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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARML20154H5291998-10-0808 October 1998 Special Rept:On 980928,meteorological Monitoring Instrumentation Channel Inoperable for Period Greater than 7 Days.Caused by Vendor to Follow Std Industry Practice for Calibr of Instrumentation.Instruments Installed ML20129B8991996-10-17017 October 1996 Special Rept:On 960919-22,DG Failures Experienced.Causes Could Not Be Conclusively Determined Although Kepner Tregoe Problem Analysis Identified Several Possible Causes. Components Identified Possible Contributors Being Monitored ML20065N1171994-04-25025 April 1994 Special Rept:On 940125,unplanned Reactor Trip & ECCS Actuation & Injection Into RCS Occurred.Total Accumulated Actuation Cycles for Four High Head Injection Lines Is Three ML20064N2381994-03-25025 March 1994 Ro:On 940316,determined Recorder 1-SM-X-6706 Inoperable for Indeterminate Period of Time.Caused by Corroded Sensors. Damaged Sensors Replaced & Recorder Returned to Svc on 940317 ML20059D9891994-01-0303 January 1994 Special Rept:On 931201,02,16,18 & 29,diesel Generator Failures Occurred.Causes & Corrective Actions Listed ML20127H3161993-01-15015 January 1993 Special Rept:On 921216,discovered That Prior to Closing EDG Output Breaker,Dg Output Voltage Was Offscale High.Caused by Valid EDG Start Failure.Silicon Controlled Recifier Bank a Placed Into Svc & Bank B Will Be Repaired or Replaced ML20079K9011991-10-31031 October 1991 Suppl to 910925 Special Rept:On 910826,train a Emergency Diesel Generator Tripped During post-maint Testing.Caused by Reversed Wiring Leads in Power Relays.Design Change Issued, Rewiring Performed & Input Leads Corrected ML20085D8251991-10-11011 October 1991 Special Rept:On 910911,EDG 1B Shutdown Due to Excessive Vibration.On 910916,EDG 1B Shutdown Due to Oil Leak on Cylinder 8.On 910919,EDG 1B Shutdown Due to Loud Noises from Air Start Distributor.Distributor Shaft Reinstalled ML20083D5741991-09-25025 September 1991 Special Rept:On 910826,A Train EDG Tripped.Trip Actuated by Reverse Power Relay.Root Cause Analysis Will Be Completed by 911030.Design Change Issued & Implemented to Correct Wiring of Subj Relays & Schematic Drawings ML20083D2951991-09-24024 September 1991 Special Rept:On 910825,Train a Emergency Diesel Generator Tripped on Low Lube Oil Pressure During post-maint Testing. Caused by Large Fluctuations in Engine Revolutions Per Minute.Procedures Re Auxiliary Lube Oil Pump Revised ML20247R5721989-09-25025 September 1989 Ro:On 890902,radiation Monitor Inoperable for Period Exceeding 7 Days.Caused by Installation of Nonfuse Dependent Isolation Devices in Communication Loops of Radiation Data Mgt Sys & Need for Relocation of Monitor Due to New Design ML20245G7151989-04-17017 April 1989 Ro:On 890316,train a Emergency Diesel Generator Tripped on Low Oil Pressure During Initial Startup.Caused by Engine Lube Oil Monitoring Circuit Becoming Active Before Engine Speed Developed Sufficient Lube Oil Pressure ML20154F3231988-09-0909 September 1988 Special Rept:On 880811,fuel Oil Leak Required Engine Shutdown & on 880812,Train B Emergency Diesel Generator Tripped.Caused by Incorrect Setting of Water Jacket Temp Controller.Adjustment Knob Protected from Misadjustment ML20207C3181988-07-22022 July 1988 Special Rept:On 880224,low Lube Oil Pressure Trip Occurred. Caused by 8-wk Maint Outage Resulting in Slower than Normal Engine Acceleration During Engine Start.Development of Design Change to Relocate Coolant Pressure Switch Underway ML20238E4601986-08-28028 August 1986 Partially Withheld Secrity Event Rept:On 860824,bomb Threat Received for Plants.Bomb Search Initiated.No Suspicious Objects Found 1998-10-08
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217H2841999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Seabrook Station. with ML20212D1461999-09-17017 September 1999 SER Accepting Request to Use Proposed Alternative to Certain Weld Repair Requirements in ASME Boiling & Pressure Vessel Code ML20216F5141999-08-31031 August 1999 Rept on Status of Public Petitions Under 10CFR2.206 ML20212B8671999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Seabrook Station. with ML20210Q7581999-08-11011 August 1999 SER Approving Proposed Merger of CES & Bec,Which Will Create New Parent Company of Canal ML20210R9781999-08-0606 August 1999 ISI Exam Rept of Seabrook Station, for RFO 6,period 3 ML20210J8681999-08-0303 August 1999 SER Approving License Transfer from Montaup Electric Co to Little Bay Power Corp & Approval of Conforming Amend for Seabrook Station Unit 1 ML20210R6001999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Seabrook Station, Unit 1.With ML20210H1151999-06-30030 June 1999 Naesc Semi-Annual Fitness-for-Duty Rept for 990101-0630 ML20209H1371999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Seabrook Station, Unit 1.With ML20195G5391999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Seabrook Station, Unit 1.With ML20195C0491999-05-25025 May 1999 Offshore Intake Seal Deterrent Barrier Design ML20206E4761999-04-30030 April 1999 LER 99-S01-00:on 990408,contractor Employee Was Granted Temporary Unescorted Access to Seabrook Station Protected Area.Caused by Failure of Contractor Employee to Provide Accurate Info.Individual Access Revoked.With ML20206N1751999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Seabrook Station, Unit 1.With ML20196L2081999-04-19019 April 1999 Rev 01-07-00 to RE-21, Cycle 7 Colr ML20205K5441999-03-31031 March 1999 Decommissioning Update ML20205L8141999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Seabrook Station. with ML20205C1981999-03-24024 March 1999 Safety Evaluation Concluding That Proposed Relief Request IR-8,Rev 1,provides Acceptable Alternative to ASME Code Requirements.Recommends Authorization of Proposed Alternative Pursuant to 10CFR50.55a(a)(3)(i) ML20207F4941999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Seabrook Station. with ML20199E6731998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Seabrook Station, Unit 1.With ML20198P1831998-12-31031 December 1998 LER 98-S01-00:on 981214,incomplete pre-employment Screening Records Was Noted.Caused by Failure of Contractor Employee to Provide Accurate Info.Subject Contractor Employees Employment Was Terminated.With ML20202E8241998-12-31031 December 1998 Naesc Semi-Annual Fitness-for-Duty Rept for 980701-981231 ML20196F5741998-12-0202 December 1998 Safety Evaluation Concluding That Licensee Has Established Acceptable Program to Verify Periodically design-basis Capability of safety-related MOVs at Seabrook ML20198B8661998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Seabrook Station, Unit 1.With ML20195D0311998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Seabrook Station, Unit 1.With ML20154H5291998-10-0808 October 1998 Special Rept:On 980928,meteorological Monitoring Instrumentation Channel Inoperable for Period Greater than 7 Days.Caused by Vendor to Follow Std Industry Practice for Calibr of Instrumentation.Instruments Installed ML20154M8421998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Seabrook Generating Station,Unit 1.With ML20151V5951998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Seabrook Station, Unit 1.With ML20237B4501998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Seabrook Station ML20236R1781998-06-30030 June 1998 Naesc Semi-Annual Fitness-for-Duty Rept for 980101-0630 ML20236M3591998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Seabrook Station, Unit 1 ML20237A4871998-06-0303 June 1998 North Atlantic Seabrook Station 1998 Exercise on 980603 ML20248M2951998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Seabrook Station, Unit 1 ML20247G2641998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Seabrook Station ML20247H3171998-04-27027 April 1998 Rev 1 to Seabrook Station SGs B & C Isi,May/June 1997 ML20216F8891998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Seabrook Station 05000443/LER-1998-002, Re Potential Safety Injection Pump Runout Conditions Identified on 980113.LER 98-002-00 Retracted1998-03-20020 March 1998 Re Potential Safety Injection Pump Runout Conditions Identified on 980113.LER 98-002-00 Retracted ML20216H9211998-03-13013 March 1998 Fitness for Duty Program Performance Data Personnel Subject to 10CFR26 ML20248L2811998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Seabrook Station, Unit 1 ML20197A7531998-02-27027 February 1998 Safety Evaluation Accepting License Request for Relief from ASME Code,Section IX Requirements Re Inservice Insp of RHR Heat Exchanger Nozzle Welds & Reactor Vessel Closure Head Nuts ML20202G3701998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Seabrook Station ML20198G0271997-12-31031 December 1997 Commonwealth Energy Sys 1997 Annual Rept ML20248L7711997-12-31031 December 1997 Western Massachusetts Electric 1997 Annual Rept. Supporting Info,Encl ML20198G1021997-12-31031 December 1997 Baycorp Holdings 1997 Annual Rept ML20198N7021997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Seabrook Station, Unit 1 ML20198G0351997-12-31031 December 1997 Eastern Edison Co 1997 Annual Rept ML20198G0681997-12-31031 December 1997 Taunton Municipal Lighting Plant 1997 Annual Rept ML20248L7671997-12-31031 December 1997 North Atlantic 1997 Annual Rept ML20198F9511997-12-31031 December 1997 United Illuminating Co 1997 Annual Rept ML20236M9561997-12-31031 December 1997 Amended Public Service of New Hampshire 1997 Annual Rept 1999-09-30
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7 N ue George S. Thomas Wee hesk$enbNuclear hodvetion UI NYN- 88123 Put2c SoMee of New Hampshire New Hampshire Yankee Division United States Nuclear Regulatory Commission p Washington, DC 20555 Attention: Document Control Desk
Reference:
Facility Operating License No. NPF-56, Docket No. 50-443
Subject:
Diesel Genetator Special Report Gentlemen:
The B Train Emergency Diesel Generator (EDG) was shutdown once on both August 11 and 1.. 1988, during maintenance testing activities. In accordance with Regulatory n4sition C.3.6 of Regulatory Guide 1.108. Revision 1. Aup,ust 1977, a determination has been made that these events are not considereu valid l tests r test failures. These events are being reported pursuant to Technical Specifications 4.8.1.1.3 and 6.8.2. At the time of these events the plant was i
in HODE 5 (cold shutdown) with the A Train EDG operable.
On August 11, 1988, at 1830, while performing post-maintenance testing and data collection on the B Train EDG, a fuel oil leak developed which required the engine to be shutdown. The leak came from the diesel fuel oil pump which had previously undergone maintenance. Corrective actions were performed to repair the fuel oil leak and during subsequent testing no furcher fuel oil leakage was observed.
On August 12, 1989, at 1030, the B Train EDG tripped on high jacket water temperature during post-maintenance testing. The engine trip was caused by an incorrect setting (,f the wt. tar jacket temperature controller which resulted in a higher temperature setpoint. The incorrect temperature controller setpoint s was caused by personnel in the area accidently bumping the temperature setpoint adjustment knob to a new position during area activities. Corrective action to add a cover or otherwise protect the controller setpoint adjustment knob has been initiated to prevent any future occurrenceJ of this type.
The determination that these events are not considered valid tests or test failures is based on the following:
When the EDG is operating under the work controi program during g maintenance testing for data collection and engine performance monitoring it is not considered a valid test condition, and g, testing that is termin.ted intentionally is not considered a valid test or failure. In this pasticular instance, the leak would not have prevented the EDG from performing in an accident O condition. The high temperature engine trip is bypassed during Q emergency operation. Had there been a bonafide emergency start g signal the engine high temperature alarm would have actuated g alerting the operator of an abnormal conditions however, the !
y EDG would have continued to operate without automatically
[
g tripping.
a.co O P.O. Box 300. Seabrook, NH 03874 . Telephone (603) 474 9574 '.
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Unitsd Stctos Nuc1 car Regulatory Commission Ssptember 9g 1988 Attention: Documsnt Control Desk Page 2 Given the events and conditions outlined above, both events are non-valid test? or'tast failu.res and do not count toward events that are considered l vaild tests or failures. No additional surveillance testing will be performed as a result of these events.
1 Corrective Actions Due to naturs of post-maintenance testing there are no corrective actions that cra be performee as a result of the fuel oil leak. As stated above, the l temperature controller setpoint adjustment knob will be protected from '
accidsnt41 misadjustment so that future occurrences will be prevented. !
It you have any questions regarding this report, please cemiset l Mr. Robert A. Gwinn at (603) 474-9574, extension 4056. t Very truly yours, 4
ofo%
George S. Thomas i
i L 1
I cc: Regional Administrator l
a USNRC P.agion 1 475 Allendale Road -
King of Prussia. PA 19405 ;
i i
Mr. D. G. Ruscitto $
! NRC Senior Resident Inspector (Acting) l Sea *orook Station '
1 Seabrook, NH 03874
! INPO -
1 Records Crater I 1100 Circle 75 Parkway ;
g Atlanta, GA 30339 l
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