Information Notice 1996-41, Effects of a Decrease in Feedwater Temperature on Nuclear Instrumentation: Difference between revisions
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| issue date = 07/26/1996 | | issue date = 07/26/1996 | ||
| title = Effects of a Decrease in Feedwater Temperature on Nuclear Instrumentation | | title = Effects of a Decrease in Feedwater Temperature on Nuclear Instrumentation | ||
| author name = Grimes B | | author name = Grimes B | ||
| author affiliation = NRC/NRR | | author affiliation = NRC/NRR | ||
| addressee name = | | addressee name = | ||
Line 14: | Line 14: | ||
| page count = 10 | | page count = 10 | ||
}} | }} | ||
{{#Wiki_filter:K) | {{#Wiki_filter:K) Ij | ||
K) | |||
UNITED STATES | |||
NUCLEAR REGULATORY COMMISSION | |||
OFFICE OF NUCLEAR REACTOR REGULATION | |||
TEMPERATURE | WASHINGTON, D.C. 20555-0001 July 26, 1996 NRC INFORMATION NOTICE 96-41: EFFECTS OF A DECREASE IN FEEDWATER TEMPERATURE | ||
ON NUCLEAR INSTRUMENTATION | |||
==Addressees== | ==Addressees== | ||
All holders of operating | All holders of operating licenses or construction permits for pressurized | ||
licenses or construction | |||
permits for pressurized | |||
water reactors (PWRs). | water reactors (PWRs). | ||
==Purpose== | ==Purpose== | ||
The U.S. Nuclear Regulatory | The U.S. Nuclear Regulatory Commission (NRC) is issuing this information | ||
Commission (NRC) is issuing this information | |||
notice to alert addressees to the potential for operation above licensed power | |||
in | as a result of a decrease in feedwater temperature event affecting nuclear | ||
instrumentation. It is expected that recipients will review the information | |||
for applicability to their facilities and consider actions, as appropriate, to | |||
avoid similar problems. However, suggestions contained in this information | |||
notice are not NRC requirements; therefore, no specific action or written | |||
response is required. | |||
==Description of Circumstances== | |||
On February 14, 1996, the licensee for the Comanche Peak Steam Electric | |||
temperature | Station was operating Unit 2 at 95 percent rated thermal power near end-of- core life when a significant reduction in feedwater temperature occurred | ||
because of the loss of feedwater heaters. This reduction, in turn, caused a | |||
reduction in the reactor coolant system cold-leg temperatures. The colder | |||
reactor coolant temperature, with a large negative moderator temperature | |||
coefficient, caused reactor power to increase to approximately 102 percent | |||
according to ex-core nuclear instrumentation. The nitrogen-16 (N-16) | |||
detection system reached the overpower turbine runback setpoint (109 percent) | |||
and initiated a turbine runback. The N-16 detection system measures N-16 activity in the primary coolant as a measure of the total power generation. | |||
This system is a substitute for the resistance temperature detector over- temperature and over-power reactor trip functions used at other Westinghouse | |||
PWRs. The plant stabil zed at an indicated power of approximately 97 percent | |||
to ex-core nuclear instrumentation. | according to the ex-core nuclear instrumentation. | ||
After approximately 90 minutes, a second similar turbine runback occurred | |||
while restoring balance-of-plant equipment. Following this runback, reactor | |||
power was stabilized at approximately 100 percent according to nuclear | |||
instrumentation. During the next 30 minutes, the reactor was operated at | |||
approximately 100 percent power as indicated by nuclear instrumentation, with | |||
reactor coolant temperatures below normal. The licensee noted that the N-16 | |||
9607220l 60ujo i 7 9,oi4 (R ~IE ctG | |||
IN 96-41 July 26, 1996 detection system indicated approximately 106 percent power and the computer- based plant calorimetric system indicated approximately 102 percent power. | |||
Subsequently, the reactor power was reduced to less than 100 percent by all | |||
indications. | |||
Discussion | Discussion | ||
There are three aspects of this event which have generic implications. | There are three aspects of this event which have generic implications. First, with a loss of secondary plant efficiency, programmed T e can no longer | ||
reliably represent core thermal power. Second, the venturi-based input into | |||
the computer-based calorimetric system may not be accurate with cold | |||
feedwater. And third, the final safety analysis report had not analyzed this | |||
transient accurately. | |||
Following the second runback, operators noted that reactor power indicated | |||
<100 percent according to nuclear instrumentation. Although the operators | |||
knew that cold feedwater could cause an increase in the amount of neutron | |||
attenuation, they believed that the nuclear instrumentation indicated | |||
conservatively (i.e., higher than actual) because they were maintaining TA"e | |||
approximately 1.7 eC [3 OF] above TRef. The licensee could not use the | |||
the second runback | computer-based calorimetric until some time after the second turbine runback | ||
due to maintenance activities. Te , based on the main turbine impulse | |||
pressure, is programmed as a functlon of turbine load and, for normal | |||
efficiency, is a good representation of thermal power. When the unit lost the | |||
feedwater heaters, the plant efficiency decreased. Because the main turbine | |||
electro-hydraulic control system maintained generator output, core thermal | |||
power increased to account for the loss of efficiency, and thus, TRef no | |||
longer accurately represented the core thermal power. | |||
The cold-leg temperature is a more appropriate indicator of the accuracy of | |||
the nuclear instrumentation than programmed TY.e. As the cold-leg temperature | |||
decreased, the amount of neutron attenuation in the downcomer area surrounding | |||
the core increased and hence affected the amount of neutrons reaching the | |||
detectors. The licensee analysis showed that for every 0.6 C (1 OF] of cold- leg temperature change, the nuclear instrumentation was affected by 0.6 to 0.8 percent power. A review of the second transient showed that the cold-leg | |||
temperature was approximately 2.5 °C [4.5 OF] lower than when the detectors | |||
were last calibrated. This corresponded to a 3 to 4 percent error, which | |||
corresponded to the difference in the actual versus the indicated power (104 percent actual versus 100 percent indicated). | |||
During the review, the licensee noted that the computer-based calorimetric was | |||
4 percent lower than the actual thermal power (N-16 power monitor). The | |||
calorimetric was based on feedwater flow measured by venturis. Although the | |||
calorimetric calculation used feedwater temperature as an input, temperatures | |||
significantly different than the normal 227 OC [440 OF] introduced errors into | |||
the calculation. | |||
the | Finally, the actual events involved temperature and power levels that exceeded | ||
those in the analysis of the Decrease in Feedwater Temperature" event | |||
presented in Chapter 15 of the licensee final safety analysis report. In that | |||
of the | IN 96-41 July 26, 1996 analysis, the inadvertent opening of the low-pressure heater bypass valve, coupled with the trip of the heater drain pumps, resulted in a feedwater | ||
than | temperature drop of less than 19 'C (35 OF], and a corresponding power | ||
increase of less than 10 percent. In the actual event, the feedwater | |||
temperature dropped by approximately 111 °C (200 OF], and the licensee | |||
calculated that reactor power would have increased by approximately 35 percent | |||
without operator or protective actions. The licensee determined that although | |||
the | the initiating events were the same, the Chapter 15 analysis did not account | ||
for the loss of extraction steam to the high-pressure heaters, which was the | |||
cause of the temperature difference. During the event, a level imbalance | |||
occurred between the two heater drain tanks, which resulted in the isolation | |||
in the | |||
of extraction steam. | |||
The NRC staff review of analyses of feedwater temperature events at similar | |||
facilities revealed that most of these analyses assumed similar initiating | |||
events as the Comanche Peak analysis and had similar conclusions concerning | |||
the amount of feedwater temperature drop. The licensee has reanalyzed the | |||
and | event to include a 119 OC [246 OF] feedwater temperature drop and concluded | ||
that all accident analysis parameters remained within requirements. | |||
This information notice requires no specific action or written response. If | |||
you have any questions about the information in this notice, please contact | |||
one of the technical contacts listed below or the appropriate Office of | |||
Nuclear Reactor Regulation project manager. | |||
Brian K. Grimes, Acting Director | |||
Division of Reactor Program Management | |||
Office of Nuclear Reactor Regulation | Office of Nuclear Reactor Regulation | ||
Technical contacts: Harry A. Freeman, RIV | |||
(817) 897-1500 | |||
E-mail: haf~nrc.gov | |||
Chu-Yu Liang, NRR | |||
(301) 415-2878 E-mail: cylenrc.gov | |||
Attachment: | Attachment: List Of Recently Issued HRC Information Notices | ||
List Of Recently Issued HRC Information | |||
A1h4 Stir A Je6tQ | |||
K> KJ | K> KJ | ||
Attachment | |||
IN 96-41 July 26, 1996 LIST OF RECENTLY ISSUED | |||
NRC INFORMATION NOTICES | |||
Information Date of | |||
Notice No. Subject Issuance Issued to | |||
96-40 Deficiencies in Material 07/25/96 All holders of OLs or CPs | |||
Dedication and Procure- for nuclear power reactors | |||
ment Practices and in | |||
Audits of Vendors | |||
96-09, Damage in Foreign Steam 07/10/96 All holders of OLs or CPs | |||
Supp. 1 Generator Internals for pressurized-water | |||
reactors | |||
of | 96-39 Estimates of Decay Heat 07/05/96 All holders of OLs or CPs | ||
Using ANS 5.1 Decay Heat for nuclear power reactors | |||
Standard May Vary Signi- ficantly | |||
96-38 Results of Steam Generator 06/21/96 All holders of OLs or CPs | |||
Tube Examinations for pressurized water | |||
reactors | reactors | ||
96-37 Inaccurate Reactor Water 06/18/96 All pressurized water | |||
Level Indication and Inad- reactor facilities holding | |||
vertent Draindown During an operating license or a | |||
Shutdown construction permit | |||
96-36 Degradation of Cooling 06/12/96 All holders of OLs or CPs | |||
Water Systems Due to Icing for nuclear power reactors | |||
96-35 Failure of Safety Systems 06/11/96 All U.S. Nuclear Regulatory | |||
on Self-Shielded Irradia- Commission irradiator | |||
and vendors | tors Because of Inadequate licensees and vendors | ||
Maintenance and Training | |||
96-34 Hydrogen Gas Ignition 05/31/96 All holders of OLs or CPs | |||
during Closure Welding for nuclear power reactors | |||
of a VSC-24 Multi-Assembly | |||
Sealed Basket | |||
OL - Operating License | |||
CP - Construction Permit | |||
*~ - K> K | |||
IN 96-41 July 26, 1996 analysis, the inadvertent opening of the low-pressure heater bypass valve, coupled with the trip of the heater drain pumps, resulted in a feedwater | |||
temperature drop of less than 19 *C [35 OF], and a corresponding power | |||
increase of less than 10 percent. In the actual event, the feedwater | |||
temperature dropped by approximately 111 *C [200 OF], and the licensee | |||
calculated that reactor power would have increased by approximately 35 percent | |||
that although | without operator or protective actions. The licensee determined that although | ||
events were the same, the Chapter 15 analysis did not account | the initiating events were the same, the Chapter 15 analysis did not account | ||
steam to the high-pressure | for the loss of extraction steam to the high-pressure heaters, which was the | ||
cause of the temperature difference. During the event, a level imbalance | |||
occurred between the two heater drain tanks, which resulted in the isolation | |||
of extraction steam. | |||
The NRC staff review of analyses of feedwater temperature events at similar | |||
facilities revealed that most of these analyses assumed similar initiating | |||
events as the Comanche Peak analysis and had similar conclusions concerning | |||
the | the amount of feedwater temperature drop. The licensee has reanalyzed the | ||
temperature | event to include a 119 *C [246 OF] feedwater temperature drop and concluded | ||
that all accident analysis parameters remained within requirements. | |||
This information notice requires no specific action or written response. If | |||
you have any questions about the information in this notice,-please contact | |||
one of the technical contacts listed below or the appropriate Office of | |||
Nuclear Reactor Regulation project manager. | |||
Original signed by Brian K.Grimes | |||
Brian K. Grimes, Acting Director | |||
Division of Reactor Program Management | |||
Office of Nuclear Reactor Regulation | Office of Nuclear Reactor Regulation | ||
Technical contacts: Harry A. Freeman, RIV | |||
(817) 897-1500 | |||
E-mail: haf@nrc.gov | |||
Chu-Yu Liang, NRR | |||
(301) 415-2878 E-mail: cyl~nrc.gov | |||
Attachment: | Attachment: List of Recently Issued NRC Information Notices | ||
List of Recently Issued NRC Information | |||
DOCUMENT NAME: G:\SSK2\INFONOT.C P | |||
To receive a copy of this docunent, tndicate in the box CO~opy So attachment/enclosure EsCopy with attachment/enctosure N | |||
* No | |||
cops | |||
OFFICE C BC:SRXBI BC:LPECB lI (A)DW M i | |||
NAME CYLiang* RJones* AChaffee* | |||
HAFreeman* ____ _ | |||
DATE 16/ 3/96 16/21/96 17/08/96 17LI/96 I | |||
OFFILIAL MLLUM LWUF | |||
* See previous concurrence Tech Editor reviewed & concurred on 05/28/96 | |||
~1~1 -,K) | |||
IN 96-XX | |||
July XX, 1996 for the loss of extraction steam to ti he high-pressure heaters, which was the | |||
cause of the temperature difference. During the event, a level imbalance | |||
occurred between the two heater drain tanks, which resulted in the isolation | |||
of extraction steam. | |||
events at similar | The NRC staff review of analyses of feedwater temperature events at similar | ||
revealed that most of these analyses assumed similar initiating | facilities revealed that most of these analyses assumed similar initiating | ||
events as the Comanche Peak analysis and had similar conclusions | events as the Comanche Peak analysis and had similar conclusions concerning | ||
the amount of feedwater temperature drop. The licensee has reanalyzed the | |||
event to include a 119 'C [246 'F] feedwater temperature drop and concluded | |||
that all accident analysis parameters remained within requirements. | |||
This information notice requires no specific action or written response. If | |||
the | you have any questions about the information in this notice, please contact | ||
one of the technical contacts listed below or the appropriate Office of | |||
Nuclear Reactor Regulation project manager. | |||
Brian K. Grimes, Acting Director | |||
Division of Reactor Program Management | |||
Office of Nuclear Reactor Regulation | Office of Nuclear Reactor Regulation | ||
Technical contacts: Harry A. Freeman, RIV | |||
(817) 897-1500 | |||
E-mail: haf~nrc.gov | |||
Chu-Yu Liang, NRR | |||
(301) 415-2878 E-mail: cyl~nrc.gov | |||
Attachment: | Attachment: List of Recently Issued NRC Information Notices | ||
List of Recently Issued NRC Information | |||
DOCUMENT NAME: G:\SSK2\INFONOT.C P | |||
To receive a copy of this document, indicate in the box CzAopy w/o attachment/enclosure E-Copy with attachment/enclosure N | |||
* No | |||
OFFICE l kd BC: SRXB BC:PECB )D:DR | |||
NAME CYLiang* RJones* AChaffee* BGrimes | |||
BGrimes | |||
HAFreeman* | |||
DATE 6/ 3/96 6/21/96 7/08/96 7/ /96 OFFICIAL RECORD COPY | |||
*See previous concurrence | |||
IN 96-XX | |||
July XX, 1996 for the loss of extraction steam to the high-pressure heaters, which was the | |||
During the event, a level imbalance | cause of the temperature difference. During the event, a level imbalance | ||
occurred between the two heater drain tanks, which resulted in the isolation | |||
the | |||
of extraction steam. | |||
The NRC staff review of analyses of feedwater temperature events at similar | |||
facilities revealed that most of these analyses assumed similar initiating | |||
events as the licensee analysis and had similar conclusions concerning the | |||
temperature | amount of feedwater temperature drop. The licensee has reanalyzed the event | ||
pursuant to Section 50.59 of Title 10 of the Code of Federal Regulations to | |||
that all | include a 119 'c [246 OF] feedwater temperature drop and concluded that all | ||
remained within requirements. | accident analysis parameters remained within requirements. | ||
This information | This information notice requires no specific action or written response. If | ||
notice | you have any questions about the information in this notice, please contact | ||
one of the technical contacts listed below or the appropriate Office of | |||
Nuclear Reactor Regulation project manager. | |||
Brian K. Grimes, Acting Director | |||
Division of Reactor Program Management | |||
Office of Nuclear Reactor Regulation | Office of Nuclear Reactor Regulation | ||
Technical contacts: Harry A. Freeman, RIV | |||
(817) 897-1500 | |||
E-mail: haftnrc.gov | |||
Chu-Yu Liang, NRR | |||
(301) 415-2878 E-mail: cyl~nrc.gov | |||
Attachment: | Attachment: List of Recently Issued NRC Information Notices | ||
List of Recently Issued NRC Information | |||
DOCUMENT NAME: G:\SSK2\INFONOT.C P | |||
To receive a copy of this document, indicate in the box C-Topy u/o attachment/enclosure E=Copy with attachment/enclosure N No | |||
copy | |||
OFFICE CONT:i kd l BC:SRXBLl BC:iPECB lI (A)iD:iDRPM I _ | |||
NAME CYLiang* RJones* AChaffee* BGrimes | |||
l _ HAFreeman* | |||
DATE 6/ 3/96 6/21/96 7/08/96 7/ /96 OFFICIAL KLLUKV UV X! | |||
* See previous concurrence | |||
IN 96-XX | |||
July XX, 1996 for the loss of extraction steam to the high-pressure heaters, which was the | |||
cause of the temperature difference. During the event, a level imbalance | |||
occurred between the two heater drain tanks, which resulted in the isolation | |||
of extraction steam. | |||
The NRC staff review of analyses of feedwater temperature events at similar | |||
facilities revealed that most of these analyses assumed similar initiating | |||
concerning | events as the licensee analysis and had similar conclusions concerning the | ||
amount of feedwater temperature drop. The licensee has reanalyzed the event | |||
pursuant to Section 50.59 of Title 10 of the Code of Federal Regulations to | |||
drop | include a 119 *C [246 *F] feedwater temperature drop and concluded that all | ||
accident analysis parameters remained within requirements. | |||
This information notice requires no specific action or written response. If | |||
you have any questions about the information in this notice, please contact | |||
one of the technical contacts listed below or the appropriate Office of | |||
Nuclear Reactor Regulation project manager. | |||
Brian K. Grimes, Acting Director | |||
Division of Reactor Program Management | |||
Office of Nuclear Reactor Regulation | Office of Nuclear Reactor Regulation | ||
Technical contacts: Harry A. Freeman, RIV | |||
(817) 897-1500 | |||
Internet:haf@nrc.gov | |||
Chu-Yu Liang, NRR | |||
(301) 415-2878 Internet:cyl nrc.gov | |||
Attachment: List of Recently Issued NRC Information Notices | |||
List of Recently Issued NRC Information | |||
DOCUMENT NAME: G:\SSK2\INFONOT.C P | |||
To receive a copy of this document, Indicate in the box Conopy w/c attachment/enclosure EnCopy with attachment/enclosure N | |||
* No | |||
OFFICE CONT: Ekd BC: SLB BC:PECB (A)D:DRPM | |||
NAME CYLiang* RJones* ACh)f BGrimes | |||
l ~~HAFreeman*tVt | |||
DATE 6/ 3/96 6/21/96 7/7/96 7/ /96 OFFICIAL RECOR COPY | |||
* See previous concurrence | |||
K-, / | |||
IN 96-XX | |||
June XX, 1996 for the loss of extraction steam to ti he high-pressure heaters, which was the | |||
cause of the temperature difference. During the event, a level imbalance | |||
occurred between the two heater drain tanks, which resulted inthe isolation | |||
of extraction steam. | |||
events at similar | The NRC staff's review of analyses of feedwater temperature events at similar | ||
revealed that most of these analyses assumed similar initiating | facilities revealed that most of these analyses assumed similar initiating | ||
events as the licensee's | events as the licensee's analysis and had similar conclusions concerning the | ||
amount of feedwater temperature drop. The licensee has reanalyzed the event | |||
pursuant to Section 50.59 of Title 10 of the Code of Federal Regulations to | |||
include a 119 'C [246 OF] feedwater temperature drop and concluded that all | |||
accident analysis parameters remained within requirements. | |||
This information notice requires no specific action or written response. If | |||
the | you have any questions about the information in this notice, please contact | ||
one of the technical contacts listed below or the appropriate Office of | |||
Nuclear Reactor Regulation project manager. | |||
Brian K. Grimes, Acting Director | |||
Division of Reactor Program Management | |||
Office of Nuclear Reactor Regulation | Office of Nuclear Reactor Regulation | ||
Technical contacts: Harry A. Freeman, RIV | |||
(817) 897-1500 | |||
Internet:haffnrc.gov | |||
Chu-Yu Liang, NRR | |||
(301) 415-2878 Internet:cyl@nrc.gov | |||
Attachment: | Attachment: List of Recently Issued NRC Information Notices | ||
List of Recently Issued NRC Information | |||
DOCUMENT NAME: G:\SSK2\INFONOT.CP | |||
To receive a copy of this document, indicate in the box Ciropy w/dattachmeft1/enctosure | To receive a copy of this document, indicate in the box Ciropy w/dattachmeft1/enctosure EnC Ioith attachment/enclosure 1 | ||
* No copy | |||
OFFICE CONT:jkd _l BC: SRXB EC:PECB I _ A)D:DRPM I | |||
NAME CYLiang* RJones AChaffee BGrimes | |||
* | |||
HAFreeman* I- _ | |||
DATE 6/ 3/96 6/2j /96 6/ /96 6/ /96 OFFICIAL RECORD COPY | |||
* See previous concurrence | |||
IN 96-XX | |||
June XX, 1996 detection system. The licensee believed that this system would probably not | |||
because of a different | be significantly affected by feedwater temperatures because of a different | ||
method. | mass flow rate determination method. | ||
final safety analysis report did not accurately | Finally, the licensee's final safety analysis report did not accurately | ||
analyze this transient. | analyze this transient. The actual events were similar to the analysis of the | ||
'Decrease in Feedwater Temperature event presented in Chapter 15. In that | |||
in | analysis, the inadvertent opening of the low-pressure heater bypass valve, coupled with the trip of the heater drain pumps, resulted in a feedwater | ||
temperature drop of less than 35 OF, and a corresponding power increase of | |||
event | less than 10 percent. In the actual event, the feedwater temperature dropped | ||
by approximately 200 OF, and the licensee calculated that reactor power would | |||
have increased by approximately 35 percent without operator or protective | |||
actions. The licensee determined that although the initiating events were the | |||
same, the Chapter 15 analysis did not account for the loss of extraction steam | |||
to the high-pressure heaters, which was the cause of the temperature | |||
difference. During the event, a level imbalance occurred between the two | |||
heater drain tanks, which resulted in the isolation of extraction steam. | |||
The NRC staff's review of analyses of feedwater temperature events at similar | |||
that | facilities revealed that most of these analyses assumed similar initiating | ||
events as the licensee's analysis and had similar conclusions concerning the | |||
amount of feedwater temperature drop. | |||
This information notice requires no specific action or written response. If | |||
you have any questions about the information in this notice, please contact | |||
one of the technical contacts listed below or the appropriate Office of | |||
Nuclear Reactor Regulation project manager. | |||
Brian K. Grimes, Acting Director | |||
Division of Reactor Program Management | |||
Office of Nuclear Reactor Regulation | |||
of | |||
Technical contacts: Harry A. Freeman, RIV | |||
(817) 897-1500 | |||
Internet:haf@nrc.gov | |||
Chu-Yu Liang, NRR | |||
(301) 415-2878 Internet:cyl nrc.gov | |||
Attachment: List of Recently Issued NRC Information Notices | |||
DOCUMENT NAME: G:\SSK2\INFONOT.C P | |||
To receive a copy of this docunent, indicate in the box Catopy w/o attachment/enclosure E-C with attachment/enclosure N | |||
* No copy | |||
OFFICE lCONT:kd l BC:SRXB l BC:PECB l (A)D:DRPM | |||
NAME CYLiang 9 RJones AChaffee BGrimes | |||
HAFreema r _ _ | |||
DATE /96 /96 6/ /96 6/ /96 OFFICIAL RECORD COPY}} | |||
{{Information notice-Nav}} | {{Information notice-Nav}} |
Latest revision as of 04:38, 24 November 2019
K) Ij
K)
UNITED STATES
NUCLEAR REGULATORY COMMISSION
OFFICE OF NUCLEAR REACTOR REGULATION
WASHINGTON, D.C. 20555-0001 July 26, 1996 NRC INFORMATION NOTICE 96-41: EFFECTS OF A DECREASE IN FEEDWATER TEMPERATURE
ON NUCLEAR INSTRUMENTATION
Addressees
All holders of operating licenses or construction permits for pressurized
water reactors (PWRs).
Purpose
The U.S. Nuclear Regulatory Commission (NRC) is issuing this information
notice to alert addressees to the potential for operation above licensed power
as a result of a decrease in feedwater temperature event affecting nuclear
instrumentation. It is expected that recipients will review the information
for applicability to their facilities and consider actions, as appropriate, to
avoid similar problems. However, suggestions contained in this information
notice are not NRC requirements; therefore, no specific action or written
response is required.
Description of Circumstances
On February 14, 1996, the licensee for the Comanche Peak Steam Electric
Station was operating Unit 2 at 95 percent rated thermal power near end-of- core life when a significant reduction in feedwater temperature occurred
because of the loss of feedwater heaters. This reduction, in turn, caused a
reduction in the reactor coolant system cold-leg temperatures. The colder
reactor coolant temperature, with a large negative moderator temperature
coefficient, caused reactor power to increase to approximately 102 percent
according to ex-core nuclear instrumentation. The nitrogen-16 (N-16)
detection system reached the overpower turbine runback setpoint (109 percent)
and initiated a turbine runback. The N-16 detection system measures N-16 activity in the primary coolant as a measure of the total power generation.
This system is a substitute for the resistance temperature detector over- temperature and over-power reactor trip functions used at other Westinghouse
PWRs. The plant stabil zed at an indicated power of approximately 97 percent
according to the ex-core nuclear instrumentation.
After approximately 90 minutes, a second similar turbine runback occurred
while restoring balance-of-plant equipment. Following this runback, reactor
power was stabilized at approximately 100 percent according to nuclear
instrumentation. During the next 30 minutes, the reactor was operated at
approximately 100 percent power as indicated by nuclear instrumentation, with
reactor coolant temperatures below normal. The licensee noted that the N-16
9607220l 60ujo i 7 9,oi4 (R ~IE ctG
IN 96-41 July 26, 1996 detection system indicated approximately 106 percent power and the computer- based plant calorimetric system indicated approximately 102 percent power.
Subsequently, the reactor power was reduced to less than 100 percent by all
indications.
Discussion
There are three aspects of this event which have generic implications. First, with a loss of secondary plant efficiency, programmed T e can no longer
reliably represent core thermal power. Second, the venturi-based input into
the computer-based calorimetric system may not be accurate with cold
feedwater. And third, the final safety analysis report had not analyzed this
transient accurately.
Following the second runback, operators noted that reactor power indicated
<100 percent according to nuclear instrumentation. Although the operators
knew that cold feedwater could cause an increase in the amount of neutron
attenuation, they believed that the nuclear instrumentation indicated
conservatively (i.e., higher than actual) because they were maintaining TA"e
approximately 1.7 eC [3 OF] above TRef. The licensee could not use the
computer-based calorimetric until some time after the second turbine runback
due to maintenance activities. Te , based on the main turbine impulse
pressure, is programmed as a functlon of turbine load and, for normal
efficiency, is a good representation of thermal power. When the unit lost the
feedwater heaters, the plant efficiency decreased. Because the main turbine
electro-hydraulic control system maintained generator output, core thermal
power increased to account for the loss of efficiency, and thus, TRef no
longer accurately represented the core thermal power.
The cold-leg temperature is a more appropriate indicator of the accuracy of
the nuclear instrumentation than programmed TY.e. As the cold-leg temperature
decreased, the amount of neutron attenuation in the downcomer area surrounding
the core increased and hence affected the amount of neutrons reaching the
detectors. The licensee analysis showed that for every 0.6 C (1 OF] of cold- leg temperature change, the nuclear instrumentation was affected by 0.6 to 0.8 percent power. A review of the second transient showed that the cold-leg
temperature was approximately 2.5 °C [4.5 OF] lower than when the detectors
were last calibrated. This corresponded to a 3 to 4 percent error, which
corresponded to the difference in the actual versus the indicated power (104 percent actual versus 100 percent indicated).
During the review, the licensee noted that the computer-based calorimetric was
4 percent lower than the actual thermal power (N-16 power monitor). The
calorimetric was based on feedwater flow measured by venturis. Although the
calorimetric calculation used feedwater temperature as an input, temperatures
significantly different than the normal 227 OC [440 OF] introduced errors into
the calculation.
Finally, the actual events involved temperature and power levels that exceeded
those in the analysis of the Decrease in Feedwater Temperature" event
presented in Chapter 15 of the licensee final safety analysis report. In that
IN 96-41 July 26, 1996 analysis, the inadvertent opening of the low-pressure heater bypass valve, coupled with the trip of the heater drain pumps, resulted in a feedwater
temperature drop of less than 19 'C (35 OF], and a corresponding power
increase of less than 10 percent. In the actual event, the feedwater
temperature dropped by approximately 111 °C (200 OF], and the licensee
calculated that reactor power would have increased by approximately 35 percent
without operator or protective actions. The licensee determined that although
the initiating events were the same, the Chapter 15 analysis did not account
for the loss of extraction steam to the high-pressure heaters, which was the
cause of the temperature difference. During the event, a level imbalance
occurred between the two heater drain tanks, which resulted in the isolation
of extraction steam.
The NRC staff review of analyses of feedwater temperature events at similar
facilities revealed that most of these analyses assumed similar initiating
events as the Comanche Peak analysis and had similar conclusions concerning
the amount of feedwater temperature drop. The licensee has reanalyzed the
event to include a 119 OC [246 OF] feedwater temperature drop and concluded
that all accident analysis parameters remained within requirements.
This information notice requires no specific action or written response. If
you have any questions about the information in this notice, please contact
one of the technical contacts listed below or the appropriate Office of
Nuclear Reactor Regulation project manager.
Brian K. Grimes, Acting Director
Division of Reactor Program Management
Office of Nuclear Reactor Regulation
Technical contacts: Harry A. Freeman, RIV
(817) 897-1500
E-mail: haf~nrc.gov
Chu-Yu Liang, NRR
(301) 415-2878 E-mail: cylenrc.gov
Attachment: List Of Recently Issued HRC Information Notices
A1h4 Stir A Je6tQ
K> KJ
Attachment
IN 96-41 July 26, 1996 LIST OF RECENTLY ISSUED
NRC INFORMATION NOTICES
Information Date of
Notice No. Subject Issuance Issued to
96-40 Deficiencies in Material 07/25/96 All holders of OLs or CPs
Dedication and Procure- for nuclear power reactors
ment Practices and in
Audits of Vendors
96-09, Damage in Foreign Steam 07/10/96 All holders of OLs or CPs
Supp. 1 Generator Internals for pressurized-water
reactors
96-39 Estimates of Decay Heat 07/05/96 All holders of OLs or CPs
Using ANS 5.1 Decay Heat for nuclear power reactors
Standard May Vary Signi- ficantly
96-38 Results of Steam Generator 06/21/96 All holders of OLs or CPs
Tube Examinations for pressurized water
reactors
96-37 Inaccurate Reactor Water 06/18/96 All pressurized water
Level Indication and Inad- reactor facilities holding
vertent Draindown During an operating license or a
Shutdown construction permit
96-36 Degradation of Cooling 06/12/96 All holders of OLs or CPs
Water Systems Due to Icing for nuclear power reactors
96-35 Failure of Safety Systems 06/11/96 All U.S. Nuclear Regulatory
on Self-Shielded Irradia- Commission irradiator
tors Because of Inadequate licensees and vendors
Maintenance and Training
96-34 Hydrogen Gas Ignition 05/31/96 All holders of OLs or CPs
during Closure Welding for nuclear power reactors
of a VSC-24 Multi-Assembly
Sealed Basket
OL - Operating License
CP - Construction Permit
- ~ - K> K
IN 96-41 July 26, 1996 analysis, the inadvertent opening of the low-pressure heater bypass valve, coupled with the trip of the heater drain pumps, resulted in a feedwater
temperature drop of less than 19 *C [35 OF], and a corresponding power
increase of less than 10 percent. In the actual event, the feedwater
temperature dropped by approximately 111 *C [200 OF], and the licensee
calculated that reactor power would have increased by approximately 35 percent
without operator or protective actions. The licensee determined that although
the initiating events were the same, the Chapter 15 analysis did not account
for the loss of extraction steam to the high-pressure heaters, which was the
cause of the temperature difference. During the event, a level imbalance
occurred between the two heater drain tanks, which resulted in the isolation
of extraction steam.
The NRC staff review of analyses of feedwater temperature events at similar
facilities revealed that most of these analyses assumed similar initiating
events as the Comanche Peak analysis and had similar conclusions concerning
the amount of feedwater temperature drop. The licensee has reanalyzed the
event to include a 119 *C [246 OF] feedwater temperature drop and concluded
that all accident analysis parameters remained within requirements.
This information notice requires no specific action or written response. If
you have any questions about the information in this notice,-please contact
one of the technical contacts listed below or the appropriate Office of
Nuclear Reactor Regulation project manager.
Original signed by Brian K.Grimes
Brian K. Grimes, Acting Director
Division of Reactor Program Management
Office of Nuclear Reactor Regulation
Technical contacts: Harry A. Freeman, RIV
(817) 897-1500
E-mail: haf@nrc.gov
Chu-Yu Liang, NRR
(301) 415-2878 E-mail: cyl~nrc.gov
Attachment: List of Recently Issued NRC Information Notices
DOCUMENT NAME: G:\SSK2\INFONOT.C P
To receive a copy of this docunent, tndicate in the box CO~opy So attachment/enclosure EsCopy with attachment/enctosure N
- No
cops
OFFICE C BC:SRXBI BC:LPECB lI (A)DW M i
NAME CYLiang* RJones* AChaffee*
HAFreeman* ____ _
DATE 16/ 3/96 16/21/96 17/08/96 17LI/96 I
OFFILIAL MLLUM LWUF
- See previous concurrence Tech Editor reviewed & concurred on 05/28/96
~1~1 -,K)
IN 96-XX
July XX, 1996 for the loss of extraction steam to ti he high-pressure heaters, which was the
cause of the temperature difference. During the event, a level imbalance
occurred between the two heater drain tanks, which resulted in the isolation
of extraction steam.
The NRC staff review of analyses of feedwater temperature events at similar
facilities revealed that most of these analyses assumed similar initiating
events as the Comanche Peak analysis and had similar conclusions concerning
the amount of feedwater temperature drop. The licensee has reanalyzed the
event to include a 119 'C [246 'F] feedwater temperature drop and concluded
that all accident analysis parameters remained within requirements.
This information notice requires no specific action or written response. If
you have any questions about the information in this notice, please contact
one of the technical contacts listed below or the appropriate Office of
Nuclear Reactor Regulation project manager.
Brian K. Grimes, Acting Director
Division of Reactor Program Management
Office of Nuclear Reactor Regulation
Technical contacts: Harry A. Freeman, RIV
(817) 897-1500
E-mail: haf~nrc.gov
Chu-Yu Liang, NRR
(301) 415-2878 E-mail: cyl~nrc.gov
Attachment: List of Recently Issued NRC Information Notices
DOCUMENT NAME: G:\SSK2\INFONOT.C P
To receive a copy of this document, indicate in the box CzAopy w/o attachment/enclosure E-Copy with attachment/enclosure N
- No
OFFICE l kd BC: SRXB BC:PECB )D:DR
NAME CYLiang* RJones* AChaffee* BGrimes
HAFreeman*
DATE 6/ 3/96 6/21/96 7/08/96 7/ /96 OFFICIAL RECORD COPY
- See previous concurrence
IN 96-XX
July XX, 1996 for the loss of extraction steam to the high-pressure heaters, which was the
cause of the temperature difference. During the event, a level imbalance
occurred between the two heater drain tanks, which resulted in the isolation
of extraction steam.
The NRC staff review of analyses of feedwater temperature events at similar
facilities revealed that most of these analyses assumed similar initiating
events as the licensee analysis and had similar conclusions concerning the
amount of feedwater temperature drop. The licensee has reanalyzed the event
pursuant to Section 50.59 of Title 10 of the Code of Federal Regulations to
include a 119 'c [246 OF] feedwater temperature drop and concluded that all
accident analysis parameters remained within requirements.
This information notice requires no specific action or written response. If
you have any questions about the information in this notice, please contact
one of the technical contacts listed below or the appropriate Office of
Nuclear Reactor Regulation project manager.
Brian K. Grimes, Acting Director
Division of Reactor Program Management
Office of Nuclear Reactor Regulation
Technical contacts: Harry A. Freeman, RIV
(817) 897-1500
E-mail: haftnrc.gov
Chu-Yu Liang, NRR
(301) 415-2878 E-mail: cyl~nrc.gov
Attachment: List of Recently Issued NRC Information Notices
DOCUMENT NAME: G:\SSK2\INFONOT.C P
To receive a copy of this document, indicate in the box C-Topy u/o attachment/enclosure E=Copy with attachment/enclosure N No
copy
OFFICE CONT:i kd l BC:SRXBLl BC:iPECB lI (A)iD:iDRPM I _
NAME CYLiang* RJones* AChaffee* BGrimes
l _ HAFreeman*
DATE 6/ 3/96 6/21/96 7/08/96 7/ /96 OFFICIAL KLLUKV UV X!
- See previous concurrence
IN 96-XX
July XX, 1996 for the loss of extraction steam to the high-pressure heaters, which was the
cause of the temperature difference. During the event, a level imbalance
occurred between the two heater drain tanks, which resulted in the isolation
of extraction steam.
The NRC staff review of analyses of feedwater temperature events at similar
facilities revealed that most of these analyses assumed similar initiating
events as the licensee analysis and had similar conclusions concerning the
amount of feedwater temperature drop. The licensee has reanalyzed the event
pursuant to Section 50.59 of Title 10 of the Code of Federal Regulations to
include a 119 *C [246 *F] feedwater temperature drop and concluded that all
accident analysis parameters remained within requirements.
This information notice requires no specific action or written response. If
you have any questions about the information in this notice, please contact
one of the technical contacts listed below or the appropriate Office of
Nuclear Reactor Regulation project manager.
Brian K. Grimes, Acting Director
Division of Reactor Program Management
Office of Nuclear Reactor Regulation
Technical contacts: Harry A. Freeman, RIV
(817) 897-1500
Internet:haf@nrc.gov
Chu-Yu Liang, NRR
(301) 415-2878 Internet:cyl nrc.gov
Attachment: List of Recently Issued NRC Information Notices
DOCUMENT NAME: G:\SSK2\INFONOT.C P
To receive a copy of this document, Indicate in the box Conopy w/c attachment/enclosure EnCopy with attachment/enclosure N
- No
OFFICE CONT: Ekd BC: SLB BC:PECB (A)D:DRPM
NAME CYLiang* RJones* ACh)f BGrimes
l ~~HAFreeman*tVt
DATE 6/ 3/96 6/21/96 7/7/96 7/ /96 OFFICIAL RECOR COPY
- See previous concurrence
K-, /
IN 96-XX
June XX, 1996 for the loss of extraction steam to ti he high-pressure heaters, which was the
cause of the temperature difference. During the event, a level imbalance
occurred between the two heater drain tanks, which resulted inthe isolation
of extraction steam.
The NRC staff's review of analyses of feedwater temperature events at similar
facilities revealed that most of these analyses assumed similar initiating
events as the licensee's analysis and had similar conclusions concerning the
amount of feedwater temperature drop. The licensee has reanalyzed the event
pursuant to Section 50.59 of Title 10 of the Code of Federal Regulations to
include a 119 'C [246 OF] feedwater temperature drop and concluded that all
accident analysis parameters remained within requirements.
This information notice requires no specific action or written response. If
you have any questions about the information in this notice, please contact
one of the technical contacts listed below or the appropriate Office of
Nuclear Reactor Regulation project manager.
Brian K. Grimes, Acting Director
Division of Reactor Program Management
Office of Nuclear Reactor Regulation
Technical contacts: Harry A. Freeman, RIV
(817) 897-1500
Internet:haffnrc.gov
Chu-Yu Liang, NRR
(301) 415-2878 Internet:cyl@nrc.gov
Attachment: List of Recently Issued NRC Information Notices
DOCUMENT NAME: G:\SSK2\INFONOT.CP
To receive a copy of this document, indicate in the box Ciropy w/dattachmeft1/enctosure EnC Ioith attachment/enclosure 1
- No copy
OFFICE CONT:jkd _l BC: SRXB EC:PECB I _ A)D:DRPM I
NAME CYLiang* RJones AChaffee BGrimes
HAFreeman* I- _
DATE 6/ 3/96 6/2j /96 6/ /96 6/ /96 OFFICIAL RECORD COPY
- See previous concurrence
IN 96-XX
June XX, 1996 detection system. The licensee believed that this system would probably not
be significantly affected by feedwater temperatures because of a different
mass flow rate determination method.
Finally, the licensee's final safety analysis report did not accurately
analyze this transient. The actual events were similar to the analysis of the
'Decrease in Feedwater Temperature event presented in Chapter 15. In that
analysis, the inadvertent opening of the low-pressure heater bypass valve, coupled with the trip of the heater drain pumps, resulted in a feedwater
temperature drop of less than 35 OF, and a corresponding power increase of
less than 10 percent. In the actual event, the feedwater temperature dropped
by approximately 200 OF, and the licensee calculated that reactor power would
have increased by approximately 35 percent without operator or protective
actions. The licensee determined that although the initiating events were the
same, the Chapter 15 analysis did not account for the loss of extraction steam
to the high-pressure heaters, which was the cause of the temperature
difference. During the event, a level imbalance occurred between the two
heater drain tanks, which resulted in the isolation of extraction steam.
The NRC staff's review of analyses of feedwater temperature events at similar
facilities revealed that most of these analyses assumed similar initiating
events as the licensee's analysis and had similar conclusions concerning the
amount of feedwater temperature drop.
This information notice requires no specific action or written response. If
you have any questions about the information in this notice, please contact
one of the technical contacts listed below or the appropriate Office of
Nuclear Reactor Regulation project manager.
Brian K. Grimes, Acting Director
Division of Reactor Program Management
Office of Nuclear Reactor Regulation
Technical contacts: Harry A. Freeman, RIV
(817) 897-1500
Internet:haf@nrc.gov
Chu-Yu Liang, NRR
(301) 415-2878 Internet:cyl nrc.gov
Attachment: List of Recently Issued NRC Information Notices
DOCUMENT NAME: G:\SSK2\INFONOT.C P
To receive a copy of this docunent, indicate in the box Catopy w/o attachment/enclosure E-C with attachment/enclosure N
- No copy
OFFICE lCONT:kd l BC:SRXB l BC:PECB l (A)D:DRPM
NAME CYLiang 9 RJones AChaffee BGrimes
HAFreema r _ _
DATE /96 /96 6/ /96 6/ /96 OFFICIAL RECORD COPY