|
---|
Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20029D0261994-04-22022 April 1994 LER 94-002-00:on 940329,inadvertent Automatic Closure of Primary Containment Isolation Valves & ESF Actuations Occurred Due to Malfunctioning Handswitch.Caused by Weak Electrical Contact Spring.Handswitch replaced.W/940422 Ltr ML20046B4961993-07-30030 July 1993 LER 93-008-00:on 930627,MCR Annunciator Alarmed Indicating That Outside Atmosphere Reactor Encl (Re) Negative Differential Pressure Decayed Due to Failure of Normal Re Ventilation Fan Motor.Subj Fan replaced.W/930730 Ltr ML20046C3961993-07-30030 July 1993 LER 92-011-01:on 920605,discovered Potential Physical Electrical Separation Deficiency in Panel 10C790.Plant Electrical Maint I&C Technicians Received Training on Electrical Separation Requirements ML20046B5051993-07-30030 July 1993 LER 91-015-01:on 910912,HPCI Sys Discovered to Be in Degraded Condition When HPCI Turbine Steam Supply Valve Failed to Fully Open.Recommendations of EPRI Improved MOV Lubricant Program implemented.W/930730 Ltr ML20046B5001993-07-30030 July 1993 LER 93-008-00:on 930630,determined That TS SR on Fire Rated Assemblies Not Satisfied Due to Personnel Error During Procedure Preparation.Surveillance Test Procedure ST-7-022-922-0 Will Be revised.W/930730 Ltr ML20046A4431993-07-19019 July 1993 LER 93-007-00:on 930617,alarm Indicated TIP Sys Shear Valve Was Inoperable.Cause Interminate.Isolated Occurrence. W/930719 Ltr ML20045D3931993-06-21021 June 1993 LER 93-007-00:on 930521,primary Containment Isolation Valve Inoperable & TS Action Statement & SR Not Implemented in Required Time.Caused by Personnel Error.Ltr Issued to Personnel Emphasizing Requirement ML20044E7431993-05-20020 May 1993 LER 93-002-01:on 930124,discovered That EDG Inoperable Since 930119 Due to Improperly Connected Wires in Circuit Breaker. Wires Restored to Proper Position & Tested Satisfactorily. Procedural & Training Changes Also Implemented ML20044D1761993-05-0707 May 1993 LER 87-028-01:on 870610,hourly Fire Watch Required by TS 3.7.7 Not Performed Due to Personnel Error.Plant Security Organization Accepted Responsibility for Hourly Firewatch Patrol Required by Ts,Effective 930104 ML20044C9231993-05-0505 May 1993 LER 93-004-00:on 930405,primary Containment & Reactor Vessel Isolation Control Sys Actuation Occurred During Test of NSSSS-refueling Area Ventilation Exhaust Duct.Caused by Personnel Error.Technician counseled.W/930505 Ltr ML20024H0901991-05-10010 May 1991 LER 91-007-00:on 910410,handling of Control Rod Prohibited by Tech Spec Surveillance Requirements 4.9.6.3b.Caused by Inadequate Procedure.Maint Procedure Changed Deleting Provisions to Reposition Mechanical stop.W/910510 Ltr ML20024G6981991-04-22022 April 1991 LER 91-003-00:on 910324,inadvertent Actuation of Reactor Protection Sys Occurred.Caused by Personnel Error.Procedural Guidance Developed,Shift Training Bulletin Issued & Operator Requalification Training Module revised.W/910422 Ltr ML20029A8251991-02-27027 February 1991 LER 91-005-00:on 910130,pressure Differential Switch Restored Incorrectly,Causing Spurious Drywell Pressure Signal & ESF Actuation.Caused by Personnel Error.Personnel Counseled & Warning Labels added.W/910227 Ltr ML20029A7101991-02-22022 February 1991 LER 91-004-00:on 910123,determined That TS Section 3.3.7.5 Surveillance Requirements Not Satisfied for Fuel Zone Level & Neutron Flux Instrumentation.Caused by Misinterpretation of Ts.Calibr Procedures revised.W/910222 Ltr ML20028H7121991-01-22022 January 1991 LER 90-035-00:on 901224,14 Valves Associated W/Various Sys & Required to Perform Function of Isolating Primary Containment Determined Inoperable.Caused by Installation Error During Initial const.W/910122 Ltr ML20028H6791991-01-18018 January 1991 LER 91-002-00:on 910109,replacement Cassette Drive Unit to Replace Inoperable Seismic Monitoring Sys Not Received by 910109,rendering Sys Inoperable for More than 30 Days.Caused by Grit on Gear.Sys repaired.W/910118 Ltr ML20024F7361990-12-0707 December 1990 LER 90-025-00:on 901110,spurious LOCA Signal Resulted in ESF actuations.W/901207 Ltr ML20028G9221990-09-26026 September 1990 LER 90-017-00:on 900828,ESF Actuation of Primary Containment & Reactor Vessel Isolation Control Sys Occurred.Caused by Technician Inadvertently Shorting Power Supply During Installation of Test Jack.Blown Fuse replaced.W/900926 Ltr ML20044A9761990-07-12012 July 1990 LER 90-013-00:on 900611,dc Distribution Sys Identified to Have Inadequate Isolation Capability Between Class IE & non-Class IE Components.Cause of Event Under Investigation. Hourly Fire Watches Established Until 900626.W/900712 Ltr ML20043C5231990-06-0101 June 1990 LER 90-003-01:on 900208,HPCI Sys Isolation Valve Inadvertently Isolated During Surveillance Test.Caused by Both Channels of Isolation Logic Being in Tripped Condition at Same Time.Isolation of HPCI Sys reset.W/900601 Ltr ML20043C3211990-05-30030 May 1990 LER 90-012-00:on 900426,inoperability of RHR Sys Modes Occurred Due to Physical Separation Deficiencies.Caused by Drawing Deficiency Resulting in Installation Error During Original Const.Nonclass 1E Cable sleeved.W/900530 Ltr ML20043B1331990-05-21021 May 1990 LER 90-011-00:on 900420,discovered That Emergency Svc Water Pump B Discharge Check Valve Not Preventing Reverse Flow. Caused by Personnel Error in That Actuating Arm Incorrectly Assembled.Actuating Arm repositioned.W/900521 Ltr ML20043B1311990-05-18018 May 1990 LER 90-006-01:on 900223,determined That Capability to Activate Emergency Public Notification Sys Sirens from Counties Lost from 900112-0205.Caused by Disconnection of Phone Lines.Lines Reconnected for All counties.W/900518 Ltr ML20043A7651990-05-17017 May 1990 LER 90-008-00:on 900417,HPCI Sys Isolation & Inoperability Occurred Due to Failure of Differential Pressure Transmitter.Cause of Transmittal Failure Under Investigation.Transmitter Returned to mfg.W/900517 Ltr ML20043A6321990-05-15015 May 1990 LER 89-060-01:on 891212,standby Gas Treatment Sys Charcoal Filter Discovered in Degraded Condition W/Possible Bypass Leakage Paths.Similar Condition Discovered on 891218.Caused by Holes in Charcoal Filter assemblies.W/900515 Ltr ML20043A4261990-05-15015 May 1990 LER 90-010-00:on 900415,ESF Actuation Occurred Closing Three Containment Isolation Valves for Analyzers.Cause Unknown. Isolation Reset,Analyzers Returned to Svc & Voltmeter Not Being Used Pending Determination of cause.W/900515 Ltr ML20042G0521990-05-0404 May 1990 LER 90-009-00:on 900405,control Room Chlorine Isolation of Habitability Control Room Isolation Sys & ESF Initiated. Caused by Failure of B Toxic Gas Detector & False Signal from Untested Analyzer.Detector replaced.W/900504 Ltr ML20012C9361990-03-12012 March 1990 LER 90-005-00:on 900211,no Fire Watch Insps for Rooms 103, 114 & 117 on Elevation 177 Ft in Reactor Encl Performed by Personnel.Caused by Personnel Error.Person Involved Disciplined.Training Program improved.W/900312 Ltr ML20012C5541990-03-12012 March 1990 LER 90-004-00:on 900209,station Personnel Discovered That on 890708,22-s Reactor Power Transient Occurred in Which Reactor Thermal Power Changed by More than 15% of Rated Thermal Power in 1 H.Procedure revised.W/900312 Ltr ML20012C7071990-03-12012 March 1990 LER 90-003-00:on 900208,HPCI Sys Inboard Isolation Valve Inadvertently Isolated & Closed When One Channel of Isolation Logic Tripped.Caused by Degradation of Darlington Output Transistor.Isolation reset.W/900312 Ltr ML20011F7911990-02-26026 February 1990 LER 90-002-00:on 900125,identified That Main Control Room Ventilation Sys Outside Design Basis.Caused by Misapplication of Design Basis Assumptions.No Immediate Actions Taken as Existing Procedures adequate.W/900226 Ltr ML20006E4271990-02-0909 February 1990 LER 90-001-00:on 900122,discovered That Monthly Instrument Channel Functional Test for RCIC Steam Supply Pressure Low Missed.Caused by Deficiency in Computer Program Used to Schedule Tests.Computer Program revised.W/900209 Ltr ML20006E3451990-02-0808 February 1990 LER 90-003-00:on 900112,primary Containment & Reactor Vessel Isolation Control Sys Isolation Signals Initiated, Closing Inboard & Outboard Isolation Valves for Rwcu.Caused by Lifting Relief Valve.Opening Time reset.W/900208 Ltr ML20006E2851990-02-0707 February 1990 LER 90-002-00:on 900105,containment H2/O2 Analyzer Declared Inoperable During Containment Inerting.Caused by Reversed Tubing Connections in Installation of Analyzer Due to Mislabeling.Analyzer restored.W/900207 Ltr ML20006D5171990-02-0707 February 1990 LER 90-001-00:on 900108,Tech Spec Violation & Reactor Encl Ventilation Isolation Occurred.Caused by Personnel Error. Chief Operator Counseled on Importance of Communicating All Pertinent info.W/900207 Ltr ML20006A8801990-01-19019 January 1990 LER 89-015-00:on 891223 & 24,problem W/Reactor Protection Sys (Rps)/Uninterruptable Power Supply Static Inverter Caused Loss of Power to RPS Panel.Caused by Failure of Gate Drive Boost Card.Isolations reset.W/900119 Ltr ML20005F9441990-01-10010 January 1990 LER 89-060-00:on 891212,standby Gas Treatment Sys Charcoal Filter a Discovered to Be Degraded W/Possible Bypass Leakage Paths.On 891218,filter B Found W/Similar Condition.Caused by Failure of Spot Welds.Filters repaired.W/900110 Ltr ML20005E6841990-01-0303 January 1990 LER 89-059-00:on 891206,instrumentation & Controls Technician Inadvertently Grounded Test Jack,Resulting in Blown Fuse.Caused by Personnel Error.Fuse Replaced. Technicians counseled.W/900103 Ltr ML20042D1961989-12-29029 December 1989 LER 89-009-02:on 890820 & 0925,RCIC Sys Injections Into RCS Occurred During Startup Test.From 891023-26,three HPCI Sys Injections Into RCS Occurred During Test.Injections Anticipated.Startup Tests performed.W/891229 Ltr ML20005E3301989-12-29029 December 1989 LER 89-014-00:on 891202,unexpected Actuation of Primary Containment & Reactor Vessel Isolation Control Sys Occurred. Caused by Insufficient Guidance in General Plant Procedure. Appropriate Procedures Reviewed & revised.W/891229 Ltr ML20005E0961989-12-26026 December 1989 LER 89-058-00:on 891123,actuation of Group III Primary Containment & Reactor Vessel Isolation Control Sys Resulted in Automatic Isolation of Rwcu.Caused by Failure of Flow Summer Card.Card replaced.W/891226 Ltr ML20011D2291989-12-19019 December 1989 LER 89-057-00:on 891120,refuel Floor Secondary Containment Isolated on Low Flow Differential Pressure,Causing Initiation of Standby Gas Treatment Sys.Caused by Severe Storm.Normal Ventilation Restored to floor.W/891219 Ltr ML19332F8631989-12-13013 December 1989 LER 89-056-00:on 891119,unexpected Nuclear Steam Supply Shutoff Sys Group Iii,Div 4 Isolation Initiated ESF Actuation.Caused by Defective read-set Selector Switch. Switch repositioned.W/891213 Ltr ML19332F7761989-12-11011 December 1989 LER 89-013-00:on 891110,reactor Scram Occurred Following Main Turbine Trip,Causing Initiation Signals on HPCI & RCIC Sys Due to Spiking of Level Transformers.Caused by Design Error.Hpci Turbine secured.W/891211 Ltr ML19332F7751989-12-11011 December 1989 LER 89-012-00:on 891110,RWCU Sys Differential Flow Oscillations Observed While Placing RWCU 2A Filter/ Demineralizer Into Svc.Caused by Leakage in Reactor HX Tube Side Safety Relief Valve.Valve removed.W/891211 Ltr ML19332F2961989-11-29029 November 1989 LER 89-009-01:on 890820,eight RCIC Sys Injections Into RCS Occurred Under Purview of Facility start-up Test Program. Caused by Abnormal Plant Conditions Requiring Safety Sys Actuations.Rcic & HPCI Sys Tests completed.W/891129 Ltr ML19332D6331989-11-27027 November 1989 LER 89-011-00:on 891027,outboard Nuclear Steam Supply Shutoff Sys Isolation Valves Isolated.Caused by Personnel Error Due to Lack of Attention to Detail by Technicians. Event Discussed at All Hands meeting.W/891127 Ltr ML19332D6251989-11-27027 November 1989 LER 89-055-00:on 891025,reactor Protection Sys 1A Shunt Trip Breaker Tripped on Undervoltage,Causing Loss of Power to Distribution Panel 1AY160 & ESF Isolation.Caused by Relief Valve Failures.Isolations reset.W/891127 Ltr ML19332C1781989-11-17017 November 1989 LER 89-053-00:on 891022,control Room Personnel Manually Initiated Ventilation Sys Chlorine Isolation,Esf.Caused by High Vinyl Chloride Concentration in Outside Air Intake Plenum.Special Event Procedure implemented.W/891117 Ltr ML19332B9841989-11-15015 November 1989 LER 89-054-01:on 891025,discovered That Daily Channel Check Surveillance Requirement for Channel D High Level Trip Not Met.Caused by Procedural Deficiency Since Initial Plant Operation.Associated Log Procedures revised.W/891115 Ltr 1994-04-22
[Table view] Category:RO)
MONTHYEARML20029D0261994-04-22022 April 1994 LER 94-002-00:on 940329,inadvertent Automatic Closure of Primary Containment Isolation Valves & ESF Actuations Occurred Due to Malfunctioning Handswitch.Caused by Weak Electrical Contact Spring.Handswitch replaced.W/940422 Ltr ML20046B4961993-07-30030 July 1993 LER 93-008-00:on 930627,MCR Annunciator Alarmed Indicating That Outside Atmosphere Reactor Encl (Re) Negative Differential Pressure Decayed Due to Failure of Normal Re Ventilation Fan Motor.Subj Fan replaced.W/930730 Ltr ML20046C3961993-07-30030 July 1993 LER 92-011-01:on 920605,discovered Potential Physical Electrical Separation Deficiency in Panel 10C790.Plant Electrical Maint I&C Technicians Received Training on Electrical Separation Requirements ML20046B5051993-07-30030 July 1993 LER 91-015-01:on 910912,HPCI Sys Discovered to Be in Degraded Condition When HPCI Turbine Steam Supply Valve Failed to Fully Open.Recommendations of EPRI Improved MOV Lubricant Program implemented.W/930730 Ltr ML20046B5001993-07-30030 July 1993 LER 93-008-00:on 930630,determined That TS SR on Fire Rated Assemblies Not Satisfied Due to Personnel Error During Procedure Preparation.Surveillance Test Procedure ST-7-022-922-0 Will Be revised.W/930730 Ltr ML20046A4431993-07-19019 July 1993 LER 93-007-00:on 930617,alarm Indicated TIP Sys Shear Valve Was Inoperable.Cause Interminate.Isolated Occurrence. W/930719 Ltr ML20045D3931993-06-21021 June 1993 LER 93-007-00:on 930521,primary Containment Isolation Valve Inoperable & TS Action Statement & SR Not Implemented in Required Time.Caused by Personnel Error.Ltr Issued to Personnel Emphasizing Requirement ML20044E7431993-05-20020 May 1993 LER 93-002-01:on 930124,discovered That EDG Inoperable Since 930119 Due to Improperly Connected Wires in Circuit Breaker. Wires Restored to Proper Position & Tested Satisfactorily. Procedural & Training Changes Also Implemented ML20044D1761993-05-0707 May 1993 LER 87-028-01:on 870610,hourly Fire Watch Required by TS 3.7.7 Not Performed Due to Personnel Error.Plant Security Organization Accepted Responsibility for Hourly Firewatch Patrol Required by Ts,Effective 930104 ML20044C9231993-05-0505 May 1993 LER 93-004-00:on 930405,primary Containment & Reactor Vessel Isolation Control Sys Actuation Occurred During Test of NSSSS-refueling Area Ventilation Exhaust Duct.Caused by Personnel Error.Technician counseled.W/930505 Ltr ML20024H0901991-05-10010 May 1991 LER 91-007-00:on 910410,handling of Control Rod Prohibited by Tech Spec Surveillance Requirements 4.9.6.3b.Caused by Inadequate Procedure.Maint Procedure Changed Deleting Provisions to Reposition Mechanical stop.W/910510 Ltr ML20024G6981991-04-22022 April 1991 LER 91-003-00:on 910324,inadvertent Actuation of Reactor Protection Sys Occurred.Caused by Personnel Error.Procedural Guidance Developed,Shift Training Bulletin Issued & Operator Requalification Training Module revised.W/910422 Ltr ML20029A8251991-02-27027 February 1991 LER 91-005-00:on 910130,pressure Differential Switch Restored Incorrectly,Causing Spurious Drywell Pressure Signal & ESF Actuation.Caused by Personnel Error.Personnel Counseled & Warning Labels added.W/910227 Ltr ML20029A7101991-02-22022 February 1991 LER 91-004-00:on 910123,determined That TS Section 3.3.7.5 Surveillance Requirements Not Satisfied for Fuel Zone Level & Neutron Flux Instrumentation.Caused by Misinterpretation of Ts.Calibr Procedures revised.W/910222 Ltr ML20028H7121991-01-22022 January 1991 LER 90-035-00:on 901224,14 Valves Associated W/Various Sys & Required to Perform Function of Isolating Primary Containment Determined Inoperable.Caused by Installation Error During Initial const.W/910122 Ltr ML20028H6791991-01-18018 January 1991 LER 91-002-00:on 910109,replacement Cassette Drive Unit to Replace Inoperable Seismic Monitoring Sys Not Received by 910109,rendering Sys Inoperable for More than 30 Days.Caused by Grit on Gear.Sys repaired.W/910118 Ltr ML20024F7361990-12-0707 December 1990 LER 90-025-00:on 901110,spurious LOCA Signal Resulted in ESF actuations.W/901207 Ltr ML20028G9221990-09-26026 September 1990 LER 90-017-00:on 900828,ESF Actuation of Primary Containment & Reactor Vessel Isolation Control Sys Occurred.Caused by Technician Inadvertently Shorting Power Supply During Installation of Test Jack.Blown Fuse replaced.W/900926 Ltr ML20044A9761990-07-12012 July 1990 LER 90-013-00:on 900611,dc Distribution Sys Identified to Have Inadequate Isolation Capability Between Class IE & non-Class IE Components.Cause of Event Under Investigation. Hourly Fire Watches Established Until 900626.W/900712 Ltr ML20043C5231990-06-0101 June 1990 LER 90-003-01:on 900208,HPCI Sys Isolation Valve Inadvertently Isolated During Surveillance Test.Caused by Both Channels of Isolation Logic Being in Tripped Condition at Same Time.Isolation of HPCI Sys reset.W/900601 Ltr ML20043C3211990-05-30030 May 1990 LER 90-012-00:on 900426,inoperability of RHR Sys Modes Occurred Due to Physical Separation Deficiencies.Caused by Drawing Deficiency Resulting in Installation Error During Original Const.Nonclass 1E Cable sleeved.W/900530 Ltr ML20043B1331990-05-21021 May 1990 LER 90-011-00:on 900420,discovered That Emergency Svc Water Pump B Discharge Check Valve Not Preventing Reverse Flow. Caused by Personnel Error in That Actuating Arm Incorrectly Assembled.Actuating Arm repositioned.W/900521 Ltr ML20043B1311990-05-18018 May 1990 LER 90-006-01:on 900223,determined That Capability to Activate Emergency Public Notification Sys Sirens from Counties Lost from 900112-0205.Caused by Disconnection of Phone Lines.Lines Reconnected for All counties.W/900518 Ltr ML20043A7651990-05-17017 May 1990 LER 90-008-00:on 900417,HPCI Sys Isolation & Inoperability Occurred Due to Failure of Differential Pressure Transmitter.Cause of Transmittal Failure Under Investigation.Transmitter Returned to mfg.W/900517 Ltr ML20043A6321990-05-15015 May 1990 LER 89-060-01:on 891212,standby Gas Treatment Sys Charcoal Filter Discovered in Degraded Condition W/Possible Bypass Leakage Paths.Similar Condition Discovered on 891218.Caused by Holes in Charcoal Filter assemblies.W/900515 Ltr ML20043A4261990-05-15015 May 1990 LER 90-010-00:on 900415,ESF Actuation Occurred Closing Three Containment Isolation Valves for Analyzers.Cause Unknown. Isolation Reset,Analyzers Returned to Svc & Voltmeter Not Being Used Pending Determination of cause.W/900515 Ltr ML20042G0521990-05-0404 May 1990 LER 90-009-00:on 900405,control Room Chlorine Isolation of Habitability Control Room Isolation Sys & ESF Initiated. Caused by Failure of B Toxic Gas Detector & False Signal from Untested Analyzer.Detector replaced.W/900504 Ltr ML20012C9361990-03-12012 March 1990 LER 90-005-00:on 900211,no Fire Watch Insps for Rooms 103, 114 & 117 on Elevation 177 Ft in Reactor Encl Performed by Personnel.Caused by Personnel Error.Person Involved Disciplined.Training Program improved.W/900312 Ltr ML20012C5541990-03-12012 March 1990 LER 90-004-00:on 900209,station Personnel Discovered That on 890708,22-s Reactor Power Transient Occurred in Which Reactor Thermal Power Changed by More than 15% of Rated Thermal Power in 1 H.Procedure revised.W/900312 Ltr ML20012C7071990-03-12012 March 1990 LER 90-003-00:on 900208,HPCI Sys Inboard Isolation Valve Inadvertently Isolated & Closed When One Channel of Isolation Logic Tripped.Caused by Degradation of Darlington Output Transistor.Isolation reset.W/900312 Ltr ML20011F7911990-02-26026 February 1990 LER 90-002-00:on 900125,identified That Main Control Room Ventilation Sys Outside Design Basis.Caused by Misapplication of Design Basis Assumptions.No Immediate Actions Taken as Existing Procedures adequate.W/900226 Ltr ML20006E4271990-02-0909 February 1990 LER 90-001-00:on 900122,discovered That Monthly Instrument Channel Functional Test for RCIC Steam Supply Pressure Low Missed.Caused by Deficiency in Computer Program Used to Schedule Tests.Computer Program revised.W/900209 Ltr ML20006E3451990-02-0808 February 1990 LER 90-003-00:on 900112,primary Containment & Reactor Vessel Isolation Control Sys Isolation Signals Initiated, Closing Inboard & Outboard Isolation Valves for Rwcu.Caused by Lifting Relief Valve.Opening Time reset.W/900208 Ltr ML20006E2851990-02-0707 February 1990 LER 90-002-00:on 900105,containment H2/O2 Analyzer Declared Inoperable During Containment Inerting.Caused by Reversed Tubing Connections in Installation of Analyzer Due to Mislabeling.Analyzer restored.W/900207 Ltr ML20006D5171990-02-0707 February 1990 LER 90-001-00:on 900108,Tech Spec Violation & Reactor Encl Ventilation Isolation Occurred.Caused by Personnel Error. Chief Operator Counseled on Importance of Communicating All Pertinent info.W/900207 Ltr ML20006A8801990-01-19019 January 1990 LER 89-015-00:on 891223 & 24,problem W/Reactor Protection Sys (Rps)/Uninterruptable Power Supply Static Inverter Caused Loss of Power to RPS Panel.Caused by Failure of Gate Drive Boost Card.Isolations reset.W/900119 Ltr ML20005F9441990-01-10010 January 1990 LER 89-060-00:on 891212,standby Gas Treatment Sys Charcoal Filter a Discovered to Be Degraded W/Possible Bypass Leakage Paths.On 891218,filter B Found W/Similar Condition.Caused by Failure of Spot Welds.Filters repaired.W/900110 Ltr ML20005E6841990-01-0303 January 1990 LER 89-059-00:on 891206,instrumentation & Controls Technician Inadvertently Grounded Test Jack,Resulting in Blown Fuse.Caused by Personnel Error.Fuse Replaced. Technicians counseled.W/900103 Ltr ML20042D1961989-12-29029 December 1989 LER 89-009-02:on 890820 & 0925,RCIC Sys Injections Into RCS Occurred During Startup Test.From 891023-26,three HPCI Sys Injections Into RCS Occurred During Test.Injections Anticipated.Startup Tests performed.W/891229 Ltr ML20005E3301989-12-29029 December 1989 LER 89-014-00:on 891202,unexpected Actuation of Primary Containment & Reactor Vessel Isolation Control Sys Occurred. Caused by Insufficient Guidance in General Plant Procedure. Appropriate Procedures Reviewed & revised.W/891229 Ltr ML20005E0961989-12-26026 December 1989 LER 89-058-00:on 891123,actuation of Group III Primary Containment & Reactor Vessel Isolation Control Sys Resulted in Automatic Isolation of Rwcu.Caused by Failure of Flow Summer Card.Card replaced.W/891226 Ltr ML20011D2291989-12-19019 December 1989 LER 89-057-00:on 891120,refuel Floor Secondary Containment Isolated on Low Flow Differential Pressure,Causing Initiation of Standby Gas Treatment Sys.Caused by Severe Storm.Normal Ventilation Restored to floor.W/891219 Ltr ML19332F8631989-12-13013 December 1989 LER 89-056-00:on 891119,unexpected Nuclear Steam Supply Shutoff Sys Group Iii,Div 4 Isolation Initiated ESF Actuation.Caused by Defective read-set Selector Switch. Switch repositioned.W/891213 Ltr ML19332F7761989-12-11011 December 1989 LER 89-013-00:on 891110,reactor Scram Occurred Following Main Turbine Trip,Causing Initiation Signals on HPCI & RCIC Sys Due to Spiking of Level Transformers.Caused by Design Error.Hpci Turbine secured.W/891211 Ltr ML19332F7751989-12-11011 December 1989 LER 89-012-00:on 891110,RWCU Sys Differential Flow Oscillations Observed While Placing RWCU 2A Filter/ Demineralizer Into Svc.Caused by Leakage in Reactor HX Tube Side Safety Relief Valve.Valve removed.W/891211 Ltr ML19332F2961989-11-29029 November 1989 LER 89-009-01:on 890820,eight RCIC Sys Injections Into RCS Occurred Under Purview of Facility start-up Test Program. Caused by Abnormal Plant Conditions Requiring Safety Sys Actuations.Rcic & HPCI Sys Tests completed.W/891129 Ltr ML19332D6331989-11-27027 November 1989 LER 89-011-00:on 891027,outboard Nuclear Steam Supply Shutoff Sys Isolation Valves Isolated.Caused by Personnel Error Due to Lack of Attention to Detail by Technicians. Event Discussed at All Hands meeting.W/891127 Ltr ML19332D6251989-11-27027 November 1989 LER 89-055-00:on 891025,reactor Protection Sys 1A Shunt Trip Breaker Tripped on Undervoltage,Causing Loss of Power to Distribution Panel 1AY160 & ESF Isolation.Caused by Relief Valve Failures.Isolations reset.W/891127 Ltr ML19332C1781989-11-17017 November 1989 LER 89-053-00:on 891022,control Room Personnel Manually Initiated Ventilation Sys Chlorine Isolation,Esf.Caused by High Vinyl Chloride Concentration in Outside Air Intake Plenum.Special Event Procedure implemented.W/891117 Ltr ML19332B9841989-11-15015 November 1989 LER 89-054-01:on 891025,discovered That Daily Channel Check Surveillance Requirement for Channel D High Level Trip Not Met.Caused by Procedural Deficiency Since Initial Plant Operation.Associated Log Procedures revised.W/891115 Ltr 1994-04-22
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217D1211999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Lgs,Units 1 & 2. with ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212A8861999-09-13013 September 1999 Safety Evaluation Authorizing First & Second 10 Yr Interval Inservice Insp Plan Requestss for Relief RR-01 ML20212A4481999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Limerick Generating Station,Units 1 & 2.With ML20211E9891999-08-20020 August 1999 LGS Unit 2 Summary Rept for 970228 to 990525 Periodic ISI Rept Number 5 ML20210L7051999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Limerick Generating Station,Units 1 & 2.With ML20209G0211999-06-30030 June 1999 GE-NE-B13-02010-33NP, Evaluation of Limerick Unit 2 Shroud Cracking for at Least One Fuel Cycle of Operation ML20209D7741999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Limerick Generating Station,Units 1 & 2 ML20207H8331999-05-31031 May 1999 Non-proprietary Rev 0 to 1H61R, LGS - Unit 2 Core Shroud Ultrasonic Exam ML20195G4651999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Lgs,Units 1 & 2 ML20209D7791999-05-31031 May 1999 Revised Monthly Operating Repts for May 1999 for Limerick Generating Station,Units 1 & 2 ML20195B3021999-05-0606 May 1999 Rev 0 to PECO-COLR-L2R5, COLR for Lgs,Unit 2 Reload 5 Cycle 6 ML20206N2901999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Limerick Generating Station,Units 1 & 2.With ML20195G4761999-04-30030 April 1999 Revised Monthly Operating Repts for Apr 1999 for Lgs,Units 1 & 2 ML20206D8971999-04-22022 April 1999 Rev 2 to PECO-COLR-L1R7, COLR for Lgs,Unit 2 Reload 7, Cycle 8 ML20205N8341999-04-0101 April 1999 Part 21 Rept Re Automatic Switch Co Nuclear Grade Series X206380 & X206832 Solenoid Valves Ordered Without Lubricants That Were Shipped with Std Lubrication to PECO & Tva.Affected Plants Were Notified ML20205N9311999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Limerick Generating Station,Units 1 & 2.With ML20204G9851999-03-11011 March 1999 Safety Evaluation Re Revised Emergency Action Levels for Limerick Generating Station,Units 1 & 2 ML20207J7461999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Limerick,Units 1 & 2.With ML20199G2371999-01-31031 January 1999 Rev 0 to NEDO-32645, Limerick Generating Station,Units 1 & 2 SRV Setpoint Tolerance Relaxation Licensing Rept ML20199L5301999-01-19019 January 1999 Special Rept:On 981214,seismic Monitor Was Declared Inoperable.Caused by Spectral Analyzer Not Running.Attempted to Reboot Sys & Then Sent Spectral Analyzer to Vendor for Analysis & Rework.Upgraded Sys Will Be Operable by 990331 B110078, Rev 1 to GE-NE-B1100786-01, Surveillance Specimen Program Evaluation for Limerick Generating Station,Unit 11998-12-31031 December 1998 Rev 1 to GE-NE-B1100786-01, Surveillance Specimen Program Evaluation for Limerick Generating Station,Unit 1 ML20205K0381998-12-31031 December 1998 PECO Energy 1998 Annual Rept. with ML20199F9611998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Limerick Generating Station.With ML20198C7151998-12-10010 December 1998 Rev 1 to COLR for LGS Unit 1,Reload 7,Cycle 8 ML20198A3871998-12-10010 December 1998 Safety Evaluation Supporting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power- Operated Gate Valves ML20206N4061998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Limerick Generating Station,Units 1 & 2.With ML20199E3281998-11-23023 November 1998 Rev 2 to PECO-COLR-L2R4, COLR for Lgs,Unit 2,Reload 4,Cycle 5 ML20195C9771998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Limerick Generating Station,Units 1 & 2.With ML20154H5691998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Limerick Generating Station,Units 1 & 2.With ML20151X3511998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Limerick Generating Station Units 1 & 2.With ML20237F0291998-08-27027 August 1998 Special Suppl Rept:On 960425,one Loose Part Detection Sys (Lpds) Was Identified to Be Inoperable.Initially Reported on 960531.Caused by Loose Parts Detector Module.Repairs Performed & Intermittent Ground No Longer Present ML20237D1041998-08-17017 August 1998 Books 1 & 2 of LGS Unit 1 Summary Rept for 960301-980521 Periodic ISI Rept 7 ML20237A7761998-08-10010 August 1998 SER Accepting Licensee Response to NRC Bulleting 95-002, Unexpected Clogging of RHR Pump Strainer While Operating in Suppression Pool Cooling Mode ML20236X7641998-07-31031 July 1998 Rev 0 to SIR-98-079, Response to NRC RAI Re RPV Structural Integrity at Lgs,Units 1 & 2 ML20237B4711998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Limerick Generating Station,Units 1 & 2 ML20236N6751998-07-0909 July 1998 Part 21 & Deficiency Rept Re Notification of Potential Safety Hazard from Breakage of Cast Iron Suction Heads in Apkd Type Pumps.Caused by Migration of Suction Head Journal Sleeve Along Lower End of Pump Shaft.Will Inspect Pumps ML20151Z4881998-06-30030 June 1998 GE-NE-B1100786-02, Surveillance Specimen Program Evaluation for Limerick Generating Station,Unit 2 ML20236P9781998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Limerick Generating Station,Units 1 & 2 ML20196K1801998-06-30030 June 1998 Annual 10CFR50.59 & Commitment Rev Rept for 970701-980630 for Lgs,Units 1 & 2. with ML20249B3501998-06-11011 June 1998 Rev 1 to PECO-COLR-L2R4, COLR for LGS Unit 2 Reload 4,Cycle 5 ML20249A5331998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Limerick Units 1 & 2 ML20247M7071998-05-14014 May 1998 Safety Evaluation Supporting Amend 128 to License NPF-39 ML20217Q5101998-05-0404 May 1998 Safety Evaluation Supporting Amend 127 to License NPF-39 ML20247H5071998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Limerick Generating Station ML20216F3601998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Limerick Generating Station,Units 1 & 2 ML20217M0791998-03-31031 March 1998 Safety Evaluation Supporting Amends 125 & 89 to Licenses NPF-39 & NPF-85,respectively ML20217D5701998-03-20020 March 1998 Part 21 Rept 40 Re Governor Valve Stems Made of Inconel 718 Matl Which Caused Loss of Governor Control.Control Problems Have Been Traced to Valve Stems Mfg by Bw/Ip.Id of Carbon Spacer Should Be Increased to at Least .5005/.5010 ML20216F9471998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Limerick Generating Station,Units 1 & 2 ML20216F3471998-02-28028 February 1998 Revised Monthly Operating Rept for Feb 1998 for Limerick Genrating Station,Unit 1 1999-09-30
[Table view] |
Text
g . - . ~ _
,x <
10 CFR 50e73 q ,
ra PHILADELPHIA ELECTRIC COMPANY i i
LIMERICK GENER ATING SYATION P.O. BOX A
- 5AN ATOG A. PENNSYLV ANI A 19464
. (215) 3271200 smt. 2000
- u. s. u.co uicx. u., e.c. December 11, 1989 u-...7".'."."."',*,.".u,. Docket No. 50-353 :
License No. NPF-85 U.S.. Nuclear Regulatory Commission Attn: Document Control ~ Desk- '
Washington, DC 20555
-SUBJFCT: Licensee Event Report Limerick Generating Station - Unit 2 This LER. reports the leakage of a Reactor Water Cleanup (RWCU) system safety relief valve which caused the Regenerative
' Heat Exchanger room temperature to increase. This resulted in an ,
isolation of the RWCU system due to a Nuclear Steam Supply l
-Shutoff System isolation actuation, an Engineered Safety Feature, l from a Steam Leakage Detection signal. i l:
L .
Reference:
Docket No. 50-353 a L .ReportLNumber: 2-89-012 j L Revision ~ Number: 00 g Event.Date: November 10, 1989 Report Date: December 11, 1989 Facility: Limerick Generating Station 1 P.O. Box A, Sanatoga, PA 19464 This LER is.being submitted pursuant to the requirements of
- 10 CFR 50.73(a)(2)(iv) . )
l l
Very truly yours,
\ ,
c CCE: kap cc: W. T. Russell, Administrator, Region I, USNRC T. J. Kenny, USNRC Senior Resident Inspector, LGS 8912190003 891211 PDR ADOCK 03000353 i 1
.J S ._. - _. FlD_C _ , _, __
a.
aseC Po,m att U 5. I"1ACLEA2 f.tiULATOAY COMMi&SION AP7CCygp OMS NO 3194 0104
, LICENSEE EVFNT REPORT (LER) '"~ "" 'l 2' S P ACILITY NAME til DOCKtY NUMeth 12) P A G8 '3' Limerick Generating Station, Unit 2 0 ls l0 [0 l0l 3 51 1 3 1 loFl 0 l 6 flTLE Idi e age of a Reactor Water leanup Safetv e alve Caused a Nuclear Steam Suppl utoff System Isolation etuation(R ating th ystem SVENT DAf t (53 LtR NUMstR 46) SitPORY DATE 171 OTHER P ActLifies INVOLVtO IS)
YtAR 'Ak OAv P Acitity NAwls DOCnti NUustR,si MONTH DAY YEAR -
8 8,Q , Qv,se MONTM vtAR 0(510l0l0l l l
~ ~
1l1 1l 0 8 9 8l9 0l1 l2 0l0 1 l2 1l1 8l9 0t5iOIOt0ill TMit REPORT IS BusMITTED PURSUANT TO TME REQUIREMENTS OF 10 CPR $:Ich.ca one er more et ene fonearm,) 111) 08006 W 20 402M 20 406tel X 90.73ieH2Hevi 73.71161 POWSR te.408teH1HQ 00.36teH1) to.73t.H2Het 73.71tsi
~ ~ - ~
'!?P 0 Ol910 a m umim e0.mmm e0nuH2H.ai OTMt R <s,-w M 4 -=r
( ,s .
- 0 405tsH1 Hall 80.73tell2Hil 90.73tsH2Hv6iiHAl Jsdal
's s. ,.m ..m -
20 40thW1Hivl 50.73teH2 Hill go.734.H2Hv4HHet
~ ~
.. 'Y? YMg: : M.40s hm HW 50.73hH2 %l 00.7hM2Hd LICINSit CONTACT ,OR THl3 LIR 4121 N&Mt TELt#MONE NUM98R ARIA CODE C. R. Endriss, Regulatory Engineer, Limerick Generating Stacion 21 115 3 l 2l 71-l 1 I 21010 l COMPLEf t ONE LING FOR LACH COMPONENT P AILURE Ot9CRISED IN THIS REPORT ttal M^N
CAust sysitM COMPON E NT MC- "EC"*'$
, [ cAust sysTIM cOMPONtNT "',y,'C' Rfn0R,T,Agt '
s-s X Cl E I I RlV Ll2l6 l5 N i i ; ; i ; s t s
s
m '
I I I I I I l I l I l 1 I I ' >
SUPPLEMENTAL REPORT EXPICTID (14l MONTM cay vtAR
~""] vis in re ,.M sutCtro suewssiO= 04rse T) NO ; i l A..Tx ACT ro,,,,, M = .o A. ,..,, .., ,m .,,- -. ...-,- A~., n ..
ABSTRACT On November 10, 1989, while placing the 2A Reactor Water Cleanup (RWCU) Filter /Demineralizer (F/D) into service, RWCU system differential flow oscillations were observed by Operations personnel. At 0700, a Nuclear Steam Supply Shutoff System (NSSSS) isolation actuation, an Engineered Safety Feature (ESP),
from a Steam Leakage Detection (SLD) signal (from a high RWCU Regenerative Heat Exchanger (RHX) room temperature) resulted in the automatic isolation of the'RWCU Outboard Primary Containment Isolation Valve (PCIV), HV-44-2F004. The RWCU system isolation was per design. Operations personnel performed an investigation
-determining that the RWCU isolation was due to steam leakage from the RHX tube side safety relief valve (PSV-44-209 - Lonergan Model D72G). The RWCU system remained isolated following the investigation until PSV-44-209 was removed and a blank flange was installed under a temporary circuit alteration. The RWCU system was returned to service on November 12, at 1350 hours0.0156 days <br />0.375 hours <br />0.00223 weeks <br />5.13675e-4 months <br />, after being isolated for approximately 55 hours6.365741e-4 days <br />0.0153 hours <br />9.093915e-5 weeks <br />2.09275e-5 months <br />. As a result of this event and other similar RWCU isolations, a re-evaluation of the potential failure mechanisms of the safety relief valve is being performed. As part of this evaluation, a different model relief valve has been installed on the RWCU system replacing PSV-44-209.
gR4,.m m. -
+ -
Ll'i [ . . 'h Pi , "g?
't
( nc P.ea. assa . U.s. hucktAR Klautatoav CouutssioN
, LICENSEE EVENT REPORT (LER) TEXT CONTINUATION '
EXPint8 8'3i 45 i Pacittiv haut m doca.tf Nuusin m ten huusta tes FAQt tai .
,,.. ..w.u... .. . e Limerick Generating Station, Unit 2 o l5 l0 jo jo l 3l5 l3 8l 9 -
0l1[2 -
0j0 012 N 016 i rtxr m u. . aa.a n. .m wc se, mu sa nn I
(
Plant Conditions Prior to the Event:1
- 4 Operating Condition: 1 (Power Operation). ,
Power Level: 90%
Description of the Event:-
On November-10,'1989, at 0700-hours, the Reactor' Water Cleanup (RWCU).(EIIS:CE) Outboard Primary Containment Isolation Valve
_(PCIV) (EIIS:ISV), HV-44-2F004, automatically isolated. This isolation was due.to a-Nuclear Steam Supply Shutoff System
'(NSSSS)((EIIS:JM) isolation actuation, an Engineered Safety .
a Feature (ESP), from a Steam Leakage Detection (SLD) (EIIS IJ) . y' isolation signal.
Operations personnel were placing the 2A RWCU Filter /Demineralizer (F/D) (EIIS FDM) into service per System '
- Procedure-S45,l'.B " Placing RWCU Filter /Demineralizer in Service,"
4 RWCU' flow-oscillations occurred. The F/D inlet valve (EIIS:V) '
was open and the F/D was pressurized to approximately 1100 psig
((see Figure 1).- When the F/D discharge valve (EIIS:FCV) was
- opened, to place the F/D in service, the "RWCU High Differential Flow Isolation Timer Initiated" annunciator (EIIS
- ANN) alarmed, and' cleared, several times. A System Engineer (SE).was
"~
, : dispatched-to the Auxiliary Equipment room to observe the RWCU differential flow instrumentation (EIIS:FFI).. The SE observed i flowloscillations on'the instrumentation from 30 gpm to 100 gpm.
Whil'e the SE was attempting to relay this information to the Main j Control Room operators, an isolation of the RWCU system occurred, -1
- at 0700 hours0.0081 days <br />0.194 hours <br />0.00116 weeks <br />2.6635e-4 months <br />. The isolation occurred when the Regenerative Heat Exchanger.(RHX) (EIIS:HX) room temperature sensing element (TE-44-2N016D) of the SLD system sensed a room temperature above its 122 degree Fahrenheit setpoint initiating a NSSSS, Group III, Division 4 isolation actuation. The RWCU isolation signal caused l the RWCU Outboard'PCIV, HV-44-2F004, to close. The isolation was j accompanied by a "Div.4 Steam Leak Det. Sys Hi Temp" annunciator i and was immediately followed by an automatic fire alarm code for , a the-" Reactor Enclosure Elevation 283 feet -' North East Area / East Side," which is for the area of the RHX room.
1
- Operations personnel conducted an investigation to determine the cause of the RWCU isolation and concluded that the RHX tube side Esafety relief valve, PSV-44-209 (Lonergan Model D72G) (EIIS
- RV),
was' leaking. During the investigation, an expected second NSSSS isolation actuation, initiated from a high RWCU system differential flow condition occurred, closing the RWCU Inboard g.a.
, g 3 . ,,,,
y-ne.g..,w ,-.w -<. *'w a >w' M' ' '- - - - - - - - - - ' ' ' - - - - - -
44 4 hRC f.qd 3891 U.$ huCLt&R Kl3ULATOAY COMMISS#ON
, LICENSEE EVENT REPORT (LER) TEXT CONTINUATION
to. ass e aiis P AC4LITV NAM 4 tts WOCKET hupata(28 i LtR huMSER t$p P&OS 133 vs." "ut.g." '
Limerick Generating Station, Unit 2 o l5 lo lo lo l 3l5 l3 Bj 9 -
0l1l 2 -
0l0 013 0F 0 16_
tnxrau nam .a m .m e cem w wIw (HV-44-2F001) and Outboard (HV-44-2P004) PCIVs, on November 10, at 1023 hour0.0118 days <br />0.284 hours <br />0.00169 weeks <br />3.892515e-4 months <br />.
The RWCU system remained isolated until PSV-44-209 was removed and a blank flange was installed using.a temporary circuit alteration. The RWCU system was returned to service on November 12, at 1350 hours0.0156 days <br />0.375 hours <br />0.00223 weeks <br />5.13675e-4 months <br />. The RWCU system was out of service'for approximately 55 hours6.365741e-4 days <br />0.0153 hours <br />9.093915e-5 weeks <br />2.09275e-5 months <br />.
A four hour notification was made to the NRC on November 10, at 1057 hours0.0122 days <br />0.294 hours <br />0.00175 weeks <br />4.021885e-4 months <br />, in accordance with the requirements of 10 CFR 50.72(b)(2)(li) since the event resulted in the automatic actuation of an ESP. Accordingly, this event is being reported in accordance with the requirements of 10 CPR 50.73(a)(2)(iv).
Consequences of the Event:
The consequences of this event were minimal. There was no release of radioactive material to the environment as a result of this event. The RWCU system isolated, as designed, when the RHX room temperature sensing element of the SLD system initiated a NSSSS Group III, Division 4 isolation signal. Had the RWCU Outboard isolation valve failed to close and steam continued to leak,-the redundant SLD/NSSSS channel (Inboard)_high temperature isolation signal would have initiated, isolating the RWCU system. -
The RWCU system was out of service for approximately 55 hours6.365741e-4 days <br />0.0153 hours <br />9.093915e-5 weeks <br />2.09275e-5 months <br />.
The Reactor Water purity remained within the limits specified by Technical Specifications. During that interval conductivity (an indicato' of Reactor Water purity) increased from a pre-event value of u.201 micro mhos per centimeter (cm) to a peak value of i 0.429 micro mhos per cm, on November 12. At 0100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br />, on November 15, the conductivity value was 0.115 micro mhos per cm indicating the return of Reactor Water purity to conditions better than prior to the event.
Cause of the Event:
K 1
The RWCU isolation was caused by the RHX tube side safety relief valve (PSV-44-209) leakage increasing the RHX room's temperature.
The RHX tube side safety relief valve leakage was possibly initiated by a pressure perturbation ~that occurred when the 2A RWCU F/D was placed in service. A root cause evaluation has determined the probable influences causing the valve leakage ga;,.a.M a...
PRC 4.es. 30e4 . U.S NUCLE AA E60VLAT03Y COMM5580N
,> LICENSEE EVENT REPORT (LER) TEXT CONTINUATION
soians e u u p m tetyasaettu docati NvMain m taa NUMata tge PACE @
n= "W.?:' 1. l';,?,?:
Limerick Generating Station, Unit 2 TLXT 15 mere sp.ce e rettererst ease eJabhanel MC form JbM 'st t1h 0 l5 l0 l0 lo l 3l5 l 3 8l 9 -
0l1l 2 -
0l0 014 0F 0l6 to be a combination of trapped air, system evolutions and operations, piping induced loads / vibrations, and thermal effects associated with these evolutions. Major elerants of the investigation included design reviews for tne heat exchanger, its relief valves, and their installation cc.ifiguration. Also included was a review of maintenance history, examinations of the failed valve, and the results of differential seat leakage and set pressure tests on a. spare valve. When the RHX tube side safety relief valve passed water, the water flashed to steam as it encountered the lower room pressure. - The flashed steam vented to the room via an open funnel drain, and increased the room temperature. The increased temperature was sensed by the SLD room temperature sensor and triggered the NSSSS isolation actuation of the RWCU system. Additionally, the water that flashed to steam in the RHX room initiated the'ior'izing chamber type smoke detector in the room and caused the Reactor Enclosure
-fire alarm code to activate.
l Corrective Actions:
Operations personnel evaluated the high RHX room temperature I isolation of the RWCU system and the alarms and annunciators that ,
L were received and concluded that a RWCU steam leak caused by a l leaking RHX safety relief valve had occurred. To confirm this, Operations personnel reset the RWCU isolation, on November 10, at 1008 hours0.0117 days <br />0.28 hours <br />0.00167 weeks <br />3.83544e-4 months <br />, using General Plant (GP) procedure, GP-8, " Primary
[ and Secondary Containment Isolation Verification and Reset." A portion of the RWCU system was pressurized and included the tube side of the RHX. As a result, Operations personnel verified that the RHX tube side safety relief valve, PSV-44-209, was leaking.
I' Continuing the investigation to determine if the RHX shell side L safety relief valve, PSV-44-208, was leaking required pressurizing the Non-Regenerative Heat Exchanger (NRHX) and the shell side of the RHX. The possibility that the pressurization could initiate a high differential flow condition of sufficient duration to initiate a second SLD/NSSSS isolation signal was considered by Operations personnel. Upon pressurizing the NRHX and the shell side of the RHX, a RWCU Inboard (HV-44-2F001) and Outboard (HV-44-2F004) PCIVs isolation occurred on high RWCU system differential flow as expected, at 1023 hours0.0118 days <br />0.284 hours <br />0.00169 weeks <br />3.892515e-4 months <br />. During the pressurization and subsequent isolation of the RWCU system, no leakage was evident from PSV-44-208.
The RWCU system remained isolated following the above investigation until PSV-44-209 was removed and a blank flange was installed under a temporary circuit alteration. The RWCU system was returned to service on November 12, at 1350 hours0.0156 days <br />0.375 hours <br />0.00223 weeks <br />5.13675e-4 months <br />.
lll**~ ***
mRC foem 3544 U.8 NUCLEAR 5 E3ULATDAY COMMIS$som
'1
. LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Anaovio ove =o vio-oio4 ExPep54 4'3115 f ACILITV NAME Ill JOCKET NVM88R (3) LER huMSERto: FAQt (3a n*= " h t.W.*
- Uff.O Limerick Generating Station, Unit 2 o 15 lo lo lo l 3l5 l3 8l 9 -
0l1l 2 -
0l0 015 OF 0l6 wuu wa.v.es.nem.a mcinmaanm Actions'Taken to Prevent Recurrence: .
-As identified in LER 88-009, Revision 3, submitted to the NRC on March'7, 1989, a modification was generated to minimize the possibility of air entering the system during maintenance, thus reducing the potential for relief' valve lifting due to trapped air and the associated system transient. Currently, air entering the pump suction and discharge piping between the block valves during system maintenance cannot be completely vented before returning the pump to service. As a result, an air slug can make its way into the system. This modification adds high point vents and demineralizer water fill connections to the RWCU pumps, thereby limiting the amount of air entering the system. This l modification will be implemented during future RWCU pump outages initiated due to pump seal failures.
l As a result of this event and sther similar RWCU i.solations, a re-evaluation of the potential failure mechanisms of the safety ;
relief valve is being performed. As part of this evaluation, a
): different model relief valve has been installed on the RWCU L system replacing PSV-44-209. The operation of the new style valve will be monitored to determine whether it is suitable for
' permanent use in both Unit 1 and Unit 2 RWCU systems.
!~
Suitability will be determined based on the safety relief valve i
performance during RWCU system evolutions and operations, piping induced loads / vibrations and thermal effects associated.with these evolutions. If the new model valve is not suitable, ,
additional' actions will be taken until a suitable valve and ,
system configuration are obtained.
l- Previous Similar Occurrences:
~.
LERs 1-86-040, 1-88-009, 1-89-033 and 1-89-055 reported isolations of the RWCU system due to leaking relief valves.
Previous evaluations of the relief valve failure mechanism were completed. In light of the new failures, the potential failure mechanisms are being re-evaluated for a more definitive cause and development of effective corrective actions. !
Tracking Code: B2 - Failure due to Abo ^rmal Wear g.o- u..
i 5 a3-. S*OEu$1no
. . au+s _k. I* .a OWZ(ww /
) B 2h EW.QOEp
- .(
6s
.ib, a = o82 a$5 3-
'I * " ' h.,
j awU o#C#hs'*C6 a d 0ua MwoC- * '# N i *ooMmm
-@ O- l O of Om o .
~E D l aE ag 1g}= iu R1Ig -
AEG - -
M%F Rr EER n AsO DsM E moo u H V- g
_e oLR m E g" na 0 aaA soc a 4 .
a srT c) 4-io c
am s
4
' Nti o
n 2
F s
A O S
V l y .
LTV W EHA -
VO*
As2 - AAL 2H FV LS 9 vC F KTV E E O-CH" AF A/
T O
a c
o D
O0 14 4
F C- 2 M' .
/
GD 2 : M c 2 r E r A n N oa .
WOF o#M ER nO o 3
2 :
xN w
[
v O O
s
.e -
eN
)E MR A T C.
O.
M
)
, g 2M FV O- _
UE ZR E
E N
S
' O0 M 44 4
R E P R
_, S A S W H V - C v-4 4-U 2 .
4 P F
. 2 U O -
H H H 0 M 2 4
E E E 9 P .
- VD* A A A AI2 yla T T T LSA Vll .
- vC-tH= il ER ER ER .
A xE XE XE .
CG CG
_ R/r CG CD HE HE HE E AN AN AN .
. N N N A'
_ G G G .
E E E R R R
~ -
+Fm
+ -
2' '2 _ _ - ~_ _
C **
_. 4
- + -
vN" A 2 <
L y
/ -
D V
+ . .
4,.
_ A 2 LL 0 VN *X VE" H H -
_ ET E E
_ F
_ 4
/ AH T AN T
_ D O O EN EN n
X- X-CR CR 2
F HE HE 0 AG AG 5 NE NE
_ 1 A V GN GN E E 4
- R R 6 6 R R
_, E E C C
_ > W - -_ - W
__ sp &.
r eg -
=