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{{#Wiki_filter:r NRC FORM 195 U.S.NUCLEAR REGULATORV COMMISSION I2.1E)NRC DISTRIBUTION FoR PART 50 DOCKET'MATERIAL DOCKET NUMBER S-3 FILE NUMBER INCIDENT REPORT Mr Moseley@LETTER 0 ORIGINAL ,@COPV QNOTOR IZED II UN C LASS I F I E D~p PROP Florida~Pwr 6 Light Co giami, Fla A D Scfimidt.INPUT FORM DATE OF DOCUMENT 6-18-76 DATE RECEIVED 7 6 76 NUMSER OF COPIES RECEIVED no originals rec'd NA/8QN8/DESCRIPTION Ltr trans the, following:
{{#Wiki_filter:r NRC FORM 195 I2.1E)                                                                                        S  -3 U.S. NUCLEAR REGULATORV COMMISSION DOCKET NUMBER FILE NUMBER NRC DISTRIBUTION FoR PART 50 DOCKET'MATERIAL                                   INCIDENT REPORT Florida~Pwr 6 Light               DATE OF DOCUMENT Mr Moseley                                                                Co giami, Fla                                       6-18-76 A D Scfimidt  .                  DATE RECEIVED 7 6   76
ENCLOSURE S.i J I 1 Licensee Event Report (R08'76-28) on 6-4-76 concerning failure of hydrogen sampling sampling system isolat on valves.........
    @LETTER                  QNOTOR IZED            PROP                  INPUT FORM          NUMSER OF COPIES RECEIVED 0 ORIGINAL          IIUN CpLASS F I E D I
),~I Kt Lucie 81 1It~'~II i NOTE: IF PERSONNEL EXPOSURE IS INVOLVED SEND DIRECTLY TO KREGER/J, COLLINS NCH CH EF'CYS FOR AC ON I LIC~ASST~'.H/CYS ACRS I CYS HQbBKR&fSE T TO LA FOR ACTION/INFORMATION 7 INTERNAL D IST RI BUTION NRC PDR IGE 2 SCHROEDER/IPPOLITO HOUSTON NOVAK CHECK GRIhIES CASE LE HANAUER TEDESCO hIACCARY EISENHUT BAER'HA'0 VOLLhIER/HUNCH EGER J COLLINS PDR~IC: S~EXTEIINAL DISTRIBUTION CONTROL NUMBER NIIC FOIIM IQS f2 161 r)h---c>.".ii (8S-i)Vi;05<)
no originals rec'd
aXOqO>.SII.~VS 99afIOOiZ gfl~lqfidl8 fI9'iqOl4gff
      ,@COPV
>0 9 XIII';61 QIIlfl I93IIOO~~~~.~~.~BOV I I'V LIOS:f GEO'.5 M33 elec.'fI~S QUG<.'
                                  ~
r E~.~P.O, IIOX 013100, NIIAMI, Ft.ORIDA 33101 FLORIOA FOVJFR&LIGHT COMPANY June 18, 1976 PRN-LI-7 6-15 0 Mr.Norman C.Moseley, Director, Region II Office of Inspection and, Enforcement U.S.Nuclear Regulatory Commission 230 Peachtree Street, N.N., Suite 818 Atlanta, Georgia 30303
NA/8QN8/
DESCRIPTION                                                   ENCLOSURE    S.i J
1 I
Ltr trans the, following:                                 Licensee Event Report (R08'76-28) on 6-4-76 concerning failure of hydrogen sampling sampling system isolat on valves.........
I ),
                                                                                                            ~
1It ~'~IIi Kt Lucie 81                            NOTE:     IF PERSONNEL EXPOSURE IS INVOLVED SEND DIRECTLY TO KREGER/J, COLLINS FOR ACTION/INFORMATION                      7 NCH CH   EF' CYS FOR AC     ON I     LIC ~ ASST ~ '.
H/     CYS ACRS   I   CYS   HQbBKR&fSE T TO LA INTERNAL D IST RI BUTION NRC PDR IGE     2 SCHROEDER/IPPOLITO HOUSTON NOVAK CHECK GRIhIES CASE LE HANAUER TEDESCO hIACCARY EISENHUT BAER
    'HA'0 VOLLhIER/HUNCH EGER J   COLLINS EXTEIINALDISTRIBUTION                                    CONTROL NUMBER PDR ~
IC:
S   ~
NIIC FOIIM IQS f2   161


==Dear Mr.Moseley:==
r)h-- -c> .".ii (8S-i)Vi;05<) aXOqO>. SII.~VS 99afIOOiZ gfl~lqfidl8 fI9'iqOl4gff >0 9 XIII';61 QIIlflI93IIOO
REPORTABLE OCCURRENCE 335-76-28 ST.LUCIE UNIT 1 DATE OP OCCURRENCE:
  ~ ~ ~ ~ . ~ ~ . ~ BOV I I'V LIOS:f GEO '.5 M33 elec.'fI ~S QUG<.'
JUNE 4, 1976 C'YDROGEN SAMPLING SYSTEM ISOLATION VALVES The attached Licensee Event Report is being submitted in accordance with Technical Specificaiton 6.9 to provide prompt notification of the subject occurrence.
 
Very truly yours,>sr.D.Schmidt Vice President Power Resources.MAS/ao Attachment cc: Jack R.Newman, Esquire Director, Office of Inspection and Enforcement (40)'irector, Of f ice of Management Inf ormation and Program Control (3)iQg/~(~HELPING BUILD FLORIDA 0~~t
P.O, IIOX 013100, NIIAMI, Ft.ORIDA 33101 r E ~
[oa~]89 r CONTROL SLOCK:~1 UCENSEE NAME, S L S 1 0 14 15 LICENSEE EVENT REPORT EVENT TYPE UCENSE TYPE UCENSE NUMBER 0 0 0 0 0-0 0 4 l.'1 1 1~01 25 26 30 31 32 (~BE PRINT ALL REQUIRED INFORMATION)
      . ~
REPORT.REPORT CATEGORY TYPE SOURCE"rQO71 CON'T~T L.0 7 8'57.58.59 60 61 EVENT OESCRIPTION'g R'f the tes'tin'OCKET NUMBER EVENT GATE REPORT OATE 5 0-0 3 3 5 0 6 0 4 7 6 G 6 1 8 7 6 68 69 74 75.80 ro osed for Unit 2 h drogen sampling system*isola-7 8'9 80 t00$~tion valVOs led to an examination of the, purchase.order for the identical 7 8 9~04 1 valves Unit 1 FSAR Section 3.11 classifies these valves as 80 7 8 9 80 Qg'ronmental'ate or lA.'owever, it has been determined that the 7 8.9 80 Q~g Unit 1 valves have not been t*e tested for the proposed environment in 7 8 9 SYSTEM CAUSE COBE COOE COMPONENT COOE[OOTI~BE~A'A L V E 7 8 910 11 12 CAUSE OESCRIPTION Qg Unit 1 h dio en sam lin X A 17 43 COMPONENT MANUFACIU PER X 9 9 9 47 VQULTQN N s stem isolation valves were not tested-for 80 7 8 9 80 (oa>]ate or 1A environmental conditions in accordance with IEEE-323{1971)7 8 9 80'Qg because the re uirement to do so was not specified in the purchase order.OTHER STATUS N/A 7 8 9 LOSS OR OAMAGE TO FACILITY TYPE OESCR{PTION uz.7>>8 9~10 PUBLICITY 7 89 7 89 FACIUTY STATUS%POWER[111'B~05 0 7 8 9.10 12 13 FORM OF ACTIVITY C0ATENT RELEASEO OF RELEASE AMOUNT OF ACTIVITY[rig~z~z N/A 7'S.S 10 11 PERSONNEL EXPOSURES NUMBER TYPE OESCR{PTION
FLORIOA FOVJFR & LIGHT COMPANY June 18, 1976 PRN-LI-7 6-15 0 Mr. Norman C. Moseley,    Director, Region  II Office of Inspection and, Enforcement U. S. Nuclear Regulatory Commission 230 Peachtree Street, N.N., Suite 818 Atlanta, Georgia 30303
~s~oo o~z 7 8 9, 11 12 13 PERSONNEL INJURIES OESCR{PTION 7 8 9 11 12 PROBABLE CONSEQUENCES
 
*t11g METHOO OF OISCOVERY~d 44-45 46 44 45 N/A N/A N/A N/A N/A OISCOVERY OESCRIPTION Purchase order review LOCATION OF RELEASE N/A 80 80 80.80 80 80 80'0 AOOITIONAL FACTORS~18 See page two (2)for continuation of Event Description., 7 8 9 Component Manufacturer
==Dear Mr. Moseley:==
-Circle Seal Corporation 7 89 80 80 NAME'AN'HONE.
 
305/552-3779 CPO ddI r dd7 REPORTABLE OCCURANCE 335-76-28 LICENSEE EVENT REPORT PAGE'TWO Event Descri tion (Continued) accordance with'IEEE-323(1971) because the requirement to do so was not specified in the purchase order.As an interim corrective action, administrative guidelines have been written to inform appropriate personnel of the action to be taken if the valves wild not operate under post-accident conditions.
REPORTABLE OCCURRENCE 335-76-28 ST. LUCIE UNIT 1 DATE OP OCCURRENCE: JUNE 4, 1976 C'YDROGEN SAMPLING SYSTEM ISOLATION VALVES The attached Licensee Event Report is being submitted in accordance with Technical Specificaiton 6.9 to provide prompt notification of the subject occurrence.
Operations personnel have been informed that they'hould actuate the hydrogen recombiners if a containment hydrogen sample cannot be taken.Based on FSAR hydrogen generation analysis for the existing pl'ant design, the operator has 45 days to actuate either hydrogen recombiner before the hydrogen concentration reaches 4%.An investigation of possible long-term corrective action is being conducted and a follow-up report will be submitted upon completion of the investigation.
Very   truly yours,
                  >sr .
D. Schmidt Vice President Power Resources
          .MAS/ao Attachment cc:   Jack R. Newman, Esquire Director, Office of Inspection and Enforcement           (40)
                'irector, Of fice of Management Information and Program Control (3) iQg/~(~
HELPING BUILD FLORIDA
 
0 ~
t
    ~
 
LICENSEE EVENT REPORT r
CONTROL         SLOCK:~                                                       (~BE PRINT ALL REQUIRED INFORMATION) 1 UCENSEE                                                                                 UCENSE              EVENT NAME,                                   UCENSE NUMBER                                TYPE                TYPE
[oa~]                                S   L   S     1         0         0   0 0 0       0   0     0         4   l.'1   1   1     ~01 89
                        ~
14    15                                          25     26                 30     31     32 REPORT. REPORT
                        'f CATEGORY                     TYPE     SOURCE           'OCKET  NUMBER                        EVENT GATE                    REPORT OATE "rQO71   CON'T                                   T           L.     0   5 0     0       3 3   5       0     6   0 4     7 6         G     6 1 8       7 6 7      8          '57              . 58      .59        60    61                              68   69                       74   75                     . 80 EVENT      OESCRIPTION'g R                                  the tes'tin              ro osed for Unit 2 h drogen sampling system*isola-7     8'9                                                                                                                                                             80 t00$ tion valVOs led to an examination of the, purchase .order for the identical
            ~
7 8 9                                                                                                                                                                 80
    ~04                               1 valves                   Unit 1 FSAR Section 3.11 classifies these valves as 7 8 9 Qg 7 8.9
                        'ronmental'ate or lA. 'owever,                                                 it   has been determined that the 80 7
Q~   g Unit 1 valves have not been 8 9 t   *e tested for the proposed environment in 80 80 SYSTEM                   CAUSE                                                             COMPONENT COBE                   COOE                 COMPONENT COOE                             MANUFACIUPER          VQULTQN
[OOTI     ~BE                           ~A'                   A L V       E X            A            X    9 9    9              N 7     8   910                           11         12                       17      43                            47 CAUSE OESCRIPTION 7
Qg8 9 Unit 1 h dio en sam lin s stem isolation valves were not tested -for 80 (oa>]         ate or 1A environmental conditions in accordance with IEEE-323 {1971) 7 8 9 because the re uirement to do so was not specified in the purchase order.                                                                             80'Qg 7     89                                                                                                                                                           80 FACIUTY                                                                     METHOO OF STATUS                         % POWER               OTHER STATUS        OISCOVERY                      OISCOVERY OESCRIPTION
[111'B                                     .10
                                                ~05         0                   N/A              ~d          Purchase        order review 7     8         9                                           12 13                       44 45      46                                                        80 FORM OF ACTIVITY                   C0ATENT RELEASEO                   OF RELEASE             AMOUNT OF ACTIVITY                                         LOCATION OF RELEASE
[rig             ~z                         ~z                     N/A                                                    N/A 7     'S       .S                             10       11                                 44      45                                                              80 .
PERSONNEL EXPOSURES NUMBER                       TYPE       OESCR{PTION
  ~s ~oo                               o       ~z                                                 N/A 7     8   9,                           11     12       13                                                                                                         80 PERSONNEL INJURIES OESCR{PTION N/A 7     8 9                             11   12                                                                                                                     80
* PROBABLE CONSEQUENCES t11g                                                                                             N/A 7 8 9                                                                                                                                                                80 LOSS OR OAMAGE TO FACILITY TYPE        OESCR{PTION uz.                                                                                    N/A 7>>    8 9    ~      10                                                                                                                                            80 PUBLICITY N/A 7      89                                                                                                                                                          '0 AOOITIONAL FACTORS
  ~18             See page two (2)                                 for continuation of Event Description.,
7 8 9                                                                                                                                                               80 Component Manufacturer                                         Circle     Seal Corporation 7     89 NAME'AN'HONE.                                                                                   305/552-3779 CPO 80 ddI r dd7
 
REPORTABLE OCCURANCE 335-76-28 LICENSEE EVENT REPORT PAGE'TWO Event Descri tion (Continued) accordance with 'IEEE-323(1971) because the requirement to do so was not specified in the purchase order. As an interim corrective action, administrative guidelines have been written to inform appropriate personnel of the action to be taken   if the valves wild not operate under post-accident conditions. Operations personnel have been informed that they'hould actuate the hydrogen recombiners if a containment hydrogen sample cannot be taken. Based on FSAR hydrogen generation analysis for the existing pl'ant design, the operator has 45 days to actuate either hydrogen recombiner before the hydrogen concentration reaches 4%. An investigation of possible long-term corrective action is being conducted and a follow-up report will be submitted upon completion of the investigation.
This was the first occurrence of this type (335-76-28)-
 
P.O. BOX 013100, MIAMI, FLORIDA 33101 FLORIDA POWER & LIGHT COMPANY June 18, 1976 PRN-LI-76-150 Mr. Norman C. Moseley,,Director, Region    II Office of Inspection and Enforcement U. S. Nuclear Regulatory Commission 230 Peachtree Street, N.W., Suite 818 Atlanta, Georgia 30303
 
==Dear Mr. Moseley:==
 
REPORTABLE OCCURRENCE 335-76-28 ST. LUCIE UNIT 1 DATE OF OCCURRENCE:  JUNE 4, 1976 HYDROGEN SAMPLING SYSTEM ISOLATION VALVES The  attached Licensee Event Report is being submitted in accordance with Technical Specificaiton 6.9 to provide prompt notification of the subject occurrence.
Very  truly yours, D. Schmidt Vice President Power Resources
,MAS/ao Attachment CC    Jack R. Newman, Esquire Director, Office of Inspection and Enforcement        (40)
Director, Office of Management Information and Program Control (3)
HELPING BUILD FLORIDA
 
~ ~
LICENSEE EVENT REPORT 4
    ~ 'I                      CONTROL BLOCK:                                                                    RASE PRINT ALL REQUIRED INFDRMATIDN) 6 UCENSEE                                                                                  UCENSE              EVENT NAME                                    UCENSE NUMBER                                TYPE                TYPE
[oaf                        S      L  S      1        0      O      OOO          O 0      0        4    111          1    ~01 89
                        ~
7                                            14    15                                            25    26                30    31    32 060476061876 REPORT. AEPOAT CATEGORY          TYPE    SOURCE              OOCKET NUMBEA                      ~ EVENT OATE                  REPORT OATE
[001IcoN          T                    E          L        0    5 0    0          3 3    5 7      8            '57  . 58        .59        60      61                                    69                      74    75                        80 I
EVENT OESCRIPTION QOg. R          .      w      of the testin ro osed for. Unit 2 h drogen sampling system isola-7      8 9                                                                                                                                                  80
            . tion valVhs led to an examination of the purchase:order for the identical 7 89                                                                                                                                                        80 1 valves                  Unit 1 FSAR Section 3.11 classifies these'alves as 7 8 9 7
Qg 8.9
                        'ronmental'ate or lA. 'owever,                                      it  has been determined that the 60 80 IH 7 89
                      '
h FAME                                                                        80 SYSTEM        CAUSE                                          COMPONENT            COMPONENT COOE          COO E                COMPONENT COOE            SUPPLER
                                                                              '3 MANUFACTURER        VQEATCIN 7    8 9 10
              ~SE              ~A              V      A L V      E X            A              X  999                  N 11        12                        17                    44                47 CAUSE OESCRIPTION gg8 9 Unit                1 h        dro en sam lin s stem isolation valves were not tested for 7                                                                                                                                                          80 Qg              ate or 1A environmental conditions in accordance with IEEE-323(1971) 7 8 9                                                                                                                                                  ~
80
,Q~O            because the re uirement to do so was not specified in the purchase order.
7      89        FACILIIY 80 METHOO OF STATUS                '%OWER                  OTHER STATUS          OISCOVEAY                    DISCOVERY OESCAIPTION
                    ~E                ~OZ        O                    N/A                ~d          Purchase      order review 7      8          9                  10              12 13                        44      45      46                                                      80 FORM OF ACTIVITY          COATENT RELEASEO          OF RELEASE            AMOUNT OF ACTNITY                                          LOCATION OF RELEASE Q1g              ~Z            . Z
* N/A                                                    N/A 7      8          9                    10      11                                  44        45                                                              80 PERSONNEL EXPOSURES NUMBER              TYPE      OESCRIPTION Qg ~oo                    0        ~z                                                  N/A 7 89                          11      12      13                                                                                                          80 PERSONNEL INJURIES OESCRIPTION
  ~4                  0      0                                                              N/A 7    8 9                    11    12                                                                                                                    80 PROBABLE CONSEQUENCES Qg                                                                                        N/A 7    89                                                                                                                                                    80 LOSS OR OAMAGE TO FACILITY TYPE        OESCAIPTION
            ~Z-                                                                            N/A 7    89-              10                                                                                                                                  80 PU8UCITY
[iirJ                                                                                      N/A 7    8 9                                                                                                                                                ~ 80 AOOITIONAL FACTORS
~18              See page two (2)                        for continuation of Event Description.
7      89 Component Manufacturer  Circle Seal Corporation 80'0 7      89 NAME'MAN                                                                          PHONE.305/552-3779 dFO ddt 4 ddT
 
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                              'I REPORTABLE OCCURANCE 335-76-28 LXCENSEE EVENT REPORT PAGE TWO Event Descri  tion (Continued) accordance with 'XEEE-323(1971) because. the requirement to do so was not'pecified in the purchase order.    =
As an interim corrective action, administrative guidelines have been written to inform appropriate personnel of the action to be taken    if the valves will not operate under post-accident conditions. Operations personnel have been informed that they'hould actuate the hydrogen recombiners if a containment hydrogen sample cannot be taken. Based on PSAR hydrogen generation analysis for the existing plant design, the operator has 45 days to actuate either hydiogen recombiner before the hydrogen concentration reaches 4%. An investigation of possible long-term corrective action is being conducted and a follow-up report will be submitted upon completion of the investigation.
~
This was the first occurrence of this type (335-76-28)-
This was the first occurrence of this type (335-76-28)-
P.O.BOX 013100, MIAMI, FLORIDA 33101 FLORIDA POWER&LIGHT COMPANY June 18, 1976 PRN-LI-76-150 Mr.Norman C.Moseley,,Director, Region II Office of Inspection and Enforcement U.S.Nuclear Regulatory Commission 230 Peachtree Street, N.W., Suite 818 Atlanta, Georgia 30303


==Dear Mr.Moseley:==
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REPORTABLE OCCURRENCE 335-76-28 ST.LUCIE UNIT 1 DATE OF OCCURRENCE:
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JUNE 4, 1976 HYDROGEN SAMPLING SYSTEM ISOLATION VALVES The attached Licensee Event Report is being submitted in accordance with Technical Specificaiton 6.9 to provide prompt notification of the subject occurrence.
              ~ ~ ~
Very truly yours, D.Schmidt Vice President Power Resources ,MAS/ao Attachment CC Jack R.Newman, Esquire Director, Office of Inspection and Enforcement (40)Director, Office of Management Information and Program Control (3)HELPING BUILD FLORIDA
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4~'I[oaf 7 89 CONTROL BLOCK: UCENSEE NAMES L S 1 0 14 15 UCENSE NUMBER-O OOO O-0 LICENSEE EVENT REPORT RASE PRINT ALL REQUIRED INFDRMATIDN) 6 UCENSE EVENT TYPE TYPE 0 4 111 1~01 25 26 30 31 32 REPORT.AEPOAT CATEGORY TYPE SOURCE[001IcoN T~E L 0 7 8'57.58.59 60 61 OOCKET NUMBEA 5 0-0 3 3 5~EVENT OATE REPORT OATE 060476061876 69 74 75 80 EVENT OESCRIPTION QOg.R.w of the testin ro osed for.Unit 2 h drogen sampling system isola-7 8 9 80 I.tion valVhs led to an examination of the purchase:order for the identical 7 89 1 valves Unit 1 FSAR Section 3.11 classifies these'alves as 80 7 8 9 60 Qg'ronmental'ate or lA.'owever, it has been determined that the 7 8.9 80 IH'h 7 89 SYSTEM CAUSE COOE COO E COMPONENT COOE~SE~A V A L V E 7 8 9 10 11 12 CAUSE OESCRIPTION gg Unit 1 h dro en sam lin FAME COMPONENT SUPPLER X A 17'3 COMPONENT MANUFACTURER X 999 44 47 VQEATCIN N s stem isolation valves were not tested for 80 7 8 9 Qg ate or 1A environmental conditions in accordance with IEEE-323(1971) 80 7 8 9~80 ,Q~O because the re uirement to do so was not specified in the purchase order.OTHER STATUS N/A 7 89 LOSS OR OAMAGE TO FACILITY TYPE OESCAIPTION
~Z-7 89-10 PU8UCITY[iirJ 7 8 9 7 89 FACILIIY STATUS'%OWER~E~OZ O 7 8 9 10 12 13 FORM OF ACTIVITY COATENT RELEASEO OF RELEASE AMOUNT OF ACTNITY Q1g~Z.Z*N/A 7 8 9 10 11 PERSONNEL EXPOSURES NUMBER TYPE OESCRIPTION Qg~oo 0~z 7 89 11 12 13 PERSONNEL INJURIES OESCRIPTION
~4 0 0 7 8 9 11 12 PROBABLE CONSEQUENCES Qg METHOO OF OISCOVEAY DISCOVERY OESCAIPTION
~d Purchase order review 44 45 46 LOCATION OF RELEASE N/A 44 45 N/A N/A N/A N/A N/A 80 80 80 80 80 80 80~80 AOOITIONAL FACTORS~18 See page two (2)for continuation of Event Description.
7 89 Component Manufacturer
-Circle Seal Corporation 7 89 80'0 NAME'MAN PHONE.305/552-3779 dFO ddt 4 ddT
~~s e-
'I REPORTABLE OCCURANCE 335-76-28 LXCENSEE EVENT REPORT PAGE TWO Event Descri tion (Continued) accordance with'XEEE-323(1971) because.the requirement to do so was not'pecified in the purchase order.=As an interim corrective action, administrative guidelines have been written to inform appropriate personnel of the action to be taken if the valves will not operate under post-accident conditions.
Operations personnel have been informed that they'hould actuate the hydrogen recombiners if a containment hydrogen sample cannot be taken.Based on PSAR hydrogen generation analysis for the existing plant design, the operator has 45 days to actuate either hydiogen recombiner before the hydrogen concentration reaches 4%.An investigation of possible long-term corrective action is being conducted and a follow-up report will be submitted upon completion of the investigation.
~This was the first occurrence of this type (335-76-28)-
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Revision as of 08:14, 21 October 2019

LER 1976-028-00 for St. Lucie Unit 1, Review of the Testing Proposed for Unit 2 Hydrogen Sampling System Isolation Valves Led to Examination of Purchase Order for the Identical Unit 1 Valves
ML18113A434
Person / Time
Site: Saint Lucie  NextEra Energy icon.png
Issue date: 06/18/1976
From: Schmidt A
Florida Power & Light Co
To: Moseley N
NRC/IE, NRC/RGN-II
References
PRN-LI-76-150 LER 1976-028-00
Download: ML18113A434 (12)


Text

r NRC FORM 195 I2.1E) S -3 U.S. NUCLEAR REGULATORV COMMISSION DOCKET NUMBER FILE NUMBER NRC DISTRIBUTION FoR PART 50 DOCKET'MATERIAL INCIDENT REPORT Florida~Pwr 6 Light DATE OF DOCUMENT Mr Moseley Co giami, Fla 6-18-76 A D Scfimidt . DATE RECEIVED 7 6 76

@LETTER QNOTOR IZED PROP INPUT FORM NUMSER OF COPIES RECEIVED 0 ORIGINAL IIUN CpLASS F I E D I

no originals rec'd

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NA/8QN8/

DESCRIPTION ENCLOSURE S.i J

1 I

Ltr trans the, following: Licensee Event Report (R08'76-28) on 6-4-76 concerning failure of hydrogen sampling sampling system isolat on valves.........

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1It ~'~IIi Kt Lucie 81 NOTE: IF PERSONNEL EXPOSURE IS INVOLVED SEND DIRECTLY TO KREGER/J, COLLINS FOR ACTION/INFORMATION 7 NCH CH EF' CYS FOR AC ON I LIC ~ ASST ~ '.

H/ CYS ACRS I CYS HQbBKR&fSE T TO LA INTERNAL D IST RI BUTION NRC PDR IGE 2 SCHROEDER/IPPOLITO HOUSTON NOVAK CHECK GRIhIES CASE LE HANAUER TEDESCO hIACCARY EISENHUT BAER

'HA'0 VOLLhIER/HUNCH EGER J COLLINS EXTEIINALDISTRIBUTION CONTROL NUMBER PDR ~

IC:

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NIIC FOIIM IQS f2 161

r)h-- -c> .".ii (8S-i)Vi;05<) aXOqO>. SII.~VS 99afIOOiZ gfl~lqfidl8 fI9'iqOl4gff >0 9 XIII';61 QIIlflI93IIOO

~ ~ ~ ~ . ~ ~ . ~ BOV I I'V LIOS:f GEO '.5 M33 elec.'fI ~S QUG<.'

P.O, IIOX 013100, NIIAMI, Ft.ORIDA 33101 r E ~

. ~

FLORIOA FOVJFR & LIGHT COMPANY June 18, 1976 PRN-LI-7 6-15 0 Mr. Norman C. Moseley, Director, Region II Office of Inspection and, Enforcement U. S. Nuclear Regulatory Commission 230 Peachtree Street, N.N., Suite 818 Atlanta, Georgia 30303

Dear Mr. Moseley:

REPORTABLE OCCURRENCE 335-76-28 ST. LUCIE UNIT 1 DATE OP OCCURRENCE: JUNE 4, 1976 C'YDROGEN SAMPLING SYSTEM ISOLATION VALVES The attached Licensee Event Report is being submitted in accordance with Technical Specificaiton 6.9 to provide prompt notification of the subject occurrence.

Very truly yours,

>sr .

D. Schmidt Vice President Power Resources

.MAS/ao Attachment cc: Jack R. Newman, Esquire Director, Office of Inspection and Enforcement (40)

'irector, Of fice of Management Information and Program Control (3) iQg/~(~

HELPING BUILD FLORIDA

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LICENSEE EVENT REPORT r

CONTROL SLOCK:~ (~BE PRINT ALL REQUIRED INFORMATION) 1 UCENSEE UCENSE EVENT NAME, UCENSE NUMBER TYPE TYPE

[oa~] S L S 1 0 0 0 0 0 0 0 0 4 l.'1 1 1 ~01 89

~

14 15 25 26 30 31 32 REPORT. REPORT

'f CATEGORY TYPE SOURCE 'OCKET NUMBER EVENT GATE REPORT OATE "rQO71 CON'T T L. 0 5 0 0 3 3 5 0 6 0 4 7 6 G 6 1 8 7 6 7 8 '57 . 58 .59 60 61 68 69 74 75 . 80 EVENT OESCRIPTION'g R the tes'tin ro osed for Unit 2 h drogen sampling system*isola-7 8'9 80 t00$ tion valVOs led to an examination of the, purchase .order for the identical

~

7 8 9 80

~04 1 valves Unit 1 FSAR Section 3.11 classifies these valves as 7 8 9 Qg 7 8.9

'ronmental'ate or lA. 'owever, it has been determined that the 80 7

Q~ g Unit 1 valves have not been 8 9 t *e tested for the proposed environment in 80 80 SYSTEM CAUSE COMPONENT COBE COOE COMPONENT COOE MANUFACIUPER VQULTQN

[OOTI ~BE ~A' A L V E X A X 9 9 9 N 7 8 910 11 12 17 43 47 CAUSE OESCRIPTION 7

Qg8 9 Unit 1 h dio en sam lin s stem isolation valves were not tested -for 80 (oa>] ate or 1A environmental conditions in accordance with IEEE-323 {1971) 7 8 9 because the re uirement to do so was not specified in the purchase order. 80'Qg 7 89 80 FACIUTY METHOO OF STATUS  % POWER OTHER STATUS OISCOVERY OISCOVERY OESCRIPTION

[111'B .10

~05 0 N/A ~d Purchase order review 7 8 9 12 13 44 45 46 80 FORM OF ACTIVITY C0ATENT RELEASEO OF RELEASE AMOUNT OF ACTIVITY LOCATION OF RELEASE

[rig ~z ~z N/A N/A 7 'S .S 10 11 44 45 80 .

PERSONNEL EXPOSURES NUMBER TYPE OESCR{PTION

~s ~oo o ~z N/A 7 8 9, 11 12 13 80 PERSONNEL INJURIES OESCR{PTION N/A 7 8 9 11 12 80

  • PROBABLE CONSEQUENCES t11g N/A 7 8 9 80 LOSS OR OAMAGE TO FACILITY TYPE OESCR{PTION uz. N/A 7>> 8 9 ~ 10 80 PUBLICITY N/A 7 89 '0 AOOITIONAL FACTORS

~18 See page two (2) for continuation of Event Description.,

7 8 9 80 Component Manufacturer Circle Seal Corporation 7 89 NAME'AN'HONE. 305/552-3779 CPO 80 ddI r dd7

REPORTABLE OCCURANCE 335-76-28 LICENSEE EVENT REPORT PAGE'TWO Event Descri tion (Continued) accordance with 'IEEE-323(1971) because the requirement to do so was not specified in the purchase order. As an interim corrective action, administrative guidelines have been written to inform appropriate personnel of the action to be taken if the valves wild not operate under post-accident conditions. Operations personnel have been informed that they'hould actuate the hydrogen recombiners if a containment hydrogen sample cannot be taken. Based on FSAR hydrogen generation analysis for the existing pl'ant design, the operator has 45 days to actuate either hydrogen recombiner before the hydrogen concentration reaches 4%. An investigation of possible long-term corrective action is being conducted and a follow-up report will be submitted upon completion of the investigation.

This was the first occurrence of this type (335-76-28)-

P.O. BOX 013100, MIAMI, FLORIDA 33101 FLORIDA POWER & LIGHT COMPANY June 18, 1976 PRN-LI-76-150 Mr. Norman C. Moseley,,Director, Region II Office of Inspection and Enforcement U. S. Nuclear Regulatory Commission 230 Peachtree Street, N.W., Suite 818 Atlanta, Georgia 30303

Dear Mr. Moseley:

REPORTABLE OCCURRENCE 335-76-28 ST. LUCIE UNIT 1 DATE OF OCCURRENCE: JUNE 4, 1976 HYDROGEN SAMPLING SYSTEM ISOLATION VALVES The attached Licensee Event Report is being submitted in accordance with Technical Specificaiton 6.9 to provide prompt notification of the subject occurrence.

Very truly yours, D. Schmidt Vice President Power Resources

,MAS/ao Attachment CC Jack R. Newman, Esquire Director, Office of Inspection and Enforcement (40)

Director, Office of Management Information and Program Control (3)

HELPING BUILD FLORIDA

~ ~

LICENSEE EVENT REPORT 4

~ 'I CONTROL BLOCK: RASE PRINT ALL REQUIRED INFDRMATIDN) 6 UCENSEE UCENSE EVENT NAME UCENSE NUMBER TYPE TYPE

[oaf S L S 1 0 O OOO O 0 0 4 111 1 ~01 89

~

7 14 15 25 26 30 31 32 060476061876 REPORT. AEPOAT CATEGORY TYPE SOURCE OOCKET NUMBEA ~ EVENT OATE REPORT OATE

[001IcoN T E L 0 5 0 0 3 3 5 7 8 '57 . 58 .59 60 61 69 74 75 80 I

EVENT OESCRIPTION QOg. R . w of the testin ro osed for. Unit 2 h drogen sampling system isola-7 8 9 80

. tion valVhs led to an examination of the purchase:order for the identical 7 89 80 1 valves Unit 1 FSAR Section 3.11 classifies these'alves as 7 8 9 7

Qg 8.9

'ronmental'ate or lA. 'owever, it has been determined that the 60 80 IH 7 89

'

h FAME 80 SYSTEM CAUSE COMPONENT COMPONENT COOE COO E COMPONENT COOE SUPPLER

'3 MANUFACTURER VQEATCIN 7 8 9 10

~SE ~A V A L V E X A X 999 N 11 12 17 44 47 CAUSE OESCRIPTION gg8 9 Unit 1 h dro en sam lin s stem isolation valves were not tested for 7 80 Qg ate or 1A environmental conditions in accordance with IEEE-323(1971) 7 8 9 ~

80

,Q~O because the re uirement to do so was not specified in the purchase order.

7 89 FACILIIY 80 METHOO OF STATUS '%OWER OTHER STATUS OISCOVEAY DISCOVERY OESCAIPTION

~E ~OZ O N/A ~d Purchase order review 7 8 9 10 12 13 44 45 46 80 FORM OF ACTIVITY COATENT RELEASEO OF RELEASE AMOUNT OF ACTNITY LOCATION OF RELEASE Q1g ~Z . Z

  • N/A N/A 7 8 9 10 11 44 45 80 PERSONNEL EXPOSURES NUMBER TYPE OESCRIPTION Qg ~oo 0 ~z N/A 7 89 11 12 13 80 PERSONNEL INJURIES OESCRIPTION

~4 0 0 N/A 7 8 9 11 12 80 PROBABLE CONSEQUENCES Qg N/A 7 89 80 LOSS OR OAMAGE TO FACILITY TYPE OESCAIPTION

~Z- N/A 7 89- 10 80 PU8UCITY

[iirJ N/A 7 8 9 ~ 80 AOOITIONAL FACTORS

~18 See page two (2) for continuation of Event Description.

7 89 Component Manufacturer Circle Seal Corporation 80'0 7 89 NAME'MAN PHONE.305/552-3779 dFO ddt 4 ddT

s e-

~ ~

'I REPORTABLE OCCURANCE 335-76-28 LXCENSEE EVENT REPORT PAGE TWO Event Descri tion (Continued) accordance with 'XEEE-323(1971) because. the requirement to do so was not'pecified in the purchase order. =

As an interim corrective action, administrative guidelines have been written to inform appropriate personnel of the action to be taken if the valves will not operate under post-accident conditions. Operations personnel have been informed that they'hould actuate the hydrogen recombiners if a containment hydrogen sample cannot be taken. Based on PSAR hydrogen generation analysis for the existing plant design, the operator has 45 days to actuate either hydiogen recombiner before the hydrogen concentration reaches 4%. An investigation of possible long-term corrective action is being conducted and a follow-up report will be submitted upon completion of the investigation.

~

This was the first occurrence of this type (335-76-28)-

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