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Issue date | Title | Topic | |
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ML20132B329 | 6 December 1996 | Special Rept:On 961113,operator Discovered Control Switch for Diesel Output Breaker in pull-to-lock Position. Investigation Was Performed to Determine How Long Aac DG Was Inoperable | |
BECO-86-173, Partially Withheld Security Event Rept:On 861107,HVAC Duct, Penetrating Vital Area,Removed by Contracted Craft Workers Before Notifying Security.Cause Not Stated.Security Oversight of Subj Contract Work Intensified | 12 November 1986 | Partially Withheld Security Event Rept:On 861107,HVAC Duct, Penetrating Vital Area,Removed by Contracted Craft Workers Before Notifying Security.Cause Not Stated.Security Oversight of Subj Contract Work Intensified | |
BECO-86-171, Partially Withheld Security Event Rept:On 861106,temporary Vital Area Barrier Insp Found Barrier Could Be Breached. Barrier Modified & Compensatory Security Measures Released | 10 November 1986 | Partially Withheld Security Event Rept:On 861106,temporary Vital Area Barrier Insp Found Barrier Could Be Breached. Barrier Modified & Compensatory Security Measures Released | |
ML20211E073 | 26 September 1986 | Unplanned Operating Event Rept 85-6, Manual Reactor Trip Following MSIV Closure Due to Inadvertent Emergency Feedwater Actuation,851009 | |
BECO-86-125, Partially Withheld Security Event Rept:On 860826,bomb Threat Received.Search Initiated.No Suspicious Objects Found | 29 August 1986 | Partially Withheld Security Event Rept:On 860826,bomb Threat Received.Search Initiated.No Suspicious Objects Found | |
ML20238E460 | 28 August 1986 | Partially Withheld Secrity Event Rept:On 860824,bomb Threat Received for Plants.Bomb Search Initiated.No Suspicious Objects Found | |
ML20211K821 | 18 June 1986 | Special Rept:On 860521,valid Failure Occurred on Div 2 Diesel Generator During Performance of Tech Spec Surveillance 4.8.1.1.2.Caused by Failure of Jacket Water Thermostatic Control Valve to Open | |
ML20238E459 | 17 June 1986 | Partially Withheld Security Event Rept:On 860612,withheld Discovery Made Re 860604 Moderate Loss of Security Effectiveness.Caused by Inadequate Post Orders & Training for Assignment.Assignments Will Be Specifically Addressed | |
05000000/LER-1986-009, Ro:On 860312,discovered That LER 2-86-04 & LER 86-009 Not Submitted to Nrc.Caused by Misplaced Repts.Repts Telecopied to Nrc.Procedure for Distribution of Repts Revised | 14 April 1986 | Ro:On 860312,discovered That LER 2-86-04 & LER 86-009 Not Submitted to Nrc.Caused by Misplaced Repts.Repts Telecopied to Nrc.Procedure for Distribution of Repts Revised | |
BECO-86-016, Partially Withheld Security Event Rept:On 860215 Security Officer Appeared to Be Asleep at Post at Vital Area Penetration.Unathorized Entry of Vital Area Did Not Occurr. Security Officer Relieved of Duty & Suspended | 20 February 1986 | Partially Withheld Security Event Rept:On 860215 Security Officer Appeared to Be Asleep at Post at Vital Area Penetration.Unathorized Entry of Vital Area Did Not Occurr. Security Officer Relieved of Duty & Suspended | |
BECO-85-220, Partially Withheld Security Event Rept:On 851204 Vertical Pipe Chase Not Locked.Lock Removed When Surveys Indicated Radiation Level Below Requirement for Locked High Radiation Level.Pipe Chase Will Be Secured | 9 December 1985 | Partially Withheld Security Event Rept:On 851204 Vertical Pipe Chase Not Locked.Lock Removed When Surveys Indicated Radiation Level Below Requirement for Locked High Radiation Level.Pipe Chase Will Be Secured | |
ML20112F684 | 11 December 1984 | Special Rept SR-84-4:on 841015,process Vent High Range RM-GW-130-2 & Ventilation Vent High Range RM-VG-131-2 Effluent Monitors Inoperable.Cause Under Investigation. Alternate Methods of Monitoring Gaseous Effluents Confirmed | |
AECM-84-0204, Special Rept 84-017/0:on 840304,Fire Doors 1A401 & OC219 Blocked Open to Support Maint Activities.Fire Watches Established Until Doors Restored | 6 April 1984 | Special Rept 84-017/0:on 840304,Fire Doors 1A401 & OC219 Blocked Open to Support Maint Activities.Fire Watches Established Until Doors Restored | |
ML20081B617 | 24 February 1984 | RO SPR-84-003:on 840206,following Trip from 100% Power, Specific Activity Sample of Reactor Coolant Showed Peak Dose Equivalent I-131 Limit of Less than or Equal to 1.0 Uci.Caused by Fuel Element Defects in Reactor Core | |
ML20087B618 | 17 February 1984 | RO SPR-84-2:on 840118,specific Activity Sample of Reactor Coolant Showed Peak Dose Equivalent I-131 Level of 1.89 Uci,Exceeding Tech Spec Limit.Caused by Fuel Element Defects in Reactor Core.Dose Level Monitored | |
ML20080N339 | 13 February 1984 | RO SPR-84-1:on 840106,specific Activity Sample of Reactor Coolant Showed Peak Dose Equivalent I-131 Level Exceeded Tech Spec Limits.Caused by Known Fuel Element Defects in Core.Tech Spec Requirements Implemented | |
ML20198H369 | 14 November 1983 | Ro:On 831003,results of as-found Tests Indicated Crosby Main Steam Relief Valves Had Lift Points Exceeding Tech Spec Limits.Valves Disassembled & Rebuilt by Mfg | |
ML20105D243 | 24 June 1983 | Special Rept:Five Individuals Found to Have Received Radiation in Excess of 10CFR20.101 Limits W/O Required Documentation.Caused by computer-based Sys Feature Allowing Use of Outdated Info & Personnel Error.Procedures Revised | High Radiation Area Locked High Radiation Area |
ML20137G450 | 24 March 1981 | Ro:During walk-through of Operator Training Program, O-ring Seal of Filter Holder Found Not Seated Properly Causing Partial Bypass of Filter for Air Sucked Into instrument.Filter-in Lock Adjusted | |
ML20071F086 | 25 September 1980 | Ro:On 800912,sample Analysis Taken from Hydrazine Addition Tank Indicated Sodium Chloride in Tank.Anonymous Telcon Indicated Salt May Have Been Added Prior to Labor Strike by Unknown Persons | |
ML20086D514 | 6 January 1978 | Telecopy Ro:On 780105,discovered That One of Two Nuclear Engineering Co Model B3-1 Shipping Casks Provided w/1-inch Diameter Lid Bolts Rather than 1-1/4 Inch Size Specified in Certificate of Compliance 6058 | |
05000280/LER-1977-012, RO S1-77-01 Re Failures of Hydraulic Shock Supports (Snubbers).Extent of Failures Reported in LER 77-12.All Snubbers Operable on 771207 Startup | 5 January 1978 | RO S1-77-01 Re Failures of Hydraulic Shock Supports (Snubbers).Extent of Failures Reported in LER 77-12.All Snubbers Operable on 771207 Startup | |
ML20086D520 | 14 December 1977 | Telecopy Ro:Heating Steam Coil Leak in Reactor Bldg Ventilation Supply Unit V-AH-4A Resulted in Freezing of Condensate at Inlet to Unit & Subsequent Inoperability of Associated Secondary Containment Isolation Dampers | |
ML20086D537 | 14 October 1977 | Telecopy Ro:Insp of Internal Torus Catwalk Support Structure Revealed That Catwalk Mitered Sections Not All Attached to Horizontal Catwalk Support Plates in Some Manner.Attachment Locations Will Be Upgraded | |
ML20086D550 | 13 October 1977 | Telecopy Ro:On 771012,local Leak Rate Testing of MSIV AO-2-80A & Nitrogen Instrument Air Sys Isolation Valve CV-7436 Indicated That Leakage Exceeded Tech Spec Acceptance Criteria.Cause Under Investigation | |
ML20086D554 | 5 October 1977 | Telecopy Ro:On 771004,local Leak Rate Testing of HPCI Sys Discharge Isolation Check Valve HPCI-9 Indicated That Leakage Exceeded Tech Spec Acceptance Criteria.Cause Under Investigation | |
ML20086S094 | 30 September 1977 | RO S2-77-01, Missing Steam Generator Tube Plug-Hot Leg,Generator B,Row 1,Column 42 | Hydrostatic |
ML20086D557 | 29 September 1977 | Telecopy Ro:On 770929,local Leak Rate Testing of Core Spray Inboard Isolation Check Valve AO-14-13A Indicated That Leakage Exceeded Tech Spec Acceptance Criteria.Cause Under Investigation | |
ML20086D561 | 14 September 1977 | Telecopy Ro:On 770913,local Leak Rate Testing of Core Spray Inboard Isolation Check Valve AO 14-13B Indicated That Leakage Exceeded Tech Spec Acceptance Criteria.Related Event on 770914 | |
ML20086D567 | 12 September 1977 | Telecopy Ro:Main Steam Drain Isolation Valve MD 2373 & Main Steam Outboard Isolation Valve AO 2-86A Exceeded Tech Spec Acceptance Criteria for Local Leak Rate Tests | |
ML20086D642 | 11 July 1977 | Telecopy Ro:On 770709,determined That Recombiner Sys a Offgas Flow Control Valve PCV 7489A Could Be Opened W/ Controlling Solenoid Valve Deenergized.Valve Held from Svc Pending Investigation | |
ML20137G446 | 23 June 1977 | Ro:On 770621,radioactive Source Containing 200 Mci Cs-137 Recovered from Brine Well 33.Incident Described in | |
ML20086F080 | 6 June 1977 | Ro:On 770506,plant Iodine & Particulate Release Rate Exceeded 4% of Facility Tech Spec Averaged Over Second Calendar Quarter of 1977.Caused by Fuel Perforations Coupled W/End of Cycle Testing & Reactor Coolant & Steam Leaks | Fuel cladding |
ML20086D691 | 2 March 1977 | Telecopy Ro:On 770301,torus Water Vol Found to Be Slightly Below Min Vol Established by Tech Specs.Water Vol Restored to Normal Operating Level | |
ML20086D703 | 24 February 1977 | Telecopy Ro:On 770223,while Withdrawing in-sequence Control Rod to Bring Reactor Critical,Reactor Period of Less than 5 Obtained | |
ML20086F418 | 9 December 1976 | RO Re Plant Iodine & Particulate Release Rate Exceeding 4% of Tech Spec 3.8.C.2 Averaged Over Fourth Calendar Quarter 1976.Caused by Leaks in Reactor Water Cleanup Sys.Leaks Repaired & Equipment Modified to Reduce Leakage | |
ML20070J868 | 20 October 1976 | RO 76-13:on 760916,normal Boric Acid Makeup to Vol Control Tank Could Not Be Accomplished Due to Plugging of Chemical & Vol Control Sys Line 1-inch-CH-56-152.Cause Unknown.Line Will Be Inspected for Indications of Solidification | Boric Acid |
ML20070J858 | 1 October 1976 | RO 76-12:on 760909,low Pressure Alarm Occurred on Safety Injection Accumulator C,Resulting in Pressure Reduction. Caused by Partially Open HCV 1936 & Body to Bonnet Leaks on HCV 1898 & 1549.Valves Repaired & Accumulator Repressurized | |
ML20070J896 | 29 September 1976 | RO 76-05:on 760915,pressurizer Level Fell Below 45% Level Setpoint,Resulting in Decreases of Pressurizer Pressure & Vol Control Tank Level.Caused by Leaking Tube in Steam Generator A.Cause of Tube Failure Will Be Evaluated | |
ML20070J880 | 24 September 1976 | RO 76-07:on 760913,monthly Average of Gaseous & Airborne Particulate Wastes for Previous 12 Months Found Greater than Tech Spec Limit.Caused by Interpretational Changes in Tech Spec Section 3.11.B.New Limit Approved | |
ML20086D788 | 10 September 1976 | Telecopy Ro:On 760909,discovered That Torus Water Vol Several Hundred Cubic Ft Below 68,000 Cubic Ft Min Required by Tech Specs.Caused by Failure to Correct for Vol Vs Level Correlation | |
ML20086S551 | 17 August 1976 | SR-S2-76-01 Re Summary of Analysis & Interpretation of Type A,B & C Containment Leak Rate Test Results Obtained During Refueling Outage.No Evidence of Structural Deterioration Found | |
ML20086Q255 | 1 July 1976 | Supplemental Rept to SR-S1-75-08 on Containment Leak Rate Testing Including Errors Inherent in Correlating Type a Leakage Test W/Type B & C Tests & Instrument Error Analysis | |
ML20086S701 | 7 May 1976 | Suppl 1 to USRE-S1-76-01:751204,no Air Flow Indicated from Local Flow Indicator on Containment Gaseous & Particulate Monitor Cabinet.Caused by Failed Bearing on Vacuum Pump. Bearing Replaced & Pump Tested Satisfactorily | |
ML20086D823 | 5 May 1976 | Telecopy Ro:On 760504,during Routine Surveillance Test, Primary Containment Oxygen Concentration Found to Be in Excess of Tech Spec Limit.Caused by Leakage from Drywell Instrument Air Sys Into Containment Nitrogen Supply Line | |
ML20086S591 | 1 April 1976 | Ro:On 760322 & 23,temp Difference Across Station Exceeded 15 F.Caused by Rapid Drop in River Water Ambient Temp Making Prediction When Action Necessary to Avoid Temp Increase Difficult | |
ML20086S698 | 4 February 1976 | Telecopy Ro:On 760204,main Steam Trip Valve TV-MS-201A Failed to Close When Operated from Control Room.Cause Under Investigation | |
ML20086S709 | 3 February 1976 | USRE-S1-76-01:on 751204,no Air Flow Indication Found from Local Flow Indicator on Containment Gaseous & Particulate Monitor Cabinet.Caused by Failed Bearing on Vacuum Pump. Bearing Replaced & Pump Tested Satisfactorily | Boric Acid |
ML20086F470 | 27 January 1976 | Ro:On 760117,gaseous Activity Release Rate Exceeded 4% of Tech Spec 3.8.C.1 for More than 48 H.Caused by Increase in Offgas Activity Due to Fuel Cladding Perforations | Fuel cladding Power change |
ML20137H384 | 12 January 1976 | Ro:On 760106,operator Left Console Key in Switch So That Reactor Not Secured Per Tech Specs.Key Withdrawn from Console.Incident Discussed W/Operators & Large Red Plastic Tag Attached to Key to Make It More Visible |