:on 970509,drywell Equipment Drain Sump & Floor Drain Sump Covers Were Not Constructed IAW Design Drawings, Due to Original Construction Error.Design Change Package Has Been Completed| ML20140D073 |
| Person / Time |
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| Site: |
Quad Cities  |
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| Issue date: |
05/29/1997 |
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| From: |
Peterson C COMMONWEALTH EDISON CO. |
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| To: |
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| Shared Package |
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| ML20140D038 |
List: |
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| References |
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| LER-97-004-06, LER-97-4-6, NUDOCS 9706100223 |
| Download: ML20140D073 (5) |
|
text
LICENSEE EVEST REPORT (LER)
Form Rsv. 2.0 F.cihry Name (1)
Docka Number G)
Page (3)
Quad Cities Unit Two 0l5l0l0l0l2l6l5 1 l of l 0 l 5 4
I l
k(>ry)well Equipment Drain Sump and the Drywell Floor Drain Sump covers were constructed not in accordance sith surement of the Technical Specification for primary containment leatage, due to an original construction error.
t Event Data (5)
LER Nurnber (6)
Report Date (7)
Other Facilities lavolved (3)
Month Day Year Year Sequential Revision Month Day Year Facihty Docket Numberts)
Number Number Names 0l5l0l0l0l l
l 0l5 0l9 9l7 9l7 0l0l4 o
0 0
5 2
9 9
7 0j5l0l0l0l l
l C'PERATING Tlw REPORT IS SUBM s a a:.u PU LSUnNT ' r0 T 4E REQU REk ENTS OF 10CFR MODE (9)
(Check one or more of the foDowing) (11) 0 20.402(b) 20.405(c) 50.73(a)(2)6v) 73.71(b)
POWER 20 405(a)(1)6) 50.36(c)(1) 50.73(a)C)(v)
- - 73.71(c)
LEVEL 20.405(a)(1)6i) 50.36(c)(2) 50.73(a)(2)(vii)
Other (Specify (10) l l
0
- - 20.405(a)(1)6ii) 50.73(a)(2)6) 50.73(a)(2)(viii)(A) in Abstract 20.405(a)(1)(iv) x 50.73(a)(2)6i) 50.73(a)(2)(viii)(B) below and in 20.405(a)(1)(v) 50.73(a)(2)(iii) 50.73(a)(2)(x)
Text)
LICENSEE CON TACT FOR THIS LER (12) 504E TELEPHONE NUMBER AREA CODE Charles Peterson, Regulatory Affairs Manager, ext. 3609 3 ol9 6l5l4l-l2l2l4l1 COMPLETE ONE LINE FOR EACH COMK)NENT FALLURE DESCRIBED IN ' FHIS REPORT (13)
~fXUIL SYSm4 COMPONENT MANUFACTURER REPORTABM CAU5E 5YSTEM COMPONENT MANUFACTURER REPORTABM TD NPRDS TO NPRD5 l
1 1
I I
I I
I I
I I
I I
I I
I I
I I
I I
I I
I I
I SUPPEMENTAL REPORT EXPECTT.D (14)
Expected Month Day Year Subaussion lYES (If yes, complete EXPECTED SUBMISSION DATE) 70 Deze (15) l l
l ABS TRACT (Lama no 1400 speece, i.e., approinnatety fifteen smgle-spece tyyewnnen imes) (16)
ABSTRACT:
Quad Cities Nuclear Station Unit Two was shutdown for refueling with no fuel in the reactor at the time of discovery for this event.
Chemistry personnel were sampling the drywell sumps when they noticed that the sump covers appeared to be opposite to what they were expecting.
Investigation proved that the Drywell Equipment Drain Sump and the Drywell 'loor Drain Sump cover were not constructed per design drawings. This sump cover problem afr2 cts the accurate measurement of the Technical Specification for primary containment leakage. The plant was shutdown at the time of this event and there was no immediate consequences.
The crysell sump covers construction error had no impact on the current operation of this or any other system.
The apparent cause of this event was an error during plant construction.
The actual root cause is unknown. The short term response to this event was to modify the Unit Two sump covers so that they now can meet Technical Specifications and to verify Unit One's sump covers by viewing them on video tape.
The long term response is to visually verify the Unit One sump covers are installed as p r design during the next refueling outage.
There was no impact on health / safety of on-site personnel or to the public. The effect of wrong sump covers on identification of reactor coolant leakage was minimal.
9706100223 97o530 ADOCK0500g5 DR LER265\\97\\004.WPF
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LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Fonn Ra.0 ACILTTY N AME (t)
DOCKE'T NUMBDt (2)
LER NUMBER (6)
PAGI )
f Year Sequenual Revision Number Number Cities Unit Two 0l5l0l0l0l2l6l5 9l7 0l0l4 0l0 2 [OFl 0 l 5
. pm Energy Industry identification System (EH5) codes are identified in the text as [XX]
PLANT AND SYSTEN IDENTIFICATION:
General Electric - Boiling Water Reactor - 2511 MWt rated core thermal power.
EVENT IDENTIFICATION:
The Drywell Equipment Drain Sump and the Drywell Floor Drain Sump covers were constructed not in accordance with design drawings, which affected the accurate measurement of the Technical Sp:cification for primary containment leakage, due to an original construction error.
A.
CONDITIONS PRIOR TO EVENT
Unit:
2 Event Date:
050997 Event Time:
1830 l
Reactor Mode: 0 Mode Name:
Refueling Power Level: 000%
This report was initiated by Licensee Event Report 265\\97-004.
No fuel in the reactor.
B.
DESCRIPTION OF EVENT
The Unit Two reactor was shutdown for refueling with no fuel in the reactor and Chemistry p Department personnel were taking routine samples from the Drywell Equipment Drain Sump d (DWEDS)[WK] and the Drywell Floor Drain Sump (DWFDS)[WK]. During the event personnel questioned which sump they were sampling since the sump covers appeared to be reversed from that which they were expecting.
Chemistry requested that Operations investigate whether the correct sump covers were on the sumps.
An operator was sent into the drywell and he concurred that the covers were on the wrong sumps. On 042497 at 1700 the operator then initiated Problem Investigation Form (PIF) 97-1980 and submitted it to the Shift Engineer (SE).
During the discovery of this event and afterwards the plant was in a stable condition.
The PIF was sent to Mechanical Maintenance who then examined the sump covers to determine if they were installed on the wrong sumps during cleaning. During this inspection they discovered that this was not the case. Due to the construction of the sumps, the grating would only fit on the DWEDS and the deck plate will only fit on the DWFDS. Therefore this problem has existed since the plant was initially constructed.
Since the sump covers could not simply be switched, Mechanical Maintenance wrote a Site Engineering Service Request (SESR) on 050197 to have Design Engineering provide a design change to make the sump covers as per the design drawings.
When Design Engineering received the SESR, they questioned the reportability screening because the DWFDS would not collect unidentified leakage occurring directly below the reactor. This concern is based on Technical Specification (TS) 3.6/4.6.H which states that reactor coolant system leakage shall be limited to:
1.
No pressure boundary leakage 2.
Less than or equal to 25 Gallons per Minute (GPM) averaged over any 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> surveillance period 3.
Less than or equal to 5 GPM unidentified leakage k
4.
Less than or equal to 2 GPM increase in unidentified leakage with any period of 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> or less (Applicable in operational mode 1 only)
LER265\\97\\004.WPF
LICENSEE EVENT REPC'IT (LER) TEXT COPUINUATION Form Rev. 2.0 ACILITY N AME (1)
DOCKET NUMBER G)
LER NUMBER (6)
PAGE (3)
Year Sequermal Revision Number Number Cities Unit Two ol5]ololol2l6l5 9l7 0lol4 olo 3 lOFl o l 5 y a Energy Industry identification System (Ells) codes are idenu6ed in the text as [XX]
With any pressure boundary leakage the unit must be in hot shutdown within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and in cold shutdown within the next 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. With the reactor coolant system unidentified leakage or total leakage rate (s) greater than the above limit (s) the unit would be required to reduce the leakage to within the limits within four hours or be in at least hot shutdown within the next 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and in cold shutdown within the following 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.
On 050697 at 1830 the Shift Engineer requested that System Engineering provide an Operability / Concern screening on the issue of the reduced ability of the DWFDS to detect unidentified leakage.
On 050997 System Engineering concluded that the DWFDS sump was unable to function as per design due to the DWFDS cover construction error preventing operations from properly monitoring unidentified leakage in the drywell in modes 1,2 or 3.
An LER was initiated.
This event applies to Unit Two only; video tape footage has been reviewed to visually verify that the Unit One sump covers are installed as per design.
C.
CAUSE OF THE EVENT
The covers installed in Unit 2 on the DWEDS and DWFDS do not agree with the configurations identified on design drawings. These applicable design drawings call for the DWEDS to have one quarter inch checkered deck plate installed over the opening while the DWFDS is identified as utilizing one and one half inch grating over the opening. The actual installed conditions are reversed. During original construction, a concrete frame recessed one and one half inch in the concrete floor was built around the DWEDS.
This was
(
intended to allow installation of a one and one half inch grating flush with the finished concrete.
The DWFDS was constructed with a concrete frame recessed one fourth inch in the concrete floor.
Additionally, steel bracing members were installed in the sump.
This installation sequence was intended provide adequate support and a flush installation of one fourth inch thick deck plating. This construction sequence is reversed from that shown on the design drawings. The as found construction of the sump covers therefore do not allow for the sump covers to be interchanged.
The apparent cause of this event is a error during the construction phase of Quad Cities Unit Two. The actual root cause is unknown.
The effect of the construction error is a reduction in the capability to accurately measure unidentified leakage directly under the Reactor Pressure Vessel (RPV) as described in the Quad Cities Updated Final Safety Analysis Report (UFSAR). Unidentified leakage inside the bioshield would have been previously mischaracterized as identified leakage.
Unidentified leakage collected in the floor drains outside of the bioshield wall is still directed to the DWFDS. The actual leakage would still have been collected and pumped to the radwaste system as per design intent. Additionally, the Unit One DWFDS and DWEDS covers have been visually verified on videotape to be in the correct orientation.
This issue therefore pertains only to Unit Two.
No other plant system or component would have been affected by this event.
O LER265\\971004.WPF
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LICENSEE EVENT REPC2T (LER) TEXT CONTIM ATION Form Rev. 2.0 1
ACILTTY NAME (1)
DothI NUMBER (2)
LER NUMBER (6)
PAGE 0)
Year sequential Revision i
Cities Unit Two.
0l5 0l0l0l2 6l5 9l7 0l0l4 0l0 4 lOFl 0 l 5 y: E...s Industry Identification 5ystem (t;ns) codes are identit ed in the text as (XXl l
D.
SAFETY ANALYSIS 0F THE EVENT:
i j
There was no impact on health / safety of on-site personnel or to the public.
i The DWEDS is used to collect " identified" leakage from the recirc pumps, relief valves, l
and other equipment via hard piped drain lines. The DWFDS is used to collect
" unidentified" leakage, or all other leakage other than the known possible inputs that go l
into the DWEDS. TS 3.6/4.6H and UFSAR section 5.2.5.5 requires shutdown of the reactor when unidentified leakage exceeds 5 GPM and/or when the total of identified and i
unidentified leakage exceeds 25 GPM.
Also since 092396, the TS require that the reactor must be shutdown if unidentified leakage increases by more than 2 GPM from the previous 24 I
hour period. With the DWEDS and DWFDS covers switched on Unit 2, operations could not i
accurately determine unidentified leakage directly under the reactor vessel.
If the leakage is inside the bioshield (i.e. Control Rod Drives (CRD), Low Power Reactivity L
Monitors (LPRM), or other leakage) then the water on the floor is supposed to go to the DWFDS and be counted as unidentified leakage. But with the grating covering the DWEDS, the unidentified leakage would have been mis-identified as "known" leakage. Leakage outside of the bioshield would have been collected by the floor drains and directed to the correct sumps for unidentified leakage detection, i
A small break Loss of Coolant Accident (LOCA) may be discovered by other methods. A large i
increase in DWEDS leakage rate would cause immediate concern by Operations and System O Engineering. Chemistry would take samples to determine the source of the leakage (i.e.
reactor coolant, Reactor Building Closed Cooling Water (RBCCW)....etc.). Also an increase in drywell temperature and pressure might be noticed.
In fact, a large leak inside the drywell would probably occur outside of the bioshield since this is where the majority of the valves, pumps, piping, and other equipment exists and would be correctly identified as
" unidentified" leakage.
System-Engineering has analyzed available drywell sump leakage data for the period of 1987 i
- - 1997.
In this analysis, both the DWEDS and DWFDS leakage was combined and counted as a single leakage amount minus the " identified" recirc pump seal leakage. The recirc pump seal leakage is a known quantity of approximately one and one half GPM. All leakage other than the recirc pump was considered unidentified leakage. Also, hydrostatic testing of the reactor coolant system pressure boundary after every refueling outage has shown no unidentified leakage inside of the bioshield that would have affected leakage calculations.
Based on this analysis System Engineering has determined that the TS for reactor coolant pressure boundary leakage has not been violated during this period. Data 1
from years previous to 1987 was also sampled and not TS violations were identified.
E.
CORRECTIVE ACTIONS
Corrective Actions Completed:
1.
Design Change Package (DCP) 9700171 has been completed to drill holes in the DWFDS deck plates and to install new deck plates on top of the DWEDS grating so that they now meet their original design functions and Technical Specifications.
2.
Video tape footage of the Unit One DWEDS and DWFDS was reviewed to determine that the sump covers were of the correct type.
LER265\\97WO4.WPF
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LICENSEE EVENT R1 : iRT (lek, TEXT CONTINUATION Form Rrv. 2.0 s a FACILrry NAME (1)
DCK ; ' NUMBER G)
LER NUMBER (6)
PAGE (3)
Year Sequenual Revision Nurnber Number Cities Unit Two 0l5l0l0l0l2l6l5 9l7
- - l0l0l4 0l0
$ lOFj 0 l 5 i c.A a Energy industry idenuficauon System (EUS) codes are idenu6ed in the text as [XX)
Corrective Actions to be Completed:
The Unit One DWEDS and DWFDS will be examined to verify the video tape determination during the next refueling shutdown to ensure the covers on that unit are installed per the applicable design drawings (System Engineering, NTS 265-180-97-004-01). This will be completed during refueling outage QlR15.
F.
PREVIOUS EVENTS:
Previous LERs related to plant construction errors are:
LER l-96-015 HPCI whip restraint J1HP-3 improperly installed due to inadequate supervisory oversight, documentation provisions and QA/QC programs.
G.
COMPONENT FAILURE DATA
There is no component failure associated with this event.
O OG LER265\\97\\004.WPF
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| | | Reporting criterion |
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| 05000254/LER-1997-001, :on 970117 & 07,discovered TS Required,Once Per Shift Channel Check Readings Not Completed within Required Twelve H Time Interval Plus 25% Max Allowable Extension. Caused by Personnel Error.Readings Performed |
- on 970117 & 07,discovered TS Required,Once Per Shift Channel Check Readings Not Completed within Required Twelve H Time Interval Plus 25% Max Allowable Extension. Caused by Personnel Error.Readings Performed
| 10 CFR 50.73(a)(2)(1) | | 05000265/LER-1997-001-01, :on 970227,initiation of High Pressure Coolant Injection Occurred Due to Deficient Procedures.Will Revise Surveillance Procedures,Will Review Prerequisites of All Im Procedures & Will Communicate Mgt Expectations to Personne |
- on 970227,initiation of High Pressure Coolant Injection Occurred Due to Deficient Procedures.Will Revise Surveillance Procedures,Will Review Prerequisites of All Im Procedures & Will Communicate Mgt Expectations to Personnel
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(B) | | 05000265/LER-1997-001, Forwards LER 97-001-00 Re Automatic Actuation of Any Esf. Commitments Made by Ltr,Listed | Forwards LER 97-001-00 Re Automatic Actuation of Any Esf. Commitments Made by Ltr,Listed | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000265/LER-1997-001-07, :on 970227,instrument Maintenance Dept Was Performing Procedure to Test HPCI Initiation Logic.Caused by Deficient Procedure.Order Was Issued for All non-routine |
- on 970227,instrument Maintenance Dept Was Performing Procedure to Test HPCI Initiation Logic.Caused by Deficient Procedure.Order Was Issued for All non-routine
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii)(A) | | 05000254/LER-1997-002-02, :on 970127,several Isolable Piping Sections Could Experience Stresses Above Update FSAR Allowables Due to post-loss of Coolant Accident Thermal Pressurization. Initial Operability Evaluation Was Completed on 970124 |
- on 970127,several Isolable Piping Sections Could Experience Stresses Above Update FSAR Allowables Due to post-loss of Coolant Accident Thermal Pressurization. Initial Operability Evaluation Was Completed on 970124
| | | 05000254/LER-1997-002, Forwards LER 97-002-00 Documenting Condition That Was Discovered at Quad Cities Nuclear Power Station.Util Commitments Made within Ltr,Listed | Forwards LER 97-002-00 Documenting Condition That Was Discovered at Quad Cities Nuclear Power Station.Util Commitments Made within Ltr,Listed | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | | 05000265/LER-1997-002-05, :on 970228,unit 2 Was Shutdown,Because Four Main Steam Relief Valve Closure Time Did Not Meet IST Program Limits.Ist Acceptance Criteria for PORVs Will Be Revised Using Data Obtained from Qcos 0203-03 on 022897 |
- on 970228,unit 2 Was Shutdown,Because Four Main Steam Relief Valve Closure Time Did Not Meet IST Program Limits.Ist Acceptance Criteria for PORVs Will Be Revised Using Data Obtained from Qcos 0203-03 on 022897
| | | 05000265/LER-1997-002-01, :on 970301,Unit 2 Was Shutdown Per TS 3.5.A & 3.6.F.Caused by Personnel Cognitive Error.Containment Procedure Changes Were Implemented to Prevent Containment Pressure Suppression Bypass |
- on 970301,Unit 2 Was Shutdown Per TS 3.5.A & 3.6.F.Caused by Personnel Cognitive Error.Containment Procedure Changes Were Implemented to Prevent Containment Pressure Suppression Bypass
| | | 05000265/LER-1997-002, Forwards LER 97-002-00 Re Condition Prohibited by Plant Tss. Util Commitments Made by Ltr,Listed | Forwards LER 97-002-00 Re Condition Prohibited by Plant Tss. Util Commitments Made by Ltr,Listed | 10 CFR 50.73(a)(2)(1) | | 05000254/LER-1997-003, Forwards LER 97-003-00 IAW 10CFR50.73(a)(2)(v)(B)(D). Procedure Qcap 0307-02, ASME Section XI Repair & Replacement Program Preparation, Attachment a, Section XI Repair/Replacement Program Will Be Revised Re VT-2 | Forwards LER 97-003-00 IAW 10CFR50.73(a)(2)(v)(B)(D). Procedure Qcap 0307-02, ASME Section XI Repair & Replacement Program Preparation, Attachment a, Section XI Repair/Replacement Program Will Be Revised Re VT-2 | 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat | | 05000265/LER-1997-003-04, :on 970321,2B Core Spray Room Cooler Fouled Due to Hydrolyzing Debris.Cs Room Cooler Was Cleaned Under Nwr 960039336-01 & Qctp 1110-12, ECCS Room Cooler Trending Program, Has Recently Been Rewritten |
- on 970321,2B Core Spray Room Cooler Fouled Due to Hydrolyzing Debris.Cs Room Cooler Was Cleaned Under Nwr 960039336-01 & Qctp 1110-12, ECCS Room Cooler Trending Program, Has Recently Been Rewritten
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000254/LER-1997-003-05, :on 970429,visual Exam (VT-2) Was Not Performed Due to Procedural Deficiencies Following HPCI Sys Valve Replacement Required by Asme,Section XI & TS Section 4.0.E. Examined VT-2 of 1-2301-45 Valve |
- on 970429,visual Exam (VT-2) Was Not Performed Due to Procedural Deficiencies Following HPCI Sys Valve Replacement Required by Asme,Section XI & TS Section 4.0.E. Examined VT-2 of 1-2301-45 Valve
| | | 05000265/LER-1997-003-01, Forwards LER 97-003-01 Re Core Spray Room Cooler 2B That Fouled Due to Hydrolyzing Debris.Commitment Listed | Forwards LER 97-003-01 Re Core Spray Room Cooler 2B That Fouled Due to Hydrolyzing Debris.Commitment Listed | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000265/LER-1997-004, Forwards LER 97-004-00,IAW 10CFR50.73(a)(2)(ii)(B).Unit 1 DWEDS & DWFDS Will Be Examined to Verify Video Tape Determination During Next Refueling Shutdown to Ensure Covers on Unit Installed Per Applicable Design Drawings | Forwards LER 97-004-00,IAW 10CFR50.73(a)(2)(ii)(B).Unit 1 DWEDS & DWFDS Will Be Examined to Verify Video Tape Determination During Next Refueling Shutdown to Ensure Covers on Unit Installed Per Applicable Design Drawings | 10 CFR 50.73(a)(2) | | 05000265/LER-1997-004-06, :on 970509,drywell Equipment Drain Sump & Floor Drain Sump Covers Were Not Constructed IAW Design Drawings, Due to Original Construction Error.Design Change Package Has Been Completed |
- on 970509,drywell Equipment Drain Sump & Floor Drain Sump Covers Were Not Constructed IAW Design Drawings, Due to Original Construction Error.Design Change Package Has Been Completed
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000254/LER-1997-004-03, :on 961026,RHR Svc Water Pumps Declared Inoperable Due to Inadequate Evaluation of Replacement Pump Casing Bolts.Rhrsw Pump Bolting Inspected & Questionable Bolting Replaced |
- on 961026,RHR Svc Water Pumps Declared Inoperable Due to Inadequate Evaluation of Replacement Pump Casing Bolts.Rhrsw Pump Bolting Inspected & Questionable Bolting Replaced
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000254/LER-1997-005-03, :on 970319,HPCI Subsystem Was Made Inoperable to Protect Equipment Due to Uncertainties Re Abandoned Power Feed Cable,Which Had Been Inappropriately Abandoned. Plant Design Documents Have Been Updated |
- on 970319,HPCI Subsystem Was Made Inoperable to Protect Equipment Due to Uncertainties Re Abandoned Power Feed Cable,Which Had Been Inappropriately Abandoned. Plant Design Documents Have Been Updated
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(viii)(A) | | 05000254/LER-1997-005, Forwards LER 97-005-00 IAW Requirements of 10CFR50.73(a)(2)(v)(D) W/Listed Commitments | Forwards LER 97-005-00 IAW Requirements of 10CFR50.73(a)(2)(v)(D) W/Listed Commitments | 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000265/LER-1997-005-01, Forwards LER 97-005-01 Re Unit 2 Reactor Placed in Mode 2 W/O Required Number of Emergency Diesel Generators Operable. Commitment Listed | Forwards LER 97-005-01 Re Unit 2 Reactor Placed in Mode 2 W/O Required Number of Emergency Diesel Generators Operable. Commitment Listed | 10 CFR 50.73(a)(2)(1) | | 05000265/LER-1997-005-02, :on 970608,Unit 2 Reactor Was Placed in Mode 2 W/O Required Number of EDGs Operable.Caused by Installation of Replacement Air Start Motors Which Did Not Have Same Characteristics as Original Motors.Revised Alternate Parts |
- on 970608,Unit 2 Reactor Was Placed in Mode 2 W/O Required Number of EDGs Operable.Caused by Installation of Replacement Air Start Motors Which Did Not Have Same Characteristics as Original Motors.Revised Alternate Parts
| 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) | | 05000265/LER-1997-006, Forwards LER 97-006-00 Re Cable in Unit 2 Being in Same Fire Area as Fire of Concern Due to Ineffective Implementation of Original Safe Shutdown Analysis.List of Commitments Provided | Forwards LER 97-006-00 Re Cable in Unit 2 Being in Same Fire Area as Fire of Concern Due to Ineffective Implementation of Original Safe Shutdown Analysis.List of Commitments Provided | 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor | | 05000265/LER-1997-006-01, :on 970729,cable 20865 Was Located in Same Turbine Bldg Fire Area as Fire of Concern & Could Have Been Damaged by Fire.Caused by Poor Work Practices.Revised Qarp 1000-01, Safe Shutdown Procedure C1 |
- on 970729,cable 20865 Was Located in Same Turbine Bldg Fire Area as Fire of Concern & Could Have Been Damaged by Fire.Caused by Poor Work Practices.Revised Qarp 1000-01, Safe Shutdown Procedure C1
| | | 05000254/LER-1997-006-03, :on 970327,loss of Reactor Coolant Inventory in Excess of Design Basis Limits Occurred Due to Inadequate Procedural Guidance.Procedure Qcop 1200-07 Was Revised to Administratively Control Power Feed Breaker |
- on 970327,loss of Reactor Coolant Inventory in Excess of Design Basis Limits Occurred Due to Inadequate Procedural Guidance.Procedure Qcop 1200-07 Was Revised to Administratively Control Power Feed Breaker
| | | 05000254/LER-1997-006, Forwards LER 97-006,Rev 00 & Submits Commitments Related to LER | Forwards LER 97-006,Rev 00 & Submits Commitments Related to LER | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000265/LER-1997-006-06, :on 970729,cable for Unit 2 in Same Fire Area as Fire of Concern Due to Ineffective Implementation of Original Safe Shutdown Analysis.Rev to Ssd Analysis to Credit Alternate Power Feeds,Will Be Performed |
- on 970729,cable for Unit 2 in Same Fire Area as Fire of Concern Due to Ineffective Implementation of Original Safe Shutdown Analysis.Rev to Ssd Analysis to Credit Alternate Power Feeds,Will Be Performed
| | | 05000254/LER-1997-007-03, :on 970331,unit One Emergency DG Inadvertently Started Due to Error by RSO While Operating Control Switch. Nso Removed from All Licensed Duties Until Completion of Remediation Plan |
- on 970331,unit One Emergency DG Inadvertently Started Due to Error by RSO While Operating Control Switch. Nso Removed from All Licensed Duties Until Completion of Remediation Plan
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000254/LER-1997-008, Forwards LER 97-008,Rev 00 & Submits Commitments.Revised Qcop 2300-13 Is to Include Steps to Fully Disengage Turning Gear If Necessary for Testing Purposes | Forwards LER 97-008,Rev 00 & Submits Commitments.Revised Qcop 2300-13 Is to Include Steps to Fully Disengage Turning Gear If Necessary for Testing Purposes | 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000254/LER-1997-008-01, :on 970402,high Pressure Coolant Injection Was Inoperable Due to Turning Gear Failure.Turbine Turning Gear Was Manually Engaged |
- on 970402,high Pressure Coolant Injection Was Inoperable Due to Turning Gear Failure.Turbine Turning Gear Was Manually Engaged
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000265/LER-1997-008, Forwards LER 97-008-00 IAW Requirements of 10CFR50.73(a)(2)(i)(B).Commitments Made by Ltr,Listed | Forwards LER 97-008-00 IAW Requirements of 10CFR50.73(a)(2)(i)(B).Commitments Made by Ltr,Listed | 10 CFR 50.73(a)(2)(1) | | 05000265/LER-1997-008-05, :on 970629,five Control Rod Drives Did Not Receive Required Scram Insertion Time Testing Prior to 40% Power.Caused by Ineffective Operations.Rods Associated with Nwr Were Scram Timed & Declared Operable |
- on 970629,five Control Rod Drives Did Not Receive Required Scram Insertion Time Testing Prior to 40% Power.Caused by Ineffective Operations.Rods Associated with Nwr Were Scram Timed & Declared Operable
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000254/LER-1997-009, Forwards LER 97-009-00 Per 10CFR50.73(a)(2)(v)(D).Commitment Included in Ltr | Forwards LER 97-009-00 Per 10CFR50.73(a)(2)(v)(D).Commitment Included in Ltr | 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000254/LER-1997-009-03, :on 970504,both Trains of Standby Gas Treatment Sys Were Inoperable.Caused by Cognitive Peersonnel Error. Blown Fuse Replaced,A Train of SBGTS Was Tested & Declared Operable & SRO Test Director Counseled |
- on 970504,both Trains of Standby Gas Treatment Sys Were Inoperable.Caused by Cognitive Peersonnel Error. Blown Fuse Replaced,A Train of SBGTS Was Tested & Declared Operable & SRO Test Director Counseled
| | | 05000265/LER-1997-009-05, :on 970713,control Room Personnel Misread Indication Delaying Discovery of Abnormal Offgas Radiation Readings Was Discovered.Caused by Personnel Error.Chemistry Sampled off-gas |
- on 970713,control Room Personnel Misread Indication Delaying Discovery of Abnormal Offgas Radiation Readings Was Discovered.Caused by Personnel Error.Chemistry Sampled off-gas
| 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(s)(2)(v) | | 05000254/LER-1997-010-02, :on 970407,train B of Control Room HVAC Sys Was Inoperable Due to Loss of Refrigerant.Caused by Failed Fitting.Replaced Fitting & Sys Tested Satisfactorily |
- on 970407,train B of Control Room HVAC Sys Was Inoperable Due to Loss of Refrigerant.Caused by Failed Fitting.Replaced Fitting & Sys Tested Satisfactorily
| | | 05000265/LER-1997-010-05, :on 970819,2B Offgas Hydrogen Analyzer Declared Inoperable.Caused by Communication Error.Offgas Hydrogen Sample Immediately Taken & Analyzed & Technicians Involved Counseled |
- on 970819,2B Offgas Hydrogen Analyzer Declared Inoperable.Caused by Communication Error.Offgas Hydrogen Sample Immediately Taken & Analyzed & Technicians Involved Counseled
| | | 05000265/LER-1997-010, Forwards LER 97-010-00 IAW Requirements of 10CFR50.73(a)(2)(i)(B).No Commitments Made | Forwards LER 97-010-00 IAW Requirements of 10CFR50.73(a)(2)(i)(B).No Commitments Made | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000254/LER-1997-010, Forwards LER 97-010-00 Which Repts Event That Occurred at Quad Cities Nuclear Station,Per 10CFR50.73(a)(2)(v)(D). Commitment Made by Ltr,Submitted | Forwards LER 97-010-00 Which Repts Event That Occurred at Quad Cities Nuclear Station,Per 10CFR50.73(a)(2)(v)(D). Commitment Made by Ltr,Submitted | 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000254/LER-1997-011-01, :on 970409,RHRSW Sys Was Made Inoperable Due to Uncertainties Related to 4 Kv Air magne-blast Horizontal Gas Circuit Breakers.Caused by Improper Manufacturers Switch Mounting Design.Pif 97-1276 Written to Investigate Cause |
- on 970409,RHRSW Sys Was Made Inoperable Due to Uncertainties Related to 4 Kv Air magne-blast Horizontal Gas Circuit Breakers.Caused by Improper Manufacturers Switch Mounting Design.Pif 97-1276 Written to Investigate Cause
| | | 05000254/LER-1997-011, Forwards LER 97-011-00 Re an Event or Condition That Alone Could Have Prevented Fulfillment of Safety Function of Structures or Sys That Are Needed to Remove Residual Heat. Commitments Made by Ltr,Submitted | Forwards LER 97-011-00 Re an Event or Condition That Alone Could Have Prevented Fulfillment of Safety Function of Structures or Sys That Are Needed to Remove Residual Heat. Commitments Made by Ltr,Submitted | 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(1) | | 05000265/LER-1997-011-05, :on 970904,determined That Offgas H Sampling Frequency Was Less than That Required by Ts.Caused by Inadequate Tracking of LCO Actions Re Recombiner Temp.Began Sampling at Four H Intervals |
- on 970904,determined That Offgas H Sampling Frequency Was Less than That Required by Ts.Caused by Inadequate Tracking of LCO Actions Re Recombiner Temp.Began Sampling at Four H Intervals
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000265/LER-1997-012-06, :on 971121,loss of Shutdown Cooling Due to Loss of Power to Reactor Protection Bus 2B.Caused by Undervoltage Condition at RPS 2B Bus When Bus Was Loaded.Voltage Regulating Transformer Cleaned & Adjusted |
- on 971121,loss of Shutdown Cooling Due to Loss of Power to Reactor Protection Bus 2B.Caused by Undervoltage Condition at RPS 2B Bus When Bus Was Loaded.Voltage Regulating Transformer Cleaned & Adjusted
| | | 05000254/LER-1997-013, Forwards LER 97-013-00 Re Any Single Cause of Inoperable Independent Train or Channel in Single Sys Designed to Remove Residual Heat.Commitments Made by Ltr,Listed | Forwards LER 97-013-00 Re Any Single Cause of Inoperable Independent Train or Channel in Single Sys Designed to Remove Residual Heat.Commitments Made by Ltr,Listed | 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | | 05000254/LER-1997-013-01, :on 970416,RCIC Area High Temperature Switch Would Not Actuate Due to Excess Sealing Varnish Applied by Technician.Caused by Personnel Error.Removed Excess Varnish from Switch,Calibrated & Functionally Tested Switch |
- on 970416,RCIC Area High Temperature Switch Would Not Actuate Due to Excess Sealing Varnish Applied by Technician.Caused by Personnel Error.Removed Excess Varnish from Switch,Calibrated & Functionally Tested Switch
| | | 05000254/LER-1997-014, Forwards LER 97-014-00 Per 10CFR50.73(a)(2)(i)(B).Listed Commitment Made by Ltr | Forwards LER 97-014-00 Per 10CFR50.73(a)(2)(i)(B).Listed Commitment Made by Ltr | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000254/LER-1997-014-01, :on 970416,target Rock Safety Relief Valve Removed from Unit 2 During Q2R13 & Unit 1 During Q1R14 Were Not Tested within 12 Months.Caused by Defective Procedure. Revised Maintenance Procedure |
- on 970416,target Rock Safety Relief Valve Removed from Unit 2 During Q2R13 & Unit 1 During Q1R14 Were Not Tested within 12 Months.Caused by Defective Procedure. Revised Maintenance Procedure
| | | 05000265/LER-1997-015-05, :on 970622,TS Required Surveillance Was Not Properly Performed Due to Apparent Unfamiliarity w/10CFR50 Appendix G Which Resulted in Insufficient Tp.Cause Is Under Investigation.No Action Taken at Present Time |
- on 970622,TS Required Surveillance Was Not Properly Performed Due to Apparent Unfamiliarity w/10CFR50 Appendix G Which Resulted in Insufficient Tp.Cause Is Under Investigation.No Action Taken at Present Time
| | | 05000254/LER-1997-015, Informs NRC of Change of Committed Due Date Contained in LER 97-015,dtd 970812.Station Changing Due Date of Commitment to 990528 | Informs NRC of Change of Committed Due Date Contained in LER 97-015,dtd 970812.Station Changing Due Date of Commitment to 990528 | | | 05000254/LER-1997-015-02, :on 970622,discovered That 10CFRE50,App G Pressure Testing Requirements Were Not Met.Caused by Failure of Station Personnel to Recognize All Organizational Challenges Which Could Occur in Controlling.Performed Test |
- on 970622,discovered That 10CFRE50,App G Pressure Testing Requirements Were Not Met.Caused by Failure of Station Personnel to Recognize All Organizational Challenges Which Could Occur in Controlling.Performed Test
| | | 05000254/LER-1997-016-01, :on 970509,DG CW IST Requirements Were Not Completed When Inaccurate Predefined Work Request Used for Scheduling Was Implemented.Caused by Inappropriately Titled Work Request.Qcos 6600-08 Was Completed for Unit 1 |
- on 970509,DG CW IST Requirements Were Not Completed When Inaccurate Predefined Work Request Used for Scheduling Was Implemented.Caused by Inappropriately Titled Work Request.Qcos 6600-08 Was Completed for Unit 1
| | | 05000254/LER-1997-016, Forwards LER 97-016-00 Re DG CW IST Requirements Not Being Completed When Inaccurate Predefined Work Request Was Implemented | Forwards LER 97-016-00 Re DG CW IST Requirements Not Being Completed When Inaccurate Predefined Work Request Was Implemented | 10 CFR 50.73(a)(2)(1) |
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