ML18100A753: Difference between revisions
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OEC 0 1 7993 ) | OEC 0 1 7993 ) | ||
Document Control Desk 2 NLR-N93192 Attachment (1) c Mr. J. c. Stone, Licensing Project Manager U.S. Nuclear Regulatory Commission One White Flint North 11555 Rockville Pike Rockville, MD 20852 Mr. c. s. Marschall (S09) | |||
USNRC Senior Resident Inspector Mr. T. T. Martin, Administrator - Region I U.S. Nuclear Regulatory Commission 475 Allendale Road King of Prussia, PA 19406 Mr. Kent Tosch, Manager, VI New Jersey Department of Environmental Protection | USNRC Senior Resident Inspector Mr. T. T. Martin, Administrator - Region I U.S. Nuclear Regulatory Commission 475 Allendale Road King of Prussia, PA 19406 Mr. Kent Tosch, Manager, VI New Jersey Department of Environmental Protection | ||
.Division of Environmental Quality Bureau of Nuclear Engineering CN 415 Trenton, NJ 08625 | .Division of Environmental Quality Bureau of Nuclear Engineering CN 415 Trenton, NJ 08625 | ||
._ "* 1 REF: NLR-N93192 | ._ "* 1 REF: NLR-N93192 | ||
Line 47: | Line 41: | ||
*~Qf-,_ 'da: o~ Al'* <p~ , 1993 | *~Qf-,_ 'da: o~ Al'* <p~ , 1993 | ||
- t>*> b.g&-h_~l2J\0U1.-r~ | - t>*> b.g&-h_~l2J\0U1.-r~ | ||
4 N tary Publ C f New Jersey KIMBERLY JO BROWN NOTARY PUBUC ~F NE~ ~~R~::e | 4 N tary Publ C f New Jersey KIMBERLY JO BROWN NOTARY PUBUC ~F NE~ ~~R~::e My Commission expires on My Commission Exp11es Ppra | ||
,J NLR-N93192 ATTACHMENT I During an NRC inspection conducted on September 5 - October 16, 1993, a violation of NRC requirements was identified. In accordance with the "General Statement of Policy and Procedure for NRC Enforcement Actions," 10 CFR Part 2, Appendix c (1992), | ,J NLR-N93192 ATTACHMENT I During an NRC inspection conducted on September 5 - October 16, 1993, a violation of NRC requirements was identified. In accordance with the "General Statement of Policy and Procedure for NRC Enforcement Actions," 10 CFR Part 2, Appendix c (1992), | ||
the violation is listed below: | |||
Salem Unit 1 Technical Specification (TS) Action Statement 3.3.2.1 requires that when an Engineered Safety Feature Actuation system instrumentation channel is inoperable, the Action shown in Table 3.3-3 of the TS must be taken. Table 3.3-3 specifies that when an automatic actuation logic channel for the safety injection, turbine trip and feedwater isolation function is inoperable, the inoperable channel must be restored to an operable status within six hours or the plant must be in Hot Standby within the next six hours and in Cold Shutdown within the following 30 hours. | Salem Unit 1 Technical Specification (TS) Action Statement 3.3.2.1 requires that when an Engineered Safety Feature Actuation system instrumentation channel is inoperable, the Action shown in Table 3.3-3 of the TS must be taken. Table 3.3-3 specifies that when an automatic actuation logic channel for the safety injection, turbine trip and feedwater isolation function is inoperable, the inoperable channel must be restored to an operable status within six hours or the plant must be in Hot Standby within the next six hours and in Cold Shutdown within the following 30 hours. | ||
Contrary to the above, at 5:30 a.m. on July 11, 1993, the Solid State Protection System Train B Feedwater Isolation Circuit at Salem Unit 1 failed a surveillance test, the failed channel was not subsequently restored to an operable status, and it was not until approximately 12 hours after the test failure that unit | Contrary to the above, at 5:30 a.m. on July 11, 1993, the Solid State Protection System Train B Feedwater Isolation Circuit at Salem Unit 1 failed a surveillance test, the failed channel was not subsequently restored to an operable status, and it was not until approximately 12 hours after the test failure that unit operators initiated a plant shutdown due to the | ||
.- inoperable channel. This is a Severity Level IV violation (Supplement 1). | .- inoperable channel. This is a Severity Level IV violation (Supplement 1). | ||
Pursuant to the provisions of 10 CFR 2.201, Public Service Electric and Gas Company is hereby required to submit to this office within 30 days of the date of the letter which transmitted this Notice, a written statement or explanation in reply, including: (1) the corrective steps which have been taken and the results achieved; (2) corrective steps which will be taken to avoid further violations; an.d (3) the date when full compliance will be achieved. | Pursuant to the provisions of 10 CFR 2.201, Public Service Electric and Gas Company is hereby required to submit to this office within 30 days of the date of the letter which transmitted this Notice, a written statement or explanation in reply, including: (1) the corrective steps which have been taken and the results achieved; (2) corrective steps which will be taken to avoid further violations; an.d (3) the date when full compliance will be achieved. | ||
: ) . | : ) . | ||
NLR-N93192 PSE&G RESPONSE PSE&G does not dispute. the violation ROOT CAUSE on July 11, 1993, operators were testing the Slave Relay K601 (Safety Injection circuit) in the "B" train of the Solid State Protection System (SSPS), using surveillance procedure Sl.OP-ST.SSP-0010~ During the performance of this surveillance, operations personnel stopped slave relay testing when a problem occurred in obtaining a test meter reading. Based upon an initial print review and past test circuit problems, operators believed that the problem was in the test circuit portion of the output relay. | |||
The SSPS system was not declared inoperable at this time, as the test circuit is independent of the normal SSPS function, and a work order was initiated to investigate the problem. Later on this date, .operations shift personnel were informed that the test circuit had not failed and that the surveillance results showed an SSPS circuit failure. | The SSPS system was not declared inoperable at this time, as the test circuit is independent of the normal SSPS function, and a work order was initiated to investigate the problem. Later on this date, .operations shift personnel were informed that the test circuit had not failed and that the surveillance results showed an SSPS circuit failure. | ||
** The SSPS (train B) was declared inoperable and the appropriate action statement was entered. Train "A" remained operable for the period such that full protection was available. | ** The SSPS (train B) was declared inoperable and the appropriate action statement was entered. Train "A" remained operable for the period such that full protection was available. | ||
The initial operability determination was based upon the Senior Reactor Operator's (SRO) technical knowledge, past experience, and review of available technical information. However, PSE&G's management review determined that the operability determination of the SSPS slave relay was not accurately diagnosed on July 11, 1993. *Additionally, PSE&G management noted that the SSPS action statement requirements, and the onset of initial troubleshooting were not commenced until the six hour action statement period had expired. Management determined that the initiation of troubleshooting was delayed inappropriately. | The initial operability determination was based upon the Senior Reactor Operator's (SRO) technical knowledge, past experience, and review of available technical information. However, PSE&G's management review determined that the operability determination of the SSPS slave relay was not accurately diagnosed on July 11, 1993. *Additionally, PSE&G management noted that the SSPS action statement requirements, and the onset of initial troubleshooting were not commenced until the six hour action statement period had expired. Management determined that the initiation of troubleshooting was delayed inappropriately. | ||
It is PSE&G's management expectation that system operability and timely pursuit of problem identification and resolution must be commensurate with the potential safety significance of the issue. | It is PSE&G's management expectation that system operability and timely pursuit of problem identification and resolution must be commensurate with the potential safety significance of the issue. | ||
The root cause of this event has been attributed to lack of appropriate oversight regarding the initiation of the troubleshooting activities. The review determined that the SSPS troubleshooting activities delay was inappropriate when considering the importance of the system and the short Technical Specification action statement requirement | The root cause of this event has been attributed to lack of appropriate oversight regarding the initiation of the troubleshooting activities. The review determined that the SSPS troubleshooting activities delay was inappropriate when considering the importance of the system and the short Technical Specification action statement requirement | ||
* CORRECTIVE ACTIONS TAKEN AND THE RESULTS ACHIEVED | * CORRECTIVE ACTIONS TAKEN AND THE RESULTS ACHIEVED | ||
: 1. Operations Department Management: | : 1. Operations Department Management: | ||
Line 74: | Line 63: | ||
Via the Night Order Book, issued instructions to all operating personnel regarding the appropriate action statement entry, including instruction to enter the SSPS action statement whenever abnormal readings are encountered during system tests. | Via the Night Order Book, issued instructions to all operating personnel regarding the appropriate action statement entry, including instruction to enter the SSPS action statement whenever abnormal readings are encountered during system tests. | ||
: 2. Positive disciplinary action has been taken with the appropriate personnel. | : 2. Positive disciplinary action has been taken with the appropriate personnel. | ||
CORRECTIVE STEPS WHICH WILL BE TAKER TO AVOID FURTHER VIOLATIONS PSE&G management strongly re-emphasized its expectation of taking timely corrective actions, specifically when dealing with Technical Specification systems or equipment. PSE&G believes | CORRECTIVE STEPS WHICH WILL BE TAKER TO AVOID FURTHER VIOLATIONS PSE&G management strongly re-emphasized its expectation of taking timely corrective actions, specifically when dealing with Technical Specification systems or equipment. PSE&G believes that adequate controls are now in place to address prompt and timely resolution of operability issues. | ||
DATE WHEN FULL COMPLIANCE WILL BE ACHIEVED PSE&G is in full compliance. | DATE WHEN FULL COMPLIANCE WILL BE ACHIEVED PSE&G is in full compliance. | ||
Public Service Electric and Gas Jo~eph | Public Service Electric and Gas Jo~eph | ||
*company | *company | ||
* J. Hagan Public Service Electric and Gas Company P.O. Box 236, Hancocks Bridge, NJ 08038 609-339-1200 Vice President - Nuclear Operations DECO 11993 NLR-N93192 United States Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Gentlemen: | * J. Hagan Public Service Electric and Gas Company P.O. Box 236, Hancocks Bridge, NJ 08038 609-339-1200 Vice President - Nuclear Operations DECO 11993 NLR-N93192 United States Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Gentlemen: | ||
RESPONSE TO NRC NOTICE OF VIOLATION INSPECTION REPORT 50-272/93-21; 50-311/93-21 DOCKET NOS. 50-272; 50-311 Public Service Electric and Gas (PSE&G) has received the NRC Inspection Report 50-272/93-21; 50-311/93-21, dated November 3, | RESPONSE TO NRC NOTICE OF VIOLATION INSPECTION REPORT 50-272/93-21; 50-311/93-21 DOCKET NOS. 50-272; 50-311 Public Service Electric and Gas (PSE&G) has received the NRC Inspection Report 50-272/93-21; 50-311/93-21, dated November 3, 1993. Within the scope of this report, a Salem Unit 1 Technical Specification Action Statement 3.3.2.1 violation was identified. | ||
Accordingly, in the attachment to this letter, PSE&G submits its assessment and response to the identified violation. | Accordingly, in the attachment to this letter, PSE&G submits its assessment and response to the identified violation. | ||
Should you have any questions regarding this transmittal, please do not hesitate to contact us. | Should you have any questions regarding this transmittal, please do not hesitate to contact us. | ||
Sincerely, | Sincerely, | ||
DEC 0 1 7993 Document Control Desk 2 | |||
DEC 0 1 7993 Document Control Desk | NLR-N93192 Attachment (1) c Mr. J. c. Stone, Licensing Project Manager U.S. Nuclear Regulatory Commission one White Flint North 11555 Rockville Pike Rockville, MD 20852 Mr. c. s. Marschall (S09) | ||
USNRC Senior Resident Inspector Mr. T. T. Martin, Administrator - Region I U.S. Nuclear Regulatory Commission 475 Allendale Road King of Prussia, PA 19406 Mr. Kent Tosch, Manager, VI New Jersey Department of Environmental Protection Division of Environmental Quality Bureau of Nuclear Engineering CN 415 Trenton, NJ 08625 | USNRC Senior Resident Inspector Mr. T. T. Martin, Administrator - Region I U.S. Nuclear Regulatory Commission 475 Allendale Road King of Prussia, PA 19406 Mr. Kent Tosch, Manager, VI New Jersey Department of Environmental Protection Division of Environmental Quality Bureau of Nuclear Engineering CN 415 Trenton, NJ 08625 | ||
\I REF: NLR-N93192 | \I REF: NLR-N93192 | ||
* STATE OF NEW JERSEY COUNTY.OF SALEM | * STATE OF NEW JERSEY COUNTY.OF SALEM | ||
Line 110: | Line 90: | ||
- 1* 1 J bv1._f.z ~ 1YJ~ OU l -'; \..._ | - 1* 1 J bv1._f.z ~ 1YJ~ OU l -'; \..._ | ||
4 N tary Publ C f New Jersey KIMBERLY JO BROWN My Commission expires on NOTARY PUBLIC OF NEW JERSEY | 4 N tary Publ C f New Jersey KIMBERLY JO BROWN My Commission expires on NOTARY PUBLIC OF NEW JERSEY | ||
~~~M~y~co=mm=-1ss~10~11E"xMpir~e'~~~pr~il*21.........,19~9~8~~~ | ~~~M~y~co=mm=-1ss~10~11E"xMpir~e'~~~pr~il*21.........,19~9~8~~~ | ||
. ~. | . ~. | ||
\I NLR-N93192 | \I NLR-N93192 ATTACHMENT I During an NRC inspection conducted on September 5 - October 16, 1993, a violation of NRC requirements was identified. In accordance with the "General Statement of Policy and Procedure for NRC Enforcement Actions," 10 CFR Part 2, Appendix C (1992), | ||
the violation is listed below: | the violation is listed below: | ||
Salem Unit 1 Technical Specification (TS) Action statement 3.3.2.1 requires that when an Engineered Safety Feature Actuation system instrumentation channel is inoperable, the Action shown in Table 3.3-3 of the TS must be taken. Table 3.3-3 specifies that when an automatic actuation logic channel for the safety injection, turbine trip and feedwater isolation function is inoperable, the inoperable channel must be restored to an operable status within six hours or the plant must be in Hot Standby within the next six hours and in Cold Shutdown within the following 30 hours. | Salem Unit 1 Technical Specification (TS) Action statement 3.3.2.1 requires that when an Engineered Safety Feature Actuation system instrumentation channel is inoperable, the Action shown in Table 3.3-3 of the TS must be taken. Table 3.3-3 specifies that when an automatic actuation logic channel for the safety injection, turbine trip and feedwater isolation function is inoperable, the inoperable channel must be restored to an operable status within six hours or the plant must be in Hot Standby within the next six hours and in Cold Shutdown within the following 30 hours. | ||
contrary to the above, at 5:30 a.m. on July 11, 1993, the Solid State Protection System Train B Feedwater Isolation Circuit at Salem Unit 1 failed a surveillance test, the failed channel was not subsequently restored to an operable status, and it was not until approximately 12 hours after the test failure that unit operators initiated a plant shutdown due to the | contrary to the above, at 5:30 a.m. on July 11, 1993, the Solid State Protection System Train B Feedwater Isolation Circuit at Salem Unit 1 failed a surveillance test, the failed channel was not subsequently restored to an operable status, and it was not until approximately 12 hours after the test failure that unit operators initiated a plant shutdown due to the | ||
* inoperable channel. This is a Severity Level IV violation (Supplement 1). | * inoperable channel. This is a Severity Level IV violation (Supplement 1). | ||
Pursuant to the provisions of 10 CFR 2.201, Public Service Electric and Gas Company is hereby required to submit to this office within 30 days of the date of the letter which transmitted this Notice, a written statement or explanation in reply, including: (1) the corrective steps which have been taken and the results achieved; (2) corrective steps which will be taken to avoid further violations; and (3) the date when full compliance will be achieved | Pursuant to the provisions of 10 CFR 2.201, Public Service Electric and Gas Company is hereby required to submit to this office within 30 days of the date of the letter which transmitted this Notice, a written statement or explanation in reply, including: (1) the corrective steps which have been taken and the results achieved; (2) corrective steps which will be taken to avoid further violations; and (3) the date when full compliance will be achieved | ||
* NLR-N93192 PSE&G RESPONSE PSE&G does not dispute the violation ROOT CAUSE On July 11, 1993, operators were testing the Slave Relay K601 (Safety Injection circuit) in the "B" train of the Solid State Protection System (SSPS), using surveillance procedure Sl.OP-ST.SSP-0010. During the performance of this surveillance, operations personnel stopped slave relay testing when a problem occurred in obtaining a test meter reading. Based upon an initial print review and past test circuit problems, operators believed that the problem was in the test circuit portion of the output relay. | * NLR-N93192 PSE&G RESPONSE PSE&G does not dispute the violation ROOT CAUSE On July 11, 1993, operators were testing the Slave Relay K601 (Safety Injection circuit) in the "B" train of the Solid State Protection System (SSPS), using surveillance procedure Sl.OP-ST.SSP-0010. During the performance of this surveillance, operations personnel stopped slave relay testing when a problem occurred in obtaining a test meter reading. Based upon an initial print review and past test circuit problems, operators believed that the problem was in the test circuit portion of the output relay. | ||
The SSPS system was not declared inoperable at this time, as the test circuit is independent of the normal SSPS function, and a work order was initiated to investigate the problem. Later on this date, .operations shift personnel were informed that the test circuit had not failed and that the surveillance results showed an SSPS circuit failure. | The SSPS system was not declared inoperable at this time, as the test circuit is independent of the normal SSPS function, and a work order was initiated to investigate the problem. Later on this date, .operations shift personnel were informed that the test circuit had not failed and that the surveillance results showed an SSPS circuit failure. | ||
Line 134: | Line 108: | ||
The root cause of this event has been attributed to lack of appropriate oversight regarding the initiation of the troubleshooting activities. The review determined that the SSPS troubleshooting activities delay was inappropriate when | The root cause of this event has been attributed to lack of appropriate oversight regarding the initiation of the troubleshooting activities. The review determined that the SSPS troubleshooting activities delay was inappropriate when | ||
* considering the importance of the system and the short Technical Specification action statement requirement . | * considering the importance of the system and the short Technical Specification action statement requirement . | ||
CORRECTIVE ACTIONS TAKEN AN.D THE RESULTS ACHIEVED | |||
: 1. Operations Department Management: | : 1. Operations Department Management: | ||
Reviewed the circumstances surrounding this event with the personnel involved and all other licensed operations personnel during requalification training. | Reviewed the circumstances surrounding this event with the personnel involved and all other licensed operations personnel during requalification training. |
Latest revision as of 05:05, 3 February 2020
ML18100A753 | |
Person / Time | |
---|---|
Site: | Salem |
Issue date: | 12/01/1993 |
From: | Hagan J Public Service Enterprise Group |
To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
References | |
NLR-N93192, NUDOCS 9312130414 | |
Download: ML18100A753 (12) | |
Text
Public Service Electric and Gas Company Joseph J. Hagan Public Service Electric and Gas Company P.O. Box 236, Hancocks Bridge, NJ 08038 609-339-1200 Vice President - Nuclear Operations DECO 11993 NLR-N93192 United states Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Gentlemen:
RESPONSE TO NRC NOTICE OF VIOLATION INSPECTION REPORT 50-272/93-21; 50-311/93-21 DOCKET NOS. 50-272; 50-311 Public Service Electric and Gas (PSE&G) has received the NRC Inspection Report 50-272/93-21; 50-311/93-21, dated November 3, 1993. Within the scope of this report, a Salem Unit 1 Technical Specification Action Statement 3.3.2.1 violation was identified.
Accordingly, in the attachment to this letter, PSE&G submits its assessment and response to the identified violation.
Should you have any questions regarding this transmittal, please do not hesitate to contact us.
Sincerely,
- ~D3R121A3D0414 931201 (i DCK 05000272 PI)R
~
Yi
OEC 0 1 7993 )
Document Control Desk 2 NLR-N93192 Attachment (1) c Mr. J. c. Stone, Licensing Project Manager U.S. Nuclear Regulatory Commission One White Flint North 11555 Rockville Pike Rockville, MD 20852 Mr. c. s. Marschall (S09)
USNRC Senior Resident Inspector Mr. T. T. Martin, Administrator - Region I U.S. Nuclear Regulatory Commission 475 Allendale Road King of Prussia, PA 19406 Mr. Kent Tosch, Manager, VI New Jersey Department of Environmental Protection
.Division of Environmental Quality Bureau of Nuclear Engineering CN 415 Trenton, NJ 08625
._ "* 1 REF: NLR-N93192
- STATE OF NEW JERSEY COUNTY.OF SALEM
)_
)
)
SS.
J. J. Hagan, being duly sworn according to law deposes and says:
I am Vice President - Nuclear Operations of Public Service Electric and Gas Company, and as such, I find the matters set forth in the above referenced letter, concerning the Salem Generating Station, Unit Nos. 1 and 2, are true to the best of my knowledge, information and belief.
Subscr,bed and wo Do before me
- ~Qf-,_ 'da: o~ Al'* <p~ , 1993
- t>*> b.g&-h_~l2J\0U1.-r~
4 N tary Publ C f New Jersey KIMBERLY JO BROWN NOTARY PUBUC ~F NE~ ~~R~::e My Commission expires on My Commission Exp11es Ppra
,J NLR-N93192 ATTACHMENT I During an NRC inspection conducted on September 5 - October 16, 1993, a violation of NRC requirements was identified. In accordance with the "General Statement of Policy and Procedure for NRC Enforcement Actions," 10 CFR Part 2, Appendix c (1992),
the violation is listed below:
Salem Unit 1 Technical Specification (TS) Action Statement 3.3.2.1 requires that when an Engineered Safety Feature Actuation system instrumentation channel is inoperable, the Action shown in Table 3.3-3 of the TS must be taken. Table 3.3-3 specifies that when an automatic actuation logic channel for the safety injection, turbine trip and feedwater isolation function is inoperable, the inoperable channel must be restored to an operable status within six hours or the plant must be in Hot Standby within the next six hours and in Cold Shutdown within the following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />.
Contrary to the above, at 5:30 a.m. on July 11, 1993, the Solid State Protection System Train B Feedwater Isolation Circuit at Salem Unit 1 failed a surveillance test, the failed channel was not subsequently restored to an operable status, and it was not until approximately 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> after the test failure that unit operators initiated a plant shutdown due to the
.- inoperable channel. This is a Severity Level IV violation (Supplement 1).
Pursuant to the provisions of 10 CFR 2.201, Public Service Electric and Gas Company is hereby required to submit to this office within 30 days of the date of the letter which transmitted this Notice, a written statement or explanation in reply, including: (1) the corrective steps which have been taken and the results achieved; (2) corrective steps which will be taken to avoid further violations; an.d (3) the date when full compliance will be achieved.
- ) .
NLR-N93192 PSE&G RESPONSE PSE&G does not dispute. the violation ROOT CAUSE on July 11, 1993, operators were testing the Slave Relay K601 (Safety Injection circuit) in the "B" train of the Solid State Protection System (SSPS), using surveillance procedure Sl.OP-ST.SSP-0010~ During the performance of this surveillance, operations personnel stopped slave relay testing when a problem occurred in obtaining a test meter reading. Based upon an initial print review and past test circuit problems, operators believed that the problem was in the test circuit portion of the output relay.
The SSPS system was not declared inoperable at this time, as the test circuit is independent of the normal SSPS function, and a work order was initiated to investigate the problem. Later on this date, .operations shift personnel were informed that the test circuit had not failed and that the surveillance results showed an SSPS circuit failure.
- The SSPS (train B) was declared inoperable and the appropriate action statement was entered. Train "A" remained operable for the period such that full protection was available.
The initial operability determination was based upon the Senior Reactor Operator's (SRO) technical knowledge, past experience, and review of available technical information. However, PSE&G's management review determined that the operability determination of the SSPS slave relay was not accurately diagnosed on July 11, 1993. *Additionally, PSE&G management noted that the SSPS action statement requirements, and the onset of initial troubleshooting were not commenced until the six hour action statement period had expired. Management determined that the initiation of troubleshooting was delayed inappropriately.
It is PSE&G's management expectation that system operability and timely pursuit of problem identification and resolution must be commensurate with the potential safety significance of the issue.
The root cause of this event has been attributed to lack of appropriate oversight regarding the initiation of the troubleshooting activities. The review determined that the SSPS troubleshooting activities delay was inappropriate when considering the importance of the system and the short Technical Specification action statement requirement
- CORRECTIVE ACTIONS TAKEN AND THE RESULTS ACHIEVED
- 1. Operations Department Management:
Reviewed the circumstances surrounding this event with the personnel involved and all other licensed operations personnel during requalification training.
Initiated SSPS surveillance procedure reviews and revision to direct attention to technical specification action statements when system performance is either deficient or operability is questionable. The procedures were revised to require that the system be declared inoperable when any deviation from the expected reading is obtained. Additionally, an Instrument &
Control technician will be present at all times during system testing.
Via the Night Order Book, issued instructions to all operating personnel regarding the appropriate action statement entry, including instruction to enter the SSPS action statement whenever abnormal readings are encountered during system tests.
- 2. Positive disciplinary action has been taken with the appropriate personnel.
CORRECTIVE STEPS WHICH WILL BE TAKER TO AVOID FURTHER VIOLATIONS PSE&G management strongly re-emphasized its expectation of taking timely corrective actions, specifically when dealing with Technical Specification systems or equipment. PSE&G believes that adequate controls are now in place to address prompt and timely resolution of operability issues.
DATE WHEN FULL COMPLIANCE WILL BE ACHIEVED PSE&G is in full compliance.
Public Service Electric and Gas Jo~eph
- company
- J. Hagan Public Service Electric and Gas Company P.O. Box 236, Hancocks Bridge, NJ 08038 609-339-1200 Vice President - Nuclear Operations DECO 11993 NLR-N93192 United States Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Gentlemen:
RESPONSE TO NRC NOTICE OF VIOLATION INSPECTION REPORT 50-272/93-21; 50-311/93-21 DOCKET NOS. 50-272; 50-311 Public Service Electric and Gas (PSE&G) has received the NRC Inspection Report 50-272/93-21; 50-311/93-21, dated November 3, 1993. Within the scope of this report, a Salem Unit 1 Technical Specification Action Statement 3.3.2.1 violation was identified.
Accordingly, in the attachment to this letter, PSE&G submits its assessment and response to the identified violation.
Should you have any questions regarding this transmittal, please do not hesitate to contact us.
Sincerely,
DEC 0 1 7993 Document Control Desk 2
NLR-N93192 Attachment (1) c Mr. J. c. Stone, Licensing Project Manager U.S. Nuclear Regulatory Commission one White Flint North 11555 Rockville Pike Rockville, MD 20852 Mr. c. s. Marschall (S09)
USNRC Senior Resident Inspector Mr. T. T. Martin, Administrator - Region I U.S. Nuclear Regulatory Commission 475 Allendale Road King of Prussia, PA 19406 Mr. Kent Tosch, Manager, VI New Jersey Department of Environmental Protection Division of Environmental Quality Bureau of Nuclear Engineering CN 415 Trenton, NJ 08625
\I REF: NLR-N93192
- STATE OF NEW JERSEY COUNTY.OF SALEM
)
)
)
SS.
J. J. Hagan, being duly sworn according to law deposes and says:
I am Vice President - Nuclear Operations of Public Service Electric and Gas Company, and as such, I find the matters set forth in the above referenced letter, concerning the Salem Generating Station, Unit Nos. 1 and 2, are true to the best of my knowledge, information and belief.
Subscr;bed and wo ~o before me
<~Qi:,, , da: 0:0 00 Yp /(l.,vi , 1993
- 1* 1 J bv1._f.z ~ 1YJ~ OU l -'; \..._
4 N tary Publ C f New Jersey KIMBERLY JO BROWN My Commission expires on NOTARY PUBLIC OF NEW JERSEY
~~~M~y~co=mm=-1ss~10~11E"xMpir~e'~~~pr~il*21.........,19~9~8~~~
. ~.
\I NLR-N93192 ATTACHMENT I During an NRC inspection conducted on September 5 - October 16, 1993, a violation of NRC requirements was identified. In accordance with the "General Statement of Policy and Procedure for NRC Enforcement Actions," 10 CFR Part 2, Appendix C (1992),
the violation is listed below:
Salem Unit 1 Technical Specification (TS) Action statement 3.3.2.1 requires that when an Engineered Safety Feature Actuation system instrumentation channel is inoperable, the Action shown in Table 3.3-3 of the TS must be taken. Table 3.3-3 specifies that when an automatic actuation logic channel for the safety injection, turbine trip and feedwater isolation function is inoperable, the inoperable channel must be restored to an operable status within six hours or the plant must be in Hot Standby within the next six hours and in Cold Shutdown within the following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />.
contrary to the above, at 5:30 a.m. on July 11, 1993, the Solid State Protection System Train B Feedwater Isolation Circuit at Salem Unit 1 failed a surveillance test, the failed channel was not subsequently restored to an operable status, and it was not until approximately 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> after the test failure that unit operators initiated a plant shutdown due to the
- inoperable channel. This is a Severity Level IV violation (Supplement 1).
Pursuant to the provisions of 10 CFR 2.201, Public Service Electric and Gas Company is hereby required to submit to this office within 30 days of the date of the letter which transmitted this Notice, a written statement or explanation in reply, including: (1) the corrective steps which have been taken and the results achieved; (2) corrective steps which will be taken to avoid further violations; and (3) the date when full compliance will be achieved
- NLR-N93192 PSE&G RESPONSE PSE&G does not dispute the violation ROOT CAUSE On July 11, 1993, operators were testing the Slave Relay K601 (Safety Injection circuit) in the "B" train of the Solid State Protection System (SSPS), using surveillance procedure Sl.OP-ST.SSP-0010. During the performance of this surveillance, operations personnel stopped slave relay testing when a problem occurred in obtaining a test meter reading. Based upon an initial print review and past test circuit problems, operators believed that the problem was in the test circuit portion of the output relay.
The SSPS system was not declared inoperable at this time, as the test circuit is independent of the normal SSPS function, and a work order was initiated to investigate the problem. Later on this date, .operations shift personnel were informed that the test circuit had not failed and that the surveillance results showed an SSPS circuit failure.
The SSPS (train B) was declared inoperable and the appropriate
- action statement was entered. Train "A" remained operable for the period such that full protection was available.
The initial operability determination was based upon the Senior Reactor Operator's (SRO) technical knowledge, past experience, and review of available technical information. However, PSE&G's management review determined that the operability determination of the SSPS slave relay was not accurately diagnosed on July 11, 1993.
- Additionally, PSE&G management noted that the SSPS action statement requirements, and the onset of initial troubleshooting were not commenced until the six hour action statement period had expired. Management determined that the initiation of troubleshooting was delayed inappropriately.
It is PSE&G's management expectation that system operability and timely pursuit of problem identification and resolution must be commensurate with the potential safety significance of the issue.
The root cause of this event has been attributed to lack of appropriate oversight regarding the initiation of the troubleshooting activities. The review determined that the SSPS troubleshooting activities delay was inappropriate when
- considering the importance of the system and the short Technical Specification action statement requirement .
CORRECTIVE ACTIONS TAKEN AN.D THE RESULTS ACHIEVED
- 1. Operations Department Management:
Reviewed the circumstances surrounding this event with the personnel involved and all other licensed operations personnel during requalification training.
Initiated SSPS surveillance procedure reviews and revision to direct attention to technical specification action statements when system performance is either deficient or operability is questionable. The procedures were revised to require that the system be declared inoperable when any deviation from the expected reading is obtained. Additionally, an Instrument &
Control technician will be present at all times during system testing.
Via the Night Order Book, issued instructions to all operating personnel regarding the appropriate action statement entry, including instruction to enter the SSPS action statement whenever abnormal readings are encountered during system tests.
- 2. Positive disciplinary action has been taken with the appropriate personnel .
- CORRECTIVE STEPS WHICH WILL BE TAKEN TO AVOID FURTHER VIOLATIONS PSE&G management strongly re-emphasized its expectation of taking timely corrective actions, specifically when dealing with Technical Specification systems or equipment. PSE&G believes that adequate controls are now in place to address prompt and timely resolution of operability issues.
DATE WHEN FULL COMPLIANCE WILL BE ACHIEVED PSE&G is in full compliance *