05-12-2016 | At 0649 on March 15, 2016 with Unit 1 shut down in MODE 5 for refueling activities, a boric acid indication upstream of the valve seating surface on the inlet of the valve body of 1CV-200B, Letdown Orifice B Outlet Control Valve was identified as a through-wall flaw. The flaw location was within the reactor coolant system ( RCS) pressure boundary as defined by 10 CFR 50.2, "Definitions." The valve body is original plant equipment.
This event is being reported pursuant to 10 CFR 50.73(a)(2)(ii)(A) for material defects in the primary coolant system that were not acceptable in accordance with ASME Section Xl.
APPROVED BY OMB: NO. 3150.0104 EXPIRES: 01/31/2017 Reported lessons learned are incorporated into the licensing process and fed back to industry.
Send comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Wa shing ton, DC 20555-0001, or by intemet e-mail to Infocollects.Resource©nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection. |
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Category:Letter
MONTHYEARML24295A0862024-10-21021 October 2024 Notification of NRC Baseline Inspection and Request for Information Inspection Report 0500026/2025002 L-2024-120, LAR 301 - Revise Renewed Facility Operating Licenses to Adopt an Alternative Approach for Addressing Seismic Risk in 10 CFR 50.69 Risk-Informed Categorization2024-10-0808 October 2024 LAR 301 - Revise Renewed Facility Operating Licenses to Adopt an Alternative Approach for Addressing Seismic Risk in 10 CFR 50.69 Risk-Informed Categorization L-2024-118, Fleet License Amendment Request to Relocate Staff Qualifications from Technical Specifications to the Quality Assurance Topical Report (FPL-1)2024-10-0808 October 2024 Fleet License Amendment Request to Relocate Staff Qualifications from Technical Specifications to the Quality Assurance Topical Report (FPL-1) L-2024-158, Supplemental Information to License Amendment Request to Adopt Common Emergency Plan with Site-Specific Annexes2024-09-25025 September 2024 Supplemental Information to License Amendment Request to Adopt Common Emergency Plan with Site-Specific Annexes IR 05000266/20240112024-09-18018 September 2024 Biennial Problem Identification and Resolution Inspection Report 05000266/2024011 and 05000301/2024011 L-2024-136, Supplement to License Amendment Request to Adopt Common Emergency Plan with Site-Specific Annexes2024-09-16016 September 2024 Supplement to License Amendment Request to Adopt Common Emergency Plan with Site-Specific Annexes L-2024-145, Notification of Deviation from EPRI MRP-227, Revision 1-A Baffle Bolt Inspection Frequency2024-09-0909 September 2024 Notification of Deviation from EPRI MRP-227, Revision 1-A Baffle Bolt Inspection Frequency ML24207A0202024-08-28028 August 2024 Response to Request for Re-Engagement Regarding the Subsequent License Renewal Environmental Review for Point Beach Nuclear Plant, Units 1 and 2 (Docket Numbers: 50-0266 and 50-0301) IR 05000266/20240052024-08-21021 August 2024 Updated Inspection Plan for Point Beach Nuclear Plant, Units 1 and 2 (Report 05000266/2024005 and 05000301/2024005) IR 05000266/20240022024-08-13013 August 2024 Integrated Inspection Report 05000266/2024002 and 05000301/2024002 L-2024-131, Response to Request for Additional Information Regarding License Amendment Request 300, Modify Containment Average Air Temperature Requirements2024-08-0909 August 2024 Response to Request for Additional Information Regarding License Amendment Request 300, Modify Containment Average Air Temperature Requirements ML24163A0012024-08-0505 August 2024 LTR-24-0119-1-1 Response to Nh Letter Regarding Review of NextEras Emergency Preparedness Amendment Review ML24214A3092024-08-0202 August 2024 Confirmation of Initial License Examination L-2024-113, License Amendment Request 294, Application to Revise Technical Specifications to Adopt TSTF- 577, Revised Frequencies for Steam Generator Tube Inspections2024-07-24024 July 2024 License Amendment Request 294, Application to Revise Technical Specifications to Adopt TSTF- 577, Revised Frequencies for Steam Generator Tube Inspections ML24194A1802024-07-24024 July 2024 – Revision to the Reactor Vessel Material Surveillance Capsule Withdrawal Schedule L-2024-125, Notice of Intent to Provide Supplemental Information to License Amendment Request to Adopt Common Emergency Plan with Site-Specific Annexes2024-07-24024 July 2024 Notice of Intent to Provide Supplemental Information to License Amendment Request to Adopt Common Emergency Plan with Site-Specific Annexes IR 05000266/20244012024-07-23023 July 2024 Public - Point Beach Nuclear Plant Cyber Security Inspection Report 05000266/2024401 and 05000301/2024401 ML24193A2432024-07-12012 July 2024 – Interim Audit Summary Report in Support of Review of License Amendment Requests Regarding Fleet Emergency Plan L-2024-116, Preparation and Scheduling of Operator Licensing Examinations2024-07-11011 July 2024 Preparation and Scheduling of Operator Licensing Examinations IR 05000266/20240102024-07-10010 July 2024 Age-Related Degradation Inspection Report 05000266/2024010 and 05000301/2024010 L-2024-114, Quality Assurance Topical Report (FPL-1 Revision 31 Annual Submittal2024-07-10010 July 2024 Quality Assurance Topical Report (FPL-1 Revision 31 Annual Submittal L-2024-105, License Amendment Request 300, Modify Containment Average Air Temperature Requirements2024-06-26026 June 2024 License Amendment Request 300, Modify Containment Average Air Temperature Requirements L-2024-107, Schedule for Subsequent License Renewal Environmental Review2024-06-25025 June 2024 Schedule for Subsequent License Renewal Environmental Review ML24176A2242024-06-24024 June 2024 Notification of an NRC Biennial Licensed Operator Requalification Program Inspection and Request for Information L-2024-102, Official Service List Update2024-06-19019 June 2024 Official Service List Update ML24149A2862024-06-12012 June 2024 NextEra Fleet - Proposed Alternative Frr 23-01 to Use ASME Code Case N-752-1, Risk-Informed Categorization and Treatment for Repair/Replacement Activities in Class 2 and 3 Systems Section X1, Division 1 (EPID L-2023-LLR-0009) - Letter L-2024-093, Steam Generator Divider Plate Assemblies Bounding Analysis Evaluation for Aging Management Commitment 14 Revision2024-06-10010 June 2024 Steam Generator Divider Plate Assemblies Bounding Analysis Evaluation for Aging Management Commitment 14 Revision IR 05000266/20244202024-06-0505 June 2024 Security Baseline Inspection Report 05000266/2024420 and 05000301/2024420 ML24149A1922024-05-28028 May 2024 Notification of NRC Baseline Inspection and Request for Information ML24141A1382024-05-20020 May 2024 Information Request to Support the NRC Annual Baseline Emergency Action Level and Emergency Plan Changes Inspection.Docx ML24127A0632024-05-0606 May 2024 Supplemental Information to License Amendment Request to Adopt Common Emergency Plan with Site-Specific Annexes IR 05000266/20243012024-04-29029 April 2024 NRC Initial License Examination Report 05000266/2024301; 05000301/2024301 L-2024-067, Annual Monitoring Report2024-04-26026 April 2024 Annual Monitoring Report ML24116A0402024-04-23023 April 2024 Periodic Update of the Updated Final Safety Analysis Report ML24071A0912024-04-22022 April 2024 Issuance of Relief Request I6-RR-03 - Extension of the Unit 2 Steam Generator Primary Nozzle Dissimilar Metal Welds Sixth 10-Year Inservice Inspection Program Interval IR 05000266/20240012024-04-11011 April 2024 Integrated Inspection Report 05000266/2024001 and 05000301/2024001 L-2024-030, Supplement to Relief Request CISl-03-01 for Relief Concerning Containment Unbonded Post-Tensioning System Inservice Inspection Requirements2024-03-27027 March 2024 Supplement to Relief Request CISl-03-01 for Relief Concerning Containment Unbonded Post-Tensioning System Inservice Inspection Requirements L-2024-043, Revised Reactor Vessel Materials Surveillance Capsule Withdrawal Schedules2024-03-25025 March 2024 Revised Reactor Vessel Materials Surveillance Capsule Withdrawal Schedules L-2024-011, and Point Beach, Units 1 and 2 - 10 CFR 50.46 Annual Reporting of Changes to, or Errors in Emergency Core Cooling System Models or Applications2024-03-13013 March 2024 and Point Beach, Units 1 and 2 - 10 CFR 50.46 Annual Reporting of Changes to, or Errors in Emergency Core Cooling System Models or Applications IR 05000266/20230062024-02-28028 February 2024 Annual Assessment Letter for Point Beach Nuclear Plant, Units 1 and 2 (Report 05000266/2023006 and 05000301/2023006) ML24053A3732024-02-22022 February 2024 Operator Licensing Examination Approval Point Beach, March 2024 L-2024-020, Refueling Outage Owners Activity Report (OAR-1) Unit 1 for Inservice Inspections2024-02-22022 February 2024 Refueling Outage Owners Activity Report (OAR-1) Unit 1 for Inservice Inspections ML24036A2652024-02-0505 February 2024 Notice of Inspection and Request for Information for the NRC Age-Related Degradation Inspection: Inspection Report 05000266/2024010 and 05000301/2024010 IR 05000266/20230042024-02-0101 February 2024 Integrated Inspection Report 05000266/2023004 and 05000301/2023004 ML24030A0352024-01-30030 January 2024 Information Request for the Cyber-Security Baseline Inspection, Notification to Perform Inspection L-2024-001, Relief Request CISl-03-01 for Relief Concerning Containment Unbonded Post-Tensioning System Inservice Inspection Requirements2024-01-26026 January 2024 Relief Request CISl-03-01 for Relief Concerning Containment Unbonded Post-Tensioning System Inservice Inspection Requirements L-2024-010, Point Units 3 and 4, Seabrook, Duane Arnold, and Point Beach Units 1 and 2, Nuclear Property Insurance - 10 CFR 50.54(w)(3)2024-01-25025 January 2024 Point Units 3 and 4, Seabrook, Duane Arnold, and Point Beach Units 1 and 2, Nuclear Property Insurance - 10 CFR 50.54(w)(3) ML24005A3242024-01-24024 January 2024 Exemption from Select Requirements of 10 CFR Part 73 (EPID L-2023-LLE-0040 (Security Notifications, Reports, and Recordkeeping and Suspicious Activity Reporting)) ML23352A2752024-01-23023 January 2024 Issuance of Amendment Nos. 274 and 276 Regarding Revision to Technical Specification 5.5.17, Pre-Stressed Concrete Containment Tendon Surveillance Program L-2023-173, Quality Assurance Topical Report (FPL-1) Revision 30 Update2023-12-15015 December 2023 Quality Assurance Topical Report (FPL-1) Revision 30 Update 2024-09-09
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000266/LER-2017-0032017-12-13013 December 2017 Degraded Condition, LER 17-003-00 for Point Beach Nuclear Plant, Unit 1, Regarding Degraded Condition 05000266/LER-2017-0022017-12-13013 December 2017 Operation or Condition Prohibited by Technica Specifications, LER 17-002-00 for Point Beach Nuclear Plant, Unit 1, Regarding Operation or Condition Prohibited by Technical Specifications 05000266/LER-2017-0012017-11-16016 November 2017 Control Room Barrier Inadvertently Disabled, LER 17-001-00 for Point Beach, Unit 1, Regarding Control Room Barrier Inadvertently Disabled 05000266/LER-2016-0032016-06-0101 June 2016 Operation or Condition Prohibited by Technical Specifications, LER 16-003-00 for Point Beach, Unit 1, Regarding Operation or Condition Prohibited by Technical Specifications 05000266/LER-2016-0022016-05-31031 May 2016 Operation or Condition Prohibited by Technical Specifications, LER 16-002-00 for Point Beach, Unit 1, Regarding Operation or Condition Prohibited by Technical Specifications 05000266/LER-2016-0012016-05-12012 May 2016 Unit 1 Degraded Condition, LER 16-001-00 for Point Beach, Unit 1, Regarding Degraded Condition 2017-12-13
[Table view] |
Description of the Event:
At 0649 on March 15, 2016 with Unit 1 shut down in MODE 5 for refueling activities, a boric acid indication upstream of the valve seating surface on the inlet of the valve body of 1CV-200B, Letdown Orifice B Outlet Control Valve was identified as a through-wall flaw. The flaw location was within the reactor coolant system (RCS) pressure boundary as defined by 10 CFR 50.2, "Definitions." The valve body is original plant equipment.
The Unit 1 Letdown Orifice B Outlet Control Valve (1CV-200B) has been replaced and returned to service.
This 60 day licensee event report is being submitted in accordance with the requirements of 10 CFR 50.73(a)(2)(ii)(A) for any event or condition that results in the condition of the nuclear power plant, including its principal safety barriers, being degraded. The material defect in the primary coolant system could not be found acceptable in accordance with ASME Section XI, IWB-3600, "Analytical Evaluation of Flaws" or ASME Section XI, Table IWB-3410-1, "Acceptance Standards.
Cause of the Event:
The most likely cause of the degraded barrier was localized corrosion near a sand inclusion indication in the valve body.
Analysis of the Event:
Maintenance activities identified a through-wall flaw on the valve body of the Letdown Orifice B Outlet Control Valve. The flaw location was upstream of the valve seating surface, on the inlet of the valve body. 1CV-200B is one of three valves in parallel in the same application. The valve was within the RCS pressure boundary, which is defined as being connected to the RCS, up to and including the outermost containment isolation valve in system piping which penetrates the primary reactor containment. A causal evaluation determined the through-wall flaw in the valve body to most likely be the result of localized corrosion near a sand inclusion indication. The indication was identified during the manufacturing examination and testing processes. The indication was accepted by the manufacturer using the acceptance criteria of ASTM Specification E71, "Reference Radiographs for Steel Casting up to 2 inches in Thickness." The localized corrosion most likely allowed system contents to leech through the sand inclusion. The valve body is original plant equipment and has been in service the entire life of the plant. The flaw has been corrected by replacement of the valve body.
Corrective Actions:
The Unit 1 Letdown Orifice B Outlet Control Valve (1CV-200B) has been replaced and returned to service. Destructive testing will be performed on the removed valve to validate the apparent cause. Additional actions/reviews will be taken as required following receipt of the destructive testing report. Examinations have been completed as part of the extent of condition on three valves from the same heat number that had manufacturing indications. A corrective action has been created to perform a visual examination of one additional valve during the next refueling outage.
Safety Significance:
The event was determined to be of very low safety significance. 1CV-200B can be isolated from the RCS by a remotely operated valve 1RC-427, Reactor Coolant Loop B Cold Leg to Charging and Volume Control System (CVCS) Letdown Isolation Valve. Components with similar sand inclusion indications have been or will be visually examined for evidence of boric acid indications. While the condition was present, there was no loss of any safety systems, structures or components needed to shut down the reactor, maintain safe shutdown conditions, remove residual heat, control the release of radioactive material or mitigate the consequences of an accident. There was no impact on the health and safety of the public as a result of this condition.
Similar Events:
There have not been similar events of this degraded condition in the past three years.
Component Failure Data:
2 INCH-1500 LB COPES-VULCAN MODEL 63 GLOBE VALVE