ferry Tennessee Valley Authority icon.png
Issue date: 09/04/1980
From:
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19337A338 List:
References
LER-80-059-03L-01, LER-80-59-3L-1, NUDOCS 8009090565
Download: ML19337A342 (2)


Text

=

"C ' 3'4 is ' w:: 84n etEcutATony a.w **wo A y

LICENSEE EVENT REPORT

'ccNmot ni ocie i, l (( l I l@

t, (PLEASE PRINT OR TYPE ALL REQUIRED INFORMAT ONI lo li] l A ' LL'LENSEE 8 't '8 l B lCooE R l F l 1*5Ql 0 l0 l- lLICENSE L4 0 l0 l0 NuusEn l0 l0 l- l0 l0 l@4 ;6 26 l1 l1 Il l1 l@l57 C lJ@

UCENSE Tvrt JO A T 'a CON.

10 l d J

h,2((lcE lL hl0l510101012l5 19 hloIAkVENT 68 11DATEIn 19 In hlnIoInl4 IR In33j@

14 75 HEPoRT O A TE A  %) t> DOCK ET %M8ga tv3 f.vf NT DESCRIPTION ANo MCBA8LE CONSEOuENCES h

[o l:] l During normal operation, lightning apparently caused Athens 161 kV line to trip

[o; ; gomentarily. Af ter one minute cooling tower transformer No. 1 tripped causing loss g.g gf Unit 3 4 kV bus tie board. After about 30 minutes the transf ormer was reener3Med ,

I g .] gnd it tripped again. Transformer was removed from service for testing and Athens ,

Io1+] ! 161 kV line reenergized. Diesel generators were available. No danger to health or j o l ] l safety of public. No previous occurrences. Re fe rence T. S . 3. 9. B.1.

L,TIO L_---- -

S t% TEM CAUSE CAUSE COMP VALVE CODE CoCE SUSCODE CO*APUNENT CODE SuecCOE SUSCOOE 101 ]n i

I E lA j g { g g lZ lg l Z l Z l Z l Z lZ l Z jg lZ lg ]g 9 to 11 17 13 is is 20 SE QUENil A L OCCUR AF'.CE REPORT 914 A '.

,,,. EVENT YE AH RE'OMT No coOE r*

  • E '..)

@ .. i.';g a ROi8IoI l-l 10lsI9l l/l l nl1 l [,,,LJ l,--J (,LJ 25 N /J 74 26 27 la 29 30 31 J.

A>F AcTfo -[N #L A T V T HOURS S8 er FC A ye SUPPL U *e

.. RE-LxJ@l zl@

' l z l@ LzJ@ 101010101 LvJ@ I42N i@ Iz l@ Iz !9 19 19 54 h J6 Ji 43 44 43 44 C li- DESCR6 prion AND CCH AECTIVE ACTIONS h I i i ] l There were no indications of what trinced the e r,n a f n ,--o ,-  % ci-nnie nv m o-e LLLl Lf eeind which could have trinced trmfor-ov. All c.ivron e vol ve n ., A % & @ -g g] l were tested. All trip indicators verified operable. Athens 161 KV line removed ,

,i]l from service temporarily to return transformer to service. No recurrence control

[,t 1l required. ,

i 4 9

'. i IJ . Pt/.VE R ONER h f A TUS 15 ERY J15CoVERY JESCRiprioN II l' l [_FJg l 0 l 7 l 3 $l NA l l Al@l Operator observed alarm A vi*, i r y .

TENT strLis un OF RELE ASE A90NNT CF ACTsviTV LOC Af ton oF RELEASE l l' Dj LzJ @ LzJ@l 7 4 1 10 N^ l I NA ,

ti 44 d5 l

2F 89%NNE t F w PoSUR E *.

l

NA

,,,,so .E,',NJ E S " '

wveE a DESCR'8 IiON I i I l lo_10 10 l@l12 NA  ;

' d i l

it I Ot;'d OH OAv s GE To F ACILITV l 1 v5 8 bE SC r*1P Tion i

WG)l tc NA

'tm 'O Tv gge t,Sr . gj, y

  • ,',i d t , OE SC hip TIOS4 LLL]g S[Njhl ,

NA l lllllll'll l*

1 <t 64 69

J AME op PnEPAsnit b009 PeiC N E .

. =

..- t iinnessee Valh y Authority Form DF-17

. Browns Ferry Nuclear Plant BF 15.2 1/10/79 LER SUPPLEMENTAL INFORMATION BFRO-50 3.9.B.1 259 / 8C59 Technical Specification Involved Repo'rted Under Technical Specification 6. 7. 2. M 2) .

Date of Occurrence 8/10/80 1639 1 Time of Occurrence _ Unit Identification and Description'of' Occurrence: During normal operation, lightning apparently_ caused the Athens 101 KV line to trip momentarily. Af ter about 1 minute cooling tower transformer No. 1 tripped causing a loss of Unit ,3 4 KV bus tie board.

After about 30 minutes the transformer was reenergized and it tripped again about 1 minute later. .There was no indication that protective current or sudden pressure relays had operated. The transfomer was removed from service for testing and the Athens 161 KV line reenergized.

Condicians prior to Occurrence:

Unit 1 @ 73%

Unit 2 @ 96%

Unit 3 @ 94%

Action :;pecified in the Technical Specification Surveillance Requirements met

!)up to inoper,61e equipment. Describe.

Diesel generators operable Apparent Cause of Occurrence: '

There was no indication of what tripped the transformer. No circuit probless were found which could have tripped the transformer.

,lnalysis of Occurrence:

There was no damage to plant equipment. There was no activity release, no personnel exposure or injury and no danger to the health or safety of the public.

Corrective Action:

All current. relays aad the transformer were tested. Trip indicators were verified operable. Af ter all transformer tests were completed the transformer was reenergized and loaded on 8/11/80. This appears to be a random trip and the trip circuit and feeder transfer scheme will be rechecked when permissible by Technical Specifications.

Athens 161 KV 'line was temporarily removed from ervice in order to reenergize the cooling tower transformer.

Failure Data:

N/A TRetention : . eriod - Lifetime; Responsibility - Administrative Supervisor

  • Hevision : . g\ / 5 Q/

-