ML18102A769: Difference between revisions

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Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038-0236 Nuclear Business Unit JAN 191997 LR-N970039 U.S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 LER 272/96-040-00 SALEM GENERATING STATION - UNIT 1 FACILITY OPERATING LICENSE NO. D£R-70 DOCKET NO. 50-272.
Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038-0236 Nuclear Business Unit JAN 191997 LR-N970039 U.S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 LER 272/96-040-00 SALEM GENERATING STATION - UNIT 1 FACILITY OPERATING LICENSE NO. D£R-70 DOCKET NO. 50-272.
Gentlemen:
Gentlemen:
This Licensee Event Report entitled "Buffer Relays Omitted From Technical Specification Required Response Time Surveillance Tests" is being submitted pursuant to the requirements of the Code of Federal            Regula~ions    lOCFRSO. 73 (a) (2) (i) (B).
This Licensee Event Report entitled "Buffer Relays Omitted From Technical Specification Required Response Time Surveillance Tests" is being submitted pursuant to the requirements of the Code of Federal            Regula~ions    10CFRSO. 73 (a) (2) (i) (B).
Sincerely, G12f.~~/
Sincerely, G12f.~~/
General Manager Salem Operations Attachment
General Manager Salem Operations Attachment
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==SUBJECT:==
==SUBJECT:==
LER #272/96-040-00 DATE:              JAN 191997 Title:           Buffer Relays Omitted From Technical Specification Required Response Time Surveillance Tests
LER #272/96-040-00 DATE:              JAN 191997
 
==Title:==
Buffer Relays Omitted From Technical Specification Required Response Time Surveillance Tests
* Reportable under 10 CFR 73(a) (2) (i) (B) any event or condition prohibited by the plant's Technical Specifications.
* Reportable under 10 CFR 73(a) (2) (i) (B) any event or condition prohibited by the plant's Technical Specifications.
* Root Cause:
* Root Cause:

Latest revision as of 16:39, 30 November 2019

Forwards Memo Which Discusses Event Re LER 96-040-00
ML18102A769
Person / Time
Site: Salem PSEG icon.png
Issue date: 01/19/1997
From: Garchow D
Public Service Enterprise Group
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
Shared Package
ML18102A770 List:
References
LR-N970039, NUDOCS 9701240309
Download: ML18102A769 (2)


Text

Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038-0236 Nuclear Business Unit JAN 191997 LR-N970039 U.S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 LER 272/96-040-00 SALEM GENERATING STATION - UNIT 1 FACILITY OPERATING LICENSE NO. D£R-70 DOCKET NO. 50-272.

Gentlemen:

This Licensee Event Report entitled "Buffer Relays Omitted From Technical Specification Required Response Time Surveillance Tests" is being submitted pursuant to the requirements of the Code of Federal Regula~ions 10CFRSO. 73 (a) (2) (i) (B).

Sincerely, G12f.~~/

General Manager Salem Operations Attachment

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LER File 3.7 9701240309 970119 PDR ADOCK 05000272 S PDR The power is in your hands.

95-2168 REV. 6/94

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Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038-0236 Nuclear Business Unit

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TO: Lou Storz FROM: David F. Garchow

SUBJECT:

LER #272/96-040-00 DATE: JAN 191997

Title:

Buffer Relays Omitted From Technical Specification Required Response Time Surveillance Tests

  • Root Cause:

The cause of this occurrence was determined to be inadequate implementation of Technical Specification requirements. This resulted in inadequate procedures for testing of the ESFAS functions.

  • Systems affected:

Engineered Safety Feature Actuation System

  • There were no safety consequences with this LER. The health and safety of the public was not affected.
  • Corrective Actions:
1. The Salem Unit 2 time response procedures will be revised and testing of the omitted relays will be completed prior to Salem Unit 2 entering Mode 4.
2. The procedures for Salem Unit 1 will be revised and testing performed prior to Unit 1 entering Mode 4.
3. A Technical Specification Surveillance Improvement Program (TSSIP) has been initiated foL Salem Units 1 and 2. The scope and content of the TSSIP program was described previously in LER 311/96-008-00. The TSSIP review is expected to be completed by December 31, 1397.

The pmver is in your hands.

95-2168 REV. 6/94