IR 05000395/2023090

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NRC Inspection Report 05000395/2023090 and Preliminary Yellow Finding and Apparent Violation
ML23268A467
Person / Time
Site: Summer South Carolina Electric & Gas Company icon.png
Issue date: 10/04/2023
From: Ladonna Suggs
Division Reactor Projects II
To: Carr E
Dominion Energy
References
EA-23-093, EPID I-2023-090-0008 IR 2023090
Download: ML23268A467 (18)


Text

SUBJECT:

VIRGIL C. SUMMER NUCLEAR STATION - NRC INSPECTION REPORT 05000395/2023090 AND PRELIMINARY YELLOW FINDING AND APPARENT VIOLATION

Dear Eric S. Carr:

The enclosed inspection report documents a finding with an associated apparent violation that the U.S. Nuclear Regulatory Commission (NRC) has preliminarily determined to be Yellow with substantial safety significance. This involved a self-revealed apparent violation of Title 10 of the Code of Federal Regulations (10 CFR) Part 50, Appendix B, Criterion XVI, Corrective Action, which was identified for the licensee failing to correct a condition adverse to quality resulting in the inoperability of the A emergency diesel generator (EDG). We assessed the significance of the finding using the significance determination process (SDP) and the best available information at the time of the significance and enforcement review panel on September 13, 2023. We are considering escalated enforcement for the apparent violation consistent with our Enforcement Policy, which can be found at http://www.nrc.gov/about-nrc/regulatory/enforcement/enforce-pol.html. Because we have not made a final determination, no notice of violation is being issued at this time. Please be aware that further NRC review may prompt us to modify the number and characterization of the apparent violation.

The NRCs significance determination process is designed to encourage an open dialogue between your staff and the NRC; however, neither the dialogue nor the written information you provide should affect the timeliness of our final determination.

Before we make a final decision on this matter, we are providing you with an opportunity to (1)

attend a regulatory conference where you can present to the NRC your perspective on the facts and assumptions the NRC used to arrive at the finding and assess its significance, or (2) submit your position on the finding to the NRC in writing. If you request a regulatory conference, it should be held within 40 days of the receipt of this letter, and we encourage you to submit supporting documentation at least one week prior to the conference to make the conference more efficient and effective. The focus of the regulatory conference is to discuss the significance of the finding and not necessarily the root cause(s) or corrective action(s) associated with the finding. If a regulatory conference is held, it will be open for public observation. If you decide to submit only a written response, such submittal should be sent to the NRC within 40 days of your receipt of this letter.

October 4, 2023 If you choose to send a response, please include your perspective of the significance of the finding along with the related facts and assumptions used to reach your determination.

Additionally, your response should be clearly marked as a Response to an Apparent Violation; (EA-23-093) and should include for the apparent violation: (1) the reason for the apparent violation; (2) the corrective steps that have been taken and the results achieved; (3) the corrective steps that will be taken; and (4) the date when full compliance will be achieved. Your response should be submitted under oath or affirmation and may reference or include previously docketed correspondence, if the correspondence adequately addresses the required response.

Additionally, your response should be sent to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Center, Washington, DC 20555-0001 with a copy to Mr. David E.

Dumbacher, U.S. Nuclear Regulatory Commission, Region II, within 40 days of the date of this letter. If an adequate response is not received within the time specified or an extension of time has not been granted by the NRC, the NRC will proceed with its enforcement decision or schedule a regulatory conference.

If you decline to request a regulatory conference or to submit a written response, you relinquish your right to appeal the final SDP determination, in that by not doing either, you fail to meet the appeal requirements stated in the Prerequisite and Limitation sections of Attachment 2 of NRC Inspection Manual Chapter 0609.

Please contact Mr. David E. Dumbacher at 404-997-4628, and in writing, within 10 days from the issue date of this letter to notify the NRC of your intentions. If we have not heard from you within 10 days, we will continue with our significance determination and enforcement decision.

The final resolution of this matter will be conveyed in separate correspondence.

For administrative purposes, this inspection report provides an update to the apparent violation documented in NRC inspection report 05000395/2023002 (Agency Documents Access and Management System (ADAMS) ML23223A006) dated August 14, 2023.

This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, LaDonna B. Suggs, Acting Director Division Of Reactor Projects Docket No. 05000395 License No. NPF-12

Enclosure:

IR 05000395/2023090 w/Attachment: A-EDG Fuel Oil Leak Detailed Risk Evaluation

Inspection Report

Docket Number:

05000395

License Number:

NPF-12

Report Number:

05000395/2023090

Enterprise Identifier:

I-2023-090-0008

Licensee:

Dominion Energy

Facility:

Virgil. C. Summer Nuclear Station

Location:

Jenkinsville, SC

Inspection Dates:

August 10, 2023 to September 13, 2023

Inspectors:

N. Childs, Senior Project Engineer

M. Read, Senior Resident Inspector

S. Sandal, Senior Reactor Analyst

Approved By:

LaDonna B. Suggs, Director

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees

performance by conducting an NRC inspection at Virgil. C. Summer, in accordance with the

Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for

overseeing the safe operation of commercial nuclear power reactors. Refer to

https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Failure to Identify and Correct a Condition Adverse to Quality Associated with the EDG Fuel

Oil System

Cornerstone

Significance

Cross-Cutting

Aspect

Report

Section

Mitigating

Systems

Preliminary Yellow

AV 05000395/2023002-01

Open

EA-23-093

None (NPP)

71111.12

A self-revealed finding that has preliminarily been determined to be Yellow (substantial safety

significance) and associated apparent violation (AV) of Title 10 of the Code of Federal

Regulations (10 CFR) Part 50, Appendix B, Criterion XVI, Corrective Action, was identified

when the licensee failed to identify and correct a condition adverse to quality (CAQ) for the

EDG fuel oil system that left the system vulnerable to piping cracks and eventually resulted in

the failure of the A EDG during testing on November 2, 2022. Specifically, inspectors

determined that, based on the failure history of the EDGs and the licensees documented

conclusions that attributed pipe cracks to prior maintenance events, the licensee had sufficient

information to identify the existence of a condition adverse to quality related to the design of

the EDG fuel oil system. This condition caused threaded fuel oil piping connections to be

vulnerable to maintenance activities that over torqued, strained, or impacted the piping.

Despite the challenge to maintain leak-tight connections and repeat occurrences of cracked

piping, no significant changes were made to maintenance practices, procedures or system

design, and the licensee continued to reactively monitor for leakage even after vulnerabilities

were identified.

Additional Tracking Items

None.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in

effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with

their attached revision histories are located on the public website at http://www.nrc.gov/reading-

rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared

complete when the IP requirements most appropriate to the inspection activity were met

consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection

Program - Operations Phase. The inspectors reviewed selected procedures and records,

observed activities, and interviewed personnel to assess licensee performance and compliance

with Commission rules and regulations, license conditions, site procedures, and standards.

INSPECTION RESULTS

Failure to Identify and Correct a Condition Adverse to Quality Associated with the EDG Fuel

Oil System

Cornerstone

Significance

Cross-Cutting

Aspect

Report

Section

Mitigating

Systems

Preliminary Yellow

AV 05000395/2023002-01

Open

EA-23-093

None (NPP)

71111.12

A self-revealed finding that has preliminarily been determined to be Yellow (substantial safety

significance) and associated AV of Title 10 of the Code of Federal Regulations (10 CFR) Part

50, Appendix B, Criterion XVI, Corrective Action, was identified when the licensee failed to

identify and correct a CAQ for the EDG fuel oil system that left the system vulnerable to

piping cracks and eventually resulted in the failure of the A EDG during testing on November

2, 2022. Specifically, inspectors determined that, based on the failure history of the EDGs

and the licensees documented conclusions that attributed pipe cracks to prior maintenance

events, the licensee had sufficient information to identify the existence of a condition adverse

to quality related to the design of the EDG fuel oil system. This condition caused threaded

fuel oil piping connections to be vulnerable to maintenance activities that over torqued,

strained, or impacted the piping. Despite the challenge to maintain leak-tight connections and

repeat occurrences of cracked piping, no significant changes were made to maintenance

practices, procedures or system design, and the licensee continued to reactively monitor for

leakage even after vulnerabilities were identified.

Description: On November 2, 2022, during the performance of a 24-hour surveillance test,

operations identified a small leak on the 3/4 fuel piping header supplying the A EDG right

bank cylinders fuel injectors. The leakage was monitored and observed to increase over

several hours until operations stopped the surveillance test, secured the engine, and

prepared the EDG for repairs. During troubleshooting and repairs, the licensee identified that

a crack between the threads of the male end of the pipe had propagated 140-degrees around

the circumference of the pipe. The location of the crack was in a section of piping that

experienced vibrations during operation. The original design of the fuel oil delivery piping

included threaded connections for ease of maintenance. An engineering assessment

determined that the EDG was unlikely to have been able to perform its 24-hour mission time.

Inspectors reviewed historical condition reports (CRs) and maintenance records and noted

that the A and B EDGs have experienced fuel oil piping cracking near the left and right fuel

header connections where vibrations are present. Inspectors noted that, on March 2, 2020,

during repairs to correct minor fuel oil leakage under WO1909952 step 2, the licensee

identified a crack on the A EDG 1 x 1/2 reducer bushing on the left bank header. A CR was

not generated to document the cracked bushing. During the retest on March 5, 2020, fuel oil

leakage was identified, and the licensee initiated CR 20-00712 as a non-condition adverse to

quality (NCAQ) to document the leakage. After subsequent repairs on March 6, 2020, during

the maintenance retest, the licensee identified a leak and a crack on the newly installed pipe

nipple that was attached to a new bushing installed on March 5, 2020, which was

documented in CR-20-00735 as an NCAQ. The nipple was replaced, and no further

evaluation was performed.

Licensee procedure SAP-0999, Corrective Action Program, Revision 19, step 1.2.3 required

the determination of CR category and evaluation type using examples and guidance in

Enclosures A and J. Although maintenance rework items were identified as NCAQs and did

not require evaluations, the identification of cracked bushing and fittings should have been

identified as a CAQ because both components were found degraded in a condition that had

the potential to inhibit a safety-related structure, system, and component from satisfactory

performance of a safety-related function. This may have driven an evaluation of previous

conditions, cause of the issue, and extent of condition, but guidance in Enclosure A to

determine the level of evaluation would have been subjective based on the perceived

consequence. Since the component cracked, it should have received at least a D-OTH

evaluation which would have identified the most probable cause of the cracks. Since the

failure was treated as a broke/fix, even though the components were cracked prior to the

maintenance window, the licensee missed an opportunity to identify if a CAQ existed.

Additionally, inspectors noted the following events in 2003 and 2014, which illustrate a history

of similar failures of the EDG fuel oil system piping:

On October 21, 2003, while performing maintenance testing on the A EDG, the right

bank fuel supply line ruptured at the threaded connection. The licensee documented

NCN-03-03500 and attributed the crack to manual manipulation of the pipe. The pipe

nipple was replaced, and the 10-foot crossover pipe between the left and right fuel oil

header banks was shortened to minimize piping spring.

On August 20, 2014, the A EDG left bank 3/4 x 2 nipple developed a 120 drops per

minute leak. The licensee initiated CR 14-04564 to repair the connection. During

repairs, mechanics identified a hairline crack in the threads. The nipple was replaced,

and the licensee initiated CR 14-04592 to document the hairline crack. The CR

actions included a quick cause evaluation and assignments for engineering to inspect

other threaded connections for evidence of leakage during the next runs of the A and

B EDGs. The quick cause evaluation noted the 2003 pipe crack on the opposite side

of the A EDG and determined that the single impact event during a 2003

maintenance activity damaged the left bank nipple and over 11 subsequent years of

operation, the crack developed due to fatigue.

On November 4, 2014, the B EDG right bank 3/4 x 15 nipple developed a small

leak. The licensee initiated CR 14-05797 to repair the connection. During repairs,

mechanics identified a hairline crack in the threads. The pipe nipple was replaced,

and the D-OTH evaluation by engineering stated that the most likely cause was a

single impact event followed by subsequent high stress low cycle fatigue. The

licensee established a corrective action to monitor the system for early signs of

leakage during EDG runs.

Each of these instances of piping or bushing cracks were remediated by replacement of the

components and monitoring for future leakage from similar components. The EDG fuel oil

system was designed to be robust to withstand the expected high vibrations for the life of the

plant. Due to the standby nature of EDGs at nuclear power plants, which only run during

testing and events involving a loss of offsite power, it is rare that an EDG would operate more

than 100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br /> per year. Although the EDG fuel oil system cracks were separated by many

years between events, the total run time of the EDGs between failures was small compared

to the expected life of the system. The licensee had evidence that maintenance activities,

including piping manipulation and impact events could not only damage multiple connections,

but the damage may not reveal itself through an open crack for years. This vulnerability of the

EDG system is exacerbated by the use of schedule-40 piping with tapered threads that is

more susceptible to cracking than thicker piping or different connection designs.

Inspectors determined that, based on the failure history of the EDGs and the licensees

documented conclusions that attributed pipe cracks to prior maintenance events, the licensee

had sufficient information to identify that a CAQ existed with the design of the EDG fuel oil

system that caused the threaded connections to be vulnerable to maintenance activities that

over torqued, strained, or impacted the piping. This vulnerability in the system was most

prevalent in the left and right bank fuel oil connections which were subject to high vibrations

during EDG operation. Despite the challenge to maintain leak-tight connections and the

history of cracked pipes, no significant changes were made to maintenance practices or

procedures, and the licensee continued to reactively monitor for leakage even after

vulnerabilities were identified. The licensee also did not make any substantive changes to the

design of the system to reduce the vulnerability to maintenance-induced challenges.

The licensee treated individual pipe failures as broke/fix rather than identifying the system

vulnerability. The licensee had evidence prior to the November 2022 failure of the A EDG

supply header pipe that cracks could propagate rapidly during EDG operation as seen in the

October 2003 rupture of the same A EDG supply header pipe. CRs documenting failures in

2020 were classified as NCAQs and represented a missed opportunity for the licensee to

perform an evaluation to identify whether a common CAQ existed and determine if previous

failures in 2003 and 2014 were indicative of a more significant problem with the EDG fuel oil

system piping.

Corrective Actions: The licensee replaced the cracked pipe nipple on the A EDG and

reperformed the 24-hour surveillance test. The licensee also replaced the same nipple on the

B EDG to extend the life of the piping.

Corrective Action References: CR 1211780

Performance Assessment:

Performance Deficiency: The licensee's failure to identify and correct a CAQ for the EDG fuel

oil system that left the system vulnerable to piping cracks was a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor

because it was associated with the design control attribute of the mitigating systems

cornerstone and adversely affected the cornerstone objective to ensure the availability,

reliability, and capability of systems that respond to initiating events to prevent undesirable

consequences. Specifically, the condition caused the threaded fuel oil piping connections to

be vulnerable to maintenance activities which resulted in the failure of a pipe nipple and

inoperability of the A EDG on November 2, 2022.

Significance: The inspectors assessed the significance of the finding using IMC 0609

Appendix AProperty "Inspection Manual Chapter" (as page type) with input value "NRC Inspection Manual 0609</br></br>Appendix A" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process., The Significance Determination Process (SDP) for Findings At-Power. The

affected cornerstone was mitigating systems, as determined by IMC 0609, Attachment 4,

Initial Characterization of Findings. The inspectors screened the performance deficiency

using Exhibit 2 of Appendix A and determined a detailed risk evaluation was required

because the degraded condition represented a loss of the Probabilistic Risk Assessment

(PRA) function of one train of a multi-train Technical Specification (TS) system for greater

than its TS allowed outage time.

A Region II Senior Reactor Analyst performed a detailed risk evaluation. The finding was

preliminarily determined to be of substantial safety significance (Yellow). The preliminary risk

estimate was obtained by performing a run-time failure conditional analysis of the A-train

EDG using a 162-day exposure period evaluated over six run intervals. The dominant

Standardized Plant Analysis Risk (SPAR) model sequences were associated with fire

initiating events with impact to the normal offsite power supply, random failure/unavailability

of the B-train EDG, and the inability to restore power from the 13.8 kV source and operator

failure to control the Turbine Driven Essential Feedwater (TDEFW) pump following battery

depletion. See Attachment, A-EDG Fuel Oil Leak Detailed Risk Evaluation, for a summary

of the preliminary risk determination analysis.

Cross-Cutting Aspect: Not Present Performance. No cross-cutting aspect was assigned to

this finding because the inspectors determined the finding did not reflect present licensee

performance.

Enforcement:

Violation: 10 CFR Part 50 Appendix B, Criterion XVI Corrective Action, states, in part that,

measures shall be established to assure that conditions adverse to quality, such as failures,

malfunctions, deficiencies, deviations, defective material and equipment, and

nonconformances are promptly identified and corrected.

Section 16, Corrective Action, of the V.C. Summer Quality Assurance Program Description,

Revision 2 (2014), described the methods to meet Criterion XVI, which stated, in part, when

complex issues arise where it cannot be readily determined if a condition adverse to quality

exist, [the licensee] documents establish the requirements for documentation and timely

evaluation of the issue.

Licensee procedure SAP-0999, Corrective Action Program, Revision 12 (2014), step 6.3.1

stated, When an issue is recognized that it is not meeting performance expectations, the

event should be documented via a CR. An example of a condition that required a CR is The

failure mechanism has implications that may affect multiple systems or components.

Contrary to the above, following discovery of cracked components in the EDG fuel oil system

dating back to 2003, the licensee fixed the cracked piping/fittings but failed to identify and

correct the failure mechanism that affected the fuel oil system piping on both the A and B

EDGs, eventually leading to the failure of the A EDG fuel oil piping during testing on

November 2, 2022. Specifically, CRs documenting failures in 2020 were classified as NCAQs

and represented a missed opportunity for the licensee to perform an evaluation to identify

whether a common CAQ existed and determine if previous failures in 2003 and 2014 were

indicative of a more significant problem with the EDG fuel oil system piping.

Enforcement Action: This violation is being treated as an AV pending a final significance

(enforcement) determination.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

On September 28, 2023, the inspectors presented the NRC inspection results to Mr.

Robert Justice, Site Vice President, and other members of the licensee staff.

ATTACHMENT: A-EDG FUEL OIL LEAK DETAILED RISK EVALUATION

OVERALL RISK SUMMARY

The V.C. Summer A-train EDG was rendered inoperable due to a fuel header through-wall leak

discovered during a surveillance test. The crack size and associated leak rate increased until the

licensee terminated the surveillance test approximately six hours into a planned 24-hour run. Analysis of

the condition indicated that the A-train EDG would not have been able to operate for its mission time and

would have prevented the EDG from providing its emergency power safety function. A risk evaluation

using a 162-day exposure period preliminarily estimated an increase in the change in core damage

frequency (delta-CDF) of 2.92E-05/year (consistent with a Yellow finding).

PERFORMANCE DEFICIENCY

The licensee's failure to identify and correct a CAQ for the EDG fuel oil system that left the system

vulnerable to piping cracks was a performance deficiency.

The inspectors determined the performance deficiency was more than minor because it was associated

with the design control attribute of the mitigating systems cornerstone and adversely affected the

cornerstone objective to ensure the availability, reliability, and capability of systems that respond to

initiating events to prevent undesirable consequences. Specifically, the condition caused the threaded

fuel oil piping connections to be vulnerable to maintenance activities which resulted in the failure of a

pipe nipple and inoperability of the 'A' EDG on November 2, 2022.

The analyst noted that the performance deficiency was also more than minor because it was associated

with the equipment performance attribute of the mitigating systems cornerstone and adversely affected

the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to

initiating events to prevent undesirable consequences. Specifically, the condition caused the threaded

fuel oil piping connections to be vulnerable to maintenance activities which resulted in the failure of a fuel

oil pipe nipple and inoperability of the A-train EDG on November 2, 2022.

EXPOSURE TIME

The component run-time failure approach discussed in Section 2.5 of Volume 1 of the Risk Assessment

Standardization Project (RASP) Manual was used to evaluate the condition exposure time. The run

history of the A-train EDG prior to the failure in November 2022 was used to determine the number of

intervals of accumulated operation for its 24-hour PRA mission time (precise condition inception time was

unknown, but the vibration-induced degradation mechanism was assumed to progress only during

operation of the EDG). The final time interval included the A-train EDG repair time after the leak was

identified during the surveillance test. A total exposure time of 162 days divided into six run intervals was

used for the analysis. The condition exposure period began on May 24, 2022, and ended following

repairs to the A-train EDG on November 2, 2022.

RISK ANALYSIS/CONSIDERATIONS

Assumptions

1.

The A-train EDG was assumed to have been able to operate an additional three hours beyond the

point that the licensee voluntarily terminated the surveillance test on November 2, 2022. This

assumption was made to avoid the overly conservative assumption that the A-EDG function had

completely failed six hours into its test. The three-hour time estimate was made based on the

reported rate of increase in leakage during the surveillance test which was assumed to be

proportional to the rate of crack growth (or 140 degrees approximately six hours into the surveillance

test). This assumption could be considered non-conservative because the crack propagation, if

allowed to continue, could reasonably have been expected to exhibit exponential growth

characteristics (vs. linear) leading to more rapid failure of the EDG and potentially adding additional

condition exposure time to the analysis. The run history of the A-train EDG was examined, and it was

determined that the EDG had been operated successfully approximately one week prior to the start

of the analysis exposure period of May 24, 2022. This indicates that the assumption, while potentially

non-conservative, would not significantly impact the overall exposure period or conclusions resulting

from the analysis.

2.

The condition was assumed to only continue to degrade when the EDG was operated and not when

in a standby status. Consequently, the component run-time failure approach discussed in Section 2.5

of Volume 1 of the RASP manual was used to evaluate the condition exposure time. Based on the

run history of the A-train EDG a condition exposure period of 162 days, divided into six separate run

intervals, and including repair time was used for the analysis. To explore the sensitivity of the

analysis results with respects to use of the run-time failure approach, a sensitivity case will be

performed that does not divide the 162-day exposure period into time intervals.

3.

No repair credit for the failure of the A-train EDG fuel header was included in the analysis.

4.

Diverse and Flexible Coping Strategies (FLEX) mitigating strategies and equipment were credited in

the analysis using a 24-hour PRA mission time. FLEX equipment reliability was modeled using

information contained in PWROG-18042-NP, Revision 1, FLEX Equipment Data Collection and

Analysis, (ADAMS ML22123A259). A sensitivity case with no FLEX credit was also performed.

Systems Analysis Program for Hands-On Integrated Reliability Evaluations (SAPHIRE) software version

8.2.8 and V.C. Summer SPAR model version 8.80 was used for the evaluation.

1.

The SPAR model was modified with the assistance of Idaho National Lab to account for the capability

of powering the A-or B-train 7.2 kV Engineered Safety Features (ESF) bus from the 13.8 kV section

of the Parr hydro unit switchyard. This offsite power supply is an underground feed via transformer

XTF-5052 that has the capability of providing power to either ESF bus and does not require manning

or start-up of the Parr hydro unit. No credit was provided in the analysis for start-up and operation of

the Parr hydro unit as an alternate source of electrical power. In addition, the SPAR model was also

modified to account for the ability of both the A and B-train emergency auxiliary transformers (XTF-31

and XTF-4) to supply offsite power to both ESF buses.

2.

The approach discussed in Section 2.5 of the RASP manual was used to evaluate the condition

exposure time. The run history of the EDG prior to the failure in November 2022 was used to

determine the number of intervals of accumulated operation of the EDG for the 24-hour PRA mission

time (condition inception time unknown but the vibration-induced degradation of the fuel line was

assumed to progress during operation of the EDG). The final time interval includes the EDG repair

time after the leak was identified. The table below summarizes the intervals that were used for the

analysis.

Date

Interval

Exposure

Period (days)

Interval Run

Time (hrs)

Cumulative Run

(hrs)

Time to

Failure (hrs)

5/24/22 11:05 PM

-

-

5.0

5.0

24.0

6/14/22 11:15 PM

21

2.0

7.0

19.0

7/12/22 11:39 PM

28

1.0

8.0

17.0

8/17/22 12:00 AM

35

3.0

11.0

16.0

9/6/22 11:19 PM

21

2.0

13.0

13.0

10/5/22 12:26 AM

28

2.0

15.0

11.0

11/2/22 6:31 PM

29

9.0

24.0

9.0

The fault tree logic for the A-train EDG was modified to split the fail-to-run (FTR) basic event into two

separate components so that adjustments could be made to credit EDG operation prior to failure. The

SAPHIRE convolution mapping tool was then used to update model convolution events using the new

fault tree logic.

For the conditional case the model was adjusted using change set 1AEXT_EDG_FTR which set event

EPS-DGN-FR-1A to TRUE so that the FTR common cause change would be calculated by SAPHIRE.

The change set also set the new basic event EPS-DGN-FR-1AEXT to 1.0 so the failure would show up in

cutsets for post-processing adjustment made for credited EDG run time.

For each time interval the mission time for basic events EPS-DGN-FR-1AT2 and EPS-DGN-FR-1AEXT

were adjusted to reflect the estimated run time before failure and each time interval also included ET

post-processing to look for A EDG FTR basic event EPS-DGN-FR-1AEXT in the cutsets and substitute

the appropriate recovery terms based on credited EDG operation. The following table shows the mission

time adjustments made to EPS-DGN-FR-1AT2 and EPS-DGN-FR-1AEXT for each time interval.

Interval

Exposure

Period (days)

Time to

Failure (hrs)

EPS-DGN-FR-1AT2

Mission Time (hrs)

EPS-DGN-FR-1AEXT

Mission Time (hrs)

21

18

2

17

7

35

15

4

13

11

28

10

6

9

15

3.

A conditional case was performed for every interval bin and the results were summed to determine

the overall risk estimate.

4.

Basic events were adjusted in the base SPAR model to enable FLEX sequences and account for

best estimate reliability of FLEX equipment using industry failure data at a 24-hour mission time.

Based on the unavailability of industry reliability data for load-run basic events, the model was

adjusted to ignore those failures. A sensitivity case will also be performed giving no credit for FLEX

mitigation of the performance deficiency. These adjusted values were used for both the nominal and

conditional case as the performance deficiency did not impact FLEX strategies.

5.

Two new Human Error Probability (HEP) basic events were created to model operator actions to

recover offsite power supplies. The first HEP (ACP-XHE-XM-PARRHYDRO) estimates the failure to

manually align the 13.8 kV offsite source from Parr hydro switchyard to either the A-or B-train 7.2 kV

ESF bus. The second HEP (ACP-XHE-XA-ALT1DA(B)) estimates the failure to manually align either

XTF-31 to the B-and A-train ESF buses or XTF-4 to the A-and B-train ESF buses. Development of

the HEPs was documented using SPAR-H worksheets.

ACP-XHE-XM-PARRHYDRO = 4.4E-02

ACP-XHE-XA-ALT1DA(B) = 5.40E-03

6.

SAPHIRE condition assessments were performed using the event tree direct solve method where

cutset results were gathered for sequences other than internal events. Conditional case change set

1AEXT_EDG_FTR was used to evaluate the change in risk that could be attributed to the EDG

failure for each time interval being evaluated over the 162-day exposure period.

Change Set 1AEXT_EDG_FTR (shown for interval 1)

Basic Event

Nominal

Conditional

EPS-DGN-FR-1A

2.68E-02

TRUE

EPS-DGN-FR-1AEXT

5.88E-03

1.0

7.

SAPHIRE condition assessments were also performed using the ECA module to generate dominant

sequence and cutset reports. Conditional case change set 1AEXT_EDG_FTR_ECA was used in the

condition assessments.

Change Set 1AEXT_EDG_FTR_ECA (shown for interval 1)

Basic Event

Nominal

Conditional

EPS-DGN-FR-1A

2.68E-02

TRUE

EPS-DGN-FR-1AEXT

5.88E-03

1.0

EPS-DGN-FR-1AT2

2.10E-02

2.10E-02

EPS-DGN-TM-1A

1.51E-02

1.51E-02

CALCULATIONS

Best Estimate:

Interval

Exposure

(days)

Fire

Delta-CDP

Internal

Events

Delta-CDP

High Wind

Delta-CDP

Seismic

Delta-CDP

Tornado

Delta-CDP

Internal

Flooding

Delta-CDP

21

3.81E-06

1.18E-07

9.20E-08

5.75E-09

3.07E-10

5.81E-12

28

4.78E-06

8.67E-08

8.04E-08

7.67E-09

4.09E-10

4.76E-12

35

5.97E-06

1.11E-07

1.03E-07

9.59E-09

5.11E-10

6.14E-12

21

3.59E-06

7.19E-08

6.73E-08

5.75E-09

3.06E-10

3.74E-12

28

4.79E-06

1.00E-07

9.47E-08

7.67E-09

4.07E-10

5.75E-12

29

5.05E-06

1.10E-07

1.04E-07

7.95E-09

4.22E-10

5.96E-12

Total

162

2.80E-05

5.98E-07

5.41E-07

4.44E-08

2.36E-09

3.22E-11

SAPHIRE condition assessments were performed using the direct solve method and conditional case

change set 1AEXT_EDG_FTR. The overall estimated increase in risk was a delta core damage

probability (delta-CDP) of 2.92E-05. FIRE sequences were determined to be strongly dominant in the

results with INTERNAL EVENTS and HIGH WINDS also significant sequence contributors. SAPHIRE

ECA condition assessments were performed to generate dominant sequence and cutset reports.

Dominant FIRE cutsets were associated with fire initiating events in the 1DB switchgear room, station

transformer area, and turbine building. These fire initiators result in a plant transient with either fire

damage impacting B-train power or random failure/unavailability of the B EDG accompanied by the

inability to restore power from the 13.8 kV source and operator failure to control the Turbine Driven

Essential Feedwater (TDEFW) pump following battery depletion.

Dominant INTERNAL EVENT and HIGH WIND cutsets were associated with weather-related loss of

offsite power with failure to align the 13.8 kV source accompanied by random failures of the B EDG and

FLEX DG and failure to recover offsite power sources.

Sensitivity 1 - No Time Intervals

To explore the sensitivity of the analysis results due to application of the run-time treatment of exposure

time, this sensitivity will determine the estimated increase in risk-based on the full exposure period

without the use of time intervals or post-processing to adjust power recovery terms.

SAPHIRE condition assessments were performed using the direct solve method and conditional case

change set 1AEXT_EDG_FTR for the full 162-day exposure period.

Exposure

(days)

Fire

Delta-CDP

Internal

Events

Delta-CDP

High Wind

Delta-CDP

Seismic

Delta-CDP

Tornado

Delta-CDP

Internal

Flooding

Delta-CDP

162

3.87E-05

1.92E-06

1.45E-06

4.44E-08

2.33E-09

1.22E-10

The overall estimated increase in risk was a delta-CDP of 4.22E-05.

As expected, the sensitivity results were higher without consideration of the run history of the A EDG or

consideration for the increased time that would have been available to potentially recover power sources

for the affected ESF bus. The higher estimate would not have been sufficient to alter the overall

conclusions of the analysis. The use of the run-time failure methodology was determined to be the most

appropriate treatment of exposure time for the analysis.

Sensitivity 2 - Increase Parr Switchyard Alignment Human Error Probability (HEP)

To evaluate the sensitivity of analysis results with respect to operator actions for alignment of the Parr

hydro 13.8 kV offsite power supply, the basic event for operator failure (ACP-XHE-XM-PARRHYDRO)

was increased by a factor of 2x for both the nominal and conditional cases.

ACP-XHE-XM-PARRHYDRO = 8.8E-02

SAPHIRE direct solve condition assessments were performed with conditional change set

1AEXT_EDG_FTR. Dominant event sequences FIRE, INTERNAL EVENTS, and HIGH WIND were

utilized for the sensitivity.

Interval

Exposure (days)

Fire

Delta-CDP

Internal Events

Delta-CDP

High Wind

Delta-CDP

21

7.53E-06

2.35E-07

1.85E-07

28

9.52E-06

1.71E-07

1.60E-07

35

1.19E-05

2.21E-07

2.07E-07

21

7.15E-06

1.42E-07

1.34E-07

28

9.63E-06

1.99E-07

1.88E-07

29

1.01E-05

2.18E-07

2.06E-07

Total

162

5.58E-05

1.19E-06

1.08E-06

The overall estimated increase in risk was a delta-CDP of 5.81E-05.

The analyst noted that the analysis results were strongly sensitive to consideration of operator actions to

align the Parr hydro 13.8 kV power supply to the B-train ESF bus. This sensitivity was consistent with the

number of SPAR model dominant cutsets containing that basic event. The sensitivity demonstrated that

increasing the HEP by a factor of two approximately doubled the estimated increase in risk but would not

have altered the overall conclusions of the analysis. Additionally, the analyst noted that given the

proportional impact on the analysis results, reducing the HEP by half would also not be expected to lower

the risk estimate enough to change the overall analysis conclusions.

Sensitivity 3 - No FLEX

To evaluate the sensitivity of analysis results with respect to crediting of FLEX mitigation strategies, the

basic event for operator failure to enter extended loss of AC power procedures was set to 1.0 for both the

nominal and conditional cases.

FLX-XHE-XE-ELAP = 1.0

SAPHIRE direct solve condition assessments were performed with conditional change set

1AEXT_EDG_FTR. Dominant event sequences FIRE, INTERNAL EVENTS, and HIGH WIND were

utilized for the sensitivity.

Interval

Exposure (days)

Fire

Delta-CDP

Internal Events

Delta-CDP

High Wind

Delta-CDP

21

3.75E-06

1.15E-07

1.23E-07

28

5.01E-06

1.78E-07

1.91E-07

35

6.26E-06

2.38E-07

2.52E-07

21

3.83E-06

1.57E-07

1.67E-07

28

5.11E-06

2.22E-07

2.36E-07

29

5.38E-06

2.46E-07

2.60E-07

Total

162

2.93E-05

1.16E-06

1.23E-06

The overall estimated increase in risk was a delta-CDP of 3.17E-05.

FLEX mitigation of the finding was not a strongly influential factor in the analysis results. This was

primarily due to the top SPAR cutsets involving Station Blackout (SBO) sequences accompanied by early

failure of the TDEFW pump. Under these conditions core damage can occur quickly and there would not

be sufficient time to implement the phase two FLEX strategies. Although not a strongly influential factor,

inclusion of FLEX mitigation was determined to be most appropriate to the circumstances and was

considered in the best estimate case.

Sensitivity 4 - Probabilistic Safety Analysis (PSA) Values

To assess the sensitivity of the SPAR model analysis results with respect to values used in the licensees

model the following adjustments were made:

Flagset

Basic Event

Description

SPAR

Value

PSA

Value

N/A

ACP-XHE-XM-PARRHYDRO

OPERATOR FAILS TO ALIGN BACKUP

POWER FROM PARR HYDRO

4.40E-02

7.39E-02

N/A

EFW-XHE-XM-CNTRL

OPERATOR FAILS TO OPERATE EFW

TDP AFTER BATTERY DEPLETION

3.00E-01

1.60E-02

FRI-IB2202-T4

EFW-TDP-FR-XPP8

EFW TDP XPP-8 FAILS TO RUN

TRUE

5.93E-02

FRI-IB2202-CMPT-9

EFW-TDP-FR-XPP8

EFW TDP XPP-8 FAILS TO RUN

TRUE

5.93E-02

FRI-YD03-CMPT-10

ACP-XHE-XM-PARRHYDRO

OPERATOR FAILS TO ALIGN BACKUP

POWER FROM PARR HYDRO

4.40E-02

TRUE

The basic events were selected based on their relative importance to dominant SPAR model sequences

and the differences in treatment between the licensees model and the SPAR model. The PSA values for

ACP-XHE-XM-PARRHYDRO and EFW-XHE-XM-CNTRL were used for used for the nominal and

conditional case for the sensitivity. Failure of EFW-TDP-FR-XPP8 was removed from the fire scenarios

for fire area IB2202 where the licensees PSA did not assume fire-induced loss of the pump. Additionally,

ACP-XHE-XM-PARRHYDRO was added to the switchyard fire scenario to account for fire-induced

unavailability of the Parr hydro switchyard power source.

SAPHIRE direct solve condition assessments were performed with conditional change set

1AEXT_EDG_FTR. Dominant event sequences FIRE, INTERNAL EVENTS, and HIGH WIND were

utilized for the sensitivity.

Interval

Exposure (days)

Fire

Delta-CDP

Internal Events

Delta-CDP

High Wind

Delta-CDP

21

4.86E-06

1.91E-07

1.41E-07

28

5.87E-06

1.10E-07

9.78E-08

35

7.34E-06

1.40E-07

1.26E-07

21

4.41E-06

8.98E-08

8.11E-08

28

5.88E-06

1.24E-07

1.13E-07

29

6.17E-06

1.35E-07

1.24E-07

Total

162

3.45E-05

7.90E-07

6.83E-07

The overall estimated increase in risk was a delta-CDP of 3.60E-05.

For the basic events being evaluated, the difference in treatment between the SPAR model and the

licensees model were not strongly influential in the analysis results. Overall, the sensitivity was higher

than the best estimate case but did not alter the resulting conclusions. The most influential factor

appears to be the value used for ACP-XHE-XM-PARRHYDRO which is addressed in Sensitivity 2 of the

evaluation.

LICENSEE EVALUATION

During the development of this detailed risk evaluation, discussions with the licensee indicated

preliminary risk estimates from the licensees risk model were consistent with NRC SPAR model results

with FIRE sequences strongly dominant in the lower portion of the E-05 range. Although the licensees

model or record does not include FLEX equipment, the top cutsets also involved SBO sequences

accompanied by failure of the TDEFW pump which would normally not include credit for FLEX mitigation.

The licensee was developing an analysis to determine if enough decay heat would be removed prior to

the expected run-time failure of the A-train EDG to allow implementation of Phase 2 FLEX strategies to

restore the heat removal function prior to core damage. The licensees evaluation was not completed at

the time of this detailed risk evaluation. A qualitative review of SPAR model cutsets for the top FIRE

sequences indicate that FLEX credit under those conditions had the potential to reduce the estimated

risk of the condition.

DELTA-CDF FOR EXPOSURE TIME

The overall results are summarized below:

EVENT SEQUENCE

Best

Estimate

Sensitivity #1

No Intervals

Sensitivity #2

SWYD HEP 2x

Sensitivity #3

No FLEX

Sensitivity #4

PSA Values

FIRE

2.80E-05

3.87E-05

5.58E-05

2.93E-05

3.45E-05

INTERNAL EVENTS

5.98E-07

1.92E-06

1.19E-06

1.16E-06

7.90E-07

HIGH WINDS

5.41E-07

1.45E-06

1.08E-06

1.23E-06

6.83E-07

SEISMIC

4.44E-08

4.44E-08

-

-

-

TORNADO

2.36E-09

2.33E-09

-

-

-

INTERNAL FLOODING

3.22E-11

1.22E-10

-

-

-

TOTAL

2.92E-05

4.22E-05

5.81E-05

3.17E-05

3.60E-05

Considering that SAPHIRE calculates the difference in core damage probability over a given exposure

time, and that changes in CDF over the same period are numerically equivalent, the change in CDF due

to the finding would be on the order of 2.92E-05/year.

EXTERNAL EVENTS CONSIDERATIONS

Internal event estimates were greater than 1E-07, therefore external events were discussed and

estimated in this risk evaluation. FIRE and HIGH WINDS event sequences were determined to be

significant contributors to the overall estimated risk and were included in sensitivity evaluations with

INTERNAL EVENTS.

LARGE EARLY RELEASE FREQUENCY IMPACT

The finding was evaluated in accordance with IMC 0609, Appendix H, Containment Integrity Significance

Determination Process, as a Type A finding. Although the estimated delta-CDF was greater than 1E-

07/year, the dominant accident sequences did not involve steam generator tube rupture or interfacing

system Loss of Coolant Accidents. Therefore, the issue associated with failure of the A-train EDG would

not be expected to be a significant contributor to an increase in large early release frequency (delta-

LERF) risk in comparison to the delta-CDF risk. Delta-CDF was determined to be the risk metric of

interest for this evaluation.

CONCLUSIONS/RECOMMENDATIONS

The preliminary estimated risk increase (delta-CDF) over the nominal case for the inoperability of the A-

train EDG was 2.92E-05/year, which should be preliminarily considered a finding of substantial (Yellow)

significance.