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1 Wisconsin Electnc POWER COMPANY Point Beach Nuclear Plant (414) 755-2321 6610 Nuclear Rd., Two Rivers. WI 54241 PBL 97-0036 February 4,1997 Document Control Desk US NUCLEAR REGULATORY COMMISSION Mail Station Pl-137 Washington, DC 20555 Ladies / Gentlemen:
DOCKET 50-266 AND 50-301 LICENSEE EVENT REPORT 97-001-00 SAFETY INJECTION DELAY TIMES IIXCEED DESIGN B ASIS VALUES POINT BEACH NUCLEAR PLANT. UNITS 1 AND 2 Enclosed is Licensee Event Report 97-001-00 for Point Peach Nuclear Plant, Units I and 2. This repon is j
provided in accordance with 10 CFR 50.73(a)(2)(ii)(B),"a condition that was outside the design basis of
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the plant." This report describes a condition where delay times assumed for the high and low head safety i
injection flow in the Large Break Loss of Coolant Accident analysis were not conservative.
If you require additional information, please contact us.
Sincerely,
/hrma WY wd.
b ouglas F. Johnson D
Manager-Regulatory Sersices & Licensing JAK f[
Enclosure
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NRC Resident Inspector NRC Regional Administrator, Region 111 9702110350 970204 DR ADOCK 05000266
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. Nic FORM 366 U.S. NUCLEAR REOULATORY COMMISSION APPROVED BY OMB NO. 3150 0104 (4 95)
EXPtRES 04/30/98 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THt$ INFORMATION COLLECTION REQUEST: 50.0 HRS.
LICENSEE EVENT REPORT (LER)
REPORTED LESSONS LEARNED ARE INCORPORATED INTO THE LICENSING PROCESS AND FED BACK TO INDUSTRY.
FORWARD COMMENTS REGARDING BURDEN ESTIMATE (See reverse for required nurnbor of TO THE INFORMATION AND RECORDS MANAGEMENT digits / characters for each block)
BRANCH (T-6 F33L U.S.
NUCLEAR REGULATORY COMMIS$10N, WASHINGTON, DC 20555-0001, AND TO THE PAPERWORK RFDUCTION PROJECT FActLITY NAME til DOCKET NUMBER (2)
P AGE 13)
Point Beach Nuclear Plant, Unit 1 05000266 1 OF 5 TITLE 14)
Safety Injection Delay Times Exceed Design Basis Values EVENT DATE (5) l LER NUMBER (El REPORT D ATE 17)
OTHER FACILITIES INVOLVED 18) s SEQUENTIAL REVISION F ACILITY NAME DOCKET NUMBER MONTH DAY YEAR YEAR NUMBER NUMDER MONTH DAY YEAR PBNP Unit 2 05000301 l
08 l 97 l 97 l
FACILITY NAME DOCKET NUMBER
'01 001 00 02 04 97 05000 l THIS REPORT IS SUBMITTED PUSISUANT TO THE REQUIREMENTS OF 10 CFR 8: { Check one or morel (11)
OPERATING MODE 19)
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20.2203(all2Hiv) 50.36tcH2) 50.73(aH2Hvil) er in NRC Form 388A LICENSEE CONTACT FOR THis LER (12)
NAME TELEPHONE NUMBER linclude Area Codel Jeff Kos, Design Basis Engineer (414) 221-4917 COMPLETE ONE LINE FOR E ACH COMPONENT FAILURE DESCRIBED IN TH18 REPORT (13)
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CAUSE
SYSTEM COMPr"^T l MANUFACRJHER REPORTABLE
CAUSE
SYSTEM COMPONENT MANUFACTURER REPORTABLE TO NPROS TO NPROS i
SUPPLEMENTAL REPORT EXPECTED 114)
EXPECTED MONTH DAY YEAR YES SUSMISSION (If yes, complete EXPECTED SUBMIS$lON DATE).
X NO DATE (15)
ABSTRACT lumrt to 1400 epaces. Lo., opprossmately 15 emg6e-spaced typewrreten hnes) (15)
On January 8,1997, with Unit 1 operating at 90% power and Unit 2 in a refueling shutdown, licensee engineers determined that me delay times assumed for high and low head safety injection (SI) flow in the Large Break Loss of Coolant Accident (LBLOCA) analysis were not conservative. The LBLOCA licensing basis analysis assumed. hat the high and low head SI systems were capable of providing full flow within five and ten seconds respecively. A conservative licensee evaluation concluded that the total delay times may be as high as 8.0 seconds for high head SI and 23.7 seconds for low head SI. The delay time assumptions for the licensing basis analysis did not account for time delays associated with SI signal processing, sequencer delay time uncertainty, or an increased time for pump acceleration to full speed due to degraded voltage conditions. A Westinghouse safety assessment concludes that the increased safety injxtion delay times do not result in exceeding any design or regulatory limit for Point Beach Units 1 and 2.
NRC FORM 366 (495)
NRC FORM 306A U.S. NUCLEGR REGULATORY COMMISSION 84-95)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (U DOCKET NUMBER 12)
LER NUMBER 16)
PAGE (3)
YEAR SEQUENTIAL REVISION
)
Point Beach Nuclear Plant, Unit 1 05000266 NUMBER NUMBER 2 OF 5 i
97 001 00 TEXY tif more space is required. use additional copoes ofIVRC Form 366A) (17}
Event Description
On January 8,1997, with Unit 1 operating at 90% power and Unit 2 in a refueling shutdown, licensee engineers determined that the delay times assumed for the high and low head safety injection (SI) flow in the existing LBLOCA analysis were not conservative. This condition was discovered during a review of the j
stroke time performance requirements for the SI system valves SI-852A,B The existing LBLOCA analysis assumes that the high and low head SI systems are capable of providing full flow within five and ten seconds respectively. These assumptions are based on a 5 second delay for the high head SI pump to come up to speed and a 10 second delay for the low head SI pumps to load on the sequencer and come up to speed. This delay time represents the time from when the SI setpoint is reached to the time when the pumps are capable of providing full flow. The delay time assumptions for the existing licensing basis analysis do not account for (1) time delays associated with SI signal processing, (2)
{ sequencer delay time uncertainty, or (3) an increased time for pump acceleration to full speed due to degraded voltage conditions. When these delays were combined, the licensee evaluation concluded that the total delay times may be as high as 8.0 seconds for high head SI and 23.7 seconds for low head SI. The impact of the increased delay times on the LBLOCA analysis is described below.
The applicable acceptance criteria for the LBLOCA analysis is a peak cladding temperature (PCT) of 2200*F, as identified in 10 CFR 50.46. The most recent submittal (which does not include the results of the additional time delay) to the NRC on ECCS Evaluation Model changes reflects a 109'F penalty in margin allocutions to the licensing basis analysis LBLOCA PCT of 2028 F, resulting in a PCT cf 2137 F.
Westinghouse formally esaluated the increase in the safety injection delay times on the LBLOCA analysis.
The revised cumulative LBLOCA PCT is 2181*F, based on a 44*F penalty due to the longer SI delay times. This evaluation concludes that the calculated maximum fuel element cladding temperature does not exceed 2200 F, the calculated total local oxidation of the cladding nowhere exceeds 0.17 times the total cladding thickness before oxidation, and the calculated total amount of hydrogen generated from the chemical reaction of the cladding with water or steam does not exceed 0.01 times the hypothetical amount that would be generated if all the metal in the cladding cylinders surrounding the fuel, excluding the cladding surrounding the plenum volume, were to react.
Conformance to the criteria above demonstrates that the core geometry is maintained such that the core remains amenable to cooling. The increase in SI system delay will not impact the long-term ability to maintain cora temperature at an acceptably low value and to remove decay 1. eat for an extended period of time required by the long-lived radioactivity remaining in the core. Therefore, the specific safety limits defined by the ECCS Acceptance Criteria of 10 CFR 50.46 for the LBLOCA licensing basis analysis j
including penalties are met.
NQC FORM 366A 14-95)
NRC FOR;.1368A U.S. NUCLEAM REOULATORY COMMISSION 84 95)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FActLITY NAME (1)
DOCKET NUMBER f 2)
LER NUMBER IS)
PAOE (3)
Point Beach Nuclear Plant, Unit 1 05000266 NU ER NU R
3 OF 5 97 001 00 iExi ut more sosce is reewroo. use soonsonal copues or tvRc Form 366A) (1D The IEEE Standard 803A-1983 component identifier for this report is:
Pump (p)
Component and System Description:
The SI system shall deliver borated cooling water to the reactor coolant system during the injection phase of SI to support core cooling and to ensure adequate shutdown margin in the event of a main steam line break.
The licensing basis accident analyses, as described in Chapter 14 of the FSAR, ensure that the SI system is capable of performing these safety-related functions. The LBLOCA analysis (FSAR Section 14.3.2),
SBLOCA (FSAR Section 14.3.1), MSLB (FSAR Section 14.2.5), SGTR (FSAR Section 14.2.4) and the Containment Integrity Evaluation (FSAR Section 14.3.4) assume SI actuation resulting in safety injection flow to the reactor coolant system.
PBNP Technical Specification 15.4.6.A.2 requires that a test be performed to demonstrate the ability of a diesel generator to automatically start, shed load, and restore particular vital equipment to operation following an actualinterruption of normal AC station service power supply to associated engineered safety systems busses together with a simulated safety injection signal. The Technical Specifications require that the test be conducted to assure that the diesel generator will start and assume required load in accordance with the timing sequence listed in FSAR Section 8.2 after the initial starting signal. These acceptance criteria are also listed in Operations Refueling Test (ORT) 3, Appendix C, Attachment 1. The acceptance criteria from this test are used in evaluating the affects on the LBLOCA analysis.
Ccuse:
The existing LBLOCA analysis provides inadequate margin in the SI system delay time assumption to accommodate for time delays associated with SI signal processing, sequencer delay time uncertainty, and an increased time for pump acceleration to full speed due to degraded voltage conditions. The basis for the delay times are a result of typical vendor methodology which may result in a non-conservative LBLOCA analysis with respect to SI system actuation ('elay times. Also, the acceptance cri;eria for the SI sequence test of ORT 3 as described in FSAR sectian 8.2 and ORT 3 Appendix C Attachment 1 should have been thoroughly reviewed to assure tat the times remain within the LBLOCA analysis assumptions.
e N'.C FOLM 36;A U.S. NUCLEAR f.EGULATOAY COMMISSION 14 951 LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME til DOCKET NUMBER (2)
LER NUMBER 16)
PAGEtt j
YEAR SEQUENTIAL REVISION Point Beach Nuclear Plant, Unit 1 05000266 NUMBER NUMBER 4 0F 5 97 001 00 TEXT IIf more space is required. use additional copies of IVRC Form 366A) (17)
Safety Assessment
The specific safety limits defined by the ECCS Acceptance Criteria of 10 CFR 50.46 are met. Therefore, the health and safety of the public is not compromised by the conditions described herem.
1 I
Corrective Actions
The following corrective actions have been taken or are planned to address this event.
1.
Westinghouse has formally evaluated the increase in the safety injection delay times on the LBLOCA analysis. This evaluation determined that the specific safety limits defined by the ECCS Acceptance Criteria of 10 CFR 50.46 impacted by an increase in safety injection delay time for the LBLOCA analysis are met.
2.
Licensee engineers will prepare FSAR change requests to reflect this LBLOCA evaluation.
3.
Licensee engineers will review the SBLOCA (FSAR Section 14.3.1), MSLB (FSAR Section 14.2.5),
SGTR (FSAR Section 14.2.4) and the Containment Integrity Evaluation (FSAR Section 14.3.4) accident analyses. These analyses assume SI actuation resulting in safety injection flow to the reactor coolant system. This review will verify the assumptions associated with SI system delay times are appropriately conservative.
4.
The acceptance criteria for SI sequence test of ORT 3 as described in FSAR sectios 8.2 and ORT 3, Appendix C, Attachment 1, will be reviewed to assure that the delay times associtted with sequenced safeguards components remain within the FSAR Chapter 14 accident ar.alysis assumptions.
Reportability
A 1-hour prompt notification per 10 CFR 50.72(a)(2)(ii)(B) was reported to the NRC duty officer at 1344 CST on January 8,1997. This Licensee Event Report is being submitted in accordance with the requirements of 10 CFR 50.73(a)(2)(ii)(B), "A condition that was outside the design basis of the plant."
NaC FORM 366A 14-95)
i.
e NAC FO;.M 3144 U.S. NUCLEAR REGULATORY COMMISSION 44-95)
+
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1)
DOCKET NUMBER 12)
LER NUMBER (6)
PAGE(3)
YEAR SEQUENTIAL REVISION Point Beach Nuclear Plant, Unit 1 05000266 NUMBER NUMBER 5 OF 5 97 001 00 TEXT (11 more space is requend, use additenal copes of NRC form 366Al (17)
Similar Occurrences:
A search of the LER database discovered a prior occurrence of non-conservative accident analysis assumptions resulting in a system being declared in a condition that is outside the design basis.
LER Iitle 266/96-015-00 Main Steam Safety Valve Lift Setpoints Exceed Design Basis Values i
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| 05000266/LER-1997-001, :on 970108,safety Injection Delay Times Exceeded Design Basis Values.Caused by Degraded Voltage Conditions.Licensee Engineers Will Prepare FSAR Change Requests to Reflect LBLOCA Evaluation |
- on 970108,safety Injection Delay Times Exceeded Design Basis Values.Caused by Degraded Voltage Conditions.Licensee Engineers Will Prepare FSAR Change Requests to Reflect LBLOCA Evaluation
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000301/LER-1997-001, Forwards LER 97-001-00,re Containment Structure Where Internal Containment Structural Members Could Have Damaged Containment Liner During Safe Shutdown Earthquake | Forwards LER 97-001-00,re Containment Structure Where Internal Containment Structural Members Could Have Damaged Containment Liner During Safe Shutdown Earthquake | | | 05000301/LER-1997-001-01, :on 970107,containment Liner Clearance Was Not IAW Plant Design Basis.Caused by Void Between Containment Liner & Concrete Containment Structure.Inspected Containment |
- on 970107,containment Liner Clearance Was Not IAW Plant Design Basis.Caused by Void Between Containment Liner & Concrete Containment Structure.Inspected Containment
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) | | 05000266/LER-1997-002, :on 970109,potential to Overpressurize Piping Between Containment Isolation Valves Occurred.Caused by Original Design Not Providing Overpressure Protection for Piping.Review Completed |
- on 970109,potential to Overpressurize Piping Between Containment Isolation Valves Occurred.Caused by Original Design Not Providing Overpressure Protection for Piping.Review Completed
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000301/LER-1997-002-01, :on 970415,potential Reactor Coolant Sys Branch Connection Stresses Beyond Design Basis,Indicated.Caused by Mod Initiated to Remove RTD Bypass Line Isolation Valves. Stress Analysis Conducted on RTD Bypass Piping |
- on 970415,potential Reactor Coolant Sys Branch Connection Stresses Beyond Design Basis,Indicated.Caused by Mod Initiated to Remove RTD Bypass Line Isolation Valves. Stress Analysis Conducted on RTD Bypass Piping
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000266/LER-1997-003, :on 970109,did Not Perform Leak Test on Spare Containment Penetrations Per Ts.Caused by Lack of Routine Testing.Tested Penetrations W/Satisfactory Results |
- on 970109,did Not Perform Leak Test on Spare Containment Penetrations Per Ts.Caused by Lack of Routine Testing.Tested Penetrations W/Satisfactory Results
| 10 CFR 50.73(a)(2)(1) | | 05000301/LER-1997-004-01, :on 970729,declared RHR Loop Inoperable Due to CCW Leak.Caused by Failure of RHR Heat Exchanger CCW Piping. Repaired Piping & Declared RHR Loop Operable |
- on 970729,declared RHR Loop Inoperable Due to CCW Leak.Caused by Failure of RHR Heat Exchanger CCW Piping. Repaired Piping & Declared RHR Loop Operable
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000266/LER-1997-004, :on 970113,potential for Particular Common Mode Failure That Could Affect Opposite Trains of Unit 2 Safeguards Equipment Was Noted.Caused by Lack of Physical Separation.Replaced Subject Circuit Breakers |
- on 970113,potential for Particular Common Mode Failure That Could Affect Opposite Trains of Unit 2 Safeguards Equipment Was Noted.Caused by Lack of Physical Separation.Replaced Subject Circuit Breakers
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000301/LER-1997-005-01, :on 970806,RHR Pump Was Declared Inoperable Due to Abnormal Seal Leakage from Loop a RHR 2P-10A.Repaired RHR Pump |
- on 970806,RHR Pump Was Declared Inoperable Due to Abnormal Seal Leakage from Loop a RHR 2P-10A.Repaired RHR Pump
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000266/LER-1997-005, :on 970116,1SI-852A Was Not Tested IAW Inservice Test Program Required by Tss.Caused Because Condition Revealed That Valve 1SI-852A Had Not Been Completely Tested.Tests Will Be Reviewed |
- on 970116,1SI-852A Was Not Tested IAW Inservice Test Program Required by Tss.Caused Because Condition Revealed That Valve 1SI-852A Had Not Been Completely Tested.Tests Will Be Reviewed
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) | | 05000266/LER-1997-006, :on 970120,refueling Cavity Drain Failed During Loca.Caused by Inadequate Evaluation of Original Design.Design of Refueling Cavity Drains Was Revised with Respect Capability to Withstand an Earthquake |
- on 970120,refueling Cavity Drain Failed During Loca.Caused by Inadequate Evaluation of Original Design.Design of Refueling Cavity Drains Was Revised with Respect Capability to Withstand an Earthquake
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000266/LER-1997-007, :on 970124,determined That Potential Existed for EDG Overload Condition.Caused by Failure to Recognize This Condition When Plants Initially Licensed W/Two Edgs. Implemented Procedure Changes |
- on 970124,determined That Potential Existed for EDG Overload Condition.Caused by Failure to Recognize This Condition When Plants Initially Licensed W/Two Edgs. Implemented Procedure Changes
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000266/LER-1997-008, :on 970131,non-seismic Ductwork Located Above safety-related Equipment in Containment Occurred.Caused by Incomplete Seismic Evaluation.Mods Will Be Completed During Current Unit 2 Refueling Outage |
- on 970131,non-seismic Ductwork Located Above safety-related Equipment in Containment Occurred.Caused by Incomplete Seismic Evaluation.Mods Will Be Completed During Current Unit 2 Refueling Outage
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000266/LER-1997-009, :on 970214,potential for Safety Injection Failure During Filling of Safety Injection Accumulator Discovered.Caused by Situation Not Adequately Covered by Procedures.Procedure OI-100 Revised |
- on 970214,potential for Safety Injection Failure During Filling of Safety Injection Accumulator Discovered.Caused by Situation Not Adequately Covered by Procedures.Procedure OI-100 Revised
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000266/LER-1997-010, :on 970219,svc Water & Component Cooling Water TS Action Requirements Were Not Met.Caused Because Licensee Did Not Comply W/Cold Shutdown Requirements of TS 15.3.3.C.2 & 15.3.3.D.2.Evaluations Were Performed |
- on 970219,svc Water & Component Cooling Water TS Action Requirements Were Not Met.Caused Because Licensee Did Not Comply W/Cold Shutdown Requirements of TS 15.3.3.C.2 & 15.3.3.D.2.Evaluations Were Performed
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000266/LER-1997-011, :on 970305,containment Fan Cooler Accident Fans Were Not Tested in Accordance with Tss.Caused by non-conservative Interpretation of Literal Requirements of Tss.Unit 1 & 2 Accident Fans Were Tested |
- on 970305,containment Fan Cooler Accident Fans Were Not Tested in Accordance with Tss.Caused by non-conservative Interpretation of Literal Requirements of Tss.Unit 1 & 2 Accident Fans Were Tested
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(1) | | 05000266/LER-1997-012, :on 970304,diesel-drive Fire Pump Day Tank Not Sampled IAW TSs.Non-conservative Interpretation of TS Led to Failure.Day Tank T-30 Sample Was Drawn & Analyzed W/Satisfactory Results |
- on 970304,diesel-drive Fire Pump Day Tank Not Sampled IAW TSs.Non-conservative Interpretation of TS Led to Failure.Day Tank T-30 Sample Was Drawn & Analyzed W/Satisfactory Results
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(1) | | 05000266/LER-1997-013, :on 970304,CCWS Found Not in Accordance W/ Plant Design Basis.Caused by Inoperable Valve Due to Overtorquing in Closed position.Cross-tie Will Be Resolved |
- on 970304,CCWS Found Not in Accordance W/ Plant Design Basis.Caused by Inoperable Valve Due to Overtorquing in Closed position.Cross-tie Will Be Resolved
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000266/LER-1997-013-01, Forwards Suppl LER 97-013-01,re Component Cooling Water Sys Not IAW Plant Design Basis.Rept Replaces LER 97-013-00 in Its Entirety & Includes Addl Similar Occurrence Not Previously Reported to NRC | Forwards Suppl LER 97-013-01,re Component Cooling Water Sys Not IAW Plant Design Basis.Rept Replaces LER 97-013-00 in Its Entirety & Includes Addl Similar Occurrence Not Previously Reported to NRC | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000266/LER-1997-014, :on 970321,auxiliary Feedwater Sys Inoperability Due to Loss of Instrument Air.Design Mods Initiated,Providing Pneumatic Supply to Control Valves |
- on 970321,auxiliary Feedwater Sys Inoperability Due to Loss of Instrument Air.Design Mods Initiated,Providing Pneumatic Supply to Control Valves
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000266/LER-1997-015, :on 970324,control Room Ventilation Sys Declared Inoperable Due to Failures of Backdraft Damper & Vent Duct Access Door.Backdraft Damper,Replaced |
- on 970324,control Room Ventilation Sys Declared Inoperable Due to Failures of Backdraft Damper & Vent Duct Access Door.Backdraft Damper,Replaced
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000266/LER-1997-016, :on 970325,SG Level Logic Was Not Tested IAW Ts.Caused by Nonconservative Interpretation of Tss.Ts Amends Proposed to Provide Consistency Between Test Requirements & LCO Associated W/Sg Tests |
- on 970325,SG Level Logic Was Not Tested IAW Ts.Caused by Nonconservative Interpretation of Tss.Ts Amends Proposed to Provide Consistency Between Test Requirements & LCO Associated W/Sg Tests
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000266/LER-1997-017, :on 920508,containment Third Door Was Blocked Open During Refueling Operations.Caused by Interpretation That Movement of Core Components Per TS Definitions Rather than Literal Wording.Routine Maintenance Procedure Revised |
- on 920508,containment Third Door Was Blocked Open During Refueling Operations.Caused by Interpretation That Movement of Core Components Per TS Definitions Rather than Literal Wording.Routine Maintenance Procedure Revised
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000266/LER-1997-018, :on 970403,potential for RHR Overpressure During Accidents Was Discovered.Original Design Did Not Provide Overpressure Protection for Isolated Piping Section. Evaluation Was Performed to Determine Stress on Piping |
- on 970403,potential for RHR Overpressure During Accidents Was Discovered.Original Design Did Not Provide Overpressure Protection for Isolated Piping Section. Evaluation Was Performed to Determine Stress on Piping
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000266/LER-1997-019, :on 970404,RHR Not Aligned IAW TS Requirements. Caused by non-conservative Decision Making & Not Recognizing When TS Were Not Controlling Plant Operations.Pbnp Mgt Philosophy Re TS Interpretations Changed to Minimize Use |
- on 970404,RHR Not Aligned IAW TS Requirements. Caused by non-conservative Decision Making & Not Recognizing When TS Were Not Controlling Plant Operations.Pbnp Mgt Philosophy Re TS Interpretations Changed to Minimize Use
| 10 CFR 50.73(a)(2)(1) | | 05000266/LER-1997-020-01, Forwards LER 97-020-01,describing Plant Conditions in Which Ability to Achieve & Maintain Safe Shutdown in Event of Postulated Fire May Have Been Adversely Affected | Forwards LER 97-020-01,describing Plant Conditions in Which Ability to Achieve & Maintain Safe Shutdown in Event of Postulated Fire May Have Been Adversely Affected | 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor | | 05000266/LER-1997-021, :on 970430,determined That Spent Fuel Pool Cooling Sys Was Not in Accordance W/Plant Design Basis.Cause Indeterminate.Closed & re-tagged Valves SF-27 & SF-28 & Investigated Basis for Fsar,App a |
- on 970430,determined That Spent Fuel Pool Cooling Sys Was Not in Accordance W/Plant Design Basis.Cause Indeterminate.Closed & re-tagged Valves SF-27 & SF-28 & Investigated Basis for Fsar,App a
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000266/LER-1997-022, :on 970507,discovered That Postulated Control Room Fire May Cause Electrical Hot Short That Disables Limit or Torque Switches for Certain Movs.Mods Initiated to Remedy Condition |
- on 970507,discovered That Postulated Control Room Fire May Cause Electrical Hot Short That Disables Limit or Torque Switches for Certain Movs.Mods Initiated to Remedy Condition
| 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor | | 05000266/LER-1997-023, :on 970508,discovered Noncompliant Emergency Lighting for Postulated App R Fires.Caused by Alternative Provisions Made in Original Safe Shutdown Analysis.Emergency Lights Will Be Installed |
- on 970508,discovered Noncompliant Emergency Lighting for Postulated App R Fires.Caused by Alternative Provisions Made in Original Safe Shutdown Analysis.Emergency Lights Will Be Installed
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000266/LER-1997-024, :on 970501,determined Post Accident Sampling Sys Degradation.Caused by Inadequate Design Review.Will Upgrade Containment Atmosphere Sample Sys & Will Perform Mod to Reduce Dose within GDC 19 Dose Limits |
- on 970501,determined Post Accident Sampling Sys Degradation.Caused by Inadequate Design Review.Will Upgrade Containment Atmosphere Sample Sys & Will Perform Mod to Reduce Dose within GDC 19 Dose Limits
| | | 05000266/LER-1997-025, :on 970520,pressurizer Level Was Controlled Higher than Assumed in Accident Analysis.Caused by Inappropriately Changing Procedures W/O Adequate Consideration.Listed Affected Procedures Will Be Revised |
- on 970520,pressurizer Level Was Controlled Higher than Assumed in Accident Analysis.Caused by Inappropriately Changing Procedures W/O Adequate Consideration.Listed Affected Procedures Will Be Revised
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000266/LER-1997-026, :on 970521,discovered TS Violation of Operability Requirement of MSL Isolation.Caused by Inadequate Consideration for Operability of All Required Functions.Verified Low RCS Sys Average Temp |
- on 970521,discovered TS Violation of Operability Requirement of MSL Isolation.Caused by Inadequate Consideration for Operability of All Required Functions.Verified Low RCS Sys Average Temp
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000266/LER-1997-027, :on 970521,non-environmentally Qualified Matl Existed in Containment Hatch Applications.Caused by Inadequate Design Review.Mods Will Be Performed to Remove Existing Teflon Material |
- on 970521,non-environmentally Qualified Matl Existed in Containment Hatch Applications.Caused by Inadequate Design Review.Mods Will Be Performed to Remove Existing Teflon Material
| | | 05000266/LER-1997-031, :on 970619,discovered That Auxiliary Feedwater (AFW) Pump Low Suction Pressure Trip Setpoints May Not Ensure Adequate Suction Pressure Protection for AFW Pumps Following Tornado Event.Caused by Inadequate Design |
- on 970619,discovered That Auxiliary Feedwater (AFW) Pump Low Suction Pressure Trip Setpoints May Not Ensure Adequate Suction Pressure Protection for AFW Pumps Following Tornado Event.Caused by Inadequate Design
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000266/LER-1997-032, :on 970630,discovered Inadequately Rated Electrical Buses Could Disable Switchgear & Cause Secondary Fires.Caused by Characteristic of Original Design. Established twice-per-shift Fire Watches |
- on 970630,discovered Inadequately Rated Electrical Buses Could Disable Switchgear & Cause Secondary Fires.Caused by Characteristic of Original Design. Established twice-per-shift Fire Watches
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000266/LER-1997-034, :on 970707,discovered Unplanned Loss of Voltage on Train B Safeguards Buses.Caused by Inadequate Design & Design Review for Installation of New Train B Edgs.Incorrect Wiring Reworked |
- on 970707,discovered Unplanned Loss of Voltage on Train B Safeguards Buses.Caused by Inadequate Design & Design Review for Installation of New Train B Edgs.Incorrect Wiring Reworked
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000266/LER-1997-035, :on 970516,discovered Inadequate Seismic Support for Reactor Coolant Pump Rotor Stand.Caused by Rotor Stand Being Stored Since Initial Plant Construction.Moved Rotor Stand & Verified as Seismically Adequate |
- on 970516,discovered Inadequate Seismic Support for Reactor Coolant Pump Rotor Stand.Caused by Rotor Stand Being Stored Since Initial Plant Construction.Moved Rotor Stand & Verified as Seismically Adequate
| 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat | | 05000266/LER-1997-036, :on 970826,potential Common Mode Failure in DC Power Supply Which Could Disable AFW Sys Was Noted.Caused by Inadequate Design & Design Review.Plant Mods Were Performed to Eliminate Potential Common Mode Failure |
- on 970826,potential Common Mode Failure in DC Power Supply Which Could Disable AFW Sys Was Noted.Caused by Inadequate Design & Design Review.Plant Mods Were Performed to Eliminate Potential Common Mode Failure
| | | 05000266/LER-1997-037, :on 970903,potential Failure of EDG Load Sequence Occurred.Caused by Inadequate Design of EDG Load Sequencing Logic.Mod Restored Operability of EDG During Load Sequencing |
- on 970903,potential Failure of EDG Load Sequence Occurred.Caused by Inadequate Design of EDG Load Sequencing Logic.Mod Restored Operability of EDG During Load Sequencing
| | | 05000266/LER-1997-038, :on 970926,determined That Inoperability of Standby Emergency Power Placed Unit 2 in 7-day Lco.Caused by Failure That Occurred When EDG G-03 Was Shutdown.Repaired Governor & Returned EDG G-03 to Service |
- on 970926,determined That Inoperability of Standby Emergency Power Placed Unit 2 in 7-day Lco.Caused by Failure That Occurred When EDG G-03 Was Shutdown.Repaired Governor & Returned EDG G-03 to Service
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000266/LER-1997-039-01, :on 970615,RHR Loop Inoperable.Caused by Removal of CCW Pump from Svc.Ccw Pump Restored |
- on 970615,RHR Loop Inoperable.Caused by Removal of CCW Pump from Svc.Ccw Pump Restored
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000266/LER-1997-039, Forwards LER 97-039-00 Re RHR Loop Inoperable,Due to Inoperable CCW Pump.New Commitments within Rept Indicated in Italics | Forwards LER 97-039-00 Re RHR Loop Inoperable,Due to Inoperable CCW Pump.New Commitments within Rept Indicated in Italics | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000266/LER-1997-040-01, Forwards LER 97-040-01 Which Documents Event That Occurred at Point Beach Nuclear Plant,Unit 1.Commitments Made within Ltr,Encl | Forwards LER 97-040-01 Which Documents Event That Occurred at Point Beach Nuclear Plant,Unit 1.Commitments Made within Ltr,Encl | 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000266/LER-1997-041, :on 971023,potential Common Mode Failure in Afws Control Circuits Was Noted.Caused by AFW Control Circuits Installed by Plant Mods.Temporary Mods Will Restore Physical Separation for Cables |
- on 971023,potential Common Mode Failure in Afws Control Circuits Was Noted.Caused by AFW Control Circuits Installed by Plant Mods.Temporary Mods Will Restore Physical Separation for Cables
| | | 05000266/LER-1997-042, :on 971030,discovered That Upper Containment Personnel Air Interlock Had Been Inoperable.Caused by Removal of Remote Operating Gear.Reinstalled Remote Operating Connector Gear |
- on 971030,discovered That Upper Containment Personnel Air Interlock Had Been Inoperable.Caused by Removal of Remote Operating Gear.Reinstalled Remote Operating Connector Gear
| 10 CFR 50.73(a)(2)(1) | | 05000266/LER-1997-043-01, Forwards LER 97-043-01,re Discovery That TS Surveillance of Reactor Trip Sys Interlocks Were Not Adequate. Supplemental Info Is Provided at End of Rept.Previous Commitments Made within Rept Also Encl | Forwards LER 97-043-01,re Discovery That TS Surveillance of Reactor Trip Sys Interlocks Were Not Adequate. Supplemental Info Is Provided at End of Rept.Previous Commitments Made within Rept Also Encl | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | | 05000266/LER-1997-044, :on 971216,use of Dedicated Operators During IST of Containment Spray Sys Constituted Operation Prohibited by Ts.Caused by Improper Consideration for Use of Dedicated Operators.Revised Procedures |
- on 971216,use of Dedicated Operators During IST of Containment Spray Sys Constituted Operation Prohibited by Ts.Caused by Improper Consideration for Use of Dedicated Operators.Revised Procedures
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