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This page provides a simple browsing interface for finding entities described by a property and a named value. Other available search interfaces include the page property search, and the ask query builder.
List of results
- 05000373/LER-1998-016, Forwards LER 98-016-00,per 10CFR50.73(a)(2)(i).Attachment a Provides Commitments for Submittal + (ML20153E782)
- ML20153E783 + (ML20153E783)
- ML20153E784 + (ML20153E784)
- ML20153E786 + (ML20153E786)
- ML20153E789 + (ML20153E789)
- 05000373/LER-1998-016-02, :on 980823,APRM Reactor Scram & Rod Block Setpoints Found to Be non-conservative After Calibr Due to Human Performance Error.Flow Converter Correctly Calibr in Accordance with Procedure LIS-NR-107 + (ML20153E790)
- ML20153E791 + (ML20153E791)
- 05000461/LER-1988-011, :on 880311,drywell Air Coolers Condensate Flow Monitoring Sys Taken Out of Svc Due to Channel Reading Low.On 880407,drywell Air Coolers Condensate Flow Rate Turbine Meters Inoperable Due to Clogged Lines + (ML20153E793)
- ML20153E795 + (ML20153E795)
- RC-98-0169, Comment on Proposed Rule 10CFR50 Re Reporting Requirements for Nuclear Power Reactors.Proposed Improvements to Current Reporting Requirements Would Have Significant & Positive Impact on Regulatory Burden to VC Summer Nuclear Station + (ML20153E797)
- PNO-I-86-019, on 860124,diesel Generator E-2 Scavenging Air Blower Failed After 21 H Continuous Operation at Low Load. Caused by Excessive Low Load Operation,As Reported by Vendor.Blower Replaced W/Higher Tolerance Blower + (ML20153E798)
- ML20153E799 + (ML20153E799)
- ML20153E801 + (ML20153E801)
- IR 05000621/2007016 + (ML20153E802)
- ML20153E803 + (ML20153E803)
- IR 05000413/1988028 + (ML20153E804)
- RBG-44562, LAR 98-07 to License NPF-47,deleting License Conditions Associated with Transamerica Delaval,Inc EDGs + (ML20153E805)
- ML20153E806 + (ML20153E806)
- ML20153E808 + (ML20153E808)
- ML20153E811 + (ML20153E811)
- ML20153E812 + (ML20153E812)
- ML20153E814 + (ML20153E814)
- ML20153E815 + (ML20153E815)
- ML20153E821 + (ML20153E821)
- ML20153E822 + (ML20153E822)
- 05000352/LER-1988-013, :on 880409,full Scram Signal Received When Intermediate Range Monitor Detector Failed.No Control Rod Motion as Result of Event Due to Control Rods Insertion When Entering Shutdown Mode.Monitor to Be Replaced + (ML20153E823)
- ML20153E825 + (ML20153E825)
- ML20153E828 + (ML20153E828)
- ML20153E830 + (ML20153E830)
- ML20153E832 + (ML20153E832)
- ML20153E833 + (ML20153E833)
- IR 05000285/1985026 + (ML20153E834)
- ML20153E836 + (ML20153E836)
- HL-5983, Comment on Proposed Rule 10CFR50 Re Reporting Requirements for Nuclear Power Reactors. Snoc in Total Agreement with NEI Comments,To Be Provided to Nrc.Requests That NRC Provide Guidance to Application of NUREG-1022,rev 1 as Listed + (ML20153E843)
- ML20153E845 + (ML20153E845)
- 05000285/LER-1988-009, :on 880406,investigation Concluded Identifying Concerns Re Capability of Listed Valves to Perform Design Function During Dba.Efforts Made to Find Alternative Method of Performing Affected Valve Functions + (ML20153E846)
- ML20153E847 + (ML20153E847)
- IR 05000255/1986003 + (ML20153E848)
- ML20153E851 + (ML20153E851)
- ML20153E852 + (ML20153E852)
- RBG-23176, Forwards Rept Containing Brief Description of Changes to Initial Test Program (ST-17,ST-18 & ST-21) & Summary of Safety Evaluation for Each Change + (ML20153E855)
- ML20153E856 + (ML20153E856)
- ML20153E857 + (ML20153E857)
- NRC-88-0200, Advises That Shift Operation Advisors Will Be Taken Off Shift & Used in Other Capacities Through End of Yr Based on Advisors Achieving Required Level of Experience + (ML20153E858)
- ML20153E859 + (ML20153E859)
- ML20153E860 + (ML20153E860)
- ML20153E862 + (ML20153E862)
- ML20153E864 + (ML20153E864)
- PNO-III-86-014, on 860212 & 17,emergency Diesel Generator 2A Failed.Caused by Broken Rocker Arms on Left Cylinders 5 & 7, Respectively.Station Will Be Shut Down for 16 Days While Licensee Investigates Problem + (ML20153E866)
- ML20153E867 + (ML20153E867)
- 05000278/LER-1987-001-03, :on 880408,actuation of Primary Containment Isolation Sys Occurred During Switching of 4 Kv Emergency Bus Feed.Caused by Lack of Procedural Guidance & Training for Operators.Training Bulletin Issued + (ML20153E870)