Similar Documents at Perry |
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Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20212J2011999-09-30030 September 1999 Safety Evaluation Supporting Transfer of Dl Ownership Interest in PNPP to Ceico ML20212A6881999-08-31031 August 1999 Safety Evaluation Supporting Amend 106 to License NPF-58 ML20207G2741999-06-0707 June 1999 Safety Evaluation Concluding That Firstenergy Flaw Evaluation Meets Rules of ASME Code & That IGSCC & Thermal Fatigue Crack Growth Need Not Be Considered in Application ML20206G6451999-05-0303 May 1999 Safety Evaluation Authorizing Requests for Relief IR-032 to IR-035 & IR-037 to IR-040 Re Implementation of Subsections IWE & Iwl of ASME Section XI for Containment Insp ML20206E2261999-04-29029 April 1999 Safety Evaluation Concluding That Proposed Alternatives Will Result in Acceptable Level of Quality & Safety.Authorizes Use of Code Case N-504 for Weld Overlay Repair of FW Nozzle Weld at PNPP & Use of Table IWB-3514 ML20205P4371999-04-15015 April 1999 Safety Evaluation Concluding That Licensee Performed Appropriate Evaluations of Operational Configurations of safety-related power-operated Gate Valves to Identify Valves Susceptible to Pressure Locking or Thermal Binding ML20205G4221999-03-31031 March 1999 Safety Evaluation Accepting Second 10-yr Interval IST Program Releif Requests for Plant,Unit 1 ML20205E0591999-03-26026 March 1999 Safety Evaluation Supporting Amend 105 to License NPF-58 ML20205D6921999-03-26026 March 1999 Safety Evaluation Supporting Amend 104 to License NPF-58 ML20205D3101999-03-26026 March 1999 Safety Evaluation Supporting Amend 103 to License NPF-58 ML20205C3761999-03-26026 March 1999 Safety Evaluation Supporting Request for Proposed Exemption to 10CFR50,app a GDC 19 ML20204C0711999-03-11011 March 1999 Safety Evaluation Supporting Amend 102 to License NPF-58 ML20207F4361999-03-0303 March 1999 Safety Evaluation Supporting Amend 101 to License NPF-58 ML20207L4881999-02-24024 February 1999 Safety Evaluation Supporting Amend 100 to License NPF-58 ML20203F8381999-02-0808 February 1999 Safety Evaluation Supporting Amend 97 to License NPF-58 ML20203A5961999-02-0202 February 1999 Safety Evaluation Accepting Licensee Proposed Revs to Responsibilities of Plant Operations Review Committee as Described in Chapter 17.2 of USAR ML20203A5211999-01-27027 January 1999 Safety Evaluation Accepting Licensee Calculations Showing That Adequate NPSH Will Be Available for HPCS Pumps ML20198R8921999-01-0707 January 1999 SER Accepting Licensee Proposed Amend to TSs to Delete Reference to NRC Policy Re Plant Staff Working Hours & Require Administrative Controls to Limit Working Hours to Be Acceptable ML20198J0031998-12-22022 December 1998 SER Accepting Licensee Response to GL 92-08,ampacity Derating Issues for Perry Nuclear Power Plant,Unit 1 ML20198K9071998-12-21021 December 1998 Safety Evaluation Supporting Amend 96 to License NPF-58 ML20196J4731998-12-0202 December 1998 Safety Evaluation Supporting Amend 95 to License NPF-58 ML20196D2751998-11-23023 November 1998 Safety Evaluation Supporting Amend 94 to License NPF-58 ML20195F6891998-11-0505 November 1998 Safety Evaluation Accepting Proposed Reduction in Commitment in Quality Assurance Program to Remove Radiological Assessor Position ML20153B8221998-09-16016 September 1998 Safety Evaluation Accepting Changes to USAR Section 13.4.3, 17.2.1.3.2.2,17.2.1.3.2.2.3 & App 1A ML20153D0311998-09-15015 September 1998 Safety Evaluation Supporting Amend 93 to License NPF-58 ML20249A1891998-06-11011 June 1998 SER on Moderate Energy Line Pipe Break Criteria for Perry Nuclear Power Plant,Unit 1 & Requests Addl Info to Demonstrate That Plant & FSAR in Compliance W/Staff Position & GDC as Discussed in SER ML20217D2051998-04-20020 April 1998 SER Authorizing Licensee to Use Code Case N-524 Until Such Time as Code Case Included in Future Rev of RG 1.147 ML20216G4711998-03-12012 March 1998 Safety Evaluation Supporting Amend 92 to License NPF-58 ML20216G3901998-03-11011 March 1998 SER on Proposed Merger Between Duquesne Light Co & Allegheny Power Sys,Inc ML20199C0471997-11-0707 November 1997 Safety Evaluation Supporting Amend 91 to License NPF-58 ML20199B2351997-11-0404 November 1997 Safety Evaluation Supporting Amend 90 to License NPF-58 ML20217E2051997-09-24024 September 1997 Safety Evaluation Supporting Amend 89 to License NPF-58 ML20211H6791997-09-18018 September 1997 Safety Evaluation Authorizing Licensees Request for Alternative from Augmented Insp of Reactor Pressure Vessel Circumferential Weld in Plant,Unit 1 ML20217B2601997-09-11011 September 1997 Safety Evaluation Supporting Amend 87 to License NPF-58 ML20211A5881997-09-11011 September 1997 Safety Evaluation Supporting Evaluation of First 10-yr Interval ISI Program Plan Requests for Relief PT-004,PT-005 & PT-006 for Plant,Unit 1 ML20217K9061997-08-12012 August 1997 Safety Evaluation Accepting Plant First 10-yr Interval ISI Program Plan Relief Request PT-007 ML20141C0081997-06-19019 June 1997 Safety Evaluation Approving Merger Agreement Between Centerior Energy Corp & Ohio Edison Co Affecting NPF-58 ML20141L9131997-05-27027 May 1997 Safety Evaluation Accepting Relief Requests for First 10-yr Interval Inservice Insp Program Plan for Plant,Unit 1 ML20147H4211997-04-0101 April 1997 Safety Evaluation Accepting Changes to USAR Sections,Which Continue to Satisfy Criteria of App B of 10CFR50 ML20134D1061997-01-27027 January 1997 Safety Evaluation on Revised EALs for Plant.Proposed EALs Changes Are Consistent W/Guidance in NUMARC/NESP-007,with One Exception,& Meets Requirements of 10CFR50.47(b)(4) & App E to 10CFR50 ML20114E4561996-06-18018 June 1996 Safety Evaluation Supporting Amend 85 to License NPF-58 ML20101G8351996-03-22022 March 1996 Safety Evaluation Supporting Amend 84 to License NPF-58 ML20100R1171996-02-27027 February 1996 Safety Evaluation Supporting Amend 81 to License NPF-58 ML20101G0761996-01-20020 January 1996 Corrected SE Supporting Amend 79 to License NPF-58. Inaccuracies in Description of Changes Has Been Corrected ML20100C8031996-01-19019 January 1996 Safety Evaluation Supporting Amend 78 to License NPF-58 ML20095G0201995-12-0808 December 1995 Safety Evaluation Supporting Amend 76 to License NPF-58 ML20095A5401995-11-29029 November 1995 Safety Evaluation Supporting Amend 75 to License NPF-58 ML20092N0611995-09-26026 September 1995 Safety Evaluation Supporting Amend 73 to License NPF-58 ML20092J1451995-09-15015 September 1995 Safety Evaluation Supporting Amend 72 to License NPF-58 ML20086C1551995-06-27027 June 1995 Safety Evaluation Supporting Amend 70 to License NPF-58 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEAR05000440/LER-1999-004, :on 990916,loss of Safety Function Resulted in TS 3.0.3 Entry.Caused by Design Deficiency in Control Complex Architectural Walls.Revised Storm Contingencies Instructions.With1999-10-18018 October 1999
- on 990916,loss of Safety Function Resulted in TS 3.0.3 Entry.Caused by Design Deficiency in Control Complex Architectural Walls.Revised Storm Contingencies Instructions.With
ML20217K1231999-10-14014 October 1999 Revised Positions for DBNPS & PNPP QA Program ML20212J2011999-09-30030 September 1999 Safety Evaluation Supporting Transfer of Dl Ownership Interest in PNPP to Ceico PY-CEI-NRR-2437, Monthly Operating Rept for Sept 1999 for Pnpp,Unit 1.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Pnpp,Unit 1.With 05000440/LER-1999-003-01, :on 990218,post-accident Dose Limits Were Exceeded.Caused by Relief Valve Leakage Outside of Containment.Removed Relief Valve on 990913,by Design Change Package Implemented Under 10CFR50.59.With1999-09-27027 September 1999
- on 990218,post-accident Dose Limits Were Exceeded.Caused by Relief Valve Leakage Outside of Containment.Removed Relief Valve on 990913,by Design Change Package Implemented Under 10CFR50.59.With
PY-CEI-NRR-2429, Monthly Operating Rept for Aug 1999 for Pnpp,Unit 1.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Pnpp,Unit 1.With ML20212A6881999-08-31031 August 1999 Safety Evaluation Supporting Amend 106 to License NPF-58 PY-CEI-NRR-2424, Monthly Operating Rept for July 1999 for Perry Npp.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Perry Npp.With ML20210J3851999-07-28028 July 1999 PNPP - Unit 1 ISI Summary Rept Results for Outage 7 (1999) First Period,Second Interval PY-CEI-NRR-2416, Monthly Operating Rept for June 1999 for Perry Nuclear Power Plant,Unit 1.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Perry Nuclear Power Plant,Unit 1.With ML20196A1951999-06-17017 June 1999 Instrument Drift Analysis ML20207G2741999-06-0707 June 1999 Safety Evaluation Concluding That Firstenergy Flaw Evaluation Meets Rules of ASME Code & That IGSCC & Thermal Fatigue Crack Growth Need Not Be Considered in Application PY-CEI-NRR-2409, Monthly Operating Rept for May 1999 for Perry Nuclear Power Plant,Unit 1.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Perry Nuclear Power Plant,Unit 1.With PY-CEI-NRR-2393, Special Rept Update:On 990327 Refueling Outage 7 Began & Troubleshooting Efforts Began.Troubleshooting of Affected Calbe Confirmed Fault in Drywell Section of Cable.Determined That Installation of Newer Technology Should Be Explored1999-05-12012 May 1999 Special Rept Update:On 990327 Refueling Outage 7 Began & Troubleshooting Efforts Began.Troubleshooting of Affected Calbe Confirmed Fault in Drywell Section of Cable.Determined That Installation of Newer Technology Should Be Explored ML20206G6451999-05-0303 May 1999 Safety Evaluation Authorizing Requests for Relief IR-032 to IR-035 & IR-037 to IR-040 Re Implementation of Subsections IWE & Iwl of ASME Section XI for Containment Insp PY-CEI-NRR-2399, Monthly Operating Rept for Apr 1999 for Perry Nuclear Power Plant,Unit 1.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Perry Nuclear Power Plant,Unit 1.With ML20206E2261999-04-29029 April 1999 Safety Evaluation Concluding That Proposed Alternatives Will Result in Acceptable Level of Quality & Safety.Authorizes Use of Code Case N-504 for Weld Overlay Repair of FW Nozzle Weld at PNPP & Use of Table IWB-3514 05000440/LER-1999-002-01, :on 990327,RHR a Pump Failed to Start & LCO 3.0.3 Was Entered Due to TS Bases Misinterpretation.Caused by Failed Optical Isolator That Provided Signal to Pump Start Permissive Circuitry.Subject Circuitry Was Replaced1999-04-26026 April 1999
- on 990327,RHR a Pump Failed to Start & LCO 3.0.3 Was Entered Due to TS Bases Misinterpretation.Caused by Failed Optical Isolator That Provided Signal to Pump Start Permissive Circuitry.Subject Circuitry Was Replaced
ML20206D7911999-04-23023 April 1999 Rev 6 to PDB-F0001, COLR for Pnpp Unit 1 Cycle 8,Reload 7 05000440/LER-1999-001-01, :on 990317,discovered That Control Complex Bldg Architectural Walls Were Not Included in Tornado Dp Loading Design.Caused by Failure to Consider Tornado Dp Loads. Compensatory Measures Were Implemented.With1999-04-16016 April 1999
- on 990317,discovered That Control Complex Bldg Architectural Walls Were Not Included in Tornado Dp Loading Design.Caused by Failure to Consider Tornado Dp Loads. Compensatory Measures Were Implemented.With
ML20205P4371999-04-15015 April 1999 Safety Evaluation Concluding That Licensee Performed Appropriate Evaluations of Operational Configurations of safety-related power-operated Gate Valves to Identify Valves Susceptible to Pressure Locking or Thermal Binding ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected PY-CEI-NRR-2389, Monthly Operating Rept for Mar 1999 for Perry Nuclear Power Plant,Unit 1.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Perry Nuclear Power Plant,Unit 1.With ML20205G4221999-03-31031 March 1999 Safety Evaluation Accepting Second 10-yr Interval IST Program Releif Requests for Plant,Unit 1 ML20206D8461999-03-31031 March 1999 Rev 1 to J11-03371SRLR, Supplemental Reload Licensing Rept for Pnpp,Unit 1 Reload 7 Cycle 8 ML20205S0601999-03-31031 March 1999 Rept on Status of Public Petitions Under 10CFR2.206 with Status Change from Previous Update,990331 ML20205E0591999-03-26026 March 1999 Safety Evaluation Supporting Amend 105 to License NPF-58 ML20205D3101999-03-26026 March 1999 Safety Evaluation Supporting Amend 103 to License NPF-58 ML20205D6921999-03-26026 March 1999 Safety Evaluation Supporting Amend 104 to License NPF-58 ML20205C3761999-03-26026 March 1999 Safety Evaluation Supporting Request for Proposed Exemption to 10CFR50,app a GDC 19 ML20204C0711999-03-11011 March 1999 Safety Evaluation Supporting Amend 102 to License NPF-58 ML20207F4361999-03-0303 March 1999 Safety Evaluation Supporting Amend 101 to License NPF-58 PY-CEI-NRR-2369, Special Rept:On 990127,PAMI Was Declared Inoperable.Caused by Low Resistance Reading Existing in Circuit That Goes to Drywell.Troubleshooting of Affected Cable Will Commence During RFO on 9902271999-03-0303 March 1999 Special Rept:On 990127,PAMI Was Declared Inoperable.Caused by Low Resistance Reading Existing in Circuit That Goes to Drywell.Troubleshooting of Affected Cable Will Commence During RFO on 990227 PY-CEI-NRR-2372, Monthly Operating Rept for Feb 1999 for Perry Nuclear Power Plant,Unit 1.With1999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Perry Nuclear Power Plant,Unit 1.With ML20207L4881999-02-24024 February 1999 Safety Evaluation Supporting Amend 100 to License NPF-58 ML20203F8381999-02-0808 February 1999 Safety Evaluation Supporting Amend 97 to License NPF-58 ML20203A5961999-02-0202 February 1999 Safety Evaluation Accepting Licensee Proposed Revs to Responsibilities of Plant Operations Review Committee as Described in Chapter 17.2 of USAR ML20203A5211999-01-27027 January 1999 Safety Evaluation Accepting Licensee Calculations Showing That Adequate NPSH Will Be Available for HPCS Pumps ML20198R8921999-01-0707 January 1999 SER Accepting Licensee Proposed Amend to TSs to Delete Reference to NRC Policy Re Plant Staff Working Hours & Require Administrative Controls to Limit Working Hours to Be Acceptable ML20206B0101998-12-31031 December 1998 1998 Annual Rept for Firstenergy Corp, for Perry Nuclear Power Plant & Davis-Besse Nuclear Power Station.Form 10-K Annual Rept to Us Securities & Exchange Commission for Fiscal Yr Ending 981231,encl ML20204J6751998-12-31031 December 1998 1998 Annual Rept for Dbnps,Unit 1,PNPP,Unit 1 & BVPS Units 1 & 2 PY-CEI-NRR-2356, Monthly Operating Rept for Dec 1998 for Perry Nuclear Power Plant,Unit 1.With1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Perry Nuclear Power Plant,Unit 1.With ML20198J0031998-12-22022 December 1998 SER Accepting Licensee Response to GL 92-08,ampacity Derating Issues for Perry Nuclear Power Plant,Unit 1 ML20198K9071998-12-21021 December 1998 Safety Evaluation Supporting Amend 96 to License NPF-58 ML20196J4731998-12-0202 December 1998 Safety Evaluation Supporting Amend 95 to License NPF-58 PY-CEI-NRR-2346, Monthly Operating Rept for Nov 1998 for Perry Nuclear Power Plant,Unit 1.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Perry Nuclear Power Plant,Unit 1.With ML20196D2751998-11-23023 November 1998 Safety Evaluation Supporting Amend 94 to License NPF-58 ML20195F6891998-11-0505 November 1998 Safety Evaluation Accepting Proposed Reduction in Commitment in Quality Assurance Program to Remove Radiological Assessor Position 05000440/LER-1998-003, :on 981001,missed TS SR on H Igniters Was Noted.Caused by Personnel Error.Missed Surveillance Was Performed on Day of Discovery of Item & Function of H Igniters Were Verified.With1998-11-0202 November 1998
- on 981001,missed TS SR on H Igniters Was Noted.Caused by Personnel Error.Missed Surveillance Was Performed on Day of Discovery of Item & Function of H Igniters Were Verified.With
PY-CEI-NRR-2335, Monthly Operating Rept for Oct 1998 for Perry Nuclear Power Plant,Unit 1.With1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Perry Nuclear Power Plant,Unit 1.With 1999-09-30
[Table view] |
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i C CEhr UNITED STATES p
NUCLEAR REGULATORY COMMISSION WASHINGTON, D.C. 30006 0001 k*****
i l
1 SAFETY EVALUATION BY THE OFFICE OF NUCLEAR REACTOR REGULATION i
}
RELATED TO ANENDNENT NO.
76 TO FACILITY OPERATING LICENSE ND. NPF-58 l
THE CLEVELAND ELECTRIC ILLUNINATING CONPANY. ET AL.
l PERRY NUCLEAR POWER PLANT. UNIT N0. I j
DOCKET NO 50-440 i
f 1.0 INTR 000CTION i
Containment leak rate testing is necessary to demonstrate that the measured i
leak rate is within the acceptance criteria cited in the licensing design basis. Periodic testing of the overall containment structure along with separate leak testing of the penetrations provides assurance that post-
+
i accident radiological consequences will be within the limits of 10 CFR Part 100. The Commission's requirements regarding leak rate testing are found in Appendix J to 10 CFR Part 50.
By letter dated October 21, 1994 (PY-CEI/NRR-1650L), the licensee requested an amendment to Fad 11ty Operating License NPF-58 for the Perry Nuclear Power 1
Plant (PNPP). The amendment would make changes to Technical Specification d
3/4.6.1.2, " Primary Containment Leakage," and its associated Bases to reflect proposed exemptions to the requirements of 10 CFR Part 50, Appendir J, Option A, Sections III.A.5(b)(2), III.B.3, III.C.3, III.A.l(d), III.D.1(a),
and III.D.3. The proposed exemptions were submitted by separate letter, also dated October 21, 1994 (PY-CEI/NRR-1651L).
The proposed exemptions to Appendix J, Option A, were subsequently approved by the staff in a letter dated December 4,1995. The approved exemptions will:
a.
Exclude main steam line isolation valve leakage from inclusion in both the containment integrated leak rate (Type A) test and the combined local leak rate (Type B and C) tests, and clarify that the main steam lines are not required to be vented and drained for Type A testing; b.
Decomple performance of the third Type A test from the shutdown for the 10-year plant inservice inspection; and c.
Allow Type C testing to be performed at times other than dFring shutdown for refueling.
9512190465 951200 PDR ADOCK 05000440 p
PDR
2.0 EVALUATION Sections III.A.5fb)(2). III.B.3. III.C.3. and III.A.lfd)
Section III.A.5(b)(2) states that the measured leakage from the containment integrated leak rate (Type A) test (L") shall be less than 75% of the maximum allowable. leakage rate (0.75 L ).
The licensee proposed to exempt main steam line isolation valve leakage from Type A test results and consider leakage.
from the main steam lines separately. - Sections III.B.3 and III.C.3 require.
that the combined leakage of valves and penetrations subject to Type B and C local leak rate testing be less than 0.6 times the maximum allowable leakage valve leaka ).
The licensee proposed to. exempt main steam line isolation rate (0.6 Lge from the contined leakage from Type B and C local leak rate testing and consider leakage from the main steam lines separately.Section III.A.1(d) requires that all fluid systems that would be open to containment following post-accident conditions, be vented and drained prior to conducting Type A tests. The. licensee proposed that the piping between the inboard and outboard main steam line isolation valves be flooded with water when Type A tests are conducted.
In support of these exemptions, the licensee proposed modifying Technical Specification Limiting Condition for Operation (LCO) 3.6.I.2.a by inserting words to clearly state that main steam line isolation valve leakage is separate from the overall integrated leakage rate. Similar wording would also be inserted in Action 3.6.1.2.a.
The licensee has also proposed to add a superscript "#" to LC0 3.6.1.2.b and to Action 3.6.I.2.b to refer to a footnote which clarifles that an Appendix J exemption is involved.
During the original staff review of the PNPP, the licensee proposed separate treatment of measured leakage past the main steam isolation valves. The licensees's radiological dose analysis assumed separate contributions from both containment leakage and main steam isolation valve leakage. This approach was reviewed and approved in the staff's Safety Evaluation Report (NUREG-0887). The PNPP Final Safety Analysis Report and technical specifications limit the maximum containment leakage to 0.20 percent per day.
In addition, technical specifications limit the maximum allowable leakage of each main steam line to 25 standard cubic feet per hour.
Consistent with separate handling of main steam line isolation valve leakage, the licensee proposed that the piping between the inboard and outboard isolation valves be filled with water when Type A tests are performed.
Filling these sections of pipe ensures that air does not pass through these lines thus inadvertently centributing to the Type A test results.
The methodology proposed by the licensee accounts for all containment leakage paths. Treat'ng main steam line isolation valve leakage separately from both the integrated Type A test and the combined Type B and C tests still verifies that the total leakage is within the design limits and, therefore, meets the underlying purpose of the rule.
On this basis, the staff found that separating main steam line isolation valve leakage from Type A, B and C leak rate tests would not present an undue risk
_3-to the public health and safety. Accordingly, the NRC approved the issuance i
of the subject exemption on December 4,1995, i
j Based on the above, and because the licensee:s proposed change to the technical specifications is consistent with the exemption approved by the NRC, j
the staff finds these changes acceptable.
j 1
l
.Section III.D.lfa)
Section III.D.l(a) requires, in part, that "...a set of three Type A tests i
shall be performed, at approximately equal intervals during each 10-year j
service period. The third test of each set shall be conducted when the plant is shutdown for the 10-year plant inservice inspections." The licensee proposes to perform the three Type A tests at approximately equal intervals within each 10-year period, with the third test of each set conducted as close as practic~al to the end of the 10-year period. However, there would be no required connection between the Appendix J 10-year interval and the inservice inspection 10-year interval.
In support of this proposed exemption, the licensee proposed modifying Technical Specification 4.6.1.2.a by deleting the sentence requiring that the two tests be performed during the same outage.
The 10-year plant inservice inspection (ISI) is the series of inspections performed every 10 years in accordance with Section XI of the ASME Boiler and Pressure Vessel Code and Addenda as required by 10 CFR 50.55a. The licensee performs the ISI volumetric, surface, and visual examinations of components and system pressure tests in accordance with 10 CFR 50.55a(g)(4) throughout the 10-year inspection interval. The major portion of this effort is
- presently being performed every refueling outage. As a result, there is no extended outage in which the 10-year ISI examinations are performed.
There is no benefit to be gained by the coupling requirement cited abovgJn that elements of the ISI program are conducted throughout each 10-year cycle rather than during a refueling outage at the end of the 10-year cycle.
Consequently, the subject coupling requirement offers no benefit either to rafety or to the economical. operation of the facility.
Moreover, each of these two surveillance tests (i.e., the Type A tests and the 10-year ISI program) is independent of the other and provides assurances of different plant characteristics. The Type A test assures the required leak-tightness to demonstrate compliance with the guidelines of 10 CFR Part 100.
The 10-year ISI program provides assurance of the integrity of the structures, systems and components as well as verifying operational readiness of pumps and valves in compliance with 10 CFR 50.55a. There is no safety-related concern necessitating their coupling in the same refueling outage. Accordingly, the staff finds that the subject exemption request meets the underlying purpose of the rule.
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On this basis, the staff found that the uncoupling of the Type A tests from the 10-year ISI program would not present an undue risk to the public health and safety. Accord' ngly, the NRC staff approved the issuance of the subject exemption on December 4, 1995.
Based on the above, and because the licensee's proposed change to the technical specifications is consistent with the exemption approved by the NRC, the staff finds these changes acceptable.
Test Methodolooies The current PNPP Technical Specification 4.6.1.2 states that the containment integrated leak rate test shall be performed using the criteria specified in Appendix J to 10 CFR Part 50 using the methods and provisions of ANSI N45.4-1972 and BN-TOP-1.
In addition, Specification 4.6.1.2 states that the test results shall also be reported based on the Mass Point Methodology described in ANSI /ANS N56.8-1981. The Mass Point Methodology of ANSI /ANS N56.8-1981 is intended for use when the Type A tests are greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> in (uration whereas BN-TOP-1 is to be used for durations less than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.
Subsequent to the original licensing of the PNPP, Appendix J to 10 CFR Part 50 has been revised to reflect istC approved methodologies and updated versions of.
ANSI standards. However, by referencing specific standards in the technical l
specifications, the licensee does not have the flexibility to incorporate updated versions without processing a license amendment. Therefore, the licensee has proposed modifying Specification 4.6.1.2 to only reference BN-TOP-1 and the criteria specified in Appendix J while eliminating references to l
ANSI N45.4-1972 and ANSI /ANS M56.8-1981. Since Appendix J now references both ANSI N45.4-1972 and ANSI /ANS N56.8-1987, the licensee will be able to adopt the latest ANSI standards along with any future updates to Appendix J.
The proposed Specification 4.6.1.2 clarifies that the provisions of BN-TOP-1 may be used for Type A tests having a duration less than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.
The proposed modification still requires the licensee to be in conformance with the criteria of Appendix J.
By deleting references to specific ANSI standards, the licensee gains the additional flexibility to adopt updated standards without processing a license amendment. Since the proposed change does not alter the licensee's compliance with the requirements of Appendix J, the staff finds the proposed : change to be acceptable.
3.0 STATE CONSULTATION
In accordance with the Commission's regulations, the Ohio state official was notified of the proposed issuance of the amendment. The state official had no comments.
4.0 ENVIRONMENTAL CONSIDERATION
This amendment involves a change to a requirement with respect to the installation or use of a facility component located within the restricted area as defined in 10 CFR Part 20 or a change to a surveillance requirement. The staff has determined that the amendment involves no significant increase in t
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I-4 the amounts, and no significant change in the types, of any effluent that may be released offsite and that there is no significant increase in individual or cumulative occupational radiation exposure. The Commission has previously i
issued a proposed finding that this amendment involves no significant hazards I
consideration and there has been no public comment on such finding (60 FP 42611). Accordingly, this amendment meets the eligibility criteria for categorical exclusion set forth in 10 CFR 51.22(c)(9). Pursuant to 10 CFR be prepa) red in connection with the' issuance of this amendment.51.22(b, no envir i-
5.0 CONCLUSION
l The staff has concluded, based on the considerations discussed above, that:
(1) there is reasonable assurance that the health and safety of the public l
will not be endangered by operation in the proposed manner, (2) such activities will be conducted in compliance with the Commission's regulations, and (3) the issuance of this amendment will not be inimical to the common j
defense and security or to the health and safety of the public.
Principal Contributor: Douglas Pickett Date:
December 8, 1995 i
4 3
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