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Category:Letter type:ULNRC
MONTHYEARULNRC-06901, Concurrent Inoperability of Control Room Air Conditioning System Train and Opposite Train Emergency Diesel Generator Results in Condition Prohibited by Technical Specifications Limiting (Letter)2024-10-0101 October 2024 Concurrent Inoperability of Control Room Air Conditioning System Train and Opposite Train Emergency Diesel Generator Results in Condition Prohibited by Technical Specifications Limiting (Letter) ULNRC-06892, Independent Spent Fuel Storage Installation Registration of Dry Spent Fuel Storage Canister HGMPC00062024-06-26026 June 2024 Independent Spent Fuel Storage Installation Registration of Dry Spent Fuel Storage Canister HGMPC0006 ULNRC-06891, Independent Spent Fuel Storage Installation, Registration of Dry Spent Fuel Storage Canister HGMPC00052024-06-26026 June 2024 Independent Spent Fuel Storage Installation, Registration of Dry Spent Fuel Storage Canister HGMPC0005 ULNRC-06886, Independent Spent Fuel Storage Installation, Registration of Dry Spent Fuel Storage Canister HGMPC00042024-06-12012 June 2024 Independent Spent Fuel Storage Installation, Registration of Dry Spent Fuel Storage Canister HGMPC0004 ULNRC-06885, Independent Spent Fuel Storage Installation, Registration of Dry Spent Fuel Storage Canister HGMPC00032024-06-12012 June 2024 Independent Spent Fuel Storage Installation, Registration of Dry Spent Fuel Storage Canister HGMPC0003 ULNRC-06884, Independent Spent Fuel Storage Installation, Registration of Dry Spent Fuel Storage Canister HGMPC00022024-06-12012 June 2024 Independent Spent Fuel Storage Installation, Registration of Dry Spent Fuel Storage Canister HGMPC0002 ULNRC-06882, Independent Spent Fuel Storage Installation Registration of Dry Spent Fuel Storage Canister HGMPC00122024-05-16016 May 2024 Independent Spent Fuel Storage Installation Registration of Dry Spent Fuel Storage Canister HGMPC0012 ULNRC-06877, Final Safety Analysis Report Revision OL-27 and Technical Specification Bases Revision 252024-05-0606 May 2024 Final Safety Analysis Report Revision OL-27 and Technical Specification Bases Revision 25 ULNRC-06856, CFR 50.59 and 10 CFR 72.48 Summary Report2024-05-0101 May 2024 CFR 50.59 and 10 CFR 72.48 Summary Report ULNRC-06869, Submittal of Callaway, Unit 1, 2023 Annual Radiological Environmental Operating Report2024-04-30030 April 2024 Submittal of Callaway, Unit 1, 2023 Annual Radiological Environmental Operating Report ULNRC-06876, Registration of Dry Spent Fuel Storage Canister HGMPC00102024-04-25025 April 2024 Registration of Dry Spent Fuel Storage Canister HGMPC0010 ULNRC-06866, Submittal of Cycle 26 Commitment Change Summary Report2024-04-17017 April 2024 Submittal of Cycle 26 Commitment Change Summary Report ULNRC-06871, Independent Spent Fuel Storage Installation, Registration of Dry Spent Fuel Storage Canister HGMPC00072024-04-17017 April 2024 Independent Spent Fuel Storage Installation, Registration of Dry Spent Fuel Storage Canister HGMPC0007 ULNRC-06872, Independent Spent Fuel Storage Installation, Registration of Dry Spent Fuel Storage Canister HGMPC00082024-04-17017 April 2024 Independent Spent Fuel Storage Installation, Registration of Dry Spent Fuel Storage Canister HGMPC0008 ULNRC-06863, Submittal of Annual Exposure Report for 20232024-03-20020 March 2024 Submittal of Annual Exposure Report for 2023 ULNRC-06852, Owners Activity Reports (OAR-1 Forms) for Cycle/Refuel 262024-03-0505 March 2024 Owners Activity Reports (OAR-1 Forms) for Cycle/Refuel 26 ULNRC-06858, Completion of License Renewal Activities Prior to Entering the Period of Extended Operation2024-02-21021 February 2024 Completion of License Renewal Activities Prior to Entering the Period of Extended Operation ULNRC-06853, Submittal of 2023 Fitness for Duty Performance Data Per Per 10 CFR 26.7172024-01-29029 January 2024 Submittal of 2023 Fitness for Duty Performance Data Per Per 10 CFR 26.717 ULNRC-06847, Supplement to Relief Request from Requirements of ASME BPV Code, Section XI, Subsection Iwl Regarding Examination and Testing of the Unbonded Post-Tensioning System (Relief Request C3R-01)2023-12-21021 December 2023 Supplement to Relief Request from Requirements of ASME BPV Code, Section XI, Subsection Iwl Regarding Examination and Testing of the Unbonded Post-Tensioning System (Relief Request C3R-01) ULNRC-06844, Request for Exemption from Specific Requirements in 2023 Security Rule, Enhanced Weapons, Firearms Background Checks, and Security Event Notification2023-12-0707 December 2023 Request for Exemption from Specific Requirements in 2023 Security Rule, Enhanced Weapons, Firearms Background Checks, and Security Event Notification ULNRC-06827, Supplement to License Amendment Request Regarding Support System Requirements for Residual Heat Removal and Control Room Air Conditioning Systems Under Technical Specifications 3.4.8, 3.7.11, and 3.9.6 (LDCN 22-0029)2023-11-20020 November 2023 Supplement to License Amendment Request Regarding Support System Requirements for Residual Heat Removal and Control Room Air Conditioning Systems Under Technical Specifications 3.4.8, 3.7.11, and 3.9.6 (LDCN 22-0029) ULNRC-06824, Response to Request for Additional Information Regarding Operating Quality Assurance Manual (Oqam) Revision 36A2023-08-17017 August 2023 Response to Request for Additional Information Regarding Operating Quality Assurance Manual (Oqam) Revision 36A ULNRC-06223, Minor Correction to License Amendment Request to Revise Technical Specification 5.5.16, Containment Leakage Rate Testing Program, for Permanent Extension of Type a and Type C Leak Rate Test Frequencies (LDCN 2020-0004)2023-07-25025 July 2023 Minor Correction to License Amendment Request to Revise Technical Specification 5.5.16, Containment Leakage Rate Testing Program, for Permanent Extension of Type a and Type C Leak Rate Test Frequencies (LDCN 2020-0004) ULNRC-06799, Submittal of Licensee Event Report 2022-003-01, Class 1E Electrical Air Conditioning System Thermal Expansion Valve Failure Resulted in Condition Prohibited by Technical Specifications2023-07-13013 July 2023 Submittal of Licensee Event Report 2022-003-01, Class 1E Electrical Air Conditioning System Thermal Expansion Valve Failure Resulted in Condition Prohibited by Technical Specifications ULNRC-06821, Post-Audit Follow-Up Information in Support of Callaways License Amendment Request and Proposed Exemption to Allow Use of Framatome Gaia Fuel (LDCN 22-0002) (EPID L-2022-LLA-0150 and EPID L-2022-LLE-00301)2023-06-21021 June 2023 Post-Audit Follow-Up Information in Support of Callaways License Amendment Request and Proposed Exemption to Allow Use of Framatome Gaia Fuel (LDCN 22-0002) (EPID L-2022-LLA-0150 and EPID L-2022-LLE-00301) ULNRC-06818, Response to Request for Additional Information Regarding License Amendment Request to Revise Technical Specification 5.5.16, Containment Leakage Rate Testing Program, for Permanent Extension of Type a and Type C Leak Rate .2023-06-0505 June 2023 Response to Request for Additional Information Regarding License Amendment Request to Revise Technical Specification 5.5.16, Containment Leakage Rate Testing Program, for Permanent Extension of Type a and Type C Leak Rate . ULNRC-06815, Request for NRC Approval of Operating Quality Assurance Manual, Revision 36a2023-06-0505 June 2023 Request for NRC Approval of Operating Quality Assurance Manual, Revision 36a ULNRC-06816, Withdrawal of Previously Submitted Enclosures Regarding License Amendment Request for Adoption of Alternative Source Term and Revision of Technical Specifications (LDCN 21-0015)2023-05-0909 May 2023 Withdrawal of Previously Submitted Enclosures Regarding License Amendment Request for Adoption of Alternative Source Term and Revision of Technical Specifications (LDCN 21-0015) ULNRC-06807, Submittal of Single Positive Test Forms2023-04-0303 April 2023 Submittal of Single Positive Test Forms ULNRC-06801, CFR 50.46 Annual Report Regarding ECCS Evaluation Model Revisions2023-03-30030 March 2023 CFR 50.46 Annual Report Regarding ECCS Evaluation Model Revisions ULNRC-06798, Submittal of Status of Plant Decommissioning Funding and ISFSI Decommissioning Funding Plan2023-03-30030 March 2023 Submittal of Status of Plant Decommissioning Funding and ISFSI Decommissioning Funding Plan ULNRC-06803, Submittal of Response to Request for Additional Information Regarding Results of Steam Generator Tube In-Service Inspection2023-03-29029 March 2023 Submittal of Response to Request for Additional Information Regarding Results of Steam Generator Tube In-Service Inspection ULNRC-06751, Application to Revise Technical Specifications to Adopt TSTF-501-A, Rev. 1, Relocate Stored Oil & Lube Oil Volume Values to Licensee Control2023-03-29029 March 2023 Application to Revise Technical Specifications to Adopt TSTF-501-A, Rev. 1, Relocate Stored Oil & Lube Oil Volume Values to Licensee Control ULNRC-06804, Submittal of Nuclear Property Insurance Reporting2023-03-29029 March 2023 Submittal of Nuclear Property Insurance Reporting ULNRC-06805, Transmittal of Special Report 2023-02 Non-Functionality of Containment Hydrogen Analyzer Channel for Greater than 30 Days2023-03-21021 March 2023 Transmittal of Special Report 2023-02 Non-Functionality of Containment Hydrogen Analyzer Channel for Greater than 30 Days ULNRC-06802, Special Report 2023-01 (PAM Report); Non-Functionality of a Post-Accident Monitoring Instrument2023-03-0909 March 2023 Special Report 2023-01 (PAM Report); Non-Functionality of a Post-Accident Monitoring Instrument ULNRC-06795, Submittal of Fitness for Duty Reports for 2022, Including Single Positive Test Forms2023-01-24024 January 2023 Submittal of Fitness for Duty Reports for 2022, Including Single Positive Test Forms ULNRC-06794, Submittal of Fitness for Duty Program Data for 20222023-01-24024 January 2023 Submittal of Fitness for Duty Program Data for 2022 ULNRC-06787, Response to Request for Additional Information Regarding License Amendment Request for Adoption of Alternate Source Term and Revision of Technical Specifications (LDCN 21-0015)2022-12-0808 December 2022 Response to Request for Additional Information Regarding License Amendment Request for Adoption of Alternate Source Term and Revision of Technical Specifications (LDCN 21-0015) ULNRC-06781, License Amendment Request to Clarify Support System Requirements for the Residual Heat Removal System and Control Room Air Conditioning System Under Technical Specifications 3.4.8, 3.7.11, and 3.9.6 (LDCN 22-0029)2022-12-0101 December 2022 License Amendment Request to Clarify Support System Requirements for the Residual Heat Removal System and Control Room Air Conditioning System Under Technical Specifications 3.4.8, 3.7.11, and 3.9.6 (LDCN 22-0029) ULNRC-06780, Additional Supplement to License Amendment Request to Adopt TSTF-439 and TSTF-505, LDCN 20-0072022-11-30030 November 2022 Additional Supplement to License Amendment Request to Adopt TSTF-439 and TSTF-505, LDCN 20-007 ULNRC-06772, 10 CFR 50.59 and 10 CFR 72.48 Summary Report2022-11-23023 November 2022 10 CFR 50.59 and 10 CFR 72.48 Summary Report ULNRC-06777, Operating Quality Assurance Manual (Oqam) Revision 362022-11-16016 November 2022 Operating Quality Assurance Manual (Oqam) Revision 36 ULNRC-06779, ULNRC-06779: Contesting of Green NCV 05000483/2022010-03, Failure to Perform Required Inservice Testing of Residual Heat Removal Heat Exchanger Pneumatically (Air) Operated Outlet and Bypass Valves2022-11-14014 November 2022 ULNRC-06779: Contesting of Green NCV 05000483/2022010-03, Failure to Perform Required Inservice Testing of Residual Heat Removal Heat Exchanger Pneumatically (Air) Operated Outlet and Bypass Valves ULNRC-06765, License Amendment Request to Revise Technical Specification 5.5.16, Containment Leakage Rate Testing Program, for Permanent Extension of Type a and Type C Leak Rate Testing Frequencies (LDCN 2020-0004)2022-11-0303 November 2022 License Amendment Request to Revise Technical Specification 5.5.16, Containment Leakage Rate Testing Program, for Permanent Extension of Type a and Type C Leak Rate Testing Frequencies (LDCN 2020-0004) ULNRC-06773, Results of Steam Generator Tube In-Service Inspection2022-11-0101 November 2022 Results of Steam Generator Tube In-Service Inspection ULNRC-06775, Submittal of Non-Functionality of Loose-Part Detection System Channel for Greater than 30 Days2022-10-27027 October 2022 Submittal of Non-Functionality of Loose-Part Detection System Channel for Greater than 30 Days ULNRC-06771, Correction to Application to Revise Technical Specifications to Adopt TSTF 577, Revised Frequencies for Steam Generator Tube Inspections (LDCN 21-0013)2022-10-25025 October 2022 Correction to Application to Revise Technical Specifications to Adopt TSTF 577, Revised Frequencies for Steam Generator Tube Inspections (LDCN 21-0013) ULNRC-06770, Cycle 25 Commitment Change Summary Report2022-10-19019 October 2022 Cycle 25 Commitment Change Summary Report ULNRC-06766, Correction of Text Contained in Enclosures Provided with Supplements to Request for License Amendment and Regulatory Exemptions for a Risk-Informed Approach to Address GSI-191 and Respond to GL 2004-02 (LDCN 19-0014)2022-09-0808 September 2022 Correction of Text Contained in Enclosures Provided with Supplements to Request for License Amendment and Regulatory Exemptions for a Risk-Informed Approach to Address GSI-191 and Respond to GL 2004-02 (LDCN 19-0014) 2024-06-26
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000483/LER-2024-002, Concurrent Inoperability of Control Room Air Conditioning System Train and Opposite Train Emergency Diesel Generator Results in Condition Prohibited by Technical Specifications Limiting2024-10-0101 October 2024 Concurrent Inoperability of Control Room Air Conditioning System Train and Opposite Train Emergency Diesel Generator Results in Condition Prohibited by Technical Specifications Limiting . 05000483/LER-2024-001, Reactor Trip Due to Turbine Trip2024-04-0404 April 2024 Reactor Trip Due to Turbine Trip 05000483/LER-2022-003-01, Class 1E Electrical Air Conditioning System Thermal Expansion Valve Failure Resulted in Condition Prohibited by Technical Specifications2023-07-13013 July 2023 Class 1E Electrical Air Conditioning System Thermal Expansion Valve Failure Resulted in Condition Prohibited by Technical Specifications ULNRC-06398, Special Report 2017-02: Non-Functional Seismic Instrument for Greater than 30 Days2017-11-0808 November 2017 Special Report 2017-02: Non-Functional Seismic Instrument for Greater than 30 Days 05000483/LER-2017-0022017-10-13013 October 2017 Inadequate Protection from Tornado Missiles Identified Due to Nonconforming Design, LER 17-002-00 for Callaway Plant, Unit 1, Regarding Inadequate Protection from Tornado Missiles Identified Due to Nonconforming Design 05000483/LER-2017-0012017-08-15015 August 2017 Violation of Technical Specification 3.7.9 Due to Ultimate Heat Sink (UHS) Cooling Tower Train Inoperability, LER 17-001-00 for Callaway, Unit 1, Regarding Violation of Technical Specification 3.7.9 Due to Ultimate Heat Sink (UHS) Cooling Tower Train Inoperability 05000483/LER-2015-0012016-12-0202 December 2016 Completion of a Shutdown Required by the Technical Specifications - TS 3.4.13, LER 15-001-01 for Callaway Plant, Unit 1, Regarding Completion of a Shutdown Required by the Technical Specifications - TS 3.4.13 05000483/LER-2015-0022016-09-0707 September 2016 Manual Auxiliary Feedwater System Actuation, LER 15-002-00 for Callaway, Unit 1, Regarding Manual Auxiliary Feedwater System Actuation 05000483/LER-2016-0012016-06-20020 June 2016 Control Room Air Conditioning Inoperability Due To Essential Service Water Pressure Transient, LER 16-001-00 for Callaway, Unit 1, Regarding Control Room Air Conditioning Inoperability Due to Essential Service Water Pressure Transient 05000483/LER-2015-0032016-01-21021 January 2016 Reactor Trip Caused by Transmission Line Fault, LER 15-003-01 for Callaway, Unit 1, Regarding Reactor Trip Caused by Transmission Line Fault ULNRC-06162, Special Report 2014-05 Inoperability of Loose Parts Monitoring Instrument for Greater than 30 Day2014-12-11011 December 2014 Special Report 2014-05 Inoperability of Loose Parts Monitoring Instrument for Greater than 30 Day ULNRC-06142, SR-14-002 Callaway, Unit 1 - Special Report 2014-02-PAM Report Inoperability of Post Accident Monitoring (PAM) Instrument2014-09-16016 September 2014 SR-14-002 Callaway, Unit 1 - Special Report 2014-02-PAM Report Inoperability of Post Accident Monitoring (PAM) Instrument ULNRC-05991, Special Report 13-001-00 for Callaway, Unit 1, Inoperability of a Seismic Instrument for Greater than 30 Days2013-05-13013 May 2013 Special Report 13-001-00 for Callaway, Unit 1, Inoperability of a Seismic Instrument for Greater than 30 Days ULNRC-05932, Special Report 2012-02 - Pam Report: Inoperability of a Post Accident Monitoring (PAM) Instrument for Greater than 30 Days2012-11-14014 November 2012 Special Report 2012-02 - Pam Report: Inoperability of a Post Accident Monitoring (PAM) Instrument for Greater than 30 Days ULNRC-05824, Special Report 2011-01 for Callway, Unit 1 Regarding Inoperability of a Seismic Instrument for Greater than 30 Days2011-11-10010 November 2011 Special Report 2011-01 for Callway, Unit 1 Regarding Inoperability of a Seismic Instrument for Greater than 30 Days ULNRC-05721, Special Report, Inoperable Channel 8 of the Loose Parts Monitoring System (Lpms)2010-07-22022 July 2010 Special Report, Inoperable Channel 8 of the Loose Parts Monitoring System (Lpms) ULNRC-05374, Special Report 07-001 Re Historical Inoperability of Seismic Instrument SGAR00082007-03-0808 March 2007 Special Report 07-001 Re Historical Inoperability of Seismic Instrument SGAR0008 ML0413203792004-05-0303 May 2004 Special Report for Callaway Plant Unit 1 Regarding Inoperability of 60 Meter Meteorological Monitoring Instrumentation on the Primary Meteorological Tower 2024-04-04
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AmerenUE P0 Box 620 Cal/awayPlant Fulton, MO 65251 March 8, 2007 U.S. Nuclear Regulatory Commission Attn: Document Control Desk Mail Stop P1-137 Washington, DC 20555-0001 ULNRC-05374 n Ladies and Gentlemen:
- "'Ame U/E DOCKET NUMBER 50-483 CALLAWAY PLANT UNIT 1 UNION ELECTRIC CO.
FACILITY OPERATING LICENSE NPF-30 SPECIAL REPORT 07-01 Historical Inoperability of Seismic Instrument SGAR0008 Enclosed is a voluntary Special Report documenting three historical occurrences of seismic instrument SGAR0008, 'C' Steam Generator Support Peak Recording Accelerometer, inoperability for which a report in accordance with Final Safety Analysis Report Section 16.3.3.2 Action 'a' was not submitted.
No new commitments are identified in this correspondence. None of the material in this report is considered proprietary by Union Electric.
If you have any questions or require additional information, please contact Mr. Keith Mills, Supervisor, Regulatory Affairs Regional/Safety Analysis at 573/676-4317.
Sincerely, F. M. Diya Director Plant Operations Enclosure 1) Special Report a subsidiaryof Ameren Corporation
ULNRC-05374 March 8, 2007 Page 2 Mr. Bruce S. Mallett Regional Administrator U.S. Nuclear Regulatory Conr2-nission Region IV 611 Ryan Plaza Drive, Suite 400 Arlington, TX 76011-4005 Senior Resident Inspector Cailaway Resident Office U.S. Nuclear Regulatory Commission 8201 NRC Road Steedman, MO 65077 Mr. Jack N. Donohew (2 copies)
Licensing Project Manager, Callaway Plant Office of Nuclear Reactor Regulation U. S. Nuclear Regulatory Commission Mail Stop O-7D1 Washington, DC 20555-2738 Missouri Public Service Commission Governor Office Building 200 Madison Street PO Box 360 Jefferson City, MO 65102-0360 Mr. Ron Reynolds Director Missouri State Emergency Management Agency P.O. Box 116 Jefferson City, MO 65102
bcc: C. D. Naslund A. C. Heflin F. M. Diya D. T. Fitzgerald G. A. Hughes D. E. Shafer S. L. Gallagher (100)
L. M. Belsky (NSRB)
K. A. Mills P. M. Bell J. W. Hiller A160.0761 Certrec Corporation 4200 South Hulen, Suite 630 Fort Worth, TX 76109 (Certrecreceives ALL attachments as long as they are non-safeguards and public disclosed).
Send the following without attachments:
Ms. Diane M. Hooper Mr. Dennis Buschbaum Supervisor, Licensing TXU Power WCNOC Comanche Peak SES P.O. Box 411 P.O. Box 1002 Burlington, KS 66839 Glen Rose, TX 76043 Mr. Scott Bauer Mr. Stan Ketelsen Regulatory Affairs Manager, Regulatory Services Pao Verde NGS Pacific Gas & Electric P.O. Box 52034, Mail Stop 104/5/536 Mail Station 7636 P.O. Box 56 Phoenix, AZ 85072-2034 Avila Beach, CA 93424 Mr. Scott Head Mr. John O'Neill Supervisor, Licensing Pillsbury Winthrop Shaw Pittman LLP South Texas Project NOC 2300 N. Street N.W.
Mail Code N5014 Washington, DC 20037 P.O. Box 289 Wadsworth, TX 77483
ULNRC-05374 March 8, 2007 Page 1 of 3 ENCLOSURE Special Report The Seismic Instrumentation Limiting Condition For Operation (LCO), Section 16.3.3.2 of the Final Safety Analysis Report (FSAR), requires seismic monitoring instrumentation to be Operable at all times. With one or more of the required seismic monitoring instruments inoperable for more than 30 days, LCO Action 'a' requires a Special Report to be prepared and submitted to the Commission within the next 10 days outlining the cause of the malfunction and the plans for restoring the instrument(s) to Operable status.
There is no current inoperability of seismic instrumentation requiring the submittal of a Special Report. However, a practice associated with surveillance testing of required seismic instrument SGAR0008, 'C' Steam Generator Support Peak Recording Accelerometer, was identified to have the potential for challenging the requirements of LCO 16.3.3.2. The practice of removing SCAR0008 from service during refueling outages was initiated in 1999 without establishing a consistent method to ensure that associated LCO actions were tracked. This issue was documented in the Callaway corrective action program as CAR 200700754 on 1/26/2007. The evaluation under CAR 200700754 revealed previous instances where Special Reports for SGAR0008 inoperability were required but not submitted.
There is no specific reporting requirement addressing historical seismic instrument inoperability or the failure to report as required under FSAR 16.3.3.2 Action 'a'.
However, a voluntary submittal is being made to document three failures to report and to address the cause and associated corrective actions.
Background
As part of the evaluation under the corrective action program, the electronically available work history for SGAR0008 was reviewed back through 1992. The review initially revealed four potential occurrences of seismic instrumentation inoperability lasting longer than 30 days (720 hours0.00833 days <br />0.2 hours <br />0.00119 weeks <br />2.7396e-4 months <br />) for which no Special Report was issued.
Further investigation of the surveillance testing documentation on SGAR0008 revealed that a suggestion documented in CAR 199301604 was written to evaluate potential false recordings due to heavy work performed near the seismic instrumentation (SGAR0008 is located in the containment building near the equipment hatch). One of the specified actions was to create an auxiliary work document in addition to the required surveillance testing. The purpose of the auxiliary work document was to read and restore, as necessary, the scratch plates for SGAR0008 at the end of each outage and to trend the results to determine any further necessary actions. As surveillance testing was performed from 1993 through 1998, testing was completed at the beginning of each outage with the instrument restored
ULNRC-05374 March 8, 2007 Page 2 of 3 during the surveillance procedure. The auxiliary work document was then performed at the end of each outage.
The 1995 performance of this surveillance was originally identified as exceeding 720 hours0.00833 days <br />0.2 hours <br />0.00119 weeks <br />2.7396e-4 months <br /> based on the work history review; however, the surveillance record shows that the seismic monitor was restored within one day of beginning the surveillance. The auxiliary document was then performed at the end of the outage as discussed above.
Sometime between the 1998 and 1999 surveillance testing, the decision was made to physically remove the instrument following the surveillance at the beginning of an outage and to replace it under the auxiliarywork document at the end. Beginning with the 1999 surveillance, guidance was added to the task instructions stating: "Store SGAR0008 in a protected location and note where located". Further review ultimately identified three occurrences where this practice resulted in SGAR0008 being removed from service for greater than 720 hours0.00833 days <br />0.2 hours <br />0.00119 weeks <br />2.7396e-4 months <br />.. A Special Report was net submitted in accordance with requirements of FSAR 16.3.3.2 Action 'a' for the removal of SGAR008 as follows:
Surveillance Removal Re.storation Awprox. Duration [Hours]
S619859 10/2/1999 1/1/1999 733 S647679 4/7/2001 5/12/2001 849 S701110 4/10/2004 5/26/2004 1119 Cause of the Failure to Submit a Special Report Callaway Plant's evaluation determined there were inadequate administrative controls established to ensure that time tracking under FSAR 16.3.3.2 was performed when the practice of removing SGAR0008 was implemented. In addition, the controls established through surveillance procedure and work document notes to initiate time tracking were not consistently implemented.
Extent of Corlition The work practices and history of the remaining eight required seismic instruments were reviewed to determine the extent of condition. The practice of instrument removal for protection against potential false recordings during heavy work activities was not implemented for these instruments. Consequently, the unavailability of these instruments has been significantly less than the 720 hours0.00833 days <br />0.2 hours <br />0.00119 weeks <br />2.7396e-4 months <br /> allowed under LCO 16.3.3.2 Action 'a'. The electronic surveillance history of all eight instruments was reviewed back through 1992. No additional reporting failures were identified.
ULNRC-05374 March 8, 2007 Page 3 of 3 Corrective Action The remedial action of adding a step to the core work document, which generates the surveillance documents for SGAR0008, has been completed. The added step requires a sign-off and causes notification to the Control Room staff to track the inoperability of SGAR0008 during surveillance testing and removal from service.
Final corrective action is to incorporate a similar step into the specific surveillance procedure associated with each required seismic instrument. These corrective actions were completed on March 1, 2007.