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This page provides a simple browsing interface for finding entities described by a property and a named value. Other available search interfaces include the page property search, and the ask query builder.
List of results
- ML20042F272 + (ML20042F272)
- ML20042F274 + (ML20042F274)
- ML20042F276 + (ML20042F276)
- ML20042F278 + (ML20042F278)
- 05000346/LER-1990-006, :on 900403,station Experienced Safety Features Actuation Sys Levels 1 Through 5 Actuation.Caused by Contact W/Breaker Switch HAAE2 in High Voltage Switchgear Room 2. Meetings Held W/Craft Personnel + (ML20042F279)
- ML20042F280 + (ML20042F280)
- 05000346/LER-1990-007, :on 900403,inadvertent,inconsequential Safety Features Actuation Signal Occured While Defueled.Caused by Incidental Contact W/Monitor in Containment.Temporary Barriers Built Around Monitors + (ML20042F281)
- NLS9000184, Clarifies Initiating Conditions Listed in Re Review of 890919 Rev 11 to Plant Emergency Plan.Gaseous Release Emergency Action Level Established as High Alarm on Effluent Monitor + (ML20042F282)
- ML20042F283 + (ML20042F283)
- TXX-9015, Supplemental Response to Generic Ltr 90-01, Request for Voluntary Participation in NRC Regulatory Impact Survey + (ML20042F285)
- ML20042F286 + (ML20042F286)
- ML20042F290 + (ML20042F290)
- ML20042F291 + (ML20042F291)
- ML20042F292 + (ML20042F292)
- ML20042F293 + (ML20042F293)
- 05000311/LER-1990-012, :on 900403,radiation Monitoring Sys Plant Vent Radioactive Noble Gas Monitor 2R41C Lost Power Resulting in Isolation in Containment purge/pressure-vacuum Relief Sys. Cause Not Determined + (ML20042F296)
- ML20042F299 + (ML20042F299)
- IR 05000458/1990009 + (ML20042F301)
- ML20042F302 + (ML20042F302)
- ML20042F303 + (ML20042F303)
- TXX-9016, Provides Revised Response to Generic Ltr 88-17 Re Loss of DHR + (ML20042F305)
- ML20042F306 + (ML20042F306)
- IR 05000267/1990005 + (ML20042F307)
- PNO-I-90-037, on 900428,power Ascension Program Torsional Test of Main turbine-generator Completed.Normal Plant Shutdown Accomplished on 900428.Temporary Mods to Shift Resonance Peak Expected to Take 4 to 6 Wks + (ML20042F308)
- ML20042F309 + (ML20042F309)
- ML20042F311 + (ML20042F311)
- IR 05000482/1990019 + (ML20042F313)
- ML20042F314 + (ML20042F314)
- ML20042F315 + (ML20042F315)
- ML20042F316 + (ML20042F316)
- ML20042F319 + (ML20042F319)
- ML20042F320 + (ML20042F320)
- 05000277/LER-1990-006-02, :on 900402,actuation of Emergency Diesel Generator Occurred.Caused by Personnel Miscommunication. Shift Mgt Will Be Reminded of Necessity to Control Activities in Control Room + (ML20042F321)
- ML20042F322 + (ML20042F322)
- PNO-IV-90-018, on 900427,notification of Incident Involving Exposure of Contractor Personnel Provided.Two Kay Ray Model 7063S Fixed Gauges Left in Unshielded Position.Caused by Personnel Error + (ML20042F323)
- ML20042F324 + (ML20042F324)
- ML20042F325 + (ML20042F325)
- 05000305/LER-1990-005, :on 900404,intergranular Attack & IGSCC Results in Both Steam Generators a & B Being Categorized as C-3.All Defective Tubes Plugged & Sludge Lancing & Crevice Flushing Conducted + (ML20042F326)
- ML20042F327 + (ML20042F327)
- IR 05000333/1990015 + (ML20042F329)
- ML20042F330 + (ML20042F330)
- ML20042F332 + (ML20042F332)
- HL-1053, Provides Response to Generic Ltr 89-19, Safety Implication of Control Sys in LWR Nuclear Power Plants. Plant Procedures Address Possibility of Vessel Overfill Events & Training Alert Operators to Potential Overfills + (ML20042F333)
- IR 05000373/1990003 + (ML20042F334)
- 2CAN059004, Forwards Nonproprietary Suppl 1 to CEN-386-NP & Proprietary Suppl 1 to CEN-386-P, Responses to Questions on C-E Rept CEN-386-P, Verification of Acceptability of 1-Pin Burnup Limit.... Proprietary Rept Withheld (Ref 10CFR2.790) + (ML20042F335)
- ML20042F336 + (ML20042F336)
- ML20042F338 + (ML20042F338)
- ML20042F339 + (ML20042F339)
- ML20042F340 + (ML20042F340)
- ML20042F342 + (ML20042F342)
- ML20042F345 + (ML20042F345)