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MONTHYEARML12335A4702011-06-22022 June 2011 Official Exhibit - NYS000309-00-BD01 - Final Safety Evaluation of EPRI Report, Materials Reliability Program Report 1016596 (MRP-227), Revision 0, Pressurized Water Reactor (PWR) Internals Inspection and Evaluation. Project stage: Approval ML11356A3072011-06-22022 June 2011 New York State (NYS) Pre-Filed Evidentiary Hearing Exhibit NYS000309, Final Safety Evaluation of EPRI Report, Materials Reliability Program Report 1016596 (MRP-227), Revision 0, Pressurized Water Reactor (PWR) Internals Inspection and Evalu Project stage: Approval L-2011-255, Response to NRC Vessels & Internals Integrity Branch Request for Additional Information Regarding Extended Power Uprate License Amendment Request2011-07-0808 July 2011 Response to NRC Vessels & Internals Integrity Branch Request for Additional Information Regarding Extended Power Uprate License Amendment Request Project stage: Request W3F1-2012-0011, Commitment Date Change for Submittal of Reactor Vessel Internals Degradation Management Program Consistent with MRP-227-A2012-02-27027 February 2012 Commitment Date Change for Submittal of Reactor Vessel Internals Degradation Management Program Consistent with MRP-227-A Project stage: Other 1CAN051403, Unit 1, Reactor Vessel Internals Aging Management Program Plan2014-05-20020 May 2014 Unit 1, Reactor Vessel Internals Aging Management Program Plan Project stage: Other ONS-2015-054, Proposed License Amendment Request for the Reactor Vessel Internals Inspection Plan; LAR Number 2010-06 - Action Item No. 6 Completion Date Change2015-05-28028 May 2015 Proposed License Amendment Request for the Reactor Vessel Internals Inspection Plan; LAR Number 2010-06 - Action Item No. 6 Completion Date Change Project stage: Request ML17361A1872017-12-18018 December 2017 Electric Power Research Institute (EPRI) - Transmittal of Revision 1 to Technical Reports MRP-175 and MRP-211 Project stage: Request 2012-02-27
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Category:Letter type:ONS
MONTHYEARONS-2018-025, 2017 Annual Radiological Environmental Operating Report (AREOR)2018-05-15015 May 2018 2017 Annual Radiological Environmental Operating Report (AREOR) ONS-2018-024, 2017 Annual Radioactive Effluent Release Report (ARERR)2018-04-30030 April 2018 2017 Annual Radioactive Effluent Release Report (ARERR) ONS-2018-032, Ufsar/Selected Licensee Commitment Changes2018-04-17017 April 2018 Ufsar/Selected Licensee Commitment Changes ONS-2018-029, Technical Specifications Task Force (TSTF) - 448, Revision 3, Control Room Habitability, License Amendment Request No. 2015-03, Supplement 32018-04-0404 April 2018 Technical Specifications Task Force (TSTF) - 448, Revision 3, Control Room Habitability, License Amendment Request No. 2015-03, Supplement 3 ONS-2018-027, Oconee, Units 1, 2, and 3, Submittal of Emergency Plan Revision 2018-0022018-03-28028 March 2018 Oconee, Units 1, 2, and 3, Submittal of Emergency Plan Revision 2018-002 ONS-2018-023, Response to Nrc'S Request for Additional Information Regarding Relief Request 17-ON-001; Alternative to Extend the Code Case N-770, Inspection Item B, Examination Frequency2018-03-20020 March 2018 Response to Nrc'S Request for Additional Information Regarding Relief Request 17-ON-001; Alternative to Extend the Code Case N-770, Inspection Item B, Examination Frequency ONS-2018-017, Oconee, Units 1, 2, and 3, Submittal of Revised Evaluation to Emergency Plan2018-03-15015 March 2018 Oconee, Units 1, 2, and 3, Submittal of Revised Evaluation to Emergency Plan ONS-2018-021, ISFSI - Submittal of 2017 Annual Effluent Release Report2018-03-0101 March 2018 ISFSI - Submittal of 2017 Annual Effluent Release Report ONS-2018-020, Refuel 28 (O2R28) In-service Inspection (ISI) and Steam Generator In-service Inspection (SG-ISI) Report, Fifth 10-Year ISI Interval2018-02-26026 February 2018 Refuel 28 (O2R28) In-service Inspection (ISI) and Steam Generator In-service Inspection (SG-ISI) Report, Fifth 10-Year ISI Interval ONS-2018-013, Technical Specification Bases Changes2018-02-22022 February 2018 Technical Specification Bases Changes ONS-2018-015, Duke Energy Response to Request for Additional Information; Request for Alternative to Codes and Standards Requirements Pursuant to 10 CFR 50.55a(z) to Satisfy 10 CFR 50.55a(h)(2) Associated with Bronze Tape Wrapped Emergency Power Cabl2018-02-19019 February 2018 Duke Energy Response to Request for Additional Information; Request for Alternative to Codes and Standards Requirements Pursuant to 10 CFR 50.55a(z) to Satisfy 10 CFR 50.55a(h)(2) Associated with Bronze Tape Wrapped Emergency Power Cables i ONS-2018-014, License Amendment Request (LAR) for Changes to the Duke Energy Physical Security Plan - License Amendment Request No. 2018-012018-02-12012 February 2018 License Amendment Request (LAR) for Changes to the Duke Energy Physical Security Plan - License Amendment Request No. 2018-01 ONS-2018-019, Submittal of Emergency Plan, Section B2018-02-0505 February 2018 Submittal of Emergency Plan, Section B ONS-2018-011, Ufsar/Selected Licensee Commitment Changes2018-01-25025 January 2018 Ufsar/Selected Licensee Commitment Changes ONS-2017-087, Spent Fuel Pool Evaluation Supplemental Report, Response to NRC Request for Information Pursuant to 10 CFR 50.54(f) Regarding Recommendation 2.1 of the Near-Term Task Force Review of Insights from ...2017-12-0404 December 2017 Spent Fuel Pool Evaluation Supplemental Report, Response to NRC Request for Information Pursuant to 10 CFR 50.54(f) Regarding Recommendation 2.1 of the Near-Term Task Force Review of Insights from ... ONS-2017-083, Core Operating Limits Report (COLR) for Cycle 29 ONEl-0400-491, Revision 02017-11-21021 November 2017 Core Operating Limits Report (COLR) for Cycle 29 ONEl-0400-491, Revision 0 ONS-2017-041, Revision to Tornado/Helb Mitigation Strategies and Regulatory Commitments2017-11-15015 November 2017 Revision to Tornado/Helb Mitigation Strategies and Regulatory Commitments ONS-2017-085, Duke Energy Comments on the October 24, 2017, Public Meeting with NRC Committee to Review Generic Requirements (CRGR)2017-11-15015 November 2017 Duke Energy Comments on the October 24, 2017, Public Meeting with NRC Committee to Review Generic Requirements (CRGR) ONS-2017-079, Supplemental Information to Support NRC Review of Relief Request No. 17-0N-001; Alternative to Extend the Code Case N-770, Inspection Item B Examination Frequency2017-11-13013 November 2017 Supplemental Information to Support NRC Review of Relief Request No. 17-0N-001; Alternative to Extend the Code Case N-770, Inspection Item B Examination Frequency ONS-2017-078, Emergency Plan Revision 2017-0042017-11-0909 November 2017 Emergency Plan Revision 2017-004 ONS-2017-074, Proposed Amendment to the Renewed Facility Operating Licenses Regarding Revisions to the Updated Final Safety Analysis Report Section Associated with Tile Standby Shutdown Facility License Amendment Request No. 2017-032017-10-20020 October 2017 Proposed Amendment to the Renewed Facility Operating Licenses Regarding Revisions to the Updated Final Safety Analysis Report Section Associated with Tile Standby Shutdown Facility License Amendment Request No. 2017-03 ONS-2017-067, Response to Request for Additional Information Regarding License Amendment Request for TSTF-448, Revision 3, Control Room Habitability, License Amendment Request No. 2015-03, Supplement 22017-10-16016 October 2017 Response to Request for Additional Information Regarding License Amendment Request for TSTF-448, Revision 3, Control Room Habitability, License Amendment Request No. 2015-03, Supplement 2 ONS-2017-069, (ONS) - Additional Information Regarding License Amendment Request for Temporary Completion Time for One Keowee Hydro Unit Inoperable for Generator Stator Replacement2017-10-13013 October 2017 (ONS) - Additional Information Regarding License Amendment Request for Temporary Completion Time for One Keowee Hydro Unit Inoperable for Generator Stator Replacement ONS-2017-070, Transmittal of Oconee, Units 1, 2, and 3, Emergency Plan Implementing Procedures Manual Volume 2, Revision 2017-0022017-10-0505 October 2017 Transmittal of Oconee, Units 1, 2, and 3, Emergency Plan Implementing Procedures Manual Volume 2, Revision 2017-002 ONS-2017-072, Fifth Ten Year Lnservice Inspection Interval, Relief Request No. 17-0N-001; Alternative to Extend the Code Case N-770, Inspection Item B Examination Frequency2017-10-0303 October 2017 Fifth Ten Year Lnservice Inspection Interval, Relief Request No. 17-0N-001; Alternative to Extend the Code Case N-770, Inspection Item B Examination Frequency ONS-2017-066, Registration for Use of General License Spent Fuel Cask Numbers 147 and 1482017-09-20020 September 2017 Registration for Use of General License Spent Fuel Cask Numbers 147 and 148 ONS-2017-061, Revised Response to NRC Regulatory Issue Summary 2017-03, Preparation and Scheduling of Operator License Examinations2017-08-10010 August 2017 Revised Response to NRC Regulatory Issue Summary 2017-03, Preparation and Scheduling of Operator License Examinations ONS-2017-060, Registration for Use of General License Spent Fuel Cask Numbers 145 and 1462017-08-0303 August 2017 Registration for Use of General License Spent Fuel Cask Numbers 145 and 146 ONS-2017-059, Transmittal of Response to March 12, 2012 Request for Information, Recommendation 2.1 Flooding, Required Response 3, Flooding Focused Evaluation Summary2017-07-31031 July 2017 Transmittal of Response to March 12, 2012 Request for Information, Recommendation 2.1 Flooding, Required Response 3, Flooding Focused Evaluation Summary ONS-2017-050, Technical Specification Bases Change 2017-042017-07-21021 July 2017 Technical Specification Bases Change 2017-04 ONS-2017-052, Technical Specification Bases Change 2017-032017-07-20020 July 2017 Technical Specification Bases Change 2017-03 ONS-2017-043, Technical Specification Bases Change 2017-012017-07-20020 July 2017 Technical Specification Bases Change 2017-01 ONS-2017-047, Registration for Use of General License Spent Fuel Cask Numbers 142, 143, and 1442017-06-27027 June 2017 Registration for Use of General License Spent Fuel Cask Numbers 142, 143, and 144 ONS-2017-042, Additional Information Regarding License Amendment Request for Temporary Completion Time for One Keowee Hydro Unit Inoperable for Generator Stator Replacement, License Amendment Request No. 2015-08, Supplement 22017-06-0101 June 2017 Additional Information Regarding License Amendment Request for Temporary Completion Time for One Keowee Hydro Unit Inoperable for Generator Stator Replacement, License Amendment Request No. 2015-08, Supplement 2 ONS-2017-040, Transmittal of Emergency Plan Implementing Procedures Manual Volume 1, Revision 2017-0032017-05-22022 May 2017 Transmittal of Emergency Plan Implementing Procedures Manual Volume 1, Revision 2017-003 ONS-2017-037, 2016 Annual Radiological Environmental Operating Report2017-05-15015 May 2017 2016 Annual Radiological Environmental Operating Report ONS-2017-026, Submittal of Ufsar/Selected Licensee Commitment Change2017-04-11011 April 2017 Submittal of Ufsar/Selected Licensee Commitment Change ONS-2017-024, Revision 028 to ERTG-001, Emergency Response Organization and Emergency Services Training Program2017-03-16016 March 2017 Revision 028 to ERTG-001, Emergency Response Organization and Emergency Services Training Program ONS-2017-001, Submittal of Emergency Plan Program Procedure HP/O/B/1009/001 Rev 0452017-03-0202 March 2017 Submittal of Emergency Plan Program Procedure HP/O/B/1009/001 Rev 045 ONS-2017-017, Emergency Plan Implementing Procedures Manual Volume 1, Revision 2017-0012017-03-0202 March 2017 Emergency Plan Implementing Procedures Manual Volume 1, Revision 2017-001 ONS-2017-018, Emergency Plan Implementing Procedures Manual Volume 2, Revision 2017-0012017-03-0202 March 2017 Emergency Plan Implementing Procedures Manual Volume 2, Revision 2017-001 ONS-2017-015, End of Cycle 29 (1 EOC29) Refueling Outage Lnservice Inspection (ISI) and Steam Generator Lnservice Inspection (SG-ISI) Report, Fifth 10-Year ISI Interval2017-02-24024 February 2017 End of Cycle 29 (1 EOC29) Refueling Outage Lnservice Inspection (ISI) and Steam Generator Lnservice Inspection (SG-ISI) Report, Fifth 10-Year ISI Interval ONS-2017-019, Technical Specification Bases Change 2015-092017-02-23023 February 2017 Technical Specification Bases Change 2015-09 ONS-2017-011, Emergency Plan Revised Evaluation2017-02-0202 February 2017 Emergency Plan Revised Evaluation ONS-2017-009, Units 1, 2 & 3 - Notification of Compliance with Order EA-12-049, Order Modifying Licenses with Regard to Requirements for Mitigation Strategies for Beyond Design Basis External Events.2017-02-0101 February 2017 Units 1, 2 & 3 - Notification of Compliance with Order EA-12-049, Order Modifying Licenses with Regard to Requirements for Mitigation Strategies for Beyond Design Basis External Events. ONS-2017-004, Submittal of Core Operating Limits Report2017-01-12012 January 2017 Submittal of Core Operating Limits Report ONS-2017-006, Emergency Plan Revision 2016-0032017-01-12012 January 2017 Emergency Plan Revision 2016-003 ONS-2016-097, Emergency Plan/Emergency Plan Implementing Procedures Manual, Revised 10CFR 50.54(q) Evaluation(S)2016-11-17017 November 2016 Emergency Plan/Emergency Plan Implementing Procedures Manual, Revised 10CFR 50.54(q) Evaluation(S) ONS-2016-098, Special Report Per Technical Specification 5.6.6, Inoperability of Post Accident Monitoring Containment High Range Radiation Monitors2016-11-14014 November 2016 Special Report Per Technical Specification 5.6.6, Inoperability of Post Accident Monitoring Containment High Range Radiation Monitors ONS-2016-096, Revised Response to NRC Regulatory Issue Summary 2015-05, Preparation and Scheduling of Operator Licensing Examinations2016-11-10010 November 2016 Revised Response to NRC Regulatory Issue Summary 2015-05, Preparation and Scheduling of Operator Licensing Examinations 2018-05-15
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,6 SCOTT L. BATSON Vice President Oconee Nuclear Station ENERGY, Duke Energy ONO I VP / 7800 RochesterHwy Seneca, SC 29672 864-873-3274 864-873-4208 fax Scott.Batson@duke-energy.com ONS-2015-054 1 OCFR50.90 May 28, 2015 ATTN: Document Control Desk U. S. Nuclear Regulatory Commission Washington, DC 20555 Duke Energy Carolinas, LLC Oconee Nuclear Station, Units 1, 2, and 3 Docket Numbers 50-269, 50-270, and 50-287 Renewed License Numbers DPR-38, DPR-47, and DPR-55
Subject:
Proposed License Amendment Request for the Reactor Vessel Internals Inspection Plan; LAR Number 2010 Action Item No. 6 Completion Date Change
References:
- 1. License Amendment Request for the Reactor Vessel Internals Inspection Plan (Supplement 1), Duke Energy Carolinas, LLC, dated June 28, 2012.
- 2. NRC Final Safety Evaluation of EPRI Report, Materials Reliability Program Report 1016596 (MRP-227), Revision 0, "Pressurized Water Reactor (PWR) Internals Inspection and Evaluation Guidelines," (TAC No. ME0680), dated June 22, 2011.
By letter dated June 28, 2012 (Ref. 1), Duke Energy committed to respond to Action Item No. 6 (A16) as described in the NRC Safety Evaluation Report associated with the pressurized water reactor internals inspection program's material reliability (Ref. 2). A16 requires the applicant provide justification for the continued operability of each of the inaccessible components and if necessary, provide a plan for the replacement of the components for NRC review and approval.
During the Oconee MRP-227 initial inspections, Request for Additional Information (RAI) 4 established that the justification would be due one (1) year from the initial inspection if inspection results met certain expansion criteria. During the initial inspections of the three Oconee Units, none of the expansion criteria for these components was met and thus, the 1-year response due date requirement did not apply.
On May 6, 2015, by conference call, Duke Energy discussed the completion status of A16 with the NRC. As part of this conference call, Duke Energy requested an additional 1-year to complete A16. Based primarily on the component inspection information collected to date (that the NRC requested be docketed [attached]), the NRC verbally approved a due date extension to May 31, 2016.
AIC
U. S. Nuclear Regulatory Commission May 28, 2015 Page 2 Any inquiries on this letter should be directed to Stephen C. Newman, Oconee Nuclear Station, Regulatory Affairs Lead Engineer, at (864) 873-4388.
I declare under penalty of perjury that the foregoing is true and correct. Executed on May 28, 2015.
Sincerely, Scott L. Batson Vice President Oconee Nuclear Station Attachment
U. S. Nuclear Regulatory Commission May 28, 2015 Page 3 cc: (w/attachment)
Mr. Victor McCree Regional Administrator U.S. Nuclear Regulatory Commission - Region 11 Marquis One Tower 245 Peachtree Center Ave., NE Suite 1200 Atlanta, Georgia 30303-1257 Mr. James R. Hall, Senior Project Manager (by electronic mail only)
Office of Nuclear Reactor Regulation U.S. Nuclear Regulatory Commission Mail Stop 0-8 G9A 11555 Rockville Pike Rockville, Maryland 20852 Mr. Jeffrey A. Whited Project Manager (by electronic mail only)
Office of Nuclear Reactor Regulation U.S. Nuclear Regulatory Commission 11555 Rockville Pike Mail Stop O-8G9A Rockville, Maryland 20852 Mr. Eddy Crowe NRC Senior Resident Inspector Oconee Nuclear Station Ms. Susan E. Jenkins, Manager, Infectious and Radioactive Waste Management, Bureau of Land and Waste Management Department of Health & Environmental Control 2600 Bull Street Columbia, SC 29201
Attachment Action Item #6 (A16) Inspection Status and Justification to Extend the Completion Date to May 31, 2016 The initial MRP-227-A inspections were completed in the fall of 2012 for Oconee Unit 1, Fall of 2013 for Oconee Unit 2 , and Spring 2014 for Oconee Unit 3. For four (4) of the inaccessible "Expansion" components, 100% of their "Primary" components were visually inspected and no relevant indications were found. They are as follows:
Expansion Component Primary Component Core barrel cylinders including Baffle plates, 100% inspected no vertical and circumferential welds relevant indications.
Former plates Baffle plates, 100% inspected no relevant indications.
Locking devices for external baffle- Locking devices, including locking welds, to-baffle bolt of baffle-to-former bolts and in internal baffle-to-baffle bolts. 100% inspected no relevant indications.
Locking devices for core barrel-to- Locking devices, including locking welds, former bolts of baffle-to-former bolts and in internal baffle-to-baffle bolts. 100% inspected no relevant indications.
The other three (3) inaccessible/un-inspectable "Expansion" components are the core barrel-to-former bolts, the external baffle-to-baffle bolts, and the internal baffle-to-baffle bolts. The "Primary" inspection for these is an ultrasonic (UT) inspection of the baffle-to-former bolts. Each of the three Oconee Units has 864 baffle-to-former bolts. The results of the initial inspections are given below:
Unit Baffle-to-Former Bolt UT Inspection Results Oconee Unit 1 4 of 864 bolts un-inspectable due to not being able seat the transducer correctly.
Oconee Unit 2 1 of 864 bolts un-inspectable due to not being able seat the transducer correctly.
Oconee Unit 3 1 of 864 bolts un-inspectable due to not being able seat the transducer correctly, and 1 was found to contain a crack like indication located in the head to shank region.
To date there have been four (4) UT examinations of the baffle-to-former bolt performed at the B&W-designed unit Crystal River Unit 3 in addition to the three Oconee Units which amounts to 3,456 bolts. Six (6) bolts were un-inspectable due to not being able to seat the UT probe and only one was identified with a crack-like indication. The core barrel-to-former and
Attachment May 28, 2015 Page 2 baffle-to-former bolts have the function of maintaining structural integrity of the baffle and former portion of the structural assembly and thus maintaining flow geometry during normal operation.
For faulted events, only a small number of the core barrel-to-former and baffle-to-former bolts are necessary to restrain the baffle so that a coolable core geometry is maintained for safety considerations. The loss of the baffle-to-baffle bolts only slightly influence core bypass flow but the baffle-to-baffle bolts are not necessary to maintain structural integrity.
The Oconee units will be re-inspected in approximately 10 years. With only one (1) crack-like indication found to date, there is reasonable assurance that there are no safety concerns to extending the A16 completion date to May 31, 2016.