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{{#Wiki_filter:U.S. NUCLEAR REGULATORY COMMiy53ON NRCFORM3h5 O            7.77)
{{#Wiki_filter:U.S. NUCLEAR REGULATORY COMMiy53ON NRCFORM3h5 O            7.77)
LICENSEE EVENT P.EPORT Q .1 CO?.*nOLSLOCK.l                        l    l    l      l  l      l                    (PLEASE KINT OR TYTE ALL REQUIRED INPO%MATION) 1                                    6 lo t l I Ni ai o f c ! Pl 1 lhl 01 O I - l 0LICENSE                                                                                                                              i I
LICENSEE EVENT P.EPORT Q .1 CO?.*nOLSLOCK.l                        l    l    l      l  l      l                    (PLEASE KINT OR TYTE ALL REQUIRED INPO%MATION) 1                                    6 lo t l I Ni ai o f c ! Pl 1 lhl 01 O I - l 0LICENSE                                                                                                                              i I 8 2            LICENSEE CC35                  14    :S l 0    l  n  l NUMSER 01    n  !  -  l n25 l n26lhl LACENSE 4    l  1  1 1 TYPE  1 40  I  I 57l'h'C-T    68 @
            '
8 2            LICENSEE CC35                  14    :S l 0    l  n  l NUMSER 01    n  !  -  l n25 l n26lhl LACENSE 4    l  1  1 1 TYPE  1 40  I  I 57l'h'C-T    68 @
                                                                                                                                                         '                      ~"
                                                                                                                                                         '                      ~"
CON T
CON T
       - Folil                : Z,"c' F L }@l 01 5101010 l 21 I l 91@l o l 6 l 01318101@l75 017REPORT                                                  74 l n iDATEi l A l n80 l@
       - Folil                : Z,"c' F L }@l 01 5101010 l 21 I l 91@l o l 6 l 01318101@l75 017REPORT                                                  74 l n iDATEi l A l n80 l@
7        8                          63            61            DOCK ET NUM8 ER                68    69        EVENT CATE EVEN f OGSCRIPTION AND PROSABLE CONS 50UENCES h e.n-                    I
7        8                          63            61            DOCK ET NUM8 ER                68    69        EVENT CATE EVEN f OGSCRIPTION AND PROSABLE CONS 50UENCES h e.n-                    I
   --t c 1 :1 F --On -June 3.1980. while cerformino the isn12tinn ennaancer Anenmaetr
   --t c 1 :1 F --On -June 3.1980. while cerformino the isn12tinn ennaancer Anenmaetr t o i 3 i -l- - -sor Calibration and Test, the trio coints of 1 of the 4 reactne hinh                                                                                                        l i
  -
t o i 3 i -l- - -sor Calibration and Test, the trio coints of 1 of the 4 reactne hinh                                                                                                        l i
pressure isolation cencenser initiation switches were fnund en ha face                                                                                    -- - - 1 lo l4i I
pressure isolation cencenser initiation switches were fnund en ha face                                                                                    -- - - 1 lo l4i I
       - d o I &i+-                  conservative than that specified in T.S.2.3.9.                                                      Pressure switch RF-1RA                                          I 1
       - d o I &i+-                  conservative than that specified in T.S.2.3.9.                                                      Pressure switch RF-1RA                                          I 1
         - -i c i e s i              which had the, laroest discrenancv. was fnund en *rin ne                                                            inAR neig in-                                    !
         - -i c i e s i              which had the, laroest discrenancv. was fnund en *rin ne                                                            inAR neig in-                                    !
I O f 7. I          stead of 1068 osia as desired. The saferv sinnificanca af the avaer te                                                                                              I I
I O f 7. I          stead of 1068 osia as desired. The saferv sinnificanca af the avaer te                                                                                              I I
I o !s I                Considered minimal.                                                                                                                                                to
I o !s I                Considered minimal.                                                                                                                                                to sa                            sy:TEV                              CAUSE                                                            COMP.          VALVE CAUSE 000;              C00E        SUSC002                    00?/ PONE";* 0005                  $UE0001          SUSCOCE loisi i si Ol@ l xi@ W@ it IN is IT IR IU lh [1)h [Zj h 3          10                          12              12                                18          19              20 4                                                  11 S EQU E NTI AL                        QCCUPAENCE            REPCRT                        ' tVisl0N 4
              -
sa                            sy:TEV                              CAUSE                                                            COMP.          VALVE CAUSE 000;              C00E        SUSC002                    00?/ PONE";* 0005                  $UE0001          SUSCOCE loisi
* i si Ol@ l xi@ W@ it IN is IT IR IU lh [1)h [Zj h 3          10                          12              12                                18          19              20 4                                                  11 S EQU E NTI AL                        QCCUPAENCE            REPCRT                        ' tVisl0N 4
EVENTvuR                                  R EPORT NC.                                C00E                TYPE                            NO.
EVENTvuR                                  R EPORT NC.                                C00E                TYPE                            NO.
n wEs ao G ;5t.i;; I 81 0122                              l-l            lo 12121                    1/1            1 01 i!                Ltj          I-I              L.q) 32 21                    23              24              26        27              23        29          20            31 ACT'ON        Pi.' f u n g            EssECT          SMUTOOWN                                      ATTACMMENT            NPRO.4        PRIME COMP.                COMPCNENT TAKEN ACTICN                        CN PLANT            METHOO                    MOUR$ 22          $USMITTED        PORM bus.          SUP8 LIER            MANUPACTURER IEl@lZl@ IZl@
n wEs ao G ;5t.i;; I 81 0122                              l-l            lo 12121                    1/1            1 01 i!                Ltj          I-I              L.q) 32 21                    23              24              26        27              23        29          20            31 ACT'ON        Pi.' f u n g            EssECT          SMUTOOWN                                      ATTACMMENT            NPRO.4        PRIME COMP.                COMPCNENT TAKEN ACTICN                        CN PLANT            METHOO                    MOUR$ 22          $USMITTED        PORM bus.          SUP8 LIER            MANUPACTURER IEl@lZl@ IZl@
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             -11 til I                ition in that the instruments had effectivalv haan noe nf caruiro in s
             -11 til I                ition in that the instruments had effectivalv haan noe nf caruiro in s
         - I i i 21 ]                relaxed condition for about 6 months.                                            The cmrectiva actinn wac en ra-                                                      I
         - I i i 21 ]                relaxed condition for about 6 months.                                            The cmrectiva actinn wac en ra-                                                      I
        ...
         -liistI                    set the cressure switches to the desired spennine and avarrica the                                                                                                    l it 14 I I switches to ensure ornner nneratinn.                                                                                                                                  l 7        8 9                                                                                                                                                                              80 ST        S              % PCWER                        OTHER $7ATUS                  Dis        RY                            OlSCOVERY DESCRIPTics l
         -liistI                    set the cressure switches to the desired spennine and avarrica the                                                                                                    l it 14 I I
__. l t l 5 l l H lh l 01 01' 0lhl" NA l    d hl        ''
                                                                                                                                                                                    -
switches to ensure ornner nneratinn.                                                                                                                                  l 7        8 9                                                                                                                                                                              80 ST        S              % PCWER                        OTHER $7ATUS                  Dis        RY                            OlSCOVERY DESCRIPTics l
    -
__. l t l 5 l l H lh l 01 01' 0lhl"
            '
NA
                                                                                                          ''
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Sneveillance Test
Sneveillance Test
                                                                                                                                                                                                        *
                       ' ACTiv Tv CO$ TENT RELEAsss CP RELEAst                                                                                                            LOCATION CP RELEASE ltl6l j h d hl                                              AMcVNT  NA              OF ACTIVITY          l 45 hl                NA ao l
                       ' ACTiv Tv CO$ TENT RELEAsss CP RELEAst                                                                                                            LOCATION CP RELEASE ltl6l j h d hl                                              AMcVNT  NA              OF ACTIVITY          l 45 hl                NA ao l
r      a e                    10            ::                                            44
r      a e                    10            ::                                            44
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: 30. ;
: 30. ;
Donald A. Ross                                                                        201-499-8784 NAME OF SoE8ARGn                                                                                            PwCNE:                                                  {
Donald A. Ross                                                                        201-499-8784 NAME OF SoE8ARGn                                                                                            PwCNE:                                                  {
                                                                                                                                                                                          '
sco722o % 3
sco722o % 3
* yf
 
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yf Jersey Central Power & Light Company
Jersey Central Power & Light Company
     'r
     'r
    '  "  *
             .N            (4"    ()                                                    Madison Avenue at Pumh Bowl Road Mornstown, New Jersey 07960 (201)455-8200 OYSTER CREEK NUCLEAR GENERATING STATION Forked River, New Jersey 08731 Licensee Event Report Reportable Occurrence No. 50-219/80-22/3L Report Date July 1, 1980 Date of Occurrence June 3, 1980 identification of Occurrence Reactor high pressure isolation condenser initiation pressure switches RE-ISA, RE-ISB and RE-15C tripped at a value greater than that specified in the Technical Specifications, Section 2.3.5 This event is considered to be a recortable occurrence as defined in the Technical Specifications, paragraph 6.9.2.b. (1) .
             .N            (4"    ()                                                    Madison Avenue at Pumh Bowl Road Mornstown, New Jersey 07960 (201)455-8200 OYSTER CREEK NUCLEAR GENERATING STATION Forked River, New Jersey 08731 Licensee Event Report Reportable Occurrence No. 50-219/80-22/3L Report Date July 1, 1980 Date of Occurrence June 3, 1980 identification of Occurrence Reactor high pressure isolation condenser initiation pressure switches RE-ISA, RE-ISB and RE-15C tripped at a value greater than that specified in the Technical Specifications, Section 2.3.5 This event is considered to be a recortable occurrence as defined in the Technical Specifications, paragraph 6.9.2.b. (1) .
Conditions Prior to Occurrence Reactor coolant temperature 157.l*F Mode switch in refuel
Conditions Prior to Occurrence Reactor coolant temperature 157.l*F Mode switch in refuel
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the RE-15A, RE-158 and RE-15C trip points were found to be less conser-vative than that specified in the Technical Specifications. Surveillance test on the high reactor pressure switches for the isolation condenser system revealed the following data:
the RE-15A, RE-158 and RE-15C trip points were found to be less conser-vative than that specified in the Technical Specifications. Surveillance test on the high reactor pressure switches for the isolation condenser system revealed the following data:
Pressure Switch                      Desired Setpoint Designation              (Head Correction included)                  As Found            As Left RE-15A                                1068                              1088            1066 RE-158                                1068                              1081            1068 RE-15C                                1066                              1077            1064 RE-150                                1066                              1066            1066 Jersey Central Power & Ught Company is a Member of the General Public UtMties System
Pressure Switch                      Desired Setpoint Designation              (Head Correction included)                  As Found            As Left RE-15A                                1068                              1088            1066 RE-158                                1068                              1081            1068 RE-15C                                1066                              1077            1064 RE-150                                1066                              1066            1066 Jersey Central Power & Ught Company is a Member of the General Public UtMties System
                                                                                                      *
                                                                                                                *


      ..
     +t
     +t
   ,=l' Reportable Occurrence No. 50-219/80-22/3L                                  Page 2 July 1, 1990 Apparent Cause of Occurrence The cause of the occurrence can be attrituted to unusual service condition in that the instruments had effectively been out of service for approxi-mately 6 months. The instruments were last tested and calibrated on December 12, 1979 and were found to be operating properly. They had not been tested since the plant was shutdown on January 5, 1980; The instru-ments have been in a relaxed condition since then; except during the hydro-static test of the reactor pressure vessel (performed only 3 days before the test of the pressure switches),      i t is noted that the instrument was operating within its design accuracy.
   ,=l' Reportable Occurrence No. 50-219/80-22/3L                                  Page 2 July 1, 1990 Apparent Cause of Occurrence The cause of the occurrence can be attrituted to unusual service condition in that the instruments had effectively been out of service for approxi-mately 6 months. The instruments were last tested and calibrated on December 12, 1979 and were found to be operating properly. They had not been tested since the plant was shutdown on January 5, 1980; The instru-ments have been in a relaxed condition since then; except during the hydro-static test of the reactor pressure vessel (performed only 3 days before the test of the pressure switches),      i t is noted that the instrument was operating within its design accuracy.
Analysis of Occurrence The safety significance of this event is considered minimal since the pres-sure switches would have actuated but at a higher setpoint.          It should also be noted'that the pressure switches would not see this type of service condition during normal plant operation.
Analysis of Occurrence The safety significance of this event is considered minimal since the pres-sure switches would have actuated but at a higher setpoint.          It should also be noted'that the pressure switches would not see this type of service condition during normal plant operation.
-
Corrective Action immediate corrective action was to reset the pressure switches to the desired setpoint and exercise the switches to insure proper operation. No further action is contemplated.
Corrective Action immediate corrective action was to reset the pressure switches to the desired setpoint and exercise the switches to insure proper operation. No further action is contemplated.
Failure Data Barksdale Switch #82T A12SS Proof 1800 psi Adjustable range.50-J200 psi
Failure Data Barksdale Switch #82T A12SS Proof 1800 psi Adjustable range.50-J200 psi N
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Latest revision as of 20:03, 31 January 2020

LER 80-022/03L-0:on 800603,reactor High Pressure Isolation Condenser Initiation Switch Trip Points Found Less Conservative than Specified.Caused by Unusual Svc Condition. Pressure Switches Reset & Exercised to Ensure Operation
ML19329F930
Person / Time
Site: Oyster Creek
Issue date: 07/01/1980
From: Ross D
JERSEY CENTRAL POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19329F927 List:
References
LER-80-022-03L, LER-80-22-3L, NUDOCS 8007110373
Download: ML19329F930 (3)


Text

U.S. NUCLEAR REGULATORY COMMiy53ON NRCFORM3h5 O 7.77)

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--t c 1 :1 F --On -June 3.1980. while cerformino the isn12tinn ennaancer Anenmaetr t o i 3 i -l- - -sor Calibration and Test, the trio coints of 1 of the 4 reactne hinh l i

pressure isolation cencenser initiation switches were fnund en ha face -- - - 1 lo l4i I

- d o I &i+- conservative than that specified in T.S.2.3.9. Pressure switch RF-1RA I 1

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liiol l The cause of this occurrence can be attrihnted en nnnenal carvica e n n a -- --- - I I

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Donald A. Ross 201-499-8784 NAME OF SoE8ARGn PwCNE: {

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yf Jersey Central Power & Light Company

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.N (4" () Madison Avenue at Pumh Bowl Road Mornstown, New Jersey 07960 (201)455-8200 OYSTER CREEK NUCLEAR GENERATING STATION Forked River, New Jersey 08731 Licensee Event Report Reportable Occurrence No. 50-219/80-22/3L Report Date July 1, 1980 Date of Occurrence June 3, 1980 identification of Occurrence Reactor high pressure isolation condenser initiation pressure switches RE-ISA, RE-ISB and RE-15C tripped at a value greater than that specified in the Technical Specifications, Section 2.3.5 This event is considered to be a recortable occurrence as defined in the Technical Specifications, paragraph 6.9.2.b. (1) .

Conditions Prior to Occurrence Reactor coolant temperature 157.l*F Mode switch in refuel

. Reactor water level 170" All control rods at '00' Source range monitor ~25 cps Description of Occurrence On Tuesday, June 3,1980, at approximately 1000 bcurs, while performing the "Isolat*on Condenser Automatic Actuation Sensor Calibration and Test",

the RE-15A, RE-158 and RE-15C trip points were found to be less conser-vative than that specified in the Technical Specifications. Surveillance test on the high reactor pressure switches for the isolation condenser system revealed the following data:

Pressure Switch Desired Setpoint Designation (Head Correction included) As Found As Left RE-15A 1068 1088 1066 RE-158 1068 1081 1068 RE-15C 1066 1077 1064 RE-150 1066 1066 1066 Jersey Central Power & Ught Company is a Member of the General Public UtMties System

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,=l' Reportable Occurrence No. 50-219/80-22/3L Page 2 July 1, 1990 Apparent Cause of Occurrence The cause of the occurrence can be attrituted to unusual service condition in that the instruments had effectively been out of service for approxi-mately 6 months. The instruments were last tested and calibrated on December 12, 1979 and were found to be operating properly. They had not been tested since the plant was shutdown on January 5, 1980; The instru-ments have been in a relaxed condition since then; except during the hydro-static test of the reactor pressure vessel (performed only 3 days before the test of the pressure switches), i t is noted that the instrument was operating within its design accuracy.

Analysis of Occurrence The safety significance of this event is considered minimal since the pres-sure switches would have actuated but at a higher setpoint. It should also be noted'that the pressure switches would not see this type of service condition during normal plant operation.

Corrective Action immediate corrective action was to reset the pressure switches to the desired setpoint and exercise the switches to insure proper operation. No further action is contemplated.

Failure Data Barksdale Switch #82T A12SS Proof 1800 psi Adjustable range.50-J200 psi N

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