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Category:MONTHLY OPERATING ANALYSIS REPORT
MONTHYEARML20217D5441999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Davis-Besse Nuclear Power Station.With ML20211R0811999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20210Q8541999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20209E6231999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20195F4871999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20206M6341999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Davis-Besse Nuclear Station,Unit 1.With ML20205M2931999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Davis-Besse Nuclear Power Station.With ML20207J1461999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20199E2501998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20197J3441998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20195D0001998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20154H5801998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20151W1611998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Dbnps.With ML20237B1681998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20236N7451998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20249A4121998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20236N7501998-04-30030 April 1998 Rev 2 to Monthly Operating Rept for Apr 1998 for Davis-Besse Nuclear Power Station,Unit ML20247F6721998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Davis-Bess Nuclear Power Station,Unit 1 ML20249A4141998-04-30030 April 1998 Revised Monthly Operating Rept for Apr 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20216B4041998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20216C5131998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20202D3721998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20198K7931997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Davis-Besse Nuclear Power Station,Unit 1 ML20203A3931997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Davis-Besse Nuclear Power Plant,Unit 1 ML20198S5371997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Davis-Besse Nuclear Power Station ML20217H7701997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Davis-Besse Nuclear Power Station,Unit 1 ML20216H3261997-08-31031 August 1997 Monthly Operating Rept for August 1997 for DBNPS ML20217K0241997-07-31031 July 1997 Monthly Operating Rept for Jul 1997 for Davis Besse Nuclear Power Station,Unit 1 ML20140H0441997-05-31031 May 1997 Monthly Operating Rept for May 1997 for Davis-Besse Nuclear Power Station Unit 1 ML20141B9521997-04-30030 April 1997 Monthly Operating Rept for Apr 1997 for Davis-Beese Nuclear Power Station Unit 1 ML20137T5271997-03-31031 March 1997 Monthly Operating Rept for Mar 1997 for Davis-Besse Nuclear Power Station,Unit 1 ML20136G7221997-02-28028 February 1997 Monthly Operating Rept for Feb 1997 for Davis-Besse Nuclear Station Unit 1 ML20134L9831997-01-31031 January 1997 Monthly Operating Rept for Jan 1997 for Dbnps,Unit 1. W/Undated Ltr ML20133G0161996-12-31031 December 1996 Monthly Operating Rept for Dec 1996 for Davis-Besse Nuclear Power Station,Unit 1 ML20149M4071996-11-30030 November 1996 Monthly Operating Rept for Nov 1996 for Davis-Besse Nuclear Power Station Unit 1 ML20134P9821996-10-31031 October 1996 Monthly Operating Rept for Oct 1996 for Davis-Besse Nuclear Power Station,Unit 1 ML20128Q0611996-09-30030 September 1996 Monthly Operating Rept for Sept 1996 for Davis-Besse NPP, Unit 1 ML20117D5341996-07-31031 July 1996 Monthly Operating Rept for July 1996 for Davis-Besse Nuclear Power Station,Unit 1 ML20117D5411996-06-30030 June 1996 Revised MOR for June 1996 for Davis-Besse Nuclear Power Station,Unit 1 ML20116E0161996-06-30030 June 1996 Monthly Operating Rept for June 1996 for Davis-Besse Nuclear Station Unit 1 ML20113B9111996-05-31031 May 1996 Monthly Operating Rept for May 1996 for Davis-Beese Nuclear Power Station Unit 1 ML20117H7231996-04-30030 April 1996 Monthly Operating Rept for Apr 1996 for Davis-Besse Unit 1 ML20112E6061996-03-31031 March 1996 Monthly Operating Rept for Mar 1996 for David-Besse Nuclear Power Station,Unit 1 ML20101G5251996-02-29029 February 1996 Monthly Operating Rept for Feb 1996 for DBNPS Unit 1 ML20149K7711996-01-31031 January 1996 Monthly Operating Rept for Jan 1996 for Davis-Besse Nuclear Power Station.W/Undated Ltr ML20096C7971995-12-31031 December 1995 Monthly Operating Rept for Dec 1995 for Davis-Besse Nuclear Power Station Unit 1 ML20095H3761995-11-30030 November 1995 Monthly Operating Rept for Nov 1995 for Davis-Besse Nuclear Power Station Unit 1 ML20094L1041995-10-31031 October 1995 Monthly Operating Rept for Oct 1995 for Davis-Besse Nuclear Power Station Unit 1 ML20093J2341995-09-30030 September 1995 Monthly Operating Rept for Sept 1995 for Davis-Besse Nuclear Power Station ML20098A2651995-08-31031 August 1995 Monthly Operating Rept for Aug 1995 for Davis-Besse Nuclear Power Station,Unit 1 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K1231999-10-14014 October 1999 Revised Positions for DBNPS & PNPP QA Program ML20217D5441999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Davis-Besse Nuclear Power Station.With 05000346/LER-1998-011, :on 981014,manual Reactor Trip Occurred.Caused by Component Cooling Water Sys Leak.Breaker Being Installed Into D1 Bus cubicle.AACD1 Was Removed from Cubicle1999-09-0303 September 1999
- on 981014,manual Reactor Trip Occurred.Caused by Component Cooling Water Sys Leak.Breaker Being Installed Into D1 Bus cubicle.AACD1 Was Removed from Cubicle
ML20211R0811999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1999-003, :on 990727,failure to Perform Engineering Evaluation for Pressurizer Cooldown Rate Exceeding TS Limit Was Noted.Caused by Inadequate Procedural Guidance.Provided Required Reading for Operators.With1999-08-26026 August 1999
- on 990727,failure to Perform Engineering Evaluation for Pressurizer Cooldown Rate Exceeding TS Limit Was Noted.Caused by Inadequate Procedural Guidance.Provided Required Reading for Operators.With
ML20211B0271999-08-13013 August 1999 SER Accepting Second 10-year Interval Inservice Insp Requests for Relief RR-A16,RR-A17 & RR-B9 for Plant, Unit 1 ML20210Q8541999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20209E6231999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1998-013, :on 981105,safety Valve Rupture Disks May Induce Excessive Eccentric Loading of Pressurizer Vessel Nozzles.Caused by Failure of RCS Pressure Boundary.Plant Mod Was Implemented in May of 1999.With1999-06-24024 June 1999
- on 981105,safety Valve Rupture Disks May Induce Excessive Eccentric Loading of Pressurizer Vessel Nozzles.Caused by Failure of RCS Pressure Boundary.Plant Mod Was Implemented in May of 1999.With
ML20212H9961999-06-22022 June 1999 Safety Evaluation Supporting Amend 233 to License NPF-3 ML20195K2871999-06-16016 June 1999 Safety Evaluation Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20207G6661999-06-0808 June 1999 Safety Evaluation Supporting Amend 232 to License NPF-3 ML20195F4871999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20206U7371999-05-19019 May 1999 Safety Evaluation Supporting Amend 231 to License NPF-3 ML20207E8011999-05-19019 May 1999 Non-proprietary Rev 2 to HI-981933, Design & Licensing Rept DBNPS Unit 1 Cask Pit Rack Installation Project ML20207F4351999-05-0404 May 1999 Rev 1 to DBNPS Emergency Preparedness Evaluated Exercise Manual 990504 ML20206M6341999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Davis-Besse Nuclear Station,Unit 1.With ML20205M2931999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Davis-Besse Nuclear Power Station.With 05000346/LER-1999-002, :on 990208,both Trains of Emergency Ventilation Sys Were Rendered Inoperable.Caused by Unattended Open Door. Door Was Immediately Closed Upon Discovery.With1999-03-0505 March 1999
- on 990208,both Trains of Emergency Ventilation Sys Were Rendered Inoperable.Caused by Unattended Open Door. Door Was Immediately Closed Upon Discovery.With
ML20207J1461999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20206U2441999-02-0909 February 1999 Safety Evaluation Supporting Amend 229 to License NPF-3 ML20199H5931999-01-20020 January 1999 Safety Evaluation Accepting Thermo-Lag Re Ampacity Derating Issues for Plant ML20204J6751998-12-31031 December 1998 1998 Annual Rept for Dbnps,Unit 1,PNPP,Unit 1 & BVPS Units 1 & 2 ML20199E2501998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20205K5781998-12-31031 December 1998 Waterhammer Phenomena in Containment Air Cooler Swss ML20206B0101998-12-31031 December 1998 1998 Annual Rept for Firstenergy Corp, for Perry Nuclear Power Plant & Davis-Besse Nuclear Power Station.Form 10-K Annual Rept to Us Securities & Exchange Commission for Fiscal Yr Ending 981231,encl ML20197J3441998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1998-012, :on 981018,reactor Trip Occurred from Approx 4% Power Due to ARTS Signal.Caused by Inadequate Design Drawing Resulting in Inadequate Procedure.Procedure Revised to Correct Deficiency.With1998-11-17017 November 1998
- on 981018,reactor Trip Occurred from Approx 4% Power Due to ARTS Signal.Caused by Inadequate Design Drawing Resulting in Inadequate Procedure.Procedure Revised to Correct Deficiency.With
05000346/LER-1998-009, :on 980909,RCS Pressurizer Spray Valve Was Not Functional with Two of Eight Body to Bonnet Nuts Missing. Caused by Less than Adequate Matl Separation Work Practices. Bonnet Nuts Replaced.With1998-11-13013 November 1998
- on 980909,RCS Pressurizer Spray Valve Was Not Functional with Two of Eight Body to Bonnet Nuts Missing. Caused by Less than Adequate Matl Separation Work Practices. Bonnet Nuts Replaced.With
05000346/LER-1998-011, :on 981014,manual RT Due to Ccws Leak Was Noted.Caused by Failure of One Letdown Cooler Rupture Disk. All Letdown Cooler Rupture Disks Were Replaced Prior to Plant Restart.With1998-11-13013 November 1998
- on 981014,manual RT Due to Ccws Leak Was Noted.Caused by Failure of One Letdown Cooler Rupture Disk. All Letdown Cooler Rupture Disks Were Replaced Prior to Plant Restart.With
ML20195D0001998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20155B6781998-10-28028 October 1998 Safety Evaluation Accepting Proposed Reduction in Commitment Changes in QA Program Matl Receipt Insp Process 05000346/LER-1998-010, :on 980924,manual Reactor Trip Was Noted.Caused by Misdiagnosed Failure of Main FW Control Valve Solenoid Valve.Faulty Solenoid valve,SVSP6B1,was Replaced & Tested. with1998-10-26026 October 1998
- on 980924,manual Reactor Trip Was Noted.Caused by Misdiagnosed Failure of Main FW Control Valve Solenoid Valve.Faulty Solenoid valve,SVSP6B1,was Replaced & Tested. with
05000346/LER-1998-008, :on 981001,documented Proceduralized Guidance for Initiation of Post LOCA B Dilution Flow Path.Caused by Design Analysis Oversight.Revised Procedures to Provide Active B Dilution Flow Path Guidance.With1998-10-0101 October 1998
- on 981001,documented Proceduralized Guidance for Initiation of Post LOCA B Dilution Flow Path.Caused by Design Analysis Oversight.Revised Procedures to Provide Active B Dilution Flow Path Guidance.With
ML20154H5801998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1998-007, :on 980824,CR Humidifier Ductwork Failure Caused Excessive Opening in Positive Pressure Boundary. Caused by Less than Adequate Fabrication.Evaluation of CR Humidifiers Conducted.With1998-09-22022 September 1998
- on 980824,CR Humidifier Ductwork Failure Caused Excessive Opening in Positive Pressure Boundary. Caused by Less than Adequate Fabrication.Evaluation of CR Humidifiers Conducted.With
ML20151W1611998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Dbnps.With 05000346/LER-1998-006, :on 980624,loss of Offsite Power Was Noted. Caused by Tornado Damage to Switchyard.Tested & Repaired Affected Electrical & Mechanical Equipment Necessary to Restore Two Offsite Power Sources1998-08-21021 August 1998
- on 980624,loss of Offsite Power Was Noted. Caused by Tornado Damage to Switchyard.Tested & Repaired Affected Electrical & Mechanical Equipment Necessary to Restore Two Offsite Power Sources
ML20237E3171998-08-21021 August 1998 ISI Summary Rept of Eleventh Refueling Outage Activities for Davis-Besse Nuclear Power Station ML20237B1681998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20236U5011998-07-23023 July 1998 Special Rept:On 980624,Unit 1 Site Damaged by Tornado & High Winds.Alert Declared by DBNPS Staff,Dbnps Emergency Response Facilities Activiated & Special Insp Team Deployed to Site by Nrc,As Result of Event ML20236R1441998-07-15015 July 1998 SER Related to Quality Assurance Program Description Changes for Davis-Besse Nuclear Power Station,Unit 1 05000346/LER-1998-004, :on 980601,ductwork for Number 2 Control Room Humidifier Found Disconnected from Humidifier.Caused by Less than Adequate Connection at Humidifier Blower Housing. Ductwork Repaired1998-07-13013 July 1998
- on 980601,ductwork for Number 2 Control Room Humidifier Found Disconnected from Humidifier.Caused by Less than Adequate Connection at Humidifier Blower Housing. Ductwork Repaired
05000346/LER-1998-005, :on 980601,both Low Pressure Injection/Dhr Pumps Were Rendered Inoperable During Testing.Caused by Inadequate Self Checking,Communication & Procedure Usage Work Practices.Operations Mgt Reviewed Expectations1998-07-11011 July 1998
- on 980601,both Low Pressure Injection/Dhr Pumps Were Rendered Inoperable During Testing.Caused by Inadequate Self Checking,Communication & Procedure Usage Work Practices.Operations Mgt Reviewed Expectations
ML20236M9411998-07-0707 July 1998 Safety Evaluation Supporting Amend 225 to License NPF-3 ML20236K3981998-06-30030 June 1998 SER Accepting in Part & Denying in Part Relief Requests from Some of ASME Section XI Requirements as Endorsed by 10CFR50.55a for Containment Insp for Davis-Besse Nuclear Power Station,Unit 1 ML20236N7451998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20236K4321998-06-30030 June 1998 Safety Evaluation Supporting Amend 224 to License NPF-03 ML20236K5131998-06-29029 June 1998 Safety Evaluation Accepting Proposed Alternate Emergency Operations Facility Location for Davis-Besse Nuclear Power Station,Unit 1 05000346/LER-1998-003, :on 980519,Mode 3 Entry Without Completion of Surveillance Requirement Occurred.Caused by Failure of I&C Technicians to Perform Each Sp as Written or Adherence. Revised Procedure1998-06-18018 June 1998
- on 980519,Mode 3 Entry Without Completion of Surveillance Requirement Occurred.Caused by Failure of I&C Technicians to Perform Each Sp as Written or Adherence. Revised Procedure
1999-09-30
[Table view] |
Text
..
AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.
50-346 Davis-Besse Unit 1 UNIT DATE November 10, 1986 COMPLETED BY Morteza Khazrai TELEPHONE (419) 249-5000, Ext. 7290 MONTH DAY AVERAGE DAILY POWER LEVEL DAY AVER AGE DAILY POWER LEVEL (MWe-Net)
(Mwe.Neig 0
0 1
,7 2
n 18 0
3 0
0 39 4
0 20 0
5 0
0 7,
6 0
22 0
7 0
0 23 8
0 0
24 9
0 0
25 10 0
0 26 11 0
0 27 12 0
0 yg 13 0
0 29 14 0
0 30 15 0
3 O
16 0
INSTRUCTIONS On this format. list the average daily unit power leselin MWe Net for each day in the reportina month. Compute to the nearest whole megawatt, (9 /77 )
i 070100
$NOO346 DR A
PDR p
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i OPERATING DATA REPORT DOCKET NO. 50-346 DATE November 10, 1986 COMPLETED BY Morteza Khazrai TELEPHONE (419) 249-5000, OPERATING STATUS
- 1. Unit Name:
Davis-Besse Unit 1 Notes
- 2. Reporting Period:
October 1986
- 3. Licensed Thermal Power IMW:):
2772
- 4. Nameplate Rating (Gross MWe):
925
- 5. Design Electrical Rating (Net MWe):
906
- 6. Maximum Dependable Capacity (Gross MWe):
904
- 7. Maximum Dependable Capacity (Net MWe):
860
- 8. If Changes Occur in Capacity Ratings (items Number 3 Through 7) Since Last Report. Give Reasons:
- 9. Power Level To Which Restricted. lf Any (Net MWe):
- 10. Reasons For Restrictions.If Any:
His Month Yr.-to.Date Cumulative II. Hours in Reporting Period 744 7.295 72.360.0
- 12. Number Of Hours Reactor Was Critical O
0.0 35,877.1
- 13. Reactor Reserve Shutdown Hours 0.0 0.0 4.058.8
- 14. Hours Generator On.Line 0.0 0.0 34.371.8
- 15. Unit Reserve Shutdown Hours 0.0 0.0 1.732.5
- 16. Cross Thermal Energy Generated (MWH) 0.0 0.0 81.297.600
- 17. Gross Electrical Energy Generated (MWH) 0 Q.
0.0 26.933.622
- 18. Net Electrical Energy Generated (MWH) 0.0 0.0 25.233.177
- 19. Unit Service Factor 0.0 0.0 47.5
- 20. Unit Availability Factor 0.0 0.0 49.9
[
- 21. Unit Capacity Factor (Using MDC Net) 0.0 0.0 40.5
- 22. Unit Capacity Factor iUsing DER Net) 0.0 0.0 38.5
- 23. Unit Forced Outage Rate 100.0 100.0 35.6
- 24. Shutdowns Scheduled Over Ne.st 6 Months (T)pe. Date,and Duration of Each1:
- 25. If Shut Down At End Of Report Period. Estimated Date of Startup:
November 11, 1986
- 26. Units in Test Status (Prior to Commercial Operation):
Forecast Achiesed INITIAL CRITICA LITY INITIAL ELECTRICITY COsl%IERCI A L OPER ATION (9/77 )
DOCKET NO.
50-346 UNIT SHUTDOWNS AND POWER REDUCTIONS UNIT NAME Davis-Besse Unit 1 DATE November 10, 1986 COMPLETED BY Morteza Khazrai
~
REPORT MONTH October 1986 TELEPHONE (419) 249-5000. Ext. 7290 "u
jg
}
Licensee ag g
Cause & Corrective m
Event g
ag juy gg gg Action to No.
Date e
uo o
u :s Report #
xv au Prevent Recurrence
$6 EMS O
8 7
85 06 09 F
744 A
4 LER 85-013 JK SC The unit remained shutdown following Cont'd the reactor trip on June 9, 1985.
See Operational Summary for further details.
I F: Forced Reason:
Method:
Exhibit G - Instructions S: Scheduled A-Equipment Failure (Explain) 1-Manual for Preparation of Data B-Maintenance or Test 2-Manual Scram Entry Sheets for Licensee C-Refueling 3-Automatic Scram Event Report (LER) File D-Regulatory Restriction 4-Continuation from (NUREG-0161)
E-Operator Training & License Examination Previous Month F-Administrative 5-Load Reduction G-Operational Error (Explain) 9-Other (Explain)
Exhibit I - Same Source (9/77)
H-Other (Explain) s
OPERATIONAL
SUMMARY
OCTOBER 1986 The unit remained shutdown the entire month of September following the reactor trip on June 9, 1985. Corrective actions and system upgrades continue.
Below are some of the major activities performed during this month:
1)
Continued testing as part of the System Review and Test Program.
1 2)
Continued Motor Operated Valves Analysis Test (MOVATS) activities.
3)
Continued Raychem repairs and followup corrective actions.
4)
All Reactor Coolant Pump vork completed.
REFUELING INFORMATION DATE: October 1986 1.
Name of facility: Davis-Besse Unit 1 2.
Scheduled date for next refueling shutdown:
February 1988 3.
Scheduled date for restart following refueling: April 1988 4.
Will refueling or resumption of operation thereafter require a technical specification change or other license amendment? If answer is yes, what in general will these be? If answer is no, has the reload fuel design and core configuration been reviewed by your Plant Safety Review Committee to determine whether any unreviewed safety questions are associated with the core reload (Ref. 10 CFR Section 50.59)?
Ans: Expect the Reload Report to require standard reload fuel design Technical Specification changes (3/4.1 Reactivity Control Systems and 3/4.2 Power Distribution Limits).
5.
Scheduled date(s) for submitting proposed licensing action and supporting information: Summer, 1987 6.
Important licensing considerations associated with refueling, e.g.,
new or different fuel design or supplier, unreviewed design or performance analysis methods, significant changes in fuel design, new operating procedures.
Ans: None identified to date.
7.
The number of fuel assemblies (a) in the core and (b) in the spent fuel storage pool.
(a) 177 (b) 204 - Spent Fuel Assemblies 8.
The present licensed spent fuel pool storage capacity and the size of any increase in licensed storage capacity that has been requested or is planned, in number of fuel assemblies.
Present:
735 Increase size by: 0 (zero) 9.
The projected date of the last refueling that can be discharged to the spent fuel pool assuming the present licensed capacity.
Date:
1996 - assuming ability to unload the entire core into the spent fuel pool is maintained.
BMS/005
COMPLETED FACILITY CHANGE REQUEST FCR NO.79-324 SYSTEM Steam Generators COMPONENT OTSG Orifice Plate CHANGE, TEST OR EXPERIMENT FCR 79-324 performed an adjustment to the orifice plates from approximately 25% open to approximately 0% open.
This FCR was closed July 22, 1986.
REASON FOR CHANGE This change was incorporated due to a letter from B&W (B&W Letter DB-79-156) which had a concern on pressure oscillations.
SAFETY EVALUATION
SUMMARY
FCR 79-324 involved the adjustment of the OTSG orifice plates to an approximate closed position. B&W has provided a safety evaluation of OTSG thermal hydraulic oscillations (DB-79-164 dated September 14, 1979). The 4
B&W safety evaluation which has been reviewed by Engineering supports the conclusion that this change does not involve an unreviewed safety question.
I TEMP 2 C/335/4
COMPLETED FACILITY CHANGE REQUEST FCR NO.82-048 SYSTEM Pressurizer COMPONENT Check Valve CHANGE, TEST OR EXPERIMENT FCR 82-048 added a non-nuclear 1500 check valve upstream of valve NN-64 in the 1" line from the Nitrogen System to the pressurizer.
This FCR was closed July 11, 1985.
REASON FOR CHANGE The nitrogen piping and related equipment are rated for a maximum pressure of 120 psi and would fail when subjected to a pressure in excess of 2,000 psi.
This FCR was generated in response to Recommendation #2 of SOER 81-16.
SAFETY EVALUATION
SUMMARY
FCR 82-048 modified the Nitrogen Supply System which will prevent reactor coolant, which has a pressure in excess of 2,000 psi, from penetrating the small nitrogen supply line. The consequences would be the failure of the lower pressure rated pipe, resulting in loss of primary coolant.
The modification will not affect the safety function of the system.
Therefore, no unreviewed safety question is involved.
TEMP 2 C/335/3
COMPLETED FACILITY CHANGE REQUEST FCR NO.83-062 SYSTEM Emergency Ventilation System COMPONENT LPDY 5000A, LPDY 5000B, LPDY 5000C, and LPDC 5000 CHANGE, TEST OR EXPERIMENT FCR 83-062 relocated LPDY 5000A, LPDY 5000B, LPDY 5000C and LPDC 5000 from the Mechanical Penetration Room 303 to Roon 304 of the Auxiliary Building.
This FCR was closed April 25, 1984.
REASON FOR CHANGE This change was made due to a recommendation report from EDS Nuclear on environmental qualification of safety related electrical equipment due to radiation following a LOCA.
SAFETY EVALUATION
SUMMARY
The above equipment is required to function during a LOCA which could be exposed to a significant post accident dose. The equipment contains sensitive electronic components which have a potential radiation sensitiv-ity. This equipment was not tested for qualification.
Shielding would not be feasible due to bulk and cost. Testing of this equipment would be costly. Relocation of the specified equipment is the best solution.
Equipment was relocated to an area where the radiation environment plus an accident dose of 1 x 103 rads would be maximum.
The work authorized by FCR 83-062 does not change the safety function, or create any new adverse environment, and doea not constitute an unreviewed safety question.
TEMP 2 C/335/5
COMPLETED FACILITY CHANGE REQUEST FCR NO.84-060 SYSTEM Pressurizer COMPONENT Pressurizer Heaters CHANGE, TEST OR EXPERIMENT FCR 84-060 disconnected essential heater cables for Pressurizer Essential Heater Bank #1 (upper heater bundle) and reconnected to heaters in the middle heater bundle. Heater cables disconnected from the middle bundle heater were reconnected to the heaters in the upper bundle previously used for Essential Heater Bank #1.
FCR 84-060 was closed September 12, 1984.
REASON FOR CHANGE This change minimizes the possibility of essential heater banks from becoming uncovered. A low-low level pressurizer interlock, which deenergizes pressurizer heaters, only functions when the heaters are in the automatic control mode.
SAFETY EVALUATION
SUMMARY
FCR 84-060 connected the essential heater cables to heaters in the middle bundle (rather than upper bundle). This does not affect the integrity of the pressurizer as a pressure boundary. The change enhances the heater operation by minimizing the possibility of uncovering the heaters when the low-low level pressurizer interlock is defeated. All wiring changes were done at the heater connectors. No changes were made within the pressur-izer heater junction boxes. The changes and additions do not create any new adverse environment and do not constitute an unreviewed safety question.
TEMP 2 C/335/2
.o COMPLETED FACILITY CHANGE REQUEST FCR NO.84-073 SYSTEM Component Cooling Water COMPONENT N/A CHANGE, TEST OR EXPERIMENT FCR 84-073 demonstrated the capabilities of the leak measuring device and acoustic leak sensing equipment on the Component Cooling Water System.
This FCR was closed February 21, 1986.
REASON FOR CHANGE The test performance and data was used to develop a topical report to the NRC. This report was prepared by H. A.F. A. International for Toledo Edison. The topical report will be used to justify reducing hydro-testing and pressure testing requirements based on information gained from this test and other tests which will be performed.
SAFETY EVALUATION
SUMMARY
This FCR affected only Component Cooling Water Train #1, while Component Cooling Water Train #2 provided normal component cooling water functions.
This test resulted in entering a 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> action statement per Technical Specification 3.7.3.
During the performance of this test, an operator and electrician were on standby to place Train #1 in service if required. The test did not prevent Component Cooling Water from providing the required cooling capacity to mitigate the consequences of an accident.
Since Component Cooling Water Train #2 was available throughout the test, and Train #1 was available with operator assistance, this test did not constitute an unreviewed safety question.
TEMP 2 C/335/1
f7..
M)LEDO
%su EDISON November 10, 1986 NE0-86-00024 File:
RR 2 (P-6-86-10)
Docket No. 50-346 License No. NPF-3 Mr. Norman Haller, Director Office of Management and Program Analysis U. S. Nuclear Regulatory Commission Washington, D.C.
20555
Dear Mr. Haller:
Monthly Operating Report, October 1986 Davis-Besse Nuclear Power Station Unit 1 Enclosed are ten copies of the Monthly Operating Report for Davis-Besse Nulcear Power Station Unit 1 for the month of October 1986.
If you have any questions, please feel free to contact Morteza Khazrai at (419) 249-5000 Extension 7290.
Yours truly, mai.
/
Louis F. Storz Plant Manager Davis-Besse Nuc1 car Power Station LFS/MK/1j k Enclosures cc:
Mr. James G. Keppler, w/l Regional Administrator, Region III Mr. James M. Taylor, Director, w/2 Office of Inspection and Enforcement Mr. Paul Byron, w/l NRC Resident Intipector Nucicar Records Management LJK/002
>N THE TOLEDO EDISON COMPANY EDISON PLAZA 300 MADISON AVENUE TOLEDO, OHIO 43G52 l