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{{#Wiki_filter:<<V 70).NDC DISTI'IIOUTION FoII P" T 50 DOCKET MATEnlAL FILC NVMIIE.A INCIDI'.WT REPOIIT: ro: I M.C.Moeeley FRolvl: Fl ord i a Power:8i Light Co..Miami , Fl ord1 a A.D.Schmidt OATC OF OOCVMCNT 6-14-76 DATE RECEIVED 7-8-76 IQLRTTEA I OOAIGINAI CFCOPV QNOTORIZEO g VNCLASSIFIEO PROP INPUT FOAM NVMOEA OF COPIES ACCEIVEO I DESCRIPTION Ltr.'rans the following.......'.
{{#Wiki_filter:<<V 70)
ENCLOSVAE icensee Event Report (R.O.k'6-23)on 5-24-76 oncerning Temperature Indication Hot ShutDown ohtrol Panel.......
FILC NVMIIE.A
(1 Carbon Signed Cy.Received)(.'3.Pages')
                      .NDC DISTI'IIOUTION FoII P"     T 50 DOCKET MATEnlAL                               INCIDI'.WT REPOIIT
'.'ACKNOWLEDG DQ NOT pZMO 9 g St.Luci e'0 1 j NOTE e IP PERSONNEL EXPOSURE IS INVOLVEDSEND DIRECTLY TO KREGER/J COLLINS SAPETY BRANCH, CHIEF: M 3 CYS POR ACTION LIC ASST: M/=--4'YS I ACRS 16 CYS XXSKNXXE/ENT TO LA FOR ACTION/INFORMATION ENVIRO E F L NRG=-PDR,.
: ro:             M.C. Moeeley                         FRolvl: Fl ord i a Power :8i   Light Co .. OATC OF OOCVMCNT I
IGE 2 INTERNAL D IST Rl BUTION=SCHROFAER/IPPOLITO NOVAKQCIIF CK IE~S tl ee GEE.Ul'EDF 8('Ogl IACCA F S~N'I BAF.R SIIAO'OLLI II'.R/1>Uti(',Il RLgl'.IQJ~OLQ IIS LPOt(:.merce, a TZC NSIC ExTEIINAL DlsTIIIHUTloN CONTrIOI.Nlli%1IIL'n 6837 I~I$~~~~"l f"~5>>i~s~~~~o~~a~I~5 I BgUII rp O.BOX 013100, MIAMI, FLORIDA 33101 FLORIDA POWER 5 LIGHT COMPANY June 24, 1976 IO PRN-LI-76-159 Mr.Norman C.Moseley, Director, Region II Office of Inspection and Enforcement U.S.Nuclear Regulatory Commission 230 Peachtree Street, N.W., Suite 818 Atlanta, Georgia 30303
Miami , Fl ord1 a                           6-14-76 A. D . Schmidt                         DATE RECEIVED 7-8-76 IQLRTTEA                           QNOTORIZEO         PROP                       INPUT FOAM         NVMOEA OF COPIES ACCEIVEO I    OOAIGINAI                    g VNCLASSIFIEO CFCOPV I DESCRIPTION                                                             ENCLOSVAE Ltr.'rans             the following.......'.                       icensee Event Report (R.O. k'6-23) on 5-24-76 oncerning Temperature Indication Hot ShutDown ohtrol Panel.......
(   1 Carbon Signed Cy. Received)
(.'3.Pages')   '.
                                                                            'ACKNOWLEDG               9 DQ NOT pZMO             g                         j St. Luci e '0 1 NOTE e IP PERSONNEL EXPOSURE IS INVOLVED SEND DIRECTLY TO KREGER/J     COLLINS SAPETY                                 FOR ACTION/INFORMATION                    ENVIRO BRANCH, CHIEF:
M 3 CYS POR ACTION LIC ASST:
M/=--4'YS I     ACRS 16 CYS               XXSKNXXE/ ENT TO LA INTERNAL D IST Rl BUTION E         F L NRG=-PDR,.
IGE             2
      =SCHROFAER/IPPOLITO NOVAKQCIIFCK IE~S tl ee GEE.Ul'EDF 8('Ogl IACCA F S~N 'I BAF.R SIIAO
    'OLLIII'.R/1>Uti(',Il RLgl'.IQJ~OLQ             IIS ExTEIINAL DlsTIIIHUTloN                                         CONTrIOI. Nlli%1IIL'n LPOt(:            . merce,     a TZC NSIC                                                                                                    6837


==Dear Mr.Moseley:==
I ~
REPORTABLE OCCURRENCE 335-76-23 ST.LUCIE UNIT 1 DATE OF OCCURRENCE:
I$
MAY 24, 1976 HOT SHUTDOWN CONTROL PANEL TEMPERATURE INDICATION The attached Licensee Event Repoit is being submitted in accordance with Technical Specification 6.9 to provide 30-day notification of the subject occurrence.
                        ~ ~
Very truly yours, D.Schmidt Vice President Power Resources MAS/cpc Attachment cc: Jack R.Newman, Esquire Director, Office of Inspection and Enforcement (30)Director, Office of Management Information and Program Control (3)
~ ~
CENBEE EVENT REPORT~O'l F.7 89 CONTROL BLOCK: UCEN SEE NAME LSLS l 14 15 UCENSE NUMBEA 0-0000[PLEASE PRINT ALL REQUIRED INFORMATION3 UCENSE EVENT TYPE TYPE-0 0 4 1 1 1~03 25 26 30 31 32 REPORT REPORT.CATEGORY TYPE SOURCE[OD1]CONT~~L~L 7 8 57 58 59 60 EVENT OESCRIPTION OOCKET NUMBER 050-033 61 EVENT OATE REPORT OATE 50524766246 68 69 74 75 80 surveillance test.on the hot shutdown control 7 8 9 80[ODg anel HSCP it was found that the cold le tern erature indication for 7 8 9 80~o4 reactor coolant loo lAl was not correct.Indicated tern erature at the 7 8 9 foal)s The tern erature instrumentation 7 8 9 SYSTEM CAUSE CDOE COBE COMPONENT COOE@~77~IF~A I N 5 T R 0 7 8 9 10 11 12 17 CAUSE OESCRIPTION
    "l  f"~5>> i
~08 This occurrence was caused b A S l 8 5 47 N the HSCP reactor coolant tern erature 7 8 9 Q~g HSCP was 555 de rees F while the correct readin as indicated in the 80 80 80 7 8 9 QOg indication bein out of calibration.
                                ~ ~ a ~ I ~
7 8 9~10 80 No defective com onents were found.80 OTHER STATUS N/A AMOUNT OF ACTIVITY N A.7 89 LOSS OR OAMAGE TO FACIUTY TYPE OESCAIPTION
      ~ s ~ ~ ~ ~ o 5 I
~z 7 89 10 PUBLICITY 7 8 9 7 89 FACUTY STATUS%POWER@~g B~05 0 7 8 9 10 12 13 FORM OF ACTIVITY COATENT RELEASEO OF RELEASE~z z 7 8 9 10 11 PERSONNEL EXPOSURES NUMBER TYPE OESCRIPTION Q~~7~00 o~z 7 8 9 11 12 13 PERSONNEL INJURIES NUMBER OESCAIPTION
 
@~47~o.o o 7 8 9 11 12 PROBABLE CONSEQUENCES Q~g METHOO OF OISCOVERY 44 45 44 45 N/A N A N A N/A 46 OISCOVERY OESCAIPTION N/A LOCATION OF RELEASE N/A 80 80 80 80 80~80 AOOITIONAL FACTORS'ee Pa e Two for continuation of Event Descri tion.7 8 9 80 7 89 NAMEI M.A.Scho man PHONE 305 552-3779 80 REPORTABLE OCCURRENCE 33 5-7 6'-23 LXCENSEE EVENT REPORT PAGE TWO Event Description (continued) associated with the HSCP was calibrated and the surveillance test was completed satisfactorily.
O. BOX 013100, MIAMI, FLORIDA 33101 BgUIIrp FLORIDA POWER 5 LIGHT COMPANY June 24, 1976 PRN-LI-76-159 IO Mr. Norman C. Moseley,    Director, Region  II Office of Inspection and Enforcement U. S. Nuclear Regulatory Commission 230 Peachtree Street, N. W., Suite 818 Atlanta, Georgia 30303
This was the first occurrence of this type.(335-76-23).}}
 
==Dear Mr. Moseley:==
 
REPORTABLE OCCURRENCE   335-76-23 ST. LUCIE UNIT 1 DATE OF OCCURRENCE:   MAY 24, 1976 HOT SHUTDOWN CONTROL PANEL TEMPERATURE INDICATION The attached   Licensee Event Repoit is being submitted in accordance with Technical Specification 6.9 to provide 30-day notification of the subject occurrence.
Very truly yours, D. Schmidt Vice President Power Resources MAS/cpc Attachment cc:   Jack R. Newman, Esquire Director, Office of Inspection and Enforcement         (30)
Director, Office of Management Information and Program Control (3)
 
CENBEE EVENT REPORT CONTROL BLOCK:                                                                  [PLEASE PRINT ALL REQUIRED INFORMATION3 UCEN SEE                                                                                  UCENSE              EVENT NAME
    ~O'l
  .7 89 F      LSLS l                                     0           0000 UCENSE NUMBEA 0       0     4   1 TYPE 1 1           ~03 TYPE
                    ~
14    15                                          25   26                 30     31     32
[OD1]CONT 7 8
                  . CATEGORY 57         58 REPORT TYPE
                                            ~L 59 REPORT SOURCE
                                                      ~L 60     61 050    OOCKET NUMBER 033           50524766246 68   69 EVENT OATE 74     75 REPORT OATE 80 EVENT OESCRIPTION surveillance test. on the hot shutdown control 7     8 9
[ODg 7 8 9 anel HSCP                           it   was found that the cold le tern erature indication for 80 80
  ~o4       reactor coolant loo lAl was not correct. Indicated tern erature at the 7 8 9                                                                                                                                               80 Q~g HSCP was 555 de rees F while the correct readin                                                          as indicated in the 7 8 9                                                                                                                                                80 foal)                                               s                           The tern erature instrumentation 7   8 9                                                                                                                                             80 SYSTEM       CAUSE 7
  @~77 8 9 CDOE
            ~IF 10 COBE
                          ~A 11          12 I
COMPONENT COOE N 5     T R     0 17 A              S  l    8 5 47 N
CAUSE OESCRIPTION
  ~08       This occurrence was caused b the HSCP reactor coolant tern erature 7 8 9                                                                                                                                               80 QOg       indication bein out of calibration. No defective com onents were found.
7 8 9                                                                                                                                                80
  ~10 7 89 FACUTY                                                                 METHOO OF STATUS                     % POWER               OTHER STATUS        OISCOVERY                    OISCOVERY OESCAIPTION
  @~g 7 8          9 B                     ~05         0                 N/A                                                N/A 10             12 13                       44    45      46 FORM OF ACTIVITY               COATENT RELEASEO         OF RELEASE                 AMOUNT OF ACTIVITY                                      LOCATION OF RELEASE
                ~z                       z                   N A                                                      N/A 7     8     9                         10     11                               44      45                                                          80 PERSONNEL EXPOSURES NUMBER                   TYPE       OESCRIPTION Q~~7     ~00         o               ~z 7     8 9             11             12     13                                                                                                   80 PERSONNEL INJURIES NUMBER                   OESCAIPTION
  @~47     ~o.o         o                                                         N/A 7     8 9             11           12                                                                                                             80 PROBABLE CONSEQUENCES Q~g                                                                             N A
.7    89                                                                                                                                            80 LOSS OR OAMAGE TO FACIUTY TYPE      OESCAIPTION
          ~z                                                                      N A 7    89          10                                                                                                                                80 PUBLICITY N/A 7    8 9                                                                                                                                          ~ 80 AOOITIONAL       FACTORS'ee Pa e Two                     for continuation of               Event Descri         tion.
7     8 9                                                                                                                                             80 7     89                                                                                                                                           80 NAMEI               M. A. Scho           man                                     PHONE   305 552-3779
 
REPORTABLE OCCURRENCE 33 5-7 6'-23 LXCENSEE EVENT REPORT PAGE TWO Event Description (continued) associated with the HSCP was   calibrated and the surveillance test was completed satisfactorily. This was the first occurrence of this type.   (335-76-23).}}

Latest revision as of 08:14, 21 October 2019

LER 1976-023-00 for St. Lucie Unit 1, During Surveillance Test on Hot Shutdown Control Panel, Cold Leg Temperature Indication for Reactor Coolant Loop 1A1 Was Not Correct
ML18113A437
Person / Time
Site: Saint Lucie  NextEra Energy icon.png
Issue date: 06/24/1976
From: Schmidt A
Florida Power & Light Co
To: Moseley N
NRC/IE, NRC/RGN-II
References
PRN-LI-76-159 LER 1976-023-00
Download: ML18113A437 (5)


Text

<<V 70)

FILC NVMIIE.A

.NDC DISTI'IIOUTION FoII P" T 50 DOCKET MATEnlAL INCIDI'.WT REPOIIT

ro: M.C. Moeeley FRolvl: Fl ord i a Power :8i Light Co .. OATC OF OOCVMCNT I

Miami , Fl ord1 a 6-14-76 A. D . Schmidt DATE RECEIVED 7-8-76 IQLRTTEA QNOTORIZEO PROP INPUT FOAM NVMOEA OF COPIES ACCEIVEO I OOAIGINAI g VNCLASSIFIEO CFCOPV I DESCRIPTION ENCLOSVAE Ltr.'rans the following.......'. icensee Event Report (R.O. k'6-23) on 5-24-76 oncerning Temperature Indication Hot ShutDown ohtrol Panel.......

( 1 Carbon Signed Cy. Received)

(.'3.Pages') '.

'ACKNOWLEDG 9 DQ NOT pZMO g j St. Luci e '0 1 NOTE e IP PERSONNEL EXPOSURE IS INVOLVED SEND DIRECTLY TO KREGER/J COLLINS SAPETY FOR ACTION/INFORMATION ENVIRO BRANCH, CHIEF:

M 3 CYS POR ACTION LIC ASST:

M/=--4'YS I ACRS 16 CYS XXSKNXXE/ ENT TO LA INTERNAL D IST Rl BUTION E F L NRG=-PDR,.

IGE 2

=SCHROFAER/IPPOLITO NOVAKQCIIFCK IE~S tl ee GEE.Ul'EDF 8('Ogl IACCA F S~N 'I BAF.R SIIAO

'OLLIII'.R/1>Uti(',Il RLgl'.IQJ~OLQ IIS ExTEIINAL DlsTIIIHUTloN CONTrIOI. Nlli%1IIL'n LPOt(: . merce, a TZC NSIC 6837

I ~

I$

~ ~

~ ~

"l f"~5>> i

~ ~ a ~ I ~

~ s ~ ~ ~ ~ o 5 I

O. BOX 013100, MIAMI, FLORIDA 33101 BgUIIrp FLORIDA POWER 5 LIGHT COMPANY June 24, 1976 PRN-LI-76-159 IO Mr. Norman C. Moseley, Director, Region II Office of Inspection and Enforcement U. S. Nuclear Regulatory Commission 230 Peachtree Street, N. W., Suite 818 Atlanta, Georgia 30303

Dear Mr. Moseley:

REPORTABLE OCCURRENCE 335-76-23 ST. LUCIE UNIT 1 DATE OF OCCURRENCE: MAY 24, 1976 HOT SHUTDOWN CONTROL PANEL TEMPERATURE INDICATION The attached Licensee Event Repoit is being submitted in accordance with Technical Specification 6.9 to provide 30-day notification of the subject occurrence.

Very truly yours, D. Schmidt Vice President Power Resources MAS/cpc Attachment cc: Jack R. Newman, Esquire Director, Office of Inspection and Enforcement (30)

Director, Office of Management Information and Program Control (3)

CENBEE EVENT REPORT CONTROL BLOCK: [PLEASE PRINT ALL REQUIRED INFORMATION3 UCEN SEE UCENSE EVENT NAME

~O'l

.7 89 F LSLS l 0 0000 UCENSE NUMBEA 0 0 4 1 TYPE 1 1 ~03 TYPE

~

14 15 25 26 30 31 32

[OD1]CONT 7 8

. CATEGORY 57 58 REPORT TYPE

~L 59 REPORT SOURCE

~L 60 61 050 OOCKET NUMBER 033 50524766246 68 69 EVENT OATE 74 75 REPORT OATE 80 EVENT OESCRIPTION surveillance test. on the hot shutdown control 7 8 9

[ODg 7 8 9 anel HSCP it was found that the cold le tern erature indication for 80 80

~o4 reactor coolant loo lAl was not correct. Indicated tern erature at the 7 8 9 80 Q~g HSCP was 555 de rees F while the correct readin as indicated in the 7 8 9 80 foal) s The tern erature instrumentation 7 8 9 80 SYSTEM CAUSE 7

@~77 8 9 CDOE

~IF 10 COBE

~A 11 12 I

COMPONENT COOE N 5 T R 0 17 A S l 8 5 47 N

CAUSE OESCRIPTION

~08 This occurrence was caused b the HSCP reactor coolant tern erature 7 8 9 80 QOg indication bein out of calibration. No defective com onents were found.

7 8 9 80

~10 7 89 FACUTY METHOO OF STATUS  % POWER OTHER STATUS OISCOVERY OISCOVERY OESCAIPTION

@~g 7 8 9 B ~05 0 N/A N/A 10 12 13 44 45 46 FORM OF ACTIVITY COATENT RELEASEO OF RELEASE AMOUNT OF ACTIVITY LOCATION OF RELEASE

~z z N A N/A 7 8 9 10 11 44 45 80 PERSONNEL EXPOSURES NUMBER TYPE OESCRIPTION Q~~7 ~00 o ~z 7 8 9 11 12 13 80 PERSONNEL INJURIES NUMBER OESCAIPTION

@~47 ~o.o o N/A 7 8 9 11 12 80 PROBABLE CONSEQUENCES Q~g N A

.7 89 80 LOSS OR OAMAGE TO FACIUTY TYPE OESCAIPTION

~z N A 7 89 10 80 PUBLICITY N/A 7 8 9 ~ 80 AOOITIONAL FACTORS'ee Pa e Two for continuation of Event Descri tion.

7 8 9 80 7 89 80 NAMEI M. A. Scho man PHONE 305 552-3779

REPORTABLE OCCURRENCE 33 5-7 6'-23 LXCENSEE EVENT REPORT PAGE TWO Event Description (continued) associated with the HSCP was calibrated and the surveillance test was completed satisfactorily. This was the first occurrence of this type. (335-76-23).