:on 970521,discovered TS Violation of Operability Requirement of MSL Isolation.Caused by Inadequate Consideration for Operability of All Required Functions.Verified Low RCS Sys Average Temp| ML20141C266 |
| Person / Time |
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| Site: |
Point Beach  |
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| Issue date: |
06/19/1997 |
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| From: |
Castell C WISCONSIN ELECTRIC POWER CO. |
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| To: |
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| Shared Package |
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| ML20141C260 |
List: |
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| References |
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| LER-97-026, LER-97-26, NUDOCS 9706250078 |
| Download: ML20141C266 (5) |
|
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NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3160-0104 i
(4-95)
EXPlRES 04/30/98 l
ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THl3 (NFORMATION COLLECTION REQUEST: 50.0 HRS.
REPORTED LESSONS LEARNED ARE INCORPORATED LICENSEE EVENT REPORT (LER)
INTO THE LICENSING PROCESS AND FED BACK TO INDUSTRY.
FORWARD COMMENTS REGARDING BUROEN ESTIMATE TO THE INFORMATION AND (See reverse for required number of RECORDS MANAGEMENT BRANCH {T-6 F33),
U.S.
digits / characters for each block)
NUCLEAR REGULATORY COMMISSloN, WASHINGTON.
DC 20555-0001, AND TO THE PAPERWORK REDUCTION PROJECT 1
[
FACILITY NAME (1)
DOCKET NUMBER (2)
PAGE (3) lPointBeachNuclearPlant, Unit 1 05000266 1 OF 5 TITLE (4)
Technical Specification Violation of Operability Requirement for Main Steam Line Isolation EVENT DATE (5)
LER NUMBER (6)
REPORT DATE (7)
OTHER FACillTIES INVOLVED (8)
IYEAR SEQUEN TIAL REVISION FACluTY NAME DOCKET PeUMBER MONTH DAY YEAR NUMBER NUMBER MONTH DAY YEAR Unit 2 05000301 l
l l
FACILITY NAME DOCKET NUMBER i
l 05 21 l 97 l 97 026 --
00 06 19 97 05000 l OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR B: (Check one or more) (11)
MODE (9)
N l 20.220i te) 20.2203iaH2Hv8 X
50.73(aH2)o) 50.73(aH2Hvm)
POWER 20.2203(aH1) 20.2203(aH3)h) 50.73(aH2Hii) 50.73(aH2)(x)
LEVEL (101 000 20.2203(aH2H )
20 2203(aH3Hio 50.73(aH2Hm) 73.7i 20.2203(aH2Hn) 20.2203(aH41 50,73(aH2Hrv)
OTHER 20.2203(aH2Hm) 50.36(cH1)
- 50. 73(aH2Hv)
Specify in Abstract below l
20.2203(a H 2)hv)
~
60.36(cH2)
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50.73(aH2Hvn) or in NRC Form 366A LICENSEONTACT FOR THIS LER 612)
IWAME TELEPHONE NUMBER (include Area Code)
Curtis A. Castell (414) 221-2019 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
CAUSE
SYSTEM COMPONENT MANUFACTURER REPOR T ABLE
CAUSE
SYSTE COMPONENT MANUFACTURER REPORTABLE TO NPROS M
TO NPRDS SUPPLEMENTAL REPORT EXPECTED (14) l EXPECTED MONTH I DAY YEAR i
l YES SUBMISSION tif yes, complete EXPECTED SU9 MISSION DATE).
X NO DATE (16)
ABSMACT q$to 1400 spaces, te., approximately 16 single-spaced typewntten lines) (16) i On May 21, 1997, while PBNP Unit I was in a cold shutdown condition and Unit 2 was in a defueled condition, it was discovered that operability of the reactor coolant system l
average temperature instrumentation input to the main steam line isolation function was not being maintained in accordance with Technical Specification operability requirements, I
It has been concluded that the Technical Specification was violated each time either ur.it was above cold shutdown conditions with scaling resistors in place and the low reactor coolant system average temperature input to main steam line was not in the trip condition. This condition was caused by insufficient or inadequate consideration for operability of all required functions that rely on this input. The low reactor coolant system average temperature input to main steam line will be verified to be in the trip condition prior to leaving the cold shutdown condition when the scaling resistors are in place. It has been concluded that this situation did not diminish the safety of the public, plant personnel, or integrity of safety barriers place at PBNP at any time.
NRC FORM 366 (4-95) 9706250078 970619 PDR ADOCK 05000266 l
8 PDR
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NR$; FOHM 366A U.S. NUCLEAR REGULATORV COMMISS60N (4-95)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILIIY NAME 11)
DOCKET NUMBER (2)
LER NUMBER (6)
PAGE (3)
YEAR SEQUENTIAL REVISION Point Beach Nuclear Plant, Unit'l 05000266 NUMBER NUMBER 2 OF 5 97 026 00 IEKI lit mort 8p0C013 f0 quired, U50 odditional Cops 0s of NHC form 366Al (11)
Event Description
l l
On May 21, 1997, while Point Beach Nuclear Plant (PBNP) Unit 1 was in a l
cold shutdown condition and Unit 2 was in a defueled condition, it was l
discovered that operability of the reactor coolant system average temperature instrumentation input to the main. steam line isolation l
function was not being maintained in accordance with Technical l
Specification Table 15.3.5-4 item 2.b operability requirements.
It has been standard practice at PBNP to install scaling resistors in the average temperature instrumentation to allow average temperature to be maintained on scale.
The scale on average temperature is 540 to 615 F.
The scaling l
resistors replace the function of the resistance temperature devices in the reactor coolant system.
The scaling resistors cause the reactor coolant system average temperature instrumentation to be maintained at about 570 F.
i l
The scaling resistors are normally installed after cold shutdown is established.
The resistors are normally removed at about 540 F.
Technical Specification Table 15.3.5-4 item 2.b provides operability requirements for main steam line isolation on hi steam flow coincident with low reactor coolant system average temperature and safety l
injection.
This Technical Specification for the low reactor coolant
)
i system average temperature input states that the affected unit must be placed in hot shutdown within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> and cold shutdown within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> if the operability requirement is not met.
Therefore, it has been concluded that the operability requirement for this input was violated, each time either unit was above cold shutdown conditions with the scaling resistors in place and the low reactor coolant system average temperature input to main steam line not in the trip condition.
The practice of installing the scaling resistors was instituted about 25 years ago to improve the configuration of the circuitry during long j
periods of shutdown by maintaining the circuitry consistent with its q
normal operating range.
1 WHC FORM 366A 14-96)
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NRC f0RM 366A U.S. NUCLEAR REGULATORY COMMISSION (4-95)
LICENSEE EVENT REPORT (LER)
I TEXT CONTINUATION FACILITY NAME (1)
DOCKET NUMBER (2)
LER NUMBER 16)
PAGE (3)
YEAR SEQUENTIAL REVISION l
Point Beach Nuclear Plant, Unit 1 05000266 NUMBER NUMBER 3OF5 l
97 026 00 TEXT tu mwe space is,equwea, use essitiones copies or nac form 366A) (1 15 l
Cause
This condition was caused by insufficient or inadequate consideration for operability of all required functions that rely on this input.
Corrective Actions
Appropria te procedure changes will be implemented to verify that the low reactor coolant system average temperature input to main steam line is placed in the trip condition prior to leaving the cold shutdown condition when the scaling resistors are in place.
This will ensure the Technical Specification operability requirements for the main steam line isolation on hi steam flow coincident with low reactor coolant system average temperature and safety injection wi11 be met.
A root cause evaluation is being completed.
Additional corrective actions
will be taken, as appropriate, from recommendations contained in the root cause evaluation.
RIportability:
This Licensee Event Report is being submitted in accordance with the requirements of 10 CFR 50.73 (a) (2) (i) (B), "Any operation or condition prohibited by the plant's Technical Specifications."
Component and System Description:
The main steam line isolation function causes a closure signal for the main steam isolation valves (MS-2017 and MS-2018).
The Technical Specifications provide the operability requirements for the inputs to this isolation function as follows:
(a) Hi Hi Steam Flow with Safety Injection, (b) Hi Steam Flow and Low Tavg with Safety Injection, (c) Hi Containment Pressure, and (d) Manual.
The condition described in this report caused the Hi Steam Flow and Low Tavg with Safety Injection isolation signal to be inoperable prior to removal of the scaling resistors.
The purpose of the steam line isolation function as described in the PBNP FSAR in section 14.2.5 states, "Each steam line has a fast closing isolation valve and a check valve.
These four valves prevent blowdown of more than one steam generator for any break location even if one valve fails to close."~,.
NSC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (4-95)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1)
OOCKET NUMBER (2)
LER NUM8ER 16)
PAGE (3)
YEAR SEQUEN TIAL REVISION Point Beach Nuclear Plant, Unit 1 05000266 NUMBER NUMBER 4OF5 97 026 00 TEXT tir,nore space,s requaes. use assitenar coon,s of NRC forn; 366A) (17)
Sofety Assessment:
The main purpose of the main steam line isolation signal is to mitigate a steam line rupture or rapid cooldown of the reactor coolant system by closure of the main steam line isolation valves.
The Hi Hi Steam Flow with Safety Injection isolation function is intended to cause isolation for relatively high steam flow rates (4 x 10' lb/hr).
The Hi Steam Flow and Low Tavg with Safety Injection is intended to cause isolation for relatively low steam flow rates (0.66 x 10' lb/hr).
If a steam line rupture or rapid cooldown occurred during the time the scaling resistors were in place and the low Tavg input was not in trip, then manual steam line isolation may have been needed to prevent blowdown of both steam generators.
At lower initial reactor coolant system temperatures than used in the FSAR section 14.2.5 " Rupture of a Steam Pipe" analysis, which is based on an initial reactor coolant system temperature of 547 F, the cooldown and hence the reactivity insertion would be less.
This reduces the chances that a return to criticality could occur for this accident.
Even if a return to criticelity occurred it is likely that it would not be as severe as the limiting transients that have been analyzed and presented in the FSAR Chapter 14.
Therafore, the inoperability of Hi Steam Flow and Low Tavg with Safety Injection input to the steam line isolation function between hot and cold shutdown conditions did not diminish the safety of the public, plant personnel, or integrity of safety barriers in place at PBNP at any time.
System and Component Identifiers The Energy Industry Identification System component function identifier for each component / system referred to in this report are as follows:
Component / System Identifier Main Steam Isolation Valve ISV Main Steam System SB j
Reactor Coolant System AB
]
High Pressure Safety injection System BQ i
ii l
I
NRC FORM 368A U.S. NUCLEAR LEGULAVOR7 COMMISSION I
(4-9 5)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1)
DOCKET NUMBER (2)
LER NUMBER 16) l PAGE 13)
YEAR SEQUENTIAL REVISION l Point Beach Nuclear Plant, Unit 1 05000266 NUMBER NUMBER l 5 OF 5 97 026 00 l
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Similar occurrences:
l A search of previously submitted licensee event reports similar to this situation for PBNP was conducted.
The specific criterion used was based on a search for licensee event reports that were submitted due to reconfiguration of instrumentation not being adequately evaluated which resulted in a Technical Specification violation.
No similar occurrences were identified.
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| 05000266/LER-1997-001, :on 970108,safety Injection Delay Times Exceeded Design Basis Values.Caused by Degraded Voltage Conditions.Licensee Engineers Will Prepare FSAR Change Requests to Reflect LBLOCA Evaluation |
- on 970108,safety Injection Delay Times Exceeded Design Basis Values.Caused by Degraded Voltage Conditions.Licensee Engineers Will Prepare FSAR Change Requests to Reflect LBLOCA Evaluation
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000301/LER-1997-001, Forwards LER 97-001-00,re Containment Structure Where Internal Containment Structural Members Could Have Damaged Containment Liner During Safe Shutdown Earthquake | Forwards LER 97-001-00,re Containment Structure Where Internal Containment Structural Members Could Have Damaged Containment Liner During Safe Shutdown Earthquake | | | 05000301/LER-1997-001-01, :on 970107,containment Liner Clearance Was Not IAW Plant Design Basis.Caused by Void Between Containment Liner & Concrete Containment Structure.Inspected Containment |
- on 970107,containment Liner Clearance Was Not IAW Plant Design Basis.Caused by Void Between Containment Liner & Concrete Containment Structure.Inspected Containment
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) | | 05000266/LER-1997-002, :on 970109,potential to Overpressurize Piping Between Containment Isolation Valves Occurred.Caused by Original Design Not Providing Overpressure Protection for Piping.Review Completed |
- on 970109,potential to Overpressurize Piping Between Containment Isolation Valves Occurred.Caused by Original Design Not Providing Overpressure Protection for Piping.Review Completed
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000301/LER-1997-002-01, :on 970415,potential Reactor Coolant Sys Branch Connection Stresses Beyond Design Basis,Indicated.Caused by Mod Initiated to Remove RTD Bypass Line Isolation Valves. Stress Analysis Conducted on RTD Bypass Piping |
- on 970415,potential Reactor Coolant Sys Branch Connection Stresses Beyond Design Basis,Indicated.Caused by Mod Initiated to Remove RTD Bypass Line Isolation Valves. Stress Analysis Conducted on RTD Bypass Piping
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000266/LER-1997-003, :on 970109,did Not Perform Leak Test on Spare Containment Penetrations Per Ts.Caused by Lack of Routine Testing.Tested Penetrations W/Satisfactory Results |
- on 970109,did Not Perform Leak Test on Spare Containment Penetrations Per Ts.Caused by Lack of Routine Testing.Tested Penetrations W/Satisfactory Results
| 10 CFR 50.73(a)(2)(1) | | 05000301/LER-1997-004-01, :on 970729,declared RHR Loop Inoperable Due to CCW Leak.Caused by Failure of RHR Heat Exchanger CCW Piping. Repaired Piping & Declared RHR Loop Operable |
- on 970729,declared RHR Loop Inoperable Due to CCW Leak.Caused by Failure of RHR Heat Exchanger CCW Piping. Repaired Piping & Declared RHR Loop Operable
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000266/LER-1997-004, :on 970113,potential for Particular Common Mode Failure That Could Affect Opposite Trains of Unit 2 Safeguards Equipment Was Noted.Caused by Lack of Physical Separation.Replaced Subject Circuit Breakers |
- on 970113,potential for Particular Common Mode Failure That Could Affect Opposite Trains of Unit 2 Safeguards Equipment Was Noted.Caused by Lack of Physical Separation.Replaced Subject Circuit Breakers
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000301/LER-1997-005-01, :on 970806,RHR Pump Was Declared Inoperable Due to Abnormal Seal Leakage from Loop a RHR 2P-10A.Repaired RHR Pump |
- on 970806,RHR Pump Was Declared Inoperable Due to Abnormal Seal Leakage from Loop a RHR 2P-10A.Repaired RHR Pump
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000266/LER-1997-005, :on 970116,1SI-852A Was Not Tested IAW Inservice Test Program Required by Tss.Caused Because Condition Revealed That Valve 1SI-852A Had Not Been Completely Tested.Tests Will Be Reviewed |
- on 970116,1SI-852A Was Not Tested IAW Inservice Test Program Required by Tss.Caused Because Condition Revealed That Valve 1SI-852A Had Not Been Completely Tested.Tests Will Be Reviewed
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) | | 05000266/LER-1997-006, :on 970120,refueling Cavity Drain Failed During Loca.Caused by Inadequate Evaluation of Original Design.Design of Refueling Cavity Drains Was Revised with Respect Capability to Withstand an Earthquake |
- on 970120,refueling Cavity Drain Failed During Loca.Caused by Inadequate Evaluation of Original Design.Design of Refueling Cavity Drains Was Revised with Respect Capability to Withstand an Earthquake
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000266/LER-1997-007, :on 970124,determined That Potential Existed for EDG Overload Condition.Caused by Failure to Recognize This Condition When Plants Initially Licensed W/Two Edgs. Implemented Procedure Changes |
- on 970124,determined That Potential Existed for EDG Overload Condition.Caused by Failure to Recognize This Condition When Plants Initially Licensed W/Two Edgs. Implemented Procedure Changes
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000266/LER-1997-008, :on 970131,non-seismic Ductwork Located Above safety-related Equipment in Containment Occurred.Caused by Incomplete Seismic Evaluation.Mods Will Be Completed During Current Unit 2 Refueling Outage |
- on 970131,non-seismic Ductwork Located Above safety-related Equipment in Containment Occurred.Caused by Incomplete Seismic Evaluation.Mods Will Be Completed During Current Unit 2 Refueling Outage
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000266/LER-1997-009, :on 970214,potential for Safety Injection Failure During Filling of Safety Injection Accumulator Discovered.Caused by Situation Not Adequately Covered by Procedures.Procedure OI-100 Revised |
- on 970214,potential for Safety Injection Failure During Filling of Safety Injection Accumulator Discovered.Caused by Situation Not Adequately Covered by Procedures.Procedure OI-100 Revised
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000266/LER-1997-010, :on 970219,svc Water & Component Cooling Water TS Action Requirements Were Not Met.Caused Because Licensee Did Not Comply W/Cold Shutdown Requirements of TS 15.3.3.C.2 & 15.3.3.D.2.Evaluations Were Performed |
- on 970219,svc Water & Component Cooling Water TS Action Requirements Were Not Met.Caused Because Licensee Did Not Comply W/Cold Shutdown Requirements of TS 15.3.3.C.2 & 15.3.3.D.2.Evaluations Were Performed
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000266/LER-1997-011, :on 970305,containment Fan Cooler Accident Fans Were Not Tested in Accordance with Tss.Caused by non-conservative Interpretation of Literal Requirements of Tss.Unit 1 & 2 Accident Fans Were Tested |
- on 970305,containment Fan Cooler Accident Fans Were Not Tested in Accordance with Tss.Caused by non-conservative Interpretation of Literal Requirements of Tss.Unit 1 & 2 Accident Fans Were Tested
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(1) | | 05000266/LER-1997-012, :on 970304,diesel-drive Fire Pump Day Tank Not Sampled IAW TSs.Non-conservative Interpretation of TS Led to Failure.Day Tank T-30 Sample Was Drawn & Analyzed W/Satisfactory Results |
- on 970304,diesel-drive Fire Pump Day Tank Not Sampled IAW TSs.Non-conservative Interpretation of TS Led to Failure.Day Tank T-30 Sample Was Drawn & Analyzed W/Satisfactory Results
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(1) | | 05000266/LER-1997-013, :on 970304,CCWS Found Not in Accordance W/ Plant Design Basis.Caused by Inoperable Valve Due to Overtorquing in Closed position.Cross-tie Will Be Resolved |
- on 970304,CCWS Found Not in Accordance W/ Plant Design Basis.Caused by Inoperable Valve Due to Overtorquing in Closed position.Cross-tie Will Be Resolved
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000266/LER-1997-013-01, Forwards Suppl LER 97-013-01,re Component Cooling Water Sys Not IAW Plant Design Basis.Rept Replaces LER 97-013-00 in Its Entirety & Includes Addl Similar Occurrence Not Previously Reported to NRC | Forwards Suppl LER 97-013-01,re Component Cooling Water Sys Not IAW Plant Design Basis.Rept Replaces LER 97-013-00 in Its Entirety & Includes Addl Similar Occurrence Not Previously Reported to NRC | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000266/LER-1997-014, :on 970321,auxiliary Feedwater Sys Inoperability Due to Loss of Instrument Air.Design Mods Initiated,Providing Pneumatic Supply to Control Valves |
- on 970321,auxiliary Feedwater Sys Inoperability Due to Loss of Instrument Air.Design Mods Initiated,Providing Pneumatic Supply to Control Valves
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000266/LER-1997-015, :on 970324,control Room Ventilation Sys Declared Inoperable Due to Failures of Backdraft Damper & Vent Duct Access Door.Backdraft Damper,Replaced |
- on 970324,control Room Ventilation Sys Declared Inoperable Due to Failures of Backdraft Damper & Vent Duct Access Door.Backdraft Damper,Replaced
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000266/LER-1997-016, :on 970325,SG Level Logic Was Not Tested IAW Ts.Caused by Nonconservative Interpretation of Tss.Ts Amends Proposed to Provide Consistency Between Test Requirements & LCO Associated W/Sg Tests |
- on 970325,SG Level Logic Was Not Tested IAW Ts.Caused by Nonconservative Interpretation of Tss.Ts Amends Proposed to Provide Consistency Between Test Requirements & LCO Associated W/Sg Tests
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000266/LER-1997-017, :on 920508,containment Third Door Was Blocked Open During Refueling Operations.Caused by Interpretation That Movement of Core Components Per TS Definitions Rather than Literal Wording.Routine Maintenance Procedure Revised |
- on 920508,containment Third Door Was Blocked Open During Refueling Operations.Caused by Interpretation That Movement of Core Components Per TS Definitions Rather than Literal Wording.Routine Maintenance Procedure Revised
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000266/LER-1997-018, :on 970403,potential for RHR Overpressure During Accidents Was Discovered.Original Design Did Not Provide Overpressure Protection for Isolated Piping Section. Evaluation Was Performed to Determine Stress on Piping |
- on 970403,potential for RHR Overpressure During Accidents Was Discovered.Original Design Did Not Provide Overpressure Protection for Isolated Piping Section. Evaluation Was Performed to Determine Stress on Piping
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000266/LER-1997-019, :on 970404,RHR Not Aligned IAW TS Requirements. Caused by non-conservative Decision Making & Not Recognizing When TS Were Not Controlling Plant Operations.Pbnp Mgt Philosophy Re TS Interpretations Changed to Minimize Use |
- on 970404,RHR Not Aligned IAW TS Requirements. Caused by non-conservative Decision Making & Not Recognizing When TS Were Not Controlling Plant Operations.Pbnp Mgt Philosophy Re TS Interpretations Changed to Minimize Use
| 10 CFR 50.73(a)(2)(1) | | 05000266/LER-1997-020-01, Forwards LER 97-020-01,describing Plant Conditions in Which Ability to Achieve & Maintain Safe Shutdown in Event of Postulated Fire May Have Been Adversely Affected | Forwards LER 97-020-01,describing Plant Conditions in Which Ability to Achieve & Maintain Safe Shutdown in Event of Postulated Fire May Have Been Adversely Affected | 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor | | 05000266/LER-1997-021, :on 970430,determined That Spent Fuel Pool Cooling Sys Was Not in Accordance W/Plant Design Basis.Cause Indeterminate.Closed & re-tagged Valves SF-27 & SF-28 & Investigated Basis for Fsar,App a |
- on 970430,determined That Spent Fuel Pool Cooling Sys Was Not in Accordance W/Plant Design Basis.Cause Indeterminate.Closed & re-tagged Valves SF-27 & SF-28 & Investigated Basis for Fsar,App a
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000266/LER-1997-022, :on 970507,discovered That Postulated Control Room Fire May Cause Electrical Hot Short That Disables Limit or Torque Switches for Certain Movs.Mods Initiated to Remedy Condition |
- on 970507,discovered That Postulated Control Room Fire May Cause Electrical Hot Short That Disables Limit or Torque Switches for Certain Movs.Mods Initiated to Remedy Condition
| 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor | | 05000266/LER-1997-023, :on 970508,discovered Noncompliant Emergency Lighting for Postulated App R Fires.Caused by Alternative Provisions Made in Original Safe Shutdown Analysis.Emergency Lights Will Be Installed |
- on 970508,discovered Noncompliant Emergency Lighting for Postulated App R Fires.Caused by Alternative Provisions Made in Original Safe Shutdown Analysis.Emergency Lights Will Be Installed
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000266/LER-1997-024, :on 970501,determined Post Accident Sampling Sys Degradation.Caused by Inadequate Design Review.Will Upgrade Containment Atmosphere Sample Sys & Will Perform Mod to Reduce Dose within GDC 19 Dose Limits |
- on 970501,determined Post Accident Sampling Sys Degradation.Caused by Inadequate Design Review.Will Upgrade Containment Atmosphere Sample Sys & Will Perform Mod to Reduce Dose within GDC 19 Dose Limits
| | | 05000266/LER-1997-025, :on 970520,pressurizer Level Was Controlled Higher than Assumed in Accident Analysis.Caused by Inappropriately Changing Procedures W/O Adequate Consideration.Listed Affected Procedures Will Be Revised |
- on 970520,pressurizer Level Was Controlled Higher than Assumed in Accident Analysis.Caused by Inappropriately Changing Procedures W/O Adequate Consideration.Listed Affected Procedures Will Be Revised
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000266/LER-1997-026, :on 970521,discovered TS Violation of Operability Requirement of MSL Isolation.Caused by Inadequate Consideration for Operability of All Required Functions.Verified Low RCS Sys Average Temp |
- on 970521,discovered TS Violation of Operability Requirement of MSL Isolation.Caused by Inadequate Consideration for Operability of All Required Functions.Verified Low RCS Sys Average Temp
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000266/LER-1997-027, :on 970521,non-environmentally Qualified Matl Existed in Containment Hatch Applications.Caused by Inadequate Design Review.Mods Will Be Performed to Remove Existing Teflon Material |
- on 970521,non-environmentally Qualified Matl Existed in Containment Hatch Applications.Caused by Inadequate Design Review.Mods Will Be Performed to Remove Existing Teflon Material
| | | 05000266/LER-1997-031, :on 970619,discovered That Auxiliary Feedwater (AFW) Pump Low Suction Pressure Trip Setpoints May Not Ensure Adequate Suction Pressure Protection for AFW Pumps Following Tornado Event.Caused by Inadequate Design |
- on 970619,discovered That Auxiliary Feedwater (AFW) Pump Low Suction Pressure Trip Setpoints May Not Ensure Adequate Suction Pressure Protection for AFW Pumps Following Tornado Event.Caused by Inadequate Design
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000266/LER-1997-032, :on 970630,discovered Inadequately Rated Electrical Buses Could Disable Switchgear & Cause Secondary Fires.Caused by Characteristic of Original Design. Established twice-per-shift Fire Watches |
- on 970630,discovered Inadequately Rated Electrical Buses Could Disable Switchgear & Cause Secondary Fires.Caused by Characteristic of Original Design. Established twice-per-shift Fire Watches
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000266/LER-1997-034, :on 970707,discovered Unplanned Loss of Voltage on Train B Safeguards Buses.Caused by Inadequate Design & Design Review for Installation of New Train B Edgs.Incorrect Wiring Reworked |
- on 970707,discovered Unplanned Loss of Voltage on Train B Safeguards Buses.Caused by Inadequate Design & Design Review for Installation of New Train B Edgs.Incorrect Wiring Reworked
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000266/LER-1997-035, :on 970516,discovered Inadequate Seismic Support for Reactor Coolant Pump Rotor Stand.Caused by Rotor Stand Being Stored Since Initial Plant Construction.Moved Rotor Stand & Verified as Seismically Adequate |
- on 970516,discovered Inadequate Seismic Support for Reactor Coolant Pump Rotor Stand.Caused by Rotor Stand Being Stored Since Initial Plant Construction.Moved Rotor Stand & Verified as Seismically Adequate
| 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat | | 05000266/LER-1997-036, :on 970826,potential Common Mode Failure in DC Power Supply Which Could Disable AFW Sys Was Noted.Caused by Inadequate Design & Design Review.Plant Mods Were Performed to Eliminate Potential Common Mode Failure |
- on 970826,potential Common Mode Failure in DC Power Supply Which Could Disable AFW Sys Was Noted.Caused by Inadequate Design & Design Review.Plant Mods Were Performed to Eliminate Potential Common Mode Failure
| | | 05000266/LER-1997-037, :on 970903,potential Failure of EDG Load Sequence Occurred.Caused by Inadequate Design of EDG Load Sequencing Logic.Mod Restored Operability of EDG During Load Sequencing |
- on 970903,potential Failure of EDG Load Sequence Occurred.Caused by Inadequate Design of EDG Load Sequencing Logic.Mod Restored Operability of EDG During Load Sequencing
| | | 05000266/LER-1997-038, :on 970926,determined That Inoperability of Standby Emergency Power Placed Unit 2 in 7-day Lco.Caused by Failure That Occurred When EDG G-03 Was Shutdown.Repaired Governor & Returned EDG G-03 to Service |
- on 970926,determined That Inoperability of Standby Emergency Power Placed Unit 2 in 7-day Lco.Caused by Failure That Occurred When EDG G-03 Was Shutdown.Repaired Governor & Returned EDG G-03 to Service
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000266/LER-1997-039-01, :on 970615,RHR Loop Inoperable.Caused by Removal of CCW Pump from Svc.Ccw Pump Restored |
- on 970615,RHR Loop Inoperable.Caused by Removal of CCW Pump from Svc.Ccw Pump Restored
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000266/LER-1997-039, Forwards LER 97-039-00 Re RHR Loop Inoperable,Due to Inoperable CCW Pump.New Commitments within Rept Indicated in Italics | Forwards LER 97-039-00 Re RHR Loop Inoperable,Due to Inoperable CCW Pump.New Commitments within Rept Indicated in Italics | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000266/LER-1997-040-01, Forwards LER 97-040-01 Which Documents Event That Occurred at Point Beach Nuclear Plant,Unit 1.Commitments Made within Ltr,Encl | Forwards LER 97-040-01 Which Documents Event That Occurred at Point Beach Nuclear Plant,Unit 1.Commitments Made within Ltr,Encl | 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000266/LER-1997-041, :on 971023,potential Common Mode Failure in Afws Control Circuits Was Noted.Caused by AFW Control Circuits Installed by Plant Mods.Temporary Mods Will Restore Physical Separation for Cables |
- on 971023,potential Common Mode Failure in Afws Control Circuits Was Noted.Caused by AFW Control Circuits Installed by Plant Mods.Temporary Mods Will Restore Physical Separation for Cables
| | | 05000266/LER-1997-042, :on 971030,discovered That Upper Containment Personnel Air Interlock Had Been Inoperable.Caused by Removal of Remote Operating Gear.Reinstalled Remote Operating Connector Gear |
- on 971030,discovered That Upper Containment Personnel Air Interlock Had Been Inoperable.Caused by Removal of Remote Operating Gear.Reinstalled Remote Operating Connector Gear
| 10 CFR 50.73(a)(2)(1) | | 05000266/LER-1997-043-01, Forwards LER 97-043-01,re Discovery That TS Surveillance of Reactor Trip Sys Interlocks Were Not Adequate. Supplemental Info Is Provided at End of Rept.Previous Commitments Made within Rept Also Encl | Forwards LER 97-043-01,re Discovery That TS Surveillance of Reactor Trip Sys Interlocks Were Not Adequate. Supplemental Info Is Provided at End of Rept.Previous Commitments Made within Rept Also Encl | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | | 05000266/LER-1997-044, :on 971216,use of Dedicated Operators During IST of Containment Spray Sys Constituted Operation Prohibited by Ts.Caused by Improper Consideration for Use of Dedicated Operators.Revised Procedures |
- on 971216,use of Dedicated Operators During IST of Containment Spray Sys Constituted Operation Prohibited by Ts.Caused by Improper Consideration for Use of Dedicated Operators.Revised Procedures
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