ML18102A372: Difference between revisions

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| issue date = 09/11/1996
| issue date = 09/11/1996
| title = Provides Commitments Pse&G Made to NRC Re LER (311/96-002-01).LER Suppl Entitled Waste Gas Decay Tank Oxygen Concentration Exceeded TSs Limit Attached
| title = Provides Commitments Pse&G Made to NRC Re LER (311/96-002-01).LER Suppl Entitled Waste Gas Decay Tank Oxygen Concentration Exceeded TSs Limit Attached
| author name = GARCHOW D F
| author name = Garchow D
| author affiliation = PUBLIC SERVICE ELECTRIC & GAS CO. OF NEW JERSEY
| author affiliation = PUBLIC SERVICE ELECTRIC & GAS CO. OF NEW JERSEY
| addressee name =  
| addressee name =  
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=Text=
=Text=
{{#Wiki_filter:.f .  
{{#Wiki_filter:e
.' e Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038-0236 Nuclear Business Unit SEP 111996 LR-N96289  
.f         .   '.*-
: u. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Gentlemen:
    *-....,*.~* .'
LER311/96-002-01 SALEM GENERATING STATION -UNIT 1 FACILITY OPERATING LICENSE NO. DPR-75 DOCKET NO. 50-311 This Licensee Event Report Supplement entitled "Waste Gas Decay Tank Ozygen Concentration Exceeded Technical Specifications Limit" is being submitted pursuant to the requirements of the Code of Federal Regulations 10CFR50. 73 (a) (2) (ii) (A). Attachment SORC Mtg. 96-122 JMO/tcp c Distribution LER File 3.7 9609180067 960911 PDR ADOCK 05000311 S PDR David F.
PS~G Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038-0236 Nuclear Business Unit SEP 111996 LR-N96289
General Manager -Salem Operations
: u.         S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Gentlemen:
.'\ _,. 95-2168 REV. 6/94 Document Control Desk LR-N96289 Attac:::hrnent A e SEP 11 7996 The following represents the commitments that Public Service Electric & Gas (PSE&G) made to the Nuclear Regulatory Commission (NRC) relative to this LER (311/96-002-01).
LER311/96-002-01 SALEM GENERATING STATION - UNIT 1 FACILITY OPERATING LICENSE NO. DPR-75 DOCKET NO. 50-311 This Licensee Event Report Supplement entitled "Waste Gas Decay Tank Ozygen Concentration Exceeded Technical Specifications Limit" is being submitted pursuant to the requirements of the Code of Federal Regulations 10CFR50. 73 (a) (2) (ii) (A).
The commitments are as follows: 1. Oxygen concentration levels were restored to Technical Specifications requirements at Unit 2. 2. Oxygen concentration levels were restored to Technical Specifications requirements at.Unit 1 as of August 1, 1996. 3. The problems with this Technical Specification have been communicated to the operating crews. Isolation of waste gas from all holdup tanks, if oxygen levels exceed 4 percent, will be carefully evaluated since such action may cause uncontrolled release of waste gas into the Auxiliary Building.
Q~,~::o~~:Gat:~ow David F.
If isolation of all waste gas is not practical, the tank with the high oxygen levels will be isolated and purged, and another tank will be placed in service, as described in the UFSAR. If this occurs prior to a change to the Technical Specifications, a supplement to this LER will be submitted.  
                                                                  ~~Q1 General Manager -
: 4. Operations Management has emphasized the need to comply with the intent and the exact wording of the Technical Specifications, and to immediately address any issues where the intent and the wording are in conflict.  
Salem Operations Attachment SORC Mtg. 96-122 JMO/tcp c             Distribution LER File 3.7
                                                                                              .'\  _,.
9609180067 960911 PDR ADOCK 05000311 S                           PDR 95-2168 REV. 6/94
 
e Document Control Desk                         SEP 11 7996 LR-N96289 Attac:::hrnent A The following represents the commitments that Public Service Electric
& Gas (PSE&G) made to the Nuclear Regulatory Commission (NRC) relative to this LER (311/96-002-01). The commitments are as follows:
: 1. Oxygen concentration levels were restored to Technical Specifications requirements at Unit 2.
: 2. Oxygen concentration levels were restored to Technical Specifications requirements at.Unit 1 as of August 1, 1996.
: 3. The problems with this Technical Specification have been communicated to the operating crews.     Isolation of waste gas from all holdup tanks, if oxygen levels exceed 4 percent, will be carefully evaluated since such action may cause uncontrolled release of waste gas into the Auxiliary Building.       If isolation of all waste gas is not practical, the tank with the high oxygen levels will be isolated and purged, and another tank will be placed in service, as described in the UFSAR.       If this occurs prior to a change to the Technical Specifications, a supplement to this LER will be submitted.
: 4. Operations Management has emphasized the need to comply with the intent and the exact wording of the Technical Specifications, and to immediately address any issues where the intent and the wording are in conflict.
: 5. A request to resolve Technical Specification 3.11.2.5 administrative/wording problems was submitted to the NRC on August 15, 1996.}}
: 5. A request to resolve Technical Specification 3.11.2.5 administrative/wording problems was submitted to the NRC on August 15, 1996.}}

Latest revision as of 09:36, 21 October 2019

Provides Commitments Pse&G Made to NRC Re LER (311/96-002-01).LER Suppl Entitled Waste Gas Decay Tank Oxygen Concentration Exceeded TSs Limit Attached
ML18102A372
Person / Time
Site: Salem PSEG icon.png
Issue date: 09/11/1996
From: Garchow D
Public Service Enterprise Group
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
Shared Package
ML18102A373 List:
References
LR-N96289, NUDOCS 9609180067
Download: ML18102A372 (2)


Text

e

.f . '.*-

  • -....,*.~* .'

PS~G Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038-0236 Nuclear Business Unit SEP 111996 LR-N96289

u. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Gentlemen:

LER311/96-002-01 SALEM GENERATING STATION - UNIT 1 FACILITY OPERATING LICENSE NO. DPR-75 DOCKET NO. 50-311 This Licensee Event Report Supplement entitled "Waste Gas Decay Tank Ozygen Concentration Exceeded Technical Specifications Limit" is being submitted pursuant to the requirements of the Code of Federal Regulations 10CFR50. 73 (a) (2) (ii) (A).

Q~,~::o~~:Gat:~ow David F.

~~Q1 General Manager -

Salem Operations Attachment SORC Mtg.96-122 JMO/tcp c Distribution LER File 3.7

.'\ _,.

9609180067 960911 PDR ADOCK 05000311 S PDR 95-2168 REV. 6/94

e Document Control Desk SEP 11 7996 LR-N96289 Attac:::hrnent A The following represents the commitments that Public Service Electric

& Gas (PSE&G) made to the Nuclear Regulatory Commission (NRC) relative to this LER (311/96-002-01). The commitments are as follows:

1. Oxygen concentration levels were restored to Technical Specifications requirements at Unit 2.
2. Oxygen concentration levels were restored to Technical Specifications requirements at.Unit 1 as of August 1, 1996.
3. The problems with this Technical Specification have been communicated to the operating crews. Isolation of waste gas from all holdup tanks, if oxygen levels exceed 4 percent, will be carefully evaluated since such action may cause uncontrolled release of waste gas into the Auxiliary Building. If isolation of all waste gas is not practical, the tank with the high oxygen levels will be isolated and purged, and another tank will be placed in service, as described in the UFSAR. If this occurs prior to a change to the Technical Specifications, a supplement to this LER will be submitted.
4. Operations Management has emphasized the need to comply with the intent and the exact wording of the Technical Specifications, and to immediately address any issues where the intent and the wording are in conflict.
5. A request to resolve Technical Specification 3.11.2.5 administrative/wording problems was submitted to the NRC on August 15, 1996.