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Category:Letter
MONTHYEARML23304A1422024-02-0101 February 2024 Issuance of Environmental Scoping Summary Report Associated with the U.S. Nuclear Regulatory Commission Staffs Review of the Oconee Nuclear Station, Units 1, 2, & 3, Subsequent License Renewal Application ML24005A2492024-01-24024 January 2024 Exemption from Select Requirements of 10 CFR Part 73 (Security Notifications, Reports, and Recordkeeping and Suspicious Activity Reporting) IR 05000269/20243012024-01-11011 January 2024 Notification of Licensed Operator Initial Examination 05000269/2024301, 05000270/2024301, and 05000287/2024301 ML23331A7982023-12-14014 December 2023 Review of the Fall 2022 Steam Generator Tube Inspection Report (01R32) ML23262A9672023-12-13013 December 2023 Alternative to Use RR-22-0174, Risk-Informed Categorization and Treatment for Repair/Replacement Activities in Class 2 and 3 Systems Section XI, Division 1 ML23317A3462023-11-14014 November 2023 Duke Fleet - Correction Letter to License Amendment Nos. 312 & 340 Issuance of Amendments Regarding the Adoption of Technical Specifications Task Force Traveler TSTF-554, Revision 1 IR 05000269/20230032023-11-14014 November 2023 Integrated Inspection Report 05000269/2023003, 05000270/2023003, and 05000287/2023003; and IR 07200040/2023001; and Exercise of Enforcement Discretion ML23219A1402023-10-10010 October 2023 Audit Report Proposed Alternative to Use ASME Code Case N-752, Risk Informed Categorization and Treatment for Repair/Replacement Activities in Class 2 and 3 Systems XI, Division 1 ML23269A1102023-10-0606 October 2023 Letter to Steven Snider-Revised Schedule for the Environmental Review of the Oconee Nuclear Station, Unit 1, 2, and 3, Subsequent License Renewal Application ML23256A0882023-09-25025 September 2023 Issuance of Alternative to Steam Generator Welds ML23195A0782023-08-29029 August 2023 Issuance of Amendments Regarding the Adoption of Technical Specifications Task Force Traveler TSTF-554, Revision 1 IR 05000269/20230112023-08-25025 August 2023 Comprehensive Engineering Team Inspection Report 05000269/2023011 and 05000270/2023011 and 05000287/2023011 IR 05000269/20230052023-08-25025 August 2023 Updated Inspection Plan for Oconee Nuclear Station Units 1, 2 and 3 (Report 05000269/2023005, 05000270/2023005, and 05000287/2023005) IR 05000269/20230022023-07-28028 July 2023 Integrated Inspection Report 05000269/2023002, 05000270/2023002 and 05000287/2023002 ML23208A0972023-07-27027 July 2023 Subsequent License Renewal List of Threatened and Endangered Species That May Occur in Your Proposed Project Location or May Be Affected IR 05000269/20230102023-07-19019 July 2023 Biennial Problem Identification and Resolution Inspection Report 05000269/2023010 and 05000270/2023010 and 05000287/2023010 and Notice of Violation ML23178A0682023-07-0303 July 2023 Audit Plan Proposed Alternative to Use ASME Code Case N-752, Risk-Informed Categorization and Treatment for Repair/Replacement Activities in Class 2 & 3 Systems Section XI, Division 1 ML23132A2392023-06-0101 June 2023 Summary of the April 2023 Remote Environmental Audit Related to the Review of the Subsequent License Renewal Application ML23144A0192023-05-25025 May 2023 Review of the Spring 2022 Steam Generator Tube Inspection Report (O3R31) IR 05000269/20230012023-05-12012 May 2023 Integrated Inspection Report 05000269/2023001 and 05000270/2023001 and 05000287/2023001 ML23121A0552023-05-0303 May 2023 Acknowledgement of Withdrawal Request to Revise TS 5.5.2 Containment Leakage Rate Testing Program ML23118A0762023-05-0101 May 2023 Approval for Use of Specific Provision of a Later Edition of the American Society of Mechanical Engineers Boiler and Pressure Vessel Code, Section XI ML23117A0432023-04-20020 April 2023 Framatome, Inc., Part 21 Notification of Existence of a Defect ML23075A0732023-04-0505 April 2023 License Renewal Regulatory Audit Regarding the Environmental Review of the Subsequent License Renewal Application Supplement (EPID Number L-2021-SLE-0002) ML23045A1332023-03-15015 March 2023 Request for Scoping Comments Concerning the Supplemental Environmental Review of Oconee Nuclear Station, Units 1, 2, and 3, Subsequent License Renewal Application - Achp Letter ML23045A1402023-03-15015 March 2023 Request for Scoping Comments Concerning the Supplemental Environmental Review of Oconee Nuclear Station, Units 1, 2, and 3, Subsequent License Renewal Application - Shpo Letter ML23045A1432023-03-15015 March 2023 Request for Scoping Comments Concerning the Supplemental Environmental Review of Oconee Nuclear Station, Units 1, 2, and 3, Subsequent License Renewal Application - State Tribe Letter ML22332A4932023-03-10010 March 2023 William States Lee III 1 and 2 - Issuance of Amendments Regarding the Relocation of the Emergency Operations Facility ML23069A1102023-03-10010 March 2023 Notification of Inspection and Request for Information for NRC Problem Identification and Resolution Inspection ML23061A1772023-03-0303 March 2023 Notification of Oconee Nuclear Station Comprehensive Engineering Team Inspection - NRC Inspection Report 05000269/2023011, 05000270/2023011 and 05000287/2023011 IR 05000269/20220062023-03-0101 March 2023 Annual Assessment Letter for Oconee Nuclear Nuclear Station, Units 1, 2 and 3 (NRC Inspection Report 05000269/2022006, 05000270/2022006, and 05000287/2022006) ML23039A1632023-02-0808 February 2023 Requalification Program Inspection ML23037A0772023-02-0606 February 2023 402 Cyber Notification and RFI Letter Final IR 05000269/20220042023-02-0202 February 2023 Integrated Inspection Report 05000269 2022004 and 05000270/2022004 and 05000287/2022004 ML22363A3942023-01-12012 January 2023 Subsequent License Renewal Environmental Report Supplement - Proposed Review Schedule ML22356A0512022-12-14014 December 2022 Curtiss-Wright Nuclear Division, Letter Regarding Potential Efect in a Configuration of the 11/2 Inch Quick Disconnect Connector Cable Assemblies Supplied to Duke Energy (See Attached Spreadsheet) for a Total of 460 of Connectors Only Suppl ML22321A0492022-12-0808 December 2022 Issuance of Amendment Nos. 426, 428 and 427, Additional Mode Change Limitations Applicable to the Adoption of TSTF- 359, Revision 9, Increase Flexibility in Mode Restraints ML22329A1042022-11-29029 November 2022 Review of the Fall 2021 Steam Generator Tube Inspection Report ML22321A1582022-11-22022 November 2022 Summary of Conference Call Regarding the Fall 2022 Steam Generator Tube Inspections ML22096A0032022-11-18018 November 2022 McGuire Nuclear Station and Shearon Harris Nuclear Power Plant Authorization of RA-19-0352 Regarding Use of Alternative for RPV Head Closure Stud Examinations ML22256A2532022-11-14014 November 2022 Issuance of Amendments Regarding the Adoption of Technical Specifications Task Force Traveler TSTF-541, Rev. 2 IR 05000269/20220032022-11-0707 November 2022 Integrated Inspection Station 05000269/2022003 and 05000270/2022003 and 05000287/2022003 ML22301A0112022-11-0303 November 2022 Request for Withholding Information from Public Disclosure Regarding the SLR Application - September 2, 2022 ML22298A0752022-10-27027 October 2022 Request for Withholding Information from Public Disclosure Regarding the Subsequent License Renewal Application Duke Energy Letter Dated July 25, 2022 ML22264A0322022-10-20020 October 2022 _Request for Withholding Information from Public Disclosure Regarding the Subsequent License Renewal Application - Duke Energy Letter Dated July 8, 2022 IR 05000269/20220112022-09-26026 September 2022 NRC Inspection Report 05000269/2022011 and 05000270/2022011 and 05000287/2022011 ML22258A0302022-09-15015 September 2022 Evacuation Time Estimate Reports ML22222A0072022-09-14014 September 2022 Request for Withholding Information from Public Disclosure Regarding the Subsequent License Renewal Application ML22231B1362022-09-0101 September 2022 Review of the Draft Environmental Assessment and Findings of No Significant Impact for Catawba Nuclear Station, H.B. Robinson Steam Electric Plant, and Oconee Nuclear Station Independent Spent Fuel Storage Installation Decommissioning Fundi ML22234A0062022-08-30030 August 2022 SLRA - Closed Public Meeting Summary - August 18, 2022 2024-02-01
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November 22, 2022 Mr. Steven M. Snider Site Vice President, Oconee Nuclear Station Duke Energy Carolinas, LLC Oconee Nuclear Station 7800 Rochester Highway Seneca, SC 29672-0752
SUBJECT:
OCONEE NUCLEAR STATION, UNIT 1
SUMMARY
OF CONFERENCE CALL REGARDING THE FALL 2022 STEAM GENERATOR TUBE INSPECTIONS (RFO 32) (EPID L-2022-NFO-0010)
Dear Mr. Snider:
On November 8, 2022, the U.S. Nuclear Regulatory Commission staff participated in a conference call with representatives of Duke Energy Carolinas, LLC, regarding the ongoing steam generator tube inspection activities at Oconee Nuclear Station, Unit 1.
A summary of the conference call is provided in the enclosure.
If you have any questions, please call me at 301-415-1009, or by email at Shawn.Williams@nrc.gov.
Sincerely,
/RA/
Shawn A. Williams, Senior Project Manager Plant Licensing Branch II-1 Division of Operating Reactor Licensing Office of Nuclear Reactor Regulation Docket No. 50-269
Enclosure:
Conference Call Summary cc: Listserv
SUMMARY
OF CONFERENCE CALL OCONEE NUCLEAR STATION, UNIT 1 FALL 2022 STEAM GENERATOR TUBE INSPECTIONS (RFO 32)
DOCKET NO. 50-269 On November 8, 2022, the U.S. Nuclear Regulatory Commission (NRC) staff, including the Corrosion and Steam Generator Branch (NCSG) of the Division of New and Renewed Licenses, participated in a conference call with Duke Energy Carolinas, LLC (the licensee), regarding the ongoing steam generator (SG) tube inspection activities at Oconee Nuclear Station, Unit 1 (Oconee, Unit 1), during refueling outage (RFO) 32.
Oconee, Unit 1, has two replacement once-through SGs designed and fabricated by Babcock and Wilcox International. Each SG has 15,631 thermally treated Alloy 690 tubes with a nominal outside diameter of 0.625 inches and a nominal wall thickness of 0.038 inches. The tubes were hydraulically expanded for 13 inches from the tube end into the 22-inch thick tubesheets. Tube support is provided by 15 stainless steel horizontal tube support plates (TSPs) with trifoil broached openings. Some of the periphery tube support openings in the 14th TSP are drilled holes.
The NRC staff notes that the inspection information provided during the call is preliminary and subject to change upon final data analysis. The discussion points are below:
At the time of the call eddy current acquisition and analysis, inspections were approximately 99 percent complete in SG A and approximately 95 percent complete in SG B.
The eddy current inspection scope for each SG included:
o A 100 percent full length bobbin probe examination of all in-service tubes.
o Array probe inspection five tubes deep on the periphery up to the first TSP.
o Array probe special interest inspections, for characterizing the deeper wear indications and drilled hole indications and for validating projections from the operational assessment.
Other inspections included:
o Foreign object search and retrieval (FOSAR) in both SGs o Visual inspection of the primary inlet and outlet bowls Enclosure
At the time of the call, the licensee had identified the following:
o Wear from TSPs was the only new degradation since the previous inspection in 2020. The new TSP wear was at existing wear indications. There were no new foreign object (FO) wear indications or changes at existing FO wear indications.
o There were 15,468 indications of TSP wear in 7,076 tubes in SG A, and 10,792 indications of TSP wear in 5,628 tubes in SG B.
o The maximum measured wear depth of 49 percent through-wall (TW) was on a tube with a measured wear depth of 37 percent TW in RFO 31 in 2020.
o There were 28 TSP wear indications in SG A and 14 TSP wear indications in SG B with measured depths of 40 percent TW or higher.
o In SG A, FOSAR found 10 metallic gasket pieces and one piece of metallic wire. All were removed. In SG B, FOSAR found three metallic gasket pieces. Two were removed. Objects left in place were evaluated for their potential to cause tube wear.
At the time of the call, all indications met the condition monitoring limits for demonstrating tube integrity is maintained. No in-situ pressure tests had been performed and none were planned. No tubes were being pulled.
In response to a question from the NRC staff about the amount of deposit on the secondary side, the licensee provided the amount of iron transported to the SGs. [Iron transport to SGs is in the form of dissolved and particulate iron in the feedwater that can deposit in the SGs.] For Cycle 32, approximately 325 pounds of iron were transported to the SGs. Approximately 2,898 pounds of iron had been transported to the SGs since they were placed into operation.
The number of tubes identified for plugging was 27 in SG A and 14 in SG B. All of these were being plugged due to TSP wear of 40 percent TW or greater.
The NRC staff did not identify any issues that required follow-up action at this time.
Steam Generator Inspection Call Attendees NRC Duke Energy Framatome Shawn Williams Jordan Vaughan Craig Kelly Gregory Makar Etienne Fonteneau Paul Klein Dan Mayes Binoy Desai Tim Thulien Nick Smalley Marie Turner Jared Nadel Adam Ruh
ML22321A158 OFFICE NRR/DORL/LPL2-1/PM NRR/DORL/LPL2-1/LA NRR/DNRL/NCSGB/BC NAME SWilliams KGoldstein (KEntz for) SBloom DATE 11/21/2022 11/21/2022 11/17/2022 OFFICE NRR/DORL/LPL2-1/BC NRR/DORL/LPL2-1/PM NAME MMarkley SWilliams DATE 11/22/2022 11/22/2022