Information Notice 1996-41, Effects of a Decrease in Feedwater Temperature on Nuclear Instrumentation: Difference between revisions

From kanterella
Jump to navigation Jump to search
(Created page by program invented by StriderTol)
(Created page by program invented by StriderTol)
 
(One intermediate revision by the same user not shown)
Line 3: Line 3:
| issue date = 07/26/1996
| issue date = 07/26/1996
| title = Effects of a Decrease in Feedwater Temperature on Nuclear Instrumentation
| title = Effects of a Decrease in Feedwater Temperature on Nuclear Instrumentation
| author name = Grimes B K
| author name = Grimes B
| author affiliation = NRC/NRR
| author affiliation = NRC/NRR
| addressee name =  
| addressee name =  
Line 14: Line 14:
| page count = 10
| page count = 10
}}
}}
{{#Wiki_filter:K) K) UNITED STATES NUCLEAR REGULATORY
{{#Wiki_filter:K)                               Ij


COMMISSION
K)
                                  UNITED STATES


===OFFICE OF NUCLEAR REACTOR REGULATION===
NUCLEAR REGULATORY COMMISSION
WASHINGTON, D.C. 20555-0001 July 26, 1996 NRC INFORMATION


NOTICE 96-41: EFFECTS OF A DECREASE IN FEEDWATER
OFFICE OF NUCLEAR REACTOR REGULATION


TEMPERATURE
WASHINGTON, D.C. 20555-0001 July 26, 1996 NRC INFORMATION NOTICE 96-41:    EFFECTS OF A DECREASE IN FEEDWATER TEMPERATURE


===ON NUCLEAR INSTRUMENTATION===
ON NUCLEAR INSTRUMENTATION


==Addressees==
==Addressees==
All holders of operating
All holders of operating licenses or construction permits for pressurized
 
licenses or construction
 
permits for pressurized


water reactors (PWRs).
water reactors (PWRs).


==Purpose==
==Purpose==
The U.S. Nuclear Regulatory
The U.S. Nuclear Regulatory Commission (NRC) is issuing this information
 
Commission (NRC) is issuing this information
 
notice to alert addressees
 
to the potential
 
for operation
 
above licensed power as a result of a decrease in feedwater
 
temperature
 
event affecting
 
nuclear instrumentation.
 
It is expected that recipients
 
will review the information
 
for applicability
 
to their facilities
 
and consider actions, as appropriate, to avoid similar problems.
 
However, suggestions


contained
notice to alert addressees to the potential for operation above licensed power


in this information
as a result of a decrease in feedwater temperature event affecting nuclear


notice are not NRC requirements;
instrumentation. It is expected that recipients will review the information
therefore, no specific action or written response is required.Description


of Circumstances
for applicability to their facilities and consider actions, as appropriate, to


On February 14, 1996, the licensee for the Comanche Peak Steam Electric Station was operating
avoid similar problems. However, suggestions contained in this information


Unit 2 at 95 percent rated thermal power near end-of-core life when a significant
notice are not NRC requirements; therefore, no specific action or written


reduction
response is required.


in feedwater
==Description of Circumstances==
On February 14, 1996, the licensee for the Comanche Peak Steam Electric


temperature
Station was operating Unit 2 at 95 percent rated thermal power near end-of- core life when a significant reduction in feedwater temperature occurred


occurred because of the loss of feedwater
because of the loss of feedwater heaters. This reduction, in turn, caused a


heaters. This reduction, in turn, caused a reduction
reduction in the reactor coolant system cold-leg temperatures. The colder


in the reactor coolant system cold-leg temperatures.
reactor coolant temperature, with a large negative moderator temperature


The colder reactor coolant temperature, with a large negative moderator
coefficient, caused reactor power to increase to approximately 102 percent


temperature
according to ex-core nuclear instrumentation. The nitrogen-16 (N-16)
detection system reached the overpower turbine runback setpoint (109 percent)
and initiated a turbine runback. The N-16 detection system measures N-16 activity in the primary coolant as a measure of the total power generation.


coefficient, caused reactor power to increase to approximately
This system is a substitute for the resistance temperature detector over- temperature and over-power reactor trip functions used at other Westinghouse


102 percent according
PWRs. The plant stabil zed at an indicated power of approximately 97 percent


to ex-core nuclear instrumentation.
according to the ex-core nuclear instrumentation.


The nitrogen-16 (N-16)detection
After approximately 90 minutes, a second similar turbine runback occurred


system reached the overpower
while restoring balance-of-plant equipment. Following this runback, reactor


turbine runback setpoint (109 percent)and initiated
power was stabilized at approximately 100 percent according to nuclear


a turbine runback. The N-16 detection
instrumentation. During the next 30 minutes, the reactor was operated at


system measures N-16 activity in the primary coolant as a measure of the total power generation.
approximately 100 percent power as indicated by nuclear instrumentation, with


This system is a substitute
reactor coolant temperatures below normal. The licensee noted that the N-16
9607220l 60ujo    i                        7            9,oi4 (R ~IE                ctG


for the resistance
IN 96-41 July 26, 1996 detection system indicated approximately 106 percent power and the computer- based plant calorimetric system indicated approximately 102 percent power.


temperature
Subsequently, the reactor power was reduced to less than 100 percent by all


detector over-temperature
indications.
 
and over-power
 
reactor trip functions
 
used at other Westinghouse
 
PWRs. The plant stabil zed at an indicated
 
power of approximately
 
97 percent according
 
to the ex-core nuclear instrumentation.
 
After approximately
 
90 minutes, a second similar turbine runback occurred while restoring
 
balance-of-plant
 
equipment.
 
Following
 
this runback, reactor power was stabilized
 
at approximately
 
100 percent according
 
to nuclear instrumentation.
 
During the next 30 minutes, the reactor was operated at approximately
 
100 percent power as indicated
 
by nuclear instrumentation, with reactor coolant temperatures
 
below normal. The licensee noted that the N-16 9 6 0 7 2 2 0l 6 0 ujo i 7 9,oi4 (R ~IE ctG
 
IN 96-41 July 26, 1996 detection
 
system indicated
 
approximately
 
106 percent power and the computer-based plant calorimetric
 
system indicated
 
approximately
 
102 percent power.Subsequently, the reactor power was reduced to less than 100 percent by all indications.


Discussion
Discussion


There are three aspects of this event which have generic implications.
There are three aspects of this event which have generic implications. First, with a loss of secondary plant efficiency, programmed T e can no longer


First, with a loss of secondary
reliably represent core thermal power. Second, the venturi-based input into


plant efficiency, programmed
the computer-based calorimetric system may not be accurate with cold


T e can no longer reliably represent
feedwater. And third, the final safety analysis report had not analyzed this


core thermal power. Second, the venturi-based
transient accurately.


input into the computer-based
Following the second runback, operators noted that reactor power indicated


calorimetric
<100 percent according to nuclear instrumentation. Although the operators


system may not be accurate with cold feedwater.
knew that cold feedwater could cause an increase in the amount of neutron


And third, the final safety analysis report had not analyzed this transient
attenuation, they believed that the nuclear instrumentation indicated


accurately.
conservatively (i.e., higher than actual) because they were maintaining TA"e


Following
approximately 1.7 eC [3 OF] above TRef. The licensee could not use the


the second runback, operators
computer-based calorimetric until some time after the second turbine runback


noted that reactor power indicated<100 percent according
due to maintenance activities. Te , based on the main turbine impulse


to nuclear instrumentation.
pressure, is programmed as a functlon of turbine load and, for normal


Although the operators knew that cold feedwater
efficiency, is a good representation of thermal power. When the unit lost the


could cause an increase in the amount of neutron attenuation, they believed that the nuclear instrumentation
feedwater heaters, the plant efficiency decreased. Because the main turbine


indicated conservatively (i.e., higher than actual) because they were maintaining
electro-hydraulic control system maintained generator output, core thermal


TA"e approximately
power increased to account for the loss of efficiency, and thus, TRef no


1.7 eC [3 OF] above T Ref. The licensee could not use the computer-based
longer accurately represented the core thermal power.


calorimetric
The cold-leg temperature is a more appropriate indicator of the accuracy of


until some time after the second turbine runback due to maintenance
the nuclear instrumentation than programmed TY.e. As the cold-leg temperature


activities.
decreased, the amount of neutron attenuation in the downcomer area surrounding


Te , based on the main turbine impulse pressure, is programmed
the core increased and hence affected the amount of neutrons reaching the


as a functlon of turbine load and, for normal efficiency, is a good representation
detectors. The licensee analysis showed that for every 0.6 C (1 OF] of cold- leg temperature change, the nuclear instrumentation was affected by 0.6 to 0.8 percent power. A review of the second transient showed that the cold-leg


of thermal power. When the unit lost the feedwater
temperature was approximately 2.5 &deg;C [4.5 OF] lower than when the detectors


heaters, the plant efficiency
were last calibrated. This corresponded to a 3 to 4 percent error, which


decreased.
corresponded to the difference in the actual versus the indicated power (104 percent actual versus 100 percent indicated).


Because the main turbine electro-hydraulic
During the review, the licensee noted that the computer-based calorimetric was


control system maintained
4 percent lower than the actual thermal power (N-16 power monitor). The


generator
calorimetric was based on feedwater flow measured by venturis. Although the


output, core thermal power increased
calorimetric calculation used feedwater temperature as an input, temperatures


to account for the loss of efficiency, and thus, TRef no longer accurately
significantly different than the normal 227 OC [440 OF] introduced errors into


represented
the calculation.


the core thermal power.The cold-leg temperature
Finally, the actual events involved temperature and power levels that exceeded


is a more appropriate
those in the analysis of the Decrease in Feedwater Temperature" event


indicator
presented in Chapter 15 of the licensee final safety analysis report. In that


of the accuracy of the nuclear instrumentation
IN 96-41 July 26, 1996 analysis, the inadvertent opening of the low-pressure heater bypass valve, coupled with the trip of the heater drain pumps, resulted in a feedwater


than programmed
temperature drop of less than 19 'C (35 OF], and a corresponding power


TY.e. As the cold-leg temperature
increase of less than 10 percent. In the actual event, the feedwater


decreased, the amount of neutron attenuation
temperature dropped by approximately 111 &deg;C (200 OF], and the licensee


in the downcomer
calculated that reactor power would have increased by approximately 35 percent


area surrounding
without operator or protective actions. The licensee determined that although


the core increased
the initiating events were the same, the Chapter 15 analysis did not account


and hence affected the amount of neutrons reaching the detectors.
for the loss of extraction steam to the high-pressure heaters, which was the


The licensee analysis showed that for every 0.6 C (1 OF] of cold-leg temperature
cause of the temperature difference. During the event, a level imbalance


change, the nuclear instrumentation
occurred between the two heater drain tanks, which resulted in the isolation
 
was affected by 0.6 to 0.8 percent power. A review of the second transient
 
showed that the cold-leg temperature
 
was approximately
 
2.5 &deg;C [4.5 OF] lower than when the detectors were last calibrated.
 
This corresponded
 
to a 3 to 4 percent error, which corresponded
 
to the difference
 
in the actual versus the indicated
 
power (104 percent actual versus 100 percent indicated).
 
During the review, the licensee noted that the computer-based
 
calorimetric
 
was 4 percent lower than the actual thermal power (N-16 power monitor).
 
The calorimetric
 
was based on feedwater
 
flow measured by venturis.
 
Although the calorimetric
 
calculation
 
used feedwater
 
temperature
 
as an input, temperatures


significantly
of extraction steam.


different
The NRC staff review of analyses of feedwater temperature events at similar


than the normal 227 OC [440 OF] introduced
facilities revealed that most of these analyses assumed similar initiating


errors into the calculation.
events as the Comanche Peak analysis and had similar conclusions concerning


Finally, the actual events involved temperature
the amount of feedwater temperature drop. The licensee has reanalyzed the


and power levels that exceeded those in the analysis of the Decrease in Feedwater
event to include a 119 OC [246 OF] feedwater temperature drop and concluded


Temperature" event presented
that all accident analysis parameters remained within requirements.


in Chapter 15 of the licensee final safety analysis report. In that
This information notice requires no specific action or written response. If


IN 96-41 July 26, 1996 analysis, the inadvertent
you have any questions about the information in this notice, please contact


opening of the low-pressure
one of the technical contacts listed below or the appropriate Office of


heater bypass valve, coupled with the trip of the heater drain pumps, resulted in a feedwater temperature
Nuclear Reactor Regulation project manager.


drop of less than 19 'C (35 OF], and a corresponding
Brian K. Grimes, Acting Director


power increase of less than 10 percent. In the actual event, the feedwater temperature
Division of Reactor Program Management
 
dropped by approximately
 
111 &deg;C (200 OF], and the licensee calculated
 
that reactor power would have increased
 
by approximately
 
35 percent without operator or protective
 
actions. The licensee determined
 
that although the initiating
 
events were the same, the Chapter 15 analysis did not account for the loss of extraction
 
steam to the high-pressure
 
heaters, which was the cause of the temperature
 
difference.
 
During the event, a level imbalance occurred between the two heater drain tanks, which resulted in the isolation of extraction
 
steam.The NRC staff review of analyses of feedwater
 
temperature
 
events at similar facilities
 
revealed that most of these analyses assumed similar initiating
 
events as the Comanche Peak analysis and had similar conclusions
 
concerning
 
the amount of feedwater
 
temperature
 
drop. The licensee has reanalyzed
 
the event to include a 119 OC [246 OF] feedwater
 
temperature
 
drop and concluded that all accident analysis parameters
 
remained within requirements.
 
This information
 
notice requires no specific action or written response.
 
If you have any questions
 
about the information
 
in this notice, please contact one of the technical
 
contacts listed below or the appropriate


Office of Nuclear Reactor Regulation
Office of Nuclear Reactor Regulation


project manager.Brian K. Grimes, Acting Director Division of Reactor Program Management
Technical contacts:  Harry A. Freeman, RIV


===Office of Nuclear Reactor Regulation===
(817) 897-1500
Technical
                    E-mail: haf~nrc.gov


contacts:
Chu-Yu Liang, NRR
Harry A. Freeman, RIV (817) 897-1500 E-mail: haf~nrc.gov


Chu-Yu Liang, NRR (301) 415-2878 E-mail: cylenrc.gov
(301) 415-2878 E-mail: cylenrc.gov


Attachment:  
Attachment: List Of Recently Issued HRC Information Notices
List Of Recently Issued HRC Information


Notices A1h4 Stir A Je6tQ
A1h4               Stir     A   Je6tQ


K> KJ Attachment
K>                           KJ


IN 96-41 July 26, 1996 LIST OF RECENTLY ISSUED NRC INFORMATION
Attachment


NOTICES Information
IN 96-41 July 26, 1996 LIST OF RECENTLY ISSUED


Date of Notice No. Subject Issuance Issued to 96-40 96-09, Supp. 1 96-39 96-38 Deficiencies
NRC INFORMATION NOTICES


in Material Dedication
Information                                  Date of


and Procure-ment Practices
Notice No.            Subject                Issuance  Issued to


and in Audits of Vendors Damage in Foreign Steam Generator
96-40          Deficiencies in Material      07/25/96    All holders of OLs or CPs


Internals Estimates
Dedication and Procure-                  for nuclear power reactors


of Decay Heat Using ANS 5.1 Decay Heat Standard May Vary Signi-ficantly Results of Steam Generator Tube Examinations
ment Practices and in


Inaccurate
Audits of Vendors


Reactor Water Level Indication
96-09,        Damage in Foreign Steam        07/10/96  All holders of OLs or CPs


and Inad-vertent Draindown
Supp. 1        Generator Internals                      for pressurized-water


During Shutdown Degradation
reactors


of Cooling Water Systems Due to Icing Failure of Safety Systems on Self-Shielded
96-39          Estimates of Decay Heat      07/05/96    All holders of OLs or CPs


Irradia-tors Because of Inadequate
Using ANS 5.1 Decay Heat                  for nuclear power reactors


Maintenance
Standard May Vary Signi- ficantly


and Training Hydrogen Gas Ignition during Closure Welding of a VSC-24 Multi-Assembly
96-38          Results of Steam Generator    06/21/96    All holders of OLs or CPs


Sealed Basket 07/25/96 07/10/96 07/05/96 06/21/96 06/18/96 06/12/96 06/11/96 05/31/96 All holders of OLs or CPs for nuclear power reactors All holders of OLs or CPs for pressurized-water
Tube Examinations                        for pressurized water


reactors All holders of OLs or CPs for nuclear power reactors All holders of OLs or CPs for pressurized
reactors


water reactors All pressurized
96-37          Inaccurate Reactor Water      06/18/96  All pressurized water


water reactor facilities
Level Indication and Inad-                reactor facilities holding


holding an operating
vertent Draindown During                  an operating license or a


license or a construction
Shutdown                                  construction permit


permit All holders of OLs or CPs for nuclear power reactors All U.S. Nuclear Regulatory
96-36          Degradation of Cooling        06/12/96  All holders of OLs or CPs


Commission
Water Systems Due to Icing                for nuclear power reactors


irradiator
96-35          Failure of Safety Systems      06/11/96  All U.S. Nuclear Regulatory


licensees
on Self-Shielded Irradia-                Commission irradiator


and vendors All holders of OLs or CPs for nuclear power reactors 96-37 96-36 96-35 96-34 OL -Operating
tors Because of Inadequate                licensees and vendors


License CP -Construction
Maintenance and Training


Permit
96-34          Hydrogen Gas Ignition          05/31/96  All holders of OLs or CPs


*~ -K> K IN 96-41 July 26, 1996 analysis, the inadvertent
during Closure Welding                    for nuclear power reactors


opening of the low-pressure
of a VSC-24 Multi-Assembly


heater bypass valve, coupled with the trip of the heater drain pumps, resulted in a feedwater temperature
Sealed Basket


drop of less than 19 *C [35 OF], and a corresponding
OL - Operating License


power increase of less than 10 percent. In the actual event, the feedwater temperature
CP - Construction Permit


dropped by approximately
*~  -                        K>                                          K


111 *C [200 OF], and the licensee calculated
IN 96-41 July 26, 1996 analysis, the inadvertent opening of the low-pressure heater bypass valve, coupled with the trip of the heater drain pumps, resulted in a feedwater


that reactor power would have increased
temperature drop of less than 19 *C [35 OF], and a corresponding power


by approximately
increase of less than 10 percent. In the actual event, the feedwater


35 percent without operator or protective
temperature dropped by approximately 111 *C [200 OF], and the licensee


actions. The licensee determined
calculated that reactor power would have increased by approximately 35 percent


that although the initiating
without operator or protective actions. The licensee determined that although


events were the same, the Chapter 15 analysis did not account for the loss of extraction
the initiating events were the same, the Chapter 15 analysis did not account


steam to the high-pressure
for the loss of extraction steam to the high-pressure heaters, which was the


heaters, which was the cause of the temperature
cause of the temperature difference. During the event, a level imbalance


difference.
occurred between the two heater drain tanks, which resulted in the isolation
 
During the event, a level imbalance occurred between the two heater drain tanks, which resulted in the isolation of extraction
 
steam.The NRC staff review of analyses of feedwater
 
temperature
 
events at similar facilities
 
revealed that most of these analyses assumed similar initiating
 
events as the Comanche Peak analysis and had similar conclusions


concerning
of extraction steam.


the amount of feedwater
The NRC staff review of analyses of feedwater temperature events at similar


temperature
facilities revealed that most of these analyses assumed similar initiating


drop. The licensee has reanalyzed
events as the Comanche Peak analysis and had similar conclusions concerning


the event to include a 119 *C [246 OF] feedwater
the amount of feedwater temperature drop. The licensee has reanalyzed the


temperature
event to include a 119 *C [246 OF] feedwater temperature drop and concluded


drop and concluded that all accident analysis parameters
that all accident analysis parameters remained within requirements.


remained within requirements.
This information notice requires no specific action or written response. If


This information
you have any questions about the information in this notice,-please contact


notice requires no specific action or written response.
one of the technical contacts listed below or the appropriate Office of


If you have any questions
Nuclear Reactor Regulation project manager.


about the information
Original signed by Brian K.Grimes


in this notice,-please
Brian K. Grimes, Acting Director


contact one of the technical
Division of Reactor Program Management
 
contacts listed below or the appropriate


Office of Nuclear Reactor Regulation
Office of Nuclear Reactor Regulation


project manager.Original signed by Brian K. Grimes Brian K. Grimes, Acting Director Division of Reactor Program Management
Technical contacts:          Harry A. Freeman, RIV


===Office of Nuclear Reactor Regulation===
(817) 897-1500
Technical
                                        E-mail: haf@nrc.gov


contacts:
Chu-Yu Liang, NRR
Harry A. Freeman, RIV (817) 897-1500 E-mail: haf@nrc.gov


Chu-Yu Liang, NRR (301) 415-2878 E-mail: cyl~nrc.gov
(301) 415-2878 E-mail: cyl~nrc.gov


Attachment:  
Attachment:       List of Recently Issued NRC Information Notices
List of Recently Issued NRC Information


Notices DOCUMENT NAME: G:\SSK2\INFONOT.C
DOCUMENT NAME:       G:\SSK2\INFONOT.C P


P To receive a copy of this docunent, tndicate in the box CO~opy So attachment/enclosure
To receive a copy of this docunent, tndicate in the box CO~opy So attachment/enclosure EsCopy with attachment/enctosure N


EsCopy with attachment/enctosure
* No


N
cops


* No cops OFFICE C BC:SRXB I BC:LPECB lI (A) DW M i NAME CYLiang* RJones* AChaffee*HAFreeman*
OFFICE         C                   BC:SRXBI          BC:LPECB lI       (A)DW M           i
____ _DATE 16/ 3/96 16/21/96 17/08/96 17LI/96 I OFFILIAL MLLUM LWUF* See previous concurrence


Tech Editor reviewed & concurred
NAME          CYLiang*            RJones*          AChaffee*
                HAFreeman*        ____                                          _
  DATE        16/ 3/96            16/21/96          17/08/96          17LI/96            I


on 05/28/96
OFFILIAL MLLUM LWUF
~1~1 -,K)IN 96-XX July XX, 1996 for the loss of extraction


steam to ti cause of the temperature
* See previous concurrence Tech Editor reviewed & concurred on 05/28/96


difference.
~1~1                  -,K)
                                                                                            IN 96-XX


occurred between the two heater drain of extraction
July XX, 1996 for the loss of extraction steam to ti              he high-pressure heaters, which was the


steam.he high-pressure
cause of the temperature difference. During the event, a level imbalance


heaters, which was the During the event, a level imbalance tanks, which resulted in the isolation The NRC staff review of analyses of feedwater
occurred between the two heater drain tanks, which resulted in the isolation


temperature
of extraction steam.


events at similar facilities
The NRC staff review of analyses of feedwater temperature events at similar


revealed that most of these analyses assumed similar initiating
facilities revealed that most of these analyses assumed similar initiating


events as the Comanche Peak analysis and had similar conclusions
events as the Comanche Peak analysis and had similar conclusions concerning


concerning
the amount of feedwater temperature drop. The licensee has reanalyzed the


the amount of feedwater
event to include a 119 'C [246 'F] feedwater temperature drop and concluded


temperature
that all accident analysis parameters remained within requirements.


drop. The licensee has reanalyzed
This information notice requires no specific action or written response. If


the event to include a 119 'C [246 'F] feedwater
you have any questions about the information in this notice, please contact


temperature
one of the technical contacts listed below or the appropriate Office of


drop and concluded that all accident analysis parameters
Nuclear Reactor Regulation project manager.


remained within requirements.
Brian K. Grimes, Acting Director


This information
Division of Reactor Program Management
 
notice requires no specific action or written response.
 
If you have any questions
 
about the information
 
in this notice, please contact one of the technical
 
contacts listed below or the appropriate


Office of Nuclear Reactor Regulation
Office of Nuclear Reactor Regulation


project manager.Brian K. Grimes, Acting Director Division of Reactor Program Management
Technical contacts:          Harry A. Freeman, RIV


===Office of Nuclear Reactor Regulation===
(817) 897-1500
Technical
                                        E-mail: haf~nrc.gov


contacts: Harry A. Freeman, RIV (817) 897-1500 E-mail: haf~nrc.gov
Chu-Yu Liang, NRR


Chu-Yu Liang, NRR (301) 415-2878 E-mail: cyl~nrc.gov
(301) 415-2878 E-mail: cyl~nrc.gov


Attachment:  
Attachment: List of Recently Issued NRC Information Notices
List of Recently Issued NRC Information


Notices DOCUMENT NAME: G:\SSK2\INFONOT.C
DOCUMENT NAME: G:\SSK2\INFONOT.C P


P To receive a copy of this document, indicate in the box CzAopy w/o attachment/enclosure
To receive a copy of this document, indicate in the box CzAopy w/o attachment/enclosure E-Copy with attachment/enclosure N


E-Copy with attachment/enclosure
* No


N
OFFICE      l        kd          BC: SRXB          BC:PECB              )D:DR


* No OFFICE l kd BC: SRXB BC:PECB )D:DR NAME CYLiang* RJones* AChaffee*  
NAME         CYLiang*           RJones*           AChaffee*           BGrimes
BGrimes HAFreeman*
DATE 6/ 3/96 6/21/96 7/08/96 7/ /96 OFFICIAL RECORD COPY*See previous concurrence


IN 96-XX July XX, 1996 for the loss of extraction
HAFreeman*
  DATE          6/ 3/96             6/21/96            7/08/96            7/ /96 OFFICIAL RECORD COPY


steam to the high-pressure
*See    previous concurrence


heaters, which was the cause of the temperature
IN 96-XX


difference.
July XX, 1996 for the loss of extraction steam to the high-pressure heaters, which was the


During the event, a level imbalance occurred between the two heater drain tanks, which resulted in the isolation of extraction
cause of the temperature difference. During the event, a level imbalance


steam.The NRC staff review of analyses of feedwater
occurred between the two heater drain tanks, which resulted in the isolation
 
temperature
 
events at similar facilities
 
revealed that most of these analyses assumed similar initiating
 
events as the licensee analysis and had similar conclusions
 
concerning
 
the amount of feedwater


temperature
of extraction steam.


drop. The licensee has reanalyzed
The NRC staff review of analyses of feedwater temperature events at similar


the event pursuant to Section 50.59 of Title 10 of the Code of Federal Regulations
facilities revealed that most of these analyses assumed similar initiating


to include a 119 'c [246 OF] feedwater
events as the licensee analysis and had similar conclusions concerning the


temperature
amount of feedwater temperature drop. The licensee has reanalyzed the event


drop and concluded
pursuant to Section 50.59 of Title 10 of the Code of Federal Regulations to


that all accident analysis parameters
include a 119 'c [246 OF] feedwater temperature drop and concluded that all


remained within requirements.
accident analysis parameters remained within requirements.


This information
This information notice requires no specific action or written response. If


notice requires no specific action or written response.
you have any questions about the information in this notice, please contact


If you have any questions
one of the technical contacts listed below or the appropriate Office of


about the information
Nuclear Reactor Regulation project manager.


in this notice, please contact one of the technical
Brian K. Grimes, Acting Director


contacts listed below or the appropriate
Division of Reactor Program Management


Office of Nuclear Reactor Regulation
Office of Nuclear Reactor Regulation


project manager.Brian K. Grimes, Acting Director Division of Reactor Program Management
Technical contacts:          Harry A. Freeman, RIV


===Office of Nuclear Reactor Regulation===
(817) 897-1500
Technical
                                        E-mail: haftnrc.gov


contacts:
Chu-Yu Liang, NRR
Harry A. Freeman, RIV (817) 897-1500 E-mail: haftnrc.gov


Chu-Yu Liang, NRR (301) 415-2878 E-mail: cyl~nrc.gov
(301) 415-2878 E-mail: cyl~nrc.gov


Attachment:  
Attachment: List of Recently Issued NRC Information Notices
List of Recently Issued NRC Information


Notices DOCUMENT NAME: G:\SSK2\INFONOT.C
DOCUMENT NAME: G:\SSK2\INFONOT.C P


P To receive a copy of this document, indicate in the box C-Topy u/o attachment/enclosure
To receive a copy of this document, indicate in the box C-Topy u/o attachment/enclosure E=Copy with attachment/enclosure N No


E=Copy with attachment/enclosure
copy


N No copy OFFICE CONT:i kd l BC:SRXBLl
OFFICE       CONT:i kd l       BC:SRXBLl         BC:iPECB lI        (A)iD:iDRPM I    _
  NAME          CYLiang*            RJones*            AChaffee*          BGrimes


BC:iPECB lI (A)iD:iDRPM
l      _    HAFreeman*
  DATE          6/ 3/96            6/21/96            7/08/96            7/ /96 OFFICIAL KLLUKV        UV    X!
* See previous concurrence


I _NAME CYLiang* RJones* AChaffee*
IN 96-XX
BGrimes l _ HAFreeman*
DATE 6/ 3/96 6/21/96 7/08/96 7/ /96* See previous concurrence


OFFICIAL KLLUKV UV X!
July XX, 1996 for the loss of extraction steam to the high-pressure heaters, which was the
IN 96-XX July XX, 1996 for the loss of extraction


steam to the high-pressure
cause of the temperature difference. During the event, a level imbalance


heaters, which was the cause of the temperature
occurred between the two heater drain tanks, which resulted in the isolation
 
difference.
 
During the event, a level imbalance occurred between the two heater drain tanks, which resulted in the isolation of extraction
 
steam.The NRC staff review of analyses of feedwater
 
temperature


events at similar facilities
of extraction steam.


revealed that most of these analyses assumed similar initiating
The NRC staff review of analyses of feedwater temperature events at similar


events as the licensee analysis and had similar conclusions
facilities revealed that most of these analyses assumed similar initiating


concerning
events as the licensee analysis and had similar conclusions concerning the


the amount of feedwater
amount of feedwater temperature drop. The licensee has reanalyzed the event


temperature
pursuant to Section 50.59 of Title 10 of the Code of Federal Regulations to


drop. The licensee has reanalyzed
include a 119 *C [246 *F] feedwater temperature drop and concluded that all


the event pursuant to Section 50.59 of Title 10 of the Code of Federal Regulations
accident analysis parameters remained within requirements.


to include a 119 *C [246 *F] feedwater
This information notice requires no specific action or written response. If


temperature
you have any questions about the information in this notice, please contact


drop and concluded
one of the technical contacts listed below or the appropriate Office of


that all accident analysis parameters
Nuclear Reactor Regulation project manager.


remained within requirements.
Brian K. Grimes, Acting Director


This information
Division of Reactor Program Management
 
notice requires no specific action or written response.
 
If you have any questions
 
about the information
 
in this notice, please contact one of the technical
 
contacts listed below or the appropriate


Office of Nuclear Reactor Regulation
Office of Nuclear Reactor Regulation


project manager.Brian K. Grimes, Acting Director Division of Reactor Program Management
Technical contacts:          Harry A. Freeman, RIV


===Office of Nuclear Reactor Regulation===
(817) 897-1500
Technical
                                        Internet:haf@nrc.gov


contacts:
Chu-Yu Liang, NRR
Harry A. Freeman, RIV (817) 897-1500 Internet:haf@nrc.gov


Chu-Yu Liang, NRR (301) 415-2878 Internet:cyl
(301) 415-2878 Internet:cyl nrc.gov


nrc.gov Attachment:  
Attachment: List of Recently Issued NRC Information Notices
List of Recently Issued NRC Information


Notices DOCUMENT NAME: G:\SSK2\INFONOT.C
DOCUMENT NAME: G:\SSK2\INFONOT.C P


P To receive a copy of this document, Indicate in the box Conopy w/c attachment/enclosure
To receive a copy of this document, Indicate in the box Conopy w/c attachment/enclosure EnCopy with attachment/enclosure N


EnCopy with attachment/enclosure
* No


N
OFFICE        CONT:      Ekd      BC: SLB            BC:PECB            (A)D:DRPM


* No OFFICE CONT: Ekd BC: SLB BC:PECB (A)D:DRPM NAME CYLiang* RJones* ACh)f BGrimes l ~~HAFreeman*tVt
NAME         CYLiang*           RJones*           ACh)f             BGrimes


DATE 6/ 3/96 6/21/96 7/7/96 7/ /96 OFFICIAL RECOR COPY* See previous concurrence
l    ~~HAFreeman*tVt


K-, /IN 96-XX June XX, 1996 for the loss of extraction
DATE          6/ 3/96            6/21/96            7/7/96            7/ /96 OFFICIAL RECOR        COPY


steam to ti cause of the temperature
*  See previous concurrence


difference.
K-, /
                                                                                            IN 96-XX


occurred between the two heater drain of extraction
June XX, 1996 for the loss of extraction steam to ti              he high-pressure heaters, which was the


steam.he high-pressure
cause of the temperature difference. During the event, a level imbalance


heaters, which was the During the event, a level imbalance tanks, which resulted in the isolation The NRC staff's review of analyses of feedwater
occurred between the two heater drain tanks, which resulted inthe isolation


temperature
of extraction steam.


events at similar facilities
The NRC staff's review of analyses of feedwater temperature events at similar


revealed that most of these analyses assumed similar initiating
facilities revealed that most of these analyses assumed similar initiating


events as the licensee's
events as the licensee's analysis and had similar conclusions concerning the


analysis and had similar conclusions
amount of feedwater temperature drop. The licensee has reanalyzed the event


concerning
pursuant to Section 50.59 of Title 10 of the Code of Federal Regulations to


the amount of feedwater
include a 119 'C [246 OF] feedwater temperature drop and concluded that all


temperature
accident analysis parameters remained within requirements.


drop. The licensee has reanalyzed
This information notice requires no specific action or written response. If


the event pursuant to Section 50.59 of Title 10 of the Code of Federal Regulations
you have any questions about the information in this notice, please contact


to include a 119 'C [246 OF] feedwater
one of the technical contacts listed below or the appropriate Office of


temperature
Nuclear Reactor Regulation project manager.


drop and concluded
Brian K. Grimes, Acting Director


that all accident analysis parameters
Division of Reactor Program Management
 
remained within requirements.
 
This information
 
notice requires no specific action or written response.
 
If you have any questions
 
about the information
 
in this notice, please contact one of the technical
 
contacts listed below or the appropriate


Office of Nuclear Reactor Regulation
Office of Nuclear Reactor Regulation


project manager.Brian K. Grimes, Acting Director Division of Reactor Program Management
Technical contacts:          Harry A. Freeman, RIV


===Office of Nuclear Reactor Regulation===
(817) 897-1500
Technical
                                        Internet:haffnrc.gov


contacts: Harry A. Freeman, RIV (817) 897-1500 Internet:haffnrc.gov
Chu-Yu Liang, NRR


Chu-Yu Liang, NRR (301) 415-2878 Internet:cyl@nrc.gov
(301) 415-2878 Internet:cyl@nrc.gov


Attachment:  
Attachment: List of Recently Issued NRC Information Notices
List of Recently Issued NRC Information


Notices DOCUMENT NAME: G:\SSK2\INFONOT.CP
DOCUMENT NAME: G:\SSK2\INFONOT.CP


To receive a copy of this document, indicate in the box Ciropy w/dattachmeft1/enctosure
To receive a copy of this document, indicate in the box Ciropy w/dattachmeft1/enctosure EnC  Ioith attachment/enclosure 1
* No copy


EnC OFFICE CONT:jkd _l BC: SRXB E C:PECB I _ A)D:DRPM I NAME CYLiang* RJones AChaffee BGrimes HAFreeman*
OFFICE       CONT:jkd _l         BC: SRXB           EC:PECB I       _   A)D:DRPM I
I- _DATE 6/ 3/96 6/2j /96 6/ /96 6/ /96 OFFICIAL RECORD COPY I oith attachment/enclosure


1
NAME          CYLiang*           RJones            AChaffee          BGrimes
* No copy* See previous concurrence


IN 96-XX June XX, 1996 detection
HAFreeman*                  I-        _
  DATE          6/ 3/96             6/2j /96          6/ /96            6/ /96 OFFICIAL RECORD COPY


system. The licensee believed that this system would probably not be significantly
*  See previous concurrence


affected by feedwater
IN 96-XX


temperatures
June XX, 1996 detection system. The licensee believed that this system would probably not


because of a different mass flow rate determination
be significantly affected by feedwater temperatures because of a different


method.Finally, the licensee's
mass flow rate determination method.


final safety analysis report did not accurately
Finally, the licensee's final safety analysis report did not accurately


analyze this transient.
analyze this transient. The actual events were similar to the analysis of the


The actual events were similar to the analysis of the'Decrease
'Decrease in Feedwater Temperature event presented in Chapter 15. In that


in Feedwater
analysis, the inadvertent opening of the low-pressure heater bypass valve, coupled with the trip of the heater drain pumps, resulted in a feedwater


Temperature
temperature drop of less than 35 OF, and a corresponding power increase of


event presented
less than 10 percent. In the actual event, the feedwater temperature dropped


in Chapter 15. In that analysis, the inadvertent
by approximately 200 OF, and the licensee calculated that reactor power would


opening of the low-pressure
have increased by approximately 35 percent without operator or protective


heater bypass valve, coupled with the trip of the heater drain pumps, resulted in a feedwater temperature
actions. The licensee determined that although the initiating events were the


drop of less than 35 OF, and a corresponding
same, the Chapter 15 analysis did not account for the loss of extraction steam


power increase of less than 10 percent. In the actual event, the feedwater
to the high-pressure heaters, which was the cause of the temperature


temperature
difference. During the event, a level imbalance occurred between the two


dropped by approximately
heater drain tanks, which resulted in the isolation of extraction steam.


200 OF, and the licensee calculated
The NRC staff's review of analyses of feedwater temperature events at similar


that reactor power would have increased
facilities revealed that most of these analyses assumed similar initiating


by approximately
events as the licensee's analysis and had similar conclusions concerning the


35 percent without operator or protective
amount of feedwater temperature drop.


actions. The licensee determined
This information notice requires no specific action or written response. If


that although the initiating
you have any questions about the information in this notice, please contact


events were the same, the Chapter 15 analysis did not account for the loss of extraction
one of the technical contacts listed below or the appropriate Office of


steam to the high-pressure
Nuclear Reactor Regulation project manager.


heaters, which was the cause of the temperature
Brian K. Grimes, Acting Director


difference.
Division of Reactor Program Management


During the event, a level imbalance
Office of Nuclear Reactor Regulation
 
occurred between the two heater drain tanks, which resulted in the isolation
 
of extraction
 
steam.The NRC staff's review of analyses of feedwater
 
temperature
 
events at similar facilities


revealed that most of these analyses assumed similar initiating
Technical contacts:          Harry A. Freeman, RIV
 
events as the licensee's
 
analysis and had similar conclusions
 
concerning
 
the amount of feedwater
 
temperature
 
drop.This information
 
notice requires no specific action or written response.
 
If you have any questions
 
about the information
 
in this notice, please contact one of the technical
 
contacts listed below or the appropriate
 
Office of Nuclear Reactor Regulation


project manager.Brian K. Grimes, Acting Director Division of Reactor Program Management
(817) 897-1500
                                        Internet:haf@nrc.gov


===Office of Nuclear Reactor Regulation===
Chu-Yu Liang, NRR
Technical


contacts:
(301) 415-2878 Internet:cyl nrc.gov
Harry A. Freeman, RIV (817) 897-1500 Internet:haf@nrc.gov


Chu-Yu Liang, NRR (301) 415-2878 Internet:cyl
Attachment: List of Recently Issued NRC Information Notices


nrc.gov Attachment:
DOCUMENT NAME: G:\SSK2\INFONOT.C P
List of Recently Issued NRC Information


Notices DOCUMENT NAME: G:\SSK2\INFONOT.C
To receive a copy of this docunent, indicate in the box Catopy w/o attachment/enclosure E-C   with attachment/enclosure N


P To receive a copy of this docunent, indicate in the box Catopy w/o attachment/enclosure
* No copy


E-C with attachment/enclosure
OFFICE      lCONT:kd l            BC:SRXB l          BC:PECB l          (A)D:DRPM


N
NAME          CYLiang 9          RJones            AChaffee          BGrimes


* No copy OFFICE lCONT:kd l BC:SRXB l BC:PECB l (A)D:DRPM NAME CYLiang 9 RJones AChaffee BGrimes HAFreema r _ _DATE /96 /96 6/ /96 6/ /96 OFFICIAL RECORD COPY}}
HAFreema       r   _                 _
  DATE            /96                   /96         6/ /96             6/ /96 OFFICIAL RECORD COPY}}


{{Information notice-Nav}}
{{Information notice-Nav}}

Latest revision as of 04:38, 24 November 2019

Effects of a Decrease in Feedwater Temperature on Nuclear Instrumentation
ML031060009
Person / Time
Site: Beaver Valley, Millstone, Hatch, Monticello, Calvert Cliffs, Dresden, Davis Besse, Peach Bottom, Browns Ferry, Salem, Oconee, Mcguire, Nine Mile Point, Palisades, Palo Verde, Perry, Indian Point, Fermi, Kewaunee, Catawba, Harris, Wolf Creek, Saint Lucie, Point Beach, Oyster Creek, Watts Bar, Hope Creek, Grand Gulf, Cooper, Sequoyah, Byron, Pilgrim, Arkansas Nuclear, Three Mile Island, Braidwood, Susquehanna, Summer, Prairie Island, Columbia, Seabrook, Brunswick, Surry, Limerick, North Anna, Turkey Point, River Bend, Vermont Yankee, Crystal River, Haddam Neck, Ginna, Diablo Canyon, Callaway, Vogtle, Waterford, Duane Arnold, Farley, Robinson, Clinton, South Texas, San Onofre, Cook, Comanche Peak, Yankee Rowe, Maine Yankee, Quad Cities, Humboldt Bay, La Crosse, Big Rock Point, Rancho Seco, Zion, Midland, Bellefonte, Fort Calhoun, FitzPatrick, McGuire, LaSalle, Fort Saint Vrain, Shoreham, Satsop, Trojan, Atlantic Nuclear Power Plant  Entergy icon.png
Issue date: 07/26/1996
From: Grimes B
Office of Nuclear Reactor Regulation
To:
References
IN-96-041, NUDOCS 9607220160
Download: ML031060009 (10)


K) Ij

K)

UNITED STATES

NUCLEAR REGULATORY COMMISSION

OFFICE OF NUCLEAR REACTOR REGULATION

WASHINGTON, D.C. 20555-0001 July 26, 1996 NRC INFORMATION NOTICE 96-41: EFFECTS OF A DECREASE IN FEEDWATER TEMPERATURE

ON NUCLEAR INSTRUMENTATION

Addressees

All holders of operating licenses or construction permits for pressurized

water reactors (PWRs).

Purpose

The U.S. Nuclear Regulatory Commission (NRC) is issuing this information

notice to alert addressees to the potential for operation above licensed power

as a result of a decrease in feedwater temperature event affecting nuclear

instrumentation. It is expected that recipients will review the information

for applicability to their facilities and consider actions, as appropriate, to

avoid similar problems. However, suggestions contained in this information

notice are not NRC requirements; therefore, no specific action or written

response is required.

Description of Circumstances

On February 14, 1996, the licensee for the Comanche Peak Steam Electric

Station was operating Unit 2 at 95 percent rated thermal power near end-of- core life when a significant reduction in feedwater temperature occurred

because of the loss of feedwater heaters. This reduction, in turn, caused a

reduction in the reactor coolant system cold-leg temperatures. The colder

reactor coolant temperature, with a large negative moderator temperature

coefficient, caused reactor power to increase to approximately 102 percent

according to ex-core nuclear instrumentation. The nitrogen-16 (N-16)

detection system reached the overpower turbine runback setpoint (109 percent)

and initiated a turbine runback. The N-16 detection system measures N-16 activity in the primary coolant as a measure of the total power generation.

This system is a substitute for the resistance temperature detector over- temperature and over-power reactor trip functions used at other Westinghouse

PWRs. The plant stabil zed at an indicated power of approximately 97 percent

according to the ex-core nuclear instrumentation.

After approximately 90 minutes, a second similar turbine runback occurred

while restoring balance-of-plant equipment. Following this runback, reactor

power was stabilized at approximately 100 percent according to nuclear

instrumentation. During the next 30 minutes, the reactor was operated at

approximately 100 percent power as indicated by nuclear instrumentation, with

reactor coolant temperatures below normal. The licensee noted that the N-16

9607220l 60ujo i 7 9,oi4 (R ~IE ctG

IN 96-41 July 26, 1996 detection system indicated approximately 106 percent power and the computer- based plant calorimetric system indicated approximately 102 percent power.

Subsequently, the reactor power was reduced to less than 100 percent by all

indications.

Discussion

There are three aspects of this event which have generic implications. First, with a loss of secondary plant efficiency, programmed T e can no longer

reliably represent core thermal power. Second, the venturi-based input into

the computer-based calorimetric system may not be accurate with cold

feedwater. And third, the final safety analysis report had not analyzed this

transient accurately.

Following the second runback, operators noted that reactor power indicated

<100 percent according to nuclear instrumentation. Although the operators

knew that cold feedwater could cause an increase in the amount of neutron

attenuation, they believed that the nuclear instrumentation indicated

conservatively (i.e., higher than actual) because they were maintaining TA"e

approximately 1.7 eC [3 OF] above TRef. The licensee could not use the

computer-based calorimetric until some time after the second turbine runback

due to maintenance activities. Te , based on the main turbine impulse

pressure, is programmed as a functlon of turbine load and, for normal

efficiency, is a good representation of thermal power. When the unit lost the

feedwater heaters, the plant efficiency decreased. Because the main turbine

electro-hydraulic control system maintained generator output, core thermal

power increased to account for the loss of efficiency, and thus, TRef no

longer accurately represented the core thermal power.

The cold-leg temperature is a more appropriate indicator of the accuracy of

the nuclear instrumentation than programmed TY.e. As the cold-leg temperature

decreased, the amount of neutron attenuation in the downcomer area surrounding

the core increased and hence affected the amount of neutrons reaching the

detectors. The licensee analysis showed that for every 0.6 C (1 OF] of cold- leg temperature change, the nuclear instrumentation was affected by 0.6 to 0.8 percent power. A review of the second transient showed that the cold-leg

temperature was approximately 2.5 °C [4.5 OF] lower than when the detectors

were last calibrated. This corresponded to a 3 to 4 percent error, which

corresponded to the difference in the actual versus the indicated power (104 percent actual versus 100 percent indicated).

During the review, the licensee noted that the computer-based calorimetric was

4 percent lower than the actual thermal power (N-16 power monitor). The

calorimetric was based on feedwater flow measured by venturis. Although the

calorimetric calculation used feedwater temperature as an input, temperatures

significantly different than the normal 227 OC [440 OF] introduced errors into

the calculation.

Finally, the actual events involved temperature and power levels that exceeded

those in the analysis of the Decrease in Feedwater Temperature" event

presented in Chapter 15 of the licensee final safety analysis report. In that

IN 96-41 July 26, 1996 analysis, the inadvertent opening of the low-pressure heater bypass valve, coupled with the trip of the heater drain pumps, resulted in a feedwater

temperature drop of less than 19 'C (35 OF], and a corresponding power

increase of less than 10 percent. In the actual event, the feedwater

temperature dropped by approximately 111 °C (200 OF], and the licensee

calculated that reactor power would have increased by approximately 35 percent

without operator or protective actions. The licensee determined that although

the initiating events were the same, the Chapter 15 analysis did not account

for the loss of extraction steam to the high-pressure heaters, which was the

cause of the temperature difference. During the event, a level imbalance

occurred between the two heater drain tanks, which resulted in the isolation

of extraction steam.

The NRC staff review of analyses of feedwater temperature events at similar

facilities revealed that most of these analyses assumed similar initiating

events as the Comanche Peak analysis and had similar conclusions concerning

the amount of feedwater temperature drop. The licensee has reanalyzed the

event to include a 119 OC [246 OF] feedwater temperature drop and concluded

that all accident analysis parameters remained within requirements.

This information notice requires no specific action or written response. If

you have any questions about the information in this notice, please contact

one of the technical contacts listed below or the appropriate Office of

Nuclear Reactor Regulation project manager.

Brian K. Grimes, Acting Director

Division of Reactor Program Management

Office of Nuclear Reactor Regulation

Technical contacts: Harry A. Freeman, RIV

(817) 897-1500

E-mail: haf~nrc.gov

Chu-Yu Liang, NRR

(301) 415-2878 E-mail: cylenrc.gov

Attachment: List Of Recently Issued HRC Information Notices

A1h4 Stir A Je6tQ

K> KJ

Attachment

IN 96-41 July 26, 1996 LIST OF RECENTLY ISSUED

NRC INFORMATION NOTICES

Information Date of

Notice No. Subject Issuance Issued to

96-40 Deficiencies in Material 07/25/96 All holders of OLs or CPs

Dedication and Procure- for nuclear power reactors

ment Practices and in

Audits of Vendors

96-09, Damage in Foreign Steam 07/10/96 All holders of OLs or CPs

Supp. 1 Generator Internals for pressurized-water

reactors

96-39 Estimates of Decay Heat 07/05/96 All holders of OLs or CPs

Using ANS 5.1 Decay Heat for nuclear power reactors

Standard May Vary Signi- ficantly

96-38 Results of Steam Generator 06/21/96 All holders of OLs or CPs

Tube Examinations for pressurized water

reactors

96-37 Inaccurate Reactor Water 06/18/96 All pressurized water

Level Indication and Inad- reactor facilities holding

vertent Draindown During an operating license or a

Shutdown construction permit

96-36 Degradation of Cooling 06/12/96 All holders of OLs or CPs

Water Systems Due to Icing for nuclear power reactors

96-35 Failure of Safety Systems 06/11/96 All U.S. Nuclear Regulatory

on Self-Shielded Irradia- Commission irradiator

tors Because of Inadequate licensees and vendors

Maintenance and Training

96-34 Hydrogen Gas Ignition 05/31/96 All holders of OLs or CPs

during Closure Welding for nuclear power reactors

of a VSC-24 Multi-Assembly

Sealed Basket

OL - Operating License

CP - Construction Permit

  • ~ - K> K

IN 96-41 July 26, 1996 analysis, the inadvertent opening of the low-pressure heater bypass valve, coupled with the trip of the heater drain pumps, resulted in a feedwater

temperature drop of less than 19 *C [35 OF], and a corresponding power

increase of less than 10 percent. In the actual event, the feedwater

temperature dropped by approximately 111 *C [200 OF], and the licensee

calculated that reactor power would have increased by approximately 35 percent

without operator or protective actions. The licensee determined that although

the initiating events were the same, the Chapter 15 analysis did not account

for the loss of extraction steam to the high-pressure heaters, which was the

cause of the temperature difference. During the event, a level imbalance

occurred between the two heater drain tanks, which resulted in the isolation

of extraction steam.

The NRC staff review of analyses of feedwater temperature events at similar

facilities revealed that most of these analyses assumed similar initiating

events as the Comanche Peak analysis and had similar conclusions concerning

the amount of feedwater temperature drop. The licensee has reanalyzed the

event to include a 119 *C [246 OF] feedwater temperature drop and concluded

that all accident analysis parameters remained within requirements.

This information notice requires no specific action or written response. If

you have any questions about the information in this notice,-please contact

one of the technical contacts listed below or the appropriate Office of

Nuclear Reactor Regulation project manager.

Original signed by Brian K.Grimes

Brian K. Grimes, Acting Director

Division of Reactor Program Management

Office of Nuclear Reactor Regulation

Technical contacts: Harry A. Freeman, RIV

(817) 897-1500

E-mail: haf@nrc.gov

Chu-Yu Liang, NRR

(301) 415-2878 E-mail: cyl~nrc.gov

Attachment: List of Recently Issued NRC Information Notices

DOCUMENT NAME: G:\SSK2\INFONOT.C P

To receive a copy of this docunent, tndicate in the box CO~opy So attachment/enclosure EsCopy with attachment/enctosure N

  • No

cops

OFFICE C BC:SRXBI BC:LPECB lI (A)DW M i

NAME CYLiang* RJones* AChaffee*

HAFreeman* ____ _

DATE 16/ 3/96 16/21/96 17/08/96 17LI/96 I

OFFILIAL MLLUM LWUF

  • See previous concurrence Tech Editor reviewed & concurred on 05/28/96

~1~1 -,K)

IN 96-XX

July XX, 1996 for the loss of extraction steam to ti he high-pressure heaters, which was the

cause of the temperature difference. During the event, a level imbalance

occurred between the two heater drain tanks, which resulted in the isolation

of extraction steam.

The NRC staff review of analyses of feedwater temperature events at similar

facilities revealed that most of these analyses assumed similar initiating

events as the Comanche Peak analysis and had similar conclusions concerning

the amount of feedwater temperature drop. The licensee has reanalyzed the

event to include a 119 'C [246 'F] feedwater temperature drop and concluded

that all accident analysis parameters remained within requirements.

This information notice requires no specific action or written response. If

you have any questions about the information in this notice, please contact

one of the technical contacts listed below or the appropriate Office of

Nuclear Reactor Regulation project manager.

Brian K. Grimes, Acting Director

Division of Reactor Program Management

Office of Nuclear Reactor Regulation

Technical contacts: Harry A. Freeman, RIV

(817) 897-1500

E-mail: haf~nrc.gov

Chu-Yu Liang, NRR

(301) 415-2878 E-mail: cyl~nrc.gov

Attachment: List of Recently Issued NRC Information Notices

DOCUMENT NAME: G:\SSK2\INFONOT.C P

To receive a copy of this document, indicate in the box CzAopy w/o attachment/enclosure E-Copy with attachment/enclosure N

  • No

OFFICE l kd BC: SRXB BC:PECB )D:DR

NAME CYLiang* RJones* AChaffee* BGrimes

HAFreeman*

DATE 6/ 3/96 6/21/96 7/08/96 7/ /96 OFFICIAL RECORD COPY

  • See previous concurrence

IN 96-XX

July XX, 1996 for the loss of extraction steam to the high-pressure heaters, which was the

cause of the temperature difference. During the event, a level imbalance

occurred between the two heater drain tanks, which resulted in the isolation

of extraction steam.

The NRC staff review of analyses of feedwater temperature events at similar

facilities revealed that most of these analyses assumed similar initiating

events as the licensee analysis and had similar conclusions concerning the

amount of feedwater temperature drop. The licensee has reanalyzed the event

pursuant to Section 50.59 of Title 10 of the Code of Federal Regulations to

include a 119 'c [246 OF] feedwater temperature drop and concluded that all

accident analysis parameters remained within requirements.

This information notice requires no specific action or written response. If

you have any questions about the information in this notice, please contact

one of the technical contacts listed below or the appropriate Office of

Nuclear Reactor Regulation project manager.

Brian K. Grimes, Acting Director

Division of Reactor Program Management

Office of Nuclear Reactor Regulation

Technical contacts: Harry A. Freeman, RIV

(817) 897-1500

E-mail: haftnrc.gov

Chu-Yu Liang, NRR

(301) 415-2878 E-mail: cyl~nrc.gov

Attachment: List of Recently Issued NRC Information Notices

DOCUMENT NAME: G:\SSK2\INFONOT.C P

To receive a copy of this document, indicate in the box C-Topy u/o attachment/enclosure E=Copy with attachment/enclosure N No

copy

OFFICE CONT:i kd l BC:SRXBLl BC:iPECB lI (A)iD:iDRPM I _

NAME CYLiang* RJones* AChaffee* BGrimes

l _ HAFreeman*

DATE 6/ 3/96 6/21/96 7/08/96 7/ /96 OFFICIAL KLLUKV UV X!

  • See previous concurrence

IN 96-XX

July XX, 1996 for the loss of extraction steam to the high-pressure heaters, which was the

cause of the temperature difference. During the event, a level imbalance

occurred between the two heater drain tanks, which resulted in the isolation

of extraction steam.

The NRC staff review of analyses of feedwater temperature events at similar

facilities revealed that most of these analyses assumed similar initiating

events as the licensee analysis and had similar conclusions concerning the

amount of feedwater temperature drop. The licensee has reanalyzed the event

pursuant to Section 50.59 of Title 10 of the Code of Federal Regulations to

include a 119 *C [246 *F] feedwater temperature drop and concluded that all

accident analysis parameters remained within requirements.

This information notice requires no specific action or written response. If

you have any questions about the information in this notice, please contact

one of the technical contacts listed below or the appropriate Office of

Nuclear Reactor Regulation project manager.

Brian K. Grimes, Acting Director

Division of Reactor Program Management

Office of Nuclear Reactor Regulation

Technical contacts: Harry A. Freeman, RIV

(817) 897-1500

Internet:haf@nrc.gov

Chu-Yu Liang, NRR

(301) 415-2878 Internet:cyl nrc.gov

Attachment: List of Recently Issued NRC Information Notices

DOCUMENT NAME: G:\SSK2\INFONOT.C P

To receive a copy of this document, Indicate in the box Conopy w/c attachment/enclosure EnCopy with attachment/enclosure N

  • No

OFFICE CONT: Ekd BC: SLB BC:PECB (A)D:DRPM

NAME CYLiang* RJones* ACh)f BGrimes

l ~~HAFreeman*tVt

DATE 6/ 3/96 6/21/96 7/7/96 7/ /96 OFFICIAL RECOR COPY

  • See previous concurrence

K-, /

IN 96-XX

June XX, 1996 for the loss of extraction steam to ti he high-pressure heaters, which was the

cause of the temperature difference. During the event, a level imbalance

occurred between the two heater drain tanks, which resulted inthe isolation

of extraction steam.

The NRC staff's review of analyses of feedwater temperature events at similar

facilities revealed that most of these analyses assumed similar initiating

events as the licensee's analysis and had similar conclusions concerning the

amount of feedwater temperature drop. The licensee has reanalyzed the event

pursuant to Section 50.59 of Title 10 of the Code of Federal Regulations to

include a 119 'C [246 OF] feedwater temperature drop and concluded that all

accident analysis parameters remained within requirements.

This information notice requires no specific action or written response. If

you have any questions about the information in this notice, please contact

one of the technical contacts listed below or the appropriate Office of

Nuclear Reactor Regulation project manager.

Brian K. Grimes, Acting Director

Division of Reactor Program Management

Office of Nuclear Reactor Regulation

Technical contacts: Harry A. Freeman, RIV

(817) 897-1500

Internet:haffnrc.gov

Chu-Yu Liang, NRR

(301) 415-2878 Internet:cyl@nrc.gov

Attachment: List of Recently Issued NRC Information Notices

DOCUMENT NAME: G:\SSK2\INFONOT.CP

To receive a copy of this document, indicate in the box Ciropy w/dattachmeft1/enctosure EnC Ioith attachment/enclosure 1

  • No copy

OFFICE CONT:jkd _l BC: SRXB EC:PECB I _ A)D:DRPM I

NAME CYLiang* RJones AChaffee BGrimes

HAFreeman* I- _

DATE 6/ 3/96 6/2j /96 6/ /96 6/ /96 OFFICIAL RECORD COPY

  • See previous concurrence

IN 96-XX

June XX, 1996 detection system. The licensee believed that this system would probably not

be significantly affected by feedwater temperatures because of a different

mass flow rate determination method.

Finally, the licensee's final safety analysis report did not accurately

analyze this transient. The actual events were similar to the analysis of the

'Decrease in Feedwater Temperature event presented in Chapter 15. In that

analysis, the inadvertent opening of the low-pressure heater bypass valve, coupled with the trip of the heater drain pumps, resulted in a feedwater

temperature drop of less than 35 OF, and a corresponding power increase of

less than 10 percent. In the actual event, the feedwater temperature dropped

by approximately 200 OF, and the licensee calculated that reactor power would

have increased by approximately 35 percent without operator or protective

actions. The licensee determined that although the initiating events were the

same, the Chapter 15 analysis did not account for the loss of extraction steam

to the high-pressure heaters, which was the cause of the temperature

difference. During the event, a level imbalance occurred between the two

heater drain tanks, which resulted in the isolation of extraction steam.

The NRC staff's review of analyses of feedwater temperature events at similar

facilities revealed that most of these analyses assumed similar initiating

events as the licensee's analysis and had similar conclusions concerning the

amount of feedwater temperature drop.

This information notice requires no specific action or written response. If

you have any questions about the information in this notice, please contact

one of the technical contacts listed below or the appropriate Office of

Nuclear Reactor Regulation project manager.

Brian K. Grimes, Acting Director

Division of Reactor Program Management

Office of Nuclear Reactor Regulation

Technical contacts: Harry A. Freeman, RIV

(817) 897-1500

Internet:haf@nrc.gov

Chu-Yu Liang, NRR

(301) 415-2878 Internet:cyl nrc.gov

Attachment: List of Recently Issued NRC Information Notices

DOCUMENT NAME: G:\SSK2\INFONOT.C P

To receive a copy of this docunent, indicate in the box Catopy w/o attachment/enclosure E-C with attachment/enclosure N

  • No copy

OFFICE lCONT:kd l BC:SRXB l BC:PECB l (A)D:DRPM

NAME CYLiang 9 RJones AChaffee BGrimes

HAFreema r _ _

DATE /96 /96 6/ /96 6/ /96 OFFICIAL RECORD COPY